ML18016A374
| ML18016A374 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 03/27/1998 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18016A372 | List: |
| References | |
| 50-400-98-01, 50-400-98-1, NUDOCS 9804070327 | |
| Download: ML18016A374 (54) | |
See also: IR 05000400/1998001
Text
U. S.
NUCLEAR REGULATORY COMMISSION
REGION II
Docket No:
License
No:
50-400
Report
No:
50-400/98-01
Licensee:
Facility:
Carolina
Power
& Light (CP8L)
Shearon Harris Nuclear
Power Plant, Unit 1
Location:
5413 Shearon Harris
Road
New Hi
llew
NC 27562
Dates:
January
18 - February
28,
1998
Inspectors:
Approved by:
J.
Brady. Senior
Resident
Inspector
G. MacDonald, Project Engineer
(Section 08.2,
M8. 1,
and E8.1)
G. Wiseman,
Reactor
Inspector
(Sections
F1.1.
F2.1,
F5.1,
F5.2,
and F7.1)
W. Miller, Reactor Inspector
(Sections Fl.1, F2.1.
F5.1, F5.2,
and F7.1)
M. Shymlock. Chief, Projects
Branch 4
Division of Reactor Projects
Enclosure
2
'7804070327
980327
ADOCK 05000400
6
I
EXECUTIVE SUMMARY
Shearon
Harris Nuclear
Power Plant, Unit
1
NRC Inspection Report 50-400/98-01
This integrated
inspection included aspects of licensee
operations,
engineering,
maintenance,
and plant support.
The report covers
a 6-week
period of resident inspection;
in addition, it includes the results of
announced
inspections
by two regional
Reactor
Inspectors
and
a regional
Project Engineer:
~0e rat i ons
~
.Operations
performance
during the period was acceptable.
Operators
appropriately
responded to alarms
and abnormal conditions
(Section Ol. 1).
~
'Communications
system alarm testing
was being conducted
as committed to
in the
FSAR, although
documented acceptance'riteria
was considered
weak
(Section 01.2).
Self-assessment
activities were acceptable.
even though the
PNSC's
discussion
associated
with a root cause investigation for a missed
surveillance
did not identify that
a root cause
had not been addressed
(Section 07.1)
.
The licensee identified an additiona'l
example of failing to ensure
main
control
room chart recorders were'properly marking and timing, which
was identified as
a violation.
Corrective action for violation
50-400/97-09-02
was not effective and additional corrective actions
had
been identified from a root cause investigation for the additional
occurrence.
The root cause investigation
found that chart recorder
timing had not been properly checked
but it was not addressed
as
an
inappropriate act because
the investigation
was focussed
on marking
only.
This nar row focusing diluted the significance of the overall
finding of the root cause investigation
(Section 08.1).
~
Further review of the "C" steam generator
blowdown system water
hammer
event that occurred in December
1997.,
revealed that fai lure to enter
Technical Specification 3.7.8 Limiting Condition For Operation
when
a
blowdown system isolation valve snubber
was
removed
was
an isolated
case
and did not result in a Technical Specification violation
(Section 08.2).
Maintenance
~
Maintenance activities observed
were generally adequate.
A paper
wipe
was found in the "B" diesel
generator
lube oil tank that was apparently
left there during the
1997 refueling outage
(RF07).
This was identified
as
a Non-Cited Violation for fai ling to establish
adequate
foreign
material exclusion controls.
Engineering
performed
an inspection of
se'veral
Agastat relays in the load sequencers
and inadequate
solder
connections
were found and the relays were replaced
(Section Ml.1).
1
A violation was identified for inadequate
rod control system work
instructions.
The inadequate
wor'k instructions
were the result of
incomplete initial trouble-shooting
(Section M1.2).
The surveillance
performances
observed
were adequately
conducted
(Section
M2. 1).
~
A fai lure to conduct
a shutdown margin calculation
as required
by TS
Surveillance
Requirement
4. 1. 1. 1. l.a.
when control
rods were declared
on January
29,
1998,
was identified as
a violation
(Section M7.1).
~
blowdown system water hammer events
were reviewed
by the
maintenance
rule expert panel after the December
1997, water
hammer
event
and determined to have
been appropriately evaluated.
The expert
panel
meeting
on the issue
was thorough
and exhibited
a proper safety
focus
(Section M8.1).
En ineer in
The engineering operability evaluation for a paper wipe found in the
diesel
generator
lube oil suction tank was thorough
and concluded that
the paper
wipe would not have affected the diesel
(Section El. 1).
The short term operability determination for containment recirculation
sump brackets
was adequate.
It concluded that foreign material
exclusion cover brackets installed during construction could remain in
the
sump and the sump would still perform its intended function.
The
conclusion
was based
on tack welds haying been strength tested during
the outage
(RF07),
on calculations
which showed that if the brackets
came loose they wouldn't be transferred into the sump,
and that grout
installed during RF07 would hold the brackets
in place (Section E1.2).
~
A trend in corporate
procedure
inadequacies
was identified.
Trending of
corporate related adverse condition reports were being diluted because
the condition reports were spread
through all three sites corrective
action data
bases.
The licensee
had identified that trending program
guidance in general
was weak and was determining
a course of action to
address this issue
(Section E7.2).
~
Management,
including the Plant Nuclear Safety Committee.
was
appropriately
focussed
on determining the root cause of the event
and
ensuring corrective actions provide
a permanent solution.
Condition
report trending
had not revealed
a trend related to the blowdown events.
which had resulted iri a lack of management
attention prior to the event
(Section E8.1).
'
Plant
Su
ort
~
The control of contamination
and dose for the site was good and was
attributable to good teamwork
between. the various departments
(Section
Rl.l).
The performance of security
and safeguards
activities were good.
Security staff responded
appropriately to the discovery of a gun during
processing of employee belongings in the access
area X-ray machine
Section S1.1).
A violation was identified for failure to adequately
implement
and
maintain in effect the applicable provisions of the fire protection
program for
=-f'i re barrier penetration
seals
P 3008,
P 447A,
and
E 156.
(Section F1.1).
The licensee did not perform engineering
evaluat'ions that followed the
guidance of NRC GL 86-10 .for deviations
from fire barrier configurations
qualified by tests.
This was considered
an engineering
program weakness
(Section F1.1).
The surveillance inspection
procedure
for the fire barrier penetration
seals
was adequate.
The three most recent inspections
had been
satisfactorily implemented:
However,
a .large number of fire protection
surveillance
procedures
continued to be implemented within the grace
period of the procedure.
Action had been
implemented
by the licensee to
address this issue
and corrective action was anticipated
(Section
F2. 1).
The fire brigade demonstrated
good response
and fire fighting
performance
during
a simulated fire brigade drill conducted during this
inspection period (Section F5.1).
seal installer
was appropriately trained to
accomplish fire barrier penetration
seal installation work and Quality
Control inspectors
were qualified to per form the appropriate
verification for installation
and repairs
made to the fire barrier.
seals
(Section F5.2).
The licensee's
1998 Nuclear Assessment
Section
assessment
of the
facility's fire protection program was of good quality and effective in
identifying fire protection program performance to management.
Corrective actions in response
to the identified assessment
issues.
were
being implemented
and completion was anticipated in 1998 (Section
F7. 1).
l
I
Summar
of Plant Status
Unit 1 began this inspection period at
100K percent
power.
The unit
maintained approximately
100K power for the entire period.
01
Conduct of Operations
01.1
General
Comments
a.
Ins ecti on Sco
e
71707
I. 0 erations
.The inspectors
conducted
frequent
reviews of ongoing plant operations to
determine if procedures
were followed and technical specification
(TS)
requi rements
were .met.
b.
Observations
and Findin s
In general,
the conduct of operations
was professional
and safety-
conscious.
Routine activities were adequately
performed.
Operations
shift crews were appropriately sensitive to plant equipment conditions
and maintained
a questioning attitude in relation to unexpected
equipment
responses.
Operators
were appropriately
responding to plant
alarms
and abnormal conditions.
In particular, the performance of post-
maintenance testing
on the rod control system
caused
a rod sequencing
problem,
as discussed
in section
M1.2,
and resulted in entering
Abnormal
Operating
Procedure
AOP-l, Malfunction of Rod Control
and Indication
System,
Revision ll.
Operators appropriately
responded to this
situation
and the shift superintendent
was involved in the trouble-
shooting to ensure that the problem was appropriately resolved.
One
operations error was described
in section
M7. 1 related to a missed
surveillance.
c.
Conclusions
Operations
performance
during the period was acceptable.
Operators
appropriately
responded to alarms
and abnormal conditions.
02.2 R~li
a.
Ins ection Sco
e
71707
The inspectors
observed
weekly alarm testing to determine if it
adequately satisfied Final Safety Analysis Report
(FSAR) commitments.
Observations
and Findin s
The inspector
observed that the sections of Operation
Management
Manual
OMM-1, Conduct of Operations,
Revision 25 applicable to this test
contained
references
to FSAR sections
9.5.2
and American National
Standards
Institute (ANSI) N18.7/ANS3.2.
The inspector
observed that
the ANSI standard
discussed
periodic testing of the communications
system.
FSAR section 9.5.2,
Communications
Systems,
described
inspection
and testing in subsection 9.5.2.7,
which indicated that all
systems
were to be inspected
regularly and undergo operational
checks to
ensure service readiness
and effectiveness.
The inspector
found that
the operational
checks
were implemented
by OMM-1.
In addition, the
licensee
indicated that the inspection
and testing requirements
were
~implemented per checklist in the preventive maintenance
system under
preventive maintenance
route CL-E0013.
The inspector
found that
OMM-1
did not have any test acceptance criteria.
When operators
were asked
what criteria they used to determine test
adequacy,
they responded that
they could hear the alarm,
and with some uncertainty.
the fact that
there was
an absence of a communications
system trouble alarm.
The
criteria stated
were not described'in
OMM-1.
The licensee initiated
CR 98-00353 to address this issue.
The licensee
determined that the approach to alarm testing did not follow the general
guidance laid out in procedure
AP-004, Description of the Plant
Operating
Manual, Revision 7.
Tests that fulfill regulatory commitments
other than
TSs were to be placed in periodic test procedures
(OPT,
MPT,
etc.).
The alarm tests
were regulatory commitments.
and identified as
such in procedure
OMM-1 by providing an "R" next to the steps that
requi re the weekly alarm testing.
The licensee
intends to remove this
test from OMM-1 and write an operational
performance test
(OPT) with the
appropriate
acceptance criteria.
The
PM checklist was also being
reviewed for inclusion in a maintenance
performance test
(MPT).
The inspector
found that. the
FSAR testing
and inspection criteria were
being implemented.
However, the testing
and documentation criteria were
weak.
Conclusions
Communications
system alarm testing
was being conducted
as committed to
in the
FSAR, although
documented
acceptance criteria were considered
~ weak.
07
07.1
(Iuality Assurance in Oper ations
Licensee
Sel f-Assessment
Activities
Ins ection
Sco
e
40500
During the inspection period, the inspe'ctors
reviewed multiple licensee
self-assessment
activities, including:
.
Plant Nuclear Safety Committee
(PNSC) meetings
conducted
on
February ll and 19.
1998;
Nuclear Safety Review Committee
(NSRC) meeting conducted
on
February
18,
1998;
~
Nuclear Assessment
Section Audits on Environmental
and Radiation
~ Control Assessment
(HNAS98-005);
Observations
and Findin s
The portion of the
NSRC meeting observed exhibited
a good questioning
attitude.
The inspector also reviewed
NSRC comments
on the corrective
action program
as captured
by the training manager in a February
20,
1998, E-Mail.
NSRC comments in the E-Mail were focussed
on industry
experience with various aspects
of the program and provided, best
practice
recommendations
for the site to consider.
The program was in
the final development
process
for a corporate corrective action
procedure
which site personnel
were reviewing.
The
PNSC meeting
on February ll, 1998,
discussed
the steam generator
blowdown event root cause investigation
(CR 975320)
from December
1997.
A discussion of that meeting is contained in section
E8. 1.
The meeting
was good and in general
exemplified
a good questioning attitude.
For the portion of the
PNSC meeting observed
on February
19,
1998. the
inspector
found the committee thorough, with one exception.
The
exception dealt with the discussion of a root cause investigation for
condition report
(CR) 98-00340,
pertaining to a missed surveillance
on
January
29,
1998, for not performing
a shutdown margin determination
with shutdown
rod bank
"C" on the hold bus
(TS 4. 1. l.l.a).
The root
cause investigation indicated that
a condition report
(CR 97-04513)
had
identified an inconsistency
between
TS 3. 1.3. 1, 3. 1. 1. 1
~
and 4. 1. 1. l.a.
on October 6,
1997.
The root cause
described that the .inconsistency
in
the requirement for shutdown margin had caused
the operations
crew to
miss the surveillance
on January
29,
1998.
The inconsistency
was
determined to be the root cause,
and was agreed to and approved
by the
PNSC.
However, the inspector determined that the root cause
was not the
inconsistency,
but lack of management
action to the
1997
CR when the
inconsistency
was first identified.
The inspector
observed that in
1997, the surveillance
was not missed.
Also, at the time, the
I
08
08.1
operations
and regulatory affairs organizations
had collectively
determined the appropriate
meaning of the TS.
However, the failure to
communicate that determination to the remaining operators
resulted in
the surveillance being missed in 1998 and was determined
by the
inspector to be the root cause.
As
a result,
no corrective action was
identified to address
the root cause of the missed surveillance.
After
the inspector
discussed this issue with the
PNSC chairman,
the
PNSC
reconvened 'and appropriately
addressed
this item.
This item will be
reviewed further after submission of the
LER.
Conclusions
Self-assessment
activities were acceptable,
even though the
PNSC's
discussion
associated
with a root cause investigation for
a missed
surveillance did not identify that
a root cause
had not been adequately
addressed.
Miscellaneous
Operations
Issues
(92901)
0 en
Violation 50-400/97-09-02:
Failure to properly check main
control
room chart recorder.
The inspector
reviewed the violation
response,
dated
November
12 '997
and the licensee's
corrective actions
which indicated they would be complete
by December
1.
1997:
The
corrective actions were completed,
but were not effective,
as evidenced
by an additional occurrence identified by the licensee.
However, the
licensee
also chose not to close the condition report for the violation
based
on the additional occurrence.
Condition Reports
97-05121
and
97-05167 were written to address
the additional
instance
which occurred
on November 30,
1997 where main control
room chart recorders
were not
properly marking and were not detected
by the operators
over two shift
turnovers
and one marking period.
The inspector
reviewed the root cause investigation for the additional
occurrence,
completed'n
December
18.
1997, which identified that the
wide range recorder for steam generator
"8" was not marking on recorder
LR-477 (green pen).
In addition, the root cause investigation
identified that the chart had not been set
on the correct time and was
approximately
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> off.
Procedure
OMM-16, Operator
Logs,
Revision 14, indicated in paragraph
5. 1.2.b that the chart recorders
are
to be checked
once per shift to ensure that they are marking properly
and timing correctly.
The chart had not been timing correctly and nine
different individuals had not identified this 'although the chart was
initialed and marked with the time the check
was performed.
The
inspector
found that the root cause investigation findings collectively
displayed
a general
misunderstanding
of the
OMM-16 requirement
and
management
expectations
for its implementation.
The inspector discussed this root cause investigation with the licensee
who intends to address
the timing aspect
during real time training for
the operators
(an identified corrective action in the root cause
investigation).
The licensee stated that the failure to time the
recorder properly was listed as
an inappropriate act in the initial
version of the root cause investigation,
but was
removed in the final
version.
That decision
was based
on focussing
on recorder
pen marking
as opposed to the broader issue of operators
checking the recorders
once
per shift to ensure they would perform their function of trend recording
(marking and timing correctly).
This narrow focussing diluted the
significance of the overall finding of the root cause investigation.
After discussion with the licensee,
the licensee
informed the inspector
that corrective actions identified in the root cause
were being
reassessed
and that
a revised
response
to violation 50-400/97-09-02
was
being prepared.
This is considered
an additional
example of'failing to implement
procedure
OMM-16 as requi red by TS 6.8. l.a.
This failure to follow
procedures
is designated
violation 50-400/98-01-01,
example
1; Failure
to Properly Check Main Control
Room Chart Recorders.
Conclusions
The licensee identified an additional
example of fai ling to ensure
main
control
room chart recorders
were properly marking and timing'hich
was identified as
a violation.
Corrective action for violation 50-400/
97-09-02
had not been effective and additional corrective actions
were
identified from a root cause investigation for the additional
occurrence.
The root cause investigation
found that chart recorder
timing had not been properly checked but it was not addressed
as
an
inappropriate act because
the investigation
was focussed
on marking
only'.
This narrow focussing diluted the significance of the overall
finding of the root cause investigation.
0 en
Violation 50-400/97-13-01:
"C" Steam Generator
Blowdown (SGBD)
System Water Hammer.
This Unresolved
Item (URI) was opened in NRC Inspection
Report 50-400/
97-13 to further review the removal of safety-related
adjacent to the containment isolation valve, without entering
a
TS
action statement
and for review of the root cause
and repetitive nature
of water
hammer events
on the
SGBD System,
including their continued
occurrences.
Additionally, the inspectors
reviewed the treatment of
this event
under the maintenance
rule 10 CFR 50.65.
Refer to section
MB. 1 of this report for the discussion of SGBD water
hammer event review
under the maintenance
rule and section
E8. 1 for the discussion of the
review of the root cause evaluation of this event.
The inspectors
reviewed
CR 9705329,
Operator Logs'ngineering
Service
Request
(ESR)
9700949 Revision
0
~
and
TS sections 3.7.8, 3.6.3.
and
TS
Interpretation
Revision 5.
No Equipment Inoperability
Record
(EIR) was written following removal of the snubber
due to
miscommunication
and misunderstanding
of ESR 9700949.
EIR 97-1352
was
written after questioning
by the
NRC.
The snubber
was restored within
the TS action statement
time requirements.
The inspectors
concluded
that the licensee's
CR evaluation of the condition was adequate.
An
additional
work request
(97AHRZ1) involving snubber
1BDH-169 was
4
reviewed
and the inspectors verified that an EIR was opened for this
work activity and
TS requirements
were met.
The inspectors
concluded
that this was
an isolated event
and that the licensee did not violate TS
requirements.
Hl.l
Conduct of Maintenance
General
Comments
Ins ection Sco
e
62707
II. Maintenance
The inspectors
observed all or portions of the following work
activities:
~
.
WR/JO .98-AACD1
"B" diesel
lube oil changeout
~
WR/JO 98-AA7B-6
"B" sequencer
Agastat relay inspection
~
WR/JO 98-AAQM1
Fuse holder
replacement
in PIC-3
Observations
and Findin s
The inspectors
found the work performed under these activities to be
professional
and thorough.
All work observed
was performed with the
work package
present
and in active use.
Technicians
were 'experienced
and knowledgeable of thei r assigned
tasks.
The inspectors
frequently
observed
supervisors
and system engineers
monitoring job progress,
and
quality control personnel
were present
whenever required
by procedure.
Peer-checking
and self checking techniques
were being used.
The inspector discussed
with the licensee the circumstances
surrounding
a paper absorbent
wipe that was found in the "B" emergency diesel
generator
lube oil tank on January
29,
1998 during lube oil replacement.
Condition Report 98-00327
was issued to address this condition.
The
inspector
observed that there were two tanks,
one on the suction to the
lube oil pumps
and one on the discharge
from the engine.
The wipe was
in the tank on the suction to the three lube oil pumps.
The wipe was
found during performance of work under
WR/JO 98-AACD1 to change the lube
oil.
While removing the lube oil below a baffle that separates
the
upper
and lower half of the tank, workers noticed the wipe came floating
out from the side of the tank.
The workers concluded that the wipe had
been left in the tank since it was cleaned during the refueling outage
(RF07).
The inspector
reviewed procedure
HMM-011, Cleanliness,
Housekeeping,
(FME), Classification of Work Practices.
Revision 14,
and its predecessor
procedure
AP-619, Foreign Material
Exclusion.
Section 5.3.5 of HMM-11 discusses
FHE zones
and provides the
minimum requirements
for each
zone.
had been
a
Zone 4
FHE area.
As discussed
in the Operability Evaluation,
9800061,
the licensee
has identified that this area
should have included
\\
C.
M1. 2
logging of material in and out of the tank.
Section 5.3.5 indicates
that supervisors
are responsible'for
setting appropriate
2one
4
controls.
The controls for the lube oil tank were inadequate to ensure
that the wipe was
removed prior to the diesel
generator
being declared
operable..
This is identified as
a violation of TS 6.8. l.a and procedure
MMM-011 for fai ling to follow procedure to establish
adequate
foreign
material exclusion criteria for the diesel
generator
lube oil tank.
This non-repetitive,
licensee-identified
and corrected violation is
being treated
as
a Non-Cited Violation, consistent with Section VII.B.1
of the
This item is designated
NCV 50-400/98-
01-02 'nadequate
Foreign Material Exclusion Controls for Diesel
Generator
Lube Oil Tank.
The operability evaluation
review is contained
in section
E1.1.
The Agastat relay inspection
was prompted
by a
10 CFR 21 notification.
from the vendor
about
a potential
bad solder
connection.
The licensee
found three relays installed that were suspect.
All had performed
without problems during prior. load sequencer
testing.
All three relays
were replaced.
Engineering
performed the inspection of the relays after
they were
removed
by maintenance
personnel
and inadequate
solder
connections
were found.
The inspector considered
the establishment
of
acceptance criteria by Engineering to be good.
Conclusions
h
Maintenance activities observed
were adequately
performed.
A paper
wipe
was found in the "B" diesel
generator
lube oil tank that was apparently
left there during the 1997 refueling outage
(RF07).
This was identified
as
a Non-Cited Violation for failing to establish
adequate
foreign
material exclusion controls.
When inspected
due to a
10 CFR 21'otification,
several
Agastat relays in the load sequencers
were found
with inadequate
solder connections
and were replaced.
Rod Control
Ur ent Failure Alarm
Ins ection Sco
e
62707
The inspector
observed trouble-shooting
and post-maintenance
testing for
a rod control urgent failure alarm received
on February
24.
1998.
The
work was performed under
WR/JO 98-ABMA1.
Observations
and Findin s
The inspector observed that initial trouble-shooting to determine the
cause of the urgent failure alarm adequately
determined the cause of the
alarm.
The trouble-shooting
found that
a multiplexer relay in the
1BD
rod control logic cabinet
had failed.
The failure occurred while the
operators
were trying to insert control
bank "D".
After the relay was replaced
and,the urgent fai lure alarm was cleared,
the post maintenance
testing required
rods to be moved in two steps
and
out two steps.
When the testing. was accomplished,
the wrong group of
J
control
bank. "D" stepped
in first causing the rod sequence
to be
improper (> 2 steps
between groups).
The trouble-shooting
had failed to
recognize that the bank and group counters in the rod control system
had
become misaligned
when the urgent failure occurred.
The inadequacy
in
the trouble-shooting
resulted in inadequate
work order instructions
(WR/JO).
The instructions
should have required the counters to be
checked
and set to the proper settings
comparable to the rod height for
the Bank "D" group I and II rods.
Procedure
ADM-NGGC-0104, Work
Management
Process,
Revision 3, indicated in 9.8.7.9.d that the work
instructions shall contain
a level of'etail appropriate to the
complexity of the task to be accomplished.
The fai lure to have adequate
work instructions for repai r of the rod control system is
a violation of
TS 6.8. 1.a.
and procedure
ADM-NGGC-0104.
This is considered
a second
example of fai lure to follow procedures
and is designated
violation
50-400/98-01-01,
example 2, -Inadequate
Work Instructions for Rod Control
System.
The trouble-shooting of the rod sequencing
problem was initially not
well coordinated.
However,
once the shift superintendent
of operations
was involved the trouble-shooting
process
improved considerably
and
provided favorable results.
The rod control counters
were reset
and the
post-maintenance
test
was conducted successfully.
Conclusions
A violation was identified for inadequate
rod control system work
instructions.
The inadequate
work instructions
were the result of
incomplete initial trouble-shooting.
Maintenance
and Material Condition of Facilities and Equipment
Surveillance
Observation
Ins ection Sco
e
61726
The inspectors
observed all or portions of the following surveillance
tests:
OST 1036,
Shutdown Margin Calculation
Modes 1-5, Revision
11
MST I0269,
Lo-Lo Tave P-12 Interlock (T-0422) Operational
Test,
Revision
8
MST I0320,
Train
B Solid State Protection
System Actuation Logic
and Master Relay Test,
Revision
18
Observations
and Findin s
The inspector
found that the testing
was adequately
performed.
Conclusions
The surveillance
performances
observed
were adequately
conducted.
M7
Ouality Assurance
in Maintenance Activities
H7.1
Hissed Surveillance
on Shutdown
Mar in
Ins ection Sco
e
40500
The inspector
reviewed the circumstances
surrounding
a January
29.
1998.
for shutdown margin.
The inspector
reviewed
TS
3. 1.3. 1, 3. 1. 1. 1,
and 4. 1. 1. l.l.a, condition report 98-00340
and
attended
the
PNSC meeting where the root cause investigation
was
discussed
(Section 07. 1).
Observations
and Findin s
The operators
had placed the shutdown
bank
"C" rods
on the hold bus to
facilitate replacement of a power supply.
Placing rods
on the hold bus
will illuminate the rod control urgent failure alarm.
Alarm Response
Procedure
APP-ALB-013 for rod control urgent 'fai lure di rects the
operator
to Procedure
AOP-001. Halfunction of Rod Control
and Indication
Systems.
The operators
declared the rods
on the hold bus inoperable per
TS 3. 1.3. 1.
The oncoming shift identified that
evaluation
had not been conducted
as required
by TS 4.,1. 1. 1. l.a when the
rods were declared
Condition report 98-00340
was written to
address
that failure.
The root cause investigation described that operators
did not correctly
interpret the
TS wording and therefore,
failed to perform the shutdown
margin calculation.
TS 4. 1. 1. 1. l.a requires
a shutdown margin be
performed within one hour after
a control rod(s) is determined
After identification by the oncoming shift. the
surveillance
was accomplished
approximately
19 minutes after the TS
surveillance
4. 1. l.l.l.a requi red one hour time limit.
The root cause investigation also noted that condition report 97-04513
was written on October 6,
1997 to identify that there
was inconsistent
wording between
TS 3. 1.3. 1., 3. 1. 1. 1,
and 4. 1. 1. 1. l.a.
The condition
report identified that the surveillance could be missed since there
was
nothing to point an operator to TS 4. 1. 1. 1. l.a when
TS 3. 1.3. 1 was
entered for a rod control urgent fai lure alarm.
The condition report
was written after
a rod control urgent fai lure alarm had been received.
The inspector
noted that
CR 97-04513
was still open
and that action
had
been assigned
to train operators.
However, there
was no interim action
identified to clarify the identified inconsistency.
The inspector
observed that the licensee
was already
aware of the
inconsistency
on January
29,
1998, but had not promptly addressed
the
issue.
There were no interim measures
in place to alert operators to
the identified inconsistency
and operator training had not been
completed.
Consequently,
the occurrence of the January
29 '998,
missed
surveillance
can
be directly attributed to management
not implementing
interim corrective actions for
a previous condition report.
The root
cause investigation identified corrective actions which included
a
10
direct link between the alarm response'rocedure
and the shutdown margin
TS.
The fai lure to conduct
a shutdown margin evaluation within the required
one hour is considered
a violation of TS 4. 1.1. 1. 1.a
and is designated
violation 50-400/98-01-03,
Failure to Conduct
Surveillance Within One Hour.
Conclusions
A fai lure to conduct
a shutdown margin calculation
as required
by
Technical Specification Surveillance
Requirement
4. 1. 1. 1. l.a.'hen
control rods were declared
was identified as
a violation.
Miscellaneous
Maintenance
Issues
(92902)
0 en
URI 50-400/97-13-01:
"C" Steam Generator
Blowdown Water
Hammer
,
A significant water
hammer event occurred
on the "C" SGBD system piping
on December
22 '997.
The maintenance
rule data
base for the steam
generator
blowdown system
was reviewed.
The inspectors
observed that
the licensee
was documenting
system
and equipment failures in the
maintenance
rule data
base including water
hammer events.
The
SGBD was
currently in A(l) status
due to valve stroke time issues
unrelated to
the water
hammers;
The licensee
reviewed this event
and the scoping of the
SGBD system at
a
Maintenance
Rule Expert panel
meeting.
The panel thoroughly discussed
the issue
and concluded that the event did not constitute
a maintenance
rule preventable
functional failure as presently
scoped.
The panel
determined that the present
scoping
was adequate
and that the plant
corrective action program was adequately
and appropriately tracking
resolution of the
SGBD system water
hammer problems.
The expert panel
meeting
on the issue
was thorough
and exhibited
a proper safety focus.
Additional reviews of this event are contained in Section
E8. 1.
Conduct of Engineering
III. En ineerin
Diesel Generator
Lube Oil Tank
Pa
er
Wi e
Ins ection Sco
e
37551
The inspectors
reviewed Engineering Service
Request
(ESR) 9800061,
Operability Assessment-
Wipe Found in 1B-SB
LO Tank, Revision
0 to
determine if procedure
EGR-NGGC-005,
Engineering Service Request.
Revision 5,
was being followed.
ESR 9800061 evaluated
the operability
of the diesel with the paper wipe in the lube oil tank.
Observations
and Findin s
11
The
ESR evaluated
the probable location of the wipe in the tank and
concluded that it was most likely crimped between
one of the baffle
plate sections
and its mounting point. which probably held it in place
unti 1 the baffle plate was
removed to allow access
to the tank.
The
wipe had
a crimp in it.
In discussing
the
ESR with the licensee.
the
inspector learned that the licensee
had placed
one of these wipes in a
barrel of oil and after several
days it had sunk to the bottom.
If that
had happened
in the tank the pumps would probably have sucked
up the
wipe.: In addition, the conclusion
was based
on the fact that the engine
had been operated
75 hours8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> since the last refueling outage,
which was
the last time the tank was opened
and that the suctions to the three
lube oil pumps should
have picked up
a loose wipe.
The
ESR also
evaluated
what would have happened if the
pumps
had picked up the wipe.
The
ESR concluded that the wipe most likely would have
been shredded
and
captured in the
10 micron duplex strainer
down stream of the pump.
The
shredded
theory was supported
by a statement
from a knowledgeable diesel
engine vendor engineer
who was fami liar with these
pumps
and had seen
a
higher strength cotton rag pass
through similar screw type pumps during
factory testing.
Conclusions
The engineering operability evaluation for a paper wipe found in the
diesel
generator
lube oil suction tank was thorough
and cohcluded that
the wipe would not have affected the diesel.
Containment
Sum
Concerns
Ins ection Sco
e
37551
The inspector
reviewed licensee actions to an investigation of concerns
related to potential
loose parts in the containment
sump that was
identified in CR 98-00295 to determine if the concerns
were properly
addressed.
During initial construction four brackets
and attached
threaded
studs
were weld to the top edge of pipes located in the bottom
of the containment
sump.
The pipes are suction pipes for containment
spray
and residual
heat
removal
pumps.
The brackets
were used during
construction to attach foreign material
exclusion cover over the suction
pipes.
These brackets
were not part of permanent plant design
and were
not being controlled.
The potential existed that
a bracket or part
could come loose
and fall into the pipe,
damaging
one of the pumps.
It
was noted that during the past refueling outage
a part of a bracket
was
found loose.
Observations
and Findin s
The inspector
observed
several
team meetings that were conducted to
determine the short term Justification for Continued Operation.
The
team was composed of several
members
from the Engineering Organization.
In addition,
a regulatory affairs person with root cause
and
human
1.
12
factors training was assigned to assist.
The team's investigation
found
that
a portion of the bracket
had
come loose
and was
removed during the
past refueling outage
(RF07).
The engineer
who removed the bracket
was
on the team.
In addition,
a design control engineer
from a different
organization
was assigned
responsibility to be an independent
assessor
of the information the team gathered.
The independent
assessor
was
assisted
by the regulatory affairs team
member in the
human factors
and
root cause .investigation aspect.
The inspector
found that only one
member of the team had been involved with the containment
sump work in
RF07, the engineer
who removed the portion of the bracket.
The rest of
the team
and the independent
assessor
were.all
independent of the
RF07
containment
sump work.
During RF07, the issue with the brackets
was addressed
as part of the
containment liner and
sump issues.
The liner was discussed
in NRC
Inspection Report'50-400/97-04.
As part of the liner issue the sumps
were regrouted to eliminate leakage of borated water from the
sump to
the gap between the containment
and the liner.
During the regrouting,
one of these brackets
was apparently
found loose
when bumped
by an
individual involved with the work.
Engineering
addressed
the loose
bracket in ESR 9700374,
Sealing of Recirculation
Revision 1, with
a statement
in Section
9, Installation Instruction, that "if feasible,
remove the temporary metal brackets that are welded to the 30" pipe
The inspector
found no other statements
concerning the
brackets
in ESR 9700374 through revision 2.
The team conducted
a short term operability evaluation which was
documented
in ESR 9800042,
Revision 0.
The
ESR was based
on interviews
and reviews of documents.
A containment entry was planned but found not
to be necessary
based
on first hand information from engineers,
quality
control inspectors,
and workers who were in the sump
and involved with
the sump regrouting effort.
The licensee
found pictures which showed
large portions of the bracket.
These pictures
agreed with the
descriptions
obtained
from the interviews.
The combination of the
pictures
and interviews,
combined with documentation'ere
considered
sufficient information by the licensee to perform the
ESR.
The inspector
reviewed the
ESR,
observed
the pictures of the bracket.
and discussed
the team's findings with licensee
personnel.
The team was
thorough
and objectively approached
the identified problems.
The team
found that only the portion of the bracket that was loose
had been
removed.
The team considered
what would happen if a bracket broke off.
This included seismic
and hydraulic flow analysis of the broken off part
to determine whether it would be carried into the
sump in an accident
situation.
The basis for the determination that the part would not be
carried into the
sump was:
~
Seismic
and hydraulic (flow) loads
imposed during design basis
events
are low.
E7
E7.1
E7.2
13
~
The one bracket that
came loose was
removed during RF07.
The
remaining brackets
were strength tested during
RF07 by striking
with a one pound
hammer.
No others
were found to have failed.
~
Grouting activities completed during
RF07 provide more than
adequate
support for the brackets.
The licensee
concluded that the recirculation
and the residual
heat
removal
and containment
spray systems
were operable.
The brackets
are planned to be removed during RF08.
A root cause investigation
was
prepared
and was presented
to the Plant Nuclear Safety Committee
on
February
19, .1998.
The presentation
was observed
by the inspector.
Conclusions
The short term operability determination for containment recirculation
sump brackets
was adequate.
It concluded that foreign material
exclusion
cover brackets installed during construction
could remain in
the
sump and the
sump would still perform its intended function.
The
conclusion
was based
on tack welds having been strength tested
during
the outage
(RF07),
on calculations
which showed that if the brackets
came loose they wouldn't be transferred into the sump,
and that grout
installed during
RF07 would hold the brackets in place.
Quality Assurance in Engineer ing Activities
S ecial
FSAR Review
37551
F
A recent discovery of a licensee
operating their facility in a manner
contrary to the Updated Final Safety Analysis Report
(UFSAR) description
highlighted the need for a special
focused -review that compares
plant
practices.
procedures
and/or parameters
to the
FSAR descriptions.
While
per forming the inspections
discussed
in this report, the .inspectors
reviewed the applicable portions of the
FSAR that related to the areas
inspected.
The inspectors
did not find any additional discrepancies
other than those identified by the licensee.
Trendin
of Cor orate Condition
Re orts
Ins ection Sco
e
40500
The inspector
reviewed
NRC violations for the past several
years to
determine if trends existed.
The inspector also discussed
with the
resident
inspectors
at the Brunswick and Robinson Nuclear Plants
any
trends related to common activities such
as corporate
procedures
or
activities.
The inspector also reviewed trending of deficiencies for
the corporate nuclear procedures
used.
b.
Obser vations
and Findin s
-14
The inspector
observed that corporate
personnel
use the Harris
corrective action program to document
adverse conditions.
The licensee
explained that
a separate
subunit of the Harris, corrective action
program was
used for corporate
generated
condition reports.
Trending of
the corporate condition reports
was conducted
by Harris plant personnel,
separate
from the Harris trending program.
However, trend reports
were
not generated
for the corporate subunit like they were for the Harris
plant generated
condition reports.
The inspector
observed that
a number of the new Nuclear Generation
Group
(NGG) procedures
were identified in NRC inspections
as having errors
and
were the subject of NRC enforcement action.
The errors included:
~
allowing configuration changes
to the plant without providing
=appropriate
design verification,
~
not requiring monitoring of occupational
exposure to radiation by
declared
pregnant
wo~en likely to receive
a dose in excess of ten
percent of the applicable .limit of 500 milli rem,
~
not specify'ing time requirements
for the updating of Environmental
Qualification Data
Packages
to maintain them current for installed
plant equipment.
~
not controlling the computer
software design process to ensure
that design activities did not affect software installed at the
sites,
and
~
allowing clearance
records
not to be designated
as Quality
Assurance
Records.
The specific
NRC Inspection
Reports
where these errors were documented
are 50-325.324/97-02,
50-325.324/96-16
50-325,324/97-12
and 50-325,324/
97-13 for the Brunswick facility, and 50-400/97-04
and 50-400/97-12 for
the Harris facility.
- The specific procedures
involved include
Procedures
EGR-NGGC-0005.
DOS-NGGC-0002.
EGR-NGGC-0156,
EGR-NGGC-0007,
CSP-NGGC-2501,
2502,
and 2503.
and OPS-NGGC-1301.
The errors identified above suggest
a trend in corporate procedural
inadequacy
which is of concern for two reasons:
~
Corrective actions
implemented to address
specific procedural
inadequacies
may not adequately
address
program-level* reasons
why
the procedures
are not adequate.
If program-level
reasons
contributed to the inadequacies.
and if corrective actions
do not
address
those
reasons,
then this trend in procedural
inadequacy
could continue.
E8
E8.1
15
~
Licensee staff did not identify and recognize this trend before
the inspectors
did.
This Suggests
that no program currently in
place effectively trends
and corrects
corporate-wide
problems.
In discussing
these
issues with Harris plant corrective action program
personnel,
the inspector
became
aware that corporate
procedure or
process
inadequacies
could be identified at the Brunswick and Robinson
Nuclear plant sites but not be entered into the corporate corrective
action program subunit at Harris.
As
a result,
common problems with
corporate activities would not be trended in the
same data
base.
diluting a potential trend such that it would not be identified.
The
'nspector
also learned that the Harris corrective action program
trending guidance
and requi rements
were limited to approximately three
lines in procedure
AP-615, Condition Reporting.
The guidance is
basically to do quarterly trending.
The licensee
had already identified
this weakness
and was determining
a course of action to address this
issue:
Conclusions
A trend in corporate
procedure
inadequacies
was identified.
Trending of
corporate related
adverse condition reports
were being diluted because
the condition reports
were spread
through all three sites corrective
action data
bases.
The licensee
had identified that trending program
guidance in general
was weak and was determining
a course of action to
address this issue.
Miscellaneous
Engineering
Issues
(92903)
0 en
Unresolved
Item 50-400/97-13-01:
"C" Steam Generator
Blowdown
System
Water
Hammer.
This Unresolved
Item (URI) was opened in NRC Inspection Report 50-400/
97-13 to review the root cause evaluation of the steam generator
blowdown
(SGBD) event of December
22,
1997,
and to review the repetitive
nature of water
hammer events
on the
SGBD System,
including their
continued occurrences.
,The inspectors
reviewed the history of SGBD water
hammer events
as
documented
by the licensee's
corrective action system.
A total of five
CRs were identified which documented
water
hammer events
on the
lines from December
21,
1996, to present.
The first documented
event
occurred in April, 1987, which was documented
in LER 87-029-01.
A 1996 Nuclear Assessment
Section
(NAS) audit identified that no formal
process
existed to document evaluations
following water
hammer events
including meeting post water
hammer snubber
requirements.
Procedure
PLP-631,
Water
Hammer Assessment
Program,
was implemented in March 1997,
and established
the current water
hammer
documentation
and evaluation
process.
16
Review of water
hammer data indicated that prior to PLP-631
~
documentation of water
hammer events
was weak and inconsistent.
Following implementation of PLP-631, the sensitivity to water
hammers
has increased
and the licensee
was documenting water
hammers
using the
condition report
(CR) and maintenance
rule processes
and evaluating the
eff'ects of water
hammers
using the
ESR process.
Data indicated that the
process is being followed.
Several
changes
were
made to the
SGBD line valves
and operating
procedures
were changed
but the problems were not resolved.
CR 975320
was
a level
1 CR, which requires
a root cause investigation
(RCI). and was assigned to Engineering.
The
CR concluded that the root
cause
was inadequate original designs
that improper communications of
the issue
between Operations
and Engineering,
and inadequate
post
modification testing following SGBD system modifications were
contributing causes.
The CR/RCI presented
procedural
enhancements
identified by the system engineer
as short term water
hammer solutions
with long term resolution via hardware modifications to the system to
provide slow fill and warmup capability.
The inspectors
concluded that
the CR/RCI did not look at all
SGBD design
documents
and did not
thoroughly review the implementation of previous
SGBD modifications
intended to prevent water
hammers during system initiation.
The inspectors
reviewed
a description of the metallurgical analysis
performed
on the failed section of SGBD piping.
The evalu'ation
was
performed
by the Metallurgy Labs at the Harris Energy and Environmental
Center.
The conclusion
was that the pipe section failed due to an
overload fai lure of the pipe consistent with a significant water
hammer
loading and did not indicate
a fatigue problem or
a problem due to
cumulative effects.
The inspectors
attended
the
PNSC meeting conducted
February
11,
1998,
which reviewed
CR 975320 Root Cause Investigation
(RCI).
The
PNSC
performed
a thorough discussion of the
RCI and requested
an additional
root cause to be added for organizational
acceptance
of water
hammers
and raised several
other questions for the incident investigation
team
to address.
The
PNSC rejected the CR/Root Cause Investigation
and
requested
that it be revised.
The inspector concluded that management,
including the
PNSC,
was appropriately
focussed
on determining the root
cause of the event
and ensuring corrective. actions provide
a permanent
solution.
The inspectors
concluded that the
SGBD water
hammers
during
initiation was
a long standing
problem which the licensee's
corrective
action program
had not corrected.
The Root Cause Investigation
concluded that original design
was the root cause
and hardware
modification corrective
action is planned.
The Root Cause Investigation
was reviewed by the
PNSC and will be revised.
'
17
The inspector discussed
trending with the licensee,
particularly in
relation to the steam generator
blowdown water
hammer event,
and in
general.
The licensee
had already identified trending
as
an area that
needed
improvement.
A new Correction Action Program manager
had been
assigned
in the last four months with guidance to review the trending-
area.
The inspector
observed that trending was being conducted in
relation to maintenance
rule, maintenance
work orders,
and condition
reports.
The inspector
concluded that trending continues to be an area of
weakness.
However,
improvement
was being
made.
The inspector
considered
the lack of trending program procedural
guidance
a
.
significant contributor to the weakness.
The integrated site-wide
trending approach
was not adequately
defined to ensure consistent
implementation.
The URI will remain open pending review of the revised
CR/Root Cause Investigation.
Conclusions
Management,
including the Plant Nuclear Safety Committee,
was
appropriately
focussed
on determining the root cause of the event
and
ensuring corrective actions provide
a permanent solution.
Condition
report trending
had not revealed
a trend related to the blowdown events,
which had resulted in a lack of management
attention prior to the event.
IV. Plant
Su
ort
Rl Radiological Protection
and Chemistry
(RP&C) Controls
Rl.l
General
Comments
Ins ection Sco
e
71750
The inspector
observed radiological controls during the conduct of tours
and observation of maintenance, activities.
Observations
and Findin s
The inspector
found radiological controls to be acceptable.
The
general
approach to the control of contamination
and dose for the site
was good.
Teamwork between the various departments
continued to be
a
major contributor to the good control of dose.
Conclusions
The control of contamination
and dose for the site was good'and
'was
attributable to good teamwork between the various departments.
S1
Sl.l
Fl
F1.1
18
Conduct of Security and Safeguards Activities
General
Comments
Ins ection Sco
e
71750
The inspector
observed security
and safeguards
activities during the
conduct of tours
and observation of maintenance activities.
Observations
and Findin s
The inspector
found the performance of these activities was good.
Compensatory
measures
were posted
when necessary
and properly conducted.
The inspector
noted from review of condition reports
and from discussion
with operations
and security staff that
a gun was discovered during
passage
of an individual's articles through the access
area
X-ray
machine
on January
22,
1998, at 6: 14 a.m.
The individual was
appropriately isolated
from the weapon
by the security staff.
The
security staff interviewed the individual and determined that the
.
individual had accidentally left the gun in their belongings.
The
security staff determined that no malevolence
occurred.
A site-wide
news bulletin was put out that
same
day to review the actions taken
and
remind the plant staff of the prohibition on weapons in the protected
area.
The inspector
observed
work conducted
on the protected
are'a security
fence to add razor wire under contract
XXA7000484.
This wire was being
appropriately installed.
The addition of the wire was in excess of the
requirements
of the security plan.
The licensee
made
a 50.72 report in relation to granting access
to an
individual that should not have
been granted
access.
This issue will be
reviewed in detail after the licensee
submits
a safeguards
event report.
Conclusions
The performance of Security and Safeguards activities were good.
Security staff responded
appropriately to the discovery of a gun during
processing of employee belongings in the access
area
X-ray machine.
Control of Fire Protection Activities
Desi
n Basis of Fire Barrier Penetration
Seals
Ins ection Sco
e
64704
The inspectors
reviewed the fire bar rier penetration
seal
designs
and
testing for compliance with the facility's licensing requirements
identified in FSAR, sections
9.5. 1.2, Barriers
and Access;
9.5. 1.5.4,
Quality Assurance
Program:
17.3,
HNP Quality Assurance
Program
Description;
arid Carolina
Power,and Light's
(CPSL) Corporate Quality
'19
Assurance
Manual, section 15.0. Quality Assurance
Program for Fire
Protection
Systems.
The inspectors
compared selected as-built fire barrier penetration
seals
to fire endurance test configurations to verify that those seals
were
ualified by appropriate fire endurance
tests
and representative
of the
esign
and construction of the fire endurance test specimens.
During
plant walkdowns the inspectors
observed the installation configurations
of selected
accessible fire barrier penetration
seals to confi rm that
the licensee
had established
an acceptable
design basis for those fire
barriers
used to separate
safe
shutdown functions.
b.
Observations
and Findin s
Fire barriers include penetration
seals,
wraps, walls, structural
member
fire resistant
doors,
and dampers,
etc.
are
used to prevent the spread of fire and to protect redundant
safe
shutdown equipment.
Laboratory testing of fire barrier materials is
done only on
a limited range of test assemblies.
In-plant installations
can vary from the tested configurations.
Under the provisions of
Implementation
of, Fire Protection
Requirements,
licensees
are permitted to develop engineering
evaluations
justifying such deviations.
The inspectors
reviewed the fire barrier penetration
seal
design
records,
Harris construction control system
(CCS) computer database
design records. quality assurance
and quality control
(QA/QC)
installation records,
seal typical detail drawings
and
testing records.
The review included nine mechanical
and electrical
seals.
In the review of penetration
seals,
the inspectors
used
FSAR sections
9.5. 1.2. Barriers
and Access,
9.5. 1.5.4. Quality Assurance
Program
and
17.3,
HNP Quality Assurance
Program Description;
CP&L Corporate Quality
Assurance
Plan, section 15.0, Quality Assurance
Program for Fire
Protection
Systems,
Revision 18; Harris Civil Modification Procedure
No.
CMP-010, Installation of Penetration
Seals,
Revision 8; Harris.
Nuclear Safety Evaluations
Nos.
1288 and 1413,
concerning
NRC
Information Notice (IN) 88-04,
dated
March 17,
1988; Harris'uclear
Safety Evaluation
No.
1406 concerning
NRC IN 88-56,
dated October 25,
1988; Harris Nuclear Safety Evaluation
No.
1209 concerning
NRC
Information, Notice (.IN) 94-28,
dated April 15,
1994; selected
seal typical vendor
(Promatec) detail drawings
1364-93035
through 1364-93072;
selected
composite penetration
location drawings
2167-S-002 through 2167-S-208:
and recognized industry fire penetration
seal testing guidance of American Society for Testing
and Material
(ASTM) Standard
E814-1988,
Standard
Test Method for Fire Tests of
Through-Penetration
Fire Stops
and Institute of'lectrical
and
Electronics
Engineers
(IEEE) Standard
634-1978,
IEEE Standard
Cable
Fire Stop Qualification Test.
l
20
Using the
FSAR Fire Hazards Analysis
(FHA) Figures
9.5A-1 through
9.5A-41 to determine the location and description of the plant fire
areas'he
inspectors
conducted
walkdowns
and inspected
seal
installations.
The inspectors'eview
focused
on verifying that the
following design
and installation parameters
for the as-built
configurations
were adequately
bounded
by tests
or justified by
licensee's
engineering
evaluations:
~
type and opening size;
~
seal material type and depth;
~
damming material type and orientation;
~
types
and thermal
mass of penetrating
items;
~
clearances
of penetrating
items;
and
~
fire test results for unexposed
surface temperatures
The following penetration
seals
were visually inspected
and the
QA/QC
engineering
and construction penetration
closure verification package
records for these
seals
were reviewed to determine whether the as-built
plant seal configurations
were representative
of those utilized in fire
seal qualification tests:
v
21
PENETRATION SEAL SUMMARY
SEAL
MATERIAL
DAMMING
MATERIAL
IDENTIFICATION/
NUMBER
LOCATION / SIZE
(INCHES)
DESIGN
DETAIL
DEPTH / TYPE
TYPE / ORIENTATION
FIRE TEST REPORTS /
QUALIFICATION
ELECTRICAL CABLE
TRAY
E 156
ELECTRICAL CABLE
TRAY
E 103
ELECTRICAL CABLE
TRAY
E 2797
ELECTRICAL
CONDUIT
INTERNAL
E 520K
MECHANICALPIPE
P 3624
MECHANICAL
SEISMIC GAP
P 4393
REACTOR AUXILIARY
BUILDING / WALL
BETWEEN FIRE
ZONES 1.A.EPA AND
1.A BALi/78X28
REACTOR AUXILIARY
BUILDING / FLOOR
BETWEEN FIRE
ZONES 1.A.EPA AND
1.A.3.MP / 26 X28
REACTOR AUXILIARY
BUILDING / WALL
BETWEEN FIRE
ZONES 1.A.SWGRA
AND 1.A-SWGRB /
28 X42
REACTOR AUXILIARY
BUILDING /FLOOR
BETWEEN FIRE
ZONES 12.A.CR AND
1.A CSR A /4
DIESEL GENERATOR
BUILDING/WALL
BETWEEN FIRE
ZONES 1.D.DTB AND
1 D.1-DG8.RM / 6
REACTOR AUXILIARY
BUILDING / WALL
BETWEEN FIRE
ZONES 1.A.EPA AND
1-A.46.ST / 2X312
EL-1
EL-1
EC-1
MS 5
GS-1
4"- LOW DENSITY
SILICONE
ELASTOMER
10 - SILICONE
FOAM
4"- LOW DENSITY
SILICONE
ELASTOMER
4"- LOW DENSITY
SILICONE
ELASTOMER
6"- SILICONE
FOAM
6"- SILICONE
FOAM
KAOWOOL
BOARD-
1 -TWO SIDES
KAOWOOL
BOARD-
1"- BOTTOM SIDE
KAOWOOL
BOARD-
1 -TWO SIDES
KAOWOOL
CERAMIC FIBER-
1"-TWO SIDES
KAOWOOL
BOARD ~
1 -TWO SIDES
KAOWOOL
CERAMIC FIBER-
1"-TWO SIDES
1063.1
3 HOURS
1001A.
3 HOURS
1063.1 ~
3 HOURS
1063.1 ~
3 HOURS
CTP 1001A.
3 HOURS
1001A-
3
HOURS'ECHANICAL
PIPE
P 3683
MECHANICAL
COPPER TUBE
P 447A
MECHANICALPIPE
WITH TWO PIPE
PENETRANTS
P 3308
DIESEL GENERATOR
BUILDING/WALL
BETWEEN FIRE
ZONES
1 D DTA AND
1-D.1.DGA-RM / 6
REACTOR AUXILIARY
BUILDING /FLOOR
BETWEEN FIRE
ZONES 1 A-BALAND
1.A.3PB /6
REACTOR AUXILIARY
BUILDING / WALL
BETWEEN FIRE
ZONES
1 A.EPA AND
1-A.46.ST / 18X38
MS.S
ML-2
MR.5
6 - SILICONE
FOAM
4"- LOW DENSITY
SILICONE
ELASTOMER
48'- PROMATEC
RADFLEX
KAOWOOL
BOARD-
1"-TWO SIDES
KAOWOOL
BOARD-
1"- BOTTOM SIDE
KAOWOOL
BOARD-
'I" .TWO SIDES
CTP 1001A.
3 HOURS
1063.1
1024.
3 HOURS
1002
CTP 1063.9.
3 HOURS
The inspectors
noted that the licensee's
evaluations of Information
Notices 88-04,
88-56,
and 94-28 did not identify any fire barrier
seal
problems at Harris.
The inspectors'isual
inspections
did not identify any missing seals
and verified that the installed fire
barrier penetration
seals
were continuous with no gaps
~ cracks,
or holes
in the barrier material that would indicate the seals
were inoperable.
22
The inspectors
reviewed the fire barrier penetration
design
documentation for mechanical
penetration fire seals
P 3308 and
P 447A.
Fire barrier seal
P 3308 consisted of an 18-inch by 38-inch block out,
with two non-sleeved
14-inch pipe penetrants
in a concrete wall.
The
entire depth of the block out was filled with Promatec
Radflex silicone
material.
Design drawing 1363-93047,
Flexible Mechanical
Seals-Radflex,
Revision
1
~
and qualifying fire test reports
CTP 1002 and 1063.9 for
this type of,seal
indicated that fire tests
had been conducted only on
single sleeved
pipe penetrations
and not on block out penetration
designs.
Fire barrier seal
P 447A included
a 6-inch diameter sleeve
with a single two and one-half inch copper tube penetrant
in a concrete
floor.
Qualifying fire test report CTP,1001A for this seal
type
indicated that fire tests
had been conducted only on steel
pipe
penetrants.
No copper tube penetrant
had
b'een tested.
Based
on these
reviews, the inspectors
concluded that the licensee
failed to have adequate test documentation to demonstrate
that the as-
built penetration
seal configurations of fire seals
P 3308 and
P 447A
had been qualified by fire tests.
The penetration
seal configurations
, were significantly different from the tested typical seal
types
and
configurations
and were not bounded
by the vendor's
design
and test
documentation.
Also the licensee
had not conducted
engineering
evaluations that followed the guidance of GL 86-10 to justify the
adequacy of these penetration
seal configuration deviations
from the
fire barrier configurations qualified by tests.
The inspectors
also conducted
a review of the fire barrier penetration
design documentation for electrical fire barrier'penetration
seal
E 156.
This penetration
seal
consisted of a 78-inch by 28-inch block out (2184
square
inch seal
area) with six vertical stacked
cable tray and conduit
penetrants
in a concrete wall.
Qualifying fire test report
CTP 1063. 1
for this seal
type indicated that successful fire tests
had been
conducted
on
a maximum block out size of 42-inch by 46-inch which
designated
1932 square
inches
as the maximum seal
area limit.
The
licensee's
field engineering
and construction penetration
closure
verification package for electrical penetration fire seal
E 156, dated
December
15.
1986,
noted
a
QA/QC hold point verification inspection of a
subdivision of the seal.
Penetration installation procedure
CMP-010,
step 7.0. 12, indicated that Engineering shall specify size
and location
of subdividing partitions
and material to be used
on large floor/ceiling
requi ring subdividing as specified
on typical detail
drawings.
The licensee's
seal typical detai
1 drawing 1364-
93035.
sheet
3
~ Revision 0. General
Note No. 4 indi'cated that
a
~
~
enetration
seal
be subdivided
by partitions if the maximum seal
area
imit is exceeded.
The note also required that the penetration
engineers
prepare
sketches/drawings
of the subdividing design
and the
materials
(including structural
support elements)
installed
and that
this subdividing design documentation
become
a permanent part of the
engineering
documentation
package of the seal.
However,
no
sketches/drawings
of the subdividing design
and the materials installed
were identified in the engineering
documentation
package of penetration
fire seal
E 156 provided to the inspectors.
At the request of the
23
inspectors,
the licensee also examined the field design
and construction
documentation for two additional
large floor/ceiling
electrical penetration fire seals
requiring subdividing.
The licensee
was unable to locate the penetration
seal
subdividing design
documentation that demonstrated
the as-built configurations
were bounded
by the vendor's
design
and test documentation.
Also, the licensee
provided no engineering
evaluation documentation that evaluated
the
adequacy of these subdivided penetration
seal configurations.
This does
not follow the guidance of GL 86-10.
The inspectors
concluded that the
licensee
had not implemented
and maintained the design engineering
documentation for large subdivided electrical floor /cei ling penetration
fire seal configurations that demonstrated
the as-built configurations
were bounded
by the vendor's
design'and test documentation.
FSAR sections
9.5. 1.2 and 9.5. 1.5.4 indicated that penetration
seal
designs
are qualified by tests
and that the Fire Protection Quali'ty
Assurance
Program elements
are included in FSAR section 17.3.
section 17.3.2,
Performance/Verification
indicates,
in part, that design
and as-
documents
and procedures
are controlled to reflect design
mod f'
-built conditions.
and, that sufficient records
are maintained to
provide documentary
evidence of the quality of items and the
accomplishment of activities affecting quality.
CP8L Corporate Quality
Assurance
Plan.
Revision
18, Section 15.0, Quality Assurance
Program for
Fire Protection
Systems
implements the
FSAR fire protection quality
assur ance requirements
and indicates in paragraph
15.4, that design
activities shall
be accomplished
in accordance
with procedures
that
assure
the applicable design requi rements
are included.
Harris
TS 6.8. l.h indicates that written procedures
shall
be established.
implemented,
and maintained covering the fire protection program
implementation.
Based
on these
reviews, the inspectors
determined that the licensee
failed to adequately
implement
and maintain the applicable design
control documentation
requirements
of the fire protection program
as
described
in the
FSAR to demonstrate
that the as-built configurations of
seals
P 3008.
P 447A,
and
E 156 were bounded
by
the vendor's
design
and test documentation.
This is
a violation of the
facilities'perating license condition 2.C.F.
and is identified as
Violation 50-400/98-01-04,
Failure to Properly
Implement
and Maintain
the Applicable Fire Protection
Program Design Control Documentation
Requirements
Seals.
In addition, the
licensee did not perform engineering evaluations that followed the
guidance of NRC GL 86-10 for devi ati ons from fire barrier configurations
qualif'ied by tests.
This was considered
an engineering
program
weakness.
c.
Conclusions
A violation was identified for failure to adequately
implement
and
maintain in effect the applicable provisions of the fire protection
program for fire barrier penetration
seals
P 3008,
P 447A,
and
E 156.
In addition. the licensee did not perform engineering evaluations that
P
F2,
F2.1
24
satisf'ied the guidance of NRC GL 86-10 for deviations
from fire barrier
configurations qualif'ied by tests.
This was considered
an engineering
program weakness.
Status of Fire Protection Facilities and Equipment
Surveillance of Fire Protection
Features
and
E ui ment
Ins ection Sco
e
64704
The inspectors
reviewed procedure
FPT-3550,
Seal
Inspection
18 Months Interval," Revision
10,
and the inspection data for
the surveillance
procedures
which were completed
December
2,
1992,
March 15,
1994,
and June 3,
1995.
These were reviewed for compliance
with the requi rements of FSAR Section 9.5. 1.
Observations
and Findin s
Surveillance
procedure
FPT-3550 required
a visual inspection
each
18
months of a random sample of 10 percent of'ach type of fire barrier
enetration seal.
The sample inspections
were requi red to include fire
arrier seals that had not been inspected within the past
15 years.
Each seal
was inspected for any apparent
change in appearance
and signs
of abnormal
degradation.
If any abnormality was found,
an additional
10
percent
was requi red to be inspected.
The inspection
and selection
process
was to continue until an acceptable
sample
was found.
The inspectors
reviewed Procedure
FPT-3550
and concluded that the
procedure
met the frequency requirements
of Procedure
Fire
Protection Surveillance
Requirements,
Revision 8, Section 5.5. 1.c and
met the commitments
made to the
NRC.
The penetration
seal surveillance inspections
completed
December
2.
1992.
Harch 15,
1994,
and June 3.
1995 were reviewed by the inspectors.
No discrepancies
were noted.
The surveillance inspection
due
January
1998 had not been completed
and was in process
during this
inspection.
The completion of this inspection
was in the grace period.
As previously documented
in NRC Inspection
Report 50-400/97-04,
the
number of fire protection survei llances
being performed in their grace
period was approximately
60 percent for long term (quarterly to 18-
month) survei llances.
This was considered
an excessive
number
and
resulted in the program being considered
not fully effective.
Action
had been taken by the licensee to correct this issue.
As of
December
1997,
47 per cent of the surveillance
procedures
were performed
in the grace period, with 45 percent of these
being performed within
seven
days of the scheduled
date.
Twenty percent of the survei llances
were performed early.
By January
1998 this number
had been further
reduced
such that
41 percent of the survei llances
were performed in the
grace period. with 92 percent of these survei llances
performed within
seven
days of the scheduled
date.
Twenty-eight percent of the
survei llances
were performed early.
Continued
improvements in this area
f
F5
F5.1
25
were anticipated
by the li'censee.
The
NRC will continue to monitor the
licensee's
performance in this area.
Conclusion
The surveillance inspection
procedure for the fire barrier penetration
seals
was adequate.
The three most recent inspections
had been
satisfactorily
implemented.
However,
a large number of fire protection
surveillance
procedures
continued to be implemented within the grace
period of the procedure.
Action had been
implemented
by the licensee to
address this issue
and corrective action was anticipated.
Fire Protection Staff Training and Qualification
Fire Bri ade
Ins ection
Sco
e
64704
The inspectors
reviewed
a fire brigade drill for compliance with the
licensee's
site procedures
and the requirements
of FSAR Section 9.5. 1.
Observations
and Findin s
The inspectors
witnessed
a fire brigade drill conducted
on February 3,
1998, at 9:00 P.N.
This drill involved
a simulated fire on the 1A-SA
steam driven auxiliary feedwater
pump located
on elevation'36 of the
auxiliary building.
The response
by the fire brigade to the simulated
fire included
a fire brigade
leader
and two fire brigade
members
from
operations,
one fire brigade
member from maintenance
and one fire
brigade
member from health physics.
Three security officers, three
auxiliary unit operators
and one health physics
employee also responded
to provide additional assistance
to the brigade,
as required.
The fire
brigade
members
responded to the simulated fire in full turnout gear
and
each
one was equipped with self contained breathing apparatus.
The
response
was timely and the brigade demonstrated
the proper use of fire
fighting equipment
and tactics.
The brigade leader's
direction and
performance
was good.
Following the drill, a critique was conducted to
discuss the brigade's
performance
and recommendations
for future
enhancements.
Conclusions
The fire brigade demonstrated
good response
and fire fighting
performance
during
a simulated fire brigade drill conducted during this
inspection period.
V
F5.2
'26
Seal Installers
and
C Ins ectors
Ins ection Sco
e
64704
The inspectors
reviewed training records for the maintenance
employee
designated
to install
and repair fire barrier penetration
seals
and the
QC inspectors
designated
to inspect the penetration
seals for compliance
with the requirements
of FSAR Section 9.5. 1.
Observations
and Findin s
Only one site employee
was qualified to install
and repai r the
facility's fire barrier penetration
seals.
This employee
had received
,
initial classroom training and practical application in the installation
of the types of fire barrier penetration
seals
used at the Harris
facility.
This training was conducted
by the vendor who supplied the
seal material for the various fire barrier penetration
seals installed
at the facility.
This employee
had received appropriate
annual
retraining
and recertification to maintain
up to date knowledge
and
performance in the installation of these seals.
The inspectors
witnessed the repai rs to a degraded
penetr ation seal
performed by this
individual.
The employee demonstrated
an excellent
knowledge of fire
barrier penetration
seal installation requi rements
and the repai r work
was of a high quality.
seal installation procedures
'contained
hold
points f'r QC inspections of the principle installation features.
Five
QC inspectors
were performing
QC inspections
and verifications of fire
barrier penetration
seal installations.
The inspectors
reviewed the
training records of two of these
employees
and verified that the
training and certification records for these
employees
were current for
the installation of fire bar rier penetration
seals.
In addition. the
inspectors
witnessed
the performance of a
QC inspector during the
oversight
and verification of repai rs to
seal.
The
QC inspectors
demonstrated
appropriate oversight
and
verification activities for these repairs.
Conclusion
seal installer was appropriately trained to
accomplish fire barrier penetration
seal installation work and
inspectors
were qualified to perform the appropriate verification for
installation
and repairs
made to the fire barrier penetration
seals.
, ~ a.')
F7
F7.1
27
guality Assurance in Fire Protection Activities
Fire Protection Audit Re orts
a.
Ins ection
Sco
e
64704
The inspectors
reviewed the Nuclear Assessment
Section
(NAS) Audit
Report
HNAS98-011, Harris Fire Protection Assessment,
dated January
29,
1998, for compliance with the licensee's
site procedures
and commitments
made to the
NRC.
Observations
and Findin s
The licensee's
Nuclear Assessment
Section performed
an assessment
of the
fire protection program on January
5-16,
1998.
The report for this
assessment
was report
No.
HNAS98-011.
The assessment
team determined
that the fire protection program was effective in support of the
operation of the facility.
Findings from the assessment
were
categorized
as strengths.
issues,
or weaknesses.
The assessment
report
identified two strengths,
no issues
and five weaknesses.
The assessment
report also identified eight previously identified 1995-1997 audit
issues
and weaknesses
that remained
open.
The licensee's
corrective
actions for these outstanding audit items were being implemented
and
completion was anticipated in 1998.
Conclusions
The licensee's
1998 Nuclear
Assessment
Section
assessment
of the
facility's fire protection program was of good quality and effective in
identifying fire protection program performance to management.
Corrective actions in response to identified assessment
issues
were
being implemented
and completion
was anticipated in 1998.
XI
Exit Meeting Summary
V.
Mana ement Meetin s
The inspectors
presented
the inspection results to members of licensee
management
at the conclusion of the inspection
on March 4,
1998.
The
licensee
acknowledged the findings presented.
The inspectors
asked the licensee
whether
any of the material
examined
during the inspection should
be considered proprietary.
No proprietary
information was identified.
r
28
Licensee
PARTIAL LIST OF
PERSONS
CONTACTED
D. Batton. Superintendent,
On-Line Scheduling
D. Braund; Superintendent,
Security
B. Clarke
General
Manager,
Harris Plant
A. Cockerill, Superintendent,
I&C Electrical
Systems
J. Collins, Manager,
Maintenance
J.
Cook,
Manager,
Outage
and Scheduling
J.
Donahue,
Director Site Operations,
Harris Plant
J.
Eads
~ Supervisor,
Licensing and Regulatory
Programs
R. German,
Manager,
Plant Support
W. Gurganious,
Superintendent,
Environmental
and Chemistry
M. Keef. Manager,
Training
B. Meyer; Manager,
Operations
K. Neuschaefer,
Superintendent,
Radiation Protection
W. Peavyhouse,
Superintendent.
Design Control
W. Robinson,
Vice President,
Harris Plant
S. Sewell, Superintendent,
Mechanical
Systems
D. Tibbitts, Manager.
Nuclear
Assessment
C. VanDenburgh,
Manager,
Regulatory Affairs
NRC
S. Flanders.
Harris Project
Manager
~
M. Shymlock, Chief, Reactor Projects
Branch 4
29
IP 40500
IP 62707
IP 71707
IP 92901
IP 92903
INSPECTION
PROCEDURES
USED
Onsite Engineering
Effectiveness of Licensee Controls in Identifying, Resolving,
and
Preventing
Problems
Surveillance
Observations
Maintenance
Observation
Fire Protection
Program
Plant Operations
Plant Support Activities
Followup - Plant Operations
Followup - Maintenance
Followup - Engineering
~0ened
50-400/98-01-01
ITEMS OPENED,
CLOSED,
AND DISCUSSED
Failure to follow procedures:
1) properly check main
control
room chart recorders,
and;
2) inadequate
work
instructions for rod control system
(Section 08. 1 and
Section M1.2).
50-400/98-01-02
NCY
Inadequate
foreign material exclusion controls for
diesel
generator
lube oil tank (Section Ml.l).
50-400/98-01-03
Failure to conduct shutdown margin surveillance within
one hour (Section M7.1).
50-400/98-01-04
Failure to properly implement
and maintain the
applicable fire protection program. design control
documentation
requirements for fire barrier
seals
(Section Fl. 1).
Closed
50-400/98-01-02
Discussed
Failure to conduct shutdown margin surveillance within
one hour (Section M7.1).
50-400/97-09-02
50-400/97-13-01
Failure to properly check main control
room chart
recorder
(Section 08.1).
"C" steam generator
blowdown system water
hammer
(Sections
08.2,
M8. 1,
and
E8. 1).
~
~
g
~
4
ti