LER-1979-017, Forwards LER 79-017/03L-0 |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2551979017R00 - NRC Website |
|
text
'
consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
- Area Code 517 788-0550 May 4, 1979 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT -
LER 79-017 On the reverse side is LER 79-017 which is reportable under Technical Specification 6.9.2.b.2.
David P Hoffman (Signed)
David P Hoffman Assistant Nuclear Licensing Administrator CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement 7905080531
Palisades NRC FORM366 17*771 U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: I I I G)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
~IMIIIP IAILl1IG)lolol -I go1010101-10101@14111111111©1 I 1© 7
8 9
LICENSEE CODE 14
~5 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T [ill]
7 8
~~~~~~ ~Io I 5 I o I o 1 o 12 f5 15 GI o 14 I o I 417 I 9 I© I o I 51 o 14 I 1 I 9 I@
60 61 DOCKET NUMBER 6EI 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
[§JI] I While taking battery voltage readings during an equalizing battery charge,1
()):!]I two cells in No. 2 station battery burst as a_result of the expJosion of [IIrJ I hydrogen inside the cells.
The battery was subsequently taken oµt of
()))) I service tci permit.jumpering of the defectiye cells.
Both battery chargers I (TI[] I for battery bus No. 2 were in operation as required by TS 3. 7. 2. 4.
This IIIIJ 1 event is reportable per TS 6.9.2.b.2.
Battery voltage and capacity with
((!!] I two jumpered cells is within specifications.
(Gould batt. Type FPS 17).
I 7
8 9 IIEl 7
8 SYSTEM CODE
!El C!@
9 10 C-;\\ LEA/RO LVENTYEAR
\\:,:/ REPORT 17 I 9 I NUMBER 21 22
CAUSE
CAUSE COMP.
CODE SUBCODE COMPONENT CODE SUBCODE L!J@ 12J@ I BI AIT IT fR I YI@ l!J@
11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REPORT NO.
CODE TYPE VALVE SU8CODE l!J@
20 I I Io 1111 I 1......-1 10 f 3 I
~ l=l 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN t::::;.,
ATTACHMENT NPRD-4 PRIME COMP, TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM :;ue, SUPPLIER UJ@W@ U.J@
UJ@)
I 01 o I 010 I 1!.J@
lliJ@
L!.J@
33 34 35 36 37 40 41 42 43
CAUSE
DESCRIPTION ANO CORREC'rlVE ACTIONS @
REVISION NO.
~
32 COMPONENT MANUFACTURER 80 I G 11 18 15 '
44 47 o::J]J I A test lead being used to take the voltage readings fell and struck a batt~ry IIIlJ connector, causing a spark which ignited the hydrogen.
To prevent recurre,ce, DJ)) the location where readings are taken will be changed.
Additionally,
[)))) I explosion~proof vent caps if available, will be procured and installed on o::m I the station battery cells.
Two replacement cells have been ordered.
7 8
9 FACILITY
'3Q\\
STATUS
% POWER OTHER STATUS \\.:::;:I ITJI] L!J@ I l IO IO l@._I _N.;..../A ____
80 METHOD OF A
DISCOVERY DISCOVERY DESCRIPTION ~
L!J~~l __
O~p_e_r_a_t_o_r __
o_b_s_e_r_v_a_t_i_o_n ____________ ___.
7 8
9 10 12 13 44 ACTIVITY CONTENT
~
RELEASED OF RELEASE I AMOUNT OF ACTIVITY o::fil ~@
W@I NA I
7 8
9 10 11 44 45 46 80 I N/A LOCATION OF REL.EASE @
45 80 PERSONNEL. EXPOSURES Q
~U'eJBER O ~;r'2;E t;.:;\\ oesCRllrP>_K ~
[I[2J I I. I l~~~
.... *-------------------------J 7
8 9
11 12 13 PERSONNEL INJURIES
/,;";\\
80 aiurere~
DESC~7'R_N6 o:::TI] I I I l@).__ ____
~--------------~--------------~--------J 7
8 9
11 12 80 LOSS O!' OR DAMAGE TO FACILITY '43' TYPE
DESCRIPTION
v::;J DJ)) L.gj~.__~N~A:.-___________________________ ~---------------~
7 8
9 10 BO PUBLICITY C\\
ISSUED~ DESCRIPTION~
[]I£J L!J~---N~/_A __________________________ __,..._______
I I I I I I I I I I I I I 7
8 9
10
. 68 :* 69 80 NRC USE ONLY
~------ ---
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000255/LER-1979-001, Forwards LER 79-001/03X-1 | Forwards LER 79-001/03X-1 | | | 05000255/LER-1979-001-03, /03L-0 on 790102:reactor Protection Sys Power Range Channels NI05,06 & 07 Bypassed W/O First Tripping NI08.Caused by Failure to Use Administrative Controls | /03L-0 on 790102:reactor Protection Sys Power Range Channels NI05,06 & 07 Bypassed W/O First Tripping NI08.Caused by Failure to Use Administrative Controls | | | 05000255/LER-1979-002-03, /03L-0 on 790103:steam Generator Specific Conductivity Increased to 7.65 micro-mho Per Cm.Steam Generator Rate Increased & Morpholine/Hydrazine Feed Rate Decreased.Caused by Air in Leakage to Main Condenser | /03L-0 on 790103:steam Generator Specific Conductivity Increased to 7.65 micro-mho Per Cm.Steam Generator Rate Increased & Morpholine/Hydrazine Feed Rate Decreased.Caused by Air in Leakage to Main Condenser | | | 05000255/LER-1979-003-01, /01T-0 on 790117:fitting in Fire Protection Piping for a Cooling Tower Broke.Resulting Leakage Could Not Be Isolated;Fire Pumps Placed in Manual.Break Caused by Freezing Weather Conditions | /01T-0 on 790117:fitting in Fire Protection Piping for a Cooling Tower Broke.Resulting Leakage Could Not Be Isolated;Fire Pumps Placed in Manual.Break Caused by Freezing Weather Conditions | | | 05000255/LER-1979-004-01, /01T-0 on 790117:svc Water Pump P-7B Taken out-of- Service W/O Prior Test of Diesel Generator 1-2.Caused by Combination of Poor Judgment & Lack of Awareness of Tech Spec Requirements by Shift Operating Personnel | /01T-0 on 790117:svc Water Pump P-7B Taken out-of- Service W/O Prior Test of Diesel Generator 1-2.Caused by Combination of Poor Judgment & Lack of Awareness of Tech Spec Requirements by Shift Operating Personnel | | | 05000255/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000255/LER-1979-005-03, /03L-0 on 790103:1/4-inch Drain Line in Diesel Generator Fuel Sys Broke,Spraying 100-150 Gal of Fuel Oil Onto Engine.Caused by Vibration | /03L-0 on 790103:1/4-inch Drain Line in Diesel Generator Fuel Sys Broke,Spraying 100-150 Gal of Fuel Oil Onto Engine.Caused by Vibration | | | 05000255/LER-1979-006-01, /01T-0 on 790125:during Preparation for Leak Testing Personnel Air Lock,Found Pressure Gauge Normally Mounted on Outer Door of Air Lock Was Missing.Caused by Procedures Not Specifying Gauge Replacement After Removal | /01T-0 on 790125:during Preparation for Leak Testing Personnel Air Lock,Found Pressure Gauge Normally Mounted on Outer Door of Air Lock Was Missing.Caused by Procedures Not Specifying Gauge Replacement After Removal | | | 05000255/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000255/LER-1979-007-03, /03L-0 on 790115:primary Computer Stopped.Caused by Computer Program Failure.Computer Reprogrammed to Restore Operability | /03L-0 on 790115:primary Computer Stopped.Caused by Computer Program Failure.Computer Reprogrammed to Restore Operability | | | 05000255/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000255/LER-1979-008-03, /03L-0 on 790126: Tank Vent Valve (CV-3051) Opened Simultaneously w/N2 Fill Valve;Tank Pressure Dropped Below Tech Specs Limit. Caused by Electrical Short Between Wires for Fill & Vent Valves | /03L-0 on 790126: Tank Vent Valve (CV-3051) Opened Simultaneously w/N2 Fill Valve;Tank Pressure Dropped Below Tech Specs Limit. Caused by Electrical Short Between Wires for Fill & Vent Valves | | | 05000255/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000255/LER-1979-009-01, /01X-1 on 790220:design Review Indicated Butterfly Valves May Not Close Under Accident Conditions.Caused by Vague Purchase Specs Which Did Not Include Requirements for Closing Against Pressure | /01X-1 on 790220:design Review Indicated Butterfly Valves May Not Close Under Accident Conditions.Caused by Vague Purchase Specs Which Did Not Include Requirements for Closing Against Pressure | | | 05000255/LER-1979-009, Forwards LER 79-009/01X-1 | Forwards LER 79-009/01X-1 | | | 05000255/LER-1979-010-03, /03L-0 on 790207:during Resin Sluicing Operations, Manual Isolation Valve (MV-CVC502) Was Left Open,Resulting in 17 Gpm Leak to Radwaste Sys.Caused by Broken Valve Stop. Valve Stop Will Be Replaced | /03L-0 on 790207:during Resin Sluicing Operations, Manual Isolation Valve (MV-CVC502) Was Left Open,Resulting in 17 Gpm Leak to Radwaste Sys.Caused by Broken Valve Stop. Valve Stop Will Be Replaced | | | 05000255/LER-1979-011-03, /03L-0 on 790227:primary Data Logger Was Inoperable.Caused by Multiplexer Failure at Computer Input/ Output.Faulty Relays Replaced | /03L-0 on 790227:primary Data Logger Was Inoperable.Caused by Multiplexer Failure at Computer Input/ Output.Faulty Relays Replaced | | | 05000255/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000255/LER-1979-012-03, /03L-0 on 790201:during Normal Plant Operation, Primary Coolant Pump Inadvertantly Stopped.Reactor Immediately Tripped.Shutdown Margin Was Less than Specified in Tech Specs.Power Conversion Sys Was Emergency Borated | /03L-0 on 790201:during Normal Plant Operation, Primary Coolant Pump Inadvertantly Stopped.Reactor Immediately Tripped.Shutdown Margin Was Less than Specified in Tech Specs.Power Conversion Sys Was Emergency Borated | | | 05000255/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000255/LER-1979-013-01, /01X-1 on 790327:level in T-82C Safety Injection Tank Decreased While Draining D Tank to Permit Increase in Boron Concentration.Caused by Seal Leakage.Cv 3004 Drain Valve Will Be Repaired During Next Refueling Outage | /01X-1 on 790327:level in T-82C Safety Injection Tank Decreased While Draining D Tank to Permit Increase in Boron Concentration.Caused by Seal Leakage.Cv 3004 Drain Valve Will Be Repaired During Next Refueling Outage | | | 05000255/LER-1979-013, Forwards LER 79-013/01X-1 | Forwards LER 79-013/01X-1 | | | 05000255/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000255/LER-1979-014-03, /03L-0 on 790315:during Normal Plant Operation, Primary Computer Stopped,Due to Computer Program Failure. Computer Reprogrammed & Restored to Operability | /03L-0 on 790315:during Normal Plant Operation, Primary Computer Stopped,Due to Computer Program Failure. Computer Reprogrammed & Restored to Operability | | | 05000255/LER-1979-015-01, /01T-0 on 790409:refer to from Dp Hoffman to Dl Ziemann Re Pipe Supports | /01T-0 on 790409:refer to from Dp Hoffman to Dl Ziemann Re Pipe Supports | | | 05000255/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000255/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000255/LER-1979-016-03, /03L-0 on 790406:diesel Generator Output Breaker Has Potential to Lockout Open.Caused by Failure of Contact on Shutdown Sequencer to Operate.Sequencer Repaired | /03L-0 on 790406:diesel Generator Output Breaker Has Potential to Lockout Open.Caused by Failure of Contact on Shutdown Sequencer to Operate.Sequencer Repaired | | | 05000255/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000255/LER-1979-017-03, /03L-0 on 790404:while Taking Battery Voltage Readings,Two Cells in Station Battery 2 Burst Due to Explosion of Hydrogen Inside Cells.Battery Taken Out of Svc. Two Replacement Cells Ordered | /03L-0 on 790404:while Taking Battery Voltage Readings,Two Cells in Station Battery 2 Burst Due to Explosion of Hydrogen Inside Cells.Battery Taken Out of Svc. Two Replacement Cells Ordered | | | 05000255/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000255/LER-1979-018-03, /03L-0 on 790409:reactor Made Critical W/O Conducting Flow Test of Lines.Caused by Misinterpretation of Tech Specs.Personnel Instructed to Exercise Care When Reviewing Operability Requirements | /03L-0 on 790409:reactor Made Critical W/O Conducting Flow Test of Lines.Caused by Misinterpretation of Tech Specs.Personnel Instructed to Exercise Care When Reviewing Operability Requirements | | | 05000255/LER-1979-019-03, /03L-0 on 790331:sump Drained to Auxiliary Bldg Floor Drains Through Test Connection Located Between Containment Bldg Isolation Valves.Caused by Communication Failure.Corrective Action Still Being Evaluated | /03L-0 on 790331:sump Drained to Auxiliary Bldg Floor Drains Through Test Connection Located Between Containment Bldg Isolation Valves.Caused by Communication Failure.Corrective Action Still Being Evaluated | | | 05000255/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000255/LER-1979-020-01, /01T-0 on 790501:restraints for Piping Between Power Conversion Sys Safety Injection Tanks B & D Not Adequate.Caused by Program Error Used by Consultant to Determine Hanger Placement | /01T-0 on 790501:restraints for Piping Between Power Conversion Sys Safety Injection Tanks B & D Not Adequate.Caused by Program Error Used by Consultant to Determine Hanger Placement | | | 05000255/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000255/LER-1979-021-03, /03L-0 on 790427:during Routine Surveillance of safety-related snubbers,S-44 (LPIS Pump Discharge) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Ald Age.Ring Replaced | /03L-0 on 790427:during Routine Surveillance of safety-related snubbers,S-44 (LPIS Pump Discharge) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Ald Age.Ring Replaced | | | 05000255/LER-1979-022-03, /03L-0 on 790426:during Routine Surveillance of safety-related snubber,S-9 (Main Steam Line) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Old Age.Ring Replaced | /03L-0 on 790426:during Routine Surveillance of safety-related snubber,S-9 (Main Steam Line) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Old Age.Ring Replaced | | | 05000255/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000255/LER-1979-023-03, /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired | /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired | | | 05000255/LER-1979-024-03, /03L-0 on 790608:level in Safety Injection Tank Fell Below Tech Spec Limit.Caused by Annunciation of Independent Level Switch.Switch Adjusted | /03L-0 on 790608:level in Safety Injection Tank Fell Below Tech Spec Limit.Caused by Annunciation of Independent Level Switch.Switch Adjusted | | | 05000255/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000255/LER-1979-025-01, /01X-1 on 790619:heat Transfer Coefficients of Component Cooling Water Heat Exchanger Were Less than Required.Caused by Fouled Tube Sides.Tubes Will Be Cleaned More Frequently | /01X-1 on 790619:heat Transfer Coefficients of Component Cooling Water Heat Exchanger Were Less than Required.Caused by Fouled Tube Sides.Tubes Will Be Cleaned More Frequently | | | 05000255/LER-1979-025, Forwards LER 79-025/01T-0 | Forwards LER 79-025/01T-0 | | | 05000255/LER-1979-026-03, /03L-0 on 790604:steam Generator Chemistry Ph Dropped Below Tech Spec Min When Condensate Polishers Placed in Svc.Caused by Resin Leakage from Polishers Due to Defective Septums.Resin Mixture Changed;Chemical Feed Ended | /03L-0 on 790604:steam Generator Chemistry Ph Dropped Below Tech Spec Min When Condensate Polishers Placed in Svc.Caused by Resin Leakage from Polishers Due to Defective Septums.Resin Mixture Changed;Chemical Feed Ended | | | 05000255/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000255/LER-1979-027-03, /03L-0 on 790614:during Normal Power Operation, Conductivity of B Steam Generator Increased to 7.65 Micro/Mhos Per Cm Beyond Tech Spec Limit.Caused by Condenser in Leakage | /03L-0 on 790614:during Normal Power Operation, Conductivity of B Steam Generator Increased to 7.65 Micro/Mhos Per Cm Beyond Tech Spec Limit.Caused by Condenser in Leakage | | | 05000255/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000255/LER-1979-028-03, /03L-0 on 790623:conductivity & Sodium Concentration in Steam Generator a Exceeded Tech Spec Limits.Caused by Combination of Condenser Tube in Leakage & Chemical Hideout Return as Result of Power Reduction | /03L-0 on 790623:conductivity & Sodium Concentration in Steam Generator a Exceeded Tech Spec Limits.Caused by Combination of Condenser Tube in Leakage & Chemical Hideout Return as Result of Power Reduction | | | 05000255/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | |
|