ML18011A957

From kanterella
Jump to navigation Jump to search
Insp Rept 50-400/95-10 on 950507-0610.Violations Noted.Major Areas Inspected:Operational Safety,Maint,Surveillance, Engineering Activities & Plant Support
ML18011A957
Person / Time
Site: Harris 
Issue date: 07/07/1995
From: Elrod S, Darrell Roberts, Verrelli D
NRC Office of Inspection & Enforcement (IE Region II)
To:
Shared Package
ML18011A955 List:
References
50-400-95-10, NUDOCS 9507140315
Download: ML18011A957 (23)


See also: IR 05000400/1995010

Text

gA~ REGS

~o

nO

~0

W**gW

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Inspectors:

.Ero

enior

e ident Inspector

b rts

Resident

Inspector

Approved by:

D.

er elli, Chief

Reactor Projects

Branch lA

Division of Reactor Projects

Report No.:

50-400/95-10

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Cond

c

e

May 7

J ne 10,

1995

License No.:

NPF-63

D

e Signed

Da e

igned

7 i'll~

ate Signed

SUMMARY

Scope:

This routine inspection

was conducted

in the areas of operational

safety,

maintenance,

surveillance,

engineering activities,

and plant support.

Numerous facility tours were conducted

and facility operations

observed.

Backshift tours

and observations

were conducted

on May 10, ll, 14,

15,

16,

25,

27; 29,

and June 6, 8,

and 9,

1995.

Results:

0 erational

Safet

Operations

were generally performed well.

One violation involving .the power

for a,power operated relief valve demonstrated

the need for vigilance during

operations,

paragraph 3.b.(2)

Maintenance

Work performance

was satisfactory with proper documentation of removed

components

and independent verification of the reinstallation.

The inspectors

identified one violation involving maintenance

implementation of the site-wide

chemistry control program,

paragraph 4.a.(2).

9507140315

950707

PDR

ADOCK 05000400

9

PDR

En ineerin

Activities

Engineering activities were performed adequately.

~PP

1

Plant housekeeping

and component material condition was satisfactory.

The

licensee's

adherence

to radiological controls, security controls, fire

protection requirements,

emergency

preparedness

requirements

and

TS

requirements

in the plant support

area

was satisfactory.

REPORT DETAILS

PERSONS

CONTACTED

Licensee

Employees

D. Batton,

Manager,

Work Control

D. Braund,

Manager,

Security

J. Collins, Manager, Training

J.

Dobbs,

Manager,

Outages

  • J. Donahue,

General

Manager,

Harris Plant

R. Duncan,

Manager,

Technical

Support

H.

Hamby,

Manager,

Regulatory Compliance

  • H. Hill, Manager,

Nuclear Assessment

  • R. Prunty,

Manager,

Licensing

& Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

  • G. Rolfson,

Manager,

Harris Engineering

Support Services

  • C. Rose, Acting Hanager,

Maintenance

H. Smith,

Manager,

Radwaste

Operation

T. Walt, Manager,

Regulatory Affairs

B. White, Manager,

Environmental

and Radiation Control

"A. Williams, Manager,

Operations

Other licensee

employees

contacted

included:

office, operations,

engineering,

maintenance,

chemistry/radiation control,

and corporate

personnel.

NRC Personnel

T. Decker, Chief, Radiological Effluents and Chemistry Section,

RII

R. Carrion, Radiation Specialist,

RII

  • S. Elrod, Senior Resident

Inspector,

Harris Plant

  • D. Roberts,

Resident

Inspector,

Harris Plant

"Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

PLANT STATUS AND ACTIVITIES

'a ~

Operating Status of the Plant Over the Inspection

Period.

The plant continued in power operation

(Mode I) for the duration

of this inspection period.

The licensee

reduced unit power to 97

percent

on Hay 14 for moderator temperature coefficient testing

and to 80 percent

on June

9 for turbine valve testing.

The unit

ended the period in day 213 of power operation

since startup

on

November 8,

1994.

b.

Other

NRC Inspections

or Meetings at the Site.

R. Carrion, Radiation Specialist,

NRC RII, was

on site from

May 15-19 conducting

an inspection in the area of radiological

effluents

and chemistry.

He was accompanied

during part of the

inspection

by T. Decker, Section Chief, Radiological Effluents

and

Chemistry Section,

NRC RII.

They conducted

an exit meeting

on

May 19 and their findings will be documented

in IR 400/95-09.

OPERATIONAL SAFETY

'a ~

Plant Operations

(71707)

(1)

Shift Logs

and Facility Records

The inspector

reviewed

numerous

records

and discussed

various entries with operations

personnel

to verify

compliance with the

TS and the licensee's

administrative

procedures.

In addition, the inspector

independently

verified clearance

order tagouts.

The inspectors

found the logs to be legible and well

organized,

and to provide sufficient information on plant

status

and events.

The inspectors

found clearance

tagouts

to be properly implemented.

The inspectors identified no

violations or deviations

in the shift logs

and facility

records

area.

(2)

Facility Tours

and Observations

Throughout the inspection period, the inspectors

toured the

facility to observe activities in progress,

and attended

several

licensee

meetings to observe

planning

and management

activities.

Inspectors

made

some of these

observations

during backshifts.

During these tours, the inspectors

observed

monitoring

instrumentation

and equipment operation.

The inspectors

also verified that operating shift staffing met

TS

requirements

and that the licensee

was conducting control

room operations

in an orderly and professional

manner.

The

inspectors additionally observed

several shift turnovers to

verify continuity of plant status,

operational

problems,

and

other pertinent plant information.

Licensee

performance

in

these

areas

was satisfactory.

During

a facility tour on May 26, the inspector learned of a

condition which had rendered

the "C" SG

PORV inoperable the

previous day.

Discussions with licensee staff members

indicated

a lack of clarity concerning

when the valve

became

inoperable

and whether or not

a TS

LCO had

been violated.

The inspector

and the licensee. pursued this subject,

which

is discussed

further in paragraph 3.b.(2).

A violation identified in the facility tours area is

discussed

in paragraph 3.b.(2).

Effectiveness

of Licensee

Control in Identifying, Resolving,

and

Preventing

Problems

(40500)

Adverse Condition and

Feedback

Reports

(ACFRs) were reviewed to

verify TS compliance,

that corrective actions

and generic

items

were identified,

and that items were reported

as required

by

10

CFR 50.73.

Inspectors

reviewed

ACFRs documenting

incidents

involving RCA entry without proper dosimetry

and containment

isolation valves which were determined

by plant personnel

to have

been inoperable

beyond the four hours allowed by TS 3.6.3:

(1)

ACFR 95-1359

was generated

when

an individual entered

the

RCA without proper dosimetry.

The inspectors

reviewed the

licensee's

corrective actions following this incident

and

found them appropriate.

This. subject is discussed

further

in the plant support section,

report paragraph

6.b.

(2)

ACFR 95-1428 discussed

hydraulically operated

containment

isolation valve 1HS-62, the "C" SG

PORV.

On Hay 25,

1HS-62

was determined to have

been inoperable for about

30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

when plant personnel

discovered

a blown fuse in its

hydraulic

pump circuit.

Events leading to this condition

are discussed

in the following paragraphs.

At approximately 9:30 a.m.

on Hay 24,

a non-licensed

operator noticed that there were no indicating lights

illuminated at

HCC breaker cubicle IA31-SA-14D, from which

the

1HS-62 hydraulic oil pump was powered.

The day before,

the operator

had observed

the green light to be

illuminated - indicating that the hydraulic oil pump control

power was then available

and the

pump was off.

The operator

replaced

the green

and red light bulbs,

however, neither

light energized.

The operator then attempted to replace the

blue indicator bulb but found it broken off at the base.

He

then initiated

a work request for maintenance

to extract the

bulb base

from the socket

and replace

the bulb.

An on-shift

SRO in the work control center reviewed

and

approved the work request.

He determined,

from lack of

associated

alarms in the main control

room, that 1HS-62's

operability was unaffected

by the

HCC indicating light

condition.

He initially treated the deficiency as

a light

bulb problem,

and assigned

a low maintenance priority to the

work request.

A day later,

on Hay 25,

a different

SRO in the work control

center determined that the light bulb deficiency might

indicate

an operability problem

and requested

a maintenance

investigation.

A few hours later,

maintenance

personnel

found that the control

power fuse

was blown.

They replaced

it and the blue light bulb within four hours

(approximately

3:30 p.m.).

Licensee

personnel

blamed the blown fuse

on the

broken light bulb, which probably overheated.

The blown

fuse

had deenergized

the hydraulic oil pump.

This pump was

necessary

to maintain hydraulic accumulator oil pressure

high enough to ensure that the valve could be closed from

the main control

room.

Following additional review, the

licensee

concluded that,

due to the loss of hydraulic

pump

power, valve IHS-62 had

been

inoperable

from Hay 24,

when

the extinguished

HCC lights were initially discovered,

until

approximately

30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> later on Hay 25 when the control

power fuse

was replaced.

Technical Specification 3.6.3 required that each containment

isolation valve specified in plant procedure

PLP-106,

Technical Specification

Equipment List Program,

shall

be

operable with isolation times less than or equal to required

isolation times.

It further required that with one or more

of the containment isolation valves inoperable,

maintain at

least

one isolation valve operable

in each affected

penetration 'that was open

and complete

one of the following

four actions:

~

Restore

the inoperable valve(s) to operable status

within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,

or

~

Isolate

each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

by

use of at least

one deactivated

automatic valve

secured

in the isolation position, or

~

Isolate

each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

by

use of at least

one closed

manual

valve or blind

flange, or

~

Be in at least

Hot Standby within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and

in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The closed

system in which the steam generator

PORVs were

located

(the main steam

system)

was considered

to be the

operable isolation valve for purposes

of complying with the

first action statement

to "maintain at least

one isolation

valve Operable..."

Although IHS-62 remained

shut during the

Hay 24-25 incident, it was not considered

"deactivated"

as

required

by the second of the four subsequent

LCO action

statements.

This was because

even with no control

power

available to the hydraulic oil pump, oil pressure

remaining

in the valve accumulator

could continue to operate

the valve

in either direction with power available to the solenoids,

as

was the case

on Hay 24-25.

Additionally, none of the

remaining

TS actions

were taken within allowed timeframes.

Because

1HS-62 was inoperable for greater

than

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,

and

only one of the two required

LCO action requirements

were

satisfied,

the licensee's

actions

on Hay 24-25 were contrary

to the requirements

of TS 3.6.3.

This is Violation 400/95-10-01,

Steam Generator

PORV

Inoperable for Greater than

Four Hours.

Subsequent

to the violation, engineers

on

an event review

team discovered

a construction-era

design deficiency which

rendered

the main control

room annunciator

inoperable for

loss of 1HS-62 hydraulic control power.

This deficiency was

not readily recognizable

by plant operators

and strongly

contributed to the licensed

SRO's initial determination that

the valve was operable

on Hay 24.

The design deficiency,

which did not affect the other two

SG

PORVs, is further

discussed

in the engineering

section,

report paragraph

5.b.

On June

1,

because

of the design error, the licensee

again

declared

the valve inoperable

and took appropriate

TS

compensatory

actions.

At the close of the inspection

period, the

TS 3.6.3 action statement

requirements

were

being met by the

"C" SG

PORV block valve,

1HS-63,

being

shut.

The licensee

planned to correct the design deficiency

before returning

1NS-62 to operable status.

The inspectors

concluded that the design

issue discussed

in

paragraph

5.b of this report

was the root cause of the

violation.

However, the inspectors

also concluded that

a

more questioning attitude

on Hay 24 by plant operators

might

have prevented

the violation.

The licensee's

Nuclear Assessment

Section

completed three

assessments

this month:

~

H-SC-95-01,

HNP Security Assessment,

~

H-HA-95-01, Work Request

& Authorization

(WR&A) Review

Process,

and

H-SP-95-02,

Harris Material Receipt Inspection Activities.

The licensee's

Site Management

Team completed

a self-assessment

of

independent verification this month.

The inspectors

reviewed the assessments

and concluded that the

assessments

were thorough

and resulted

in substantive

findings.

The inspectors identified no violations or deviations .in the

Nuclear Assessment

area.

One violation was identified in the operational

safety area.

HAINTfNANCE

a ~

Haintenance

Observation

(62703)

The inspector

observed

or reviewed maintenance activities to

verify that correct equipment clearances

were in effect; work

requests

and fire prevention work permits were issued

and

TS

requirements

were being followed.

Haintenance

was observed

and

work packages

were reviewed for the following maintenance

activities:

(1)

WR/JO 95-AFRKl, Replace

Locking Pin Cylinder on Personnel

Air Lock Door.

WR/JO 95-AFRLl, Troubleshoot

and Replace

Control

Power

Fuse

for PAL Door.

On Hay ll, when

a containment

PAL door operator closed the

outer door following a routine containment entry,

a locking

(load-bearing)

pin and its attached cylinder broke off from

the door's hydraulic control unit and fell to the floor.

The locking cylinder, which measured

about

5 inches

long and

1 inch in diameter,

did not physically provide

a door

locking function by design,

but was

a key component in two

other aspects

of the

PAL door's operation.

With the outer

door closed, this locking cylinder would engage

a limit

switch which would then provide the permissive for the inner

door to be opened.

Additionally, the engaged limit switch

would send

a signal to the door's electro-hydraulic control

system indicating that the door closing sequence

was

complete.

This signal

would shutoff the associated

hydraulic pump.

The broken locking cylinder alone did not render the

PAL

door inoperable.

However,

because

the cylinder had not

engaged

the limit switch, the hydraulic

pump continued to

operate

in the absence

of the shutoff signal, eventually

blowing a fuse in the hydraulic control circuitry.

This

removed

PAL door power and the ability to verify the

presence

of an interlock designed to prevent

both

PAL doors

from opening simultaneously.

Since the interlock

verification was

a TS surveillance requirement,

operators

appropriately declared

the door inoperable

and entered

a 24

hour shutdown action statement.

Three maintenance

work

tickets were subsequently

generated

to repair the door.

The inspector

observed

two of the three maintenance

jobs

associated

with returning the

PAL door to operability.

These

included replacing the hydraulic cylinder unit

(complete with a new locking pin and cylinder)

and replacing

the blown control

power fuse.

The third job, for which the

inspector reviewed

a completed

work ticket, involved

adjusting another limit switch.

This switch caused

the

locking cylinder to engage

before another locking device

could clear

a path for it during the earlier door closing

sequence.

When the locking cylinder impacted this device

during that sequence,

the load-bearing

pin yielded under

excessive

stresses.

The licensee

completed the work, successfully

tested

the

door interlock,

and exited the

LCO action statement within a

few hours.

The inspector

observed

good workmanship during

the jobs

he observed.

Plant personnel

adequately

documented

all maintenance

on the work tickets.

WR/JO 94-AHHN1 Change Trim in 1CS-231

Per

PCR-6796.

FCV 1CS-231's

purpose

was to vary charging flow to maintain

programmed pressurizer level.

The original valve internals

were oversize

- resulting in poor control response

to

pressurizer

level transients

and inability to maintain

a

steady charging flowrate below about

85 gpm.

Operators

had

routinely operated with the valve in manual control.

The inspector

observed

the mechanics

disassemble,

modify,

and reassemble

valve 1CS-231.

Worksite activities inspected

included worksite preparation,

radiological control

practices,

conduct of maintenance,

and

use of calibrated

tools when called for.

Since this valve routinely had

reactor coolant flowing through it, the worksite was

prepared

as

a highly contaminated

area with a roped-off

boundary, stepoff pad, containers for used

anti-contamination

clothes,

and covered floor area.

The

area

was adequately

sized for work and included laydown

space for both old and

new parts.

The valve components

were

handled with care.

Workmanship, radioactive work practices,

and torquing techniques

were excellent.

The inspector

determined that both torque wrenches

used

were current in

the calibration program.

The inspector

observed

a quality

control person performing

a thorough post-maintenance

VT-2

visual inspection of boundary leakage.

No leakage

was

found.

WR/JO 94-AHHNl required that the shop erect

a scaffolding

enclosure

over radiation monitor 3502A located

under this

valve to prevent

something

being dropped

on it and causing

entry into a

LCO.

The inspector identified that the

scaffolding was not built.

Inquiry found that the

supervisor

had evaluated this requirement

and decided that

a

scaffold was not necessary

because

the deck grating floor

between the two items, in conjunction with the temporary

covering placed

on the deck grating floor for this job,

performed the

same protective function.

The inspector

concluded that the supervisor's

actions

were within the

allowed scope

and provided adequate

protection,

but that the

work package

was neither changed

nor annotated

to show what

actually happened.

The licensee

subsequently

corrected the

work package

and

added this documentation

problem to their

trending data

base

used to find organizational

and

programmatic deficiencies.

The inspector

concluded that

this resolution

was appropriate.

The inspector

reviewed the use of consumable

materials

during this job.

The review included observation of the

material

as it was being used,

and resolution of actual

practice with statements

in the applicable

Chemical

and

Consumables

Fact Sheets.

Haterials

reviewed included:

~

Gas leak detection fluid [part no. 731-778-00],

~

Spray cleaner

and degreaser

[part no. 737-832-76],

and

~

Nickel-based antisieze

compound [part no. 737-263-66].

Though the inspector

found no problems with the use of the

gas leak detection fluid or the spray cleaner,

the antisieze

compound being used to lubricate the valve packing was

contrary to conditions specified in the Chemical

and

Consumables

Fact Sheet.

Chemical

and Consumables

Fact Sheet

AP-501-00565,

Rev 4, dated

Harch 6,

1994, for antisieze part

no. 737-263-66,

specified that:

This compound

was to be used

as

a lubricant for

metal-to-metal

contact in primary or secondary

system

components,

and

~

This compound

was not permitted to contact reactor

coolant.

Part of the basis for this internal specification

was

an

unsupported

statement,

mentioning

a simila} material,

in an

external proprietary document.

, In contrast,

applicable

maintenance

procedure

HHH-017,

Rev I/2, Valve Packing

Reference

Hanual, specified throughout the procedure to coat

the valve stem,

the inside of the stuffing box,

and the

packing rings with the subject antisieze

compound.

The inspector

found that:

~

Lubrication of packing

was not

a "metal-to-metal

contact"

use,

and

~

Any antisieze

compound entering the valve bonnet from

the packing gland would certainly contact reactor

coolant

and

some would be transported

into the main

coolant loops.

~

Haintenance

procedure

HNN-017 did not adequately

implement the site chemical

and consumable

material

control program described

in AP-501,

Rev 8, Plant

Chemical

and Consumable

Controls.

Procedure

AP-501,

Rev 8,

and associated

fact sheet

AP-501-

00565,

Rev 4,

implemented

TS 6.8. l.a and

RG 1.33,

Rev.

2,

February

1978, Section

10, which required chemical

and

radiochemical

control procedures

prescribing the limitations

on concentrations

of agents that may cause corrosive attack

or fouling of heat transfer surfaces

or that

may become

sources of radiation hazards

due to activation.

Failure to adequately

implement Procedure

AP-501 is

Violation 400/95-10-02.

In general,

the performance of work was satisfactory with proper

documentation of removed

components

and independent verification

of the reinstallation.

The inspectors identified one violation

involving maintenance

implementation of the site-wide chemistry

control program.

Surveillance Observation

(61726)

The inspector

observed

several

surveillance tests to verify that

approved

procedures

were being used; qualified personnel

were

conducting the tests; tests

were adequate

to verify equipment

operability; calibrated

equipment

was used;

and

TS requirements

were followed.

Test observation

and data review included:

(1)

OST-1119,

Rev 6/2, Containment

Spray

Oper ability - Train B,

quarterly Interval.

The inspector

observed plant personnel

perform this

procedure,

which included

ASME Code Section

XI ISI testing

requirements for the "B" containment

spray

pump

and various

system valves

as required

by TS 4.0.5.

Operators

measur ed

or calculated

various

pump performance

indicators including

differential pressure,

recirculation flow and

pump

10

vibration.

All parameters

were within specified

acceptance

criteria and were appropriately

documented

on test data

sheets.

The inspector verified that operators

were using

an

approved

procedure

and calibrated test equipment.

Licensee

personnel

performed this test satisfactorily.

Acceptance test

EPT-815T,

approved

May, 8,

1995,

Temporary

Procedure

for Acceptance

Test for ESR-00196.

The acceptance

test focused

on response

to pressurizer

level

transients

at both normal

and low charging rates.

This test

collected data at I-minute intervals using the

ERFIS

computer monitoring system.

It also collected stroke time

data.

The inspector

observed

portions of the test

performance.

Test control

and data collection were

effective from the control

room.

The valve system generally

performed well, however the test for normal

(high) flow from

pressurizer

level

above the setpoint

was terminated

because

of high letdown heat exchanger outlet temperature.

The

valve was stable but control

was

somewhat

slow.

Subsequently,

the licensee

adjusted

the valve control

response

speed.

MST-E0006,

Rev 3, 480/240

VAC Molded Case Circuit Breaker

Test,

and MST-E0007,

Rev 2/3,

120/208

VAC Molded Case

Circuit Breaker Test.

TS 4.8.4. 1 required that each containment penetration

conductor overcurrent protective device shall

be

demonstrated

operable at least

once per

18 months

by

selecting

and functionally testing

a representative

sample

of at least ten percent of each type of lower voltage (less

than

6900 volts) circuit breaker.

This functional test

consisted of removing the breakers

to the shop,

applying

substantial

electrical currents to the breaker using

a test

machine,

and verifying various thermal trip functions per

the subject procedures.

Following recent industry issues

concerning

molded-case

circuit breaker testing,

licensee

personnel

questioned

whether or not practices

contained

in their surveillance

procedures

were acceptable.

Specifically, the procedures

directed plant personnel

to manually cycle the breakers

open

and closed several

times prior to performing the thermal

trip tests.

This practice,

enhancing

personnel

(and

equipment)

safety, verified that the breakers

operated

smoothly and with a fast snap action.

The practice could

have

been considered

as "preconditioning" the breakers prior

to testing

them, thus eliminating potential failure

11

mechanisms

which might have

been present.

The licensee's

initial analysis

was that its testing

program was acceptable

and

was supported

by various industry standards

and previous

NRC correspondence.

The inspector consulted

the previous

NRC correspondence

on

this subject,

NRC Bulletin 88-10,

Nonconforming Molded-Case

Circuit Breakers.

This bulletin proposed

a test program for

this type of breaker

and cited such industry standards

as

NEHA AB-1, Molded-Case Circuit Breakers;

NEHA AB-2,

Procedures

for Field Inspection

and Performance Verification

of Molded-Case Circuit Breakers

Used in Commercial

and

Industrial Applications; UL-489, Molded Case Circuit

Breakers

and Circuit Breaker Enclosures;

and

NETA STD ATS-

1987, National Electrical Testing Association,

Acceptance

Testing Specifications.

The test

sequence

outlined in the

bulletin included manually operating the breakers

open

and

closed

"a minimum of five times to ensure that the latching

surfaces

a'e free of any binding" prior to an electrical

current test.

The inspectors

concluded

(and informed

licensee

management)

that the licensee's

testing practice

related to cycling these

breakers,

as

implemented in

HST-E0006

and HST-E0007,

was acceptable.

The inspector also concluded that, since mechanical

cycling

of the breaker

was part of the licensee's

test program,

any

related failures represented

a failed functional test.

TS 4.8.4. la.2 and the licensee's

surveillance

procedures

required that another ten percent

breaker

sample

be tested

if any of the first breakers failed functional testing.

Hence,

as

a followup to the licensee's

question,

the

inspectors

reviewed the latest procedure revisions to verify

that mechanical

breaker failures were being treated

as valid

test failures.

Based

on the procedure

review, the inspector

concluded that

a newer procedure

adequately

considered

mechanical

breaker failures,

but the licensee's

procedures

historically did not address

mechanical

problems

as valid

test failures.

Specifically,

a newer revision to procedure

HST-E0006

(Rev 3 effective February

24,

1995) contained

a

specific data sheet entry for mechanically cycling the

breaker,

while a current but older revision to procedure

HST-E0007

(Rev

2 approved April 13,

1992) did not.

Licensee

personnel

indicated that they were considering

enhancements

to procedure

HST-E0007 before the next scheduled

surveillance test.

The inspectors

reviewed results of the last performance of

procedure

MST-E0007

and found no indications of problems

with either manually or thermally cycling the breakers.

12

The inspectors

found satisfactory surveillance

procedure

performance with proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization

of control

room personnel,

and knowledgeable

personnel

having

performed the tasks.

The inspectors

observed

no violations or

deviations in this area.

ENGINEERING ACTIVITIES

a ~

Design/Installation/Testing

of Hodifications (37551)

ESRs involving the installation of new or modified systems

were

reviewed to verify that the changes

were reviewed

and approved

in

accordance

with 10

CFR 50.59, that the changes

were performed in

accordance

with technically adequate

and approved

procedures,

that

subsequent

testing

and test results

met approved

acceptance

criteria or deviations

were resolved in an acceptable

manner,

and

that appropriate

drawings

and facility procedures

were revised

as

necessary.

ESRs documenting

engineering

evaluations

were also

reviewed.

The following engineering

evaluations

were inspected.

(1)

PCR-6796 evaluated

the flow control valve

1CS-231 flow

range.

This valve's

purpose

was to vary charging flow to

maintain

programmed pressurizer level.

The original valve

internals

were designed

oversize resulting in poor response

to pressurizer

level transients

and inability to maintain

a

steady charging flowrate below about

85 gpm.

Operators

had

routinely operated with the valve in manual control.

The

PCR-6796 evaluation

found that the original operating point

was

16 percent of total travel

from "closed"

(a non-linear

range)

and that

a small

change

in plug position resulted

in

a large flow change.

The new design featured linear control

at about

43 percent of the total travel from "closed".

The inspector

reviewed

PCR-6796 while inspecting the on-site

installation of the design

change.

The

PCR evaluated

seismic conditions

and also valve body thrust loads

caused

by using

a stronger spring.

The licensee's

10

CFR 50.59

review,

and the inspector,

concluded that there were

no

unreviewed safety questions.

The design

package

included

an

equipment data

base

change

request for the valve trim parts,

and

a change to applicable

vendor manual

"BJT."

The testing specified in the design

package

focused

on

demonstrating

the valve's response

in two ways:

Pressurizer

level transient

response

demonstrated

by

manually varying pressurizer

level

and then letting

the automatic control return it to normal,

and

System ability to maintain level at lower than normal

flow rates of about

40 gpm.

13

The inspectors

concluded that this

PCR was satisfactory

and

identified no violations or deviations in the

design/installation/testing

of modifications area.

(2)

ESR 9500572 evaluated

the use of anti-sieze

agents

in

contact with reactor coolant,

such

as

when used

as valve

packing lubricant.

One valve packing vendor

had specified

a

specific

compound to use during valve packing installation

while another type vendor

had instructed the plant not to

use similar materials

in contact with reactor coolant.

Plant procedure

AP-501, Plant Chemical

and

Consumable

Controls,

had implemented the requirement

not to use the

material while maintenance

procedure

HHM-017,

Rev 1, Valve

Packing Reference

Manual,

implemented the direction to use

the material.

Following NRC identification,

CR 95-01452

requested

engineering resolution.

This resolution focused

on licensee

standards

and directed certain

shop practices

such

as applying the material

only to certain surfaces-

which would actually negate its effectiveness

as

a valve

packing lubricant.

The resolution also did not resolve the

one vendor's instruction not to use the material

in contact

with reactor coolant.

Following discussions

with the

inspector

and maintenance

department,

the engineering

division reconsidered

the

ESR response,

consulted with

vendors,

and issued

replacement

ESR 9500582.

This second

ESR had

a clearer

evaluation - including reference to vendor

discussions,

and better documented

the reasons

why use of

these materials,

in the amounts

normally used for packing

valves,

was satisfactory without specific restrictions.

The inspector concluded that the engineering division produced

adequate

products,

with one exception found.

Onsite

System Engineering

(37551)

The inspectors

reviewed engineering activities associated

with the

root cause determination for the violation discussed

in paragraph

3.b.(2) of this report.

As discussed

in that paragraph,

an error

in the design of the "C" SG

PORV control

room trouble annunciator

made it unavailable

when the valve's hydraulic control

power was

lost for about

30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

on Hay 24-25.

The following paragraphs

discuss this design

problem, which was not readily recognizable

by

plant operators

on Hay 24.

A design

change during plant construction

involved relocating

a

ventilation fan's

power supply from HCC 1A31-SA to

a non-safety

HCC, leaving

a spare cubicle

and associated

control

components

in

the lA31 HCC.

The spare cubicle had extra components

to account

for the original fan being controllable from either the main

control

board in the control

room or the auxiliary control panel

if the main control

room was uninhabitable.

14

Later, the designers

(via DCN 251-595,

approved

August 22,

1985)

powered the

1MS-62 valve hydraulic

pump from this spare location.

The AE, by practice,

did not include unused or extra components

in

CWDs.

Additionally, the construction practice

was to not label

components

such

as fuses

and relays in MCCs.

Therefore,

CWD 2166-

B-401,

Sheet

1257 did not show the second

fuse

and second relay

actually located in the cubicle,

and the second

fuse

and second

relay were physically not labeled.

The control board alarm terminals referenced

on the

CWD were

actually attached

to a relay,

but the

CWD referenced

the second

[wrong] relay.

If one tested

the motor controller by opening the

supply breaker, all the correct alarms would sound.

If the

operative control

power fuse blew, the

pump would die with no

alarm.

On May 24,

1995,

when the control

power fuse blew, operators

were

misled

by the absence

of an alarm in the control

room.

Plant

operators

were used to seeing this alarm for the other two

SG

PORVs for similar problems.

The only indication of a blown fuse

was the extinguished light bulbs at the cubicle, which operators

initially treated

as

a bulb problem.

The licensee initiated an event review team after the violation on

May 24-25.

The team

s activities were still continuing at the end

of the inspection period.

Engineers

on the team conducted

a

rigorous search

on the modification history associated

with MCC

cubicle lA31-SA-14D.

The engineers

also conducted

a verification

walkdown of safety-related

cubicles,

containing similar design

features,

which may have

been susceptible

to the

same errors.

No

similar design errors were found.

The inspector inquired about field verification walkdowns to

support the

1985 design

change.

Licensee

personnel

have found no

record of any particular field verification walkdowns related to

the modification.

The inspectors

concluded that

an adequate

verification walkdown during that time would have identified the

drawing/field discrepancy.

The inspectors

also concluded that the

licensee's'efforts

to identify the root cause of the

SG

PORV

inoperability were thorough.

However, while the root cause

stemmed

from an old design issue,

current practices to not label

fuses

and relays could lead to future problems related to working

inside

MCC cubicles.

The inspectors identified no violations or

deviations in the systems

engineering

area.

The:inspectors

concluded that the engineering activities were performed

adequately.

The inspectors

identified no violations or deviations in

the engineering activities area.

g

6.

PLANT SUPPORT

15

a ~

b.

Plant Housekeeping

Conditions

(71707)

- The inspectors

reviewed

storage of material

and components,

and observed

cleanliness

conditions of various areas

throughout the facility to determine

whether safety or fire hazards

existed.

The inspectors

found

plant housekeeping

and material condition of components

to be

satisfactory.

Radiological Protection

Program

(71750)

- The inspectors

reviewed

radiation protection control activities to verify that these

activities were in conformance with facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also verified that selected

doors which controlled

access

to very high radiation areas

were appropriately locked.

Radiological postings

were likewise spot checked for adequacy.

As mentioned in report paragraph 3.b.(l),

ACFR 95-1359

was

generated

when

an individual entered

the

RCA without proper

dosimetry.

Specifically, the individual logged into the

licensee's

computerized radiation exposure tracking system with

one electronic dosimeter

and erroneously

used another

"non-activated" dosimeter to enter the

RCA, leaving the

"activated" dosimeter at the computer log-in station.

In a

separate

incident,

another individual entered

the

RCA without a

dosimeter after leaving his at the computer log-in station.

Both

individuals reported their own actions.

Self reporting

was

commended

by both the inspectors

and licensee

management.

The main entrance

to the

RCA was provided with three computer log-

in terminals

and

a storage

rack for electronic dosimeters.

Individuals wishing to enter the

RCA would acquire

a personal

electronic dosimeter

and log it into the licensee's

exposure

tracking system using

a computerized

reader.

Once the dosimeter

was logged in and "activated", the individual would use it to

track personal

dose while in the

RCA.

Upon returning from the

RCA, the individual would log out using the computerized

reader

- which would assign

the person's

new dose to a permanent

record.

The individual would then return the newly "de-activated"

dosimeter to one of the storage

racks.

Because

the storage

racks were located

about waist high and just

below the log-in terminal, plant personnel

could just as easily,

due to distraction or lack of attention,

pick up the wrong

dosimeter prior to entering the

RCA.

To correct this

human

factors situation,

licensee

personnel

moved the dosimeter storage

racks to a location

a few feet to the side of the log-in

terminals.

This action should reduce the recurrence

rate of this

problem since,

to have the problem,

personnel

would have to

deliberately walk .over and get

a second

dosimeter after logging

one dosimeter into the computer.

16

The inspectors

were provided with data showing that, in 1995,

seven

ACFRs were related to improper log-in on electronic

dosimetry.

Of these,

four involved entering the

RCA with a

"deactivated"

dosimeter.

The other three involved entering the

RCA with no dosimeter.

For the period between

January I and

Hay 31, plant personnel

made about 44,000 separate

entries into

the

RCA.

The inspector

concluded that seven

incidents represented

a very small trend in this area.

The inspectors

concluded that, while preventing individuals from

"forgetting to take

a dosimeter with them" would be harder to

solve,

the licensee's

attempts to reduce the occurrences

of

individuals entering the

RCA with the wrong dosimeter

were

commendable.

Security Control

(71750)

- During this period, the inspectors

toured the protected

area

and noted that the perimeter fence

was

intact and not compromised

by erosion or disrepair.

The fence

fabric was secured

and the barbed wire was angled.

Isolation

zones

were maintained

on both sides of the barrier

and were free

of objects

which could shield or conceal

an individual.

The

inspectors

observed

various security force shifts perform daily

activities, including searching

personnel

and packages

entering

the protected

area

by special

purpose detectors

or by a physical

patdown for firearms,

explosives

and contraband.

Other activities

included vehicles

being searched,

escorted

and secured;

escorting

of visitors; patrols;

and compensatory

posts.

In conclusion,

the

inspectors

found that selected

security program functions

and

equipment

met requirements.

Fire Protection

(71750)

- The inspectors

observed fire protection

activities, staffing and equipment to verify that fire brigade

staffing was appropriate

and that fire alarms,

extinguishing

equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

During plant tours,

areas

were inspected

to ensure fire hazards

did not exist.

The

licensee's

adherence

to fire protection requirements

was

satisfactory.

Emergency

Preparedness

(71750)

- The inspectors

toured

emergency

response facilities to verify availability for emergency

operation.

Duty rosters

were reviewed to verify appropriate

staffing levels were maintained.

As applicable,

the inspectors

observed

emergency

preparedness

exercises

and drills to verify

response

personnel

were adequately trained.

The licensee

conducted

an augmentation

response drill on June

9,

beginning at 4:50 a.m.

The shift supervisor declared

a "Site Area

Emergency" at 4:58 a.m.,

and initiated

a staff callout.

The

emergency

response facilities were adequately

staffed

and declared

activated at 5:50 a.m.

This response

easily met the emergency

plan requirement of 75 minutes to activate the facilities.

17

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to radiological

controls, security controls, fire protection requirements,

emergency

preparedness

requirements

and

TS requirements

in these

areas

was

satisfactory.

The inspectors identified no violations or deviations in

the plant support area.

EXIT INTERVIEW

F

The inspectors

met with licensee

representatives

(denoted in

paragraph

1) at the conclusion of the inspection

on June 9,

1995.

During this meeting,

the inspectors

summarized

the scope

and findings of

the inspection

as they are detailed in this report, with particular

emphasis

on the Violations addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not

identify as proprietary

any of the materials

provided to or reviewed

by

the inspectors

during this inspection.

The inspector recognized that

one document

reviewed

was marked proprietary,

but it was not used

as

a

basis for concluding acceptability of items inspected.

No dissenting

comments

from the licensee

were received.

Item Number

,

Status

. Description

and Reference

400/95-10-01

400/95-10-02

Open

Open

VIO

Inoperable

Steam Generator

PORV for

greater

than

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,

paragraph

3.b.(2).

VIO

Failure to adequately

implement

Procedure

AP-501, paragraph 4.a.(2).

ACRONYHS AND INITIALISHS

ACFR

AE

ASHE

ATS

CFR

CR

CWD

DCN

encls-

EPT

ERFIS-

ESR

FCV

FSAR

GPM

HNP

IR

ISI

LCO

HCC

Adverse Condition and Feedback

Report

Architect/Engineer

[Design

and Construction

Firm]

American Society of Mechanical

Engineers

Acceptance Testing Specifications

Code of Federal

Regulations

Condition Report

Control Wiring Diagram

Design

Change Notice

Enclosures

Engineering

Performance

Test

Emergency

Response

Facility Information System

Engineering Service

Request

flow control valve

Final Safety Analysis Report

Gallons

Per Minute

Harris Nuclear Plant

[NRC] Inspection

Report

Inservice Inspection

Limiting Condition for Operation

Motor Control Center

18

MMM

NEMA

NETA

NPF

NRC

OST

PCR

PORV

RCS

RII

SG

SRO

STD

TS

UL

VAC

VIO

WR/JO-

Maintenance

Management

Manual

National Electrical Manufacturer's

Association

National Electrical Testing Association

Nuclear Production Facility [a type of license]

Nuclear Regulatory

Commission

Operations Surveillance Test

Plant

Change

Request

Power Operated Relief Valve

Reactor Coolant System

NRC Region II

Steam Generator

Senior Reactor Operator

Standard

Technical Specification [Part of the Facility License]

Underwriters Laboratories,

Incorporated

'Volts - Alternating Current

Violation [of NRC Requirements]

Work Request/Job

Order