ML18037A390

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Insp Repts 50-259/93-23,50-260/93-23 & 50-296/93-23 on 930515-0618.Violation & Deviation Noted.Major Areas Inspected:Surveillance Observation,Maint Observation, Operational Safety Verification & ESF Walkdown
ML18037A390
Person / Time
Site: Browns Ferry  
Issue date: 07/12/1993
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036B366 List:
References
50-259-93-23, 50-260-93-23, 50-296-93-23, NUDOCS 9308050042
Download: ML18037A390 (30)


See also: IR 05000259/1993023

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 30323-0199

Report Nos.:

50-259/93-23,

50-260/93-23,

and 50-296/93-23

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1,

2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

Hay

15 - June

18,

1993

at

ent

nspector

a

e

lgne

Accompanied

by:

J.

Hunday,

Resident

Inspector

R. Musser,

Resident

Inspector'.

Schnebli,

Resident

Inspector

T. Liu, Intern

Approved by:

au

7

Re ctor

.r.', Secti

n 4A

Division of

eactor Projects

SUMMARY

/~ W3

ate

)gne

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety

verification, engineered

safety feature

walkdown, configuration

control drawings, modifications, Unit 3 restart activities,

reportable

occurrences,

and action

on previous inspection

findings.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted daily from

Hay 22,

1993, to June

4,

1993.

930805'0042

930713

PDR

ADOCK 05000259

8

PDR,

'

Unit 2 was returned to service this period.

However, several

problems occurred that could have

been prevented

by better

planning.

First, the reactor

was manually tripped after several

unexpected

neutron monitoring instrumentation

responses

occurred

during the startup.

Although,

a pre-existing procedure

existed to

make

an adjustment

in indicated

response,

this was not anticipated

or cross-referred

by the startup procedure.

Second,

the

recirculation

pump shaft seals failed and were replaced.

The

apparent

cause of the failure was due to venting flow up through

the seals

instead of establishing

purge seal

flow down through the

seals first.

Third, the main generator excitor brushes

had to be

replaced

due to excessive

sparking

caused

by inadequate

alignment

and placement of the brushes.

One violation was identified by an

NRC inspector concerning

the

control

room emergency ventilation system valve lineup checklist,

paragraph

six.

Several

valves

were found out of position,

no red

mark existed for damper position,

and

a difference

between

the

A

and

B train checklist.

One deviation with two examples

was identified by an

NRC inspector

concerning

a commitment

made- in the Nuclear Performance

Plan,

Volume 3, with the issuance

of configuration control drawings,

paragraph

seven.

A control

room emergency ventilation drawing was

revised after

a modification and issued

as

an as constructed

drawing instead of a configuration control drawing.

Numerous Unit

1 and Unit 3 drawings

have

been

issued

as configuration control

drawings without

a system

walkdown and resolution of

discrepancies.

One unresolved

item was identified concerning failure to take the

required technical

specification action statement within one-hour

for tripping an inoperable trip channel

input signal,

paragraph

five.

=

Licensee

management

was informed that two licensee

event reports,

one inspector followup item,

and three violations were closed.

REPORT DETAILS

Persons

Contacted

Licensee

Employees:

  • 0. Zeringue',

Vice President

J. Scalice,

Plant Manager

J. Rupert,

Engineering

and Modifications Manager

R. Baron, guality and Licensing Manager

D. Nye, Recovery Manager

  • H. Herrell, Operations

Manager

J.

Haddox,

Engineering

Manager

  • H. Bajestani,

Technical

Support

Manager

A. Sorrell, Radiological

and Chemistry .Manager

  • C. Crane,

Maintenance

Manager

  • P. Salas,

Licensing Manager

  • R. Wells, Compliance

Manager

J.

Corey, Radiological

Control

Manager

J. Brazell, Acting Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators;

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

R. Crlenjak,

Branch Chief

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • J. Hunday,

Resident

Inspector

  • R. Husser,

Resident

Inspector

  • G. Schnebli,

Resident

Inspector

  • T. Liu, Intern
  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance

Observation

(61726)

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews of the SIs for technical

adequacy

and

conformance to TS, verification of test instrument calibration,

observations

of the conduct of testing,

confirmation of proper removal

from service

and return to service of systems,

and reviews of test data.

The inspectors

also verified that

LCOs were met, testing

was

accomplished

by qualified personnel,

and-the'SIs

were completed within

the required frequency.

The following SIs were reviewed during this

reporting period:

HPCI Flow Test

On May 22,

1993, the inspector

observed portions of the

performance of 2-SI-4.5.E;l.e,

HPCI Flow Rate Test at

150 PSIG.

The test

was being performed to satisfy

TS 4.5.E. l.e and 4.5.H.3

and

as post maintenance

testing for

WO 92-58171-03

which replaced

the booster

pump seal.

During the test

no problems

were

identified with the

new seal;

however,

the

AOP did not stop

operating

when the

HPCI turbine reached

operating

speed.

When the

turbine reaches

rated

speed

the gear driven oil pump supplies the

required lube oil pressure

and the

AOP is designed to

automatically stop.

Troubleshooting

indicated that the pressure

switch that automatically stops the

AOP was out of calibration

high.

This was repaired

under

WO 93-06737-00.

The surveillance

was completed satisfactorily.

Turbine Stop Valve Limit Switch Failure

On June

16,

1993, at approximately 6:37 a.m., during the

performance of surveillance instruction 2-SI-4. 1.A-15(II), the

licensee

determined that the number

one turbine stop valve closure

'PS

function (> 10 per cent valve closure)

was inoperable.

More

specifically,

a half-scram

was expected

and not received while

simultaneously closing the number

one

and three turbine stop

valves.

While in process of troubleshooting. the problem, the

valves were closed individually and the licensee

determined that

the appropriate

relays were being deenergized

for the number three

stop valve but not the number one stop valve.

TS 3. 1.A (Table

3. 1.A) states

that if the minimum number of instrument

channels

per trip system cannot

be met for one trip system,

the inoperable

channels

on the entire trip system shall

be placed in a tripped

condition within one hour.

The licensee

determined that by

pulling fuse 5A-FlOB, the applicable

RPS relays in the 'Bl'rain

of RPS logic would be deenergized

and therefore satisfy the

TS

action statement.

This action was taken at approximately 7: 10

a.m.

At approximately 8:00 a.m. the inspector entered to the Unit

2 control

room to investigate

the licensee's

actions

as they

related to the failed stop valve

RPS function.

While reviewing

the applicable

RPS logic diagrams,

the inspector questioned

the

operations shift if they had taken the appropriate

actions

(removing the fuse) for the 'Al'rain of RPS

as it appeared

that

the number

one stop valve had

an input to this portion of RPS

logic also.

The licensee

investigated

the inspector 's concern

and determined

that

an additional

fuse was also required to be removed.

This

action was taken at approximately 8:32 a.m. or 55 minutes in

excess of the

LCO delineated

in TS 3. 1;A, Table 3. 1.A, note one.

Pending further review, this matter will be tracked

as

URI 260/93-23-01,

Failure to Perform TS Action Within the Required

Time Frame.

No violations or deviations

were identified in the Surveillance

Observa-

tion area.

Maintenance

Observation

(62703)

Plant maintenance activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain

that they were

conducted

in. accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations 'were performed prior

to returning components

or systems

to service,

gC records maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological controls

as required.

Work documents

(HR,

WR,

and

WO) were reviewed to determine the status of

outstanding jobs

and to assure that prioi ity was assigned

to safety-

related

equipment

maintenance

which might affect plant safety.

The

inspectors

observed

the following maintenance activities during this

reporting period:

'a ~

b.

C.

Recirculation

Pump Shaft Seal

Assembly Replacement

The inspector reviewed HHI-9A, Removal

and Replacement

of Reactor

Coolant Recirculation

Pump Shaft Seal

Assembly

and HHI-9B, Repair

of Reactor Coolant Recirculation

Pump Shaft Seal

Assembly.

These

were reviewed to see if any steps

would have prevented

the seal

failure due to the venting technique

problem discussed

in

paragraph

4.

No procedure

steps

could be found.

Leaking Rel'ief in Seal

Purge Line

During

a routine tour of the reactor building on June 6,

1993, the

inspector identified

a leaking relief valve in the

CRD water

supply to the recirculation

pump seal.

The inspector

inspected

the local

CRD seal

flow meters

because

of high seal

flow

annunciators'in

alarm in the control

room.

The relief valve

associated

with the 'B'ump is 2-68-55& while 2-6&-553 is

associated

with the 'A'ump.

The inlet pi'ping to both reliefs

was warm; however, the relief outlet from the 'B'as

warm while

the 'A'as cold.

This problem was discussed

with the

SOS.

The

licensee verified by use of a pyrometer this condition did exist.

WO 93-07471-00

was performed to determine the problem which

indicated the line to the seal

was not plugged

and the relief

valve was leaking.

Continuous Air Monitor

On June

18,

1993, the inspector observed

maintenance activities

associated

with the continuous air particulate monitor,

2-RM-090-

0057, located in the unit 2-Reactor Building 565 foot elevation.

The controlling document

was

WO 93-01365

and indicated that the

monitor was spuriously spiking high.

Haintenance

believed the

spikes

were due to electronic noise

induced into the system but

could not pinpoint the location.

The inspector

noted that

maintenance

personnel

were following approved

procedures

and using

qualified test equipment.

Troubleshooting will continue until the

cause is determined.

The inspector

had

no concerns with this

activity.

d.

HPCI Hechanical

Seal

On Hay 17,

1993, during the performance of 2-SI-4.5.E. I.e,

HPCI

Flow Rate Test at

150 PSIG, Operations

noticed

smoke emitting from

the booster

pump inboard mechanical

seal

area.

The turbine was

tripped

and

WO 92-58171-03

was initiated to troubleshoot

and

repair the damage.

The seal

was disassembled

and,inspected

using

HCI-0-073-PHP002.

It was determined that the seal failed due to

the shaft rubbing the flange bushing which resulted

in high

seal'emperatures

and subsequent

damage.

A new seal

was installed

and

the system restarted

to verify proper temperatures

and vibrations

could be attained.

The inspector

reviewed the work documents

and

noted

no discrepancies.

e.

HV/I Converter Troubleshooting

On June

16,

1993, the inspector

observed

portions of the

licensee's

troubleshooting effort on the

2A recirculation flow

control

system in accordance

with

WO 93-07613-00.

Hore

specifcally,

a ground

was detected

and traced to the HV/I

converter portion of the control circuitry.

Due to problems

described

in paragraph

4d below, the HV/I converter

was replaced

with a converter from Unit 3 and the ground condition cleared.

No violations or deviations

were identified in the Haintenance

Observation

area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and any significant

safety matters related to plant operations.

Daily discussions

were held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power=supplies,

emergency

power sources

available for automatic operation,

the purpose of

temporary tags

on equipment controls

and switches,

annunciator

alarm

status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

operability, temporary alterations

in effect; daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This

inspection activity also included numerous

informal discussions

with

operators

and supervisor s.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general 'plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger

conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply and breaker alignments,

radiation

"and contaminated

area controls,

tag controls

on e'quipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held with selected

plant personnel

in their functional

areas

during these tours.

a 0

Unit Status

Unit 2 completed the refueling outage this period.

Initial

criticality was

on Hay 25,

1993,

and the main generator

was

initially tied to the grid on June 2,

1993.

'The generator

was

loaded to 160

HW for several

hours to obtain vibration reading for

turbine balancing.

The unit was removed from service

on

June

2,

1993, for addition of a balance

shot.

The unit was tied

to the grid on June 3,

1993, for power escalation.

At the end of

the report period the unit had

been on-line for 14 days.

Three

separate

problems

occurred during the recovery of the unit

that'ould

have

been prevented

by better planning.

1)

Hanual

Scram Downscale

IRHs

Following initial criticality on Hay 25,

1993,

a manual scram

was initiated due to problems

when ranging the

IRHs

from range six to seven.

Several

IRH's unexpectedly

went

downscale.

This caused

a rod withdrawal block.

Control

rods were inserted to reduce

power to range six and one rod

double notched causing

an insert rod block in the

RWN.

Operations

decided to manually scram the reactor at this

time.

The problem was that

an amplifier gain adjustment

needed to be performed

when going from range six to seven.

This

same adjustment

was performed

on the initial startup

for cycle six.

A procedure

already existed to perform this

adjustment,

but was overlooked or not cross referenced

in

the startup procedure.

The licensee is conducting

an

incident investigation of this event.'his will be reviewed

by the inspector

and subsequent

LER closed.

2)

Recirculation

Pump Seal Failure

The second

problem occurred with the recirculation

pump seal

failure.

Both recirculation

pump seals

were replaced during

the outage.

On Nay 27,

1993, the

2A recirculation

pump seal

failed.

The

pump was stopped

and the unit shutdown.

While

in the process of shutting

down the unit, the

2B

recirculation

pump seal

also failed.

The licensee

found

an

estimated

one-half teaspoon of gritty material in the seal.

From discussions

with plant personnel this was attributed to

starting the

pump without CRD purge flow through the seal.

This allowed flow from the recirculation system

up into the

seal

area.

If clean

CRD water had

been flowing into the

seal, this could have

been prevented.

The licensee

revised

2-01-68,

Reactor Recirculation

System,

to establish

seal

purge flow first.

The licensee is submitting

an

LER due to

the plant shutdown.

3)

Excitor Brushes Incorrectly Installed

The third problem occurred

when initially preparing to

synchronize

the main generator to the grid.

The main

turbine was manually tripped. due to excessive

sparking at

the excitor brushes.

The brushes

and housing were not

properly aligned

and metal-to-metal

contact occurred

on the

collector rings.

The brushes

were replaced

and the

collector rings polished.

The licensee is conducting

an II,

II-B-93-032, to review this problem.

All three events

could have

been prevented

by better planning

and

control of maintenance activities for recovery of systems after

the outage.

Enforcement Discretion

On May 17,

1993, the licensee

was granted

enforcement discretion

for the required actions of TS 3.5.8.9.

The time allowed was from

4:00 p.m.

May 17,

1993, until 4:00 a.m.

May 21,

1993.

The

discretion

was necessary

to make repairs

on

an inboard

RHR

injection valve.

With the other loop in shutdown cooling neither

loop would 'be capable of providing an automatic

LPCI flow path

as

required

by TS 3.5.8.9.

As compensatory

measures

the licensee

committed to maintain both

loops of CS operable during the repair activity.

The

RHR loop

used for shutdown cooling was capable of being manually realigned

for operation in the

LPCI mode.

Plant operators

reviewed existing

procedures for this realignment..

The inspector confirmed that the conditions of the enforcement

discretion were met.

The valve was repaired

and the

RHR loop

returned to an operable

status within the allotted time.

Drywell Closeout

On May 20,

1993, the inspectors

conducted

a drywell inspection in

preparation

for final closeout

and unit startup.

Particular

attention

was given to loose items that could possibly. end

up in

the suppression

pool,

as described

in Bulletin 93-02,

Debris

Plugging Of Emergency

Core Cooling Suction Strainers.

Items

identified included,

two screws missing

on

a drive motor

connection for SRM C,

unused wire hanging from the overhead,

several

broken light bulbs,

and

a section of drain 'hose.

One

particular item found was

a section of rope laying in one of the

drywell to torus

downcomer vent pipes.

These

items were brought

to the attention of plant management

and were corrected

on

subsequent

entries.

On May 20,

1993, the final drywell inspection

was performed

by the licensee

per 2-GOI-200-2, Drywell Closeout.

Electromagnetic

Interference

Mapping in Control

Room

From May 25 - 27,

1993, during Unit 2 reactor startup,

EMI mapping

surveys

were performed in Unit 1, 2, 3,

and control

room locations

in proximity to the

RBVRMs.

The

same

surveys

were performed

on

Unit 1, Unit 2,

and Unit 3; refuel floor locations in proximity to

the reactor;

and refuel

zone radiation monitors during Unit 2

Cycle

6 refueling outage.

Three types of surveys

were made.

First was the conducted

interference,

second

was the radiated interference,

and third was

the

DC magnetic fields.

Surveying conducted

interference

on the signal leads

arid power

leads

on each monitor involved clamping

on current probes to the

line of interest

and then measuring

the noise

on the lines with a

spectrum analyzer for frequency

domain data.

The range of

frequency monitored for conducted

interference

was

30

HZ to 50

MHZ.

For surveying radiated interference,

antennae

were placed in the

direct vicinity of panel 9-10, (in which the

RBVRMs are located)

in each control

room.

The survey was for both electrical

and

magnetic fields,

and was performed

on both the front and rear of

the panels.

The survey in the rear of the cabinets

was

conservatively

performed with the rear doors

open

and closed .as

an

assurance

that the survey would cover normal activities in and

around the cabinets.

Four antennae

were placed in the direct

vicinity of the

RBVRMs (approximately

1 meter)

and the area

was

monitored with frequency

sweeps.

These

sweeps

were captured

using

a spectrum analyzer.

The following antennae

were used during the

survey:

Loop antenna

for AC magnetic fields - frequency of 30

HZ to

50 KHZ.

Active rod antenna for electrical fields frequency range

of 14 KHZ to 30 MHZ.

Biconical antenna for electrical fields frequency range of

30

MHZ to 300 MHZ.

Time period antenna for electrical fields - frequency range

of 300

MHZ to 1000

MHZ.

DC magnetic fields were also surveyed

in and around the 9-10

cabinets.

This activity involved using

a gauss

meter

and hall

effect probe covering the direct vicinity of the equipment.

The survey results indicated the plant's

ENI environmental

conditions are within the tested

envelope,

which is 65

volts/meter.

The maximum radiated electric field from the

ENI

mapping survey was found to be around

8 volts/meter

when

a plant

hand-held radio was

keyed in Unit I control room.

The inspector

observed portions of the survey conducted,

reviewed

the test results,

and held discussions

with licensee

representatives.

No deficiencies, were identified.

Recirculation

Flow Control

Problems

Following the startup of Unit 2, the licensee

experienced

a number

of problems with the portion of the recirculation flow control

system associated

with the

2A recirculation

pump.

During the

power ascension,

.a problem with the NV/I converter

caused

a ground

to be introduced into the control circuitry.

Another NV/I

converter

was installed

and it exhibited

a similar problem.

Troubleshooting

by the licensee

revealed that

a screw inside the

NV/I converter(s)

had penetrated

the bottom of the chassis

and

penetrated

a circuit card causing the ground.

Both NV/I

'convertors

had

been refurbished

by different vendor s,'et

both had

the identical problems.

The NV/I converter

was replaced with a

converter from Unit 3 and the ground condition cleared.

Another problem experienced

by the licensee

was noise introduced

into the

2A control. system from a failed 75 percent

speed limiter.

The limiter failed such that noise being introduced into the-

control

system

caused

a slight oscillation in the control signal

with a frequency of 20 cycles per minute.

The limiter was

replaced

and noise

was eliminated.

The licensee

has yet to

determine the cause of the limiter's failure.

In addition to the previously mentioned

problems,

a runback signal

to the 75 percent limiter was received during the startup.

However,

because total recirculation flow was less than'5

percent,

no actual

runback occurred.

The two requirements for a

recirculation runback are

one feedpump less than

20 percent flow

and reactor water level less than

27 inches.

Although,

one feed

pump was secured

at the time of the runback signal, reactor water

level did not reach

27 inches

(normal level being approximately

35

inches).

The licensee

suspects

that

an instantaneous

spike

.

downward in a water level signal

from a

F'H control system level

switch may have caused

the runback signal to occur.

The licensee

is monitoring level switch 3-538 and plans to troubleshoot

the

component during the next window of opportunity.

g.

The inspectors will continue to monitor the licensee's

progress

related to the recirculation flow control system.

It appears

that

problems

are continuing to plague the licensee

as they did during

the previous operating cycle.

However, at the end of this

reporting period, the recirculation flow control

system

was

performing adequately.

Expired Welding and Grinding Permit

On June

14,

1993, the inspector noted that

a fire watch

had signed

on

a Grinding and Welding permit which had expired June

11,

1993.

The permit,

1379,

was posted for work in the Unit 3 drywell for

the period of June

7 11,

1993,

and required

a firewatch while

work was being performed.

The inspector notified Operations

who

determined that no work was actually taking place

as described

by

this permit.

Following completion of the work activities the

foreman is to remove the permit and have it canceled.

In this

case

the permit had not yet been

removed.

No specific time

interval is stated for the removal of the permits.

Hissed Appendix

R Required Firewatch

On June 4,

1993, Fire Protection

Impairment Permit (Att. F) Number

93-0014-013,

which was issued for an inoperable Unit 3 Diesel

Generator building carbon dioxide system,

was closed out and the

required

compensatory

measure

was removed.

The compensatory

measure

was

an hourly roving firewatch.

On June

5,

1993, it was

discovered that required post-maintenance

testing

had not been

performed prior to cancelling the compensatory

measure.

A

firewatch was re-established

and

a new Att. F, 93-0248-001,

was

initiated for the impairment.

The required post-maintenance

test

was performed

and completed satisfactorily after which the

C02

system

was declared

operable

and the compensatory

measure

again

canceled.

Problem Evaluation Report

BFPER930082

was generated

by

the 'licensee to document this event.

The inspector will continue

to monitor this activity and evaluate

the licensee's

corrective

actions in the

PER.

This is identified as IFI 296/93-23-04,

Hissed Appendix

R Firewatch.

ESF Walkdown (71710)

During this inspection period the inspector performed

a system

walkdown

of the

CREVs system installed this outage.

Portions of the valve lineup

and the system drawing, 2-47-E2865-4,

were compared to the configuration

existing in the field.

Discrepancies

noted are

as follows:

CREV A and

B damper position, required

by the val.ve lineup is

'HROTTLED.

The procedure

stated that the damper handle

should

be

positioned over the red mark painted

on the duct work.

There

was

no red mark on the duct work.

0

10

b.

Three drain valves

O-DRV-31-7361, for unit A and O-DRV-31-7366,

and 0-DRV-31-7367 for unit B, are required to be closed

by the

valve lineup. The'rawing indicated they should

be open.

An

additional drain valve on unit A, O-DRV-31-7360,

was inadvertently

left out of the valve lineup.

Although the completed valve lineup

indicated these

valves were closed,

the inspector

found them all

open

and the drain pipes capped.

c.

The instrument checklist identified the location of the 0-PDIS-31-

7316,

as the Unit 2 Ventilation Tower.

The location is actually

the

CREV Room,

El 617'.

TS Section 6.8. l.l.a requires that procedures

shall

be implemented

covering procedures

in Appendix A of Regulatory

Guide 1.33

Revision 2, February

1978.

Appendix A of Regulatory

Guide 1.33

includes

procedures for controlling the operation of the Control

Room Emergency Ventilation System.

Operating Instruction,

0-OI-'1,

is the controlling document for this system

and identifies the

required position of the aforementioned

components.

Failure to

maintain the required position of"these

components

is

a violation

of this Operating Instruction

and is identified as

VIO 259,

260,

296/93-23-02,

CREVs Components

Not In Required Position.

Licensee

management

was informed of the findings and they were

corrected.

Several

other system valve lineups were checked

by the

licensee

and similar problems

were not identified.

One violation was identified in the

ESF walkdown area.

Configuration Control Drawings

In IR 93-08 concerns

were raised related to CCDs.

In a site bulletin

issued

Hay 20,

1993,

a caution

was noted for use of Unit 3 and Unit

1

drawings issued

as

CCDs because all discrepancies

had not been resolved.

The inspector

reviewed the Browns Ferry NPP,

Volume 3, Section 2.2.2.3,

Issuance

of CCDs,

and concluded

a deviation from the commitment

had

occurred.

CCDs were to be issued -to replace

as-constructed

drawings

and

as-designed

drawings to reflect the plant configuration

and differences

reconciled.

Two examples

were identified of not meeting the commitments.

One

example

was for the Unit

1 and Unit 3 drawings discussed

above.

The as-

constructed

and as-designed

drawings were simply combined.

No walkdown

was performed of the system to confirm the actual plant configuration.

Also, stated in the caution in the site bulletin was that these

drawings

are being scrubbed

and discrepancies

resolved during the drawing

improvement program

and final clearup during the

SPAE(SPOC

process for

system restoration.

The second

example

was that for a

CREVS drawing discussed

in this report

for a system

walkdown of the

CREVS.

Drawing 2-47E28654

was revised

on

April 21,

1993,

and issued

as

an as-constructed

drawing after major

11

plant modifications.

This again deviated

from the commitment to issue

CCDs after plant modification.

This deviation will be tracked

as

DEV

259,

260, 296/93-23-03,

Issuance of Configuration Control Drawings.

One deviation

was identified in the configuration control drawings area.

Modifications (37700,

37828)

The inspectors

maintained

cognizance of modification activities to

support the restart of Unit 2.

This included reviews of scheduling

and

work control, routine meetings,

and observations

of field activities.

Throughout the observation of modifications being performed in the field

gC inspectors

were observed monitoring and documented verification at

work activities.

a ~

Third Phase of Instrument Tubing Program

Phases

I and II of the instrument tubing program concerning

a lack

of design criteria for seismic Class

I tubing and associated

supports

were implemented prior to restart

from the Unit 2 cycle

5

outage.

Phase III of the program required the licensee to

complete

an engineering evaluation

and necessary

modifications to

meet the final design criteria which were deferred

from

Pre-Restart/Safe

Shutdown

Scope

and are .required in support of the

long term operation of Unit 2.

The engineering

evaluation

was

accomplished

by Stone

and Webster

as documented

in Report

No.

02836-REP-S156,

dated

September

17,

1992.

The required tubing and

support modifications were performed

by

DCN W17283A,

W17285A,

and

W17286A which were completed during the Unit 2 cycle

6 outage.

The inspectors

reviewed the licensing closure

packages

(NCO

860326205

and

NCO 890128001,

the

SWEC engineering

evaluation,

and

the DCN's associated

with issue)

and determined the requirements

of the licensee's

commitment were met.

Cable Installation Issues

Several

cable installation issues

were identified prior to the

Unit 2 cycle

5 restart,

including vertical drop for low voltage

and medium voltage cables,

testing

and tren'ding of Group

2 cables,

and medium voltage cable

bend radius concerns.

The issue concerning vertical drop for medium voltage cables

was

resolved prior to the cycle

5 restart.

The subject cables

were

analyzed

and were justified technically acceptable

or were

replaced

as documented

in CA(R BFP 881066.

The low voltage cables

were evaluated

using the vertical support

requirements

of the General

Engineering Specification

G-38,

Rev.ll,

as

an acceptance criteria for vertical drop.

Bechtel

Engineering

performed walkdowns

on over 400 conduits containing

low voltage cables'.

The results

were documented

in Data

Package

BW001-001.

Those cables

which exceeded

the vertical drop limits

12

C.

d.

were identified as

an exception to G-38.

The Nuclear Engineering

staff prepared calculation

ED-(0000-910143,

Cable Support in

Vertical Conduit, which calculates

the maximum distance of

vertical drop a.particular cable

can withstand without exceeding

static sidewall pressure limits.

Based

on the engineering

evaluation the subject cables

were found to be technically

acceptable

due to the actual vertical drop length -being less in

all cases

than the allowable vertical drop shown in the

calculation tables.

This evaluation

was completed in Hay 1992.

The licensee modified their commitments

concerning

medium voltage

cable

bend radius

and testing

and trending of Group

2 cables

in

letter From TVA to

NRC dated

Harch 17,

1993.

The initial

commitments

were modified to require the replacement

of only one

cable,

PP434-IE,

during the Unit -2 cycle

6 outage,

which was

accomplished

under

DCN W17775.

The letter is currently being

reviewed

by NRR.

The inspectors

reviewed the documentation

associated

with the cable installation issues

discussed

above

and

determined

the licensee

met the requirements

of their commitments.

Pending

NRR approval of the licensee's

Harch 17,

1993, letter this

issue

may be closed.

Core Spray System

In IR 93-18, it was discussed

that the written approval for the

hydrostatic test methodology for a weld repair-on the

CS spray

system

had not been received.

The

NRC approved the hydrostatic

test pressure

in a letter dated

Hay 21,

1993.

No other

open issue

remained with the

CS hydrostatic test.

Completion of Restart

Commitments

In a letter to the

NRC Region II Regional Administrator, dated

Hay 24,

1993, the licensee

informed the

NRC of the completion of

commitments for the Unit 2 cycle 6 outage.

The inspectors

sampled

these

commitments in this IR and

IR 93-18

and concluded that the

licensee

had completed the Unit 2 cycle

6 outage

commitments.

Unit 3 Restart Activities

(30702,

37828,

61726,

62703,

71707)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work, and gA/gC activities; attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and management

meetings;

and periodic discussions

with both

TVA and contractor

personnel, 'skilled craftsmen,

supervisors,

managers

and executives.

The licensee is still working on the Unit 3 Recovery Schedule

which

should

be finalized in the near future.

The inspectors will continue to

follow the progress of the schedule

and will provide copies of it to

NRC

13

management

when issued.

Currently, the work is being scheduled

and

tracked

by a Summer Semester

Schedule

which provides

a three month look

ahead for both maintenance

and modifications.

Progress

on the three

month schedule will be used

as input to more accurately project work

duration

on the long range schedule.

Construction activities are increasing'lightly with the completion of

the Unit 2 cycle

6 refueling outage.

Major activities in progress

include:

CRDR work in the control

room panels;

reactor internals

T Box

repairs; fire protection systems;

seismic

upgrades

and pipe supports.

No violations or deviations

were

identified.'eportable

Occurrences

(92700)

The

LERs listed below wire reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event description,

the corrective actions

taken,

the existence of potential generic problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

a ~

(CLOSED)

LER 296/89-05,

Unplanned

Engineering Safety Feature

Actuations

Due to Loss of Power to Radiation Monitors.

On October

25,

1989, the radiation monitors for the Unit 3 reactor

and refueling zones

experienced

a loss of power and

as designed,

tripped upscale

actuating

numerous

ESFs.

Specifically, the

CREVS

and the

SBGT systems

were automatically started

and the Refuel

Zone

and Unit 3 Reactor

Zone Ventilation and the Unit 3 Group

6

PCIS system received isolation signals.

The cause of the event

was determined to be the failure of a fuse in the radiation=

monitors power supply.

The initial corrective action performed

was to replace the

radiation monitors power supply.

The final corrective action

committed to in the

LER was to replace the reactor

and refuel

ventilation radiation monitors with monitors having

a revised

logic scheme

and redundant

power supplies.

The licensee .initially

committed to have these corrective actions

performed prior to the

startup of Unit 2 for. cycle 6.

However,

on July 2,

1990, the

licensee

informed the

NRC (via revised

LER) that due to

procurement

lead time, the radiation monitors could not be

replaced until the Unit 2 cycle 6 refueling outage.

The inspector

verified through review of records

and in plant observations

that

the reactor

and refueling zone ventilation exhaust radiation

monitors

had

been replaced

in all three units.

14

b.

(CLOSED)

LER 296/92005,

Compensatory Action Fire Watch Discovered

A Compromising Position Resulting

In A Violation of Technical

Specifications.

This

LER is closed

and the basis discussed

in paragraph

10.c. for

the discussion of VIO 92-37-03.

10.

Action on Previous

Inspection

Findings

(92701,

92702)

a ~

(OPEN) IFI 259,

260, 296/92-30-03, Circuit Breaker Coordination.

On June

1,

1993,

SBGT trains A, B, C,

and

CREVS automatically

started

due to breaker

3D on Shutdown

Board

1B tripping'.

At the

time the breaker tripped it was supplying alternate

power to

Unit -1

RPS.

The licensee

tested

the breaker'and

found it to be

satisfactory.

They then concluded that the spurious trip was

caused

by a design

problem in the breaker's trip device which was

previously identified in November

1992.

The licensee

issued

a

Part

21 report

on November 25,

1992, identifying a defect in

GE

supplied

RHS-9 breaker trip devices with instantaneous

trip

function.

Per

GE, to prevent spurious trips,

a hold-off circuit

ensures

that the fault condition persists for a sufficient

duration

(300 microseconds)

to insure that

a trip is warranted.

Subsequent

testing,

performed

by TVA as part of their

investigation into the cause of spurious

breaker trips,

demonstrated

that the

RHS-9 unit would trip in response

to pulse

widths .of substantially less duration than

300 microseconds if the

current value was sufficiently above the instantaneous

trip

setpoint.

GE agreed with the licensee's

findings as documented

in

GE letter G-ER-3-126,

dated

March 18,

1993.

In this letter

GE

committed to develop

a modified RHS-9 unit for application at

Browns Ferry.

The design

and development

process

is expected to

be completed

by August 1,

1993, with production units available

by

the end of October

1993.

When the licensee identified the defect in the

RHS-9 units, in

October 9,

1992; they performed plant walkdowns to determine

which

breakers utilized the

RHS-9 trip unit.

Of the 39 RMS-9 conversion

kits purchased for use at the facility only'0 were installed,

6

in safety related

equipment

and

4 in non-safety related

equipment.

The

6 installed in safety related

equipment

were located

as

follows:

480V Shutdown

Board

1A (compt.

3D - Units -1

18C Bus A);

480V Shutdown

Board

1A (compt.

5A control air compressor

A);

480V Shutdown

Board 1B,(compt.

3D Unit

1

ISC Bus B); 480V

Shutdown

Board

2A (compt.

5A control air compressor

D); 480V

Shutdown

Board

3A (compt.

2B Unit 3 ISC Bus A); 480V Shutdown

Board

3B (compt.

5B - Unit 3 IKC Bus B).

The licensee. formally

discontinued installation of the

RMS-9 trip devices with the

instantaneous trip function on October 5,

1992,

and performed

an

engineering

evaluation which determined that it was acceptable

to

allow the six breakers listed above to remain- installed.

The

15

inspectors will continue to follow this issue until the redesigned

RMS-'9 units are installed

and proven reliable.

(CLOSED) VIO 260/92-33-01,

Failure to Confirm Drywell

CAN Alarm.

On September

25,

1992,

an immediate action was not taken to

confirm an alarm at 2:55 a.m.

on drywell detection radiation

monitor detector,

2-RH-90-256.

TS Table 3.2.E note

3 requires

that immediate corrective actions will be taken to assess

the

possibility of increased

leakage

whenever

a drywell

CAN alarm is

received.

The sample

was requested

but not analyzed.

At

7:10 a.m., the monitor was declared

inoperable

and logged

as

inoperable because'he

particulate

channel

was erroneously in

alarm.

A work order was initiated to troubleshoot

and correct the

problem with the channel

in alarm.

Later from 4:00 to 8:00 a.m.

unidentified floor leakage

provided indication of increased

drywell leakage

and Unit 2 was shutdown.

On December

2,

1992, the licensee

denied this violation on the

basis that plant personnel

took immediate action to confirm the

drywell on

CAN alarm.

The staff reviewed the licensee's

response

and concluded the violation occurred

as stated.

The ARP was revised to ensure that the proper samples

are

identified and obtained for specific alarm conditions.

The

inspector

reviewed the closure

package,

the revised

alarm response

procedure,

2-ARP-9-3,

and concluded that the corrective actions

have

been taken to preclude recurrence

of this issue.

(CLOSED) YIO 260/92-33-02,

Inattentive Firewatch

(CLOSED) VIO 259,

260,

296/92-37-,03,

Inattentive Firewatch

On October 2,

1992, the

NRC resident

inspector

observed

a fire

watch

who was inattentive to duty and appeared

to be sleeping.

The inspector

informed Operations

and,the fire watch was replaced.

This was documented

as

VIO 92-33-02.

On November

11,

1992,

a

Technical

Support Supervisor

observed

another fire watch

who was

inattentive to duty and appeared

to be sleeping.

He too was

replaced.

This was documented

as

VIO 92-37-03

and also

as

LER

'96/92005.

Fire watches

in both events

were given disciplinary =action.

New

fire watches

were hired and provided with training on the expec-

tations of management

and the responsibilities of a fire watch.

The inspector verified that the overtime

had

been reduced to

acceptable

amounts

and that the fire watches

were

on their

stations

and alert.

In addition the inspector verified the fire

watches

are rotated hourly from one location to another

and that

the foreman is periodically touring these locations.

16

Exit Interview (30703)

The inspection

scope

and findings were summarized

on June

22,

1993, with

those

persons

indicated in paragraph

1 above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection findings

listed below.

The licensee

did not identify as proprietary any of the

material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

The Site Vice President

stated that the efforts on drawings were to make

the drawings reflect the actual plant configuration

as systems

were

returned to service.

The Site Vice President

stated,

additionally, that

the wording in the commitment

needed to be reviewed.

Item Number

Desc i tion and Reference

260/93-23-01

259,

260,

296/93-23-02

259,

260, 296/93-23-03

296/93-23-04

URI, Failure to Perform

TS Action Within

the Required

Time Frame,

paragraph

two.

VIO, CREVs Components

Not in Required

Position,

paragraph five.

DEV, Issuance

of Configuration Control

Drawings,

paragraph

six.

IFI, Missed Appendix

R firewatch

Licensee

management

was informed that

2 LERs,

1 IFI, and

3 VIOs were

closed.

Acronyms

and Initialisms

AOP

ARP

BFNP

CAM

CAQR

CCD

CFR

CRD

CREVS

CS

DCN

EMI

ESF

GE

GOI

HPCI

IFI

IRM

Auxiliary Oil

Pump

Alarm Response

Procedure

Browns Ferry Nuclear .Power Plant

Continuous Air Monitor

Condition Adverse to Quality Report

Configuration Control Drawing

Code of Federal

Regulations

Control

Rod Drive System

Control

Room Emergency Ventilation System

Core Spray

Design

Change Notice

Electromagnetic

Interference

Engineered

Safety Feature

General Electric

General

Operating Instructions

High Pressure

Coolant Injection

Inspector

Followup Item

Intermediate

Range Monitor

17

IR

IVVI

LCO

LER

HHI

HR

HW

NPP

NRC

NRR

OI

PCIS

PSIG

QC

RBVRH

RH

RHR

RPS

RWH

SBGT

SI

SOS

SPAE

SPOC

SRH

SWEC

TS

VIO

WO

WP

WR

Inspection

Report

In Vessel

Visual Inspection

Limiting Condition for Operation

Licensee

Event Report

Mechanical

Maintenance

Instruction

Maintenance

Request

Megawatt

Nuclear Performance

Plan

Nuclear Regulatory

Commission

Nuclear Reactor Regulation

Operating Instruction

Primary Containment Isolation System

.Pounds

Per Square

Inch Gauge

Quality Assurance

Quality Control

Reactor Building Ventilation Radiation Monitor

Radi aiton Monitor

Residual

Heat

Removal

Reactor Protection

System

Rod Worth Minimizer

Standby

Gas Treatment

System

Surveillance Instruction

Shift Operations

Supervisor

System Plant Acceptance

Evaluation

System Pre-Operational

Checklist

Source

Range Monitor

Stone

L Webster Engineering

Corp.

Technical Specifications

Violation

Work Order

Work Plan

Work Request