ML18012A378

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Insp Rept 50-400/96-07 on 960721-0831.Violations Noted.Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML18012A378
Person / Time
Site: Harris 
Issue date: 08/31/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A376 List:
References
50-400-96-07, 50-400-96-7, NUDOCS 9610030017
Download: ML18012A378 (31)


See also: IR 05000400/1996007

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

License

No:

50-400

NPF-63

Report

No:

Licensee:

50-400/96-07

Carolina

Power 5 Light (CPSL)

Facility:

Shear on Harris Nuclear

Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates

July 21

- August 31,

1996

Inspectors:

Approved by:

J. Brady, Senior Resident

Inspector

D. Roberts,

Resident

Inspector

M. Miller, Reactor Inspector

(M3.1, M3.2, M8.2)

R. Chou,

Reactor Inspector

(E1.2)

P. Fillion, Reactor Inspector

(E2.1)

G. Wiseman,

Project Engineer (Fl, F2)

M. Shymlock, Chief, Projects

Branch 4

Division of Reactor

Projects

9hi00300i7 960927

PDR

ADQCK 05000400

8

PDR

EXECUTIVE SUMMARY

Shearon Harris Nuclear

Power Plant, Unit 1

NRC Inspection Report 50-400/96-07

This integrated inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident

inspection;

in addition, it includes the results of

announced

inspections

by three regional reactor inspectors

and two regional

project engineers.

Operations

~

The conduct of operations

during the period was adequate

(Section 01.1).

However,

a negative trend in personnel

performance

was noted during this

e

eriod (Section 04.1).

Two examples

were found where Shift Supervisor

ogbooks

were incomplete with respect to status of instrument

channel

oper abilities (Section 02. 1).

~

Self assessment

activities were good (Section 07.1).

Maintenance

Those maintenance activities observed

were conducted well (Section

Ml.1).

An Unresolved

Item was identified in relation to maintenance

rule classification for components listed in the Equipment Data Base

System being inaccurate

(Section M3.2).

Overall, plant equipment

appeared to be in good material condition.

However,

two deficiency tags

were found still hanging for work completed several

years

ago (Section

M2.3).

A failure to follow procedure violation with two examples

was identified

for the performance of surveillance activities:

(1) during service

water valve testing,

and (2) during engineered

safety feature slave

relay testing (Section

M2).

Surveillance

procedures

were appropriately

receiving engineering

reviews (Section

M3. 1).

En ineerin

The licensee's

Generic Letter 96-01 reviews for the containment

spray

actuation circuitry and associated

Technical Specification surveillance

testing

was good (Section E2.1).

Spent fuel cask receiving and unloading procedures

were adequate.

The

crane capacity

had been adequately tested to handle the cask weight.

Measures to prevent the casks

and crane accidentally moving outside the

lift path were in place (Section E1.2)

Engineering support for the SIII instrument

bus inverter repair was good

(Section El. 1) .

~P1

tP

t.

~

Although control

room personnel

were well equipped to perform an offsite

dose

assessment

prior to manning of the emergency

response facilities,

the procedure did contain

some

ambiguous information which demonstrated

that attention to detail

was lacking during the procedure's

development

and validation process

(Section P3).

The general

approach to the control of contamination

and dose for the

site was good (Section R1.1).

The security and safeguards

activities were performed well.

A recent

licensee

audit identified problems pertaining to access

control

(Sections Sl. 1) .

Fire protection activities were acceptable.

Good compliance with plant

fire prevention procedures

has resulted in a low incident of fire within

the plant protected

area

(Section F1.1).

When fire protection systems

are found degraded

or inoperable

a high priority is assigned to promptly

return these

systems to service

(Section F2.1).

The licensee's

program

to maintain the fire protection water supply was completed in accordance

with the licensee's

procedures

and

NRC requirements

(Section F2.2).

Re't Details

Summar

of Plant Status

Unit 1 maintained approximately

100 percent

power for the entire inspection

period.

I. 0

rations

01

01.1

02

02.1

Conduct of Operations

Gener al

Comments

71707

Using Inspection Procedure 71707, the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety-conscious.

Specific events

and

noteworthy observations

are detailed in the sections

below.

Operational

Status of Facilities and Equipment

Review of Shift Lo s

a.

b.

Ins ection Sco

e

71707

The inspectors

reviewed operator logs to verify that activities

including operational

transients,

Technical Specification Limiting

Condition For Operations

(TS

LCO) entries,

and equipment

downtimes were

appropriately documented.

Observations

and Findin s

Control

room shift log entries

between July 23 and 26,

1996 associated

with inoperable safety related instrument channels

were incomplete.

This observation

was specific to the Shift Superintendent

of

Operations'SSO)

logs.

The inspectors

noted that one of the four Refueling Water

Storage

Tank

(RWST) level channels

was documented in the logs as being

out of service

on July 23.

On July 24, the log referenced

that another

channel

was taken out of service

when its power supply was deenergized.

There were

no

SSO log entries reflecting the first channel

being

returned to service prior to the second

channel

being deener gized,

indicating that

a potential

TS

LCO 3.0.3 entry had occurred.

The

inspector s later verified via the reactor

operator 's

(RO) logs that the

first channel

had been restored

nearly four hours before the second

channel

was deenergized.

This noted problem incident occurred prior to

the actual

TS

LCO 3.0.3 entry discussed

in report Section 08.1

A second

example of a log entry problem involved a reference to two

inoperable

steam pressure

channels

which prevented

operators

from

calibrating nuclear instrumentation

on July 26.

All of the

SSO log

entries

up to that point had only mentioned

one specific steam pressure

channel

having failed.

The inspector's

concern

was that the two

inoperable

channels

may have involved a TS violation.

This concern

was

alleviated during further investigation by the inspectors

which

alleviated during further investigation by the inspectors

which

determined that the two channels

were associated

with different steam

generators.

This key information had not been included in the

SSO log

entr y.

Conclusions

,040

P4.1

a.

The inspector

concluded that although the

SSO logbook was incomplete

with respect to status of certain instrument

channel

oper abilities, the

information was either available in the

RO logbook or could be explained

by the operators.

The

SSO log omissions indicated that more attention

to detail

was warranted in logkeeping.

Operator

Knowledge and Performance

Ne ative Trend In Personnel

Performance

Ins ection Sco

e

71707

b.

The inspectors

reviewed condition reports to identify potential

adverse

trends

and the effectiveness

of the licensee's

control in identifying,

resolving,

and preventing problems.

Observations

and Findin s

The inspectors

noted several

examples of personnel

error s in the

oper ations

area during this period.

Sever al of those

were associated

with valves being found out of position.

Others

had to do with improper

control switch manipulations during routine operations

or surveillance

activities.

Another

example involved

a recent revision to an operations

procedure

that resulted in one train of the fuel handling building

ventilation system being inoperable for a short period of time.

Two of the examples,

an

NRC identified failure to follow a surveillance

procedure

and

an inadvertent

Engineered

Safety Features

(ESF) actuation,

are discussed

in report section

H2 as Violation 50-400/96-07-01.

The

other

examples,

all licensee identified, provided further indication

that improvement

was needed.

Personnel

errors

had trended

up during the

second half of 1995,

and error reduction efforts had been

implemented to

help reduce the error rate.

However, the latest trend indicated that

either the techniques

were not being implemented properly or were

currently not effective.

The latest err or s individually had minimum

safety consequences

or effect on the plant, but taken collectively could

be seen

as precursors to a more serious

concern if not corrected.

Licensee

management

was aware of the declining trend and,

by the end

of'he

inspection period,

had initiated a root cause investigation

and

requested

a special

Nuclear Assessment

Section surveillance

assessment

of Operations.

All of the errors noted by the inspector

had been

documented in Condition Reports.

Conclusions

07

07.1

A negative trend in personnel

performance

was noted during this period.

Licensee

management

planned efforts to identify causal

factors

and

corrective actions for this trend.

These efforts were being initiated

near the end of the inspection period.

Ouality Assurance in Operations

Licensee

Self-Assessment

Activities

Ins ection Sco

e

40500

b.

During the inspection period, the inspectors

reviewed multiple licensee

self'-assessment

activities, including:

~

the Plant Nuclear Safety Committee

(PNSC) meeting

on July 25 and

August 2,

1996;

~

Nuclear

Assessment

Section.(NAS) Audit of Engineering

(HNAS96-174)

~

Event Review for Condition Report

(CR) 96-01868,

Resin Spill.

Observations

and Findin s

C.

The inspector

found that the

PNSC discussions

were good and that members

had the proper safety perspective.

However, the inspector

found that

the members

were not well versed

on the

NRC position on TS

LCO 3.0.3,

the use of enforcement discretion,

and TS re'Iief.

The inspector

referred the licensee to current

NRC guidance

on these subjects.

The inspector

found that one of the strengths

in the

NAS audit related

to the plant's surveillance

procedure

review program was not supported

by any technical

review.

NAS acknowledged this problem and later

conducted

a review which verified. that the surveillance

procedure

review

program implementation

was

a strength.

The Event Review identified

a number of personnel

errors

and

communications errors in the waste processing

operations

areas.

The

Event Review was thorough

and corrective actions identified were

appropriate.

Operations

management

was integrating these errors with

others

discussed

in section 04.1 to determine if further,

more generic

corrective actions

were needed.

Conclusions

The

PNSC exhibited the proper safety perspective.

A NAS audit strength

was identified without any supporting review.

The Event Review

performed for CR 96-0186

was good.

Hiscellaneous

Operations

Issues

(92700,

92901)

Closed

LER 50-400/96-012-00:

Technical Specification 3.0.3 entry when

transferring the SIII Instrument

Bus back to the inverter with RWST

Level Transmitter

LT-993 out of service.

This

LER reported the TS

LCO 3.0.3 entry that occurred

on July 25,

1996.

The SIII inverter (Uninterruptible Power Supply for the SIII instrument

bus)

was taken out of service for repair on July 24,

1996 at 9:58 p.m.

Initial problems with the inverter had started

on July 19,

1996 when the

inverter

went into saturation/overload

after the backup

power supply for

rocess

instrumentation

cabinet

(PIC)

9 was returned to service.

The

icensee

performed troubleshooting of the problem over the next four

days

and had discussions

with the vendor before concluding that the

problem was the inverter.

The inspectors

observed the response

to the

initial problem and

a portion of the troubleshooting.

Prior to beginning the work on July 24,

1996 the SIII bus

was

transferred to the alternate

AC power

supply per procedure

OP 156.02,

AC

Electrical Distribution, Revision 10.

TS

LCO 3.8.3.1 action c was

entered

which allowed continued

oper ation in that configuration for 24

hours while the transformer,

choke,

and rectifiers were being replaced.

The inspector

observed

a portion of the repair (see Section Hl.1).

The

inverter

was repaired,

tested,

and was ready to be placed into service

around

noon on July 25,

1996.

RWST level channel

IV had been declared

inoperable at 12:09 a.m.

on

July 25,

1996 due to spiking observed

by control

room personnel.

The

licensee

was replacing the transmitter

and several

instrumentation

cards

in an effort to make the

RWST level channel

IV operable.

To return the

SIII inverter to service

and exit TS

LCO 3.8.3.1,

the SIII instrument

bus must be deenergized

from the alternate

power

source

and then

reenergized

from the SIII inverter.

Because

RWST level channel III was

powered

from the SIII instrument bus,

which would be deenergized

while

performing

OP 156.02 to place the bus

on the SIII inverter, the plant

would have two of four

(channel III and IV) RWST level channels

inoperable

at the

same time resulting in TS

LCO 3.0.3 being applicable.

The licensee

convened the

PNSC to discuss this issue

(Section 07.1).

The decision for the entry was based

on the following facts:

(1) the TS

allows

a second

RWST level transmitter

to be out of service for two

hours'or

surveillance testing;

(2) transfer ring the SIII bus to the

SIII inver ter places the bus on the more reliable power supply;

and (3)

the evolution did not present

an adverse

impact to plant safety.

After

the

PNSC meeting,

the inspectors

observed the licensee

deenergize

the

SIII instrument

bus and reenergize

the bus from the inverter per

OP 156.02.

TS

LCO 3.0.3

was entered for approximately

12 minutes.

The

inspectors

concluded that the licensee decision to place the plant in

the safest configuration was appropriate.

Hl

Conduct of Haintenance

H1.1

Gener al

Comments.

II. Haintenance

a

~

Ins ection Sco

e

62703

The inspector s observed

work performed

on the SIII inverter:

~

WR/JO 96-AEDE1, Replacement of transformer,

choke,

and rectifier

on SIII uninterruptible

power supply.

The inspectors

also observed

various activities associated

with a failed

emergency service water

pump suction valve

(1SW-3) at the Hain Reservoir

intake structure:

~

WR/JO 96-AFLT1, Troubleshoot

(valve) operator to determine

possible

cause of valve not opening;

~

WR/JO 96-AFLT2, Inspect valve to determine

cause of trouble,

includes diver inspection;

and

~

WR/JO 96-AFLT8, (Valve) Stops

found damaged.

Repair/replace

as

needed.

b.

Observations

and Findin s

The inspectors

found the work performed under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced

and knowledgeable of their

assigned

tasks.

The inspectors

frequently

observed

supervisors

and system engineers

monitoring job progress,

and

quality control personnel

were present

whenever

required by procedure.

Heasurement

and test equipment

used were within their calibration

frequency.

The

1SW-3 valve disk is attached to

a shaft which is between

60 and 70

feet long and is submerged

under

roughly 40 feet of water.

Working on

the valve required efficient planning,

an adequate

clearance

boundary,

and good workmanship by the many parties involved.

The inspectors

verified that clearances

were in place, that good safety practices

were

used

by the divers and other workers,

and that TS

LCO requirements

were

met.

All work was properly documented.

c.

Conclusions

The maintenance activities observed

by the inspectors

were conducted

well.

H2

H2.1

Haintenance

and Haterial Condition of Facilities and Equipment

Surveillance Observation

Ins ection

Sco

e

61726

The inspectors

observed all or portions of the following surveillance

tests:

~

HST-I0145,

Steam Generator

A Narrow Range

Level

Loop (L-0476)

Operational

Test,

Revision 4

~

HST-E0010,

1E Battery Weekly Test,

Revision

6

~

OST-1214,

Emergency Service Water System Operability Train A,

Revision

7

~

HST-I0148,

Steam Generator

B Narrow Range

(L-0486), Revision 4

~

HST- I0148,

Steam Generator

A Narrow Range

(L-0476), Revision 4

Observations

and Findin s

Licensee

personnel

performed portions of procedure

OST-1214 to satisfy

post-maintenance

testing requirements for work conducted

on the "A"

scr eenwash

pump and on valve

1SW-3 (report Section Hl.1).

Section 7.7

of the procedure directed personnel

to install

a differential pressure

(d/p) gauge indicating from 0-100 inches water column

(INWC) on the

suction line of the screenwash

pump.

Operators

would use this gauge

while setting

up flow for the pump.

Other gauges

(indicating from 0-200

pounds

per square

inch gauge (psig) were intended to determine

pump

differential pressure

and were installed

on the

pump suction

and

discharge lines.

The inspector verified that the gauges

were installed

properly and were within calibration

frequencies.

Step 7.7. 17 of the procedure directed the operator to obtain

a pump

flowrate between

31-33

INWC (150-155 gallons per minute (gpm)) on the

installed d/p gauge

by throttling pump discharge isolation valve 1SC-23.

Because

the operator

was stationed at the valve and the instrument

gauges

were several

feet

away and out of immediate view,

a maintenance

technician assisted

in providing gauge readings.

The operator

erroneously directed the technician to monitor the 0-200 psig discharge

pressure

gauge instead of the 0-100

INWC d/p gauge while setting

up

flow.

The operator throttled discharge

valve 1SC-23 almost completely

shut while attempting to obtain

a reading of between

150 and

155 psig on

the discharge

pressure

gauge,

which was initially reading

130 psig.

The

inspector questioned

the operator's

actions

as it appeared

that the

pump

was operating with very little flow.

The operator

and another

technician placed their

hands

on the discharge

pipe and indicated that

flow was still available.

They continued throttling the valve until the

discharge

pressure

gauge indicated

150 psig.

Moments later, the inspector

observed that the d/p gauge installed

on

the suction line was reading

0

INWC (0 GPM).

The inspector

indicated to

the test personnel

that the d/p gauge

on the suction line was the gauge

they were supposed to be monitoring.

Realizing this, the operator

opened the discharge

valve to restore flow indication.

The pump later

failed the surveillance test after only delivering 29-30

GPM.

The

inspector

had noted that the d/p gauge

was indicating approximately

35

gpm before the error occur red.

It was determined that an impeller

clearance

adjustment

was necessary

for the

pump to meet the flow

requirements.

After the adjustment

was completed,

the

pump was retested

and satisfied the flow acceptance criteria.

Technical Specification 6.8. l.a requires that written procedures

shall

be established,

implemented,

and maintained covering the activities

referenced

in Appendix A of Regulatory Guide 1.33, which includes

surveillance tests for service water systems.

Using the incorrect

gauge

while setting

up flow requirements

on the "A" emergency service water

(ESW) screenwash

pump constituted

a failure to follow procedure

OST-1214

and is

a violation of TS 6,8.l.a (50-400/96-07-01).

This violation is of regulatory concern

because it resulted in operating

the safety related

screenwash

pump under

conditions

(minimum to no flow)

for which it was not'intended.

The error

created

delays

and extended

out-of-service time for the

ESW system.

Additionally, this was one of

several

operator

errors during the inspection period, indicating

a need

for increased

management

attention in this area.

The licensee initiated

Condition Report 96-02155 to document this item.

Conclusions

The inspector identified

a violation of'S 6.8. 1.a during the

performance of OST-1214.

This example,

along with several

others during

the inspection period, indicated

a need for increased

management

attention in the area of human performance.

Inadvertent

ESF Actuation Durin

Slave Rela

Testin

Ins ection Sco

e

61726

The inspectors

reviewed the circumstances

surrounding

an inadvertent

engineered

safety features

actuation during slave relay testing.

In

addition to gaining an understanding of the incident, the inspectors

verified that the event

was properly reported to the

NRC and that the

licensee

performed

a root cause determination.

Observations

and Findin s

On August 12,

1996,

NRC-licensed operators

were performing OST-1045,

ESFAS Train B Slave Relay Test, quarterly Interval, Revision 9.

Section

7.20 tested the go-circuit relay for containment ventilation isolation.

Step 7.20.5 directed the operator to turn test switch S938 clockwise and

momentarily depress it.

The switch is located in protection system

safeguards

test train

B cabinet

number

2.

Depressing

the switch was

expected to cause certain

dampers

and

a fan in the containment

ventilation system to isolate and/or

shut off.

During the test,

the

operator accidentally turned

and depressed

switch S931 instead,

which

was associated

with the main steam line isolation signal.

As

a result,

three main steam line drain-before-seat

isolation valves shut.

No other

main steam line valves were affected.

The incident was determined to

constitute

an inadvertent

ESF actuation

and was properly reported to the

NRC in accordance

with 10 CFR 50.72(b)(2)(ii).

According to statements

in the Condition Report

and discussions

with

licensee

personnel,

the operator initially identified the correct switch

to be manipulated,

momentarily removed his hand from that switch, then

accidentally placed his hand on the S931 switch, located directly above

the S938 test switch, without properly self-checking it.

Licensee

management

has recently conducted training on human error reduction

techniques

following a series of errors that occurred during the fall of

1995.

However, this er ror indicated that those techniques

were not

adequately

employed during this surveillance activity.

The error had no adverse

impact on plant operations

as it only affected

the three drain-before-seat

valves.

However, given different operating

circumstances

and the'otential

impact of other equipment operated

by

switches in these test cabinets, this type of error during slave relay

testing could easily have caused

a more complicated plant transient.

TS 6.8. l.a and Regulatory Guide 1.33 collectively require that written

procedures

for surveillance tests

be established,

implemented,

and

maintained.

Hanipulating the wrong switch during the August 6 test

constituted

a failure to follow procedure

OST-1045

and is the second

example of Violation 50-400/96-07-01

discussed

in section

H2. 1 above.

Conclusions

The inadvertent

ESF actuation,

along with .other

personnel

errors

.

discussed

in report section 04.1 above, all demonstrated

a need for more

management

attention in the area of human performance

during routine

tasks.

Haterial Condition of Facilities

and

E ui ment

Ins ection Sco

e

61726

The inspector s performed walkdowns to ver ify that equipment

was in good

mater ial condition and that deficiencies

were identified and

appropriately corrected.

Observations

and Findin s

The inspector

observed

some nearly four -year-old deficiency tags

on two

valves.

These were associated

with an incorrectly installed leakoff

valve for the "A" charging/safety injection pump (CSIP) suction valve,

and

a leaking containment isolation valve in the demineralized

water

system.

The inspector

asked licensee

personnel

to check the status of

the associated

work tickets.

Both of the deficiencies

had been

corrected

two or

more year s earlier, yet the tags were still hanging

on

the components.

This indicated that personnel

closing the maintenance

work orders

were not necessarily

removing deficiency tags

upon

completion of work.

This also indicated that people

who routinely tour

plant areas

were not always attentive to old deficiency tags.

To assist

maintenance

personnel

in this area,

Operations

issued

a Night Order to

operators

reminding them to be more attentive to old tags during plant

walkdowns.

Conclusions

H3

H3.1

Overall, plant equipment

appeared

to be in good material condition.

However, the above two examples

indicated that more attention

was

warranted in the area of removing deficiency tags

from components

upon

successful

completion of work.

Haintenance

Procedures

and Documentation

Surveillance

Procedures

Ins ection Sco

e

61726

The inspectors

reviewed samples of documentation,

including the

"Procedure

Review Forms"

and "Procedure

Change

Forms" to determine if

engineering

personnel

were performing reviews of surveillance

procedures

and revisions to procedures

in accordance

with administrative site

requirements.

In addition, the inspectors

reviewed Plant Operating

Hanual, Administrative Procedures;

AP-100, Revision 5, Procedure

Use and

Adherence;

AP-005, Revision 10, Procedure Writing Guide;

and Plant

Programs

Procedure,

PLP-100,

Revision 7, Conduct of Infrequently

Performed Tests or Evolutions to identify the site requirements.

Observations

and Findin s

The inspectors verified that the electrical

engineering section

satisfactorily reviewed procedures

1) HST-E-0012,

Revision 5,

1E Battery

18 Honth Test;

2) HST-E-0027,

Revision 5,

1E Battery Service Test;

and

3) PH-E-0014,

Revision 5,

Non Class

lE Battery Connections

and

Haintenance

Resistance

Checks.

The inspector

verified that the instrumentation

and control section

appropriately reviewed procedures

1) HST-I-0001, Revision 8, Train A

Solid State Protection

System Actuation Logic and Haster Relay Test;

2)

OST-1845T,

Revision 0, Safety Injection Actuation Switch test;

3)

OST-

9016T,

Temporary Procedure

For Containment

Spray System

Hanual Actuation

Switch Operability Verification; 4) OST-9018T,

Temporary Procedure to

Test A Train Sequencing

Blocking Functions;

and OST-1094,

Revision 0,

Sequence

Block Circuit and Containment

Cooler Testing Train A.

10

c.

Conclusions

The Engineering

Department

was performing adequate

reviews of

surveillance

procedures

and revisions to procedures.

H3.2

Condition Re orts

62700

a.

Ins ection Sco

e

The inspectors

examined

two condition reports

(CR) concerning

maintenance

items to determine if requirements

in the Plant Operating

Hanual Administrative Procedure,

AP-615, Revision 18, Condition

Reporting

and ADH-NGGC-0101, Revision 3, Haintenance

Rule Program

were

being addressed.

b.

Observations

and Findin s

1)

CR No. 96-02021

- "Haintenance

Plan for

1CS-559"

On July 28,

1996, Boric Acid Filter Inlet Valve 1CS-559 failed to

stroke closed during the per formance of surveillance test

OST-

1093,

CVCS/SI System

Oper ability Train

B Quarterly Interval,

Rev.

3.

The concerns listed in the

CR were:

(1) there

was

no clear

written trouble shooting plan;

(2) the practice of stroking the

valve prior to timing appeared to violate guidelines for

"preconditioning" valves prior to stroke timing; and (3) the

problem was repetitive.

The inspector investigated

the repetitive portion in relation to

the maintenance

rule,

10 CFR 50.65.

Procedure

ADH-NGGC-0101,

Haintenance

Rule Program,

Revision 3, provides maintenance

rule

implementation instructions.

It also contains

a listing of the

systems that are scoped within the maintenance

rule in Attachment

1.

When the inspectors

requested

the maintenance

rule

classification for the valve, it was listed in the Equipment

Data

Base

System

(EDBS) as Haintenance

Rule

-

No (N).

The valve is

part of the emergency boration flow path in the chemical

and

volume control system.

Because

1CS-559 could affect reactivity

control, the inspectors

concluded that the

EDBS was inaccurate

for

its maintenance

rule classification.

The licensee

showed the

inspectors

where this inaccuracy

was already

known; however,

a

condition report was not written and the problem was not corrected

when the inspectors

found it.

The

EDBS has

been

used by the licensee

as

a centralized

means of

identifying and storing plant component information so that it is

easily and conveniently retrievable.

The licensee informally

decided to use this existing data

base to implement the expert

panel

maintenance

rule scoping determinations.

The expert panel

scoping determination

was accurate in identifying the bor ation

flowpath (which includes

1CS-559)

as

a maintenance

rule function.

However, the valve had been identified in the wrong system (filter

backwash)

when the

EDBS was originally created.

The filter

backwash

system

had been determined

by the expert panel

not to

have

a maintenance

rule function and all of its components

were

classified in the

EDBS as Maintenance

Rule

- .N.

The erroneous

classification of 1CS-559 in the

EDBS,

and other errors discovered

later

by the licensee,

indicated that the licensee

had not done

an

adequate quality check of the

EDBS prior to implementation of the

maintenance

rule.

When the inspectors

expressed

concerns

about the accuracy of the

EDBS,'icensee

personnel

wrote Condition Report 96-2175 for valve

1CS-559

and initiated

a further review.

This review found

numerous other examples of components with maintenance

rule

functions that were listed in non-maintenance

rule systems

in the

EDBS ~

A discrepancy with a nitrogen system valve, identified by the

licensee in early July 1996,

had prompted

a similar review which

provided ample opportunity to identify the larger problem.

This

review performed in July 1996,

found none of the examples that

were found during the later

review prompted by the inspectors.

The inspector s concluded that the licensee's

handling of the

previously identified discrepancies

in maintenance

rule

implementation

was poor.

Procedure

AOM-NGGC-0101, Maintenance

Rule Program,

Revision 3,

implements

10 CFR 50.65

and provides maintenance

rule

implementation instructions.

Section 9.3.1,

under

scoping,

directed personnel

to obtain systems lists from the

EDBS and

supply to the Expert Panel for evaluation.

The inspector

found

that the

EOBS was being used to implement the expert panel

system

determinations

on a component level

and was being used

as the

primary tool to implement the maintenance

rule on

a daily basis.

Maintenance rule decisions

were being

made

on the assumption that

the

EDBS was accurate.

As a result of the

EDBS inaccuracies,

the

inspectors

were concerned that maintenance

rule decisions

could be

adversely

impacted.

The licensee

was in the process of correcting

the

EDBS problems

and assessing

the impact of these errors

on

previous maintenance

rule implementation decisions at the end of

the inspection.

Procedure

AP-615, Condition Reporting,

Revision

19 defines

adverse

conditions

as nonconformances

in items or activity which has

affected or could affect nuclear safety

or quality, or compliance

with other regulations

not included in nuclear safety or quality

above.

These conditions are to be reported

on

a condition report.

The licensee

had not initiated

a condition report for the

EDBS

maintenance

rule problems until their significance

was identified

by the inspectors.

12

This issue is identified as Unresolved

Item (URI) 50-400/96-07-02,

Corrective Actions for Maintenance

Rule Implementation

Problems,

pending

NRC review of the licensee

impact assessment.

2)

CR No. 96-01811

- "E-17 Failed to Start"

On July 7,

1996, after the completion of OST-1032

RAB Emergency

Exhaust

System Train A Operability Honthly Interval,

Rev.

6, test

personnel

attempted to restart

fan E-17.

It did not start.

The

breaker

was racked out, cycled in the "test" position,

and racked

back in.

The breaker

closed

and the fan started.

The inspectors

were concerned that the practice of racking the

breaker out and cycling it in test after it failed to operate

would not be tracked

as

a component failure in the Maintenance

Rule Program.

During this event,

the Maintenance

Rule was not in

effect and E-17 was not Class

1E.

However,

E-17 is classified

as

a Maintenance

Rule Component.

The inspectors

discussed this

concern with licensee

personnel

who issued

an Operations

Night

Order reminding operators of the need to implement formal

troubleshooting

procedures

following such failures.

c.

Conclusions

The inspectors identified that the

EDBS needs to be updated

for the

Haintenance

Rule Classification.

In addition,

when components fail to

operate,

the problem needs to be addressed

for root cause prior to

cycling in test or returning it to service.

H8

Miscellaneous

Maintenance

Issues

(92700,

92902)

M8. 1

0 en

LER 50-400/94-001-00:

Technical Specification surveil'lance

violation due to inadequate

procedure.

This event report

was issued to

report that the slave relay test for relay K623 did not verify actuation

of the reactor coolant drain tank pump discharge

valve (lED-121).

The

event

was caused

by a deficiency in procedure

OST-1044,

ESFAS Train A

Slave Relay Test.

The inspector verified that the procedure

had been

changed to include this valve on Hay 26,

1994 for Revision 4,

Change

5.

The inspector

confirmed that the current revision (7) also contained

this item.

The inspector

was also

aware that

LER 95-07 contained

corrective action that included

a comprehensive

surveillance

program

review which was still ongoing and addressed

Generic Letter 96-01,

Testing of Safety-Related

Logic Circuits.

Th'ose reviews

have generated

33 reportable

items.

This item will be reviewed collectively with the

associated

LERs for overall program adequacy.

M8.2

0 en

LER 50-400/96-008:

Reactor trip due to failure of an output

breaker disconnect

device.

The licensee's

April 25,

1996,

planned

corrective action for maintenance/engineering

items was examined to

determine its adequacy for the event.

Some of the corrective action

items were as follows:

13

1)

Investigation

and testing of the under -voltage relay momentary

contact closure

and false under-voltage signal.

Action Item 96H0228 was completed

June 27,

1996.

The testing

identified the problem as premature contact

bounce

from the one-

second timer.

The timer was mounted

on the front panel of the

cubicle and was subject to vibrations from 6.9kV breakers

operating.

The licensee

was investigating

means to suppress

the

vibrations.

Installation was planned for the next refueling

outage.

2)

Additional testing to duplicate the

86DG lockout relay trip in the

A EDG control circuity is planned.

Action Item 96H0198 was completed

June

14,

1996.

The testing of

an identical

spare relay did not provide conclusive evidence

on

the exact cause or that the

86DG relay tripped due to a spurious

voltage transient.

However, there is no safety concern since the

86DG relay will not inhibit a valid EDG start.

3)

The plant system engineer will become

more intrusive in

coordinating switchyar d activities including predictive

and

preventive maintenance.

Scope of switchyar d work will be

established

and integrated into refueling outage schedule.

This item was not completed.

However, the system engineer

,

provided test results

from the June ll, 1996,

thermography testing

(infrared heat) of the disconnect

switches.

The temperature for

the disconnect

switches

was within tolerance.

The licensee

was implementing appropriate corrective action in a timely

manner

.

The

LER wi')1 remain open pending completion of all corrective

actions.

III. En ineerin

E1

Conduct of Engineering

El. 1

SI II Invertor

a.

Ins ection Sco

e

37551

The inspectors

observed the engineering

support for the SIII invertor

events

b.

Observations

and Findin s

Engineering

personnel

were heavily involved with the SIII inverter

problem discussed

in 08.1

and H1.1.

The SIII invertor was noisy prior

to this event

and was being trended

by engineer ing personnel.

The

licensee

was planning on refurbishing the inverter at the next outage.

Parts

were available if the need to refurbish earlier was necessary.

14

Engineering discussed

the inverter saturation

problem with the vendor

and concluded the problem was the inverter, not the instrumentation

power supplies

which passed

bench tests.

The problem parts were

narrowed to the transformer,

choke,

and rectifiers (parts

on site).

The

repair resulted in the inverter noise level being significantly reduced

and invertor performance

being returned to normal.

c.

Conclusions

The inspector

concluded that engineering

support for this issue

was

good.

E1.2

Review of S ent Fuel

Cask Receivin

a.

Ins ection Sco

e

37700

The inspectors

reviewed the adequacy of the spent fuel cask receiving

and crane operation procedures;

verified through record review that the

crane received

proper testing during the original construction

and was

qualified to liftthe cask;

and walked down the spent fuel pool area to

examine the cask receiving area

and the crane to be used to liftthe

casks.

The inspectors

reviewed the codes

and standards

that were

referenced

in the licensee's

crane

oper ation procedures.

The procedures

reviewed are listed below:

Procedure

No.

Rev.

No.

Procedure Title

CH-H0300

HMM-020

PH-H0074

HST-M0040

15

10

Spent

Fuel

Cask Handling

(IF-300 Cask)

Oper ation, Testing,

Maintenance,

and Inspection of

Cranes

and Special Lifting

Equipment

Equipment

Lube Oil Sampling

Cask Handling Crane Interlocks

and Physical

stops Weekly

Interval During Crane

Operations

The spent fuel pool facility contains

a 150-ton crane which handles

receiving

and unloading of casks transported

by rail cars

from the other

CPEL sites.

The crane

vendor test procedure

and manual

were reviewed

and listed below:

15

Document

No.

Rev.

No.

Title

b.

Proc.

1-8200-P-01

Hanual

LXZ

Observations

and Findin s

Spent

Fuel

Cask Handling Crane

Preoperational

Test

Operating

and Haintenance

Hanual for Fuel Handling

Building Cask Crane

150 Tons

Capacity

C.

The inspectors

reviewed the procedures

for receiving and unloading of

the spent fuel casks.

Procedure

HHH-020 contains the crane safe load

paths,

heavy load item listing for each crane,

and inspection

check

lists for all the cranes in the plant.

Procedure

CH-H0300 contains the

detailed operation for receiving

and unloading the cask including the

removal of the assemblies

from the received

cask.

Procedure

HST-H0040

contains

measures

to prevent the cask handling crane

from moving heavy

loads over the spent fuel pool.

The cask is lifted from the rail car to

a decontamination pit, then lifted over

a cask closure

head storage pit

to the unloading pool.

The 150-ton crane is restricted in its load path

by Procedure

HST-H0040 to prevent the crane

from moving over spent fuel

pool

D, which is in the vicinity of the unloading pool.

The inspector s toured the spent fuel pool area

and reviewed the

potential operational

risks associated

with lifting of casks

from rail

car s to the unloading pool.

A steel barrier is installed to prevent the

cask, if dropped,

from rolling or falling into spent fuel pool

D.

The inspectors

reviewed the crane test records which showed the cask

crane hoist load block was tested to 186.5 tons,

which is 125 percent of

the 150 ton lifting capacity per the requirements of ANSI B30.2 Code.

The test

manual

allowed

a +5/-5 ton margin from 187.5 tons.

Conclusions

E2

E2.1

The licensee

procedures

and test data for the spent fuel cask crane were

adequate

and could be safely used for moving the casks.

Engineering Support of Facilities and Equipment

Testin of'afet -Related

Lo ic Circuits

a.

Ins ection Sco

e

37550

Pursuant to Generic Letter 96-01, Testing of Safety-Related

Logic

Circuits, the licensee

has

been in the process of reviewing logic

circuits

and associated

TS test procedures.

The purpose of the review

was to determine

whether there were functions or features of the logic

circuits that had not been tested

by periodic sur veillances.

The

licensee's

status report for this project indicated that the project was

16

C.

95 percent

complete.

During the course of the project, the licensee

had

identified functions and featur es of the safety related logic circuits

that had not been tested.

When this occurred,

the procedure

was

revised,

and the circuit was tested

using the

new procedure within the

required time frame.

These

problems

and corrective actions were

described in LER 96-02 which has multiple supplements.

The inspectors

performed

a detailed review of the circuitry for

containment

spray actuation

and the associated

Technical Specification

surveillance

procedures.

The inspectors

also reviewed the licensee's

documentation

which had been generated

by their Generic Letter 96-01

program for this circuit.

Observations

and Findin s

The inspectors

noted that the licensee's

review of the containment

spray

actuation circuit y identified several

cases

where features

or functions

had not been tested

by the TS surveillance

program.

For each of the

problems,

a Condition Report was generated

to develop the appropriate

corrective action

and track its implementation.

The inspector

did not

identify any problems with the test procedures

for the containment

spray

actuation circuitry above

and beyond those already identified by the

licensee.

Based

on his independent

review and review of the Condition

Reports,

the inspector

concluded that the licensee's

methodology

and

level of detail for the review was good.

The inspector

also noted that

the documentation of the review process

and results

was good.

The

documentation

included

a tabulation of each circuit function and feature

together with an assessment

of whether they had been tested

as well as

any problems identified.

Conclusions

The inspector

concluded that the licensee's

methodology,

level of detail

for the review,

and documentation of the review process

and results

were

good.

E7

Quality Assur ance in Engineering Activities

E7.1

S ecial

FSAR Review

37551

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for

a special

focused

review that compares

plant

practices,

procedures

and/or parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

The inspector s verified that the

FSAR wording was consistent

with the observed plant practices,

procedures

and/or parameters.

17

IV. Plant

Su

rt

R1.1

Radiological Protection

and Chemistry

(RP8C) Controls

General

Comments

71750

P3

The inspector

observed radiological controls during the conduct of tours

and observation of maintenance activities and found them to be

acceptable.

The general

approach to the control of contamination

and

dose for the site was good.

EP Procedures

and Documentation

a.

Ins ection Sco

e

71750

b.

The inspector

conducted

a brief review of control

room procedures

and

interviewed shift operators

to assess

the control

room staff's readiness

to perform offsite dose calculations during potential

events

when the

Technical

Support Center

(TSC)

and Emergency Operations

Facility (EOF)

had not yet been

manned.

Observations

and Findin s

The inspectors

found that

a procedure

was in place,

PEP-340,

Revision 2,

Radiological

Assessment.

This procedure

was located at the Emergency

Communicators

desk in the main control

room.

It referenced all of the

important radiological effluent monitors necessary

to make offsite dose

calculations.

The inspector later interviewed operators

(on two shifts)

who were able to quickly reference the procedure

and direct the

inspector to the computer where the dose calculations

would be

performed.

Procedure

PEP-340 contained

a table in Step 2.0.1 listing those

radiation monitors whose alarming status

would be an initiating

condition for performing an offsite dose

assessment.

The table listed

the accuracy

ranges

for each of the monitors

as

a reminder for operators

to disregard

readings outside of the ranges.

For three of the vent

stack effluent monitors, the accuracy

ranges

were listed in units of

concentration

(microcuries per milliliter).

To verify oper ability, the

inspector

asked operators

to access

the specific effluent monitors on

the control

room radiation monitor panel.

The effluent monitors

indicated in flowrate units of micro-curies per second,

The inspector

asked operators

about this discrepancy

and whether

a calculation

was

necessary

to convert to the concentration units listed in the procedure

table.

Operators

were not sure of the answer

and contacted

the

emergency

preparedness

staff who had originally developed the procedure.

Emergency

preparedness

personnel

later explained to the residents that

vent stack

gas detection

channel

outputs (in units of concentration)

are

usually coupled with flowrates established

by isokinetic sampling skids

in determining overall radioactive effluent flowrates,

as indicated by

the effluent monitor s.

The vent stack effluent monitors

and their

18

S1

S1.1

corres'ponding

gas detection

channels

have similar

noun names.

Since the

table listed the effluent monitors which indicate in units of flowrate,

specifying their ranges

in units of concentration

added

a confusion

factor in the procedure.

The similarity in noun

names

between the

effluent and gas monitors contributed to this procedural

oversight.

Based

on their discussions

with operators,

emergency

preparedness

personnel

were convinced that the ambiguity would not impede the offsite

dose calculation process,

but acknowledged that the procedure

should be

revised.

Subsequent

to the inspection period, Revision

3 was issued

which deleted the reference to accuracy

ranges in the table of Step

2.0. 1 and relocated this information (in microcuries

per

second) to that

point in the procedure

where operators

would be performing the

calculations.

Conclusions

Control

room personnel

were well equipped to perform an offsite dose

assessment

in the event the TSC and

EOF were not yet manned during

a

potential

event.

However,

ambiguous

information in a table in the

offsite dose calculation procedure

demonstrated

that attention to detail

was lacking during the procedure's

development

and validation process.

Conduct of Security and Safeguards Activities

Gener al

Comments

71750

S7

S7.1

The inspector

observed

security and safeguards

activities during the

conduct of tours, observation of maintenance activities,

and the

emergency

preparedness drill, and found them to be good.

Compensatory

measures

were posted

when necessary

and proper ly conducted.

Quality Assurance in Security and Safeguards Activities

Licensee

Self-Assessment

Activities

General

Comments

40500

During the inspection period, the inspectors

reviewed Performance

Evaluation Section Audit PES96-033,

Access Authorization and Fitness

for Duty Programs

Assessment.

This corporate audit identified problems

pertaining to access

control which is the subject of NRC Inspection

Procedure

TI 2515/127.

F1

Control of Fire Protection Activities

Fl. 1

Gener al

Comments

64704

71750

During maintenance activities the inspector

observed that fire

protection equipment

was readily accessible.

Recently,

the licensee

formed

a new Fire Protection

Issues

Review Team

to review the plant fire protection program implementation.

The

19

F1.2

inspectors

received

a good briefing on the teams task and the action

items they were reviewing.

Fire Re orts

Ins ection

Sco

e

64704

The inspector

reviewed the plant fire incident reports for 1995 and

1996, to assess

maintenance

related

or material condition problems with

fire protection systems

and equipment.

The inspector verified that

plant fire protection requirements

were met in accordance

with procedure

FPP-013,

Fire Protection,

Revision 16,

when the equipment

was declared

out of service.

Observations

and Findin s

Three fires had occur red during the last two year period,

two in 1996

and one in 1995.

However, these

were not significant fires.

Only one

of these fires had occurred within the plant protected

area.

This fire

was caused

by a minor organic chemical spill in a laboratory. It was

immediately extinguished

by plant personnel.

Conclusions

F2

F2.1

Good compliance with plant fire prevention procedures

has resulted in a

low incident of fire within the plant protected

area.

Status of Fire Protection Facilities and Equipment

Fire Protection

Records of Haintenance

a.

Ins ection Sco

e

64704

The inspectors

reviewed fire protection out-of-service logs from Harch

1996 to the present to assess

maintenance-related

or material condition

problems with fire protection systems

and equipment.

The inspector

verified that plant fire protection requirements

were met in accordance

with procedure

FPP-013,

Fire Protection,

Revision 16,

when the equipment

was declared

out of service.

b.

Observations

and Findin s

The fire protection out-of-service logs indicated that

a small

number

(49) of impairments for repairs

were recorded f'r the six month period.

With the exception of the diesel-driven fire pump, these repair

impairments

had been restored to service within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

A small

backlog of work orders

remained for scheduled

completion.

Host of these

repair

impairments involved fire doors:

20

Conclusions

When fire protection systems

are found degraded

or inoperable

a high

priority is assigned to promptly return these

systems to ser vice.

A

small

number of impairments for repairs

were recorded

for the most

recent six month period.

With the exception of the diesel-driven fire

pump, these

repair

impairments

had been restored to service in a timely

manner.

Review of Ino erable Diesel-driven Fire

Pum

Ins ection Sco

e

64704

The inspectors

reviewed the adequacy of the fire protection water supply

Design Basis

Document

(DBD), System Description

(SD),

and Fire

Protection

Procedures

(FPP); verified through record review that the

diesel-driven fire pump received proper testing following maintenance

activities;

and walked down the fire pump areas to examine the pumps

and

testing connection

ar rangement.

The inspectors

reviewed the

FSAR and

National Fire Protection Association

(NFPA) code/standards

that were

referenced

in the licensee's

protection program procedures.

The

documents

reviewed are listed below:

Document

No.

Rev.

No.

Title

FSAR Section 9.5.1

FPP-013

Amendments

27,

46 Fire Protection

Revision

16

Fire Protection

DBD No. 306

SD-149

Revision

2

Revision

5

Fire Protection

and

Detection System

Fire Protection /

Detection System

The plant diesel-driven fire pump was declared out of service

on July 8,

1996, after failing to meet the test acceptance criteria found in FPT-

3004, Fire Pump Operability Test.

The acceptance

criteria require the

pump to produce

a water flow rate of

2500

gpm at 125 psig.

The diesel-driven fire pump was only capable of

116 psig at the required water. flow.

The pump was replaced with a

rebuilt pump which also failed the test acceptance criteria.

With the

assistance

of a representative

from the

pump manufacturer,

this pump was

inspected.

A hole caused

by erosion

was found in the discharge

casing.

The pump casing

was replaced,

the

pump rebuilt,

and tested.

This pump

passed

the criteria of FPT-3004

and was returned to service

on July 25,

1996.

During the inspectors

review, minor inconsistencies

in references

to

design fire pump capacity information, technical

manuals,

and

21

C.

engineering calculations in the fire protection

DBD and

SD were noted.

These

items were discussed

with the plant fire protection

program

engineer

and manager

.

There minor inconsistencies

did not affect design

inputs or

cause discrepancies

in the

FSAR.

The marginal fire pump capacity

was being evaluated

by the Harris

engineering organization.

The inspectors

noted that the status of this

condition was also addressed

in daily plant management

meetings.

During

the period the

pump was inoperable,

an alternate fire protection water

supply was provided as discussed

in NRC in report 50-400/96-06.

Conclusions

Overall, the inspectors

concluded that the licensee's

program to

maintain the fire protection water supply was completed in accordance

with the licensee's

procedures

and

NRC requirements.

The recorded test

data

was complete,

accurate,

met fire protection acceptance

criteria,

test discrepancies

were properly documented

and rectified,

and the

system

was properly returned to service.

However,

some examples

were

identified where there were minor inconsistencies

in references

to

design fire pump capacity information and engineering calculations in

the fire protection

DBD and

SD.

There minor inconsistencies

did not

affect design inputs or cause discrepancies

in the

FSAR.

V. Hang ement Heetin s

X1

Exit Meeting Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on September

3,

1996.

The licensee

acknowledged the findings presented.

The inspector s asked the licensee

whether

any material

examined during

the inspection

should be considered proprietary.

No proprietary

information was identified.

X2

Pre-Decisional

Enforcement Conference

Summary

On August 22,

1996,

a pre-decisional

enforcement

conference

was held at

the

NRC Region II office to discuss potential

enforcement

issues

identified in Inspection Report 50-400/96-06.

The issues

related to

missing interlocks on the spare charging/safety injection pump and spare

component cooling water

pump intended to prevent overload of the

emergency diesel

generator.

In addition,

key interlocks for the

same

pumps that were intended to protect train separation

and redundancy

were

removed without appropriate

design control measures'

22

Licensee

PARTIAL LIST OF PERSONS

CONTACTED

D. Alexander,

Supervisor,

Licensing and Regulatory

Programs

D. Batton, Superintendent,

On-Line Scheduling

D.

Br aund,

Superintendent,

Security

B. Clark, General

Manager,

Harris Plant

A. Cockerill, Superintendent,

I&C Electrical

Systems

J. Collins, Manager, Training

J.

Dobbs,

Manager,

Outage

and Scheduling

J.

Donahue,

Director Site Operations,

Harris Plant

R. Duncan,

Superintendent.

Mechanical

Systems

W. Gautier,

Manager,

Maintenance

W. Gurganious,

Superintendent,

Chemistry

M. Hamby, Supervisor,

Regulatory Compliance

M. Hill, Manager,

Nuclear Assessment

D. McCarthy, Superintendent,

Outage

Management

K. Neuschaefer,

Acting Manager,

Environmental

and Radiation Control

W. Peavyhouse,

Superintendent,

Design Control

W. Robinson,

Vice President,

Harris Plant

G. Rolfson,

Manager, Harris Engineering Support Services

S. Sewell,

Manager,

Operations

T. Walt, Manager,

Performance

Evaluation

and Regulatory Affairs

NRC

T. Le, Harris Project Manager,

NRR

M. Shymlock, Chief, Reactor Projects

Branch

4

IP 37550:

IP 37551:

IP 37700:

IP 40500:

IP 61726:

IP 62700:

IP 62703:

IP 64704

IP 71707

IP 71750

IP 90712:

IP 92700:

IP 92901:

IP 92902:

23

INSPECTION

PROCEDURES

USED

Engineering

Onsite Engineering

Design Changes

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Surveillance Observations

Maintenance

Implementation

Maintenance

Observation

Fire Protection

Plant Operations

Plant Support Activities

In-Office of Written Reports of Non-Routine Events at Power

Reactor Facilities

Onsite Followup of Events

Followup

- Plant Operations

Followup

- Haintenance

~0ened

ITEMS OPENED,

CLOSED,

AND DISCUSSED

50-400/96-07-01

VIO

Failure To Follow Procedure

During Performance

Of

Surveillance Testing

(2 examples),

Paragraph

H2.

50-400/96-07-02

URI

Corrective Actions For Maintenance

Rule Implementation

Problems,

Paragraph

H3.2.

50-400/94-001-00

LER

Technical Specification Surveillance Violation Due To

Inadequate

Procedure,

Paragraph

M8. 1.

Closed

50-400/96-012-00

LER

Discussed

Technical Specification 3.0.3 Entry For SIII Inverter,

Par agr aph 08.1

50-400/96-008-00

LER

April 25,

1996 Reactor Trip, Paragraph

H8.2.