LER-1979-023, /03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised |
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NRC FORM 366
'(7.77}
U. S. NUCLEAR REGULATORY COMMISSION
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Go 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO Durin stead state o eration i 1 0
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EVENT DATE 74 75 REPORT DATE LICENSEE EVENT REPORT
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~04 bl03 Diesel Generator, the associated coolin water um tri ed due to breaker mal function.
Before the breaker was manuall closed and coolin water um restarted the enerator cool in water inlet tern er-
~OS ature increased to 210OF.
The diesels r
~O7 heat dama e but none was found.
The cool in water um brea er wa in-s ected and the contacts wer e found to be burned and an au
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENTCODE SUBCODE SUBCODE
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9 Io I I 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERiRO EVENT YEAR REPORT NO.
CODE TYPE NO.
Q17 REPOIIT ~79
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~0 21 22 23 24 26 27 28 29 30 31 32 ACTION.FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ 'RIMECOMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS
+22 SUBMITTED FORM SUB, SUPPLIER MANUFACTURER [B JQIR ~GQIE
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Diesel Generator 103 coolin water um tri was caused b
breaker mal-function.
The contacts in the breaker were found to be burned and a
.auxiliary contact was found stuck in the o en osition.
The breaker was repaired and the pump was manually started to test o erabilit
. The 4
cooling water pump breaker preventative maintenance rocedure will be 7
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FACILITY
~3P, METHOD OF STATUS
'4 POWER OTHERSTATUS ~
'ISCOVERY E
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10 44 45 PERSONNEL EXPOSURES NUMBER TYPE DLSCRIPTION Q39
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11 12 13 PERSONNEL INJURIES s
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Qoo NA DISCOVERY DESCRIPTION Q32 Operability Test LOCATIONOF RELEASE Q 80 80 80 80 7
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NAME OF PREPARFR 9
11 12 LOSS OF OR DAMAGETO FACILITYQ43 9
10 PUBLICITY ISSUED DESCRIPTION~
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U. S. NUCLEAR REGULATORY COMMISSION LICENSE NUMBER Qs.
NRC FORM 366 (7.77)
CONTINUED PAGE 2
LER 79-23 ~
LICENSEE EVENT REPQRT CONTROL BLOCK:
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(PI.EASE PRINT OR TYPE ALLREQUIRED INFORMATION)
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LICENSEE CODE 14 15 25 26 LICENSE TYPE 30 57 CAT 58 CON'T Q
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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10
~02 tact was found stuck in the o en osition.
The breaker was re aired
~03 0
4 and the pump was restarted manually to check its operation.
The Diesel Generator Operability Test was subsequently performed and successfull
~OS
~06 completed.
This event had minimal safety implications due to the re-dundancy of the system.
~07
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8 80
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8 REVISION LJ COMPONENT MANUFACTURER 44 47 SYSTEih'I
CAUSE
CAUSE CohIP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCOOE SUBCOOE Gi GE
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT LEAIAO EVENT YEAR RFPORT NO.
CODE TYPE Q17 REPORT
~79
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~02 3
21 22 23 24 26 27 28 29 30 31 ACTION. FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD.4 PRIME COMP.
TAKEN ACTION ON PI.ANT METHOD HOURS ~22 SUBMITTED FORM SUB.
SUPPI.IER
~GREIGE
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 0
revi sed to incorporate a separate operabi 1 ity test of the cool ing water OE.
pump prior to performing the entire diesel generator operability test.
3 4
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9 FACILITY STATUS
'4POWER OTHER STATUS Q30 [115]
Q25~ Q25 7
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10 12 13 44 ACTIVITY CONTENT RELEASEO OF RELEASE AMOUNTOF ACTIVITYQ36
~ Q33 Q34 7
8 9
10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q30 zz ~QuS 7
8 9
11 12 13 PERSONNEL INJURIES CKl~Q LOSS OF OA DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
9 Q42 7
8 9
10 PUBLICITY ISSUED DESCRIPTION~
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10 NAME OF PREPARER METHOD OF DISCOVERY
~Q3I 45 46 45 80 LOCATIONOF RELEASE Q 80 80 80 80 68 69 PHONE:
80 NRC USE ONLY ER 5
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DISCOVERY DESCRIPTION 32
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| 05000220/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000220/LER-1979-001-03, /03L-0 on 790218:during Performance of Surveillance,Test Flow Comparator 11 Did Not Produce Rod Block within Required Tolerance.Caused by Defective Rod Comparator.Component Replaced & Setpoint Left at 14% | /03L-0 on 790218:during Performance of Surveillance,Test Flow Comparator 11 Did Not Produce Rod Block within Required Tolerance.Caused by Defective Rod Comparator.Component Replaced & Setpoint Left at 14% | | | 05000220/LER-1979-002, Forwards LER 79-002/01X-1 | Forwards LER 79-002/01X-1 | | | 05000220/LER-1979-002-01, /01X-1 on 790306:during Refueling Outage While Preparing Emergency Condenser Steam Nozzle 5-NB for Replacement of safe-end,discovered Inconel Weld Was Removed from Nozzle.New Safe End Installed | /01X-1 on 790306:during Refueling Outage While Preparing Emergency Condenser Steam Nozzle 5-NB for Replacement of safe-end,discovered Inconel Weld Was Removed from Nozzle.New Safe End Installed | | | 05000220/LER-1979-005-03, /03L-0 on 790401:during Periodic Type C Leakage Test,Valves IV-68-06,IV-201-09,IV-201-10 & IV-58.1-02 Were Found to Be in Excess of Tech Specs.Cause Unknown.Repairs Will Be Made During Outage | /03L-0 on 790401:during Periodic Type C Leakage Test,Valves IV-68-06,IV-201-09,IV-201-10 & IV-58.1-02 Were Found to Be in Excess of Tech Specs.Cause Unknown.Repairs Will Be Made During Outage | | | 05000220/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000220/LER-1979-008-03, /03L-0 on 790510:during Refueling Outage, Containment Spray Heat Exchangers 112 & 121 Failed Leak Rate Test.Caused by Tube Leaks.Tubes Plugged | /03L-0 on 790510:during Refueling Outage, Containment Spray Heat Exchangers 112 & 121 Failed Leak Rate Test.Caused by Tube Leaks.Tubes Plugged | | | 05000220/LER-1979-009-03, /03L-0 on 790510:during Refueling Outage,Site Operations Review Committee Failed to Review Temporary Change to Maint Procedure N1-MP-7.11 within 7-day Limit. Change Subsequently Reviewed | /03L-0 on 790510:during Refueling Outage,Site Operations Review Committee Failed to Review Temporary Change to Maint Procedure N1-MP-7.11 within 7-day Limit. Change Subsequently Reviewed | | | 05000220/LER-1979-010-03, /03L-0 on 790424:during Refueling Outage, Containment Vacuum Relief Valve 68 IV-10 Flange Failed Leak Rate test.O-rings Replaced on Flange | /03L-0 on 790424:during Refueling Outage, Containment Vacuum Relief Valve 68 IV-10 Flange Failed Leak Rate test.O-rings Replaced on Flange | | | 05000220/LER-1979-011, Submits Rept of Individual Employee Overexposure to Radiation.General Inability to Adhere to Radiation Work Permit May Have Contributed to Overexposure.Dosimeter & Film Data Encl.Case Reported in LER 79-011/03L-0 | Submits Rept of Individual Employee Overexposure to Radiation.General Inability to Adhere to Radiation Work Permit May Have Contributed to Overexposure.Dosimeter & Film Data Encl.Case Reported in LER 79-011/03L-0 | | | 05000220/LER-1979-011-03, /03L-0 on 790517:during Refueling Outage, Discovered That Radiographer Received Overexposure of 3,790 Millirems for Second Quarter 1979.Cause Unknown & Under Investigation.Discussed Further in to NRC | /03L-0 on 790517:during Refueling Outage, Discovered That Radiographer Received Overexposure of 3,790 Millirems for Second Quarter 1979.Cause Unknown & Under Investigation.Discussed Further in to NRC | | | 05000220/LER-1979-012, Forwards LER 79-012/01T-0 | Forwards LER 79-012/01T-0 | | | 05000220/LER-1979-012-01, /01T-0 on 790523:concrete Anchor Bolt Deficiencies & Missing Seismic Restraints Were Discovered on Class I Seismic Piping Sys.Caused by Incorrect Installation.Concrete Anchor Bolt Repair Program Will Be Completed by 791231 | /01T-0 on 790523:concrete Anchor Bolt Deficiencies & Missing Seismic Restraints Were Discovered on Class I Seismic Piping Sys.Caused by Incorrect Installation.Concrete Anchor Bolt Repair Program Will Be Completed by 791231 | | | 05000220/LER-1979-013, Forwards LER 79-013/03L-1 | Forwards LER 79-013/03L-1 | | | 05000220/LER-1979-013-03, /03L-1:on 790525,during Refuelling Outage,Three Instrument Surveillance Procedures Were Implemented Before Required Temporary procedure-change Signatures Were Obtained.Cause Not Stated | /03L-1:on 790525,during Refuelling Outage,Three Instrument Surveillance Procedures Were Implemented Before Required Temporary procedure-change Signatures Were Obtained.Cause Not Stated | | | 05000220/LER-1979-014-03, /03L-0 on 790319:during Refueling Outage,Core Spray Sys Snubber 40-HS-10 Found Inoperable.Caused by Worn Piston Seals on Core Spray Snubber Resulting in Loss of Fluid from Snubber.Seals Replaced & Snubber Reinstalled | /03L-0 on 790319:during Refueling Outage,Core Spray Sys Snubber 40-HS-10 Found Inoperable.Caused by Worn Piston Seals on Core Spray Snubber Resulting in Loss of Fluid from Snubber.Seals Replaced & Snubber Reinstalled | | | 05000220/LER-1979-014, Forwards LER 79-014/02L-0 | Forwards LER 79-014/02L-0 | | | 05000220/LER-1979-015, Forwards LER 79-015/03X-1 | Forwards LER 79-015/03X-1 | | | 05000220/LER-1979-015-03, /03X-1:on 790610,during Refueling outage,10-s Time Delay 12K62 Failed in Conservative Direction,Creating Alarm Condition.Caused by Natural end-of-life.Clutch Coil Replaced | /03X-1:on 790610,during Refueling outage,10-s Time Delay 12K62 Failed in Conservative Direction,Creating Alarm Condition.Caused by Natural end-of-life.Clutch Coil Replaced | | | 05000220/LER-1979-016, Forwards LER 79-016/03L-0 & LER 79-017/03L-0 | Forwards LER 79-016/03L-0 & LER 79-017/03L-0 | | | 05000220/LER-1979-016-03, /03L-0 on 790626:failure to Review Temporary Electrical Maint Procedure within Seven Days.Review Made & Approvals Received | /03L-0 on 790626:failure to Review Temporary Electrical Maint Procedure within Seven Days.Review Made & Approvals Received | | | 05000220/LER-1979-017-03, /03L-0 on 790612:containment Spray Water Intertie Valves Leaked Causing Failure of Integrated Leak Rate Test. Valves Removed,Cleaned & re-installed | /03L-0 on 790612:containment Spray Water Intertie Valves Leaked Causing Failure of Integrated Leak Rate Test. Valves Removed,Cleaned & re-installed | | | 05000220/LER-1979-018-03, /03L-0 on 790726:vacuum Relief Sys Switch 68-12B Failed to Open at Proper Setpoint.No Cause Identified.Switch Adjusted to Proper Setpoint | /03L-0 on 790726:vacuum Relief Sys Switch 68-12B Failed to Open at Proper Setpoint.No Cause Identified.Switch Adjusted to Proper Setpoint | | | 05000220/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000220/LER-1979-019-03, /03L-0:on 790816,during Steady State Operation, Routine Mgt Review Disclosed Failure to Complete Five Surveillance Tests on Schedule.Tests Immediately Performed & Completed.Personnel Instructed to Follow Published Schedule | /03L-0:on 790816,during Steady State Operation, Routine Mgt Review Disclosed Failure to Complete Five Surveillance Tests on Schedule.Tests Immediately Performed & Completed.Personnel Instructed to Follow Published Schedule | | | 05000220/LER-1979-020-03, /03L-0:on 790901,during Steady State Operation, Drywell Cooler 14 Tripped & Leakage Increased to Above Five G/Minute.Caused by Cooler Tube Leak.Cooler Isolated & Returned to Acceptable Level.Shutdown Terminated | /03L-0:on 790901,during Steady State Operation, Drywell Cooler 14 Tripped & Leakage Increased to Above Five G/Minute.Caused by Cooler Tube Leak.Cooler Isolated & Returned to Acceptable Level.Shutdown Terminated | | | 05000220/LER-1979-021-04, /04T-0:on 790905,noted That Analysis of Excesssive Nuclide Water Sample Concentrations Was Not Completed within 30 Days.Caused by Late Rept by Contractor & High Influx of Samples.Addl Personnel Added | /04T-0:on 790905,noted That Analysis of Excesssive Nuclide Water Sample Concentrations Was Not Completed within 30 Days.Caused by Late Rept by Contractor & High Influx of Samples.Addl Personnel Added | | | 05000220/LER-1979-021, Forwards LER 79-021/04T-0 | Forwards LER 79-021/04T-0 | | | 05000220/LER-1979-022, Forwards LER 79-022/01T-0 | Forwards LER 79-022/01T-0 | | | 05000220/LER-1979-022-01, /01T-0:on 790918,noted Failure to Install Seismic Constraint on Containment Spray Sys Outside Primary Containment Per Const Drawings.Initiated Design & Order to Install Constraint.Containment Spray Loop Inoperable | /01T-0:on 790918,noted Failure to Install Seismic Constraint on Containment Spray Sys Outside Primary Containment Per Const Drawings.Initiated Design & Order to Install Constraint.Containment Spray Loop Inoperable | | | 05000220/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000220/LER-1979-023-03, /03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised | /03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised | | | 05000220/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000220/LER-1979-025-03, /03L-0:on 791027,during Surveillance Testing, Personnel Unable to Zero Side Average Power Range Monitor Flow Converter 11.Caused by Component Failure.Entire Unit Replaced & Problem Eliminated | /03L-0:on 791027,during Surveillance Testing, Personnel Unable to Zero Side Average Power Range Monitor Flow Converter 11.Caused by Component Failure.Entire Unit Replaced & Problem Eliminated | | | 05000220/LER-1979-079, Forwards LER 79-079/03L-0 | Forwards LER 79-079/03L-0 | |
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