ML18058A385

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Insp Rept 50-255/92-11 on 920212-14,25-27,0324-27 & 0416.Two Apparent Violations Noted.Major Areas Inspected:Potential for MSIV Actuator Solenoid Valves Being Inoperable in Event of HELB
ML18058A385
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/27/1992
From: Hausman G, Jablonski F, Schrum D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18058A384 List:
References
50-255-92-11, NUDOCS 9205040081
Download: ML18058A385 (9)


See also: IR 05000255/1992011

Text

..

U. S. NUCLEAR REGULATORY COMMISSION

REGION* III

Report No.:

50-255/920ll(DRS)

Docket No.:

50-255

License No.:

DPR-20

Licensee:

Consumers Power company

1945 West Parnall Road

Jackson, MI 49201

Facility Name:

Palisades Nuclear Plant

Inspection At:

Palisades Site, Covert, Michigan

Inspection Conducted:

February 12-14, 25-27, March 24-27, and

April 16, 1992

Inspectors:

(-/_ > 7- 9 2__

Approved By:

D. Schru111

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Inspection on Februarv 12-14, 25-27, March 24-27, and April 16,

1992 (Report No. 50-255/9201l(DRS))

Areas Inspected: Special inspection of matters associated with

the main steam isolation valve actuator solenoid valves being

inoperable in the event of a high energy *line break due to an

inadequate design.

Portions of NRc* Inspection Procedure 62705

were used during the .inspection.

.

Results~ In December 1990, the licensee's contractor* issued a

report of an extensive environmental quaiification review that

identified a large number of discrepancies.

.The licensee failed

to start a thorough review of the report until December 1991.

As

a result of the review, the licensee identified on February 5-,

1992,*that the main steam isolation valves were inoperable due to

an unqualified electrical circuit.

Since the reactor was at 100%

pqwer, the licensee requested and received a temporary waiver of

compliance.

However, the licensee's request for*the waiver did

no.t fully disclose how the unqualified cir.cuits were identified,

the existence of a contractor's report, or the other deficiencies

identified within the report .. SubsequeJ?.tly, a number of other

9205040081 920427

PDR

ADOCK 05000255

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PDR

Inspection Summary *

2

equipment environmental* qualification prcibl~ms were identified by

the licensee, which were reported to the NRC.as licensee event.

reports *.

Two apparent violations were identified.

Section 3.4.2 describes

problems with supplying the NRC with complete and accurate

information, and Section 3.4.3 describes problems with inadequate

corrective action .

DETAILS

1. 0

~rincipal Persons Contacted

consumers Power Company (CPCo)

  1. G. Slade, Plant General Manager
    • D. Day, Environmental Qualification Engineer
    • P. Donnelly, Plant Safety and Licensing Director
    • R. Hamm, Instrumentation and Control Section Head
    • J. Kuemin, Licensing Manager
    • R. Mccaleb, Nuclear Program Audit Department Specialist
    • K. Osborne, System Engineering Manager
    • K. Toner, Electric/I&C/Computer Engineering Manager
  1. D. Vandewalle, Mech & Civil/Structural Engineering Manager
  1. R. Orosz, Nuclear Engineering Manager

U. s. Nuclear Regulatory Commission (NRC)

  1. M. Ring, Engineering Branch Chief, Division of Reactor Safety
  1. M. Gamberoni, Licensing Project Manager, by Telephone
    • J. Heller, Senior Resident Inspector
  1. B. Jorgensen, Chief, Reactor Projects Section 2A
  • R. Roton, Resident Inspector

The NRC inspectors also contacted and interviewed other licensee

personnel during the inspection.

  • Denotes those present at the exit meeting held March 27, 1992.
  1. Denotes those present at the exit meeting held April 16, 1992.

2.0

Licensee Action on Previous Inspection Findings

2.1 (Closed) Open Item (255/87027-02) Weakness with tracking the

status_of NRC issues.

The licensee improved the ability to update the data base for

open items so that ongoing knowledge of what actions have been

completed is available.

The licensee's correspondence to the NRC

on January 28, 1988, was correct in stating that a Region III

special task *force had reviewed this system and concluded in a

May 16, 1986, report that for the intended purpose of tracking

commitments that the Correspondence Logging & Commitment Tracking

system (CLCTS) works adequately.

The special task force had

performed a spot check of 100 open items, unresolved items, and

violations from the CLCTS and compared them with records,

specifically to determine whether those classified as externally

closed were in agreement with those listed as closed in the

Region III records.

With only one exception all the remaining

items checked were accurately recorded .

No additional problems have been noted by the regional or

resident staff subsequent to the occurrence of the above

concerns.

The inspector agrees with the licensee's assessment

that this was an isolated incident.

This item is closed.

2.2 (Closed) Unresolved Item (255/87027-03) Effectiveness of the

Configuration Control Project (CCP).

The inspectors determined that Schematic Diagram E-5, Sheet 15,

Revision 5 had not been revised to incorporate modification FC-

687. The NRC stated that the effectiveness of the CCP could be

adversely affected if management attention was not given to

future modifications.

The licensee stated that this type of problem is discovered and

corrected during the revie~ pr6cess by the CCP el~ctrical drawing

verification and correction task group.

The inspector .. deterfuined

that the CCP has been effective in f~nding and correcting these

types of problems.

The licensee invested substantial time in the

review of each modification with each drawing being redlined

during its comparison to the as-built configuration in the plant.

The discrepancies were appropriately prioritized for importance

to ensure timely corrective actions for the items important to

safety.

No additional NRC concerns exist for this problem.

This

item is closed.

2.3 (Closed) Unresolved Item (255/88020-6A) Licensee failed to

take proper corrective actions when discrepancies were identified

by the* CCP team.

The licensee failed to correct and .resolve discrepancies with

approximately 300 electrical~ drawings during electrical plant

walkdown-inspections.

The licensee's corrective action was to

bring the CCP discrepancy c~tegorization and evaluation process

into agreement with the actual drawing walkdown.

The inspector

determined that the corrective actions were adequate to prevent_

the condition as described in the unresolved item.

The licensee

had made substantial progress with the CCP efforts since this

unresolved item was issued and it appeared that the majority of

the work will be completed by the end of 1992.

This item is

closed.

3.0

Inspection Results

3.1

Purpose of the Inspection

The purpose of the inspection was to review the matters

associated with the main steam isolation valve (MSIV) solenoid

actuator valves being inoperable in the event of a high energy

line break, which led to a plant shut down on February 6, 1992.

3 . 2 .

Description of Event

2

On *February 5, 1992, the, licensee determined that the solenoid

valves that actuate the MSIVs .could cause a short circuit during

a postulated high energy line break and prevent the MSIVs from

closing on demand.

on February 6, 1992, the licensee promptly

reported the problem to the NRC and requested a Temporary Waiver

of Compliance (TWOC) .

On the same dayj after determining that

the problem could not be repaired, the licensee appropriately

declared the MSIVs inoperable per Technical Specification 3.5.lf

and shut down the plant.

As described in licensee event report (LER) 92-07, "Main Steam

Isolation Valves Inoperable Due to -an Unqualified Electrical

Circuit," and as determined by the NRC this condition was caused

by:

a design deficiency involving the installation of non-

enyironmentally qualified solenoid valves;

lack of adequate isolation between Class lE and non-Class lE

circuitry; and

lack of adequate isolation between redundant Class lE

components located in different areas.

3 .. 3

Significance of Event

Although a main steam line break .in the area of concern is not

likely, the failure of the MSIVs to close during a steam line

break outside containment (the event which could disable* the MSIV

solenoid valves) is considered significant.

The MSIVs would not

fail safe, that is, electric power would be needed to actuate

solenoids to cause the mechanical operator to move and close the

MSIVs.

Failure of the MSIVs would create the potential for a

double steam generator blow down, possible tube rupture, and

possible off-site release of radiation greater than 10 CFR 100

limits.

3. 4

Inspection Findings

3. 4. 1

Immediate Actions and Corrective Actions

On February 6, 1992, the*licensee promptly reported the problem

with the MSIV actuator solenoids to the NRC and asked for a TWOC

t6 evaluate the problem and implement 6orrective action.

After

determining that the problem could not be repaired within the

available time, -the licensee shut down the plant two weeks prior

to a scheduled refueling outage.

The MSIV solenoid problem was

reported in LER 92-07 within the 30-day limit.

On February 25, 1992, the licensee completed a detailed review of

the contractor's report, which had contributed to the finding of

the MSIV solenoid problem.

This report included approximately

3

2500 items, which resulted in about 800 discrepancies with the

majority being'documentation problems.

The inspectors reviewed

about 10% of the licensee's review of the contractor's findings.

All of those items had been appropriately reviewed for

significance.

Seven Deviation Reports (DR) -Were written for-the

most significant problems.

The inspectors reviewed the DRs for

start up concerns and-determined that the resolutions were

adequate.

The licensee made modifications or appropriately

justified why operations could resume.

The licensee's corrective

actions for the several hundred documentation problems are

projected to be completed by the end of 1992; however, initiation

of corrective actions had just recently been started.

The modification to the MSIV solenoids, which was completed

during the recent refueling outage, did eliminate the specific

component environmental qualification (EQ) problems with the.

solenoids.

The MSIV solenoids were moved from the component

cooling water (CCW) room to an electrical switchgear room, which

is in a mild environment.

The inspector reviewed the MSIV

modification package and determined that it was comprehensive and

thorough.

A detailed evaluation was made that met the

requirements of 10 CFR 50.59.

The inspectors were initially

concerned that one set of solenoid valves was located in a non-

vital area; however, following additional reviews ~y the NRC, the

location was determined to be acceptable.

The licensee's efforts to improve the EQ.program were apparent in

that EQ and modification procedures had improved during the past

few years.

The inspectors determined that the procedures

contained information that will contribute to the licensee's

compliance with EQ requirements.

However, during the review of

the licensee's corrective actions the inspectors determined that

the station EQ Technical Group was understaffed to accomplish the

necessary improvements to the electrical environmental

qualification (EEQ) list and program in a timely manner.

There

was a high turnover of EQ staff for the past 7 years and very few

of the staff held the job for more than 1 year.

The experience

ievei of the staff was very low.

The in$pectors reviewed the EQ

staff training records and concluded that EQ training had not

been comprehensive.

However, the licensee had recently initiated

improvements to the EQ training.

The EEQ list and program were

being reviewed and improved by a person trained and dedicated to

that task.

On March 11, 1992, members of the licensee's staff came to Region

III for a management meeting to discuss operability issues for

the projected April 15, 1992, restart.

The licensee stated

during the meeting that there were plans for an extensive effort

similar to the CCP program to find any remaining Eti problems in

the plant.

The licensee also stated that future EQ efforts would

be documented in a letter to NRC on April 30, 1992_.

Following

4

additional NRC review of the significant issues, there were no

additional* concerrts for plant restart. *

3.4.2

Temporary Waiver of Compliance

.. As* noted *in Section 3. 4 .1, . on February 6, 1992, _the licensee

requested that the NRC grant a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> TWOC to.operate the plant

and *resolve the problem with the MSIV operator solenoids.

The

TWOC was granted based on the information provided by the

licensee and the low probability qf ri~k to *the plant.

However,

the licensee determined that the problem could not be fixed

during the TWOC time period, so the reactor was shut down 2 weeks

.*prior to. a. s'cheduleq 60 day refueling outage~

.

.

.

When the. licensee orally requested the TWOC they failed to

provide

information to the NRC.about the contractor's report,

which is discussed in Section 3.4.3. _The report contained othe~

EQ probl"ems that were potentially s*ignif icant.

The NRC' s. *

deci~ion to grant the TWOC may not have occurre~ had -the NRC

known about the additional EQ discrep~ncies~

In addition,

neither the subsequently wtitten-TWOC, nor LER 92-07, mention the

matters.discussed in the contract~r's report.

Failur~ to provide

complete and accurate information.to the NRC is an .apparent

. violation bf 10 CFR 50.9. (255/92011-0l(DRS))

.3.4.3*.

Licensee's Response to a Contractor's Review of EQ

Problems

As a result of EEQ problems the licensee initiated a contractor

review of EQ problems.

In December 19go~ the contrac~6r issued a

report to.the licensee.

The report, indicated that there.were

approximately 2500 problems*with 63'listed as potent~ally*

~ignifiqant. ~Throu~h interviews with licensee personnel, the

inspectors determined that upon rec~ipt of the report, the

licensee performe'd a cursory review of the report but found no

-apparent significant problems, so no actions were taken.

on

March 14,. 1991, the plant was returned to service following a six

  • .month outage without .the iicensee having fully evaluated the

probiems in the report.

The licensee's reviewer had an item on

his "things to do iist"' to review and corr~ct the problems found

by the contractor, which he considered to be do.cumentation

discrepancies.

The report remained with the reviewer even after

-a plant staff reorganization in May 1991.

In December 1991, the repo~t w~s ~u~ned oVer to the site EQ

  • improvement person for review after the CCP identified a

discrepancy that also appeared _in the contractor's rep6rt.

This

occurred 12 months after the contr~ctor's.report was issued.

On

February 5, ~992i during the review of the contractor's report,

the licensee identified the MSIV control circuitry problem.

A

short in the MSIV solenoid or circuitry due to a steam line break

in the CCW room could rerider the turbine.building solenoids

5

, ,'

inoperable. because both sets of solenoids share a common pow.er

supply.

This problem was found as a result of reviewing

schematic diagram E~238 SH.1, for the MSIVs. *The problem was

also noted in the contractor's report as a discrepancy with an

'unqualified hand switch in the MSIV operator solenoid circuit.

On Febrriary 25, 1992, the licensee b6mpleted a detailed review of

the contractor's EQ report.

As a result, DRs were written on the

following equipment: residual heat exchanger temperature

elements, pressurizer level Jnstrumentation, main steam line

radiation moriitors, component cabling water heat exchanger

  • solenoid valves and position switches, and feed water system

motor operated valves.

These problems were reported to the NRC

in LERs.

As indicated in this Section, and in Sections 3.4.1 and 3.4.5, it

appears that the licensee did not perform adequate corrective

actions *to d°isp.osition EQ problems. in a timely* manner even though

the contractor's repoit contained ~vidende of EQ discrepaneies

and was available to the licensee for over 1 year~ This is an

apparent violation of 10 CFR 50 Appendix B, Criterion XVI,

Corrective Actions. (255/92011-02(DRS))

3.4.4

Background Facts on the MSIV Actuator Solenoids

In 1973, the Atomic Energy .commission -(AEC) identified a concern

with high energy.line breaks (HELB) outside containment.

The

MSIV solenoid val~es, locat~d inside the CCW room, were not

qualified for -the postulated environmental conditions*of*a break

of the main steam line which passes through this room.

The

licensee's response in "Special Report No. 6, 11 dated1973,

committed to install a redundant set of solenoid*valves outside

.the CCW room to isolate ~nd vent air from MSIV operators!. In

_1974~ a spare set of MSIV operator solenoid valves was iristalled

in the turbine building for the high energy line break conditioh.

In 1979, the licensee developed the initial EEQ list in iesp6nse

ta~RC'Bulletin 79-01.

At that time the MSIV operator solenoid

v~l~es were on the EEQ list.

Two years later, they were removed

from the EEQ list because the redundant solenoid valves were

considered to be in a non-harsh environment.

In 1984, during

reviews to meet the requirements of the EQ Rule, 10 CFR 50.49,

the licensee took credit for the MSIV operator solenoid v~lves in

the turbine building; therefore, EQ requirements-were not

considered necessary.

However, the licensee failed to evaluate

the electrical design, which did not meet the single failure

requirements.

A HELB in* the turbine building c.ould. cause. the.

solenoid valves to short circuit, blow a fuse, ~nd disable both

sets of scilerioid valves, which rec~jved voltage from the same

source.

6

\\. .

3.4.5

History of Equipment Environmental Qualification (EQ)

Problems

Numerous EQ problems have occurred at Palisades since

November 30,. 1985, when licensees were required to meet EQ

requirements and be in full compliance to 10 CFR 50.49.

In

December 1986, the NRC identified eight significant EQ

  • deficiencies at Palisades.

Two violations and a civil penalty

were issued to the licensee regarding EQ problems with 55

transmitters, 38 solenoids, and 15 motor-operated valve

actuators.

A violation was issued after an inspection in March

1990 when an EQ problem was found' with two relays installed in

the auxiliary feedwater control circuitry, and action was not

taken to adequately resolve a violation identified in 1986.

In

1992, EQ problems were identified with eight electrical splices

and a violation was issued because the licensee.failed to take

adequate corrective action to resolve a previously identified EQ

problem.

In January 1989, the NRC issued Information Notice 88-

86,

Suppl~ment 1, which specifically described the adverse

conditions with solenoid valves that could be caused by high

energy line breaks.

The licensee reviewed the situation but did

not include the MSIV operator solenoid valves because they were

not on the EEQ list.

The NRC issued.numerous other Information

Notices, Bulletins, and inspection reports on EQ.

The inspectors reviewed the licensee's self-assessment ~ctivities

for the EQ area.

The inspectors found that even though the plant

had problems in the EQ area since 1985, the licensee had only

performed one EQ quality assurance (QA) audit since that time.

The audit was performed in March 1991.

This audit had been

previously evaluated in NRC Inspection Report 50-255/92003, as a

QA audit with a very limited scope.

Based on all of the previous

problems in the EQ area it appeared to the inspectors that the

audit should have been much broader in scope.

4.0

Exit Meeting

The inspectors met with the licensee at the site on March 27,

1992, for an interim exit and on April 16, 1992, for a final exit

to summarize the purpose, scope, and findings of the inspection.

A verbal summary of the inspection findings was provided to the

licensee at that time.

The inspectors discussed the likely

informational content of the inspection report with regard to

documents or processes reviewed by the inspectors during the

inspection.

The licensee did not identify any such documents or

processes as proprietary .

7