ML18009A381

From kanterella
Jump to navigation Jump to search
Insp Rept 50-400/89-34 on 891118-900105.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance Observation, Maint Observation,Lers & Sys Engineer Program
ML18009A381
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 01/31/1990
From: Dance H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18009A379 List:
References
50-400-89-34, NUDOCS 9002150260
Download: ML18009A381 (21)


See also: IR 05000400/1989034

Text

~p8 REcy

~C+ 'p0

Cy

n0

t

Cy

~>>*<<+

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/89-34

Licensee:

Carolina

Fewer

and Light Company

P.

0.

Box ".551

Raleigh,

N" 27602

Docket No.:

50-400

Facility Name:

Harris

1

License

No.:

NPF-63

Inspection

Conducted:

November

18,

1989

January

5,

1990

,/

Inspectors:

J'.

Tedrow, Senior Resi)ent

Inspector

'4>~ !~

.M. Shannon,

Resident

Inspector

Approved by:

C

.

H. Dance,

Se tion Chief

Division of Reactor Projects

Da'te Signed

/ ~3i ~FD

Date Signed

i)/,/

Date Signed

SUMMARY

Scope:

This routine inspect'n

was

conducted

by two resident,

inspectors

in the areas

of

plant

operation.;

radiological

controls;

security;

fire protection;

surveillance

observa:ion;

maintenance

observation;

licensee

event

reports;

non-conformance

repo";s;

system

engineer

program;

fitness for duty training;

design

changes

and modifications;

plant startup

from refueling;

followup of

onsite events;

and

1

=ensee

action

on previous inspection

items.

Results:

Two violations were identified:

Failure to perform surveillance testing for an

inoperable

emergency

diesel

generator,

paragraph

3.a;

Failure

to

properly

implement surveillance

procedures,

paragraphs

3.b and 3.c.

An unresolved

item is identified in paragraph

6.a concerning

the operability of

the main

steam lines when filled with condensate.

A licensee

identified violation is discussed

in paragraph

6.b concerning

a

failure to perform

a visual inspection of check-valve internals.

9OP21-02 ", O~,OOI)4OO

90013k

PDR AQOCDC

0

Operational

weaknesses

are

discussed

in

paragraph ll, concerning

secondary

plant transients

causing

AFM actuations,

and paragraph

6.a, fai lure to control

heatup activities which resulted

in a main

steam safety actuation,

and filling

of main steam lines with condensate

during plant heatup.

REPORT DETAILS

Persons

Contacted

Licensee

Employees

S. Allen, Fitness for Duty Site Coordinator

D. Braund',

Supervisor,

Security

J. Collins, Manager,

Operations

  • G. Forehand,

Director,

QA/AC

"C. Gibson, Director,

Programs

and Procedures

"P. Hadel, Project Spec'ialist,

Planning

"J.

Hammond,

Manager,

Onsite Nuclear Safety

"C. Hinnant, Plant General

Manager

"D. McCarthy, Unit Manager,

Site Engineering

T. Morton, Manager,

Maintenance

C. Olexi k, Supervisor, Shift Operations

"H. Powell, 'Manager, Training

"R. Richey,

Manager,

Harris Nuclear Project Department

  • J. Sipp,

Manager,

Environmental

and Radiation Monitoring

  • J. Smith, Supervisor,

Radwaste

Operation

"D. Tibbits, Director, Regulatory

Compliance

  • R. Van Metre, Manager,

Technical

Support

  • M. Wallace,

Senior Specialist,

Regulatory Compliance

E. Willett, Manager,

Outages

and Modifications

Other

licensee

employees

contacted

included

office,

operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms

used

through-out this report

are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant

began

this

inspection

period in

a refueling

outage with the

reactor vessel

defueled.

The outage activities included repairs of damage

which

resulted

from

the

turbine

generator/main

transformer

fire

on

October

9,

core refueling,

an integrated

leak rate test of containment,

and

steam

generator

eddy-current

testing.

On

November

23

refueling

activities

(Mode 6) were

recommenced

and the core

was completely refueled

on November 25.

Following installation

and torquing of the reactor vessel

head,

the plant entered

cold shutdown

(Mode 5) at 4:30 p.m.

on December

1.

A plant

heatup

was

commenced

and

the

hot-standby

condition

(Mode

3)

reached

on

December

17.

On

December

20

a reactor start-up

was performed

followed by reactor criticality at 9:47 a.m.

Power operation

(Mode I) was

resumed

at

5: 17

a.m.

on

December

22.

The plant

continued

in

power

operation

(Mode 1) for the duration of this inspection period.

Power

was

limited to approximately

75;o due to an inoperable

main

steam safety valve

(see

paragraph

6.a for details).

The

inspector

reviewed

records

and

discussed

various

entries

with

operations

personnel

to

verify

compliance

with

the

Technical

Specificat,ions

(TS)

and

the

licensee's

administrative

procedures.

The

following records

were reviewed:

Shift Foreman's

Log; Control Operator's

Log; Auxiliary Operator'

Log;

Night, Order

Book;

Equipment

Inoperable

Record; Active Clearance

Log; Jumper

and Mire Removal

Log; Shift Turnover

Checklist;

and selected

Chemistry/Radiation

Protection

and

Radwaste

Logs.

Throughout

the inspection

period facility tours were conducted to observe

operations

and maintenance

activities in progress.

Some

operations

and

maintenance activity observations

were conducted

during backshifts.

Also,

during this

inspection

period,

licensee

meetings

were

attended

by the

inspectors

to observe

planning

and

management

activities.

The facility

tours

and

observations

encompassed

the

following

areas:

security

perimeter

fence;

control

room;

emergency

diesel

generator

building;

reactor

auxiliary building;

waste

processing

building;

fuel

handling

building; emergency

service water building; battery

rooms;

and electrical

.switchgear

rooms.

During these tours,

the following observations

were

made:

a.

Monitoring

Instrumentation

-

Equipment

operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

lineup,

reactor

operating

parameters,

and

auxiliary

equipment

operating

parameters

were observed

to verify that indicated

parameters

were

in

accordance

with the

TS for the current operational

mode.

During

a control

room tour

on December

30,

1989 the inspector

noted

that the

upper

and

lower power

range

nuclear

instruments

for NI-44

were

in

channel

defeat.

The

instruments

had

not

been

declared

inoperable

and

no surveillance

testing

was

in

progress.

During

discussions

with

plant

operators,

the

inspector

learned

that

operators

had placed the channel

in defeat

because

of low NI readings

which caused

both

an upper

and lower flux deviation alarm.

Although

no apparent

TS action applied,

this action to remove

an

instrument

channel

from service without declaring it inoperable is considered

to

be

a poor practice.

b.

Shift Staffing -

The

inspectors

verified that

operating

shift

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner

.

In addition,

the

inspector

observed

shift turnovers

on

various

occasions

to verify

the

continuity

of plant

status,

operations

problems,

and

other

pertinent

plant

information during

these

turnovers.

C.

Plant

Housekeeping

Conditions - Storage

of material

and components,

and cleanliness

conditions of various

areas

throughout the facility

, were

observed

to

determine

whether

safety

and/or fire

hazards

existed.

Radiological

Protection

Program

-

Radiation

protection

control

activities

were

observed

routinely to verify that

these activities

were in conformance with the facility policies

and procedures,

and in

compliance

with

regulatory

requirements.

The

inspectors

also

reviewed

selected

RWPs to verify that the

RWP

was current

and that

the controls were adequate.

Security

Control

In the

course

of the

monthly activities,

the

inspector

included

a

review of the

licensee's

physical

security

program.

The performance

of various shifts of the security force was

observed

in the conduct of daily activities to include:

protected

and vital area

access

controls;

searching

of personnel,

packages,

and

vehicles;

badge

issuance

and retrieval;

escorting

of visitors;

patrols;

and compensatory

posts.

In -addition, the inspector

observed

the operational

status

of Closed Circuit Television

(CCTV) monitors,

the Intrusion Detection

system

in the central

and

secondary

alarm

stations,

protected

area -.lighting, protected

and vital area barrier

integrity,

and the security organization

interface

with operations

and maintenance.

Fire Protection - Fire protection activities, staffing and equipment

were

observed

to verify that fire brigade staffing

was appropriate

and that fire alarms,

extinguishing

equipment,

actuating

controls,

fire fighting equipment,

emergency

equipment,

and fire barriers

were

operable.

No violations or deviations

were identified.

3.

Surveillance Observation

(61726)

Surveillance

tests

were

observed

to verify that approved

procedures

were

being

used;

qualified

personnel

were

conducting

the tests;

tests

were

adequate

to

verify

equipment

operability;

calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following

GP-002

OST-1004

OST-1005

OST-1036

OST" 1073

OST-1804

EPT-069

tests

were observed

and/or data

reviewed:

Normal Plant Heatup

From Cold Solid to Hot Subcritical

Power

Range

Heat Balance

'ontrol

Rod and

Rod Position Indicator Exercise

Shutdown Margin Calculation

1B-SB Emergency

Diesel Generator Operability Test

RHR Remote Position Indication and Timing

Initial Criticality

EPT-152T

Main Steam Safety Valve Test at Power

EST-202

Main Steam Safety Valve Test

During- the performance

of-OST-1073

on December

31, the "B" Emergency

Diesel

Generator

started

but did not stabilize within the required

frequency

range.

TS 4.8.1.1.2.a.4

requires that the diesel

generator

shall

start

and

accelerate

to

synchronous

speed

with

a generator

voltage

of

6900

+690 volts

and

frequency

of

60 +1.2

hertz

(Hz)

within

a

10

second

time period.

The diesel

generator initially

stabilized at

a frequency

of

62

Hz

and

returned

to

60

Hz in

58

seconds.

Operators

declared

the diesel

inoperable at 10:40 p.m.

and

implemented

the requi rements

of TS 3.8. 1. 1 action "b".

This action

statement

specifies that with one diesel

generator

inoperable,

the

AC

offsite

power

sources

shall

be

demonstrated

operable

by verifying

correct

breaker alignment

and power availability wi,thin one hour and

at least

once per

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter.

Subsequent

review of this matter

by licensee

personnel

determined

that

the

diesel

generator

was

capable

of performing its safety

function

and therefore

should

not

have

been

considered

inoperable.

At 9:45 a.m.

on January

1, the diesel

generator

was declared

operable

even

though it was not capable

of satisfying

the requirements

of

TS 4.8. 1. 1.2.a.4.

implementation

of

the

requirements

of

TS 3.8. 1. 1

action "b" were discontinued at this time.

During

a

review of

the

shift

foreman's

log

on

January

2,

the

inspector

noticed

the

above

sequence

of events

and

discussed

this

situation with licensee

management.

The licensee

was

informed that

the

TS

had

not

been

complied with and that the "B" diesel

generator

should

not

be

considered

operable.

The

"B" diesel

generator

was

subsequently

determined

to be inoperable

by the licensee at 2:35 p.m.

on January

2.

Although the offsite

power

source

remained

available

during this

event, failure to continue to perform the breaker alignment

and power

availability

verification

surveillance

for

the

AC offsite

power

sources

for

an inoperable diesel

generator

every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, is contrary

to

the

requirements

of

TS 3.8. 1. 1

and

is

considered

to

be

a

violation.

Violation (89-34-01):

Failure to perform surveillance testing for an

inoperable

emergency diesel

generator.

During

the

performance

of

procedure

OST-1804

on

November

28,

operators

observed

an

increase

in reactor

vessel

level.

The plant

was in

Mode

6

on "B"

RHR system cooling.

The "A" RHR system

was

aligned for standby

operation

with valves

RH-1

and

RH-2,

Reactor

Coolant

System

Loop

Suction

Valves,

open.

Procedure

OST-1804

directed

valve 1SI-322,

Refueling Water Storage

Tank Suction to "A"

RHR Pump, to be stroked

open

and then closed.

When operators

stroked

open this valve,

a flowpath was created

from the

RWST to the reactor

'vessel

through

valves

RH-1

and

RH-2,

allowing

borated

water

to

gravity drain into the reactor vessel.

The reactor

vessel filled,

and

contaminated

water

overflowed

into

the

seal

table

area

of

containment

through

open

instrument guide tubes.

Licensee

personnel

estimated

that approximately

25 gallons of water overflowed into the

seal

table

area.

No

personnel

contaminations

or equipment

damage

resulted

from this event.

Step

3. 1 of procedure

OST-1804

specifies

a prerequisite

for

the

performance

of this test

and requires that the

system being tested

be

aligned in

a

manner that will support

the

performance

of the test.

This

step

had

been

completed

and initialed by the senior control

operator.

Failure to'dequately

review the "system lineup to ensure

that the

system

was aligned for the safe

performance of the test is

contrary to the requirements

of procedure

OST-1804

and is considered

to be

a violation of TS 6.8. l.a.

Violation (89-34-02):

Failure to adhere

to the requirements

of

plant

procedures

which resulted

in

a spill of contaminated

water

into the seal

table area of containment.

Upon further review of procedure

OST-1804,

the inspector

noticed

a

discernible

lack of precautions

and limitations.

Only

a

statement

addressing

system operability and

a statement

regarding

radiological

controls

were

included.

The

lack of

any

specific

precautions

alerting- operators

to the potential

for this

type .of

event

is

considered

to be

a contributing cause for this event.

The

inspector

conducted

a

review of the

licensee's

activities to

adjust the

power

range

nuclear

instruments

following a calorimetric

calibration.

Following the calorimetric, plant personnel

noted that

the "fine" gain potentiometer

for the nuclear

instruments

did not

have

an

adequate

range

to adjust

the NI's to the required

values.

The fine gain potentiometer

is located

on the front panel of each

NI

channel

and is used

by operations

personnel

following a calorimetric

calibration to adjust

the

channel

as

needed.

Therefore,

a

course

gain potentiometer,

which is located

inside

the channel

drawer,

was

used

to

make

the calorimetric adjustment.

The inspector

discussed

this action with the

I&C foreman

and

learned that

he was not aware

that

a course

adjustment

had been

made.

Attachment VII of procedure

OST-1004 specifies

the steps

necessary

to

adjust

the

NI gain,

and

states

that if there

is insufficient

adjustment

on gain potentiometer

R303 (fine gain adjust),

then

a work

request will be initiated for I&C personnel

to adjust the course

gain

potentiometer.

This work request

was not generated

as required.

The inspector

was also

informed that the course

adjustment

was

made

without utilizing plant

procedures.

The

existing

procedure

for

performing this evolution would not have

been

adequate

to achieve

the

required final course

adjust position.

The licensee

plans in future

cases

to set the course adjust

by detailed

work instructions

in the

work request.

The

failure

to

generate

the

work

request,

which

would alert

management

to

changing

plant conditions

as

required

by procedure

OST-1004,

is

considered

to

be

another

example

of the violation

discussed

in paragraph

3.b of this report.

'ne violation with two examples

was identified.

4.

Maintenance

Observation

(62703)

The

inspector

observed/reviewed

maintenance

activities to verify that

correct

equipment

clearances

were

in effect;

work requests

and fire

prevention

work permits,

as

required,

were

issued

and

being

followed;

quality control

personnel

were available

for inspection

activities

as

required;

and,

TS requirements

were being followed.

Various

open

and closed work request

packages

were reviewed for the safety

injection/charging

system,

in coordination

with the

system

walkdown

inspection.

No violations or deviations

were identified.

5.

Review of Licensee

Event Reports

(92700)

The following LERs were

reviewed for potential generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that

were reported

immediately

were

reviewed

as

they occurred

to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with

the current

NRC Enforcement Policy.

(Closed)

LER 87-64:

This

LER reported

that

a

special

report

for

an

inoperable radiation monitor was not submitted

as required.

The inspector

reviewed

and verified the licensee'

corrective action

as

stated

in this

report.

(Closed)

LER

89-17:

This

LER

reported

an electrical

fault

on

main

generator

output bus causing plant trip and fire damage.

The licensee's

corrective action included

bus repairs,

redesign of the isolated

phase

bus

duct supports,

redesign

of the radio frequency monitor and

redesign

of

the

bus duct

fan cooling

system

to prevent debris intrusion.

All.items

have

been

completed satisfactorily

and the unit

was

returned

to

power

operation.

Review of Nonconformance

Reports

(71707)

Significant

Operational

Occurrence

Reports

(SOORs)

and

Nonconformance

Reports

(NCRs) were'eviewed

to verify the following:

TS were

complied

with, corrective actions

as identified in the reports

were accomplished

or

being pursued for completion,

generic

items were identified and reported,

and items were reported

as required

by the TS.

SOOR

89-164

reported

that

a

steam

generator

safety

valve lifted

during plant heatup.

On December

17 the plant was in Mode

3 with RCS.

pressure

at 2235

PSIG and

RCS temperature

at 557

+ 2 degrees

F.

The

"B" steam generator

PORV was isolated

due to problems with the valve

actuator.

Also, the main condenser

was under clearance

and the drain

lines from the main

steam

headers

were closed.

Plant operators

were

experiencing

some difficulty in maintaining

the

established

RCS

temperature

band

(+2F) due to the

"B"

PORV being isolated

and

the

slow response

of the

"A" and

"C" PORVs in automatic.

The operators

'herefore

placed

the

"A"

and

"C"

PORV controllers

in

manuals

Operator

inattentiveness

allowed reactor

coolant

system

temperature

to increase

above

normal

temperature.

Due to saturation

conditions

in the

steam

generators,

the

increase

in primary system temperature

to

approximately

565

F

corresponded

with

an

increase

in

steam

generator

pressure

until

the setpoint of

a

steam

generator

safety

valve

was

reached.

After lifting the

safety

valve,

operators

promptly reduced

temperature

and pressure

which allowed the safety

valve to reseat.

The safety valve remained

open for approximately

20

seconds.

The licensee's

investigation determined that

a safety valve

for the "A" steam generator

had lifted.

The failure of the reactor operator to adequately

control the heatup

activity with the

degraded

condition of the

PORVs, is considered

to

be weak.

A lack of supervisory

involvement in the heatup

process

was

also evident.

On

December

18,

1989,

at

approximately

11:20

a.m.

a

"B"

steam

generator

safety valve (1MS-44) opened for approximately

20

seconds.

Steam

generator

pressure

had

reached

approximately

1093

PSIG which

was well below the

lowest valve lift setpoint

of

1170

PSIG.

The

setpoint for this valve had recently

been tested satisfactory during

the refueling

outage

in October.

Licensee

personnel

investigated

this

event

and

reverified

the

setpoint

for

the

valve.

On

December

21,

1989, at approximately

12:19 p.m.,

1MS-44 again lifted

for approximately

5

seconds.

Steam

generator

pressure

had

reached

approximately

1097

PSIG

and

was still well below the required lift

setpoint

for

the

valve.

The

valve

was

subsequently

declared

inoperable

and the requirements

of TS 3.7. 1. 1 implemented.

The main

steam line drains

had been isolated during plant heatup

and

while the

plant

was

maintained

at

hot standby.

This allowed the

steam lines to partially fill with condensate.

The water interaction

with the safety

valve could

have

been

a contributing factor in the

low lifting of the safety valves.

It was

noted

by various

plant

personnel

that

an unusually

large

amount of water

was

found

on the

building roof following the first two safety

valve lifts.

Further,

problems associated

with the turbine driven auxiliary feedwater

pump,

which

resulted

in

pump

overspeed

trips

on

two

occasions,

were

attributed

to water in the

steam lines.

Also the

seismic

analysis

for the main

steam lines

may not

be valid when the

steam lines

are

filled with water.

This could lead to an unanalyzed

plant condition

during

a seismic event,

which would result in an overcooling accident

and

a containment

overpressurization

accident,

both

due to multiple

steam

line failures.

The

licensee

agreed

to

perform

a

seismic

analysis

for this

system

assuming

the

main

steam

lines

were filled

with condensate.

This item is considered

to

be unresolved

pending

completion of the licensee's

seismic analysis.

Unresolved

Item (89-34-03):

Operability of the main

steam lines when

filled with condensate.

The failure of operations

to adequately

drain the

main

steam

lines

during plant heatup,

which resulted

in

an

inoperable

condition for

the turbine driven

AFM pump, potential

safety valve actuation,

and

potential

unreviewed

safety

question

is

considered

to

be

an

,operational

weakness.

b.

NCR 89-56 reported that during

a disassembly

of cold leg accumulator

check

valves

1SI-251

and

1SI-252

during

the

refueling

outage,

a

visual inspection of the valve internal

surfaces

was not performed

as

required

by

the

licensee's

inservice

inspection

program.

The

licensee's

technical

support

group

has revised its internal

document

used for reviewing

proposed

work requests

to prevent

recurrence

of

this

nonconformance.

In addition,

the valves will be disassembled

and

inspected

during

the

next

scheduled

refueling

outage.

This

matter will be

considered

to

be

a

licensee

identified

Non-Cited

Violation (NCV).

NCV (89-34-04):

Failure to perform

a visual inspection of cold leg

accumulator

check valve internal

surfaces.

7.

Review of the

System Engineer

Program (71707)

A

survey

of

the

licensee's

implementation

of the

system

engineering

concept

was performed in accordance

with a

NRC Region II Memorandum dated

November

15,

1989.

The

number

of

system

engineers,

as

well

as their

responsibilities,

interfaces,

and reporting hierarchy were reviewed.

The system engineers

report directly to the Manager of Technical

Support.

Their duties

and

responsibilities

are

formally defined

in

procedure

TMM-100, Technical

Support

Conduct of Operations.

These

duties include,

in part,

log reviews,

system

walkdowns,

special test preparation,

review

of system modifications,

system description preparation,

and assistance

to

various other plant organizations.

The system engineers

perform

an active

role in troubleshooting

system

problems

and serve

as the lead contact in

coordinating corrective actions

This support provided to plant operation

is considered

to be

a strength of the licensee's

technical

support group.

No violations or deviations

were identified.

Inspection of Initial Fitness

for Duty Training (2515/104)

The

inspector

attended

selected

licensee

fitness

for

duty training

sessions

to determine

whether

required training

was

being

conducted

to

implement

the

Fitness

for Duty

Program.

A policy awareness

training

session

for

general

employees

as

well

as

a

training

session

for

supervisory

personnel

were

observed.

~ The licensee's

program

and

10 CFR Part 26

were

reviewed

to

determine

the

training

requirements.

The

inspector

also

discussed

the

program with the Site

Fitness

for Duty

Coordinator.

All personnel

who held

an active security

badge at the plant were required

to attend

the policy awareness

training.

Although escorts

did not receive

separate

training, their duties

and responsibilities

were discussed

during

the

policy

awareness

training.

In addition

to

the policy awareness

training,

supervisors

also

received additional

training

on their duties

and responsibilities.

The class

room discussion

did not discuss

techniques

for recognizing drugs

or indications

of

the

sale

or

possession

of drugs.

A booklet

was

distributed,

however,

which provided

information

on the identification,

use,

and description

of drug

paraphernalia.

The

booklet

was

to

be

reviewed

by the individual at his convenience.

A handout

provided

to

supervisors

included

a

copy of the

program

and

training notes

which could serve

as

a valuable future reference.

No violations or deviations

were identified.

Design

Changes

and Modifications (37828)

Installation of new or modified

systems

were reviewed to verify that the

changes

were

reviewed

and

approved

in accordance

with 10 CFR 50.59, that

the

changes

were performed

in accordance

with technically

adequate

and

approved

procedures,

that

subsequent

testing

and

test

results

met

acceptance

criteria or deviations

were

resolved

in an acceptable

manner,

and that

appropriate

drawings

and facility procedures

were

revised

as

necessary.

This review included

selected

observations

of modifications

and/or testing in progress.

'

10

The following plant change

requests

(PCRs)

were reviewed and/or associated

testing

observed:

- PCR-4007,

Electrical Penetration

Protection

- PCR-4682,

Consequences

of Losing Both S-4

Fans

PCR-4434,

480 volt Circuit Breaker

Replacement

PCR-4869,

NH Seri'es

Hydromotor Operators

- PCR-4922,

Engineering

Evaluation for Hanger

Removal

on

RHR System

i

PCR

4869

provided

instructions

to

modify various

HVAC system

damper

actuators.

During troubleshooting

of

an

HVAC damper

in October,

1989,

licensee

personnel

noticed that

the oil in the

actuator

motor for the

damper

was

discolored

and

the wiring insulation

had

degraded

and

was

brittle.

The investigation

into the

cause

for this condition

revealed

that

previous

modifications

to install oil pressure

switches

and

to

eliminate

an oil control valve in the actuator,

resulted

in an increase

in

the oil

temperature

inside

the

actuator.

The

increase

in internal

temperature

resulted

in the design

temperature

being

exceeded

and thereby

reduced

the

environmentally

qualified life of

the

wiring.

These

modifications

had

been

performed

on several

damper

actuators

in various

plant

HVAC

systems.

Systems

affected

included

the

Diesel

Generator

Building HVAC, Emergency

Service Water Intake Structure

HVAC, and

Reactor

Auxiliary Building HVAC.

The licensee

has established

a schedule

to send

the affected actuators

to the vender for refurbishment.

Due to the length

of time

involved (the licensee

estimates

approximately

12-18

months to

refurbish all the actuators),

the licensee

has

performed

an evaluation

and

justification

for continued

plant

operation.

Most of the

affected

actuator s fail to the position required for the performance of its safety

function.

However,

three

actuators

associated

with

RAB

HVAC switchgear

room cooling

have

been

modified (blocked

open)

so that the

dampers will

remain

open

pending

failure.

Other

compensatory

measures

include

monitoring the Diesel Generator

Building room temperature

and placement of

portable heaters if excessively

low temperatures

are experienced.

Inspector

Followup Item (89-34-05):

Follow the licensee's

activities to

r epl ace

HVAC system actuators.

10.

Plant Startup

From Refueling (71711)

The

inspector

observed

plant activities during unit startup

following

refueling to verify that plant

systems

were properly returned to service

and that the startup

was conducted

in accordance

with approved

procedures

and in compliance with the TS.

The plant

began

deboration

to criticality on December

20 and entered

the

startup

mode

(Mode 2) at 3:23 a.m.

Criticality was achieved at 9:47 a.m.

on

December

20.

The inspectors

observed

the approach

to criticality and

ll

verified that criticality occurred within the limits calculated

by the

licensee.

mplementation

of the following procedures

was verified:

- GP-004,

Reactor Startup

- EPT-069, Initial Criticality

No violations or deviations

were identified.

11.

Followup of Onsite

Events

(93702)

On December

20,

1989 at 8:35 p.m., during the initial start of the

a main

feedwater

(NFW)

pump following the refueling

outage,

the

"A"

NFW

pump

failed to start.

The start failure satisfied

the circuitry for an

AFW

actuation

signal

due to both

MFW pumps being in a tripped condidtion.

All

AFW components

functioned

as

designed

and

plant

personnel

initiated

a

maintenance

work request

to investigate

and repair the discrepancy.

Following a breaker

check for the "A" MFW pump,

a

second attempt to start

the

pumps

was

made

on December

21, at 3:20 a.m.

The

pump again failed to

start

and

another

AFW actuation

signal

was

generated.

Subsequently,

a

third attempt

was

made to start the "A" MFW pump at 5:40 a.m.

even

though

no apparent

corrective maintenance

had

been

performed

following the last

trip.

The

"A"

MFW pump tripped

again

and

caused

another

AFW actuation.

Following this actuation,

licensee

personnel

determined that the low lube

oil pressure

switch

was

causing

the

pump to trip.

The lube oil pressure

switch was recalibrated

and the "A" NFW pump was started

successfully.

On

December

27,

1989 at 4:50 p.m., the "A" NFW pump tripped resulting in

yet another

AFW actuation.

This trip of the

"A" MFW pump

was

due to

operator

errors while operating

at

low power

(12%) with all three

feed

regulating

valves

in

manual.

Upon

increasing

flow to

two

steam

generators,

the

MFW pump recirc valve closed automatically

as

designed,

which

resulted

in

an

increase

in

feedwater

flow to all

the

steam

generators.

The

operator

therefore

reduced

flow

through

the

feed

regulating

valves

in response

to increasing

steam

generator

level.

The

decreasing

feedwater flow actuated

the

MFP low flow trip and,

due to the

already

secured

"B"

MFW pump,

thereby satisfied

the

AFW actuation

logic

for loss of both

MFWs.

Once into this transient

the operator

had little

chance of recovery.

This

AFW actuation is considered

to be

an operational

weakness,

in that the

new inexperience

operator

needed

additional

guidance

during this difficult startup evolution.

12.

Licensee

Action

on

Previously Identified Inspection

Findings

(92702

92701)

(Closed)

Unresolved

Item 400/89-28-01,

Review the licensee's

engineering

evaluation of

RHR system operability with two pipe supports missing.

12

'he

inspector

reviewed

PCR 4922,

Engineering

Evaluation for Hanger

Removal

on

RHR System.

The licensee

determined that the affected

system

remained

operable

with the

missing

supports.

Calculations

showed that

supports

adjacent

to

the

ones

missing

were still capable

of performing their

intended

function

even with the additional

loads which resulted

from the

missing supports.

(Closed)

IFI

400/89-21-02,

Emergency

Service

Water

Flow

Balance

Inconsistencies.

This

item

was

previously

discussed

in

NRC Inspection

Report

50-400/89-28.

Following

the

Licensee's

completion

of

flow

balance/pressure

testing

of the

emergency

service

water

system,

the

licensee's

nuclear

engineering

department

reviewed

the test

data

and

calculated

minimum supply flows to equipment

under worse

case conditions.

The calculations

confirmed that

the

emergency

service

water

system

was

capable of supplying adequate

cooling flow to safety related

components

as

originally designed

and

as

assumed

in

the

FSAR.

The

inspector

was

informed that

the

licensee

intended

to develop

a

computer

model

to

facilitate future

system work and to assist

in their response

to the

NRC

service water system generic letter.

13.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1)

at the

conclusion

of the

inspection

on

January

5,

1990.

During this

meeting,

the

inspectors

summarized

the

scope

and

findings of the

inspection

as they are detailed

in thi s report,

with particular

emphasis

on the Violations, Unresolved

Item,

and Inspector

Follow-up item addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or

reviewed

by the inspectors

during this inspection.

Item Number

Descri tion and Reference

50-400/89-34-01

50-400/89-34-02

Violation - Failure to perform surveillance

testing

for

an

inoperable

emergency

diesel

generator,

(paragraph

3.a).

Violation - Failure to adhere

to the

requirements

of plant procedures,

paragraphs

3.b

and 3.c).

50-400/89-34-03

Unresolved

Item -

Operability of the main

steam

lines

when filled with condensate,

(paragraph

6.a).

13

Item Number

(cont'd)

50-400/89-34-04

50-400/89-34-05

Acronyms and Initialisms

Oescri tion and Reference

Licensee Identified Violation - Failure to

perform

a

visual

inspection

of

cold

leg

accumulator

check

valve

internal

surfaces,

(paragraph

6.b).

IFI - Follow the licensee's

activities to

replace

HVAC system actuators,

(paragraph

9).

AC

AFW

CCTV

CFR

EPT

EST

F

FSAR

HVAC

HZ

GP

I&C

IFI

LER

MFW

MS

NCR

NCV

NI

NRC

OST

PCR

PORV

PSIG

QA

QC

RAB

RCA

RCS

RHR/RH

RWP

RWST

SI

SOOR

TMM

TS

Alternating Current

Auxiliary Feedwater

Closed Circuit Television

Code of Federal

Regulations

Engineering

Performance

Test

Engineering

Surveillance

Test

Fahrenheit

Final Safety Analysis Report

Heating, Ventilation and Air Conditioning

Hertz

General

Procedure

Instrumentation

and Control

'nspector

Follow-up Item

Licensee

Event Report

Main Feedwater

Main Steam

Non-conformance

Report

Non-cited Violation

Nuclear Instrumentation

Nuclear Regulatory

Commission

Operations

Surveillance

Test

Plant

Change

Request

Power Operated

Relief Valve

Pounds

per Square

Inch Gage

Quality Assurance

Quality Control

Reactor Auxiliary Building

Radiation Control Area

Reactor Coolant System

Residual

Heat

Removal

Radiation

Work Permit

Refueling Water Storage

Tank

Safety Injection

>>

Significant Operational

Occurrence

Report

Technical

Support

Management

Manual

Technical Specification