05000220/LER-1979-019-03, /03L-0:on 790816,during Steady State Operation, Routine Mgt Review Disclosed Failure to Complete Five Surveillance Tests on Schedule.Tests Immediately Performed & Completed.Personnel Instructed to Follow Published Schedule

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/03L-0:on 790816,during Steady State Operation, Routine Mgt Review Disclosed Failure to Complete Five Surveillance Tests on Schedule.Tests Immediately Performed & Completed.Personnel Instructed to Follow Published Schedule
ML18037A197
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 09/10/1979
From: Duda E
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18037A196 List:
References
LER-79-019-03L, LER-79-19-3L, NUDOCS 7909170512
Download: ML18037A197 (4)


LER-1979-019, /03L-0:on 790816,during Steady State Operation, Routine Mgt Review Disclosed Failure to Complete Five Surveillance Tests on Schedule.Tests Immediately Performed & Completed.Personnel Instructed to Follow Published Schedule
Event date:
Report date:
2201979019R03 - NRC Website

text

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ATTACHMENT TO LE 79-19 Event Description and Probable Consequences During steady state operations, a routine management review disclosed failure to complete five monthly surveillance tests on schedule.

These included Nl-ST-H1, Liquid Poison Pump Flow Rate Discharge Pressure Test; Nl-ST-M2, Emergency Cooling System Makeup Tanks Level Control Valves Exercise; Nl-ST-M4, Emergency Diesel Generator Manual Start 8

1 Hour Rated Load Test; Nl-ST-H8, Emergency Ventilation System Operability Test, which were all two days late, and Nl-ST-H5, Radwaste Discharge Radiation Monitor Instrument Channel Test, which was one day late.

This resulted in minimal safety implications, since all these sur-veillance tests were successfully completed, and therefore, the systems involved would have operated properly if required.

ATTACHMENT TO LER 79-19e

.,Event Description and. Probable Consequences, 0

During steady state operations, a routine management review disclosed failure to complete five monthly surveillance tests on schedule.

These included Nl-ST-Ml, Liquid Poison Pump Flow Rate Discharge Pressure Test; Nl-ST-M2, Emergency Cooling System Makeup Tanks Level Control Valves Exercise; Nl-ST-M4, Emergency Diesel Generator Manual Start 5

1 Hour.

Rated Load Test; Nl.-ST-M8, Emergency Ventilation System Operability Test, which were all two days late, and Nl-ST-M5, Radwaste Discharge Radiation Monitor Instrument Channel Test, which was one day late.

This resulted in minimal safety implications, since all these sur-veillance tests were successfully completed, and therefore, the systems involved would have operated properly if required.