| | | Reporting criterion |
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| 05000255/LER-1992-001, :on 911209,observed That Seal Oil Pressure on Air Side of Electrical Generator Had Decreased from Previous Reading.Caused by Malfunction of Electrical Generator Seal Oil Sys Due to Plugged Filter.Filter Cleaned |
- on 911209,observed That Seal Oil Pressure on Air Side of Electrical Generator Had Decreased from Previous Reading.Caused by Malfunction of Electrical Generator Seal Oil Sys Due to Plugged Filter.Filter Cleaned
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-002, :on 911216,discovered That Selected Reactor Protective Sys Instrument Surveillance Requirements Not Being Performed,Per Tech Spech.Caused by Procedural Weakness.Ts Surveillance Procedures Reviewed |
- on 911216,discovered That Selected Reactor Protective Sys Instrument Surveillance Requirements Not Being Performed,Per Tech Spech.Caused by Procedural Weakness.Ts Surveillance Procedures Reviewed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000255/LER-1992-003, :on 911215,both Diesel Generators Inadvertently Started Due to Undervoltage Condition.Caused by Failure to Properly Calculate Cable Impedance.Analysis Being Performed of Voltage Transient |
- on 911215,both Diesel Generators Inadvertently Started Due to Undervoltage Condition.Caused by Failure to Properly Calculate Cable Impedance.Analysis Being Performed of Voltage Transient
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-004, :on 920107,loss of Containment Integrity Due to Failure of Emergency Escape Airlock Equalizing Valve Occurred.Caused by Lubricant on Valve Stem.Maint Procedure for Airlocks Being Revised |
- on 920107,loss of Containment Integrity Due to Failure of Emergency Escape Airlock Equalizing Valve Occurred.Caused by Lubricant on Valve Stem.Maint Procedure for Airlocks Being Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000255/LER-1992-005, :on 920115,NRC Notified Plant Staff of Apparent Misrouting of Class 1E Pressurizer Level Instrument Loop. Caused by Inadequate Design Control During Equipment Mod. Loop Disconnected |
- on 920115,NRC Notified Plant Staff of Apparent Misrouting of Class 1E Pressurizer Level Instrument Loop. Caused by Inadequate Design Control During Equipment Mod. Loop Disconnected
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-006, :on 920120,temp Element Was Not Environmentally Qualified in Accordance W/Regulatory Guide 1.97.Caused by Personnel Error & Inaccurate Documentation.Mod Prepared to Replace TE-0351B Instrument |
- on 920120,temp Element Was Not Environmentally Qualified in Accordance W/Regulatory Guide 1.97.Caused by Personnel Error & Inaccurate Documentation.Mod Prepared to Replace TE-0351B Instrument
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-007, :on 920205,determined That MSIV Actuator Solenoid Valves Could Be Rendered Inoperable by Main Steam Line Break Outside Containment.Caused by Installation of Unqualified Electrical Circuit.Valve Relocated |
- on 920205,determined That MSIV Actuator Solenoid Valves Could Be Rendered Inoperable by Main Steam Line Break Outside Containment.Caused by Installation of Unqualified Electrical Circuit.Valve Relocated
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000255/LER-1992-008, :on 920206,both HVAC Trains Inoperable When Air Conditioning Condensing Unit Bypass Line Leaked.Caused by Lack of Clearance Between Hot Gas Bypass Line & Penetration. Condensing Units Will Be Inspected |
- on 920206,both HVAC Trains Inoperable When Air Conditioning Condensing Unit Bypass Line Leaked.Caused by Lack of Clearance Between Hot Gas Bypass Line & Penetration. Condensing Units Will Be Inspected
| |
| 05000255/LER-1992-009, :on 920213,control Room Ventilation Sys Inadvertently Switched to Emergency Mode.Caused by Combination of Inadequate Job Planning & Personnel Error. Job Planning Requirements Reviewed |
- on 920213,control Room Ventilation Sys Inadvertently Switched to Emergency Mode.Caused by Combination of Inadequate Job Planning & Personnel Error. Job Planning Requirements Reviewed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-010, :on 920213,SIRWT Liquid Sample Exceeded MPC of Radionuclides.Caused by Inadequate Corrective Action for Prior Event & Defective Review of MPC Limit.Evaluation to Be Performed of PCS Operating Procedures |
- on 920213,SIRWT Liquid Sample Exceeded MPC of Radionuclides.Caused by Inadequate Corrective Action for Prior Event & Defective Review of MPC Limit.Evaluation to Be Performed of PCS Operating Procedures
| |
| 05000255/LER-1992-011, :on 920212,discovered Inadequate Electrical Isolation of Class 1E Pressurizer Pressure Indicator Cable. Caused by Inadequate Design Control When Equipment Installed in 1980.Mod Controls Re Changes Revised |
- on 920212,discovered Inadequate Electrical Isolation of Class 1E Pressurizer Pressure Indicator Cable. Caused by Inadequate Design Control When Equipment Installed in 1980.Mod Controls Re Changes Revised
| |
| 05000255/LER-1992-012, :on 920214,determined That Main Steam Line Radiation Elements Not Environmentally Qualified.Caused by Personnel Error.Main Steam Line Radiation Elements Will Be Modified or Justification Will Be Provided |
- on 920214,determined That Main Steam Line Radiation Elements Not Environmentally Qualified.Caused by Personnel Error.Main Steam Line Radiation Elements Will Be Modified or Justification Will Be Provided
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-013, :on 920217,lack of Enviornmental Qualification for Stack Gas Flow Transmitter FT01818 Noted.Caused by Lack of Appropriate Controls.Temporary Mod Performed on Radioactive Gaseous Effluent Monitor Sys |
- on 920217,lack of Enviornmental Qualification for Stack Gas Flow Transmitter FT01818 Noted.Caused by Lack of Appropriate Controls.Temporary Mod Performed on Radioactive Gaseous Effluent Monitor Sys
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-014, :on 920217,unauthorized Individual Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Personnel Reminded of Need for Attention to Detail & Log Revised |
- on 920217,unauthorized Individual Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Personnel Reminded of Need for Attention to Detail & Log Revised
| |
| 05000255/LER-1992-015, :on 900923,heavy Load Moved in Load Path Which Deviated from Established Safe Load Paths & Was Not Approved by Reactor Engineer.Caused by Inappropriate Procedure Rev. Reactor Engineer Will Approve Subj Deviations |
- on 900923,heavy Load Moved in Load Path Which Deviated from Established Safe Load Paths & Was Not Approved by Reactor Engineer.Caused by Inappropriate Procedure Rev. Reactor Engineer Will Approve Subj Deviations
| 10 CFR 50.73(a)(2)(i) |
| 05000255/LER-1992-016, :on 920225,determined That Solenoid Valves & Position Switches for Control Valves Controlling Svc Water Flow from CCW HXs Not Environmentally Qualified.Caused by Inadequate Analysis.Schemes Modified |
- on 920225,determined That Solenoid Valves & Position Switches for Control Valves Controlling Svc Water Flow from CCW HXs Not Environmentally Qualified.Caused by Inadequate Analysis.Schemes Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000255/LER-1992-017, :on 920229,unusual Event Declared When Upper Guide Structure Raised for Removal from Reactor Vessel & Fuel Assembly Observed Hanging from Structure.Caused by Bent Fuel Alignment Pins.Pins Straightened |
- on 920229,unusual Event Declared When Upper Guide Structure Raised for Removal from Reactor Vessel & Fuel Assembly Observed Hanging from Structure.Caused by Bent Fuel Alignment Pins.Pins Straightened
| |
| 05000255/LER-1992-018-01, :on 920309,discovered That Electrical Connections Not Environmentally Qualified Existed in Electrical Circuits for Position Switches Due to Inadequate Review.Wire Nut Connections Replaced |
- on 920309,discovered That Electrical Connections Not Environmentally Qualified Existed in Electrical Circuits for Position Switches Due to Inadequate Review.Wire Nut Connections Replaced
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-018, :on 920305,determined That Containment Electrical Penetration Connectors Were Not Qualified W/ 10CFR50.49.Caused by Lack of Adequate Technical Guidance. Subj Connectors Replaced |
- on 920305,determined That Containment Electrical Penetration Connectors Were Not Qualified W/ 10CFR50.49.Caused by Lack of Adequate Technical Guidance. Subj Connectors Replaced
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-020, :on 920303,discovered That Four SI Valves Which Should Have Been Closed Arranged W/Two Closed by One Safety Injection Signal Channel.Caused by Personnel Error. HPCI Sys Modified to Use Existing Piping |
- on 920303,discovered That Four SI Valves Which Should Have Been Closed Arranged W/Two Closed by One Safety Injection Signal Channel.Caused by Personnel Error. HPCI Sys Modified to Use Existing Piping
| |
| 05000255/LER-1992-021, :on 920314,determined That Containment Integrity Had Been Breached Due to Simultaneous Opening of Sys Boundaries.Caused by Personnel Error.Reiterated to Staff That Work Should Begin on Proper Work Orders |
- on 920314,determined That Containment Integrity Had Been Breached Due to Simultaneous Opening of Sys Boundaries.Caused by Personnel Error.Reiterated to Staff That Work Should Begin on Proper Work Orders
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000255/LER-1992-023, :on 920327,discovered That Previously Unidentified Junction Boxes in Electrical Circuits Contained Environmentally Unqualified Connections.Caused by Design Failure.Terminal Blocks to Be Replaced |
- on 920327,discovered That Previously Unidentified Junction Boxes in Electrical Circuits Contained Environmentally Unqualified Connections.Caused by Design Failure.Terminal Blocks to Be Replaced
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-024, :on 920327,inadvertent Opening of Station Power Breaker Resulting in ESF Actuation & Interruption of Shutdown Cooling.Caused by Supervisor Allowing Work to Proceed on C Bus.Event Discussed W/Maint |
- on 920327,inadvertent Opening of Station Power Breaker Resulting in ESF Actuation & Interruption of Shutdown Cooling.Caused by Supervisor Allowing Work to Proceed on C Bus.Event Discussed W/Maint
| |
| 05000255/LER-1992-025, :on 920331,determined That Longitudinal Welds on 36-inch Main Steam Line Piping Not Included in Inservice Insp Program.Caused by Personnel Error.All Welds Inspected Using Volumetric/Surface Methods |
- on 920331,determined That Longitudinal Welds on 36-inch Main Steam Line Piping Not Included in Inservice Insp Program.Caused by Personnel Error.All Welds Inspected Using Volumetric/Surface Methods
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000255/LER-1992-026, :on 920331,discovered That During LOCA, Concurrent W/Loss of Offsite Power,Overcurrent Trip of EDG 1-1 Could Occur.Caused by Oversight in Original Plant Design.Time Delay Relay Installed |
- on 920331,discovered That During LOCA, Concurrent W/Loss of Offsite Power,Overcurrent Trip of EDG 1-1 Could Occur.Caused by Oversight in Original Plant Design.Time Delay Relay Installed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
| 05000255/LER-1992-027, :on 920401,wire Cage Door on 625-ft Elevation in Containment Found Closed But Wire Cut So That Person Could Have Reached Through to Unlock Door.Possibly Caused by Vandalism.Door Secured by Steel Plate |
- on 920401,wire Cage Door on 625-ft Elevation in Containment Found Closed But Wire Cut So That Person Could Have Reached Through to Unlock Door.Possibly Caused by Vandalism.Door Secured by Steel Plate
| 10 CFR 50.73(a)(2)(i) |
| 05000255/LER-1992-028, :on 920331,potential Inability to Maintain Diesel Generator Room Temp Qualification Due to non-1E Qualified Cooling Fan Noted.Procedures Revised & Design Will Be Corrected |
- on 920331,potential Inability to Maintain Diesel Generator Room Temp Qualification Due to non-1E Qualified Cooling Fan Noted.Procedures Revised & Design Will Be Corrected
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000255/LER-1992-028-02, Informs of Completion of Mod Re Emergency Diesel Generator Room Cooling Per LER 92-028-02 | Informs of Completion of Mod Re Emergency Diesel Generator Room Cooling Per LER 92-028-02 | |
| 05000255/LER-1992-029, :on 920404,inadvertent Actuation of Left Channel Sequencer Occurred.Caused by Failure to Follow Test Procedure.Importance of Incident Was Discussed W/All Shifts on Rotation |
- on 920404,inadvertent Actuation of Left Channel Sequencer Occurred.Caused by Failure to Follow Test Procedure.Importance of Incident Was Discussed W/All Shifts on Rotation
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-030, :on 920403,inadvertent Start of Both Diesel Generators Occurred.Caused by Electrical Discontinuity in Contacts.Fuse Panels for Both 2400 Volt Engineered Safeguard Buses Were Inspected |
- on 920403,inadvertent Start of Both Diesel Generators Occurred.Caused by Electrical Discontinuity in Contacts.Fuse Panels for Both 2400 Volt Engineered Safeguard Buses Were Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000255/LER-1992-031, :on 920402,left Channel DBA Sequencer Inadvertently Activated by Technician Preparing to Test Left Normal Shutdown Sequencer Due to Inadequate Test Procedures. Procedures RT-13A & B & RT-8C & D Revised |
- on 920402,left Channel DBA Sequencer Inadvertently Activated by Technician Preparing to Test Left Normal Shutdown Sequencer Due to Inadequate Test Procedures. Procedures RT-13A & B & RT-8C & D Revised
| |
| 05000255/LER-1992-031-01, Forwards LER-92-031-01 Re Inadvertent ESF Actuation Caused by Inadequate Test Procedures.Original Corrective Action to Revise Test Connection Drawings No Longer Required Because Plant Procedures Revised in Such Detail to Eli | Forwards LER-92-031-01 Re Inadvertent ESF Actuation Caused by Inadequate Test Procedures.Original Corrective Action to Revise Test Connection Drawings No Longer Required Because Plant Procedures Revised in Such Detail to Eliminate Need | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-032, :on 920406,unplanned Actuation of Right Channel of Safety Injection Sys Relays Occurred.Caused by Inadequate Procedure.Instructions & Steps Added to TSs Surveillance Procedures |
- on 920406,unplanned Actuation of Right Channel of Safety Injection Sys Relays Occurred.Caused by Inadequate Procedure.Instructions & Steps Added to TSs Surveillance Procedures
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-033, :on 920414,inoperable Control Room Penetration Occurred.Caused by Misapplication of Procedures & Inaccurate Procedures.Plant Administrative Procedure on Control of Equipment Status Will Be Updated |
- on 920414,inoperable Control Room Penetration Occurred.Caused by Misapplication of Procedures & Inaccurate Procedures.Plant Administrative Procedure on Control of Equipment Status Will Be Updated
| |
| 05000255/LER-1992-034, :on 920701,reactor Automatically Tripped on Loss of Load Signal,Resulting in Turbine Generator Trip & Loss of Signal.Caused by Momentary Loss of Power to Turbine Sys computers.Post-trip Review Completed |
- on 920701,reactor Automatically Tripped on Loss of Load Signal,Resulting in Turbine Generator Trip & Loss of Signal.Caused by Momentary Loss of Power to Turbine Sys computers.Post-trip Review Completed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-035, :on 920724,reactor Tripped Due to Loss of Turbine Digital Electrohydraulic Control Sys.Caused by Momentary Loss of Power to Electrohydraulic Sys Computers. Power Supply Switching Circuits Replaced |
- on 920724,reactor Tripped Due to Loss of Turbine Digital Electrohydraulic Control Sys.Caused by Momentary Loss of Power to Electrohydraulic Sys Computers. Power Supply Switching Circuits Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-036, :on 920802,during Monthly TS Procedure for 1-1 Edg,Noted That Exhaust Temp Indicated Low Reading.Caused by Lack of Adequate Controls in DG Cylinder Latch.Edg Test Procedures Will Be Revised |
- on 920802,during Monthly TS Procedure for 1-1 Edg,Noted That Exhaust Temp Indicated Low Reading.Caused by Lack of Adequate Controls in DG Cylinder Latch.Edg Test Procedures Will Be Revised
| 10 CFR 50.73(a)(2)(i) |
| 05000255/LER-1992-037, :on 920814,reactor Tripped Due to Low SG Level Resulting from Broken Air Line on Main Feedwater Regulating Valve.Air Lines to Main Feedwater Regulating Valves CV-0701 & CV-0703 Replaced & Satisfactorily Tested |
- on 920814,reactor Tripped Due to Low SG Level Resulting from Broken Air Line on Main Feedwater Regulating Valve.Air Lines to Main Feedwater Regulating Valves CV-0701 & CV-0703 Replaced & Satisfactorily Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-038-01, Forwards LER 92-038-01,providing Final Results of Testing Program Performed on Sola Electric Constant Voltage Transformers & Results of Evaluation of Failure of Charging Pump auto-start Circuit | Forwards LER 92-038-01,providing Final Results of Testing Program Performed on Sola Electric Constant Voltage Transformers & Results of Evaluation of Failure of Charging Pump auto-start Circuit | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000255/LER-1992-038, :on 920825,reactor Tripped,Resulting from Loss of Preferred Ac Bus Y-20,coincident W/Blown Fuse in Second Channel of Rps.Caused by Failure of Inverter ED-07.All Fuses Checked & Plant Drawings/Vendor Manuals Updated |
- on 920825,reactor Tripped,Resulting from Loss of Preferred Ac Bus Y-20,coincident W/Blown Fuse in Second Channel of Rps.Caused by Failure of Inverter ED-07.All Fuses Checked & Plant Drawings/Vendor Manuals Updated
| |
| 05000255/LER-1992-039, :on 921030,reactor Automatically Tripped Due to Loss of Load Resulting from Unstable Voltage to Turbine Control Sys Computers.Caused by Failure to Maintain Power Voltage to Ups.New Transformers Installed |
- on 921030,reactor Automatically Tripped Due to Loss of Load Resulting from Unstable Voltage to Turbine Control Sys Computers.Caused by Failure to Maintain Power Voltage to Ups.New Transformers Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation |