ML18029A779

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Insp Repts 50-259/85-36,50-260/85-36 & 50-296/85-36 on 850621-0726.Violation & Deviation Noted:Failure to Conduct post-maint Testing on CRD Hydraulic Unit & to Maintain Reactor Bldg Flood Level Switches,Respectively
ML18029A779
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 08/01/1985
From: Brooks C, Cantrell F, Patterson C, Paulk G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18029A776 List:
References
50-259-85-36, 50-260-85-36, 50-260-895-36, 50-296-85-36, NUDOCS 8508130331
Download: ML18029A779 (30)


See also: IR 05000259/1985036

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.IN.

ATLANTA,GEORGIA 30323

Report Nos.:

50-259/8S-36,

50-260/85-36,

and 50-296/85-36

Licensee:

Tennessee

Valley Authority

SOOA Chestnut Street

Tower II

Chattanooga,

Tennessee

37401

Docket Nos.:

50-259,

S0-260,

and 50-296

License

Nos.

DPR-33

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry 1, 2,

and

3

Inspection

Conducted:

June

21 - July 26;

1985

Inspectors:

G.

L.

Pau

, Senior

R si

nt

at

Signed

C. A.

Pa

erson,

Res

e

C.

R. Br

ks,

Reside t

D te Signed

P]

VS

D t

Signed

Approved by:

F.

S. Cantrell,

Section

C

f,

Division of Reactor

Proj cts

te Signed

SUMMARY

Scope:

This routine

inspection

involved

200 resident

inspector-hours

in the

areas

of operational

safety,

maintenance

observation,

reportable

occurrences,

program for control of measuring

and test

equipment,

surveillance

observation,

RPIP progress,

and organization

changes.

Results:

VIOLATIONS:

As

a result

of inspections

conducted

on

February 20-

March

1 (85-13)

and March 21-28,

1985, (85-20), violation ( 1) was identified.

For

administrative

purposes

this violation is

being

included

in

this

report.

(259/260/296/85-36-01).

( 1)

Technical Specification 6.3.A.

violation for failure

to

conduct

post

maintenance

testing

on

a control rod drive hydraulic unit and to perform

a

safety evaluation

on the High Pressure

Coolant Injection (HPCI) System

when

open

surge

suppression circuit resistors

were found.

8508130331

850807

pDR

hooch, 05000259

8

r,

(2).

10 CFR 50, Appendix B, Criterion

V violation for failure to have

HPCI torus

suction

valve

(73-27)

electrically

connected

in

accordance

with

TVA

drawings'3).

Technical Specification 6.3.A. for failure to have

an adequate

residual

heat

removal cross-tie

procedure

and to adhere

to high pressure fire protection

system valve lineups

(4)

10 CFR 50,

Appendix

B, Criterion XII. for failure to adhere

to the program

for maintaining measuring

and test equipment.

DEVIATIONS: One deviation of FSAR section

10. 11.5. 1 for not maintaining portions

of the reactor building flood level switches

operable

and seismically qualified.

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

J.

A. Coffey, Site Director

R.

L. Lewis, Plant Manager (Acting)

J.

E. Swindell, Superintendent

- Operations/Engineering

T.

D. Cosby,

Superintendent

Maintenance

(Acting)

J.

H. Rinne, Modifications Manager

J.

D. Carlson, guality Engineering

Supervisor

D.

C. Mims, Engineering

Group Supervisor

C.

G. Wages,

Mechanical

Maintenance

Supervisor

J.

C. Crowell, Electrical Maintenance

Supervisor (Acting)

R.

E. Burns,

Instrument Maintenance

Supervisor

A.

W. Sorrell, Health Physics

Supervis'or

R.

E. Jackson,

Chief Public Safety

T. L. Chinn, Senior Shift Manager

T.

F. Ziegler, Site Services

Manager

J .

R. Clark,

Chemical Unit Supervisor

B.

C. Morris, Plant Compliance Supervisor

A. L. Burnette, Assistant Operations'Group

Supervisor

R.

R. Smallwood, Assistant Operations

Group Supervisor

T.

W. Jordan,

Assistant Operations

Group Supervisor

S.

R. Maehr,

Planning/Scheduling

Supervisor

G.

R. Hall, Design Services

Manager

W.

C. Thomison,

Engineering

Section Supervisor

A. L. Clement,

Radwaste

Group Controller

Other

licensee

employees

contacted

included

licensed

reactor

operators,

auxiliary operators,

craftsmen,

technicians,

public safety officers, guality

Assurance,

Design

and engineering

personnel.

Exit Interview

(30703)

The inspection

scope

and findings were

summarized

on July 26,

1985 with the

Plant

Manager

and/or Assistant

Plant

Managers

and

other

members

of his

staff.

The licensee

acknowledged

the findings and took no exceptions.

The licensee

did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Licensee Action on Previous

Enforcement Matters (92702)

a.

(Closed)

Deviation

(259,260,296/83-23-03)

Special

Test

ST-8322,

High-Density

Fuel

Storage

System

Corrosion Surveillance

Program,

was

initiated October

26,

1983

and boral test

specimens

installed in unit

three

spent fuel pool

on October 25,

1983.

This item is closed.

b.

(Closed)

Open

Item (259,260,296/8Z-37-93)

- Contamination reports

have

been

revised

to include

the whole

body count date

and

number.

This

item is closed.

(Closed)

Violation.(260/81-18-05,

296/81-18-04)

The first example of

this violation was previously closed against unit one in Report 82-07.

A similar violation for failure to restore

fire protection

system

alignments after surveillance

(85-28-10) relates

to the

second

example.

For the third example,

similar problems

in the quality assurance

area

were noted in the Region II Inspection

Report

259/260/296/85-03

and

a

violation

was

issued

for "programmatic

breakdown

of the

program".

Future tracking in these

areas will be the recent violation.

This item

is closed.

d.

(Closed)

Unresolved

(296/85-25-07)

- Unit

3

High Pressure

Coolant

Injection (HPCI) System Motor Operated

Valve 73-27 timing discrepancy.

The inspectors

identified that the

HPCI valve 73-27 was noted to have

a

timing discrepancy

during

a review of the surveillance instruction,

SI

4.5.E. 1.C., for stroke time testing.

The licensee

followed up on this

concern

and determined that the valve motor windings were miswired such

that the motor was operated

as s differential

compound

D.C. motor vice

a cumulative

compound

D.C.

motor

as

designed.

The licensee

=conducted

special

test

8508 to verify the valve would operate

adequately

under

stimulated

accident

conditions.

The

valve

operated

with

a

27

psig

differential pressure

across

the valve.

This item is closed

and will

be addressed

as

a violation of 10 CFR 40, Appendix

B, Criterion

V for

failure to

have

the valve electrically

connected

in accordance

with

TVA drawings

45N714-2RB,

45N3711-3RA and 45N3711-5RA.

(296/85-36-02).

4.

Unresolved

Items* (92701)

Two unresolved

items

were identified during this inspection

period.

One

unresolved

item concerning

chemistry is identified in paragraph

eight.

The

second

unresolved

item is identified below.

The

licensee

discovered

on

June

28,

1985 that the

Standby

Gas

Treatment

(SBGT) charcoal

bed heaters

required resetting after operation of the

SBGT

system.

The Vicensee

was previously unaware of this fact.

The charcoal

bed

temperature

is controlled at

125 degrees

F.

to prevent

condensation

while

the

system is idle.

The

licensee

has

placed

"Caution"

signs

at

the

SBGT control

boards

and

initiated

a change

request

to replace

the heater control switches with ones

that will automatically restart

the heaters.

"An Unresolved

Item is

a matter

about

which

more

information is required

to

determine

whether it is acceptable

or may involve

a violation or deviation.

On July 24,

1985,

the inspector questioned

how it was

known that the heaters

had been reset

and were operating

properly after

system

operation.

It was

learned

that

no

routine

log

readings

were

taken

for the

charcoal

bed

temperature

or otherwise

to verify system

operation.

It could

not

be

determined if the heaters

had

been previously reset.

Additionally, no tour

of the

SBGT room is made

on the operator

rounds

sheets.

A previous

problem

was identified on

a tour by the inspector

where the relative humidity heater

breaker

was found tripped.

( IE Report 85-15).

Discussions

with cognizant

maintenance

and

operations

personnel

revealed

there is

a general

lack of understanding

of how the

SBGT heater circuitry

works.

There is an additional

temperature

switch set at

150 degrees

F. for

the charcoal

bed which gives

an annunciation

in the control

room.

Once the

annunciation

is received

the temperature

switch must

be locally reset.

Train

C of SBGT has

an additional

safety switch set at 450 degrees

F. which

the other trains

do not have.

This

item will remain

unresolved

pending

a further

review of the

system

operation

and charcoal

bed history.

(259/260/296/85-36-03).

Operational

Safety

(71707,

71710)

The

inspectors

were

kept

informed on-a daily basis

of the overall plant."

status

and

any significant

safety

matters

related

to plant

operations.

Daily discu'ssions

were held each morning with plant

management

and various

members of the plant operating staff.

The inspectors

made frequent visits to the control

rooms

such that each

was

visited at least daily when

an inspector

was

on site.

Observations

included

instrument

readings,

setpoints

and

recordings;

status

of

operating

systems;

status

and

alignments

of emergency

standby

systems;

onsite

and

offsite emergency

power

sources

available for automatic operation;

purpose

of temporary

tags

on

equipment

controls

and

switches;

annunciator

alarm

status;

adherence

to

procedures;

adherence

to limiting conditions

for

operations;

nuclear

instruments

operable;

temporary alterations

in effect;

daily journals

and logs;

stack monitor recorder

traces;

and control

room

manning.

This

inspection

activity

also

included

numerous

informal

discussions

with operators

and their supervisors.

General

plant <ours were conducted

on at least

a weekly basis.

Portions of

the turbine building, each reactor building and outside

areas

were visited.

Observations

included

valve positions

and

system

alignment;

snubber

and

hanger

conditions;

containment

isolation

alignments;

instrument

readings;

housekeeping;

proper

power supply

and breaker;

alignments;

radiation

area

controls;

tag controls

on equipment;

work activities in progress;

radiation

protection

controls

adequate;

vital

area

controls;

personnel

search

and

escort;

and vehicle search

and escort.

Informal discussions

were held with

selected

plant

personnel

in their functional

areas

during

these

tours.

Weekly verifications of system status

which included major flow path valve

alignment,

instrument

alignment,

and

switch

position

alignments

were

performed

on

the

Containment

Atmospheric

Dilution

(CAD)

and

Standby

Gas

Treatment

(SBGT) systems.

A complete

walkdown

of the

accessible

portions

of the

CAD

system

was

conducted

to verify system operability.

Typical of the items

checked during

the

walkdown were:

lineup procedures

match plant drawings

and the as-built

configuration,

hangars

and

supports

operable,

housekeeping

adequate,

electrical

panel

interior conditions, calibration dates

appropriate,

system

instrumentation on-line, valve position ali'gnment correct,

valves

locked

as

appropriate

and

system indicators functioning properly.

During the

CAD system walkdown, the following discrepancies

were identified

and discussed

with lice~see

representatives:

1)

Host of the fasteners

for the electric

heater

enclosure

cover plate

were missing

on both

CAD trains.

2)

The "A" train electric heater controller was found TRIPPED.

3)

Valve 0-HCV-84-103

was

no longer installed

in the system.

This valve-

is

shown

on flow diagram 47W862-l.

Although an operator

had discovered

this condition

and

documented it on the

system

abnormal

status

data

sheet

on 10-29-83,

the licensee's

discrepancy

report

has just recently

been actively pursued.

4)

Both trains of the

CAD system

had sections of their piping covered with

ice apparently

from the

expansion

of liquid nitrogen

due to leaking

valves.

5)

Numerous valves were missing identification labels.

0-84-104,

FE-84-7,

0-84-562,

PCV-84-10

and 0-84-108).

FSAR Section

10. 11.5. 1,

Fire Protection

Systems

Seismic Analysis,

states

that failures of the non-seismically-designed

High Pressure

Raw Water Fire

Protection

System in the Reactor Building could allow raw water to enter the

building.

All such

failures

are

detected

by at least

two seismically

qualified meatus

such

as the initiation of the

Reactor

Building floor drain

system,

and the water level switches

six inches off the floor in the torus

area,

HPCI room

and

RCIC

room.

An inspection

of the water level

switches

revealed

that

some

are

not seismically qualified.

The deficiencies

found

are listed below:

a.

Unit Three - Reactor

Core Isolation Coo'ling

Room Level Switch

(1)

The

top

mounting

plate

contains

only one of the four mounting

bolts.

,

(2)

The lower mounting plate contains

only two of the four mounting

bolts.

Unit Three

High Pressure

Coolant Injection

Room Level Switch

( 1)

The top mounting plate contains

only two of four mounting bolts.

One bolt is cocked

and

not fully inserted.

The plate is pulled

away from the wall one quarter of an inch.

(2)

The

lower mounting plate contains

only two of the four mounting

bolts.

The plate is pulled away from the wall and

one bolt is not

fully inserted.

Additionally, the inspector questioned

whether the level switches

were

routinely checked

for operability.

The switches

were not found to be

on any schedule

for a periodic functional test.

A functional test

was

performed

on all

three

units

and

the following instruments

did not

pass:

(1)

Unit One corner

room

residual

heat

removal

level

switch

(RHR)

LS-77-25C

(2)

Unit One corner

room

residual

heat

removal

level

switch

(RHR)

LS-77-25D

(3)

Unit Two corner

room - reactor

core isolation cooling level switch

- LS-77-25A

Unit one torus

level

switch was

found- to

be enclosed

in

a metal

box.

The inspector questioned

whether

the level

switch could still perform

its function.

The

licensee

conducted

an

evaluation

and

stated

the

switch was still operable.

The metal

box was installed to protect

the

switch while torus modifications

were

being

conducted.

The

box was

removed.

On July 24,

1985,

the inspector

was

informed that

a design

change

request

had

been initiated for specification of the

necessary

seismic

mounts.

The flood level

switches

were installed

per

a plant

drawing

which

specified,

"field to install".

Collectively,

these

deficiencies

were given as

a deviation in an exit meeting

on July 26,

1985 with plant

management

(259/260/296/85-36-04).

During

a routine

tour of the Unit one reactor building on June

17,

1985,

the inspector

observed water overflowing from

a drain

funnel

onto the floor of the

565 foot elevation.

Workers in the area

were performing

an annual fire

protection

system

surveillance

instruction,

SI-4. 11.A. l.a,

Simulated

Automatic

and

Manual

Actuation

of

High

Pressure

Fire

Pumps

and

Automatic

Valve Operability.

Simulated

operation

of deluge

valves

FCV-1-26-77

had just

occurred

when

the

flooding

occurred.

Header

isolation valve 1-26-1082

was shut to stop the flooding.

The inspector

requested

an evaluation

of the

event

on June

17,

1985,

from the safety supervisor

and informed plant management

in a daily

NRC

meeting.

On June

25,

1985,

the inspector

was notified by the fire protection

engineer that

a one inch normally closed drain valve (26-77-SD)

on the

outlet of the deluge valve

had

been inadvertently left open in the past

which

resulted

in

the

flooding.

Also,

the

drain

line

was

not

completely

centered

over

the

drain

funnel

resulting

in

the

water

spillage

on the reactor building floor.

It was

not

known

how the drain valve (26-77-SD)

was misaligned to the

open

position prior to

performance

of the surveillance

instruction.

The valve is physically located

10 feet above

ground level.

This valve

is

checked

closed

during

a

monthly surveillance,

SI 4.11.D.1,

Fire

Protection

System

Inspection

(Monthly);

and

the

procedure

was

last

performed

on May 31,

1985.

Also, during the annual

surveillance after

testing

the

deluge

the drain -valve is

opened

to drain

the

piping

between

the deluge

valve

and

the outlet header

isolation valve.

The

valve

is

then

checked

closed.

The

annual

surveillance

was

last

performed

on June

12,

1984.

Independent

verification that

the drain

valve is closed

was not in either surveillance

procedure.

The inspector

expressed

the

concern

to plant

management

on June

25,

1985

that

there

might

be

other

system

valves

misaligned

and

the

significance of the

reduction

of available

flow through

the

deluge

valve

The fire protection engineer

stated that the drain valve being

open

was

estimated

to be equivalent to the addition of two to three additional

sprinkler

heads

to

the

system

but

no

formal

calculations

were

performed.

Also,

no additional

valve lineups

were

conducted

to check

for additional misaligned valves.

A review of Operating

Instruction

26 (High Pressure

Fire Protection

System)

revealed

that on'he

valve checklist,

valve

1-26-77-SD

is

required to

be in shut position.

This lineup was

shown

as current

on

May 16,

1985.

Plant

management

was

informed

in

an exit meeting

on

July 26,

1985,

this

was

a

second

example

of the violation against

T.S. 6.3.A. for failure to adhere

to plant fire protection

procedures

(259/85-36"05).

The

inspector

reviewed

the

licensee's

procedures

related

to

the

Residual

Heat

Removal

(RHR)

System cross-tie

feature

as

described

in

paragraphs

4.8.6.4

and F.7. 16 of the

FSAR.

The cross-ties

are provided

to maintain

long-term

reactor

core

and

primary

containment

cooling

capability irrespective of primary containment integrity or operability

of the

RHR system associated

with a given unit.

Suppression

pool water

which

has

been circulated

through the

RHR heat exchangers

on one unit

can

be

used

to

flood

the

reactor

core,

spray

the

drywell

and

suppression

chamber

or

return

to

the

suppression

chamber

of

the

adjacent

unit.

The

shared

feature

is designed

to provide continuing

core cooling in the

most degraded

state of the effected units

RHR and

Core Spray Systems,

namely, that of complete failure due to inundation

from tor'us,

torus

header

piping failure, or other causes.

The shared

system

is

normally valved off.

Valves

are

located

high

enough

to

insure

adequate

time

for

lineup

before

they

become

inundated.

Instrumentation

is provided to annunciate

a flooding condition to the

operators.

Operating

Instruction

74,

Residual

Heat

Removal

System,

addresses

the

cross-tie

function in Section

IV.F., cross

connecting

between

loops.

The procedure

specified

in this section

was

found to

be

unworkable.

The

RHR

pumps

are interlocked with their suction

valves

to prevent

damage

due to overheating

at no-flow.

The cross-tie

lineup specified

in OI-74

requires

the adjacent unit

pump suction

valves to

be closed

but does

not require bypassing

the suction valve inter lock in the

pump

start circuitry.

This cross-tie

procedure

is also limited for use

in

the containment

cooling mode only and does not'ddress

the reactor core

cooling

mode

discussed

in the

FSAR.

These

two problems

shall

be

identified

as

the first example

of

a violation for compliance with

T.S.6.3.A: (259/260/296/85-36-05).

1

The inspectors

also determined that the Reactor

Building Basement

flood

level

switches

(LS-77-25A,

B,

C,

D,

E

and

F)

are

not periodically

tested

to

assure

operability

and

that

the

annunciator

response

procedure for these

instruments

contained

no reference

to the potential

for torus failure

and

the

need

to initiate

the

RHR cross-tie

valve

lineup

prior to

valve

inundation

from flooding.

Plant

personnel-

initiated

a maintenance

request to functionally test the level switches

and the annunciator

response

procedure

is to be revised.

The licensee

called

in

a

4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> report per

10 CFR 50.72

on July 19,

1985 regar ding the Containmant

Atmosphere Dilution (CAD) System.

While

investigating

the

cause

of the improperly installed pressure

switches

(PS-84-21

and PS-84-22)

the

licensee

discovered

that the flow element

orifices

(FE-84-19

and

FE-84-20)

were

not

in accordance

with the

original

system

design.

The

design

called

for orifices

sized

to

provide

a 20"

WC pressure

drop at

100

SCFM.

The installed orifices

were found to provide

a 20"

WC pressure

drop at 200

SCFM.

The licensee

additionally identified that

the

flow control

valves

( FCV-84-19

and

FCV-84-20)

to which

these

orifices

provide

flow sensing

input

are

over sized.

The ,combined effect of the as-found

discrepancies

is that

upon initiation of drywell/suppression

chamber

post-accident

venting

with the

CAD system,

a pressure

increase

in the

CAD system would occur

in excess of the

1 psig design

pressure

down-stream

of the orifice.

This condition would cause

the protective

pressure

switches

PS-84-21

~ and

PS-84-22

to isolate

the

CAD vent

valves

and

prevent

drywell/

suppression

chamber

venting.

The

licensee

was

unable

to determine

whether the error in buying the orifices

came

from the

purchasing

or

design

groups

but the

purchasing

contract

erroneously

specified

the

orifice was to provide

a 20"

WC pressure

drop at

200

SCFM.

The error

in buying

the

flow control

valves

was

suspected

to

be

due

to the

improper acceptance

of substitute

valves

by the

licensee

which were

provided

by the manufacturer.

The event

was considered

reportable

by

the licensee

since

the

CAD system

could

have failed to

perform its

~ l

intended

function

and

the plant

was considered

to be in an unanalyzed

condition.

6.

Maintenance

Observation

(62703)

Plant

maintenance

activities

of

selected

safety-related

systems

and

components

were

observed/reviewed

to ascertain

that they were conducted

in

accordance

with requirements.

The following items

were considered

during

this review:

the limiting conditions for operations

were

met; activities

were

accomplished

using

approved

procedures;

functional

testing

and/or

calibrations

were

performed

prior to

returning

components

or

system

to

service;

quality

control

records

were

maintained;

activities

were

accomplished

by qualified personnel;

parts

and materials

used

were properly

certified;

proper tagout clearance

procedures

were

adhered

to;

Technical

Specification

adherence;

and

radiological

controls

were

implemented

as

required.

Maintenance

requests

were

reviewed to determine

status of outstanding

jobs

and

to

assure

that priority was

assigned

to

safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the

below listed maintenance activities during this report period:

a.

System

Instrument

Maintenance

Instruction

65 - Standby

Gas

Treatment

System Calibration

and Maintenance

b.

Electrical Maintenance

Instruction

90 - Reactor Building and

RHRSW pump

room flood level switches functional test

c.

Special

Operating

Instruction

12 - Jet

Pump

Instrumentation

Nozzle

Replacement

and Repair of Crack in Recirculation

Discharge

Piping

d.

Special

Mechanical

Maintenance

Instruction

20 - Repair of cracked

sensing

line from Penetration

N-28

e.

Mechanical

Maintenance

Instruction

107

TVA Test Procedure

for Target

Rock Valves Model 7567

F

The licensee

made

a one-hour report

on July

16,

1985 after declaring

loop

one of the residual

heat

removal

system

on unit three inoperable.

A snubber

(R-41)

was

found with the

rod disconnected

from the

cam

and

a restraint

(H-3)

had

twe- broken

welds

causing

a one-half

inch

gap

at

the

break.

Vibration was suspected

as the cause of the fai lure.

An engineering

design

evaluation

was requested

by the plant to address

the vibration problem.

7.

Surveillance Testing Observation

(61726)

The

inspectors

observed

and/or

reviewed

the

below listed

surveillance

procedures.

The inspection

consisted

of

a

review of the

procedures

for

technical

adequacy,

conformance

to technical

specifications,

verification

of test

instrument calibration,

observation

on

the

conduct

of the test,

removal

from service

and return to service of the system,

a review of test

data,

limiting condition

for

operation

met,

testing

accomplished

by

qualified personnel,

and that the surveillance

was completed at the requi red

frequency.

, a.

Surveillance

Instruction 4.2.B-26

Instrumentation

that initiates

or

controls the

CSCS Condensate

Header

Low Level.

b.

Surveillance

Instruction 4.6.D - Main Steam Relief Valves

c.

Surveillance

Instruction

4.11.D - Fire Protection

System

Inspection

(Monthly)

d.

Surveillance

Instruction

4. 11.A. l.a - Simulated

Automatic

and

Manual

Actuation of High Pressure

Fire

Pumps

and Automatic Valve Operability

e.

Surveillance

Instruction

4. 10'. 1

Refueling

Interlocks

Functional

Test

No deviations or violations were identified in this section.

8.

Reportable

Occurrences

(90712,

92700)

The below listed licensee

events

reports

(LERs) were reviewed to determine-

if the

information

provided

met

NRC

requirements.

The

determination

included:

adequacy

of event description,

verification of compliance with

technical

specifications

and

regulatory

requirements,

corrective

action

taken,

existence

of potential

generic

problems,

reporting

requirements

satisfied,

and

the relative safety significance of each event.

Additional

in-plant reviews

and discussion

with plant personnel,

as appropriate,

were

conducted

for

those

reports

indicated

by

an

asterisk.

The

following

licensee

event reports

are closed:

LER No

"260/85-04

296/85-06

R1

Date

7-03-85

2-13-85

EVENT

Reactor

Water Chemistry-

Low pH

Unit 3 Reactor Water Level

Mismatch

"259/85-07

3-18-85

Unmonitored Stack

Gas

Release

0

The inspector's

review of LER 260/85-04 indicated that

a detailed

review of

the

low reactor water

pH incident was warranted.

The statement

in the

LER

indicating that

no corrective action

was planned

was found to be inaccurate

since

an ongoing evaluation

was still in progress.

The following inspector

10

concerns

were discussed

with licensee

representatives

and will be tracked

as

an unresolved

item (259/260/296/85-36-06)

pending resolution:

a.

No formal

procedure

exists for correcting

low pH coolant chemistry

or

additional

sampling

and analysis

requirements

for determination

of. the

cause.

b.

The action

level

assignments

in TI-38 provided insufficient margin to

allow corrective

action

of

degrading

chemistry

trends

prior

to

exceeding

technical

specification limits (only upon violation of the

technical

specification limit was the lowest action level triggered).

c.

Apparent

inadequacy

of sample flush volumes for the bottom drain

sample

location.

d.

Conflicting statements

in the event

memorandum

regarding the cause of

the

low

pH condition

(one

paragraph

indicates

than

an

RBCCW ingress

does

not match

the

observed

chemical

analysis

whereas

the conclusion

states

that

an ingress of

RBCCW is the most likely cause).

e.

The

possibility

that

weld

repair

activities

caused

the

low

pH

condition.

f.

Lack of

a

formal

inspection

or -monitoring

program

to confirm the

suspected

leak in the

RWCU non-regenerative

heat exchanger.

g.

Lost

information

on

chemistry

trend

graphs

due

to off-scale

data

points.

h.

Loss of resin lot number traceabi lity due to incomplete demineralizer

data

sheets

(Log Sheet 754-1).

i.

The incident evaluation

failed to

address

the

source

of oxalate

(a

chemical

species

from degraded

resin)

which was found in a post event

sample.

j.

The

cause

for

the

month

long

downward

trend

in

pH

has

not

been

evaluated

(see

the attached

trend chart,

Attachment 1).

10.

Measuring

and Test Equipment

Program

(61724B)

The licensee's

program for control of measuring

and test

equipment

(MME)

was

inspected

to

assure

compliance

with Regulatory

Requirements,

TVA's

Topical

Report,

TVA-TR-75-1A, Quality Assurance

Program

Description

for

Design,

Construction

and Operations,

and

TVA's Nuclear Quality Assurance

Manual - Operations

(N-OQAM).

The

upper-tier

documents

were

found

to

be

general

in nature,

setting

requirements

and policies

which were

delegated

to the

various

sections

(Operations,

Mechanical

Maintenance,

Instrument

Maintenance,

Electrical

Maintenance

etc.) for detailed

implementation

through

section

instructions

and procedures.

As

a result,

each section's

program is different with some

sections

having

MKTE coordinators

and detailed

instructions with prepared

data

sheet

formats while other sections

lack

a coordinator

and pencil data

sheets

are prepared

as required.

This lack of consistency

presents

problems

in record

retrieval

and verification of adequate

program

implementation.

Accountability of the utilization of MKTE, which is necessary

for evaluating

the effect of an as-found out-of-tolerance

condition

on previously completed

work, is

a prime example of this concern.

All sections

maintain

some

form

of

use

log with the

exception

of the

mechanical

maintenance

small tool

repair

and

calibration

shop.

This

shop

uses

working

standards

for

calibration

and

calibration

checks

on

such

METE

as

micrometers,

dial

indicators

and torque

wrenches.

This oversight

shall

be identified

as

an

example

of

a violation for failure to carry

out the quality

assurance

program in accordance

with written instruction (259/260/296-85-36-07).

0

The

program for adjusting

the calibration

frequency

of

M&TE based

upon

experience

with the equipment

as required

by Section 3.2. 1 of the

N-OgAM is

implemented

in Browns Ferry Standard

Practice

17.5, Control of Measuring

and

Test Equipment.

BF-17.5 requires that when

an out-of-tolerance

condition is

discovered,

in addition to an investigation of all activities involving the

MME subsequent

to its previous acceptable

calibration,

an evaluation

shall

be

made to determine

the

need

to increase

the calibration

frequency.

Two

examples

of

a

breakdown

in this

program

were

discovered.

Oscilloscope

number

251425

was

found out-of-tolerance

on its last five annual calibra-

tion s

(11/5/80,

10/26/81,

10/19/82,

10/21/83

and

10/19/84) .

The

out-of-tolerance

investigation report for these

occurrences

either did not

address

the

calibration

interval

or

concluded

that

the

interval

was

adequate.

The last investigation

report stated

"past

performance

of this

instrument

has

been

good,

so there is

no need

to increase

the calibration

frequency

at

this

time."

Pressure

gage

number

E00895

was

found

out-of-tolerance

on

two consecutive

semi-annual

calibrations

(2/29/84

and

8/28/84) yet the 'out-of-tolerance

investigation

reports failed to address

the

adequacy

of the calibration interval.

This

breakdown

is

a

second

example

of

a

failure

to

carry

out

the

quality

assurance

program

(259/260/296/85-36"07).

11.

Organization

Changes

On July 19,

1985 the site director announced

the following management

change

effective July 22,

1985:

Robert

L.

Lewis wi 11

become

Acting Plant Manager.

Mr. Lewis has

been

with TVA 31 years.

He

has held

a Senior Reactor Operator license

and

formerly

was Assistant

Plant

Manager

at

Watts

Bar

Nuclear

Plant.

Following an 18-month period

as

an evaluation

team manager for INPO he

returned

to

TVA in

1985 to

become

a senior shift manager

at

Browns

Ferry.

George

T.

Jones

has

been

reassigned

as

an assistant

to the

Director of Nuclear Services

in Chattanooga.

0

12

John

R. Pittman,

Superintendent

of Maintenance,

has

been

reassigned

as

a -project

engineer

in

the

Instrument

and

Controls

Branch

in

Chattanooga.

Tom D. Cosby,

Supervisor of Electrical

Maintenance,

will

serve

as the Acting Superintendent

of Maintenance.

Robert

McKeon will become

Operations

Supervisor.

Mr.

McKeon comes to

TVA from INPO where

he was

a Senior Plant Evaluator.

He previously was

, Manager of Operations

at Oyster Creek Nuclear Plant in New Jersey.

Ray

Hunkapi lier has

been

reassigned

as

a

senior shift

manager

on

the

7:00 a.m.

to

3:30

p.m. shift.

Mr.

Hunkapi lier's

reassignment

will

become effective August

19, 1985,'hen

Mr.

McKeon reports

to work at

Browns Ferry.

The site director gave the reasons

for the changes

as indicated below:

These

changes

provide

Browns Ferry with

a

new management

team in the most

critical

areas

of plant

operations

and

maintenance.

This action

is

an

integral

part of our efforts to strengthen

TVA's nuclear

program

and is

intended to bring performance

'at

Browns Ferry

up to the level

expected

by

TVA, NRC and the public.

12.

Regulatory

Performance

Improvement

Program

(RPIP)

The

responsible

Region II section chief reviewed

the status

of RPIP

and

'ctions

taken

by

TVA to

implement

specific

items

as

required

by

NRC

Confirmatory Order

EA 84-34 dated July 13,

1984.

TVA has assigned

a senior

manager

as

RPIP

Coordinator

at

the site.

His responsibilities

include

verifying that

each

task

has

been

implemented

as

described,

has

met

objectives,

and that the

necessary

programs

are

in place

to insure

that

objectives will continue to be met.

The status of RPIP

and action taken

by

TVA to

implement

specific

items

as

required

by

NRC Confirmatory

Order

EA 84-34

was

reviewed

during

a site visit July 10-12,

1985.

All of the

short

term items

and

most of the

long term

items

have

been

accepted

as

complete

by

TVA.

This

review

included

discussions

with responsible

personnel

and records of action taken to close the specific items.

Based

on

the above

review the following items are closed:

Short Term

Item Number

Descri tion

3.2

(84-SC"19)

Assign modification on

a project basis

Long Term

Item Number

5.1

(84-SC-70)

OgA review division and plant procedures

and

make

recommendation

for improvement

5.2

(84-SC-71)

Develop surveillance

and audit plant that

emphasizes

review of weak areas

0

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RWCU

'Y ~ w

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Tech.

Spec. Limit Shutdown

(5.3)

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21 Apr

25 Apr

28 Apr

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02 Jun

10 Jun