05000220/LER-1979-025-03, /03L-0:on 791027,during Surveillance Testing, Personnel Unable to Zero Side Average Power Range Monitor Flow Converter 11.Caused by Component Failure.Entire Unit Replaced & Problem Eliminated

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/03L-0:on 791027,during Surveillance Testing, Personnel Unable to Zero Side Average Power Range Monitor Flow Converter 11.Caused by Component Failure.Entire Unit Replaced & Problem Eliminated
ML18037A209
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 11/19/1979
From: Duda E
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17053B235 List:
References
LER-79-025-03L, LER-79-25-3L, NUDOCS 7911300484
Download: ML18037A209 (2)


LER-1979-025, /03L-0:on 791027,during Surveillance Testing, Personnel Unable to Zero Side Average Power Range Monitor Flow Converter 11.Caused by Component Failure.Entire Unit Replaced & Problem Eliminated
Event date:
Report date:
2201979025R03 - NRC Website

text

I7.77 I LlCENSEE EVENT REPORT Ql (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 6 0

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04~05 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CONTROL BLOCK:

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LICENSEE CODE CON'T Qs 1

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9 Q9 EVFNT DATE 74

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SOURCE 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO During steady state operatio'ns, personnel performing instrument sur-

~03 veillance tests were unable to zero 811 Side APRH Flow Converter.

The error in flow indication was in the conservative direction and all trip

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~O7 points were operable.

The faulty converter unit was replaced by a new unit and the problem was eliminated.

This event had no safety implica-tions

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CODE TYPE NO.

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UL LJ 21 22 23 24 26 27 28 29 30 31 32 ACTION. FUTURE EF F ECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER

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0 Q 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION ANDCORRECTIVE ACTIONS Q27 Technicians were unable to zero APRH flow converter unit due to compo-nent failure.

The entire unit was replaced and the roblem was elim-inated.

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METHOD OF OTHER STATUS ~

DISCOVERY 8 0 45 46 45 7

9 FACILITY STATUS 91 POWER 5

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10 12 13 44 ACTIVITY CONTENT RELEASEO OF RELEASE AMOUNTOF ACTIVITYQSS Z

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10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 2

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11 12 13 PERSONNEL IENBURIES DISCOVERY DESCRIPTION Q32 Instrument Surveillance Test LOCATIONOF RELEASE Q NA 80 80 80 9

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10 PUBLICITY ISSllED DESCRIPTION~

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10 NAME OF PREPARER 80 P7 9 1l 0 0 0 gP/

NRC USE ONLY 80 68 69 80 o

(315) 343-2110 Ext 1558 0

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