05000220/LER-1979-023-03, /03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised

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/03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised
ML18037A207
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 11/02/1979
From: Duda E
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17053B179 List:
References
LER-79-023-03L, LER-79-23-3L, NUDOCS 7911130338
Download: ML18037A207 (4)


LER-1979-023, /03L-0:on 791004,cooling Water Pump of Diesel Generator 103 Tripped.Caused by Burned Contacts in Breaker. Breaker Repaired & Pump Started Manually.Preventative Maint Procedure Will Be Revised
Event date:
Report date:
2201979023R03 - NRC Website

text

NRC FORM 366

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~04 bl03 Diesel Generator, the associated coolin water um tri ed due to breaker mal function.

Before the breaker was manuall closed and coolin water um restarted the enerator cool in water inlet tern er-

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The cool in water um brea er wa in-s ected and the contacts wer e found to be burned and an au

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Diesel Generator 103 coolin water um tri was caused b

breaker mal-function.

The contacts in the breaker were found to be burned and a

.auxiliary contact was found stuck in the o en osition.

The breaker was repaired and the pump was manually started to test o erabilit

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~02 tact was found stuck in the o en osition.

The breaker was re aired

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4 and the pump was restarted manually to check its operation.

The Diesel Generator Operability Test was subsequently performed and successfull

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This event had minimal safety implications due to the re-dundancy of the system.

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revi sed to incorporate a separate operabi 1 ity test of the cool ing water OE.

pump prior to performing the entire diesel generator operability test.

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