ML18011A446

From kanterella
Jump to navigation Jump to search
Insp Rept 50-400/94-06 on 940219-0402.Violations Noted. Major Areas Inspected:Plant Operations,Review of Licensee Control of Overtime Hours,Review of Nonconformance Repts, Preparations for Refueling & Refueling Activities
ML18011A446
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 04/15/1994
From: Christensen H, Darrell Roberts, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18011A443 List:
References
50-400-94-06, 50-400-94-6, NUDOCS 9405230101
Download: ML18011A446 (34)


See also: IR 05000400/1994006

Text

~p,g RECy

Vp

+

0

Cy

An

p

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report No..

50-400/94-06

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

February

19 - April 2,

1994

Inspectors:

J.

row,

S

ior

sident Inspector

Licensee

No.:

NPF-63

4-i -e

Date Signed

D.

er

,

sid

Inspector

Approved by:

. Christensen,

Section Chief

Division of Reactor Projects

Date

igned

Date

igned

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

review of licensee's

control of overtime hours,

review of

nonconformance

reports,

preparations

for refueling, refueling activities,

followup of onsite events,

maintenance

observation,

surveillance observation,

design

changes

and modifications, plant housekeeping,

radiological controls,

security,

and fire protection.

Numerous facility tours were conducted

and

facility operations

observed.

Some of these tours

and observations

were

conducted

on backshifts.

Results:

One violation was identified:

Failure to properly control vehicles inside the

protected

area,

paragraph

5.c.

Several

instances

were noted where the conduct/control

of activities was

deficient:

inadequate

supervision during deenergization

of a process

instrumentation

cabinet,

paragraph

2.a(4);

poor coordination of testing

and

deenergization

of a process

instrumentation

cabinet,

paragraph

3.b.

Examples

of poor planning activities were noted:

planning/briefings for draining down

the reactor coolant system were deficient,

paragraph

2.c;

efforts to

establish

a containment closure plan were poor, paragraph 2.b(1);

coordination of preventive maintenance

with surveillance testing

was less than

940M30iOi 9404i5

PDR

anOCV 0SO00400

'

PDR

e~

L

I/

" C'

'

~

'~

1~>>t'a'I

'I

Aa

~ I

ll

r

II

J A,

'

~

4

2

adequate,

paragraph

3.a(2).

In addition,

implementation of procedure

changes

following modifications

was poor, paragraph

4.b.

The content

and conduct of pre-evolution briefings for fuel handling

and lift

of the upper internals

were considered

to be very good,

paragraphs

2.c.

The

conduct

and content of several

major tests

were likewise found to be very

thorough,

paragraph

3.b.

The development of an outage

schedule to preclude reactor coolant system

reduced

inventory and mid-loop operations

was considered to be

a strength,

paragraph

2.b.

Overview and mockup training for the

RTD bypass manifold removal modification

was considered

to be

a strength,

paragraph

4.

Good efforts were noted to reduce radiation hot spots,

paragraph

5.b.

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees

D. Batton,

Manager,

Work Control

  • D. Braund,

Manager,

Security

  • B. Christiansen,

Manager,

Maintenance

  • J. Collins, Manager,

Training

  • J. Dobbs,

Hanager,

Outages

  • H. Hamby,

Manager,

Corrective Action Programs/Operational

Events

  • J. Kiser, Manager,

Radiation Control

D. HcCarthy,

Manager,

Regulatory Affairs

J.

Moyer, Hanager,

Site Assessment

  • R. Prunty,

Manager,

Licensing

3 Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

W. Seyler,

Manager,

Project

Management

H. Smith,

Manager,

Radwaste

Operation

  • D. Tibbitts, Manager,

Operations

B. White, Manager,

Environmental

and Radiation Control

A. Williams, Manager, Shift Operations

  • L. Woods,

Manager,

Technical

Support

M. Worth, Manager,

Onsite Engineering

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

2.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Operations

a ~

Operational

Safety Verification (71707)

The plant began .this inspection period in power operation

(Node

1).

On March 19,

1994, the unit was taken off-line and

a plant

shutdown performed to commence

a scheduled

refueling outage.

A

plant cooldown was subsequently

performed

and

on March 20 the unit

was placed in the cold shutdown

(Node 5) condition.

On March 26

at 5: 18 p.m. the reactor vessel

closure

studs

were detensioned

and

refueling operations

(Node 6) commenced.

The plant remained in

Mode

6 for the duration of this inspection period.

(1)

Shift Logs and Facility Records

The inspector reviewed records

and discussed

various entries

with operations

personnel

to verify compliance with the

Technical Specifications

(TS)

and the licensee's

administrative procedures.

The following records

were

reviewed:

shift supervisor's

log; outage shift manager'

~

~

log; control operator's

log; night order book; equipment

inoperable record; active clearance

log; grounding device

log; temporary modification log; chemistry daily reports;

shift turnover checklist;

and selected

radwaste

logs.

In

addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well

organized,

and provided sufficient information on plant

status

and events.

Clearance

tagouts

were found to be

properly implemented.

No violations or deviations

were

identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were

conducted to observe operations,

surveillance,

and

maintenance activities in progress.

Some of these

observations

were conducted during backshifts.

Also, during

this inspection period, licensee

meetings

were attended

by

the inspectors

to observe

planning

and management

activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control

room;

emergency

diesel

generator building; reactor auxiliary

building; reactor containment building; waste processing

building; turbine building; fuel handling building;

emergency

service water building; battery rooms; electrical

switchgear

rooms; technical

support center,

and the

emergency

operations facility.

During these tours,

observations

were

made

on monitoring

instrumentation

which included equipment operating status,

area

atmospheric

and liquid r adi ation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters.

Indicated parameters

were

verified to be in accordance

with the

TS for the current

operational

mode.

The inspectors

also verified that

operating shift staffing was in accordance

with TS

requirements

and that control

room operations

were being

conducted in an orderly and professional

manner.

In

addition, the inspector

observed shift turnovers

on various

occasions

to verify the continuity of plant status,

operational

problems,

and other pertinent plant information

during these turnovers.

The licensee's

performance

in these

areas

was satisfactory.

No violations or deviations

were identified.

Control of Overtime

The inspectors

conducted

a detailed inspection of the

licensee's

program for controlling the usage of overtime.

The inspection

included

a review of the licensee's

administrative

procedure,

AP-012, Control of Overtime Hours,

and

a study of overtime data dating back to January

1991.

The historical review of overtime records

was done to

develop

a trendline for overtime usage

and to compare data

for the two most recently completed refueling outages

(Fall

1992

and Spring 1991).

As noted in paragraph

2.a of this

report, the plant recently

began

Refueling Outage

(RFO)

5 on

Harch 19,

1994.

Therefore,

overtime data for the current

outage could not be analyzed during this inspection period.

In addition,

November

1992 data

was not available for the

operations

group.

The inspectors

compared

the licensee's

program

as described

in procedure

AP-012 to requirements

contained

in NRC Generic Letters 82-02,

82-12,

82-16,

and 83-14

and

TS 6.2.2.f.

The

inspectors

found that the licensee's

administrative

procedure satisfied

NRC requirements.

Specifically,

procedure

AP-012 prohibited the routine heavy use of

overtime for specific job categories,

except in the event of

unforeseen

problems requiring substantial

overtime.

In

those special

cases,

the licensee's

procedure limited

individuals from working more than

16 consecutive

hours,

working more than

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> in a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period, working more

than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> period, or working more than

72

hours in a seven

day period.

The above restrictions

were

extended for STAs whose

seven

day limit was

84 hours9.722222e-4 days <br />0.0233 hours <br />1.388889e-4 weeks <br />3.1962e-5 months <br />.

All

of the above restrictions

excluded

hours which were

attributed to shift turnover.

Any instances

where

an

individual was expected

to exceed

the limits had to be

approved

by the Plant General

Hanager

(PGH)

on a case

by

case

basis

before the fact.

Additionally, the

PGH or his

designee

were required to review overtime monthly for each

of the affected job categories

to assure

that excessive

hours

had not been assigned.

The job categories

affected

by

AP-012 included all licensed operators,

auxiliary operators,

radwaste

operators,

EKRC technicians,

maintenance

technicians,

and their first line supervisors.

All other

job categories

were exempted

from the requirements

of AP-

012.

During a review of overtime extensions that had

been

approved

over the previous three years

encompassing

the last

two completed refueling outages,

the inspectors

found that

the licensee

complied with its procedure for controlling and

approving overtime.

Overtime use for the affected work

groups

was heaviest

during the refueling outages,

especially

in the areas of operations,

maintenance,

and

EKRC.

For

example,

during

RFO-4 (September

- December

1992), the

PGH

approved

over

600 instances

of overtime where the

TS limits

were expected to be exceeded.

Approximately two-thirds of

those

instances

were assigned

to the maintenance

unit, with

the balance divided between

the operations

and

E&RC

organizations.

During RFO-3

(March - May 1991), the numbers

were less for the maintenance

unit (approximately

100

instances

were pre-approved),

but greater for the

EKRC (over

40 instances)

and operations

groups.

During March 1991,

virtually all of the operations shifts were pre-approved

to

attend

a mid-loop training class,

which contributed heavily

towards that outage's

overtime totals.

The inspector

found that the occasions

where overtime use

exceeded

TS limits were substantially lower during non-

outage

months for all work groups except the radwaste

operators.

Only one example

was found during each of the

last two completed refueling outages

where radwaste

operators

needed

approved extensions.

However,

an average

of five overtime extensions

per month were granted for

radwaste

operators

between

non-outage

months April 1993

and

November

1993.

Licensed

and auxiliary operators

also

had

an

average of five overtime extensions

approved

per month from

the end of RFO-4

(December

1992) to February

1994, but this

average

represented

decreases

from outage

months for those

groups.

Maintenance

(2.3 per mo'nth)

and

EKRC (1.4 per

month) also registered

fewer extensions

since

RFO-4.

While the inspectors

did not identify any explicit

violations of TS requirements,

questions

were raised

on

various aspects

of the licensee's

implementation of overtime

controls.

For instance,

the inspector

noted inconsistencies

in how the maintenance

organization attributed excessive

hours to shift turnover time.

Specifically,

cases

were

identified where individuals worked

13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />

a day for seven

consecutive

days.

In such cases,

both the

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in two

days

and the

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in seven

days limits were exceeded

during the

same work week, with 26 and

91 hours0.00105 days <br />0.0253 hours <br />1.50463e-4 weeks <br />3.46255e-5 months <br /> having been

worked, respectively.

However, only the two hours that

exceeded

the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> limit were regarded

as shift turnover

time, while the

19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> that exceeded

the

72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

requirement

were given approvals

by the

PGM.

No specific

guidance

appeared

in procedure

AP-012 on

how to determine

shift turnover time.

Discussions

with maintenance

personnel

indicated that typically one hour per shift was classified

in this manner.

The inspector also noted that the plant technical

support

organization

was not formally included in the licensee's

program for controlling overtime.

The inspector identified

that certain technical

support engineers

have

been actively

involved in safety related activities,

and in some cases

have performed surveillance tests related to plant startup

activities.

A recent

issue

was documented

in ACFR 94-947

regarding the scheduling of engineers'ours

during RF0-5.

It was identified by licensee

personnel

that

a few engineers

had

been

scheduled

to exceed

the limits outlined in TS 6.2.2.f. without the

PGM's approval.

Licensee

management

corrected the specific scheduling

problems prior to RFO-5

and

a procedure

change

was submitted to incorporate

the

technical

support organization

in the licensee's

program.

The inspector also addressed

the scheduling of overtime to

cover for vacationing operators,

operators

in training,

and

other routine situations that

may be considered

to be

"foreseen"

by management.

The inspector

reviewed weekly

operations

schedules

for non-outage

months

and concluded

that, while overtime is being

used in those situations, it

is not being used excessively

and is therefore in compliance

with the intent of Technical Specification 6.2.2.f and other

NRC guidance.

The inspectors

concluded that overall the licensee

had the

proper program in place for controlling overtime,

and that

implementation

was satisfactory.

The inspectors

informed

plant management

of the areas

noted

above related to the

classification of shift turnover time and the incorporation

of technical

support engineers

into the licensee's

program.

No violations or deviations

were identified.

Review of Nonconformance

Reports

Adverse Condition Feedback

Reports

(ACFR) were reviewed to

verify the following:

TS were complied with, corrective

actions

and generic

items were identified and items were

reported

as required

by 10 CFR 50.73.

Adverse Condition

& Feedback

Report 94-1027

documented

an

example of poor communications

which occurred

on March 26,

1994.

An off-shift operator

was tasked with removing the

clearance

from process

instrumentation

cabinet ¹3 (PIC-3)

and then reenergizing it.

The operator

was

handed the

applicable procedure,

OP-156.02,

AC Electrical Distribution,

which had

been

marked

up by a shift operator

who was

originally intended to perform the activity.

Prior to

performing the task,

the off-shift operator

informed control

room operators

what was about to occur.

After discussions

with control

room operators,

the off-shift operator

proceeded

with energizing cabinet

PIC-3.

Moments later, the

control

room received

several

alarms

and indications that

the "A" ESW pump had auto-started.

A shift operator

was

dispatched

to the IDP-lA-SIII instrument

bus

(which powers

PIC-3) who discovered that the off-shift operator

had

performed steps

in procedure

OP-156.02 for reenergizing

the

entire instrument 'bus.

That evolution involved deenergizing

several

other instrument cabinets first, including one which

processed

"A" ESW header

pressure

and flow data.

The

resultant

"loss of

ESW pressure"

led to the "A" pump auto-

starting.

Operators

quickly corrected

the situation

by

reenergizing

the affected instrument cabinets.

Operator

accounts of this event later identified that the

operator

who originally marked

up the procedure

had marked

steps for cabinets

PIC-3,

9 and

13.

However, this operator

understood that

he was only to perform steps for energizing

PIC-3.

That intent had not been effectively communicated to

the off-shift operator ultimately tasked with performing the

evolution,

by neither the shift supervisor or the senior

reactor operators.

In reviewing this event,

the inspectors

concluded that the only safety

consequence

was that

an

ESF

component

was started

unnecessarily.

However, the above

circumstances

demonstrated

weak supervisory control

and

direction.

No violations or deviations

were identified.

Preparations

for Refueling

(60705)

Outage

Risk Assessment

Review

As discussed

in

NRC Inspection

Report 50-400/94-05,

licensee

personnel

had performed

an outage risk assessment

for the

refueling outage

using procedure

PLP-700,

Outage

Management.

During this inspection period, the inspectors

compared

the

licensee's

risk assessment

with the requirements

contained

in procedure

PLP-700,

and reviewed the level II outage

schedule,

to verify that the licensee

had avoided scheduling

high risk evolutions

when possible.

The inspectors

compared

procedure

PLP-700 to guidelines

contained

in NUREG-1449, the

NRC's Final Report

on Shutdown

and Low-Power Operation at

Commercial

Nuclear

Power Plants in the United States.

The

inspectors verified that procedure

PLP-700 addressed

all of

the shutdown or low power operations

requirements

referenced

in NUREG-1449,

and concluded that the procedure

was adequate

to be used

as

a basis for the licensee's

outage risk

assessment.

The inspectors

independently verified selected

attributes of

the outage

schedule.

The inspectors

noted that the outage

schedule

had

been developed to avoid establishment

of RCS

reduced

inventory or mid-loop conditions.

Since several

industry events

have occurred with the

RCS in reduced

inventory conditions,

the inspector considered

the exclusion

of these situations to be

a substantial

benefit to safe

operation while the plant was shutdown.

The outage

schedule

was discussed

with licensee

personnel

who demonstrated

to

the inspectors that the re'quirements

of procedure

PLP-700

were properly considered.

0

v

I J

~

N

5 ~i

g+

w)p

~-lq

The risk assessment

identified that two high risk evolutions

existed

in the outage

schedule.

Similar to the previous

refueling outage,

the activity to switch electrical

power

for the "A" spent fuel cooling

pump following the "A" train

electrical

bus outage

was considered

to be

a higher risk

evolution due to only one spent fuel cooling pump being

available to provide cooling water to the unloaded core.

The other evolution involved repairs to component cooling

water relief valve

1CC-129 which necessitated

the use of a

freeze

seal to isolate the valve.

Potential failure of the

freeze

seal

would jeopardize

CCW system availability.

The

inspectors

reviewed the licensee's

contingency plans for

these activities.

The plan for the

CCW valve repairs

minimized the time during which the freeze

seal

was relied

upon

and provided for a wooden plug to be installed if

necessary

to isolate leakage.

In addition, the availability

of the demineralized

water system

was ensured to provide

sufficient makeup water to the system in the event of freeze

seal failure.

As a followup to the comments

made in NRC Inspection

Report

50-400/94-05,

the inspectors

reviewed the licensee's

response

to an assessment

finding that no comprehensive

plan

for containment closure existed contingent

on a loss of RHR

shutdown cooling.

This item was discussed

with outage

management

and operations

personnel.

The licensee

made

revisions to procedure

AOP-20 to include necessary

PA

announcements

and to check containment penetration

breaches

for closure.

Containment penetration

status

would be listed

on

a tracking copy of procedure

OST-1091 in the work control

center.

A night order was written to notify operating

personnel

of the penetration

tracking requirement.

On March

24 the inspector

checked

the licensee's

actions

and asked to

view the status of containment penetrations.

The inspector

was informed that the previous shift had discarded

the

OST-

1091 tracking procedure.

A new tracking procedure

was

promptly reinitiated.

The inspector also noted that the

night order did not require the tracking status to include

persons

responsible for resealing

the penetrations if

necessary.

The inspector concluded that the licensee's

efforts in establishing

a containment closure plan were

poor.

No violations or deviations

were identified.

Independent

Procedure

Review

Prior to the onset of the refueling outage,

the inspectors

reviewed various

shutdown

and refueling related

procedures

to verify that certain areas,

including- prerequisites for

refueling, provisions for spent fuel inspections,

and

provisions for maintaining proper decay heat removal,

were

addressed.

The following procedures

were reviewed:

PLP-616

FHP-010

FHP-014

FHP-020

OST-1817

OST-1818

OST-1091

MST- I0169

MST- I0170

AOP-020

Fuel Handling Operations

Core Mapping Following Fuel

Loading

Fuel

and Insert Shuffle Sequence

Fuel Handling Operations

Refueling Machine (Manipulator Crane)

Operability Modes:

100 Hours Prior to Fuel

Movement in Pressure

Vessel

Auxiliary Hoist Operability:

100 Hours

Before Control

Rod Drive Movement in the

Reactor

Vessel

Containment

Closure Test Weekly Interval

During Core Alterations

and

Movement of

Irradiated fuel Inside Containment

Nuclear Instrumentation

System Source

Range

N31 Operational

Test

Nuclear Instrumentation

System Source

Range

N32 Operational

Test

Loss of RCS Inventory or Residual

Heat

Removal

While Shutdown

The fuel handling procedures all contained clear statements

of responsibilities for the key personnel

involved in fuel

movement activities.

Various precautions

and limitations

were contained

in the procedures

which addressed

requirements for flux monitoring; containment integrity;

communications

between

the main control

room, the

containment building,

and the fuel handling building; and

expected

actions following identification of damaged fuel

assemblies.

Additionally, the procedures

contained

provisions for checking refueling equipment operability,

underwater lighting, and adequate

water level

above the

reactor

vessel

flange during refueling.

Overall, the

inspectors

concluded that the above procedures

were

technically adequate

to accomplish the desired tasks.

No violations or deviations

were identified.

Refueling Activities (60710)

The inspectors

witnessed refueling activities

and verified that

the refueling was being performed in accordance

with TS

requirements

and approved

procedures.

Areas inspected

included

containment integrity, housekeeping

in the refueling area, shift

staffing during refueling, surveillance testing,

and periodic

monitoring of plant status

during refueling operations.

As part

of this inspection,

implementation of the following procedures

was

observed:

GP-008

Draining the Reactor Coolant System

II

GP-009

FHP-014

FHP-020

CH-H0094

Refueling Cavity Fill, Refueling,

and Draindown

of the Refueling Cavity

Fuel

and Insert Shuffle Sequence

Fuel Handling Operations

Integrated

Reactor

Vessel

Head

and Upper

Internals

Removal

The inspectors

witnessed

the removal of the core upper internals,

initial core offload,

and fuel sipping.

The licensee utilized an

underwater

camera to verify that no fuel elements

were lifted with

the upper internals.

Pre-evolution briefs were attended for the

upper internals lift and unlatching of the

RCCAs.

These briefs

were considered

to be very thor ough

and cautioned

operating

personnel

of excessive

reliance

on the contractors

performing the

work.

Licensee

performance

o'f these activities

was satisfactory.

The inspectors

also observed

the draindown of the

RCS to -10

inches

below the reactor vessel

flange

on Parch

26 in preparation

for head removal.

The controlling procedure for this evolution,

GP-008,

was reviewed.

The inspectors

noted that the procedure

contained

precise administrative controls to prevent

an

inadvertent

loss of RHR shutdown cooling.

These

procedure

controls were found to be properly implemented.

Even though

reduced

RCS inventory and mid-loop operations

were not entered,

the inspectors

detected

a heightened

sense of awareness

among the

control

room staff during this evolution.

The level in the

RCS

was monitored during the draindown with remote standpipe

level

indication,

a continuous

standpipe

watch inside containment,

and

the RVLIS.

The

RCS draindown

was stopped

at approximately

96 inches

when

operators

detected

a deviation between

RVLIS and the standpipe

indication.

The licensee utilized a curve which compared

RVLIS

upper range to the standpipe

indication.

The deviation

was caused

by two factors which included using the

RVLIS full range

indication vice upper range,

and disconnection of the RVLIS

reference

leg at

a different location from that in the past.

The

difference in length of the

new reference

leg necessitated

the

generation of a new comparison

curve.

When the

new curve was

implemented,

the

RVLIS and standpipe

indications

agreed

and the

draindown

recommenced.

The inspectors

considered

the control of

this evolution to be good.

However, the inspectors

considered

the

pre-evolution planning

and briefings to be deficient which did not

identify the appropriate

RVLIS range to utilize or where the

RVLIS

reference

leg would be disconnected.

Following a partial refueling cavity fill, the seal ring was found

to be leaking approximately

8 gpm.

This necessitated

another

dr aindown of the refueling cavity with the reactor vessel

head off

and the

RVLIS reference

leg capped.

Licensee

personnel

used

procedure

GP-009 to perform this activity.

This procedure

was

written under the assumption that the core

was offloaded prior to

0

~

L

0

F

wl

~,

1

'"*g * l

l 4

~

f~."j

10

draindown of the refueling cavity and did not include provisions

for diverse

RCS level monitoring.

Operators

nonetheless

monitored

RVLIS indications

and stationed

a watchstander

at the

standpipe

to monitor

RCS level.

The inspector considered

these

precautions

to be very good

and minimized the potential for a loss

of RHR shutdown cooling.

It was also noted that procedure

GP-009

could

be strengthened

by the addition of these precautions.

No violations or deviations

were identified.

Followup of Onsite

Events

(93702)

At approximately

10:00 p.m.

on March 27,

1994 while in the main

control

room, the inspector

observed that operators

received

a

call from the corporate

load dispatcher notifying them that

a

tornado watch was in effect.

The operators

promptly entered

administrative

procedure

AP-301, Adverse Weather Operations,

and

documented

the entry in the control

room logs.

Upon receiving

notice of a tornado watch,

procedure

AP-301 required operators

to

complete

a detailed checklist that verified certain controls were

in place (i.e., loose material

removed or tied down, outlying area

doors shut, fire pumps operable,

external lighting energized,

operability of various safety related

equipment including EDGs).

However, the inspector

knew the tornado watch

had

been in effect

prior to 9:00 p.m. that evening

and inquired to operations

personnel

about the suspected

delay in notification.

Operations

personnel

informed the inspector that the load dispatcher

had only

been

informed ten minutes prior to plant notification.

The

inspector contacted

the National

Weather Service

(NWS) to

ascertain

when the tornado watch actually went into effect.

According to the

NWS, Tornado Watch 847, covering

Wake County and

the majority of the state of North Carolina,

went into effect at

7:30 p.m.

on Harch 27,

1994

and did not cease until 2:00 a.m.

on

March 28,

1994.

The inspector determined that there

had

been

a

two and one-half hour delay between the tornado watch being

declared

and key plant personnel

being notified.

Considering the number of actions

necessary

to take following

notification of a tornado watch or warning, the rapid rate at

which severe

storms

can travel,

and potential

damage

which could

be inflicted upon plant equipment, it is beneficial for the plant

to receive

such information promptly.

The inspectors

discussed

this notification delay with plant management

who stated that they

would investigate it.

No violations or deviations

were identified.

J

~

J'

'

l

11

Maintenance

a.

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify

that correct equipment

clearances

were in effect; work requests

and fire prevention work permits were issued

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following maintenance activities:

~

Preventive

maintenance

on battery charger

IA-SB in

accordance

with procedure

PM-E0023,

C&D Battery Chargers.

Installation of new manually operated

valve lAF-208 for "B"

motor driven

AFW pump discharge

isolation in accordance

with

modification PCR-6502.

Replacement

of rotating element for the "A" motor driven

AFW

pump in accordance

with procedure

CM-N0039, Ingersoll-Rand

Motor Driven Auxiliary Feedwater

Pump Size

3 HHTA-9

Disassembly

and Maintenance.

Replacement

of motor operator with hand wheel for valve 1AF-

5 in accordance

with modification PCR-6925

and procedure

CN-

M0051, Limitorque Valve Operator Size

SB/SMB-00 Disassembly

and Maintenance.

Switchover power feed for the "C"

CCW pump motor from "A"

train to "B" train in accordance

with procedure

CH-H0013,

Electrical

Power

Feed Switchover For Component

Cooling Water

Pump

1C-SAB.

Packing adjustment

on 1AF-51

Bridge and megger

"C" CSIP motor in accordance

with NPT-

E008, Environmentally gualified 6.9

KV Motor Electrical

Inspection;

and troubleshooting to determine

cause of-

ground.

Secure

cables to the

DC distribution panel cabinet

raceway

as described

in drawing 2166-B-060 Sheet

97.

Perform lifttest

on relief valve

1SW-171 'in accordance

with

procedure

EST-211, Auxiliary Relief Valve Testing.

In general,

the performance of work was satisfactory with proper

documentation of removed

components

and independent verification

of the reinstallation.

(1)

The inspectors

reviewed the activities of the

EKRC planner

who has

been

assigned

to the work control center.

The

~ licensee

has attributed substantial

radiation exposure

dose

0

I

12

savings to these efforts.

Planning activities included dose

reduction

and contamination control technique

incorporation

into maintenance

work requests.

Work tickets were grouped

for work in high radiological risk areas for better

HP

coverage

and work for areas that had

been shielded for other

jobs was coordinated

and scheduled.

Scheduling of RHR

system outage

PMs online to avoid working on this system

when dose rates

are higher was also performed.

The

inspectors

considered this aspect of work control to be

effective in lowering personnel

exposures.

(2)

As a followup to the comments

in

NRC Inspection

Report 50-

400/94-05,

the inspectors

noted another

example of poor

coordination of work activities with planned surveillance

testing.

During the week of February

28,

1994, licensee

personnel

performed maintenance

on several different valves

associated

with the

ESW system

(1SW-130,

1SW-127,

1SC-30,

1SW-204,

1SW-132,

and

1SW-129) which necessitated

partial

performances

of procedure

OST-1215,

Emergency Service Water

System Operability Train

B quarterly Interval, to stroke

time the valves

as part of post maintenance

testing.

Approximately four partial tests

were performed during this

week.

On the following week of March

7 the entire test

-procedure

was scheduled

to be performed.

The inspector

considered

the work activities/test

scheduling effort to be

deficient

and resulted

in redundant

component testing

and

equipment out of service time.

(3)

The inspector

observed

the performance of preventive

maintenance

on the battery charger which verified the

current limiting device.

Battery charger current

was found

to be limited to 172 amperes.

The inspector noticed that

procedure

PM-E0023 specified

an acceptable

range for this

current

between

171.64 - 173.36

amperes.

The inspector

further noticed that the computerized test

system

measured

this current

and provided indication to the nearest

whole

ampere.

- The -inspector -considered

the specified

acceptance

criteria to be irrelevant

since current indication could not

be measured

to the nearest

hundredth of an ampere.

This

observation

was brought to the attention of the maintenance

supervisor

who stated that appropriate

procedure

changes

would be implemented.

No violations or deviations

were identified.

Surveillance Observation

(61726)

Surveillance tests

were obse} ved to verify that approved

procedures

were being used; qualified personnel

were conducting

the tests; tests

were adequate

to verify equipment operability;

calibrated

equipment

was utilized; and

TS requirements

were

followed.

The following tests

were observed

and/or data reviewed:

1'I

13

HST-EOOll, lE Battery quarterly Test

HST-I0133, Hain Steamline

Pressure,

Loop

3 (P-0496)

Operational

Test

OST-1813,

Remote

Shutdown

System Operability 18 Honth

Interval

Hades

5 or 6.

OST-1091,

Containment

Closure Test Weekly Interval During

Core Alterations

and Hovement of Irradiated

Fuel Inside

Containment.

HST-E0010,

lE Battery Meekly Test

OST-1011, Auxiliary Feedwater

Pump lA-SA Operability Test

EST-209,

Type

B Local

Leak Rate Tests

The performance of these

procedures

was found to be satisfactory

with proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and knowledgeable

personnel

having performed the

tasks.

The quarterly battery test

was being accomplished

on

a

monthly frequency.

Good use of personnel

protective equipment

was

observed

during the performance of this test.

The inspectors

observed

some of the preparations

for complex tests

to be performed during this refueling outage.

Operations

personnel

have prepared briefing packages

for the complex tests.

These

packages

included

a summary of the test procedure,

breakdown

of manpower requirements

to perform specific tasks,

the

PLP-100

briefing papers for the performance of infrequent tests

and

evolutions,

and applicable industry events

which have occurred

during the performance of the specific test.

The inspectors

attended

a pre-evolution briefing for procedure

OST-1813.

The items discussed

above were thoroughly covered.

The

test

was subsequently

performed without incident.

The inspectors

considered

the preparations

for the performance of these

types of

tests to be

a program strength.

An activity was allowed to be performed concurrently with

procedure

OST-1813 to deenergize

instrument cabinet

PIC-3 for RTD

bypass elimination modification wor k.

When cabinet

PIC-3 was

deenergized

the P-13 permissive

was activated

which generated

a

turbine trip/reactor trip signal.

The reactor trip breakers

were

open at the time this signal

was generated

which alleviated

reporting requirements.

However, this event necessitated

delaying

the performance of procedure

OST-1813 since the reactor trip

breakers

were required to be closed during performance of other

portions of the test.

The inspectors

considered

the decision to

4

4

4

~

4

1

deenergize

PIC-3 during the performance of the test procedure to

be poor.

No violations or deviations

were observed.

Engineering

Design

Changes

and Modifications (37828)

Plant

Change

Requests

(PCR) involving the installation of new or

modified systems

were reviewed to verify that the changes

were reviewed

and approved

in accordance

with 10 CFR 50.59, that the changes

were

performed in accordance

with technically adequate

and approved

procedures,

that subsequent

testing

and test results

met approved

acceptance

criteria or deviations

were resolved in an acceptable

manner,

and that appropriate

drawings

and facility procedures

were revised

as

necessary.

In addition,

PCR's documenting

engineering

evaluations

were

also reviewed.

The following modifications and/or testing in progress

was observed.

a 4

The inspector

attended

an

RTD bypass manifold overview training

course

which was presented

to a wide variety of licensee

personnel

involved with modification

PCR 0420,

RTD Bypass Elimination.

The

overview training was

an introductory level course

which covered

the history of the

RTD bypass manifold problems which led to the

pending removal.

It also covered the logistics of the whole

project from demolition of the old manifold piping, to

installation

and welding of the

new

RTDs (to be directly immersed

in the

RCS loop piping).

By using floor elevation sketches,

the

course instructor discussed

radiological protection plans which

included low dose waiting areas for personnel

and logistics for

removing highly radioactive

bypass manifold piping from the

containment structure.

b.

In addition, the inspector walked down and observed training on

a

mockup of the

RTD bypass

manifolds which was setup in one of the

plant's warehouses.

The mockup training classes

were presented

to

individual work groups which were responsible for various aspects

of the

RTD bypass

removal project.

The training classes

were

custom designed for each work group depending

on that group's job

(e.g., insulation removal, demolition of old piping, placement of

radiological shielding,

or decontamination).

The mockup was

an

impressive

model of a typical Harris

RCS loop.

An entire

RTD

bypass manifold was depicted

as

was its associated

isolation

and

drain valves,

and its connections

to the

RCS hot, cold,

and

crossover

legs.

Physical conditions

such

as elevations,

scaffolding,

and layout of trash

removal

paths

were also mimicked.

The

RTD bypass manifold training efforts were considered to be

good.

Several

ACFRs were generated

over the past

few months related to

untimely revision of procedures

affected

by PCRs.

An engineer

15

reviewing procedures

in August

1993 noted that

PCR-6540

was closed

in April 1993 but the affected

procedures

were never revised.

An

ACFR was generated

(ACFR 93-317) to document this discrepancy.

The

PCR was

a document-change-only

PCR which revised torque values

for fasteners

used in electrical

connections.

In January

1994,

one of these

procedures

was being used for maintenance

when

electricians

discovered that the

same

procedures still had not

been revised to incorporate

the

new torque values.

Another ACFR

was generated

(ACFR 94-400)

on January

26,

1994 to document this

fact.

Due to previous

and subsequent

problems with timely procedure

changes

caused

by PCRs,

an event review team

was established

to

investigate

the above

ACFRs and to recommend corrective actions.

Since there

had

been

no formal method for ensuring that procedures

affected

by document-change-only

PCRs were revised following PCR

closeout,

one corrective action that had already

been

implemented

for ACFR 93-317 was to develop

a list of required procedure

changes

from document-change-only

PCRs

and incorporate the list

into the newly created

Nuclear Revision Control

System

(NRCS)

computer tracking system.

Procedure writer groups routinely

received

a printout of the outstanding

procedure

change list

generated

by NRCS.

Some procedure writers effectively utilized

the NRCS-generated list.,

However, others did not fully understand

the relationship

between

PCRs,

the

new

NRCS system,

and the

procedure

change

process.

The event review team noted that no

existing plant procedures

described

the above relationship or how

NRCS should

be used.

The team

recommended

the development of such

a plant procedure,

along with the training of procedure writers on

NRCS,

as corrective actions.

Concerning

ACFR 94-400

the event review team noted that the

corrective actions for ACFR 93-317 focused

on correcting the

generic

problem (updating the

NRCS database

with outstanding

procedure

changes)

and not the specific maintenance

procedures

identified in ACFR 93-317.

The

ACFR was closed

based

on

completion of the more generic corrective actions.

The'event-

review team

recommended

that this situation

be reviewed with the

involved organizations

to improve their understanding

of the

ACFR

process

and improve communications

between

work groups.

In a separate

incident,

on January

27,

1994,

an operator initiated

ACFR 94-401 to document that control

room alarm response

procedures

had not been revised to incorporate

new alarm setpoints

for three

emergency

exhaust

fan units.

Plant

Change

Request

6731,

modified the setpoints

and required that the documents

be changed

prior to

PCR turnover but not prior to implementation.

Since

partial implementation

occurred well before turnover,

a delay

occurred

between

the time that the setpoints

were changed

in the

field and the time the procedures

would have reflected those

changes.

Upon discovery,

the affected procedures

were revised via

the temporary

change

process.

i

~ E

Ilk

7

16

The event review team for ACFRs93-317

and 94-400 also

investigated

ACFR 94-401.

The corrective action proposed for ACFR

94-401

was to develop

a process for linking work tickets to

prerequisite

or subsequent

manual

tasks (i.e., procedure

and/or

drawing changes).

These

manual

tasks

would be formally tracked

by

the work control process

to ensure that field changes

affecting

working procedures

are incorporated

into those

procedures

in

a

timely manner.

The event review team presented

the

above

recommended

actions for

the two events

before the

PNSC

on Harch ll, 1994.

The proposed

corrective actions

were approved.

In addition, the team provided

an assessment

of the safety significance of the

above events

and

concluded that neither of the specific cases

had

any safety

consequences.

In the case of the fastener

torque specifications,

the worst consequence

in using the unrevised

procedures

would have

been using old values to which the plant had always

been designed.

For the three

emergency

exhaust

fan units,

PCR-6731 actually

lowered their alarm setpoints to ensure that alarms

came in before

TS differential pressure limits were exceeded.

Due to the low

significance of these

items, the event review team

recommended

that the corrective actions

be given due dates

beyond the

completion of the current refueling outage.

The inspector

attended

the

PNSC meeting

and concluded that while

the specific examples

noted

above did not have safety

significance,

the licensee

had identified areas

in need of

improvement.

Along with the areas

discussed

above,

the inspectors

noted that even after corrective actions

were implemented for the

initial discovery of PCR-6540 procedural

deficiencies,

the

NRCS

system which was

used for verifying working documents

(and relied

upon heavily in the event review team's

recommended

corrective

actions)

did not flag to the user in January

1994 that the

maintenance

procedures

required

changes.

The inspector's

overall conclusion

was that the licensee's

implementation of procedure

changes

following modifications

was

poor.

Licensee

management

agreed that more attention

was

needed

in the area of PCR implementation.

No violations or deviations

were identified.

Plant Support

'a ~

Plant Housekeeping

Conditions

(71707)

- Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout

the facility were observed to determine

whether safety and/or fire

hazards

existed.

b.

Radiological Protection

Program

(71707) - Radiation protection

control activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

17

procedures,

and in compliance with regulatory requirements.

The

inspectors

also reviewed selected

radiation work permits to verify

that controls were adequate.

The inspectors

reviewed licensee efforts in reducing radiation

"hot spots" which existed in several

plant areas.

These efforts

were responsible for significant reductions

in radiation dose

rates for the

VCT room,

RCS filter valve gallery,

and for the

filter backflush storage

tank room.

Reductions

by a factor of 10

were achieved

in these

areas.

The inspectors

considered

the

licensee's

dose reduction efforts to be successful.

On February 8,

1994, the inspectors

found

a key which was similar

to those

used

by the

HP department to control

access

to plant

areas.

The inspector

informed licensee

personnel

of this matter

and discussed

possible

doors which this key could provide access

through.

The inspector

was informed that this type of key (RCl-1)

was

a generic

key which would allow access

to equipment

storage

areas

and to several

plant areas

which contained

abandoned

equipment.

Typically the storage

areas

were for supplies

in

general

use

by decontamination

personnel.

The abandoned

equipment

rooms were infrequently visited and not routinely surveyed

therefore,

access

was controlled by these

types of keys.

The

inspectors

toured plant areas

which were classified

as

LHRAs.

The

inspectors verified that the RCl-1 key would not allow access

to

these

areas.

The key was subsequently

returned to

HP personnel

on

February

25.

The inspector discussed

control of these

keys with

HP personnel.

In contrast to the good controls established

for

LHRA keys, the licensee

simply maintained

an informal log of RCl-1

key holders.

No plant procedure controlled the issuance/use

of

these

types of keys.

No violations or deviations

were identified.

Security Control

(71707)

- The performance of various shifts of

the security force was observed

in the conduct of daily activities

which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed the operational

status of

closed circuit television monitors, the intrusion detection

system

in the central

and secondary

alarm stations,

protected

area

lighting, protected

and vital area barrier integrity,

and the

security organization interface with operations

and maintenance.

On March 5,

1994, while on routine patrol,

a security officer

located

an unattended

vehicle with keys left in the ignition.

The

vehicle was parked inside the protected

area

and

had

been driven

by a contract

employee.

Upon discovery,

the keys were removed

from the vehicle

and returned to the responsible

individual's

supervisor

who was reminded of the importance of maintaining

proper control of vehicles within the protected

area.

18

d.

Previous

problems

have

been identified regarding vehicle control.

A non-cited violation (400/93-20-03)

was issued

in October

1993

for failing to secure

a vehicle parked within the protected

area

on April 15,

1993.

In addition, the licensee's

NAD organization

has identified three other occasions

(September

27,

30 and October

13,

1993) where vehicles

were not positively controlled

as

required

by the licensee's

Physical Security Plan.

Following

those

instances,

the licensee

implemented

several

corrective

actions which included briefing licensee

and contract personnel

on

the importance of securing designated

vehicles.

Written articles

on the control of designated

vehicles

appeared

in the weekly plant

newsletter

and

on video screens

located throughout the plant.

Interviews with security personnel

indicated that the individual

responsible for the March 5,

1994 incident

had signed

a roster

indicating that training on the requirement for controlling

designated

vehicles

had

been provided.

In addition, the affected

vehicle

had

been

equipped with a placard

on the dashboard

reminding the driver to "Remove Ignition Key Prior to Exiting

Vehicle".

The licensee

concluded that the Harch

5 incident was

clearly due to personnel

error.

The licensee's

Physical

Security Plan,

paragraph

1.6.4. l.a,

and

Procedure

SP-007,

Access

Control

5 Personnel

Identification,

require positive control over designated

vehicles.

The several

examples

above indicate that the licensee's

security plan is not

being properly implemented

which is considered

to be

a violation.

Violation (400/94-06-01):

Failure to properly control vehicles

inside the protected

area.

Fire Protection

(71707)

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing was

appropriate

and that fire alarms,

extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to radiological

controls, fire protection requirements,

and

TS requirements

in these

areas

was satisfactory.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

I) at the conclusion of the inspection

on April 2,

1994.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violation addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received.

19

Item Number

Descri tion and Reference

400/94-06-01

Failure to properly control designated

vehicles,

paragraph

5.c.

Acronyms

and Initialisms

ACFR

AFW

CCW

CFR

CSIP

EDG

ESF

ESW

E&RC

GP

GPM

HP

KV

LHRA

NAD

NRC

NRCS

NWS

PA

PCR

PIC

PGM

PM

PNSC

RCCA

RCS

RFO

RHR

RTD

RVLIS-

STA

TS

VCT

Adverse Condition Feedback

Report

Auxiliary Feedwater

Component

Cooling Water

Code of Federal

Regulations

Charging Safety Injection

Pump

Emergency Diesel

Generator

Engineered

Safety Feature

Emergency Service

Water

Environmental

and Radiological Controls

General

Procedure

Gallons

Per Minute

Health Physics

Kilovolt

Locked High Radiation Area

Nuclear Assessment

Department

Nuclear Regulatory

Commission

Nuclear Revision Control

System

National

Weather Service

Public Address

Plant

Change

Request

Process

Instrumentation

Cabinet

Plant General

Manager

Preventive

Maintenance

Plant Nuclear Safety Committee

Rod Cluster Control Assembly

Reactor Coolant System

Refueling Outage

Residual

Heat

Removal

Resistance

Temperature

Detector

Reactor

Vessel

Level Indication System

Shift Technical Advisor

Technical Specification

Volume Control Tank

4

0