05000255/LER-1981-005, Forwards LER 81-005/01L-0

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Forwards LER 81-005/01L-0
ML18046A402
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/16/1981
From: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18046A403 List:
References
NUDOCS 8102190567
Download: ML18046A402 (3)


LER-1981-005, Forwards LER 81-005/01L-0
Event date:
Report date:
2551981005R00 - NRC Website

text

consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201 * (517) 788-0550 February l6, l98l Mr James G Keppler Office of Inspection and Enforcement Region III U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60l27 DOCKET 50-255 - DPR PALISADES PLANT -

LICENSEE EVENT REPORT 81 INOPERABLE DIESEL GENERATOR On the reverse side in LER 81-005 which is reportable under Technical Specifi-cations 6.9.2.B(2).

David P Hoffman Nuclear Licensing Administrator cc Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector, Palisades Plant s

fEB 191981

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rr::IIJ I During normal plant operation, conper tubing to PS-1473 __ (1-2 diesel-

~I generator service water low pressure alarm) broke.

To make repairs.

the diesel generator was made inoperable;* as a result, the LCO of TS

[§))] 1 3.7.21 was entered.

Engine was restored to operable status within time__J

((TI] I required by 'I'S 3.7.2I~ Eyent*not repetitjye.

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I During normal Dlant oDeration, coDper tubing to PS-1473 (l-2 diesel-

[III] I gener"tor service water low b1"essure a 1 am) broke.

To ma.'lce.,.eDairs.

the diesel generator was made inouerable;* as a result. the LCO of TS 3.J.2I was entered.

Engine was restored to operable status within time reauired bir TS 3.7.2L Event not -..ew:)+;i-;-,iye.

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