05000255/LER-1980-026, Forwards LER 80-026/03L-0

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Forwards LER 80-026/03L-0
ML18045A520
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/18/1980
From: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18045A521 List:
References
NUDOCS 8008220233
Download: ML18045A520 (2)


LER-1980-026, Forwards LER 80-026/03L-0
Event date:
Report date:
2551980026R00 - NRC Website

text

General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201 * (517) 788-0650 August 18, 1980 Mr James G Keppler Office of Inspection and Enforcement Region III U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LICENSEE EVENT REPORT 80-026 - INOPERABLE HPSI FLOW INSTRUMENT On the reverse side is Licensee Event Report 80-026 which is reportable under Technical Specification 6.9.2.B.2.

~G.~

David P Hoffman Nuclear Licensing Administrator CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector - Palisades s

j' PALISADES PLANT NRC FORM366 17*771 U.S. NUCLEAR REGULATORY COMMISSION LICENSE*E EVENT REPORT CONTROL BLOCK: I I G)

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

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LICENSEE CODE 14

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ZS Ll~ENSE. TYPE 30 57 CAT 58 CON"T

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&O 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE BD EVENT DESCRIPTION AND PROBABLE CONSEQUENCES @

((IT] I During refilling of Saf'ety In,1ection tanks f'ollowing sampling, it was I))!] I observed. that FT-0313 (HSPI f'low to loop 2B) was inoperable.

Instrument

~I was restored to operable status within time required by LCO of' TS 3.17.

[IITJ I (See LER 80-13. )

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SYSTEM

CAUSE

CAUSE COMP.

VALVe CODE CODE SUBCODE COMPONENT CODE.

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9 10 11 12 13 18 19 20

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LERIRO CVENTYEAR

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REPORT I 8 I 01

  • NUMBER 21 22 SEQUENTIAL OCCURRENCE REPORT REPORT NO.

CODE TYPE 10 121 61 I/I P 13 I

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Z3 24 26 27 28 29 3D 31 REVISION NO *.

lQJ 32 BO ACTION FUTURE EFFECT SHUTDOWN

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ATTACHMENT NPRD-4 PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORMliUB.

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CAUSE DESCRIPTION ANO CORAEC"rlVE ACTIONS @

((ill I Following the most recent calibration of FT-0313 in Sent. 79. the

.OJ:IJ I instrument equalizing valve was not closed.

Subsequent to Sept 79, the

.IJII] I procedure for calibrating HPSI now instrwnents has been reyised to reguire o::IIl I verification of valve alignment during restoration to service.

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9 FACILITY

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METHOD OF

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STATUS "POWER OTHER STATUS ~ DISCOVERY DISCOVERY DESCRIPTION ~

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10 12 13 45 46 ACTIVITY CONTENT t.:::'I RELEASED OF RELEASE AMOUNT OF ACTIVITY IIE1 LIJ @) W@I NA I

7 B

9 ID 11 411 LOCATION OF RELEASE@

NA 45 so BO 80 PERSONNEL EXPOSURES t:::::..

NUMBER t:::;,, TYPE DESCRll"TION

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9 11 12 13 80 PERSONNEL INJURIES

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NUMBER DESCRll'TION~

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9 11 12 80 LOSS oc OR DAMAGE TO FACILITY '4J'I TYPE

DESCRIPTION

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ID 80 PUBLICITY C\\

NRC USE ON y ISSUED(.'.;\\ DESCRll'TION ~

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