ML18057A446

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Insp Rept 50-255/90-17 on 900730-0803.No Violations Noted. Major Areas Inspected:Adequacy of Evaluations Performed,Per 10CFR50.59 W/Primary Focus on Steam Generator Replacement Project
ML18057A446
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/29/1990
From: Hasse R, Phillips M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18057A445 List:
References
50-255-90-17, NUDOCS 9009070208
Download: ML18057A446 (14)


See also: IR 05000255/1990017

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Report No. 50-255/90017(DRS)

Docket No. 50-255

Licensee:

Consumers Power Company

1945 West Parnall Road

Jackson, MI

49201

Facility Name:

Palisades Site

Inspection At:

Covert, MI 49043

Inspection Conduc~~:

J~ly 30

Inspectors: ~a"S~I

Team Leader

8. Holian, NRR

R. Anand, NRR

G. Tan, NRR

E. Murphy, NRR

T. Rotella, NRR

August 3, 1990

Approved By~~hief

Operational Programs Section

Inspection Summary

License No. DPR-20

Date

I

Inspection on July 30 - August 3, 1990 (Report No. 50-255/90017(DRS)).

Areas Inspected:

Special, announced inspection of the adequacy of evaluations

performed pursuant to 10 CFR Part 50, Section 59 with primary focus on the

Steam Generatof Replacement Project (SGRP).

This inspection was conducted in

accordance with Inspection Module 37700.

Results:

No violations were identified.

The engineering supporting the SGRP

was ~uite thorough.

Some ~eaknesses were identified in the 10 CFR 50.59

evaluations with the primary concern being the failure to identify when

associated Technical Specification changes were required .

~: ~~',;:; ') (1 ~~ ;;~ ;~; g

~}:

I)

DETAILS

1.

Persons Contacted*

D. Joos, Vice President, ESSD

D. Vandewalle, Plant Technical Director

J. Kuemin, Plant Licensing

B. Gerling, Accident and Transient Analysis Supervisor

R. Rice, Operations Manager

R. Vincent, Plant Safety Engineering (PSE) Administrator

P. Bruce, PSE

J. Erickson, PSE

K. Toner, Projects Superintendent

T. Tai, Nuclea~ Support (Bechtel)

J. Lewis~ Steam Generator Replacement Project Licensing

US-NUCLEAR REGULATORY COMMISSION (NRC)

  • J. Zwolinski, Assistant Director for Region III Reactors, DRSP

R. Pierson, Director, Project Directorate III-I, DRSP

  • E. Swanson, Senior Resident Inspector

J. Heller, Resident Inspector

  • With these exceptions, all personnel listed above attended the exit

interview held on August 3, 1990.

2.

.Introduction

The purpose of this inspection was to determine the adequacy of the

licensees evaluations performed pursuant to 10 CFR Part 50, Sectton 59.

This regulation allows the licensee to make c_hanges to the facility as

described in the FSAR, revise procedures described in the FSAR, or

perform tests and experiments not described in the FSAR without prior

NRC approval as long as no unreview~d safety question is generated or

technical spetification changes are required.

It also requires the

licensee to document the bases for concluding that these requirements

have been met when making changes pursuant to this regulation.

The inspection focused primarily on the licensee's steam generator

replacement project (SGRP).

A small effort was devoted to a review of

the l.O CFR 50.59 evaluations for changes submitted to the NRC pursuant

to 10 CFR 50.71 {annual FSAR updates).

The safety evaluations {which encompass the 10 CFR 50.59 evaluations)

for the SGRP reviewed by the inspectors had been prepared by the

licensee's contractor (Bechtel).

The licensee's review and approval of

these documents. had not been completed; therefore, it was necessary to

treat these as draft documents from a regulatory standpoint. This is

pertinent because they contained erroneous conclusions with respect to

technical specification changes required prior to plant startup (see

Paragraph 3.m).

Had these conclusions been final, they would represent

inadequacies in the 10 CFR 50.59 evaluation and a potential violation.

2

3.

-

Steam Generator Replacement Project (SGRP)

The SGRP consisted of a series of facility change (FC) packages plus

several packages not falling within the definition of a facility change

(e.g., rigging for SG lifts and the interim storage facility for the old

SGs).

Each package was supported by its own safety evaluation (SE). The

inspectors reviewed the SEs, FCs, and supporting analyses to determine

if any unreviewed safety questions were generated or technical

specification changes not previously identified would be required.

The

results of these reviews are discussed in the following paragraphs.

a.

FC-909, "Steam Generator Replacement"

This facility change encompassed the removal of the existing Steam

Generators (SGs) and the impact of the installation of the new

steam generators. Section 1.0 of the Safety Evaluation (SE)

supporting this change provided a description of the effects of

the replacement SGs on normal plant operation and the Palisades

Final Safety Analysis Report (FSAR) accident and transient

analysis. Systems interactions were also discussed. Sections 2.0

and 3.0 addressed the decontamination and coating of the existing

SGs and the installation of nozzle cover plates prior to SG

removal from containment.

Consumers Power Company (CPCo)

concluded that the overall SG performance changes associated with

the replacement SGs would not adversely affect current FSAR

conclusions or plant performance ~equirements .

Specifi~ areas reviewed by the inspector in~luded the impact on

net positive suction head (NPSH) for the reactor coolant pumps

(RCP) and the*affected transient .analyses.

The accidents

determined to require reanalysis were the Main Steam Line Break

(MSLB) and Stea~ Generator Tube Rupt~re (SGTR).

Certain specific

references, delineated for RCP NPSH considerations, and the MSLB

and SGTR accidents were examined in detail. A discussion of the

findings for FC~909 is provided below.

It should be noted with respect to FC-909 that the package did not

include a signed Design Input Checklist nor a completed Design

Review Sign Off.

However, the supporting documentation including

references were provided to the inspector with the proper .

signatures.

(1)

Reactor Coolant Pump NPSH and Core Uplift

The replacement SGs, which were manufactured by Combustion

Engineering (CE), are designed to physically match the

essential parameters of the existing SGs.

The replacement

_ SGs should ~losely duplicate the physical, thermal, and

hydraulic characteristics of the original SGs while *

ihcorporating a combination of design improvements.

The

overall heat transfer coefficient, U, times the tube area

available for heat transfer, A, is the same as the existing

3

SGs (i.e., (UA) original= (UA) *new).

Therefore, the design

limits of operationally interconnected plant systems should

be minimally affected.

The most significant effect of the

new SGs would be on primary coolant system (PCS) flow.

PCS

loop flow would be increased due to a decrease in

differential pressure across the new SGs.

Although the flow

increase would be primarily beneficial (e.g., fuel heat

transfer) other parameters such as RCP motor effects, core

upl.ift forces and RCP av~ilable NPSH must be evaluated.

The

inspector reviewed the licensee's calculations supporting

RCP NPSH and ~ore uplift considerations.

The calculations

adequately addressed both the RCP NPSH and core uplift

concern~. Starting of the fourth RCP should not occur until

RCS temperature reaches 450°F.

This is a change from

current operating practice but will not effect the Technical

Specifications.

(2)

Final Safety Analysis Report (FSAR) Accident Reanalyses

Section 1.3 of FC-909 provid~d an evaluation of the effects

of th~ replacement SGs on the FSAR accident and transient

analyses.

CPCo concluded that based on the results of a

disposition-of~events review and the detailed reanalysis of

main steam line break and SG tube rupture accidents that no

unreviewed safety questions would exist due to operation

with the replacement SGs .

(a)

Steam Generator Tube Rupture

Reference 17 of FC-909 provided a reanalysis of the

Palisades Steam Generator Tube Rupture Accident.

Although the outside diameter of the new SG tubes

would be unchanged (0.750 inches), the inside *diameter

has increased by 0.012 inches.

CPCo stated that the

SG tube rupture event with a loss of offsite power

upon reactor trip was reanalyzed in accordance with

the guidelines of SRP 15.6.3.

The results of the.

reanalysis indicated that the slightly larger inside

diameter of the U-tubes is not a significant factor in

the analysis. Rather, it was found that the

differences in methodology between the FSAR analysis-

of-record and CE's current analysis methodology had a

gr~ater impact on.the results.

During a presentation by CPCo on* June 6, 1990 and

during this inspection, the inspector questione.d the.

use of minimum primary coolant system pressure as an

assumption in the reanalysis of the worst case SGTR.

On August 3, 1990 a conference call.between CPCo, CE,

and the NRC was conducted to ascertain the basis for

this assumption.

CE representatives stated that the

assumption of minimum primary coolant system pressure

4

(b)

for the limiting SGTR accident was in error and was

nonconservative for Palisades.

CE realized this

nonconservative assumption subsequent to the June 6,

1990 presentation to the staff but prior to this

inspection and had corrected their error. The SGTR

reanalysis documentation provided during the

.

inspection was claimed by CE to have delineated this

change.

However, the inspector found the reanalysis

to be unclear in this regard. CPCo agreed with the NRC

on this point.

The results of the reanalysis

demonstrated that all *calculated doses remained within

General Design Criterion 19 guidelines and within 10

CFR Part 100 acceptance criteria. Therefore, the

inspector found the 10 CFR 50.59 supporting reanalysis

to be acceptable because the Palisades licensing basis

stated that .the acceptance criterion for the SGTR

accident is 10 CFR Part 100.

Main Stem Line Break (MSLB)

Reference 18 of FC-909 provided a reanalysis of the

worst case MSLB.

During the inspection, several

discussions were held with CPCo to ascertain the basis

of certain assumptions used in the reanalysis

including the reliance on conclusions made by CPCo in

a 1985 submittal. to the NRC addressing single failure

issues .. The staff S~R referenced in the MSLB

-

reanalysis addressing CPCo's submittal is entitled,

"Single Failure Issues for Main Steam Isolation Valves

and Main Feedwater Isolation Valves," dated February

28, 1986.

As a result of the MSLB reanalysis, iri March 1990, CE

identified that the worst case MSLB for Palisades was

-not a double-ended 100 percent break,. as was

previously believe_d, but a small break (approximately.

30%).

Corrective action by tPCo was to install a

.containment high pressure (CHP) initiated feedwater

regulating valve closure actuation circuitry to

provide a quicker response to the transient.

The 30

percent break size results in a higher peak .

containment pressure due to the delay in receiving a

low SG pressure initiated feedwater valve closure.

The new SGs have a nozzle on the steam outlet which

limits a full double-ended MSLB to a 30 percent

blowdown.

The CHP-initiated feedwater valve closure

modification provides feedwater isolation in time to

limit the peak containment pressure to 52.45 psig

which is below.the Palisades containment design limit

of 55 psig and below the previous MSLB analysis-of-

record peak containment pressure of 54.1 psig.

5

The inspector concluded that the FC-909 supporting *

reanalysis for MSLB does not present an unreviewed

safety question. Also, during the inspection, CPCo

committed to amend the Palisades Technical

Specifications to include the feedwater regulating

valve CHP actuation logic and the Low SG Pressure.

Surveillance Requirements (SR).

The SR frequencies

will be consistent with other safety related

equipment.

(3)

Impact on Technical Specificitions

Section 4.14 of the Palisades Technical Specification

specifies the plugging limits (acceptance criteria) to

be applied to the results of steam generator tube*

-

inspections. These limits were developed spetifically

for the 0.75 inch diameter x 0.48 thick tubes in the

existing SGs.

These limits are not appropriate for

the 0.75 inch diameter X 0.042 thick tubes in the new

SGs.

The licensee stated on page 43 of the attachment

to the safetj analysis for Facility Change 909) that

it would propose a new 40% wall thinning plugging

. limit, consistent with the ASME Code,Section XI, for

inclusion in the Technical Specifications.

Plugging limits w~re not an issue duri~g the

preservice inspection of the new steam generators

(discussed on page 38 of the attachment to the safety

analysis) since no tubing flaws were found.

However,

experience indicates that tubing flaws can develop

durinij the initial operating cycle.

New plugging

limits should be in place prior to the first inservice

inspection (ISI) to ensure that any flaws found are

assessed ~gainst criteria appropriate to the new SGs.

The licensee planned to submit a proposed Technical

Specification change to incorporate new plugging

limits prior to.the first ISi of SG tubes.

The SG replacement program did not require a change to

the inspection frequency and sampling requirements in

Section 4.14 of the Technical Specifications.

Nevertheless, the licensee planned to propose-updated

requirements in this area, consistent with Standard

Technical Specification requirements.

b.

FC-912, "Auxiliary Feedwater System Piping Modification"

This facility change involved a portion of the existing auxiliary

feedwater system piping to be rerouted to accommodate the location

of the new steam generator auxiliary feedwater nozzles.

The 3"

and 4" diameter auxiliary feedwater piping from the steam

generator nozzles would be removed back approximately 5 feet at

6

. I

steam generator E50A and approximately 11 feet at steam generator

E50B.

These lines would be shortened approximately 20 inches and

reoriented approximately 7 1/2 degrees from the old steam

generator nozzle locations to fit the new steam generator nozzles.

The modification was being performed under ASME B&PV Code, Section

XI.

The new piping was designed to meet seismic category I

requirements and was to be in accordance with the codes and

standards required by FSAR Table 5.2-3.

The piping was procured

in accordance with ASMt Section III, Class 2 requirements.

The licensee had analyzed for potential new pipe break locations.

No new jet impingement or pipe whip targets were identified.

The

auxiliary feedwater line would be rerouted to minimize horizontal*

runs to prevent water hammer in the auxiliary feedwater system.

The new position of the piping being installed had been evaluated

to assure that the stress levels would not exceed code allowable.

The licensee's analyses indicated .that the removal and subsequent

replacement of the auxiliary feedwater lines would not constitute

an unreviewed safety questions.

c.

FC-893, "Blowdowh Piping Modification

This facility change involved the replacement of the 2 inch

nominal

pip~ size (NPS) steam generator bottom blowdown system

- piping with 4 inch NPS piping from the steam generatqr nozzle up

to but not including the containment isolatitin valve outside

containment.

The replacement would consist of removing the

existing 2" piping and associated supports and installing new 4"

piping, pipe supports and thermal insulation.

High point vents,

low point drains, and sample connections were alsd to be added.

Although the existing piping had been uninsulated, the replacement

piping would be insulated with a flexible insulation to prevent

any increase in heat load due to the ihcreas~d heat transfer area.

Modifications to the blowdown piping outside containment beyond

-

the isolation valve would be made later.

The piping and piping supports were designed as seismic Category I

in accordance with the requirements of ASME Section XI.

The

existing containment penetration was to be ~odified to accept a 4"

pipe.

The licensee had analyzed the penetration sleeve to

demonstrate that it w_as capable of carrying the design loads

associated with the 4" pipe. Also, the licensee performed

calculations to ensure that the*concrete temperature around the

penetration remained within acceptable limits.

The licensee's

analysis postulated pipe breaks in accordance with the high energy

line break (HELB) criteria given in FSAR Section 5.6. The

analysis concluded that a HELB in the replacement 4 inche pi~e

would not increase the consequence of an accident as it relates to

the containment temperature or pressure responses.

Pipe whi~ and

7

jet impingement targets had been identified and whip restraints

were to be added where the consequences of unrestrained whip were

unacceptable.

The existing structures have been evaluated for the

additional loads.

The licensee had committed to perform

nondestructive examination (NDE) of all welds performed during

this modification. All butt welds in piping were to be 100%

radiographed and ex_amined by liquid penetrant or magnetic particle

techniques.

Based on the above, the inspectors concluded that the replacement

and/or modification of the blowdown piping did not involve an

unreview~d safety question.

The licensee committed to amend the

plant Technical Specifications to revise the containment

penetration description.

d.

FC-894, "Replace Existing Surface Slowdown Pipe With 4" SG

Recirculation Pipe"

This facility change involved the replacem~nt of the 2 inch

nominal pipe size (NPS) steam generator surface blowdown system

piping with 4" NPS piping from the steam generator nozzle up to.

but not including the containment isolation valve outside the

containment.

A1so, high point vents and low point dr~ins would be

provided in the new piping. Since the system .would only be used

during cold shutdown, only the line from the steam generator to

the containment shield wall was to be insulated.

The tirculation system is a non-safety system-except the portions

from the steam generators to the containment isolation valves (CV-

739 for steam generator 50A and CV-738 for steam generator 508),

which is designed as seismic Category I. Modification to the

recirculation lines outside the containment beyond the isolation

valve was to be made later.

The licensee had postulated pipe breaks in accordance with the

high energy line break (HELB) criteria. Pipe whip and jet

. impingement targets had been identified and whip restraints were

  • to be added.

The existing containment penetration was to be

,

modified to accept a 4" pipe.

The penetration sleeve had been

analyzed to.demonstrate that it was capable of carrying the design

loads associated with the larger pipe.

The existing structures

had been evaluated for the additional loads imposed by the new

pipe supports.

The* licensee committed to perform non-destructive

examinatio~ (NDE) of all welds performed during this modification.

All butt welds in the piping were to be 100% radiographed and

examined by liquid penetrant or magnetic particle techniques.

Based on the above, the inspectors concluded that the replacement

and/or modification of the recirculation piping did not involve an

unreviewed safety question.

The licensee committed to amend the

plant Technical Specification to revise the containment

penetration description.

8

e.

FC-915, "Component Cooling Water (CCWl Surge Tank Room

Modifications"

This FC provided for an opening of approximately 48" by 21" in the

ceiling of the CCW surge tank room and drilling a 2" hole in the

floor of the room.

The room would be returned to its original

configuration after the SGRP was completed.

The openings were

required to provide ~quipment access to the containment post-

tensioning system tendons located on the west side of containment

buttress B.

The inspector reviewed the FC package, the SE, and toured the

affected area. Several concerns were identified with the SE:

o

The SE did not address the potential for *the release of*

airborne radioactivity through these openings ..

o

Some potential .for damage to the CCW surge tank and other .

components in this area exists while thg. de-tensioning

process is in progress.

The heat load on the CCW system

during this period were not addressed in the SE.

The SE *

noted that the surge tank was required only for "long term"

CCW operatio~. The duration of "long term" or heat loads

during that period wee not addressed;

Further, no

contingency actions were identified if damage to the CCW

system should occur.

The incorporation of these issues into the SE will be tracked as

an open item (255/90017-01).

f.

. FC-910, PCS Piping Replacement

The facility change involved modification of Primary Coolant

System (PCS) piping to facilitate steam generator (SG)

replacement.

T~is included replacing the first cold leg elbow at

each SG outlet nozile and cutting each hot leg pipe at the SG

nozzle weld and machining the pipe ends to accept the new SG~.

One or both hot leg elbows. were to be replaced if necessary to

facilitate SG replacement.

The pipe-to-elbow and elbow-to-SG

nozzle circumferential butt welds would employ the GTAW process

and were to be accomplished by automatic welding machines using a

"narrow gap" welding procedure.

The inspectors reviewed both the facility change package and the

accompanying safety evaluation.

Inspector review activities at

the site were supplemented by a review by NRR headquarters

personnel (from the Materials and Chemical Engineering Branch) of

the narrow gap welding technique and the ongoing program to

qualify this technique in accordance with ASME Code,Section IX

requirements.

9

The inspector's review uncovered no issues involving either a

potential unreviewed safety question or a need for changes to the

Technical Specifications.

g.

FC-911, "Main Steam Piping"

This facility change involved removal and subsequent replacement

of the main steam line to accommodate the replacement of the SGs:

Removal was to be accomplished by cutting the steam line at the SG

main steam nozzle and in the vertical riser section. During

reinst~llation, the vertical riser portion would be extended

approximately 32 inches to compensate for the added height*of the

replacement SGs due to the incorporation of a flow restrictor at

the main steam nozzle.

The inspectors reviewed the facility change package, including the

Design Input Checklist and Design Documents Checklist, and the

associated 10 CFR 50.59 safety evaluation.

No areas of concern

were identified.

The inspectors nqted that internal reviews of

the facility change package had not yet been completed by Bechtel

and CPCo.

In addition, certain pipe support drawings and

mechanical and civil calculations, as identified on sheets 7, 8,

and 9 of the Design Document Checklist, had yet to be incorporated

into the package.

The inspectors review of Facility Change 911 uncovered no issues

involvin~ either a potentlal unreviewed safety question or a

potential need for changes to the Technical Specifications.

h.

FC-914, "Containment Construction Opening"

This FC provides for the installation of a 28' by 26' opening in

the containment structure to permit the removal of the existing

SGs from the containment and transfer of the new SGs into the

containment.

The containment will be returned to its original

condition following the completion of the SG transfer.

The inspectors focused their review of this FC package and SE on

the finite element analyses for various loads and load

combinations during the existence of the containment opening and

after its closure.

The inspectors concluded that the licensee had

made a comprehensive and thorough analysis of the containment

during the existence of the opening and after its closure;

however, some concerns were identified that still needed to be

addressed:

o

There was a large discrepancy between the stress levels

calculated at the containment foundation by two different

analyses. This discrepancy should be reconciled or the

larger valves should be used to determine if the stress

levels are acceptable.

10

o

The finite element stress analysis of the containment

averaged stresses in adjacent elements (i.e., an overstress

in one element was averaged with understresses in adjacent

elements).

The basis for the acceptability of this

technique should be provided.

o

The results of the tests performed by the licensee on the

concrete mix to be used to close the containment opening

should be provided to sup.port the creep and shrinkage va 1 ues

used in the analysis of the reconstructed portion of the

containment.

o

The containment liner will. be cut as a part of the process

for providing the containment opening.

The section removed

will be welded back in place.

An analysis should be

.

performed to demonstrate the structural integrity of the

repaired *1ining.

o

The reinforcing steel used in the reconstructed area was to

be spliced to existing reinforcing steel via Cadweld

splicing. Assurance should be provided that the relative

location of these splices in adjacent bars does not

jeopardize the structural integrity of the containment.

o

It would be necessary to remove the containment prestressing

tendons which would cross the containment opening.

These

tendons will be inspected and the undamaged ones re~sed. An

analysis should be performed to show that the creep and

relaxation that has occurred in thes~ tendons will not

result in an increase in prestress loss after reinstallation

and tensioning.

-

o

The prestressing tendons are contained in a sheathing which

i~ filled with grease for corrosion protection of the

tendons. The sheathing crossing the containment openirig will

be removed and discarded: New sheathing will be installed

in this ar_ea when the open*ing is closed.

The details of

connecting the new sheathing to the existing sheathing

should be provided.

o

It will be necessary to withdraw some tendons from their

sheathing and then reinsert it. The potential for damaging

this sheathing should be addressed.

o

The integrity of the Cadwell splices of the reinforcing bars

is very important~ Mockup training on the installatiori of

these splices should be provided.

o

The licensee plans to perform a structural integrity test

(SIT) at 115% of containment design pressure after repairing

the containment.

The effect of this test on containment

integrity considering the loss of prestress in the

11

undisturbed tendons (which will riot be retensioned) should

be evaluated.

The resolution of th~se concerns will be tracked as an open item

(255/90017-02).

i.

FC-904, "Auxiliary Building Modification for Containment Access"

This FC provided for a 6'-6" by 7'-2" personnel and equipment

.

access opening in the auxiliary building east wall. The wall would

be returned to its original configuration upon completion of the

SGRP.

The inspectors reviewed the FC package and SE.

One concern

was identified. The SE failed to address the potential release bf

airborne radioactivity via the access opening.

The resolution of this concern will be tracked as an open item

(255/90017-03).

j.

FC-895, "Wide Range Instrumentation* Tubing"

This FC revised the configuration of the SG wide range

instrumentation tubing. This modification was necessary because

of the different configuration-of the instrumentation taps dn th~

new SGs.

The inspectors reviewed the FC package and associated SE.

The

only operationally ~ignificant change was increasing the wide

range level readings from -138% - +100% to -140% - +150%.

No unreviewed safety question or Technical Specification changes

were identified.

k;

FC-913, "Secondary Sample System Piping"

This FC added sampling points to the new SG blpwdown p1p1ng and at

the sampling connections on each SG.

Rerouting of sample lines

was also required beca~~e of configurational differences between

the old and new SGs.

The inspector reviewed the SE for this FC and identified no

unreviewed safety question or Technical Specification changes.

1.

Other SGRP Support Activities

The inspectors reviewed the FCs and associated SEs for two

activities not directly affecting the plant:

(1) the installation

of a feinforced earth retaining wall outside the containment

structure (FC-903); and (2) the construction of cast-in-place

reinforced spread footings to support the lift system outside

containment (FC-908).

These packages were reviewed to assess any

potential impact on plant facilities in the vicinity.

12

m.

These facilities appeared to be well engineered and no concerns

were identified,

Summary of Technical Specification Changes Required as a Result of .

the SGRP.

There were six Technical Specifications (TS) that need to be

addrssed as a result of the SGRP.

The licensee addressed these

changes in the SE for FC-909, "Steam Generator Replacement."

The

SE concluded that none of these changes were required before

startup with the new SGs.

This conclusion was in error,and

contrary to the requirements of 10 CFR 50.59, which states that

prior NRC approval is required if an applicable TS change is

involved.

The TS chahges and when they are applicable are

discussed below:

o

TS 2.3.l, Item 5

This TS specifies the low SG level trip setpoint to be "not

lower than the centerline of the feedwater ring which is

6'0" below the normal water level." The feedwater ring in

the *new SGs is 5'8" below the normal water level. The. *

location of the feedwater ring must be revised.

The basis

for this TS is unchanged and there is no apparent impact on

any margin.

Since this TS is applicable during operation, it must be*

revised prior to startup.

o

TS 3.1.5.d

This TS specifies that the primary-to-secondary leakage in a

steam generator must not exceed 0.3 gpm.

The basis for this

TS is a maximum throu~h wall track in a SG tube of 1/4"

superimposed on a 64% wasted area.

This assures structural

integrity of the tube.

The licensee plans to change the

basis to be consistent with IWB-3521 of ASME Section XI.

This specifies that the maximum through wall crack assure

structural integrity if superimposed on a 40% wasted area of

a tube.

(This basis is tied to TS 4.14 which specifies the

maximum permissible wall thinning.

As such, it would be

updated coincident with the update of TS 4.14.)

o

TS Table 3.5.l

This table lists the containment penetrations and valves;

including the line sizes .. The line sites for the SG

blowdown and recirculation systems must be revised. This TS

is applicable during operations and must be changed prior to

startup.

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o

TS 4.4;a

This TS specifies that the4P across the SG tubes must not

exceed 1380 psi.

The basis for this TS is to prevent a tube

rupture assuming a 64% wasting of a tube wall (originally

0.048" thick).

The licensee plans to change this basis to a

40% wasting of a tube wall to be consistent with ASME

Section XI.

This TS would be conservative as it currently reads on

startup. It would continue- to be conservative after TS 4.14

is changed.

o

TS 4.14

Among other issues, this TS specifies the maximum tube

wastage (thinning) allowable for the SGs.

Since the new SGs

have tubes with thinner walls (0.042" vs 0.048"), this TS

must be changed before the first ISI of the SG tubes.

o

TS 5.3.1.a

This TS states the codes and editions for the p1p1ng systems

and components.

This must be revised to reflect the later

editions used for the new SGs and replacement piping. This

TS applies during operation and must be changed prior to

startup.

-

The licensee agreed to submit the TS change requests commensurate

with the required dates.

The revision of the SE for FC-909 to reflect the required schedule

for TS changes will be track~d as an open item {50-255/90017-04).

4.

FSAR Updates

A sampling of modification packages and drawing changes from the most

recent FSAR update (Rev. 10) were reviewed to determine if all aspects

of the changes were addressed.

No discrepancies were noted.

5.

Open Items

Open items are matters which have been discussed with the* licensee which

will be reviewed further by the inspectors, and which involve some

action on the part of the NRC or licensee or both.

Open items disclosed

during the inspection are discussed in Paragraphs 3.e, 3.h, 3.i, an 3.m.

6.

Exit Interview

The inspectors met with licensee representatives (denoted in Paragraph

1) at the conclusion of the inspection on August 3, 1990, and summarized

the purpose, scope and findings of the inspection.

The licensee stated

that the inspectors had no access to proprietary information.

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