ML18012A806

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Insp Rept 50-400/97-04 on 970330-0510.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML18012A806
Person / Time
Site: Harris 
Issue date: 06/09/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A804 List:
References
50-400-97-04, 50-400-97-4, NUDOCS 9706180250
Download: ML18012A806 (90)


See also: IR 05000400/1997004

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

License

No:

50-400

NPF-63

Report

No:

50-400/97-04

Licensee:

Carolina

Power

IE Light (CPImL)

Facility:

Shearon Harris Nuclear

Power Plant, Unit 1

Location:

5413 Shearon

Har ris Road

New Hill, NC 27562

Dates:

March 30

- May 10,

1997

Inspectors:

Approved by:

J. Brady, Senior Resident

Inspector

D. Roberts,

Resident

Inspector

J. Coley, Reactor

Inspector

(Sections

H2.5, H2.6,

and

H2.7)

P. Fillion, Reactor

Inspector

(Sections El, E2,

and

E7)

J.

Lenahan,

Reactor Inspector

(Sections

E1.

E2.

E7,

and

E8)

G. HacDonald,'Project

Engineer

(Section H1.3)

W. Rankin, Senior Project

Manager

(Section Rl)

H. Whitener,

Reactor

Inspector

(Sections Hl.2 and

H2.2)

G. Wiseman,

Reactor

Inspector

(Sections

Fl through

F8)

R. Hall, General

Engineer

(Intern)

H. Shymlock, Chief, Projects

Branch 4

Division of Reactor Projects

Enclosure

2

9'706180250

970609

'DR-

ADQCK 05000400

O.-

PDR

EXECUTIVE SUMMARY

Shearon Harris Nuclear

Power Plant,'Unit

1

NRC Inspection Report 50-400/97-04

This integrated

inspection included aspects

of licensee operations,

engineering,

maintenance,

and plant support.

The report covers a'ix-week

period of resident inspection;

in addition, it includes the results of

announced

inspections

by six regional specialists

and

a regional project

engineer.

0 erations

~

Movement of fuel assemblies

during refueling was conducted in an

acceptable

manner.

The licensee

made conservative

decisions

when

problems

arose while moving fuel assemblies,

and the use of specialized

equipment

was beneficial

(Section 01.2).

~

A violation was cited f'r failing to comply with Technical Specification 3.0.4.

Although the violation was licensee-identified,

the licensee's

initial corrective actions

were inadequate

(Section 01.3).

~

Equipment operability, material condition,

and housekeeping

were

acceptable

in all cases

observed

by the inspectors.

No substantive

concerns

were identified during plant walkdowns (Section 02.1).

~

A violation with three

examples of failure to properly implement

corrective actions

was identified.

Two of the examples

involved boron

dilution events

(Sections

04. 1 and 04.2).

Each dilution event

represented

failures of control

room supervision to adequately

supervise

board operators

and properly communicate expectations.

Additionally,

each event pointed out weaknesses

in the management

of reactivity

manipulations.

The third example involved ineffective corrective action

for LER 96-013-01

as evidenced

by recurrence of a Technical Specification 3.0.3 entry during chemical addition to the component

cooling water

system

(Section 08.1).

Maintenance

Maintenance

personnel

were knowledgeable of their assigned

tasks,

approved

procedures

were at the job and followed, work areas

were

controlled and instruments

were calibrated

(Section Hl.l).

Transportation of the Reactor Coolant

Pump motor into containment

was

well executed.

Load paths

were evaluated

and contingencies

for

potential

damage to the Refueling Water Storage

Tank were taken (Section

H1.2) .

Inspection of Emergency Diesel Generator

(EDG) overhaul

met the

requirements of plant procedures,

the vendor manual,

and the vendor

service information memorandum

regarding

10-year

surveillance

and

mai.ntenance activities.

The

EDG work activities were conducted in a

professional

manner

by knowledgeable

personnel.

The engine/component

inspections

performed were thorough

and identified problems

were

conservatively resolved.

Some discrepancies

were noted regarding

documentation of NDE inspections

on, EDG cylinder liners.

(Section Hl.3)

Licensee activities involving the detection

and recovery of foreign

objects in the "A" Steam Generator

were conducted in an acceptable

manner

.

The licensee

performed

an adequate

analysis of the cause of the

foreign objects,

and

a review of the potential for foreign objects

entering the other

steam generators

(Section Hl.4).

Surveillance procedure

problems were observed in several tests during

the refueling outage including the remote

shutdown

system test

and the

high head safety injection pump test (Sections

H2.1, H2.2,

and H2.3).

A non-cited violation was identified for failing to establish

and

implement adequate

procedures

for using test equipment

on the

"A"

emergency battery.

The use of an improper jumper cable resulted in a

small battery fire (Section H2.4).

Ultrasonic examinations

and interpretation/evaluation/acceptance

of the

reactor

vessel

ISI test results

were conducted in a proficient manner

by

experienced

and knowledgeable

examiners

(Section H2.5).

Steam generator

eddy current activities were well managed.

Program

and

examination procedures

were very good, knowledgeable/skillful

vendor

personnel

were utilized,

and state-of-the-art

examination

equipment

was

used

(Section H2.6).

The licensee's

disposition of the containment liner thickness

issue

was

resolved in a sound technical

manner.

Licensee ultrasonic

examination

personnel

performing the containment liner thickness

measurements

were

resourceful, skillful and very knowledgeable of the ultrasonic method

(Section H2.7).

An apparent violation was identified for an inadequate

10

CFR

50.59'afety

evaluation which ultimately led to the removal of containment

equipment

hatch missile shield protection while it was required to

remain installed

dur ing Hode 3 operations

(Section H3.1).

En ineerin

The licensee's

current design

change control procedures

complied with

the requirements of 10

CFR 50.59,

and

10 CFR 50, Appendix B,

Criterion III (Section El.l).

I

A non-cited violation was identified for failure to implement the

design verification requirements of 10 CFR 50, Appendix B,

Criterion III for safety-related

configuration change Engineering.

Service Requests

completed

between

June 3,

1996,

and February

11,

1997 (Section E1.1).

Hodifications packages

reviewed were of good quality and complied with

design control requirements

(Sections

E1.2 and E1.3).

Plant engineers

conducted

a good indepth evaluation of the containment

lines corrosion problem after it was identified by the inspectors

(Section E1.4).

The licenseee

has established

acceptable

procedures

for the review and

evaluations of NRC information notices

(Section E2.2).

The licensee's

self-assessments

in engineering

were adequate

(Section E7.2).

The Harris Engineering Support Section

was proactive in support of

the plant when emergent

conditions were identified (Sections

E2. 1

and E2.3).

Plant

Su

ort

The radiological controls program was being effectively implemented

overall with good radiation control performance

demonstrated

during

outage conditions (Section Rl.1).

One non-cited violation was identified for failure of radiation workers

to promptly leave

a work area

when their electronic dosimeters

alarmed

(Section R1.2) .

One non-cited violation was identified for failure to tag and label

radioactive material in accordance

with procedure

(Section R1.3).

Contamination control

was effective overall with personnel

contamination

events

on

a favorable reducing trend (Section R1.4).

The ALARA program was effectively controlling total site dose to record

lows for the site (Section Rl.5).

The l-icensee

has

been proactive in the resolution of the Thermo-Lag

issue

(Section F1.2).

Good compliance with plant fire prevention procedures

has resulted in a

low incident of fire within the plant protected

area

(Section F1.3).

There

was not

a significant corrective action maintenance

backlog

associated

with the fire protection systems.

The material condition of

fire protection

components

was good (Section

F2. 1).

A violation of Technical Specification 6.8. l.a was identified for

failing to establish written procedures

to verify the functional

operability of the seismic fire protection check valves that provide

fire protection

and emergency service water

system integrity following a

Safe

Shutdown Earthquake

(Section F2.2).

4

C

Implementation of the fire protection suiveillance

program

has not been

fully effective.

As previously identified in licensee self assessments,

the number of fire protection surveillance

procedures

being performed

within their grace period continued to be excessive

(Section F2.3).

The fire protection program implementing procedures

were good and met

licensee

and

NRC requirements.

The fire fighting pre-fire plans were

satisfactory.

Appropriate fire prevention controls were being applied

to refueling outage activities (Section F3).

The fire brigade organization

and training met the requirements of the

site procedures

(Section F5).

A 1997 assessment

of the facility's fire protection program was

comprehensive

and was effective in identifying fire protection program

performance deficiencies to management.

Planned corrective actions in

response to the audit issues

were acceptable

(Section F7).

4

R~Dt

Summar

of Plant Status

Unit 1 began this inspection period at 100 percent

power.

The unit was

maintained at this power level until April 4,

1997,

when operator s reduced

power in preparation for the refueling outage,

RFO-7.

Operators

manually

tripped the reactor

and the unit entered

Hode 3 (Hot Standby)

on April 5.

Hode 4 (Hot Shutdown)

was entered

on April 5 and operators

continued to reduce

reactor coolant system temperature,

placing the plant in Hode 5 (Cold

Shutdown)

on April 6.

The unit entered

Hode

6 (reactor vessel

head

detensioned

with fuel in the vessel)

for refueling on April 16 and defueling

of the reactor

core was completed

on April 23.

The reactor

vessel

10-year

inspection

was completed during the defueled period.

Node

6 was re-entered

on

Hay 6,

and the unit remained there until Hay 14 when Hode

5 was entered

(reactor

vessel

head fully tensioned with fuel in the vessel).

The unit

remained in Hode

5 for the remainder

of the period.

I. 0

rations

01

Conduct of Operations

Ol. 1

General

Comments

71707

Using Inspection Procedure 71707, the inspectors

conducted

frequent

reviews of ongoing plant operations.

These included reactor

shutdown

and plant cooldown activities conducted in accordance

with procedures

GP-006,

Normal Plant Shutdown from Power Operation to Hot Standby

(Hode

1 to Hode 3), Revision 13;

and GP-007,

Normal Plant Cooldown

(Hode 3 to

Hode 5), Revision 15.

The inspector s also observed all or portions of the following core

alterations

during the use of procedure

GP-009,

Refueling Cavity Fill,

Refueling and Drain of the Refueling Cavity, Revision 13:

Integrated

Reactor

Vessel

Head removal

and installation

Removal

and installation of the Upper Internals

Package

from the

reactor vessel

Removal

and installation of the Lower Internals

Package

from the

reactor vessel to facilitate the 10-year reactor vessel

inspection.

In general,

the conduct of plant operations

was professional

and safety-

conscious.

Technical specification requirements

for equipment

oper ability, instrument

channel

checks,

and plant cooldown rates

were

adhered to for specific activities observed

by the inspectors.

Specific

events

and noteworthy observations

covered

by other procedures

are

detailed in the sections

below.

0

01.2

Fuel

Novement

a.

b.

Ins ection Sco

e

60710

The inspectors

used Inspection

Procedure

60710 to observe the refueling

activities involving fuel assembly

movement.

The inspectors

observed all or portions of the following fuel handling

procedures:

~

FHP-014,

Fuel

and Insert Shuffle Sequence,

Revision 12/1.

~

FHP-020, Refueling Operations,

Revision

13 and 13/1.

~

FHP-025,

HNP Insert Handling Operations,

Revision 6.

Observations

and Findin s

The inspectors

found the fuel movement performed under these activities

to be professional

and thorough.

All work observed

was performed with

the procedures

present

and in active use.

Operators

were experienced

and knowledgeable of their assigned

tasks.

The inspectors

frequently

observed

supervisors

and system engineers

monitoring job progress,

and

quality control personnel

were present

whenever

required by procedure.

Foreign material exclusion areas

were maintained

as required.

The licensee

had problems with three fuel assemblies.

A leaking fuel

rod in assembly

(HA-50) was identified by using in-mast sipping,

a

technique

used to detect the presence of certain radionuclides

along the

length of the fuel assembly.

Assembly HA-50 was not scheduled to be

reloaded in the core and was stored in the spent fuel pool.

Assembly,

HJ-48, did not indicate being fully latched to the fuel handling crane

in the spent fuel handling building.

This was caused

by the indicator

flag not remaining in the full up position when the assembly

was lifted.

After several

attempts

and troubleshooting,

the licensee

used

an

- underwater

camera to verify the assembly

was latched before finally

moving the fuel assembly in the fuel handling building.

This assembly

was subsequently

reloaded in the core with no problems.

Another

,assembly,

HJ-57,

had

a thimble guide tube lodged in the instrument tube

of the assembly.

The licensee

was able to remove the thimble guide tube

using

an underwater

camera

and consultation with fuel vendor

representatives.

Assembly,

HJ-57,

was ultimately reloaded in the core,

but was placed in a location where insertion of a thimble guide tube was

not necessary.

c.

Conclusions

The inspectors

concluded that licensee activities involving the movement

of fuel assemblies

were conducted in an acceptable

manner.

The licensee

made conservative troubleshooting

and contingency decisions

when

problems

arose,

and the use of specialized

equipment

was beneficial.

01.3

Prohibited

Hode

6 Entr

Ins ection Sco

e

71707

b.

On Hay 8,

1997 at 7:18 a.m. the unit entered

Hode 6 (fuel in the reactor

vessel,

reactor vessel

head

removed or detensioned)

to load the core for

cycle 8.

The inspectors

observed the Hode

6 entry from defueled to

determine if procedures

were followed and Technical Specification

Limiting Conditions for Operations

(TS LCOs) were satisfied.

Procedure

GP-009,

Refueling Cavity Fil'1, Refueling

and Drain of the Refueling

Cavity, Revision 13,

was applicable to this evolution.

Observations

and Findin s

The inspectors

observed that the prerequisites

for Hode

6 entry from

defueled

were completed prior to the 6:30 a.m. shift turnover meeting

on

Hay 8,

1997.

The prerequisites

were contained in procedure

GP-009.

A

problem with the IDP-lA-SIII instrument

bus occurred at 6:44 a.m. that

morning which caused the SIII inverter output breaker to trip.

This

caused

equipment served

by that bus to be inoperable

as listed in

AOP-24,

Loss of Uninterruptible Power

Supply, Revision 11.

Included

were the fuel handling building (FHB) emergency

exhaust train "A" (E-12

fan)

and the control

room emergency filtration train "A" (R-2A fan)

which were required for Hode 6.

Immediately after the shift turnover,

FHB emergency exhaust train "B" (E-13 fan)

was placed in service to

comply with TS 3.9. 12 since the operable

emergency

power supply

(emergency diesel

generator

B-SB) was on that train.

The shift

operations

crew assumed that entry into the 7-day action statement

for

TS

LCO 3.7.6 for having one train of control

room ventilation inoperable

would allow compliance with that specification.

The shift operations

crew assessed

that Hode 6 could be entered in this condition and that

TS 3.0.4,

which prohibits TS Operational

Hode entry while relying on TS

LCO

action statements,

did not apply.

The operations

crew did not reassess

the control

room ventilation equipment failure against the GP-009

Hinimum Equipment List in Attachment

6 for the defueled to Hode

6

change.

Attachment

6 identified that both trains of control

room

ventilation were required for Hode

6 entry.

Hode

6 was subsequently

entered

at 7:18 a.m. with one train of'ontrol

room ventilation

inoperable.

The inspector

observed that at 8: 15 a.m. the work control center

informed the control

room operators that Technical Specification 3.0.4

had been violated due to the plant reliance

on

a TS 3.7.6 action

statement

for

Hode

6 entry.

Condition Report 97-02485

was written to

document this problem.

The inspector

noted that TS 3.9.12 (for FHB

emergency

exhaust)

had

an exemption to TS 3.0.4 while TS 3.7.6 did not.

The licensee

evaluated this failure to comply with TS 3.0.4

and

determined that since it had been missed, it would not make sense to

defuel, wait for restoration of the "A" train control

room ventilation

system to operable,

and then re-enter

Hode 6.

The licensee

continued

with fuel reload

as if TS 3.0.4

had been met,

and continued to rely upon

the TS 3.7.6 action statement

for the inoperable ventilation train.

The

work to repair the SIII instrument

bus was not considered

as

a restraint

to fuel movement.

The inspector

reviewed the TS 3.0.4 Bases section

and discussed

the

significance of TS 3.0.4 with licensee

management.

The TS 3.0.4 basis

state that the intent is to ensure that facility operation is not

initiated with either required equipment or systems

inoperable or other

specified limits being exceeded.

The inspector pointed out that TS 3.0.4 established

the safety level at which

a mode change

can

be made

by

ensuring that the full complement of systems,

equipment,

and components

are operable.

The inspector

also pointed out that TS 3.0.4 does not

have

an action statement,

therefore it must

be complied with.

Even

though

a mistake

had been

made in making the mode change without

complying with TS 3.0.4,

once discovered,

the intent must be complied

with.

After discussing

TS 3.0.4 with the licensee,

the inspector

observed that the licensee

immediately stopped fuel load until all

equipment required for Node

6 was operable.

Re ulator

Si nificance

02

02.1

Technical Specification 3.0.4 requires that entry into an Operational

Hode or other specified condition shall

not be made unless the

conditions for the Limiting Condition for Operation

are met without

reliance

on provisions contained in the Action requirements.

Exceptions

to these

requirements

are stated in the individual specifications.

In

this case

TS 3.7.6

was not met at the time that

Node

6 was entered

from

defueled

and did not contain

an exception to TS 3.0.4.

This was also

contrary to the prerequisites

established

in procedure

GP-009.

This

failure was identified by the licensee,

but not corrected until prompted

by the inspectors.

The failure to comply with TS 3.0.4

and procedure

GP-009 is identified as

a violation (50-400/97-04-01).

Conclusions

The inspectoi

concluded that

a violation of TS 3.0.4

had occurred'.

Although the violation was licensee-identified,

the inspector

concluded

that the licensee's initial corrective action was inadequate.

Operational

Status of Facilities and Equipment

En ineered Safet

Feature

S stem Walkdowns

Ins ection Sco

e

71707

The inspectors

used Inspection

Procedure

71707 to walk down accessible

portions of the following ESF systems

inside reactor

containment during

the refueling outage:

~

Residual

Heat Removal/Low Head Safety Injection System

(FSAR

Section 5.4.7)

~

Auxiliary Feedwater

System

(FSAR Section 10.4.9)

~

Containment

Spray System

(FSAR Section 6.5.2)

~

Component Cooling Water

System

(FSAR Section 9.2

~ 2)

~

Chemical. and Volume Control System

(FSAR Section 9.3.4)

The inspectors

used the current simplified flow diagrams

and equipment

lineup checklist from the operating procedures of each

system to verify

the correct valve and instrument lineup.

Observations

and Findin s

The inspectors

found valve and breaker positions to be in accordance

with the applicable

mode of the unit.

Haterial condition of'he systems

were adequate.

Conclusions

'quipment

operability, material condition,

and housekeeping

were

acceptable

in all cases.

The inspectors identified no substantive

concerns

as

a result of these

walkdowns.

Operator

Knowledge and Performance

.Boron Thermal

Re eneration

S stem

BTRS

Over -Dilution Event

Ins ection Sco

e

71707

The inspectors

reviewed

and evaluated the circumstances

surrounding the

first of two reactor coolant system

(RCS) boron dilution events

which

occurred within two weeks of each other.

The first event occurred

on

Harch 29,

1997, the last day of the previous inspection period,

and was

fully evaluated

during this inspection period to assess

root and

contributing causes

along with corrective actions.

Observations

and Findin s

On Harch 29,

1997, with the plant operating in Hode

1 at 100 percent

power,

a control board operator initiated

a routine

RCS boron dilution

evolution for what was intended to be 2 minutes using the

BTRS in dilute

mode.

This system

uses

a temperature

dependent

ion-exchange

process

via

one of several

demineralizer

beds to raise

or lower boron concentration.

The

BTRS system

reduces

radioactive waste

and offers finer control of

average

RCS temperature

near

the end of the fuel cycle when control rods

are full out and cannot

be relied upon for that function.

The operator

intended to "bump up"

RCS average

temperature

(to match reference

temperature)

just before shift turnover for the oncoming shift.

The operator obtained permission

from the Unit Senior Control Operator

(SCO) to perform the evolution and initiated the dilution at 5:16 a.m.

without notifying anyone else

on shift of his actions.

The operator

was

somehow distracted

and his attentions

were diverted from this evolution.

The

RCS dilution via BTRS continued for thirty minutes until

approximately 5:46 a.m.

when the operator walked by the digital nuclear

instrumentation

drawers which indicated that reactor

power

was at 100.3

percent.

The operator

immediately realized the error,

secured

the

dilution, and informed his management of the incident.

Operations

personnel

generated

Condition Report 97-01348 for this event.

Safet

Si nificance

As

a result of the error,

RCS temperature

increased

approximately 0.2

degrees

Fahrenheit,

and indicated reactor

power increased to 100.3

ercent.

A subsequent

required flux map indicated that no core thermal

imits were exceeded.

RCS boron concentration

was reduced less than

approximately

6 parts per million as determined

by comparing the

Harch 29,

1997

RCS sample results to those of the previous day.

While

these

numbers

represented

only a slight adjustment in core reactivity,

the event itself uncovered

some nonconservative

approaches

to reactivity

management.

First,

BTRS dilution evolutions were not routinely entered

in the control

operator

's logbook by all operators.

These dilutions

were considered to be so frequent

and short in duration that logging was

arbitrary.

Secondly,

the reactor operator did not feel the need to

communicate this reactivity manipulation to the

BOP operator

or other

crew members.

The operator also did not use

a 5-minute timer that was

provided

as

an operator

error reduction tool for this evolution.

Finally, the Unit SCO did not adequately

supervise

the

RO or monitor

reactivity manipulations.

The inspectors

considered

these actions to be

precursors

to potentially more significant reactivity control problems

given different circumstances.

Re ulator

Si nificance

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires that

conditions adverse to quality, such

as failures, malfunctions,

deficiencies,

deviations,

defective material

and equipment,

and

nonconformances

are promptly identified and corrected.

This requirement

is further delineated in the licensee's

Corporate Quality Assurance

Program Hanual, Section 12.0, Conditions Adverse to Quality (CATQ) and

Corrective Action, Revision 18.

The licensee's

corrective actions for

recent violations associated

with operator errors included establishing

a Near

Term Improvement Plan with several initiatives for improving

performance.

These corrective actions

were discussed

in the licensee's

response to

NRC Violation 50-400/96-09-01

dated

December

9,

1996.

Among those initiatives were improving consistency

between shifts,

improving communications within operations,

improving utilization of

human error prevention techniques,

and improving human performance in

general.

Licensee

personnel

failed to effectively implement the

previous corrective actions

as exemplified by the

human errors which

lead to the Harch 29 over-dilution event is considered

a violation of

10 CFR 50, Appendix B, Criterion XVI (50-400/97-04-02,

Example 1).

Conclusions

The Harch 29 over-dilution event represented

failures in several

areas

including operations

crew supervision, reactivity management,

and

communications

between operators.

This example

marked

a continuing

trend in human performance

problems which have lead to

a number of LERs

and

NRC violations in late

1996 and early 1997.

One violation was

identified for ineffective implementation of actions to correct this

adverse trend.

04.2

Chemical

and Volume Control

S stem

CVCS

Boron Dilution Event

a.

Ins ection Sco

e

71707

The inspectors

reviewed

and evaluated

the circumstances

surrounding the

second of two boron dilution events

which occurred within two weeks of

each other.

The second

event involved errors in operations

and

engineering with respect to the design

and operation of the primary

makeup portion of the

CVCS.

The inspectors'eviewed

the licensee's

root cause investigation for this event to determine if root and

contributing causes

and corrective actions

were adequately

addressed.

The engineering contributions to the primary makeup system

problems

were

thoroughly resear ched by the licensee

and are discussed

in report

Section E2.1

~

b.

Observations

and Findin s

On April 7,

1997, with the plant in Cold Shutdown

(Node 5), operators

were preparing to fill the

RCS pressurizer

solid in accordance

with

plant procedures.

Initial RCS boron concentration

was 2340 parts per

million (ppm).

During previous plant outages,

operators

had received

boric acid flow deviation alarms while attempting to maintain adequate

boric acid flow to support the required

RCS boron concentration of 2340

ppm during

RCS fill evolutions.

In preparation for the April 7

evolution, operators

discussed

the potential for the deviation alarms

and

recommended

corrective actions

based

on previous experiences

following indications of'nadequate

boric acid flow from flow control

valve FCV-113A.

A combination of erroneous

assumptions

and poor

communications

between. shift super vision and control board operators

lead to the events that followed.

Se

uence of Events

Following an automatic

makeup to the volume control tank

(VCT) on

April 7,

a boric acid flow deviation alarm occurred which automatically

secured

primary makeup.

This alarm was due to inadequate

boric acid

makeup flow to the blender, (actual flow did not match the

demand flow of

39 gpm as sensed

by flow transmitter

FT-113).

Operators

responded

by

starting the standby boric acid transfer

pump

(BATP) and restarting

automatic

makeup.

This initial action cleared the flow deviation alarm

but was not an action identified in annunicator

panel

response

procedure

(ALB-006-8-4).

All subsequent

makeups

were to be performed in the

manual

mode,

as instructed to operators

by the shift superintendent.

The April 7 automatic

makeup occur red due to low VCT level

and was

unrelated to the pressurizer fillingevolution.

All subsequent

(manual)

makeups

were

made to support fillingthe pressurizer

to

a solid (water-

filled) condition.

The control board operator initiated

a manual

makeup

to the

VCT at 5:00 a.m on April 8 in accordance

with OP-107,

Chemical

and Volume Control System,

Revision 15, Section 8.7.

Blended primary

makeup/boric acid flow was directed to the top of the

VCT (through the

VCT spray nozzle)

versus the normal flow path to the suction of the

charging/safety injection pumps

(CSIPs).

The operator

chose this

flowpath because of a concern for possible thermal affects

on reactor

coolant

pump seals

(even though this concern

was unfounded since

automatic

makeup normally flows to the suction of the CSIPs

anyway).

Flowing blended primary makeup/boric acid water to the top of the

VCT

through the spray nozzle limited boric acid flow to approximately half

of the 39

gpm needed to support the shutdown boron concentration of over

2340

ppm.

Both boric acid flow deviation and total

makeup water flow

deviation alarms

came in but were assumed

by the control board operator

to be expected

due to the manual

mode of operation.

The control board

operator did not refer to the annunciator

panel

response

procedures for

these

alarms

and did not check boric acid or primary makeup water

flow

rates.

The control board operator initiated three subsequent

manual

makeups with similar results

(actual boric acid flow rates of 19-20

gpm

versus the demanded

39 gpm and resultant flow deviation alarms).

The

flow deviation alarms

were dismissed

as

"nuisance alarms".

Two of the

.three subsequent

evolutions were not entered in the control operator's

logbook.

Each of the four manual

makeups during this shift lasted only

minutes at

a time and involved single

BATP operation.

Following shift turnover at 6:54 a.m.

on April 8, the oncoming shift,

who had been briefed on the "nuisance

alarms", initiated its first

manual

makeup to the

VCT per OP-107 using the

same potentiometer

settings for boric acid flow and total

makeup flow that were used

by the

previous shift.

Upon receiving the flow deviation alarms again, the

control operator

referred to the annunciator

panel

response

procedure

and, in an attempt to increase

boric acid flow, started the standby

BATP.

This only increased

boric acid flow from 18 to 20

gpm as limited

by the flow path alignment to the top of the

VCT.

The operator

initiated

a second

manual

makeup to the top of the

VCT a few minutes

later (the first had been secured

due to the

VCT reaching the upper

end

of its operating pressure

band).

Again boric acid flow was .limited and

deviation alarms

came in.

Operators

suspected

that the boric acid

filter was clogged

and directed

an auxiliary operator to bypass it.

With the boric acid filter bypassed,

a third and final manual

make-up

was initiated at 7:40 a.m.,

again with two BATPs running and similar

results.

Following the third (seventh total) manual

makeup,

the April 8 day shift

Unit Senior

Control Operator

made

a decision to return the primary

makeup system to the automatic

mode and that both BATPs would be used.

The rationale

was that the automatic alignment (to CSIP suction versus

the top of VCT) would provide sufficient boric acid addition to keep

up

with the pressurizer fill rate at the higher boron concentrations.

At

this point, another control board operator

raised the concern that the

previous

manual

makeups

might have reduced overall

RCS boron

concentration.

At 8:20 a.m, the plant was declared solid and

an

RCS

boron sample

was ordered.

The resultant

boron concentration

was 2283

ppm, or 57

ppm less than the last sample indicated the day before.

This

boron dilution represented

the cumulative result of the seven

manual

makeup operations

performed

between 5:00 a.m and 7:40 a.m on April 8..

Licensee

personnel

generated

Condition Report 97-01582 for this event.

Safet

Si nificance

An important implication of this event

was that operators

inadvertently

inserted positive reactivity into a shutdown reactor.

The safety

consequences

from this event were minimized by the fact that the minimum

required boron concentration to ensure

shutdown margin was 801 ppm.

The

2283

ppm boron concentration

at the end of the dilution event

was more

than twice this amount.

However, this incident,

when coupled with the

example discussed

in report Section 04. 1, represents

a failure of the

licensee's

organization to effectively implement corrective actions or

lessons

learned

from previous events.

These include other industry

events related to reacti,vity management

and events at the Harris plant

related to recent operator

human performance trends.

Another

consequence

of the second shift's actions to start

a second

BATP

.with blended primary makeup/boric acid water discharging to the

VCT

spray nozzle

was that the "A" BATP was deadheaded

for several

minutes.

Previous

NRC generic

correspondence

to licensees

(IE Bulletin 88-04,

Potential

Safety-Related

Pump Loss) cautioned against parallel

pump

operation with both pumps in a piping configuration that did not

preclude

pump-to-pump inter action during miniflow operation.

While the

bulletin and the licensee's

resultant

procedural

cautions

were focused

on restrictions during miniflow operation,

the intent of this guidance

was to prevent the type of operation that occurred

on April 8,

1997.

The inspectors

concluded that

some operations

personnel

did not fully

under stand the intent of the guidance

and that this guidance

was not

clearly stated in oper ating procedure

OP-107,

Revision 15,

or in the

CVCS System Description,

SD-107, Revision 6.

The practice of not.referring to annunciator

panel

response

procedures

following alarms

was the most safety significant factor related to

overall plant operation

revealed

from this event.

This practice

had

been previously discussed

in Inspection Report 50-400/97-300,

in

relation to operator

license examination observations;

Inspection Report

50-400/97-03,

in relation to tr aining staff performance;

and for

Violation 50-400/96-11-01,

Example 2, in relation to heat trace

temperature

monitoring alarms.

Re ulator

Si nificance

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires that

conditions adverse to quality, such

as failures, malfunctions,

deficiencies,

deviations.

defective material

and equipment,

and

nonconformances

are promptly identified and corrected.

This .requirement

is further delineated in the licensee's

Corporate Quality Assurance

Program Hanual, Section 12.0, Conditions Adverse to Quality (CATQ) and

10

Cor rective Action, Revision 18.

As discussed

in report'section

04. 1,

the licensee

has initiated extensive corrective actions to address

previous violations associated

with operator

performance.

Although this

event

was licensee identified, the licensee's

implementation of actions

in response

to previous violations was not effective in preventing the

dilution events

discussed

in this report.

The failure to effectively

implement corrective actions to prevent the April 8 dilution event is

considered

the second

example of the violation cited in report section

04. 1 against

10 CFR 50, Appendix B, Criterion XVI (50-400/97-04-02,

Example 2).

Corrective actions

completed during this inspection period included

replacing the valve trim (plug and cage

assembly) for FCV-113A to allow

greater

boric acid flow.

Post-modification testing

had not been

completed at the end of the inspection period.

Additionally, procedure

OP-107 was revised to preclude aligning blended boric acid/primary

makeup water flow to the

VCT spray nozzle

and to provide better

guidance

for responding to the boric acid and total flow deviation alarms.

Conclusions

07

07.1

. The boron dilution event discussed

in this section

was the result of

human performance error s during the operation of the primary makeup

portion of the

CVCS system.

The inspectors

concluded that, prior to the

event,

some operators

did not thoroughly under stand certain limitations

of the system.

This lack of understanding

lead to errors in judgement

and decision making.

The practice of not referring to annunciator

panel

response

procedures

following alarms

was also

a significant factor.

In

addition,

poor communications

between shift supervision

and control

board operators

contributed significantly to the event.

One violation

was identified for failing to effectively implement actions to correct

human performance

problems associated

with previous violations in plant

operations.

guality Assurance in Operations

Licensee Self-Assessment

Activities

40500

During the inspection period, the inspectors

reviewed multiple licensee

self-assessment

activities, including the root causes

for the violation

examples

discussed

in Operations

and Haintenance.

The inspectors

considered

the licensee's

root cause efforts to be thorough for the

boron dilution events

and the TS 3.0.3. entry for CCW.

As discussed

in

report section

H3. 1, the root cause investigation for the containment

hatch missile shield removal did not consider

prior opportunity to

identify or

address this issue.

4

11

Niscel 1aneous

Operations

Issues

(92700,

90712,

92901)

08

08. 1

Closed

LER 50-400/97-007-00:

Inoperable

Component Cooling Water

System

-Technical Specification 3.0.3 Entry

This event

was reported

because

the li'censee

connected

the non-

seismically qualified chemical addition piping section to both trains of

the Component Cooling Water

(CCW) System at the

same time.

LER 96-013-

Ol had reported

the licensee's

discovery that the chemical

addition

section piping was not seismically qualified.

In LER 96-013-01 the

licensee stated in the corrective actions

completed section that the

CCW

System Operating Procedure

(OP-145)

was revised

on November 14,

1996 to

ensure that the

CCW trains are separated

prior to and during chemical

addition and that the affected

CCW train during this evolution would be

declared

inoperable.

LER 97-007-00 states that the November

1996

procedure revision did not separate

the trains.

This was discovered

on

January 4,

1997 when operations

personnel

were reviewing the procedure

prior to use.

The procedure

was revised

and was used successfully after

that.

On Harch 25,

1997, this procedure

was used to add chemicals to the

CCW

.system

and both trains were connected to the chemical addition piping

section.

A note

had been left in the procedure that stated to ensure

the chemicals

are flushed to the in-service header.

This note did not

make sense

because

the procedure

required the headers to be split prior

to the chemical addition evolution which placed both headers

in ser vice.

This confused the operators

and after stopping the evolution and

discussing this note they decided that the A-train was the previously

in-service

header

and would be the train that the chemicals

would be

discharged into.

The operators f'rgot that the 8-train had been lined

up to the chemical addition piping to supply flushing water.

Nine

minutes after the alignment

was established

the operators

realized that

they had made

an error,

stopped the evolution,

and realigned the valves.

The

LER listed the cause

as

a combination of not following procedure

convention regarding the use of parenthetical

component

names/numbers

for dual tr ain systems,

inadequate familiarity with the intent of a

procedure

change,

and

a misleading note in the procedure that

contributed to confusion in this scenario.

However, the inspector

concluded that the note concerning

alignment to the inservice

header

was

what caused the confusion

and that this should have

been

removed by

November

14,

1996 as stated in LER 96-013-01.

The confusion in

following convention

was caused

by trying to comply with the note.

Re ulator

Si nificance

10 CFR 50 Appendix 8 Criterion XVI requires that conditions adverse to

quality be identified and corrected.

For significant conditions adverse

to quality, measures

shall

be taken to determine the cause

and

corrective action taken to preclude repetition.

The licensee

established

corrective actions for a significant condition adverse to

quality in LER 96-013-01.

Those corrective actions

were not adequately

12

implemented in that the procedure

change identified was not adequate

to

. correct the problem, resulting in its recurrence

on March 25,

1997.

This is considered

a violation of 10 CFR 50 Appendix B Criterion XVI for

ineffective corrective action (50-400/97-04-02,

Example 3).

Corrective action for this

LER will be tracked

and reviewed

as part of

the violation.

This

LER is closed.

08.2

Closed

LER 50-400/97-005-00:

Failure to Perform Core Flux Mapping

Following Plant Operation with Reactor

Power Greater than

100 percent.

This event

was reported

due to

a failure to perform core flux mapping

when power was found above

100 percent.

This event is addressed

by

violations 50-400/97-01-03

and 50-400/97-03-01.

Corrective actions will

be reviewed during closure of the violations.

This

LER is closed.

II. Maintenance

H1

Conduct of Haintenance

Hl.l

.General

Comments

62707

The inspectors

observed all or portions of the following work

activities:

96-AHBH1

96-ACMB1

AMPA-001

AGWG-.002

ALCC-001

HST-E0001

LP-T-0408

FHP-044T

PH-I0009

AEQP-001

Perform CM-M0009, Jamesbury Butterfly Wafer-Sphere

Valves

- 14-20" Disassembly

and Maintenance,

Revision

5,

on Valve 1SW-83.

'erform

CH-M0226, Anchor/Darling Butterfly Valves,

Revision 0,

on Valves

1SW-274 and

1SW-40.

Perform HPT-H0091,

Heat Exchanger

Opening/Closing for

NRC Generic Letter 89-13 Inspection,

Revision 4,

on

the Component Cooling Water "B",Heat Exchanger..-

Perform CM-I0002,

AC Limitorque Setup

Check

and

Stroking, Revision 9,

on Valve 1SI-327.

Perform PH-I0043,

Motor Operated

Valve Testing

and

Calibration, Revision 5,

on Valve 1RH-63.

6.9 kv Reactor

Coolant

Pump Circuit Breaker Inspection

and Testing,

Revision 6.

TAVGKDelta T Control Including:

Rod Control,

Power

Hismatch,

Low Power

Feedwater Control,

Steam

Dump

Control,

TREF-TAVG, Rod Control

(speed

and direction),

and Reduced

TAVG Load Follow, Revision 6.

Siemens

S-0253-31/NF991004

Temporary Procedure for

Instrument Thimble Extraction from Fuel Assembly HJ57,

Revision 0.

Incore Instrument Thimble Insertion, Retraction,

Removal,

and Replacement,

Revision 5.

Perform MST-M006, Emergency Diesel Generator

Fuel Oil

Storage

Tank Inspection,

Revision 7.

13

H1.2

The inspectors

found the work performed under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced

and knowledgeable of their assigned

tasks,

procedures

were present

and

followed, work areas

were controlled,

and instrumentation

was

calibrated.

The inspector s frequently observed

supervisors

and system

engineers

monitoring job progress,

and quality control personnel

were

present

whenever required by procedure.

When applicable,

appropriate

radiation control measures

were in place.

Transfer of Heav

load Into Containment

a. Ins ection Sco

e

62707

b.

The inspectors

reviewed

and observed portions of the movement of a

replacement

Reactor Coolant

Pump

(RCP) motor into the containment.

Structural

engineering evaluations

and contingency plans were also

reviewed.

Observations

and Findin s

The licensee

changed

out one of the

RCP motors with a refurbished

motor

as part of their preventative

maintenance

program.

The licensee

plans

to replace the other two RCP motors during the next two refueling

outages

at

a frequency of one per

outage.

The licensee will then

replace

each

RCP motor on

a ten year

cycle at the refueling outage.

This outage,

RCP "B" motor was replaced.

The inspector observed the

replacement

motor lifted by the vendor's

crane

over the refueling water

storage

tank

(RWST) and lowered into the containment

hatch bay.

Transport of the motor

was well controlled.

From the bay, the motor

was

moved into containment

on

a specially constructed rail car,

and was

seismically restrained to the equipment

hatch platform.

The inspectors

reviewed the preparations

for transporting

the

RCP motor.

Since the path exposed the

RWST to potential

damage if the load dropped,

lant systems

were realigned to provide alternate

bor ation sources.

The

oad was over the tank for

a minimal time (20 seconds).

The alternate

path,

over the waste process building, required walking the crane with

the load lifted high and.involved lowering the crane

boom to

a

potentially dangerous

angle to reach the equipment

hatch bay.

The Plant

Nuclear Safety Committee reviewed

and approved the transport path.

The

inspector s determined that prior to the load lift, the crane

was

inspected

and load tested to 125 percent of capacity.

Also, crane

operators

were experienced

and certified.

Conclusions

The inspectors

concluded that transport of the reactor coolant

pump

motor into containment

was well executed.

4

H1.3

14

Observation of RFO-7

Emer enc

Diesel Generator

10-Year'ns ection /

'ver

haul

Ins ection Sco

e

62707

b.

The inspectors

reviewed the work scope for the RFO-7 Emergency Diesel

Generator

(EDG) 10-Year inspection/overhaul,

observed

inspections

and

over haul work in progress

on the "A" and "B" EDGs,

and reviewed

completed

wor k packages

for the "B" EDG.

Training records

were also

reviewed for selected

EDG outage

maintenance

personnel'bservations

and Findin s

Review of RFO-7

EDG Work Sco

e

RFO-7 was the first 10 year inspection/overhaul

scheduled f'r the two

EDGs.

The inspectors

reviewed: Harris Operating License,

Technical

Specifications,

NUREG 1216

[SER on Operability and Reliability of

Transamerica

Delaval, Inc.

(TDI) EDGs],

TDI EDG Owners Group Generic

Topical Report TDI-EDG-001A, TDI EDG Vendor Manual

MBO, Procedure

PLP-113,

Emergency Diesel

Generator Reliability Program,

Revision 2,

.Cooper Enterprise Service Information Memorandum

(SIH) 402A (Nuclear

Haintenance

Management

System

- Preventive

Maintenance

Program),

and the

RFO-7

EDG work activities.

PLP-113 included the requirements

specified

in the TDI EDG vendor manual

MBO and Cooper Enterprise

SIH 402A.

Observation of EDG Ins ection/Overhaul

Work Activities

The inspectors

witnessed

work activities and inspections in progress

during the overhaul of "A" and "B" EDGs.

Activities were well

coordinated

and controlled and work was done in accordance

with wor k

packages

which were present

at the work location.

The work was

performed by a crew consisting of licensee

shared

resource

personnel

and

vendor maintenance/engineering

personnel

under direction of Harris

maintenance

personnel.

The personnel

were knowledgeable of their

assigned

tasks.

Engine/Component

inspections

performed were thorough

and marginal

components

and parts

were identified f'r disposition.

System engineer

and vendor

engineers

were involved in resolving the issues.

Examples of

marginal parts discovered

and replaced

included the "8" EDG camshafts,

and

a fuel tappet

and jacket water drive gear

on the "A" EDG.

EDG

C linder Liner Ins ection

During RF0-7,

6 cylinder liners were replaced

as scheduled

in the "A"

EDG and

10 in the "B" EDG.

These cylinder liners were removed

and

inspected

using pro'cedure

CH-H0151,

Emergency Diesel Generator

Piston,

Rod and Liner Removal

and Inspection,

Revision 6.

The inspectors

witnessed

wet bath fluorescent

magnetic particle non-destructive

examination

(NDE) inspection of the cylinder liner flange radius area

on

several

cylinder liners removed from the

"A" EDG.

There

was

a 10

CFR 21

report on loose fit liner cracking in this area

and the'inspections

were

..

recommended

by the vendor.

The vendor recommendation

was that for

engines with less than 3000 operating hours,

25 percent of the cylinder

liners should be inspected 'for circumferential

cracking at the top liner

flange radius at the next refueling outage.

All liners should

be

inspected/replaced

prior to 3000 operating hours.

The "A" EDG and the

"B". EDG had approximately

1300

and

1000 operating

hours respectively.

If any liner was detected to have

a continuous circumferential

(360

degree)

indication then that liner would be removed from service

and

additional liner s would be inspected.

Cylinder liners removed from the

Harris

EDGs were replaced with new liners,

no liners were reused.

Upon

initial NDE inspection,

2 liners showed

360 degree indications,

2 showed

partial indications,

and two showed

no indications.

These were

documented

on

NDE data sheets.

Subsequently

the liner radius areas

were

further cleaned

and re-examined.

This additional examination

was not

documented

on the

NDE data sheets.

The licensee

sectioned

several of

the liner s and sent them to the

CP8L metallurgical laboratory for

analysis.

Licensee

system engineering

and the vendor

were involved in

evaluating the liner issue

The CPEL metallurgical laboratory indicated that the liner surface

.conditions

obser ved were machining marks

and grain boundaries

and not

true indications.

The inspectors

observed the samples

at the

metallurgical laboratory and discussed

the issue with laboratory

personnel.

Cooper

Energy Services

Engineering personnel

provided

an

engineering evaluation which indicated that all the liners 'should

be

inspected

by the 3000 hour0.0347 days <br />0.833 hours <br />0.00496 weeks <br />0.00114 months <br /> operating limit.

The inspectors

reviewed the

licensee

EDG overhaul

plan and verified that the liner replacement

would

be complete

by RFO-10 well before the 3000 hour0.0347 days <br />0.833 hours <br />0.00496 weeks <br />0.00114 months <br /> operating limit.

The

evaluation of the

EDG cylinder liner issue

was thorough.

Review of Com leted

Wor k Packa

es

The inspectors

reviewed the following completed work packages

for work.

,

performed

on the "B" EDG: 96-AEDX1, AGXH002, 97-AEBG1, 97-ADRK1,-96-- "

AFZL1, 95-ALLJ1, AEOT001,

and 96-AFZHl. Training records for selected

CP8L shared

resource

personnel

and vendor personnel

were reviewed.

The

inspectors

noted that the instrumentation

used

was in calibration and

that personnel

signing procedure

steps

had been trained for the work

activities.

Work packages

were generally complete

however

a discrepancy

was noted

regarding the

NDE data sheet

for the cylinder liner flange filet radius

inspections

performed

on the liners removed

from the

"B" EDG.

The

description of work performed in work package

96-AEDXl indicated that

the inspections

were performed

on 10 liners removed from the "B" EDG and

that no reportable indications were observed.

The

NDE report was not

contained in the work package

and could not be located.

The

NDE

inspector

was interviewed

and the inspectors verified from the

discussion

and his notes that

he had performed the inspection

and that

no reportable indications were found.

This information agreed with the

C.

16

description of work included in the work package.

The licensee

completed

a new data sheet to include in the package.

Conclusions

H1.4

The work scope for the RFO-7

EDG inspection overhaul

met the

requirements

of plant procedures,

the vendor manual,

and the vendor

service information memorandum

regarding 10-year surveillance

and

maintenance activities.

The

EDG wor k activities observed

were conducted

per procedure in a professional

manner

by knowledgeable

personnel.

The

engine/component

inspections

performed were thorough

and identified

problems

were conservatively resolved.

Some discrepancies

were noted

regarding documentation of NDE inspections

on

EDG cylinder liners.

"A" Steam Generator

Forei

n Ob 'ects

a.

Ins ection Sco

e

71707

b.

The inspectors

used Inspection Procedure 71707 to observe the licensee's

activities involving the removal of foreign objects

from the "A" steam

generator.

The inspectors

observed the videotapes of the licensee's

.inspection of the "A" steam generator,

the foreign objects

removed from

the

"A" steam generator,

and the feedwater

check valve,

1FW-158,

where

two bushings

found in the "A" steam generator

originated from.

Observations

and Findin s

A foreign object was detected in the feedwater preheater

section of the

"A" Steam Generator,

during the inservice inspection of the tubes.

A

section of the feedwater line was

removed

and

a camera

was used to

search for foreign objects.

The licensee

found two hinge pin bushing

sets

from feedwater

check valve 1FW-158,

a piece of duct tape,

and

a

piece of the center rib from the preheater

section of the "A" steam

generator

.

These objects

were removed from the "A" steam generator,

and

the licensee

evaluated

and plugged the tubes

damaged

by the foreign

objects'he

two hinge pin bushing sets

(each consisting of'wo eccentric

bushings

held together

by a tack weld) were located

on individual shafts

inside valve 1FW-158 and each held in place by a single tack weld to the

check valve disk.

Each weld was in the feedwater

flow path,

and

had

deteriorated

due to erosion.

Once the welds broke, the bushings

came

off their respective shafts

and entered the "A" steam generator

through

the main feedwater nozzle.

All three of the feedwater

check valves

(1FW-158,

1FW-216,

and

1FW-276) were inspected

and refurbished using

new

bushings.

The bushings

were attached to the disk using several

welds of

increased

size in lieu of the original single tack weld method.

Parts of the "A" steam generator

preheater

ribs around the inconel

target plate were found to be eroded.

The licensee

documented

the

erosion of the center

ribs (upper

and lower)

and the two side ribs of

the "A" steam generator

preheater

region in Condition Report

(CR)

17

, 97-02600.

The steam generators'endor

was evaluating their condition

for operability at the end of the inspection period.

c.

Conclusions

The inspectors

concluded that licensee activities involving the

detection

and recovery of foreign objects in ihe "A" Steam Generator

were conducted in an acceptable

manner

.

The licensee

performed

an

adequate

analysis of the cause of the foreign objects,

and

a review of

the potential

for foreign objects entering the other steam generators.

The licensee

was evaluating the operability of the "A" steam generator

for the degraded

preheater

condition at the end of the inspection

period.

H2

Maintenance

and Material Condition of Facilities and Equipment

M2.1

Surveillance Observation

a.

Ins ection Sco

e

61726

The inspectors

observed all or portions of the following surveillance

tests:

OST-1033, Daily Surveillance

Requirements

Daily Interval,

Revision 12.

OST-1091,

Containment Closure Test Weekly Interval During Core

Alterations and Movement of Irradiated

Fuel Inside Containment,

Revision 4.

OST-1801,

ECCS Throttle Valve,

CSIP and Check Valve Verification,

Revisions

10, 10/1,

and 10/4.

OST-1824,

1B-SB Emergency Diesel Generator Operability Test,

Revision 11/1.

EST-209,

Type

B Local Leak Rate Tests,

Revision 9.

HST-M0006,

Emergency Diesel Generator

Fuel Oil Tank Inspection,

Revision 7.

b.

Observations

and Findin s

The inspector

found that the testing

was adequately

performed.

During

the loss of offsite power and safety injection actuation testing

(procedure

OST-1824), plant equipment

responded

as expected.

Some of

.

the outage-related

surveillance

procedures

required temporary

changes

either immediately prior to or during their performances.

The changes

were either technical or administrative in nature,

but indicated that

some of the test conditions

or requirements

had not been fully thought

out during the procedure

development

and review stages.

Specific

problems with certain surveillance tests

are discussed

in sections

H2.2

and M2.3 below.

Conclusions

18

M2.2

The sur veillance performances

were adeq'uately

conducted.

However,

many

of the surveillance test procedures

required temporary

changes

immediately prior to or during their performance indicating that many of

the test conditions or requirements

had not been thoroughly examined

during the procedure

development

and review stages.

The deficiencies

were identified by licensee

personnel

and documented in condition

reports.

Problems with Remote

Shutdown

S stem Test Procedure

a.

Ins ection Sco

e

62700

b.

The inspectors

reviewed

and observed portions of Operations Surveillance

Test

OST- 1813,

Remote

Shutdown System Operability, Revision 7/4..

Observations

and Findin s

E

Subsequent

to the test the licensee

issued

a condition report

(CR)

97-01890

on anomalies of the test.

Fifteen recommendations

were

made to

improve the test consisting mostly of procedure

changes to identify

expected

equipment

responses

and improve test

sequences.

OST-1813,

an 18-month

(outage) surveillance test,

was performed to

verify the ability to control plant cooldown from outside the main

.control

room.

Operability of transfer

switches,

monitoring

instrumentation

and annunciators

were verified as required by Technical Specification 4.3.3.5.2.

The inspectors

observed the pre-briefing,

portions of Section 7.2 Test

B:

NNS Transfer

Panel

1A-SA and Auxiliary

Transfer

Panel

1A-SA,

and portions of Section 7.3 Test

C: Transfer

Panel

1B.-SB and Auxiliary Transfer

Panel

1B-SB.

Observations

were

made from

the transfer panels,

the auxiliary transfer panels,

and the auxiliary

control panel.

The inspectors

noted that

an approved,

continuous

use

procedure

was present

and followed by the test personnel.

Communications

were established

between the control

room, auxiliary

control panel,

the auxiliary transfer panels,

and the transfer

panels.

The steps

were performed in sequence

at the

command of the test

director,

and the results

recorded

and evaluated.

The inspectors

noted that

some events

such

as equipment starts

and

annunciator

alarms

were not anticipated

as the transfers

were made.

The

- inspectors

considered that the procedure

caused

a number of unnecessary

delays.

In one case,

upon the initiation of transfer of the

SSPS,

.annunciator

alarms

(Low Pressurizer

Pressure

SI and

Low Steam Line

Pressure

SI) were unexpectedly

received.

The licensee

stopped the test

and investigated the cause of the alarms.

The alarms

were determined to

be valid but were not identified as expected

by the procedure.

4

19

Conclusions

As

a result of the procedure

problems,

the test performance

was

considered

weak.

This test

has

been performed at each of the previous

six outages

and procedure

problems still existed.

Pr'oblems with Hi h 'Head Safet

In 'ection

S stem Test

Ins ection Sco

e

61726

The inspector

observed portions of OST-1801,

ECCS Throttle Valve, CSIP,

and Check Valve Verification, 18-Honth Interval,

Node 6, Revision 10.

Observations

and Findin s

The inspectors

observed

operators

perform Section 7.3 of OST-1801,

which

established

a differential

pressure

for the "B" charging/safety

injection pump (CSIP) to setup for collecting pump performance

data.

During the test, after operators

started the

pump and throttled the

discharge isolation valve to obtain the desired differential pressure,

the pressure

exceeded

the allowable band by 47 psid.

The pump was

secured

and the procedure

reviewed to determine if there

was

a problem

with the system alignment.

Plant personnel

discovered that the'B" CSIP

was aligned to the alternate

cold leg injection path for this test which

was

a different alignment than

had been specified in previous procedure

revisions.

The procedure

was revised to incorporate the normal flow path through

the boron injection tank (BIT) and when the test

was subsequently

run,

the

pump performance

data

was still outside the acceptance criteria.

The pump was again secured

and troubleshooting

began.

Plant personnel

determined that the seal injection flow path from the CSIPs

was not in

service,

another

anomaly that was different from the previous revisions

of the procedure.

The procedure

was again

changed

and the test rerun

with similar ly unacceptable

results.

The procedure

went through four

temporary changes

before the test data

(which was still outside the

acceptance criteria range established

in the procedure)

was presented

to

engineering for further. evaluation.

Licensee

personnel

later determined that the pump's data matched the

test performance

curve with negligible degradation

indicated, that the

pump's operability was unaffected,

and that the procedural

acceptance

criteria was erroneous

(for either of the flow paths).

Licensee

personnel

later informed the inspector that the flow and differential

pressure criteria specified in the test procedure

was the

same criteria

established

in the procedure

during the previous refueling outage

and

that test results then exceeded

the allowable range

as well.

Conclusions

The inspector

concluded that although the licensee's

actions to evaluate

the data against the

pump performance

curve for operability before

H2.4

20

making any changes to the system flow characteristics

were commendable,

the licensee's

surveillance

procedure

review process

was deficient to

not have identified the erroneous criteria during or following the

previous outage's

performance of OST-1801.

Safet

Batter

Fire Durin

Five-Year Dischar

e Test

Ins ection Sco

e

61726

b.

The inspectors

reviewed circumstances

surrounding

a small fire on the

1A-SA emergency battery during

a discharge

performance test

on

April 28,

1997.

The inspectors

assessed

licensee

performance errors

that led to the event

and observed

subsequent

reperformance of the test

to verify that the proper corrective actions

had been

implemented.

Observations

and Findin s

On April 28,

1997,

maintenance

technicians

were per forming procedure

HST-E0013,

lE Battery Performance

Test,

Revision

6 for the 1A-SA

emergency battery.

This procedure

implemented Technical Specification

Surveillance

Requirement 4.8.2.1.e.

by verifying every five years that

the emergency batteries'apacities

were at least

80 percent of the

manufacturer's

rating when subjected to a performance

discharge test.

About one hour into the test,

the technicians,

who were sitting outside

the battery

room monitoring test parameters

on

a computer,

smelled

smoke

coming from the room.

Upon entry, they discovered

small

flames coming

from a jumper cable attached to the number

1 battery cell.

A technician

extinguished the fire with a carbon dioxide extinguisher while another

notified the main control

room who then sounded

an alarm and dispatched

the plant fire brigade to the scene.

The inspectors

arrived at the battery room within minutes of the fire

and noted that minimal

damage

had occurred.

The top plastic cover of

the

number

1 cell was burned through in an approximated

two square

inch

area

due to hot melted plastic insulation from the jumper cable that

had

been attached to it.

The number

1 cell was the only one (of 60 total)

that was damaged.

The discharge test

had been terminated

and

technicians

had secured

the test equipment.

The damaged cell

was later

replaced

and the discharge test

was rerun the next day after the battery

was recharged.

The inspectors

learned through discussions

with the technicians that the

wrong jumper cable

had been

used to connect the load unit to the

battery.

Instead of using the parallel

conductor

1/0 cables

(with a

mechanical

bolted connection)

which had been specifically designed

for

this test,

the technician

connected

a single conductor

1/0 cable which

used

a standard alligator-style clamp-on connection.

The combined

effect of using

a single conductor

cable with a questionable

connection

to carry 298

amps resulted in the jumper cable. plastic insulation

heating

up excessively,

which caused

the fire.

The single conductor

was

usually used for another (lesser

ampacity)

18-month surveillance test.

The five-year test

had been prebriefed the day before,

and the

21

technician performing the test

knew which cable to use,

but made

a'ognitive

error while connecting the load unit to the battery.

The

procedure

did not specify which of the two jumper cable types to use.

Prior to reperforming the test,

HST-E0013 was revised to include

cautions to use the parallel

conductor cables.

The inspector

observed

the retest

and verified that battery test acceptance

criteria were

satisfied.

The inspector considered

licensee

personnel

actions to

revise this procedure to specify the parallel conductor cables to be

appropriate.

Technical Specification 6.8.1.a.

and Regulatory Guide 1.33,

Appendix A,

Section B.b.(l)(q), require written procedures to be established,

implemented,

and maintained covering emergency

power tests.

The failure

to adequately establish

and implement procedural

guidance for using the

correct test equipment for the 1A-SA Emergency Battery was contrary to

this requirement

and is considered

a violation.

This licensee-

identified and corrected violation is being treated

as

a Non-Cited

Violation, consistent with Section VII.B.1 of the

NRC Enforcement Policy

(NCV 50-400/97-04-03).

Conclusions

A small fire resulted

from using improper cables to test the 1A-SA

emergency battery.

The safety consequences

from the fire were minimal

in terms of plant equipment

damage

and personnel

safety.

One Non-Cited

Violation was identified.

Observation of Inservice Ins ection

ISI

Work Activities For the

Reactor

Vessel

Ins ection Sco

e

73753

The inspector

reviewed examination procedures,

vessel

scan plans,

programmed calibration setup data,

examiner certifications,

and observed

examination/evaluation

activities for the first 10-year interval

ultrasonic examinations of the Shearon Harris Reactor

Vessel.

See

NRC

Inspection Report

No. 50-400/97-03 for a programmatic review of the

first 10-year

inservice inspection interval program.

Observations

and Findin s

Shearon Harris started

commercial

operation

on Hay 2,

1987; therefore,

the April 1997 refueling outage is the final outage of the first 10-year

ISI Inspection Interval.

One major inspection required for completion

of the first ISI interval is the volumetric examination of the Reactor

Pressure

Vessel

(RPV) and the attachment

piping welds.

The vessel

examinations

were conducted

by Southwest

Research Institute

(SwRI) and

selected

examinations

were witnessed

by the inspector during the

refueling outage

(RFO-7).

The 1983 Edition with Summer

1983 Addenda

(83S83) is the

ASNE BSPV Code,

Section XI "Code-of-Record" for the first

10-year inspection interval.

22

The inspector

reviewed the ISI outage examination plan, 'the vessel

scan

plan,

programmed calibration setup parameters,

examiner certification

records

and the following ultrasonic examination/operation

procedures

to

determine

whether

the procedural

content,

technical instructions

and

'erification

documentation

were adequate:

SHH-AUT14, Automated Ultrasonic Inside Surface Examination of

Pressure

Piping Welds, Revision

1

~

SHH-AUT15, Automated Inside Surface Examination of Ferritic

Vessels

Greater than 4.0 Inches in Thickness,

Revision

1

~

SwRI-AUT2, Automated Inside Surface

Examination Indication

Resolution,

Revision. 10

SwRI-AUT5, Southwest

Research

Institute

PaR Device and Attachments

Operation,

Revision 4

~

SwRI-AUT7, Southwest

Research

Institute

PaR Device Assembly,

Revision 4

SwRI-AUT8, Southwest

Research

Institute

PaR Device Calibration,

Revision

3

~

SwRI-AUT34, Southwest

Research

Institute

PaR Device Checkout,

Revision

3

~

SwRI-AUT36, Checkout

and operation of the 8-channel

Enhanced

Data

Acquisition System,

Revision

0

~

SwRI-AUT38, Automated Ultrasonic System Performance Verification,

Revision

1

~

SwRI-EDAS2,

Enhanced

Data Acquisition System-II Performance

Verification Procedure

(Test Plan), Revision 3

~

SwRI-PDI-AUTl, Automatic Inside Surface Ultrasonic Examination of

Ferritic Vessel

Wall Greater than 4.0 Inches in Thickness,

Revision

2

~

SwRI-PDI-AUT2, Automated Inside Surface Ultrasonic Flaw Evaluation

and Sizing, Revision

2

In addition to the above reviews, the inspector

analyzed examination

data for the following welds concurrently with the

SwRI Level III

'nalyst to determine if the examiner

was knowledgeable of the procedure

requirements

and whether

examination results

were recorded

as specified

in the ISI program

and in the nondestructive

examination

(NDE)

procedures:

~

Outlet Nozzle to Shell

9 25

, Weld No. RV-NOZ-AO-N-06

~

Outlet Nozzle to Shell 9 265',

Weld No.

RV-NOZ-BO-N-02

23

Meridional Weld 8 165',

Weld No.

MHW-RV-14

Meridional Weld 8 285',

Weld No.

MHW-RV-12

Meridional Weld 8 345',

Weld No. MHW-RV-ll

Intermediate

Shell to Lower Shell

Weld No.

CSW-RV-03

Outlet Nozzle to Shell

8 145',

Weld No. RV-NOZ-CO-N-04

Meridional Weld 8 45',

Weld No.

MHW-RV-16

Conclusions

Ultrasonic examinations

witnessed

by the inspector,

and interpretation

/evaluation/acceptance

of the test results

were conducted in a

proficient manner

by experienced

and knowledgeable

examiners.

Steam Generator

SG

Edd

Current Examination

and Data Evaluation

Activities

Ins ection Sco

e

73753

and 50002

The inspector

reviewed the licensee's

steam generator

eddy current

program

and examination procedures,

examiner certification records,

and

observed site resolution analysts

evaluating

eddy current data.

The

site resolution group analysts

resolved differences

encountered

in

interpretation of data

from the first eddy current data review group

made

up with a combination of Duke and ASEA, Brown, Boveri

(ABB)

analysts

and located at the McGuire Nuclear Plant

and the 2nd eddy

current data review group performed by Framatone

Technologies in

Lynchburg, Virginia.

Observations

and Findin s

During RF0-7, the licensee

had planned to perform

a total of 18,948 eddy

current examinations in the three Shearon Harris Steam Generators.

The

examinations

were conducted

using

a combination of bobbin and Plus Point

coil probes.

The examinations

performed with the Plus Point probe

was

a

new addition to the technology used by the licensee to properly identify

discontinuities in areas

such

as the top of tubesheet

on the hot leg,

rows

1 thru 3 U-behds,

special interest

areas,

and the preheater

expansion

zone for steam generator

A only.

As a result of using the

plus point probe, the licensee

also expected to plug

a higher number of

tubes this outage.

The inspector

examined the licensee's

steam generator

eddy current

activities by reviewing the procedures listed below:

Carolina

Power

and Light Company

(CP8L) Steam Generator Strategic

Plan,

"Harris Nuclear Plant Strategic Plan," Revision

0

CPSL Procedure

PLP-651,

Steam Generator

Program,

Revision

0

CP&L Procedure

EST-216,

Steam Generator

Tube Indication Tracking

and Reporting Procedure,

Revision

5

~

CP&L Procedure

HNP-100-005,

Steam Generator

Eddy Current

Interpretation Guidelines,

Revision

1

In addition, the inspector

reviewed all examiner certification records

and observed

two resolution group analysts

perform their analyses

of the

eddy current data.

During the eddy current examinations

on "A" Steam

Generator,

foreign objects

were discovered in the preheat

area

below the

feedwater inlet adjacent to the

Row 49,

Column 59 tube.

These

items

were subsequently

removed (report section H1.4).

At the conclusion of

the inspection,

the licensee

was also predicting that approximately 28

tubes

would have to be plugged this inspection.

This was

a much higher

number than normally plugged during previous outages.

However, it

reflected the improvements in inspection technology used this outage for

the detection

and evaluation of eddy current indications.

Discussions

with licensee

cognizant engineers

and vendor

analyst 'personnel

indicated

that these individuals were well-trained,

knowledgeable,

and dedicated.

c.

Conclusions

Steam generator

eddy current activities were well-managed.

Program

and

examination procedures

were very good, knowledgeable/skillful

vendor

personnel

were utilized,

and state-of-the-art

examination equipment

was

used.

H2.7

Ultrasonic Examination of Containment

Liner

a.

Ins ection Sco

e

57080

The inspector

observed ultrasonic thickness

examinations of the

containment liner below the top surface of the concrete floor slab at

the 0'nd 85'zimuth.

This inspection

was performed to investigate

corrosion noted

on the liner during walkdown visual inspections

documented in Condition Report 97-01880.

The engineering evaluation of

this issue is addressed

in section E1.4 of this inspection report.

b.

Observations

and Findin s

The following account of the inspection

observed

by the inspector

was

written in part,

by the Level III ultrasonic examiner

who developed the

techniques

used to acquire the containment liner measurements.

"As part of resolution of potential

containment liner corrosion, it was

deemed

necessary to perform ultrasonic thickness testing

(UT-T) of the

liner below the 221-foot floor elevation.

Because of the narrow gap

where the Ethafoam

had been

removed

between the containment liner

and

the concrete floor slab

(1 inch

- 5/8 inch range),

conventional direct

contact ultrasonic thickness testing with an inspector's

hand

on the

UT

transducer

could not be done.

Thus, it was necessary

to devise

an

extension

piece which could be used to position the transducer

down in

the gap and in suitable contact with the liner surface to obtain the

thickness

measurements.

25

The transducer

extension

was devised

by mounting

a select

UT transduc'er

on the end of an approximately 5i-foot length of i inch x 1 inch flat

metal bar stock.

The actual transducer

mounting location on the bar was

machined to form a depression

with a gradual

taper

so 'as to somewhat

'ecess

the transducer

body and it's coaxial cable connection in the

bar,

thereby reducing the overall thickness

dimension of the extension piece.

UT couplant

was delivered to the transducer

face area

by small plastic

tubing connected to a plastic

hand syringe.

Index marks were

made

on

the bar at six inch intervals measured

from the transducer

centerline to

facilitate positioning the 'transducer to obtain thickness

measurements

at six inch intervals

down the liner from the floor level.

To'obtain thickness

measurements,

the extension

was lowered down into

the gap to the first measurement

position at the bottom, the couplant

syringe

pumped couplant to the transducer

face area

and the bar

positioned

so that the transducer

face was in contact with the liner

plate surface.

For each oi the subsequent

thickness

measurements,

the

bar

was raised to the next 6 inch index mark on the bar was at floor

level

and the operation

repeated.

Thickness

measurements

of the liner below 221-foot floor elevation using

the extension

process

were taken at two containment

azimuth locations:

355'zimuth

(general

referred to as the zero degree

azimuth)

and 85'

azimuth (general

referred to as the 90'zimuth).

The nominal thickness of the containment liner was

.375 inch.

The

minimum UT thickness

reading obtained at the 0'zimuth was

.401 inch.

The minimum UT thickness

reading obtained at the 85'zimuth

was

.403

inch.

C.

Conclusions

The inspector considered

the licensee disposition of the containment

liner thickness

issue

documented in Condition Report 97-01880, to have

been resolved in a sound technical

manner.

Licensee ultrasonic

examination personnel

who performed the containment liner thickness

measurements

were resourceful, skillful and very knowledgeable.

Haintenance

Procedures

and Documentation

H3.1

Containment

E ui ment Hatch Hissile Shield Removal

a.

Sco

e

37551

The inspector

reviewed the licensee's

investigation

and actions related

to a problem found while removing the containment

equipment

hatch

missile shields.

Condition Report 97-01499

was written to address this

issue.

The inspector

reviewed procedure

CH-H0100, Containment

Equipment

Hatch Removal

and Replacement,

Revision

6 to determine whether the

procedure

allowed removal of the missile shields in Hode 3.

The

inspector

reviewed the

10

CFR 50.59 safety evaluation screen,

performed

as Attachment

1 to procedure

AP-011,

10

CFR 50.59 Safety Evaluations.

26

The inspector

reviewed Technical Specification 3.6. 1.1 and its

associated

basis,

and

FSAR section 3.3, 3.5,

and 3.8.

Observations

and Findin s

The inspector

found that the licensee

Nuclear Assessment

Section

had

identified on April 5,

1997 at approximately 1:00 p.m. that the

containment

equipment

hatch missile shields

were being removed

and

questioned

whether containment integrity as required by Technical Specification 3.6.1.1

was being maintained.

The licensee's

investigation concluded that the plant had entered the Limiting

Condition for Operation of Technical Specification 3.6. 1. 1 at 3:20 a.m.

on April 5,

1997.

The action statement

required that the unit be in Hot

Standby in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,

however,

the unit was already in that condition,

and

Cold Shutdown in the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The licensee initiated

Condition Report 97-01499 'einstallation of the missile shields

was

completed at 4:50 a.m.

on April 6,

1997, within the time required by the

action statement.

The inspector

found that procedure

CH-H0100 was revised

on April 2,

1997

(Revision 6).

The revision included

a note under section

7. 1, Hissile

Shield Removal, that allowed the missile shields to be removed anytime

in Hode 3 through 6.

The 10

CFR 50.59 safety evaluation screen

was

completed

on April 1,

1997 and concluded that the activity does not

require

a change to the Technical Specifications.

The licensee

concluded that the 50.59 screening

review was inadequate

because it did

not identify that the change to allow removal of the missile shields in

Hode 3 required

a Technical Specification

change.

Technical Specification 3.6. 1. 1 requires

containment integrity be maintained in

Hodes

1 through 4.

The inspector observed that

FSAR section 3.3,

Wind and Tornado Loadings,

described

the containment structure

as

one that was designed to

withstand design wind and tornado generated

missiles.

FSAR se'ction.3.5,

Hissile Protection,

states that protection of safety related

systems

and

equipment,

including the containment liner, from missiles is

accomplished

by various methods including barriers.

Table 3.5.2. 1,

Barriers

Designed

For Hissiles, lists the containment building as the

structure that is designed to prevent external missiles

from damaging

the liner.

Figure 3.5.1-01,

Safety Related Structures

Systems

and

Component Protected Against Tornado Hissiles,

shows the removable

missile shield

as protection for the equipment hatch.

The inspector

found that the missile shields

were not specifically called out in the

written portion of the

FSAR.

However,

based

on the written words for

the containment building being

a barrier for the liner

and the missile

shields being shown on Figure 3.5.1-01

around the equipment hatch,

the

missile shields

performed the

same function for the equipment

hatch that

the containment building performed for the liner.

Licensee

review of

this information during the post event discussion

on April 6,

1997 had

come to the same conclusion.

27

The inspectors

considered that reviews of the outage schedule,

out'age

risk assessment,

and operations

review and work authorization could have

caught this problem prior to initiation of missile shield removal.

The

inspector

discussed this aspect with licensee

management

who initiated

condition report 97-02333,

since the original investigation

had focused

only on the inadequate

procedure

change

and safety review.

Re ulator

Si nific nce

10

CFR 50.59,

Changes,

Tests,

and Experiments,

allows licensees

to make

changes in the facility and procedures

as described

in the safety

analysis report without

NRC approval

unless it involves

a change,to

the

technical specifications

or an unreviewed safety question.

The

procedure

change authorized

an evolution in

a mode that was prohibited

by the plant's technical specifications

and therefore required that

a

technical, specification

change

be submitted

under

10

CFR 50.90.

This is

considered

an apparent violation of 10

CFR 50.59 for making

a change to

the facility through

a procedure that required

a technical specification

change without first seeking

NRC approval

(50-400/97-04-04).

Conclusions

The inspector

concluded that

an apparent violation of 10 CFR 50.59

had

occurred.

The violation was licensee-identified

and was promptly

addressed

and corrected.

III. En ineerin

El

El. 1

Conduct of Engineering

Desi

n Chan

e Processes

'a.- Ins ection Sco

e

37550

The inspectors

reviewed the procedures

listed below which control design

and design

changes to determine if the procedure

implement the

requirements of 10 CFR 50, Appendix B, Criterion III and

10

CFR 50.59.

The following procedures

were reviewed:

EGR-NGGC-0001,

Conduct of Engineering Operations,

Revision 2,

dated February 3,

1997

EGR-NGGC-0003,

Design Review Requirements,

Revision 0, dated

June 3,

1996

EGR-NGGC-0005,

Engineering Service

Requests,

Revision 4, dated

March 25,

1997

EGR-NGGC-0006,

Vendor Manual

Program,

Revision 1, dated August 6,

1996

28

EGR-NGGC-0007,

Haintenance of Design Documents,

Revision" 0, dated

December

17,

1996

EGR-NGGC-0156,

Environmental Qualification of Electrical

Equipment

Important to Safety,

Revision 0, dated

March 5,

1997

EGR-NGGC-0320, Civil/Structural Operability Reviews,

Revision 0,

dated

Hay 8,

1996

EGR-NGGC-0351,

Performance

Monitoring of Structures

and Tanks,

Revision 3, dated

March 17,

1997

ENP-011,

Preparation

and Control of Design Analyses

and

Calculations,

Revision 5, dated

December

19,

1996

Observations

and Findin s

The inspectors verified that the procedures

adequately

addressed

design inputs,

design calculations,

design verification, drawing

changes,

post-modification testing,

control of field changes,

10

CFR 50.59 safety evaluations,

training,

and ALARA reviews.

The inspectors verified that Revision 4 of procedure

EGR-NGGC-0005

complied with the design verification requirements of 10 CFR 50, Appendix B, Criterion III. This procedure is

a corporate

procedure

which specified the requirements

for preparation of

design

changes

at the Brunswick, Harris,

and Robinson plants.

The

inspectors identified

a violation at the licensee's

Brunswick

Plant

(see

NRC Inspection Report number 50-325,

324/97-02)

because

Revision

3 and previous editions of procedure

EGR-NGGC-0005 did

not comply with the design verification requirements of 10 CFR 50, Appendix B, Criterion III.

The violation is summarized

as

follows.

The engineering service requests

(ESR) is the process

used for

performing engineering

work.

EGR-NGGC-0005 defines three types of ESRs.

These

are design

change

(DC), configuration change

(CC),

and engineering

disposition

(ED) ESRs.

Design change

ESRs were defined

as

a change

which affects the design input of a system,

structure,

or component

(SSC); while a configuration change

was

a change to a

SSC which did not

change the design inputs.

Both of these

ESRs produced design output

documents

which could have resulted in modifications to a SSC.

Engineering disposition

ESRs were used to supply information and do not

produce design output documents

or change

any SSC.

ESRs designated

as

design

change

ESRs required design verification to meet the requirements

of 10 CFR 50 Appendix B, Criterion III, ANSI N45.2.11,

and Regulatory

Guide 1.64.

The qualifications for design verifier s were addressed

in

paragraph

4.9 of EGR-NGGC-0001.

ESRs designated

as configuration

changes

required

an engineering

review, instead of a design

verification.

There were

no specific requirements listed for

individuals who performed the engineering

review.

The engineering

review,

as defined by CP8L procedure

EGR-NGGC-0003 did not meet the in-

29

depth review and independent

review requirement's of Appendix B,

Criterion III, ANSI N45.2.11,

and Regulatory Guide 1.64.

These

requirements

specify that the design control measures,

including design

verification activities,

be established to assure

the design basis is

cor rectly translated into design outputs (e.g.,

drawings,

specifications,

procedures,

and/or instructions).

The requirements

also

specify that design

changes

be subjected to the

same controls

as those

applied to the original design.

On February 11,

1997,

as

a result of the identification of'his concern

at the Brunswick Nuclear Plant, the licensee

issued

a temporary change

to procedure

EGR-NGGC-0005 which implemented the

NRC requirements

for

design verification of safety-related

ESRs.

This temporary change

included provisions for all in-process

and non-field-complete

configuration change

ESRs to receive design verifications prior to their

next approval

step.

The licensee

issued

CR 97-01255

on Harch 25,

1997,

to document

and disposition this problem at the Harris plant.

In

addition to revising procedure

EGR-NGGC-0005, the licensee's

corrective

actions,

which were in progress

during the inspection,

also included

review of all safety-related

configuration change

ESRs to determine if

an appropriate

design verification was performed.

Use of Revisions

0 through

3 of EGR-NGGC-0005 to control design

activities

and failing to perform design verification of safety-related

ESRs

was identified as

a violation of 10 CFR 50, Appendix B, Criterion

III. This violation is considered licensee-identified

at the Harris

facility because

plant personnel

took immediate action to resolve the

issue

once it was identified as

a violation at another facility.

This

licensee-identified

and corrected violation is being treated

as

a

Non-Cited Violation, consistent with Section VII.B.l of the

NRC

Enforcement Policy (NCY 50-400/97-04-05,

ESR Design Verification

Requirements).

Conclusions

4

The inspectors

concluded that the licensee's

current design

change

control procedures

complied with the requirements of 10 CFR 50.59,

and

10 CFR 50, Appendix B, Criterion III.

However,

a non-cited violation

was identified for failure to perform design verification of safety-

related configuration change

ESRs from June 3,

1996, the effective date

of Revision

0 of'GR-NGGC-0005,

through February

11,

1997,

when

NRC

identified that

EGR-NGGC-0005 did not comply with 10 CFR 50, Appendix B,

Criterion III at the Brunswick Plant.

Review of modifications to Electrical

S stems

Ins ection Sco

e

37550

The inspectors

performed

a review of modifications planned for refueling

outage

(RFO) 7, with a concentration

on electrical

systems.

There were

18 modification packages

prepared

for implementation

on electrical

systems:

eight "safety-related",

seven considered

important to safety by

30

the inspector,

and the remainder nonsafety-related.

Some of the

requirements

applicable to the areas of review were

10 CFR 50, Appendix B,

10

CFR 50.59,

10

CFR 50.71

and

FSAR Sections

7 and 8

~

Each of the

18 modifications was discussed

with the cognizant engineer.

For

several

modifications, specific additional information was requested

and evaluated

by the inspectors.

Findin s and Observations

Each of the engineers

contacted

were knowledgeable of their assigned

modification, the technical

issues

involved and the relevant

requirements.

No problems

were identified with the design control

program or process.

The inspectors

observed

an effectiveness

in

resolving safety issues

and maintaining the design basis

as evidenced

by

the following examples:

The ground detection

system for the safety-related

batteries

was

upgraded (this was actually an on-line modification).

Root cause evaluations

for circuit breaker

problems were good.

Hodifications in the switchyard under the control of the

transmission

group (i.e., non-plant personnel)

were treated

as

a

plant modification for purposes of performing 50.59 evaluations.

During observation of work in progress,

the inspectors

noted

a problem

with modification

ESR 9500233,

Telemecanique

Disconnect Switch Obsolete.

This modification replaced

a number of fused disconnect

switches with

ones

from a different manufacturer.

The dimensions

provided in the

installation instructions

were incorrect which resulted in work stoppage

to revise the dimensions.

This one example of apparently not verifying

through walkdowns or

mockups the accuracy of work instructions

was

considered

an isolated

case.

Conclusions

Based

on

a review of modifications to electrical

systems

implemented in

the current refuel cycle, the licensee's

performance in the area of

design control

and compliance with the requirements

stated in the

inspection

scope section

was good.

Permanent

Cavit

Seal Installation

Ins ection Sco

e

37550

The inspectors

reviewed drawing and procedures

for installation of

a permanent cavity seal.

b.

Observation

and Findin s

31

C.

E1.4

The inspectors

reviewed

ESR 94-00013,

Permanent

Cavity Seal

Ring.

The purpose of this modification was to eliminate the need for

installation of a temporary seal

each refueling outage

which used

a pneumatic

seal with caulking

(RTD) materials to enable flooding

of the reactor cavity for refueling operations.

This modification

was originally scheduled

for installation during RF0-6, but,fit-up

problems resulted in rework of the permanent

seal

components

and

delayed installation until RFO-7.

The inspectors

reviewed

procedure

EPT-219T, Revision 4,

Permanent

Cavity Seal

Ring

Installation which contained

requirements for the seal

installation.

This procedure specified prerequisites,

installation procedures,

QC inspection requirements,

and

acceptance

testing of the completed installation.

Acceptance

testing included hatch cover leak testing,

pre-floodup inspection,

and the floodup inspections for leaks.

The procedures

also

specified requirements

for visual inspection

and non-destructive

examination

(dye penetrant testing) of welds.

The inspectors

reviewed vendor drawing numbers

6445E71 through 6445E74,

and

6445E76

and vendor technical

manual

HSE-REE-725 which specified

the installation details.

The inspectors

noted that problems

identified during

RFO 6 had been resolved.

Conclusions

The inspectors

concluded that the installation documents

were

adequate to assure

proper installation of the

new permanent cavity

seal.

The acceptance

testing specified

was adequate

to assure

the

seal

would perform its intended function.

Walkdown Ins ection of Reactor

Containment Buildin

Ins ection Sco

e

37550

The inspector

performed

a walkdown inspection of the containment

building to examine the condition of the structure

and installed

systems.

Findin s and Observations

The inspectors,

accompanied

by two engineers

from the Nucl'ear

Assessment

Section

(NAS), walked down the containment building on

elevations

221 (feet above

sea level), 236,

261,

and 286 and

. examined the containment structure,

pipe supports,

instrumentation

and cable tray supports

and the condition of protective coatings.

During the walkdown, the inspector

identified some areas

where the

liner plate appeared to be corroded at elevation

221 from azimuth

60 through

120

adjacent to the concrete slab..

Some small

areas

with corrosion were also identified adjacent to the sumps,

and the

silicone expansion joint sealer

was separated

from the liner plate

in some areas.

The purpose of .the silicon seal

was to keep

c

~

E2

E2.1

32

moisture out oi the one inch wide Ethafoam expansion joint between

the liner plate

and five foot thick concrete

base slab inside

containment.

The licensee initiated CR'7-01880 to document

and

disposition this problem.

'The licensee

removed the corrosion

and

perform

NDE (ultrasonic testing) to determine if the corrosion

had

reduced the thickness of the liner plate.

The

UT showed that the

liner plate exceeded

the nominal thickness of 0.375 inches.

The-

licensee

removed p'ortions of the silicon seal

and the expansion

joint material

(one inch thickness of ethafoam)

and examined the

liner visually and with UT.

The inspectors

witnessed

the

UT exams

and concur red with the licensee's

testing methods

and test results

which showed that the liner exceeded

0.375 inches (section H2.6).

The results

were documented

and evaluated

in ESR 97-00359.

During

the visual

exams,

licensee

engineers

determined that the expansion

joint gap was filled with water up to elevation

219'.

This was

the

same elevation

as the water level in the containment

sumps.

The licensee

pumped the water

from the expansion joint, pumping

out in excess of 5000 gallons.

Chemical analysis of the water

showed

a

pH of'.8,

and

a boron concentration of 2700

ppm.

The

licensee

concluded that the apparent

source of water in the

expansion joint was from the sumps.

The licensee

repaired the

coatings

on the liner, repaired seals

between the expansion joint

and sumps,

and installed

a system to monitor the water level

during plant operations.

The licensee

plans to complete long term

corrective actions

(discussed

in ESR 97-00359) during the next

refueling outage.

Conclusions

Plant engineers

conducted

a good indepth evaluation of this

problem after it was identified by the inspectors.

Engineering Support of Facilities and Equipment

General

Comments

37551

The licensee's

root cause investigation into the second

reactor

coolant

system boron dilution event discussed

in report section 04.2 uncovered

several

previous engineering

problems.

These included incomplete

update

of vendor information related to the

new valve coefficient for the boric

acid flow control valve (1FCV-113A) after its internals

were replaced in

the mid-1980s.

Also, incor rect assumptions

were

made about the

capability of 1FCV-113A when

RCS boron concentration

requirements

were

increased after

a plant upgrade to

a higher enrichment of nuclear fuel

in 1992.

The valve was never tested to verify that its flow capacity

would support the

new higher boron concentration

requirements.

After

repeated

problems with flow deviation alarms

due to.inadequate

boric

acid flow through the valve,

a Plant

Change

Request

(PCR 7285)

was

issued to change the valve trim.

This

PCR was subsequently

canceled in

1995 for no apparent

reason.

33

As mentioned in report section 04.2, the above engineering

problems all

contributed to the system malfunctions that ultimately lead to the

April 8,

1997 boron dilution event identified as example

3 to Violation

50-400/97-04-02.

The licensee's

root cause investigation into the

engineering

issues

related to the April 8 event

was thorough.

The

FCV-

113A valve trim was replaced during RFO-7 and was being tested

subsequent

to this inspection period.

En ineerin

Review of NRC Information Notices

Ins ection Sco

e

40500

The inspectors

reviewed the licensee's

system for processing

and

evaluating

NRC information notices.

Observations

and Findin s

The inspectors

reviewed

CPSL procedure

number AP-31, Operating

Experience

Feedback,

Revision 5, dated February

1,

1996.

This

procedure specifies the process for review and evaluation of NRC

information notices

(INs) and other operating experience

.documents.

The inspectors

also discussed

the licensee's

system

for review and evaluation of INs with licensing engineers

and

reviewed the status of recently issued

INs.

The review and

discussions

disclosed that with the exception of IN 97-09 through

97-13, all other

INs has

been reviewed in licensing

and forwarded

to.the appropriate

group (engineering,

operations,

maintenance,

etc) for evaluation.

IN 97-09,

dated

Harch 12,

1997, through IN 97-13,

dated

Harch 24,

1997,

had not yet been processed

by

licensing

and forwarded to engineering

due to the recent

retirement of the individual in licensing

who previously was

responsible for processing

the INs.

These

INs were forwarded to

engineering for evaluation.

An ESR was opened to document

Engineering actions to address

the issues

in individual INs.

Additional documents

are issued

as required to initiate

appropriate

actions to resolve

any identified issues.

A recent

assessment,

number H-SP-97-05,

completed

on April 1,

1997,

by the

Nuclear Assessment

Section

(NAS) identified an issue regarding

some discrepancies

in procedure

AP-31.

The licensee

issued

CR 97-01423 to document this finding.

The procedure will be

revised

as necessary

to address

the discrepancies.

An item for

management

consideration

was also identified by NAS regarding the

fact that the computer

database

used to track operating experience

items was not "user friendly."

The inspectors

questioned

licensee

engineers

regarding their plans

for followup on IN 97-10, Liner Plate Corrosion in Concrete

Containments.

Since this IN had not yet been sent to engineering,

no specific actions

had yet been developed to address

the IN.

However discussions

with the containment

engineer disclosed that

the licensee

was in the process of implementing the requirements

to comply with revisions to 10

CFR 50.55a which requires

34

containment inspections

and repairs

be performed in accordance

with ASME Section XI, Subsections

IWE and

IWL.

This inspection

was scheduled to be performed prior t'o the containment

leak rate

test,

approximately three

days after the inspectors

completed the

containment

walkdowns discussed

in paragraph

El, above.

Conclusion

The inspectors

determined that the licensee

has established

acceptable

procedures

for the review and evaluation of NRC

information notices.

Forei

n Material

Found in B CCW Heat Exchan

er

Ins ection Sco

e

40500

The inspectors

reviewed the licensee's

evaluations

and resolution of

foreign material

found in B CCW Heat Exchanger.

Observations

and Findin s

During the licensee's

inspection of the "B" component cooling

water

(CCW) heat exchanger,

foreign materials

were found.

The

source of the materials

was determined to be from the emergency

service water strainers that failed due to corrosion.

The purpose

of the strainers

was to filter the service water

and prevent

materials

from being introduced into the system.*

The licensee

initiated

CR 97-01661 to document

and disposition this problem.

Inspection of the "A" train

ESW pump strainers

disclosed that these

strainers,

which were the original materials,

were still functional.

The "B" train pump strainers

were replaced during

RFO 6.

The original

strainers

were fabricated

from 304 stainless

steel.

The replacement

str ainers

were made of Monel 400.

The inspectors

reviewed Material

Evaluation Report

number 001394.00 which was prepared to evaluate

the

replacement

strainers.

The substitution of Monel 400 for 304 stainless

was considered

a material

upgrade since the monel is more corrosion

resistant

than 304 stainless.

The monel

was selected

due to the

unavailability of new stainless

steel strainer s.

The material

evaluation report showed that the monel

was acceptable.

The cause of

the failure was still under investigation by licensee materials

engineers.

The licensee

decided to replace the failed monel str ainers with

new strainers

fabricated

from 304 stainless

since this was the

material originally specified,

and the service life of the 304

strainers

was satisfactory in the ."A" pumps.

The inspector s

reviewed Material Evaluation

number 002703.00

which was completed

to obtain replacement

strainers

for the failed gonel strainers

from another utility.

Replacement

strainers

were not available

from the vendor.

Documentation supplied

by the original vendor

indicated that the replacement

strainer s had been fabricated

from

35

304 stainless.

However,

upon receipt inspection

and testing

performed

by the licensee

when the .new strainers

were received at

the Harris site, the licensee

determined that

some of the

strainer s had been fabricated

from 316 stainless.

A material'old

was placed

on the strainers

pending further investigation by

procurement

engineering.

Procurement

and receiving activities were handled

under the

CPKL

corporate

Operations

and Environmental

Support Department's

Haterials Services

Section,

designated

as Procurement

Engineering.

This is

a separate

organization

from the Harris Engineering

Ser vices Section

and the corporate

Nuclear

Engineering Department.

The following documents

were reviewed which specified requirements

for procurement,

evaluation

and selection,

and receiving

inspection of plant components:

~

HCP-NGGC-0401, Haterial Acquisition, Rev. 2, dated April 15,

1997.

~

EGR-NGGC-0204,

Evaluation

and Selection of Haterials for

Plant Components,

Rev.

0, dated

December

6,

1996.

~

Procurement/Design

Engineering Interface Agreement,

dated

January 5, 1996.

The inspectors

concluded that the licensee's

controls for

procurement of replacement

hardware

complied with NRC

requirements.

The cause of the corrosion of the monel strainers

in the "B" ESW pump was still under investigation at the end of

the inspection period.

Conclusions

The inspectors

concluded that the failure of the strainers

in the

"B" ESW train were not related to an inadequate

evaluation for the

replacement

strainers.

The licensee's

procurement

engineering

program meets

NRC requirements.

Licensee engineers

wer e very

proactive in the evaluation of the strainers'ailure.

Quality Assurance in Engineering Activities

S ecial

FSAR Review

37551

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for a special

focused review that compares

plant

practices,

procedures

and/or

parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

4

h

36

The licensee

made

a presentation

to the

NRC on May 31,

1996 concerning

their corporate-wide

plan for reviewing the

FSAR at the

CPSL sites.

The

program

has generated

a large

number of condition reports at the Harris

Plant

(311 by the end of the inspection period).

The results'from this

program will be reviewed in the closure of Unresolved

Item 50-400/96-04-

04, Tracking

FSAR Discrepancy Resolution.

The inspectors

did not find

any additional discrepancies

other

than those identified by the

licensee.

ualit

Assurance

Assessment

and Oversi ht

Ins ection Sco

e

40500

The inspectors

reviewed self-assessments

performed within the

Harris Engineering Support Section.

Observations

and Findin s

Self-assessments

are part of the overall

CPSL quality assurance

program at Harris.

The self-assessments

were performed in

accordance

with procedure

PLP-03,

Self-Assessment,

Revisions

4 and

.5.

The results of these

assessments

were categorized

as

strengths,

or findings.

The following self-assessments

were

reviewed by the inspector:

HESS96-016,

EQ Program,

May 6

- 9.

1996,

HESS96-025,

Procedure

compliance

- Corrective Action

Effectiveness,

October

1

- November 22,

1996,

HESS96-028, Service Water Program,

and

HESS97-002,

EDBS Program,

January,

1997.

Several

findings were identified in Assessment

96-016.

Six Condition

Reports

(CRs) were written to document discrepancies

identified in the

EQ program;-

However

none of the problems resulted in identification of

any inoperable

equipment.

The conclusion of the assessment

was that the

Harris

EQ program meets overall requirements.

The issues identified

primarily involved procedural

discrepancies

which were being addressed

through issuance of new procedures.

A corporate

procedure,

NGGC-EGR-

0156 was recently issued to resolve

some of the discrepancies

and

clarify some of the

EQ requirements.

One weakness

and two issues for

management

consideration

were identified in Self-assessment

96-028.

The

weakness

involved lack of'cceptance criteria in a service water

surveillance test procedure.

The areas

for management

consider ation

involved procedural

issues.

A CR was opened to address

the weakness

and

areas for management

consideration.

Five issues

and two items f'r

management

consideration

were identified in self-assessment

97-002.

Condition reports

were initiated to document

and resolve these

problems.

The primary areas of concern identified by the self-assessment

involved

inadequate

controls in procedures.

Corrective actions

were in progress

at. the end of the inspection period.

37

C.

Conclusions

The inspectors

concluded that the self-assessments

performed by

HESS were effective in identifying engineering

performance

deficiencies

and were useful in providing oversight to management.

Managers in HESS have

been proactive in following up on the

EQ

problems identified at other sites to address

any

EQ program

deficiencies.

E8

E8.1

E8.2

Miscellaneous

Engineering Issues

(92700,

92903)

Closed

Unresolved

Item 50-400/96-02-03:

Use of Potentially

Unconfirmed Information Obtained via Telecons in Design Calculations.

During review of engineering service requests

during the

inspection

documented in NRC Inspection Report 50-400/96-02,

the

inspectors identified three examples of licensee

design

engineers'pparent

use of information obtained

from vendors over the

telephone without proper verification of the'accuracy of the

information.

This issue

was originally identified during

NAS

Assessment

H-MOD-94-01.

The examples

were identified in ESR

.numbers

9400076,

9400118,

and 9500120.

Further review of the

ESRs

disclosed that additional information was available in the design

backup section of the

ESR which showed the vendor

provided

additional

data to confirm the information originally provided in

the telecon.

The inspectors

reviewed the additional information

provided by the licensee

and verified that the telecon data

was

properly documented.

In one case,

ESR 9400118,

the telecon

information was used to develop the

ESR.

The

ESR wa's then sent to

the vendor for concurrence.

Licensee

engineers

reviewed design

change

packages

installed during the previous three refueling

outages,

RF0-4,

5,

and 6,

and determined that no other examples

were identified of the use of information obtained in telecons

with vendors

for design information with the exception of the

example identified by NAS.

Precautions

regarding the use of

vendor supplied design. inputs were discussed

in CPLL procedure

numbers

EGR-NGGC-0005

and 0006.

This issue

was also discussed

.

with engineering

personnel

during training.

The inspectors

also

verified during review of the

ESRs listed in paragraph

El above

that unconfirmed information was not used in preparation of design

documents.

This item is closed.

0 en

URI 50-400/96-04-04:

Tracking

FSAR Discrepancy Resolution

(Spent

Fuel

Pool Cooling).

An initial review of the spent fuel pool cooling system

based

on

problems at another facility'resulted in the opening of IFI 50-400/96-

02-04.

This item was later closed

and converted to this unresolved

item

based

on the licensee's

FSAR review program.

The

NRC completed

a

generic licensing review of spent fuel pool safety issues

and by letter

dated July 1,

1996

and September

17,

1996, transmitted the results to

the licensee.

The licensee

responded to the July 1,

1996 letter

on

38

August 8,

1996

and committed to updating the current spent fuel pool

'eat

load analysis,

updating the

FSAR to clarify the terms

abnormal

and

  • normal fuel off-loads,

and revising the

FSAR to reflect the current

installed spent fuel pool configuration.

The inspectors

found that the

FSAR change

(RAF 2295)

was approved

Harch

12,

1997.

The inspectors

reviewed the

FSAR change

and associated

safety

evaluation

(per

10

CFR 50.59)

and found that the commitments

were

completed prior to core off-load.

The heat load analysis

was updated to

reflect the latest calculation.

The

FSAR was clarified to remove the

words "abnormal"

and "normal" off-load, replacing them with "full core

offload shuffle" and "post outage full core offload".

The

FSAR was

revised to reflect the current spent fuel pool cooling configuration and

latest description of equipment,

since the equipment originally

described in the

FSAR that supported the unit 2 spent fuel pools have

not been completely installed.

This item remains

open pending the

licensee's

completion of their overall

FSAR review program.

IV. Plant

Su

rt

Rl

R1.1

Radiological Protection

and Chemistry Controls

Radiolo ical Controls

a.

Ins ection Sco

e

83750

The inspectors

evaluated

radiological controls with emphasis

on external

occupational

exposures

during outage conditions'.

Areas inspected

included contro)s for locked high and very high radiation areas,

radiation area postings,

radiation work permits

(RWPs),

and controls for

radioactive material in accordance

with the requirements of 10

CFR 20.

b.

Observations

and Findin s

The inspectors

made frequent tours of the radiation controlled area

.

(RCA), observed

personnel

compliance with radiation protection

procedures

for high dose work evolutions'nd

conducted interviews with

licensee

personnel

to ascertain

knowledge of radiological controls

and

working conditions.

The inspectors verified controls for external

and

internal

exposures

met applicable regulatory requirements

and were

designed to maintain exposures

as low as reasonably

achievable

(ALARA).

The inspector s reviewed select

RWPs which controlled ongoing outage

work

within the

RCA, including high dose activities within containment,

and

noted that the controls observed

were appropriate

for the described

tasks

and radiological conditions.

During plant walkdowns within the

RCA, the inspectors

conducted

interviews at random with radiation workers both inside

and outside of

containment.

The interviews were conducted with radiation

wor kers of

various disciplines in order to determine the level of understanding

of

RWP requirements

from a representative

cross-section

of plant workers.

39

All of the workers interviewed were verified to have signed onto an

RWP,

were wearing dosimetry appropriate to their work activities

and in

accordance

with their

RWP,

and were performing specific work activities

permitted within the scope of their specific

RWP.

The workers,

by

signing onto an

RWP via the access

control computer, signified that they

understood

the conditions

and requirements of the

RWP being logged onto

in accordance

with Environmental

and Radiation Control

(EIIRC)

procedures.

The questions

asked included the

RWP number of the

RWP

signed onto, dosimetry alarm and cumulative dose limits, available

dose

remaining,

and general

radiological working conditions for the areas

wor ked in.

The workers demonstrated

generally good knowledge of RWP

requirements

and radiological working conditions.

The inspectors

reviewed totaI whole body exposures

for all licensee

radiation

wor kers

and determined that all whole body exposures

assigned

during 1996 and

1997 through the end date of inspection

were within

10 CFR 20 regulator y limits.

A review of licensee

personnel

exposure

records indicated the following maximum individual exposures

at the

plant during 1996 were: Total Effective Dose Equivalent

(TEDE): 795 mrem

and Shallow Dose Equivalent

(SDE):

5660 mrem from a hot particle.

No

internal

exposures

were reported f'r the period.

Through Harch 1997,

the licensee

incurred

a maximum TEDE of 115 mrem with no contamination

events that exceeded

the

SDE threshold requiring

a dose

assessment.

The

inspectors

determined the licensee

had adequately

monitored

and tracked

individual occupational

radiation exposures

in accordance

with 10

CFR

Part

20 requirements

and that all doses

reported

were at

a small

percentage

of applicable regulatory limits.

The inspectors

evaluated

the licensee's

program for controlling access

to high radiation areas

(HRAs) and locked high radiation areas

(LHRAs).

These

areas

were inspected

during tours for proper postings

and access

controls.

No HRAs or LHRAs were identified where required postings

wer e

needed

but not posted.

Areas controlled

as

LHRAs were inspected

and

f'ound locked or otherwise controlled in accordance

with licensee

procedures.

The licensee

had completed

a posting upgrade with respect,

to radiation areas to achieve full compliance with the regulatory intent

of 10

CFR 20.1902.

Key controls for entry into locked high radiation areas

were evaluated

against the requirements of the licensee's

administrative procedure

and

determined to be appropriate.

During a tour of the spent fuel building,

the inspectors

observed

no items hanging from the side of the pool that

were not labelled or properly controlled in accordance

with procedure.

Good radiological controls were observed to be in place in the entire

spent fuel building.

A sample of survey instruments available for

issuance

was inspected

and determined to have current calibration

dates

and be in operable condition.

Radiation workers were observed exiting

the

RCA during peak traffic periods in accordance

with procedures

for

frisking out of the

RCA.

40

Conclusions

The radiological controls

program in general

was being effectively

implemented with good radiation control performance

demonstrated

during

the refueling outage.

Radiation

Work Permit

RWP

Doses

Exceeded

Ins ection Sco

e

83750

The inspector

reviewed circumstances

surrounding

a licensee-identified

RWP dose limit violation that occur red on April 12,

1997.

Observations

and Findin s

During the removal

and replacement of insulation from the chemical

and

volume control system regenerative

heat exchanger

on the 236-foot

elevation of the reactor

containment building,

a Radiation Control

(RC)

Technician

and

an insulation contractor

each

exceeded their RWP-allowed

doses of 400 mrem. This occurred

when both individuals failed to

immediately exit their

wor k area

when their electronic dosimeters

alarmed at the accumulated

dose setpoint of 320 mrem.

Doses received

by

the

RC Technician

and the insulator during the entry were 530 mrem and

495 mrem, respectively.

The individuals indicated in written statements

they did not hear their electronic dosimeters'nitial

alarms

due to

high noise levels in the work area

and only became

aware they had

exceeded their

RWP limits when they came out to undress.

Based

on the inspector 's review of the workers'tatements,

radiation

control oversight

was inadequate

in that the

RC Technician providing

health physics

(HP) job coverage actively participated in the insulation

work in order to expedite job completion

and lost focus

on the primary

assigned

role of radiation control.

Although no administrative or

regulatory dose limits were exceeded

during the incident, the failure of

the workers to promptly exit the work area

when thei r electronic

dosimeters

alarmed is

a violation of Administrative Procedure

AP-535,

Revision 8, Section 5. 16.5,

Performing Work in Radiation Control Areas,

which required workers to immediately leave

a work area

when

an

electronic dosimeter is in alarm.

The licensee

took prompt and thorough

action in response

to the incident to include assigning

a significant

Level

1 Condition Report which will require

an in-depth root cause

analysis,

expedited

completion of required corrective actions,

counselling

and discipline with respect to the workers involved,

and

a

stand.-down

meeting with all site

HP personnel

to increase

emphasis

on

the need for strict compliance with RWP requirements

and safe radiation

worker practices.

This licensee-identified

and corrected violation is

being treated

as

a Non-Cited Violation consistent with Section VII.B.1

of the

NRC Enforcement Policy

(NCY 50-400/97-04-06).

41

Conclusions

R1.3

One Non-Cited Violation was identified for failure of radiation workers

to promptly leave

a work area

when their electronic dosimeters

alarmed.

Inade uate Labelin

of Radioactive Haterial

Ins ection Sco

e

83750

b.

The inspector

performed routine walkdowns inside the

RCA on

April 14-15,

1997, to verify that radioactive material

was tagged

and

labeled in accordance

with licensee

procedures.

Observations

and Findin s

The inspector

identified examples of radioactive material that were not

tagged

and labeled in accordance

with licensee

procedures.

The

inspectors

surveyed miscellaneous

hand tools and scrap metal pieces that

were found in an unmar ked five gallon bucket located in the vicinity of

the bead-blast

unit on the 236-foot elevation of the waste processing

building.

The inspectors identified

a hand chisel with fixed

. contamination levels which required marking per procedure or controlled

as radioactive material

and tagged

(greater than

100 net counts per

minute).

Upon the inspector's

request,

licensee

personnel

frisked the

remaining unmarked/untagged

materials in the bucket

and found additional

items not controlled in accordance

with procedure

HAS-NGGC-0003.

Another example

was identified by the inspectors

on the 291-foot

elevation of the

same building where

a bag of wrapped lead shielding was

not tagged properly as radioactive material.

All of the items

identified were judged to be of minimal safety risk due to the low

radiation levels detected.

. The failure of the licensee to label the radioactive materials with a

-clearly visible label bearing the radiation symbol

and the words

"Caution, Radioactive Haterial" is contrary to licensee

procedure

HPS-

NGGC-0003, Revision 1,

Paragraph

9.2, Tagging

and Labeling of

Radioactive Haterial which requires

each container holding radioactive

material to be so-labeled.

Additionally, in accordance

with the

same

procedure

and paragraph,

hand tools with fixed contamination greater

than

100 net counts per minute are required to be marked with purple or

magenta paint.

Based

on the relatively isolated nature of the items

identified, the licensee's

prompt and thorough corrective actions,

and

the relatively low safety significance of the radiation hazard, this

failure constitutes

a violation of minor significance

and is being

treated

as

a Non-Cited Violation, consistent with Section

IV of the

NRC

Enforcement Policy (NCV 50-400/97-04-07).

Conclusions

One Non-Cited Violation was identified for failing to tag and label

radioactive material in accordance

with procedure.

R1.4

a.

Contamination Controls

Ins ection Sco

e

83750

42

b.

The inspectors

evaluated the licensee's

controls for personnel

contamination

events

(PCEs)

and adequacy of related

PCE followup.

Also

evaluated

was the adequacy of contamination

surveys

and contaminated

area controls.

Observations

and Findin s

The inspectors

reviewed the records of all

PCEs incurred during 1996 and

1997 through the date of inspection.

During 1996, the site incurred 41

PCEs which was well within the licensee's

1996 annual

goal

of. 50 PCEs.

Based

on the history of PCEs at the site, the inspectors

determined that

the original

PCE goal

was aggressive

based

on prior PCE performance.

During 1995 and 1994, periods with outage activity, the licensee

experienced

177 and 226 PCEs,

respectively.

Although the number of PCEs

incurred is

a minor radiation safety concern,

PCEs reflect on the

effectiveness

of a licensee's

contamination control

program and on

radiation work practices.

During an evaluation of 1996 PCEs, the

.inspectors

noted that each contamination event

was evaluated

by the

licensee in accordance

with PCE procedure with corrective actions taken

in each

case,

as appropriate.

Only 5 of the 41

PCEs in 1996 were skin

contaminations

and only 2 of these

contaminations

resulted in a

SDE dose

greater

than the

100

mrem threshold requiring full dose

assessment.

Within the total 41

PCEs in 1996,

18 resulted

from work in designated

clean areas

which is

a high proportion representing

a challenge

area for

the licensee.

The inspectors

reviewed the

PCE evaluations

and noted

no

assessment

or procedural

errors.

The inspectors verified skin dose

assessments

had been performed with conservative

dose

assessment

methodology utilized.

Overall, licensee

actions with respect to

improving personnel

contamination controls were determined to be

effective with no regulatory concerns

noted.

During 1996, the licensee

achieved

a monthly average of 4183 square feet

of recoverable

contaminated floor area which was well within the 1996

goal of 4600 square feet.

This goal represents

approximately

1 percent

of the

RCA area which is relatively low.

The equivalent monthly average

for 1995 was 6362 square feet.

During the first three months of 1997,

the licensee

was able to achieve

a monthly average of 3324 square feet

prior to the RFO-7 outage.

The licensee effectively reduced

contaminated

square

footage by tracking performance

goals for each

building, eliminating contributors to contamination,

and continued

decontamination of recoverable

areas.

Overall, contaminated

areas

were

being maintained to less than one percent of total

RCA square

footage

which represents

good performance in this area.

The inspectors

reviewed

documented

contamination

surveys

performed during the ongoing refueling

outage

and observed

HP technicians

performing contamination

surveys in

accordance

with procedure.

Also, during inspection of the tool issuance

rooms,

good controls for slightly contaminated tools inside the

RCA and

for clean tools outside the

RCA were noted.

43

C.

Conclusions

Rl. 5

Contamination control

was effective overall with surface contamination

controlled adequately

at its source.

The licensee

continued to

effectively reduce

PCEs with adequate

procedural

followup on

contamination events.

Licensee initiatives to reduce

contaminated

square

footage were effective in maintaining contaminated

areas to less

than one percent of the

RCA.

As Low As Reasonabl

Achievable

ALARA

Pro

ram Effectiveness

a.

Ins ection Sco

e

83750

This area

was evaluated to determine

whether the licensee

was

establishing

and tracking ALARA goals

and to evaluate the overall

effectiveness of the ALARA program.

10

CFR 20.1101(b)

requires that the

licensee

use procedures

and engineering controls based

upon sound

radiation protection principles to achieve occupational

doses that are

as low as reasonably

achievable.

Observations

and Findin s

Collective personnel

dose of 17.238 person

rem for

1996 was

a record low

for the site for

a non-outage

year.

During 1997, through the end of

Harch, the licensee

incur red 4.42 person-rem,

which continued the low

dose rate trend during periods of power operations

experienced

during

1996.

Based

on NUREG-0713 data,

the licensee's

dose performance

ranks

among the lowest doses

for single unit

PWR sites.

A relatively large

and unique dose contributor was that which occurred

due to receipt

and

decontamination of Brunswick and Robinson spent fuel shipments.

This

dose accounted for approximately

28 percent of overall site dose during

1996.

Another large non-recurrent

dose contributor during 1996 was

a

material

upgrade

and painting project that resulted in 2.256 person-rem

and represented

a 13 percent

dose contribution. Exclusive'f non-

recurrent

dose,

the licensee's

effective dose rate in person-rem

per

thousand

RWP hours

was exceptionally low and indicative of an effective

ALARA program.

The inspector

reviewed implementation of the

ALARA program with licensee

representatives

and noted that several initiatives to reduce overall

dose were implemented in 1996 and more were underway or planned for

1997.

Dur ing 1996 ALARA initiatives included:

completed loop trainer

for mock-up and scenario training; implemented

advanced

radworker

training; developed list of satellite valves for maintenance

planning;

and initiated

a radiological information tracking system for survey

and

job history records retrieval.

Planned initiatives in 1997 include:

fabricate

a seal

table'mock

up, installed permanent

cavity, seal

ring,

evaluate

increased

use of robotics,

evaluate

permanent

shielding

packages;

and initiate study on use of sub-micron filtration.

Conclusions

The licensee's

ALARA program was effectively controlling collective dose

and collective dose

was on

a favorable reducing trend.

Operational

doses

during 1996,

a non-outage year,

were at record lows for the plant.

Conduct of EP Activities

General

Comments

71750

93702

The inspectors

observed the licensee's

activities for various challenges

that involved the implementation of emergency

preparedness

procedures

during the inspection period.

These

included two RCS boron dilution

events,

a

bomb threat,

and

a small fire in the reactor auxiliary

bu'ilding.

The inspectors

concluded that emergency action level

procedures

were properly implemented

by control

room personnel

during

and following these

occurrences.

Communication between control

room

personnel

and other involved organizations

was adequate.

Licensee

personnel

properly notified the

NRC via the Emergency Notification

System in accordance

with 10

CFR 50.72 for the

bomb threat.

No

Emergency Action Level declarations

were required for the above events.

.No emergency

preparedness

drills were conducted during this period.

Conduct'of Security and Safeguards Activities

General

Comments

71750

93702

The inspectors

observed security and safeguards

activities during the

conduct of tours

and observation of maintenance activities,

and found

them to be good.

Compensatory

measures

were posted

when necessary

and

properly conducted.

Security personnel's

response to a

bomb threat

on

Hay 8,

1997 was adequate.

The bomb threat

was determined to be non-

credible.

Offsite law enforcement

agencies

were notified and

a four-

hour..report

was

made to the

NRC in accordance

with 10

CFR 50.72.

Control of Fire Protection Activities

Gener al

Comments

71750

The inspectors

observed fire protection equipment

and activities during

the conduct of tours

and observation of maintenance activities

and found

them to be acceptable.

Resolution of Thermo-La

Fire Barrier Issue

64704

Ins ection Sco

e

The inspector

reviewed the action taken to resolve the degraded

Thermo-

Lag fire barrier

issue at Harris to determined if the licensee's

action

was consistent with commitments

made to the

NRC.

Observations

and Findin s

45

In 1991, the

NRC identified that Thermo-Lag fire barrier material did

not perform to the manufacturer 's specifications.

NRC Bulletin 92-01'Failure

of Thermo-Lag 330 Fire Bar rier System to Haintain Cabling in

Wide Cable Trays

and Small Conduits

Free from Fire Damage"

was issued

which requested

licensees

with Thermo-Lag fire barriers to consider

these fire barriers to be degr aded

and take appropriate

compensatory

measures

for the areas

where the Thermo-Lag fire barriers

were

installed.

Initially, the plant had approximately 1,800 square feet of Thermo-Lag

fire wall/ceiling configurations.

This also included

a partial height,

one-hour

rated fire wall and protection associated

with fire door

transoms

and mullions.

The fire wall/ceiling configurations

are located

in the Auxiliary Control

Panel

Room and Cable Spreading

Rooms

"A and B".

The fire doors are located

on various elevations in the Reactor

Auxiliary Building (RAB).

The licensee

has evaluated

the results of data from various tests

performed by the nuclear

industry on Thermo-Lag fire barrier

.installations.

In addition, the licensee

has performed three full scale

fire tests of plant Thermo-Lag configurations

independent of industry

fire test programs to document the acceptance

of the tests

against the

as-found condition of the fire barriers.

Also, seismic evaluations

and

testing

has

been completed

on Thermo-Lag configurations.

The partial height,

one-hour fire wall was redesigned

and the Thermo-Lag

material

removed

and replaced with an alternate

gypsum board material.

Engineering evaluations

have

been

completed to address

Thermo-Lag use on

fire door

transoms.

Also, revisions to combustible loading calculations

to reflect Thermo-Lag combustibility and ampacity derating evaluations

have

been completed.

A safe

shutdown methodology re-analysis

was performed to identify the

components

required for plant shutdown following an Appendix

R fire.

The re-analysis

specified the separation to be provided between

safe

shutdown

components to meet the separation

requirements of 10 CFR 50, Appendix R,Section III.G.

This separation

was to be provided by

rerouting several

safe

shutdown cables for source

range instrumentation

and reactor

head vents to eliminate the need for Thermo-Lag protection.

As of the date of this inspection,

the licensee

had initiated the

implementation of corrective actions for Thermo-Lag issues,

except for

the installation of Thermo-Lag sleeve

upgrades

(ESR 95-00715),

corrective actions for a recently identified Thermo-Lag barrier

deficiency

(LER 50-400/97-06 discussed

in report section

F8. 1), safe

shutdown cable rerouting

(ESR 95-00682),

and completion of remaining

engineering evaluations

(ESR 95-00620).

The licensee's

LER 50-400/97-06

stated that the Thermo-Lag issue at Harris would be resolved

by

September

15,

1997.

46

Conclusions

The licensee

has

been proactive in the resolution of the Thermo-Lag

issue at Harris.

Fl.3

Fire Re orts

Ins ection Sco

e

64704

The inspector

reviewed the plant fire incident reports for

1996

and

1997, to assess

maintenance

related or material condition problems with

plant systems

and equipment that initiated fire events.

The inspector

verified that plant fire protection requirements

were met in accordance

with procedure

FP-003,

Fire Investigation Report,

Revision 6,

when fire

related events occurred.

b.

Observations

and Findin s

The fire incident reports indicated that there were two incidents of

fire in 1996,

and three fire events in 1997,

which required fire brigade

response.

No significant fires

had occurred during this period.

There

had been

one minor fire event in the turbine building involving cutting

or welding activities

and one minor electrical fire involving the "A"

battery

room during the current refueling outage (section H2.4).

Only

three of the five fires had occurred within the plant protected

area.

Conclusions

F2

F2.1

Good compliance with plant fire prevention procedures

resulted in a low

incident of fire within the plant protected

area.

Status of Fire Protection Facilities and Equipment

0 erabilit

of Fire Protection Facilities and

E ui ment'4704

a.

Ins ection Sco

e

b.

The inspector

reviewed open Condition Reports

(CRs)

on fire protection

components

and operation's out-of-service logs for fire protection

equipment to assess

the licensee's

performance

for returning degr aded

fire protection components to service.

In addition,

walkdown

inspections

were made to assess

the material condition of the plant's

fire protection systems,

equipment,

and features.

Observations

and Findin s

As of Hay 6,

1997, there were approximately 40 fire protection related

CRs in which the corrective actions

had not been completed.

Host of

these

involved minor

program improvement items

and did not affect the

operability of fire protection components.

All of these

CRs were

initiated in 1997 or late 1996.

The inspector

concluded that there

was

47

no significant corrective action backlog associated

with the fire

protection program or components.

Also,

as of Hay 6,

1997, there were approximately

22 degraded

or

inoperable fire protection

components.

Host of these

items were related

to degraded fire doors

and the refueling outage which was in progress.

For example,

a number of fire barrier penetrations

were open for passage

of temporary cabling for outage activities

and fire detection

was

removed from service

due to maintenance

work being performed.

The remaining degraded

features

were either in nonsafety-related

areas

or were minor discrepancies

which did not affect the operability of the

system or component.

Host of these

items,

which had been degraded

since

late 1996,

were fire doors.

The inspector verified that appropriate

compensatory

measures

had been

implemented for the degraded

components

where required.

Routine general

inspections of plant areas

are conducted

by plant

'perations

personnel

during operations

rounds in accordance

with the

Plant Overview Program

(POP) Generic

Rounds Guidance,

provided in

Attachment

1 to procedure

OHH-016, Operator

Logs, Revision 10.

Guidance

for inspection of fire protection features

and equipment include:

~

Deficiencies in fire wraps,

Thermo-lag,

and penetrations

~

Transient

combustibles

controlled

and documented

per AP-302, Fire

Protection,

Housekeeping,

and Temporary Storage,

Revision

6

~

8ot work in progress

controlled per

FPP-005,

Duties of a

Firewatch,

Revision 12;

and FPP-006,

Control of Ignition Sources-

Hot Work Permits,

Revision

16

~

Trouble or alarm conditions

on local fire detection control panels

~

Fire system controls

and actuation

components in order

~

Oily rag cans

are emptied once per day (Day Shift)

The inspector

toured the

RAB on Hay 6,

1997, with the Senior Support

Analyst in charge of Fire Protection

and

a plant Auxiliary Operator

on

rounds within the

RAB.

The inspector

noted that the operator

performed

a thorough general

inspection of the assigned

areas in accordance

with

the fire protection guidelines provided in POP-6.

Within the areas

toured, the fire detection

and suppression

systems

were well maintained

and the material condition was good.

Conclusions

Based

on the inspector's

review of open Condition Reports

(CRs)

on fire

protection

components

and inspection of the fire protection components,

the inspector

concluded that there

was not

a significant corrective

action maintenance

backlog associated

with the fire protection systems'

48

In addition, the material condition of the fire protection

components

was good.

Surveillance

Procedures

for Fire Protection Stand i e and Hose

S

stem'ns

ection Sco

e

64704

The inspector

assessed

the scope of the licensee's fire protection

surveillance

and tests identified in procedure

FPP.;014,

Fire Protection

- Surveillance

Requirements,

Revision 8, to determine

compliance with

FSAR Section 9.5. 1,

and Technical Specifications

(TS).

Observations

and Findin s

The inspector

reviewed

FSAR Section 9.5. 1.2.3, Fire Protection Standpipe

and Hose System,

which described the functional interface of the

emergency service water

system.and

the fire protection system to provide

post-Safe

Shutdown Earthquake

(SSE)

manual fire protection capability in

areas

required for safe plant shutdown.

Valves included in this

FSAR

section were the seismically qualified check valves

(numbered

3FP-180

and 186;

and 1FP-205,

218.

2079 and 2080) designed to prevent backflow

and outflow to other (non-seismically qualified) portions of the fire

protection water distribution system which may fail during

a seismic

event.

These

check valves were intended to prevent the loss of ESW and

maintain hose line protection after the earthquake.

The inspector

noted

that no surveillance test procedures

existed to verify that the check

valves would perform their intended function.

Technical. Specification 6.8. l.a and Regulatory Guide 1.33, Appendix A.

Section 8.b.l.h,

requi re written procedures

for fire protection

functional tests.

The failure to provide fire protection surveillance

procedures

to verify the functionality of the seismically qualified fire

protection check valves that provide fire protection

and emergency

service water system integrity (following- a SSE) is considered

a

violation of TS 6.8.1.a

(50-400/97-04-08).

Conclusion

A violation of Technical Specification 6.8.1.a

was identified for

failing to establish written procedures

to verify the functionality of

the seismically qualified fire protection check valves that provide fire

protection

and emergency service water

(ESW) system integrity following

an SSE.

This condition had existed since plant commercial operation.

Periodic Surveillance Testin

of Fire Protection Features

and

E ui ment

Ins ection Sco

e

64704

The inspectors

reviewed the following completed surveillance tests:

~

FPT-3560/F,

18 Honth, Fire Wrap Inspection.

Completed

August 13,

1995.

49

~

FPT-3002,

Monthly, Fire Main Valve Position Verification.

Completed April 4, 1997.,

~

FPT-3002,

Monthly, Reactor Auxiliary Building Fire Hose

Rack

Inspection.

Completed

March 27,

1997.

The frequency of selected

sur veillance test procedures

were also

reviewed.

b.

Observations

and Findin s

The surveillance tests

reviewed by the inspectors

had been appropriately

completed

and met the acceptance criteria.

The test procedures,

were

well written and met the fire protection surveillance

requirements of

FPP-014,

Fire Protection Surveillance

Requirements,

Revision 8.

A review of the open scheduled

surveillance tests for 1997, indicated

'that approximately

60 percent of the long-term (either quarter ly, six-

month, annually, or 18-month frequency) fire protection surveillance

test procedures

currently scheduled

had not been completed

and have

been

extended into the allowed grace period.

The inspector

considered

the

number of fire protection surveillances

being performed in their grace

period to be excessive.

This issue

was previously identified as

a

weakness

(Wl) in a licensee fire protection assessment,

Nuclear

Assessment

Section Report H-FP-97-01,

dated February 26,

1997.

Licensee

management

was currently evaluating corrective actions to resol.ve this

issue.

There did not appear to be

a formal program for trending fire protection

condition reports

and performance of fire protection system testing.

However, periodic informal interface

between operations

and engineering

personnel

assigned fire protection related functions

was being made to

coordinate the implementation of the fire protection program.

The

surveillance

procedure test data for the capacity tests

on the fire

pumps

and the diesel fire pump oil analysis

data were reviewed by the

plant system engineer.

This data provided good verification of the

pump's performance.

c.

Conclusions

F3

Implementation of the fire protection surveillance

program

has not been

fully effective.

As previously identified in licensee self assessments,

the number of fire protection surveillance

procedures

being performed

within their grace period continued to be excessive.

Fire Protection Procedures

and Documentation

a.

Ins ection Sco

e

64704

The inspector evaluated the adequacy

and implementation of the

licensee's

Fire Protection

Program described in the

FSAR and in Plant

Operating

Manual Fire Protection

Procedure

FPP-001,

Fire Protection-

I

+j)

l

50

Conduct of Operations,

Revision 16.

In addition,

a comparison

was

made

of the program to selected

NRC Safety Evaluation Reports which approved.

the station fire protection program.

The inspector

reviewed the

following procedures for compliance with the

NRC requirements-and

guidelines:

FPP-001,

Revision 16, Fire Protection

- Conduct of Operations

FPP-002,

Revision 13, Fire Emergency

FPP-003,

Revision 7, Transient

Combustibles

Tracking

FPP-005,

Revision 12, Duties of a Fire Watch

FPP-006,

Revision 16, Control of Ignition Sources

- Hot Work

Permits

FPP-012,

Revision 2, Fire Pre-Plans

FPP-013,

Revision 16, Fire. Protection

- Hinimum Requirements

and

Hitigating Actions

FPP-014,

Revision 8, Fire Protection

- Surveillance

Requirements

FPP-016,

Revision 4, Fire Protection

and First Aid Team Training

ONN-016, Revision 11, Operator

Logs

Plant tours were also performed to assess

procedure

compliance.

Observations

and Findin s

The above procedures

were the principle procedures

issued to implement

the facility's fire protection program.

These procedures

contained the

requirements

for program administration,

controls over combustibles

and

ignition sources, fire brigade organization

and training,

and

operability requirements

for the fire protection systems

and features.

The procedures

were well written and met the licensee's

commitments to

the

NRC, except that

no surveillance test procedures

existed to verify

the functionality of the seismically qualified fire protection check

valves

as discussed

in section

F2.2 of this report.

The pre-fire plans reviewed by the inspector

were found to be

satisfactory

and proper ly addressed

the fire potential,

area location,

means of fire brigade

approach, fire protection equipment available,

fire brigade action, special

instructions

and hazards to be considered,

operational

safe

shutdown considerations,

and communications available.

A general

plant walkdown inspection

was performed by the inspector to

verify acceptable

housekeeping;

compliance with the plant's fire

prevention procedures

such

as

"Hot Work" permits

and transient

combustibles;

operability of'he fire detection

and suppression

systems;

emergency lighting; and installation

and operability of fire barriers,

fire stops,

and penetration

seals

(used

on fire doors,

dampers,

and

electrical penetrations).

Within the areas

observed,

the inspector determined that general

housekeeping

was satisfactory,

considering that the unit was in an

extended

outage

and major

maintenance

and repair activities had been

ongoing.

The majority of storage pallets

used during outage activities

were noncombustible

and constructed of'etal.

Fire retardant plastic

C.

sheeting

and film materials

were also being used.

Lubri'cants

and oils

were properly stored in approved safety containers.

Appropriate

controls for cutting and welding operations

were being enforced.

Controls were being maintained for transient

combustibles

and areas

containing potential lubrication oil and diesel

fuel leaks,

such

as the

diesel

generator

rooms.

No discrepancies

were noted with the outside fire hose

houses, fire main

valves or headers.

However, the inspector

noted two isolated bent

sprinkler

head deflector

plates in the reactor auxiliary building

sprinkler piping.

Operability of the sprinkler system

was not impacted

by the bent deflectors since other overlapping sprinklers installed

'ear by were not affected.

The licensee

issued Deficiency Log Entry No.

97-D01184 to identify the problem and initiate corrective actions.

Corrective actions in this area will be reviewed during future

NRC

inspections.

Conclusions

F5

Except for the large

number of fire protection surveillance test

procedures

being performed in the grace period, the fire protection

program implementing procedures

were good

and met licensee

and

NRC

requirements.

The fire fighting pre-fire plans were satisfactory.

Appropriate fire prevention controls were being applied to refueling

outage activities.

Fire Protection Staff Training and Qualification

a.

Ins ection Sco

e

64704

I,

The inspectors

reviewed the fire brigade organization

and training

program for compliance with the

NRC guidelines

and requirements.

b.

Obser vations

and Findin s

The organization

and training requirements

for the plant fire brigade

were established

by FPP-016,

Revision 4, Fire Protection

and First Aid

Team Training.

The fire brigade for each shift was

composed of a fire

brigade leader

and at least four additional

brigade

members.

As of the

date of this inspection,

there were

a total of 72 trained fire brigade

. members of which 39 were from Operations,

21 from Environmental

and

Radiation Control

(ESRC),

and

11 from Haintenance.

The fire brigade

leader

was

a senior

reactor operator.

The other

member s from Operations

were non-licensed plant operators.

The inspector verified that

sufficient shift personnel

were available to staff each shift's fire

brigade with at least five qualified fire brigade

members.

Each fire brigade

member

was required to receive initial, quarterly

and

annual fire fighting related training and to satisfactorily complete

an

annual

medical evaluation

and certification by a physician for

participation in fire brigade fire fighting activities.

In addition,

each

member

was required to participate in at least two drills per year.

j

I t

52

Due to the unit being in an outage

and the high priority work in

progress,

a fire brigade drill was not.conducted. during this inspection.

c.

Conclusions

F7

The fire brigade organization

and training met the requirements of'he

site procedures.

Quality Assurance in Fire Protection Activities

a.

Ins ection Sco

e

64704

The following audit report

and the plant response to the issues

were

reviewed:

~

Assessment

H-FP-97-01 Harris Annual Fire Protection Assessment,

File No.:

HNAS97-011

~

Response

to Nuclear

Assessment

Section Report H-FP-97-01, File No.

NS-970432

b.

Observations

and Findin s

The licensee's

Nuclear

Assessment

Section

(NAS) performed

a two week

.

assessment

of fire protection

on January

13 through 24,

1997.

The

report for this assessment

(Report

No. H-FP-97-01)

was issued

on

January

29,

1997.

Findings from these

assessments

were categorized

as

strengths,

issues,

or weaknesses.

The inspector

reviewed the final report

and the licensee

response to the

identified issues,

dated February 26,

1997.

The assessment

report

identified two issues

and three weaknesses.

The issues identified by

the

NAS assessment

included problems with fire brigade training and

drill schedules

(Issue Il) and engineering

design controls associated

with a design modification that degraded fire protection in the Waste

Processing

Building (I2).

The weaknesses

identified included

insufficient management

oversight

and self-assessment

of the fire

'rotection

program

(Weakness

Wl); excessive

number of fire protection

surveillance

procedures

being performed in their grace period (Wl);

declining material condition of plant fire doors

(W2); and problems with

various types of emergency lighting (W3).

The weaknesses

identified in

the assessment

wer e in close

agreement

with problems

noted during this

inspection

and licensee identified findings such

as

LERs,

CRs, etc.

Planned corrective actions in response to the two identified issues

were

addressed

in the line organization's

response

and were acceptable.

Action on the three weaknesses

which were identified to enhance

the fire

protection program were not addressed

in the line organization's

response to NAS.

Comprehensive

resolution of the weaknesses

of the

NAS

assessment

should provide significant improvement in the implementation

of .the fire protection program at this facility.

53

c.

Conclusions

The 1997 assessment

of the facility's fire protection program

was

comprehensive

and was effective in identifying fire protection program

performance deficiencies to management.

Planned corrective

actions in

response

to the audit issues

were acceptable.

The weaknesses

identified

in the assessment

were in close

agreement

with problems

noted during

this inspection

and licensee identified findings such

as

LERs,

CRs, etc.

F8

Miscellaneous Fire Protection Issues

(92700)

F8.1

0 en

LER 50-400/97-006-00:

Breach in Reactor Auxiliary Building 3-hour

rated fire barrier (Thermo-lag wall in Cable Spread

Room).

This

LER described

a breach in the Thermo-Lag fire barrier wall which

separ ated the "A" train and "B" train cable spread

rooms within the

Reactor Auxiliary Building.

The breach

was identified during

maintenance activities to resolve

a long-standing

Thermo-Lag issue.

Follow-up investigation revealed

an additional

Thermo-Lag fire barrier

deficiency in a floor drain assembly in the cable spreading

room.

These

breaches

made it possible that

a fire in the cable spreading

room could

adversely affect the "A" and "B" train safety-related

cables.

These

conditions did not comply with the 3-hour fire-rated-barrier

requirement

contained in the Harris

FSAR and were determined to constitute operation

outside the design basis of the plant.

The licensee will resolve the

barrier breach via an on-going penetration

upgrade effort prior to

September

15,

1997.

This

LER will remain open pending the licensee's

completion of the upgrade effort.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on May 15,

1997.

The

licensee

acknowledged the findings presented.

Proprietary information was reviewed during the inspection but is not

contained in this inspection report.

54

PARTIAL LIST OF PERSONS

CONTACTED

Licensee

D. Alexander,

Super visor, Licensing

and Regulatory

Programs

D. Batton, Superintendent,

On-Line Scheduling

D. Braund, Superintendent,

Security

B. Clark, General

Hanager,

Harris Plant

A. Cockerill, Superintendent,

I8C Electrical

Systems

J. Collins, Hanager,

Training

J.

Dobbs,

Hanager,

Outage

and Scheduling

J.

Donahue,

Director Site Operations,

Harris Plant

R. Duncan,

Superintendent,

Hechanical

Systems

W. Gautier,

Hanager,

Haintenance

W. Gurganious,

Superintendent,

Environmental

and Chemistry

H. Hamby, Supervisor,

Regulatory Compliance

H. Hill, Hanager,

Nuclear Assessment

D. HcCarthy, Superintendent,

Outage

Hanagement

B. Heyer,

Hanager,

Operations

K. Neuschaefer,

Superintendent,

Radiation Protection

.W. Peavyhouse,

Superintendent,

Design Control

W. Robinson,

Vice President,-Harris

Plant

G. Rolfson,

Hanager,

Harris Engineering Support Services

D. Shockley, Supervisor,

Configuration Hanager

V. Stephenson,

Hanager,

Rapid Response

T. Walt, Hanager,

Performance

Evaluation

and Regulatory Affairs

NRC

T. Le, Harris Project Hanager,

NRR

H. Shymlock, Chief, Reactor

Projects

Branch 4

V

IP 37550:

IP 37551:

IP 40500:

IP 50002:

IP 57080:

IP 60710:

IP 61726:

IP 62700:

IP 62707:

IP 64704:

IP 71707:

IP 71750:

IP 73753:

IP 83750:

IP 90712:

IP 92700:

IP 92901:

IP 92903:

IP 93702:

55

INSPECTION PROCEDURES

USED

Engineering

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Steam Generators

Nondestructive Ultrasonic Examination Observation

Refueling Activities

Surveillance

Obser vation

Haintenance

Implementation

Haintenance

Observation

Fire Protection

Program

Plant Operations

Plant Support Activities

Inservice Inspection

Occupational

Radiation Exposure Controls

In-Office Review of Written Reports of Nonroutine Events at Power

Reactor Facilities

Onsite Followup of Events

Followup

- Plant Operations

Followup

- Engineering

Onsite

Response to Events

~0ened

50-400/97-04-01

50-400/97-04-02

50-400/97-04-03

50-400/97-04-04

50-400/97-04-05

50-400/97.-04-06

ITEHS OPENED,

CLOSED,

AND DISCUSSED

VIO

Failure to comply with TS 3.0.4 prior to entry into

Hode 6 from defueled condition (Section 01.3).

VIO

Three examples of failure to effectively implement

cor rective actions for previous non-conformances

(Sections 04.1, 04.2,

and 08.1).

NCV

Failure to establish

and implement procedures

for

using appropriate test equipment

on emergency battery

during discharge test

(Section H2.4).

EEI

Inadequate

10

CFR 50.59 safety evaluation for removal

of containment

equipment

hatch missile shields while

in Hode

3 (Section H3.1).

NCV

Failure to implement the design veritication

requirements of 10 CFR 50, Appendix B, Criterion III

for safety-related

configuration changes

(Section

El.l).

NCV

Failure of workers to promptly leave

a work area

when

their electronic dosimeters

alarmed

as required

by

procedure

AP-535, Section 5.16.5 (Section Rl.2).

.50-400/97-04-07

50-400/97-04-08

Closed

56

NCV

Failure to tag and label radioactive material in

accordance

with procedure

HPS-NGGC-0003,

paragraph

9.2, Tagging and Labeling of Radioactive Material

(Section R1.3).

VIO

Failure to provide functional testing for seismically

, qualified check valves in the fire protection system

(Section F2.2).

50-400/96-02-03

URI

Use of potenti al ly unconfirmed information

obtained via telecons

in engineering

design work

(Section E8.1) .

50-400/97-007-00

LER

Inoperable

component cooling water system

- technical specification 3.0.3 entry (Section 08.1).

50-400/97-005-00

LER

Failure to perform core flux mapping following plant

operation with reactor

power greater than

100 percent

(Section

08.2)'iscussed

50-400/96-04-04

URI

Tracking

FSAR discrepancy resolution (Section E8.2).

50-400/97-006-00

LER

Breach in reactor auxiliary building 3-hour

rated fire

bar rier (thermo-lag wall in cable spread

room)

(Section F8.1) .

w) ~,,

t

'