ML17349A787

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Initial SALP Repts 50-250/93-03 & 50-251/93-03 for 910929- 930120
ML17349A787
Person / Time
Site: Turkey Point  
Issue date: 04/02/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17349A786 List:
References
50-250-93-03, 50-250-93-3, 50-251-93-03, 50-251-93-3, NUDOCS 9304130113
Download: ML17349A787 (44)


See also: IR 05000250/1993003

Text

ENCLOSURE

INITIALSALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-250/93-03 AND 50-251/93-03

FLORIDA POWER AND LIGHT

TURKEY POINT UNITS 3 AND 4

SEPTEMBER 29, 1991 - JANUARY30, 1993

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TABLE OF

CONTENTS

I.

INTRODUCTION .............................

Pa<ac

II. SUMMARY OF RESULTS .........................................

III. CRITERIA ...............

3

IV.

PERFORMANCE ANALYSIS

A.

B.

C.

D.

E.

F.

G.

Plant Operations ...................

Radiological

Controls ..............

Maintenance/Surveillance ........

Emergency

Preparedness .............

Security ...........................

Engineering/Technical

Support ......

Safety Assessment/equality

Verification

3

6

9

13

15

17

20

V.

SUPPORTING

DATA

A.

B.

C.

D.

E.

F.

G.

H.I.

Licensee Activities ................

Reactor Trips and Unplanned

Shutdown

Direct Inspection

and Review Activit

Escalated

Enforcement Actions ......

Confirmatory Action Letters ........

Licensee

Conferences ...............

Licensing Activities ...............

Review of Licensee

Event Reports ...

Enforcement Activity ...............

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23

23

25

25

25

25

25

26

27

'e,

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is an

integrated

Nuclear Regulatory

Commission

(NRC) staff effort to collect

available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

on the basis of this information.

The

SALP program

is supplemental

to normal regulatory processes

used to ensure

compliance

with NRC rules

and regulations.

It is intended to be sufficiently

diagnostic to provide

a rational basis for allocation of NRC resources

and to provide meaningful

feedback to the licensee's

management

regarding

the

NRC assessment

of their facility's pe}formance in each functional

area.

An NRC SALP Board,

composed of the staff members listed below,

met on

March 15,

1993, to review the observations

and data

on performance,

and

to assess

licensee

performance

in accordance

with NRC Manual

Chapter

0156,

"Systematic

Assessment

of Licensee

Performance."

This report is the NRC's assessment

of the licensee's

safety performance

at Turkey Point Units 3 and

4 for the period September

29,

1991, through

January

30,

1993.

The

SALP Board for Turkey Point was

composed of:

J.

R. Johnson,

Deputy Director, Division of Reactor Projects

(DRP),

Region II (RII) (Chairman)

J.

P. Stohr, Director, Division of Radiation Safety

and Safeguards

(DRSS), RII

A. F. Gibson, Director, Division of Reactor Safety

(DRS), RII

M. V. Sinkule, Chief, Reactor Projects

Branch 2,

DRP, RII

R.

C. Butcher,

Senior Resident

Inspector,

Turkey Point,

DRP, RII

H.

N. Berkow, Director, Project Directorate II-2, Office of Nuclear

Reactor Regulation

(NRR)

L. Raghavan,

Project Manager,

Turkey Point, Project Directorate

II-2,

NRR (by telephone)

Attendees

at

SALP Board Meeting:

K. D. Landis, Chief, Project Section

2B,

DRP, RII

W. H. Rankin, Chief, Facilities Radiation Protection Section

(FRP),

DRSS, RII

A. T. Boland, Radiation Specialist,

FRP,

DRSS, RII

G.

B. Kuzo, Senior Radiation Specialist,

Radiological Effluents

and

Chemistry. Section .(REC),

DRSS, RII

W.

M. Sartor,

Senior Radiation Specialist,

Emergency

Preparedness

Section

(EP),

DRSS, RII

A. Gooden,

Radiation Specialist,

EP,

DRSS, RII

W. J. Tobin, Senior Physical Security Specialist,

Safeguards

Section

(SS),

DRSS, RII

D.

H. Thompson,

Physical Security Specialist,

SS,

DRSS, RII

G. A. Hallstrom, Reactor Inspector,

Materials

and Processes

Section,

DRS, RII

R.

P. Schin, Project Engineer,

Project Section

2B,

DRP, RII

SUMMARY OF

RESULTS

During this 16-month

assessment

period,

Turkey Point continued to

demonstrate

improved performance.

Preparations

for and recovery from

Hurricane Andrew were conservative,

timely, and effective.

Excellent performance

in the Plant Operations

area continued.

Operators

performed well during plant startups,

plant shutdowns,

and transient

conditions.

Conservative

management

actions in preparing, operators

and

the plant for Hurricane

Andrew, control

room oversight, verification of

operator log keeping,

control of shared

systems

(fossil/nuclear),

and

comprehensive

plan of the day meetings contributed to the strong

performance

in this area.

Conservatism

was also demonstrated

by the

performance of full-scale post-refueling type star tup tests

on Unit 3

following the dual-unit outage.

Post-hurricane

morale problems, staff

attrition,

and personnel

errors were aggressively

addressed

by management

actions

but continued to be

a challenge.

Improved performance

was noted in the area of Radiological Controls.

Personnel

exposure controls

and collective doses

were improved by

effective As Low As Reasonable

Achievable

(ALARA) Program efforts

including resistance

temperature

detector

(RTD) bypass

removal

and

effective contamination control.

A strong environmental

monitoring

program, effective management 'of liquid and gaseous

effluents,

and

a

substantial

reduction in onsite

r adwaste

volume also contributed to this

improvement.

Areas for further improvement included procedural

adherence

and resin transfer controls.

Improvement continued in the Maintenance/Surveillance

area.

Work

planning

and scheduling,

equipment reliability initiatives, corrective

maintenance

backlog reductions,'and

general

plant material condition

and

housekeeping

were improved.

Areas for further improvement included

surveillances

and the quality of maintenance

work.

Superior performance

in Emergency

Preparedness

(EP)

was maintained.

Strengths

included preparation for and recovery from Hurricane Andrew,

management

support for the

EP program,

and performance

during

EP

exercises.

Areas for further improvement included originality of

exercise

scenarios

and in-plant paging audibility.

Superior performance

in Security was also maintained,

with strengths

in

site management,

tactical

response .training, .equipment condition,

and the

Fitness-For-Duty

program.

Improved performance

in Engineering/Technical

Support

was demonstrated

by

the quality of modification packages,

reduction in engineering

backlogs,

prioritization of engineering

work, training, self-assessments,

and

excellent support for Hurricane Andrew recovery.

Conservative

actions

were demonstrated

by the performance of IOOX eddy current testing

on

steam generator

tubes.

Areas for further improvement included drawing

0'

. quality, contractor oversight,

and equipment selection

and procurement.

The Safety Assessment/guality

Verification area

performance

continued to

be excellent.

Management

involvement

and support,

a strong quality

organization,

effective audit programs

and self-assessments,

and good

root cause

evaluations directly contributed to this performance.

Areas

for further improvement included timeliness

and quality of licensing

submittals.

Overall, performance

continued to improve in almost all areas.

This

improved performance

was due to the licensee's

continued

commitment to

self-identification and correction of potential

problems;

a strong

management

team;

and

a dedicated,

experienced staff.

Facilit

Performance

Summar

Functional

Area

Rating Last

Rating This

Period

Period

Plant Operations

(Operations

& Fire Protection)

Radiological

Controls

Maintenance/Surveillance

Emergency

Preparedness

.

Security

Engineering/Technical

Support

Safety Assessment/

equality Verification

Outage

III. CRITERIA

2 improving

2 improving

1

1

2

1

2 improving

1

1

2 improving

1

NA

The evaluation criteria which were used,

as applicable,

to assess

each

functional

area

are described

in detail in NRC Manual Chapter 0516.

This

chapter is in the Public Document

Room.

Therefore,

these criteria are

not repeated

here,

but will be presented

in detail at the public meeting

to be held with licensee

management.

IV.

PERFORMANCE ANALYSIS

A. Plant

0 erations

I .

~Anal

s i s

s

This functional

area

addresses

control

and performance of activities

directly related to operating the unit,

as well as fire protection.

During this assessment

period, there were no reactor trips due to

operator errors.

Unit 3 had one manual reactor trip in response

to

a mechanical

failure of a fitting in the turbine control oil piping,

and Unit 4 had

one automatic reactor trip due to

a switch failure

during surveillance testing of the containment isolation racks.

0

During the previous

SALP period, Unit 4 had one automatic trip due

to

a personnel

error.

On

an operating time basis, this represented

a performance

improvement over previous

SALP periods.

Operations

personnel

performed well during plant startups,

shutdowns,

and transients.

Performance

on NRC-administered

operator

license

examinations

was excellent (all five crews

and

41 of 42

operators

passed),

as further discussed

in the Engineering/

Technical

Support section.

Several

positive operator actions

were

noted during this

SALP period.

For example,

during

a surveillance

that inappropriately permitted axial flux deviations outside the

target

band at

100X power,

an operator recognized

the discrepancy

and immediately reduced reactor

power to less

than 90X.

In

addition,

when Unit 3 entered

Node

3 following the dual-unit outage,

an oncoming operator recognized that the Unit 4 refueling water

storage

tank did not meet the technical specification-required

water

volume.

Also, prompt operator actions

aided in preventing

two

reactor trips following plant transients

due to equipment failures.

The licensee routinely made conservative

decisions affecting plant

operations.

For example,

following the dual-unit outage,

the

licensee

performed

a full-scale post-refueling type startup test

program even though Unit 3 had not been refueled.

The Unit 3 fuel

had

been offloaded

and reinstalled in the

same configuration.

In

addition, the stationing of managers

in the control

room during

critical plant evolutions

and the use of shutdown risk management

controls during shutdowns

were noted

as strengths.

In response

to

industry events

and prior to a related

NRC Information Notice, the

licensee

aggressively initiated operator log reviews.

These

reviews

identified problems with non-licensed

operator logs, for which

prompt corrective action

was taken.

In preparation for Hurricane

Andrew, licensee

management

required all operating

crews to attend

simulator training to practice the most likely scenarios

they might

encounter (i.e., loss of offsite power, loss of intake cooling

water, etc.).

Operator

and reactor plant performance during

Hurricane Andrew was excellent.

During previous

SALP periods,

the

NRC expressed

concern regarding

high operator turnover

and overtime.

During the last

SALP period,

the licensee

increased

the licensed

operator training class size

and

increased

incentives to retain personnel

such that six shifts could

be implemented.

During this period, the oper ating staff remained

on

a six-shift rotation with eight-hour shifts.

A second Assistant

Nuclear,. Plant .Supervisor..(ANPS)

position was added, -creating

a Unit

3- and

a Unit 4-specific

ANPS position.

This provided additional

supervisory oversight for each unit.

The increase

in operations

staffing and six-shift rotation aided in reducing operator overtime

from 14X in 1991 to

12X in 1992.

However, the attrition rate for

operations

personnel

increased after Hurricane Andrew.

From August

24,

1992, to January

30,

1993, eight licensed

and three non-licensed

operators

resigned.

To compensate

for the loss of licensed

operators,

a licensed

operator training class of nine career

path

non-licensed

operators

was started

in October,

1992.

To fill the

operator career

path,

a non-licensed entry-level class of 20 was

authorized to start in February,

1993.

The licensee

had addressed

operator attention to detail

and

equipment clearance

problems during the last

SALP period.

During

this

SALP period, there

were

an increased

number of operator errors

after Hurricane Andrew (i.e. inadvertent

power operated relief valve

lifts and

a clearance

error with personnel

contamination).

To

further address

the operator error and clearance

problems during the

post-hurricane

Unit 3 refueling outage,

licensee

management

formed

a

configuration control review team to review evolutions requiring

increased

management

attention.

Prior to performance of a task,

the

team was chartered

to review all clearances

to ensure that adequate

boundaries

existed

and that all vents

and drains were located within

the isolation boundary,

to review clearance

releases

for correct

order, to review all clearance

boundary modifications

and test

releases

prior to implementation,

and to review complex evolutions

to ensure that all precautions

were taken to minimize any risks.

Pre-evolution briefings were conducted prior to releasing

clearances

to ensure

system integrity.

Also,

a third (independent)

verification was performed

on all clearances

on radioactive

systems.

Poor quality drawings were noted

as contributing to several

personnel

errors.

The licensee

has prepared

upgraded

and

computerized plant operating drawings,

which are scheduled

to be in

place early this year.

At the

end of the

SALP period, operator

personnel

errors

were still being observed,

indicating

a continuing

need for management

attention.

The plan-of-the-day

(POD) meeting continued to be comprehensive

and

well controlled such that all disciplines

were involved in the

planning

and defining of the next few days'ork objectives

and

critical path work.

This helped minimize the time spent in limiting

conditions for operation

when equipment

was taken out of service.

The

POD tracked several critical indicators

such

as off-normal

annunciators,

control

room green tags,

the leak list, open temporary

system alterations,

and equipment out of service.

To emphasize

the

need to address

the plant work order backlog,

the ten oldest plant

work orders in each discipline were highlighted.

The number of

control

room deficiency tags

was reduced

from about

65 during the

last

SALP period to about

15 at the end of this

SALP period.

During th'e last

SALP period, control of work on shared

systems

(between

the. fossil

and nucl.ear..units)

was .noted

as

a problem.

The

licensee initiated program

changes

to control work in the switchyard

and

on other shared

systems.

One of the controls

was

a requirement

to notify the nuclear plant supervisor prior to any work in the

switchyard.

There were

no fossil/nuclear interface

problems

identified during this

SALP period.

An inspection of the fire protection

program was conducted

following

the recovery from Hurricane Andrew.

The results indicated that the

0

fire protection

program improved over the previous

SALP period.

For

example,

the number of fire protection

system impairments,

which had

averaged

between

40 and

60 in 1990,

was reduced to an average of

less than

10 by the end of 1991

and was maintained at about that

level during this assessment

period.

Hissed surveillances

in the

fire protection

area

were noted

as

a problem in the last

SALP

period; there were none noted during this

SALP period.

The

licensee's

response

to Bulletin 92-01

(Thermo-lag insulation)

was

prompt

and effective.

That response

included the installation of

video camera

coverage for Thermo-lag areas that did not have

installed fire detection.

2.

Five violations were cited in the Operations

area during this

assessment

period.

Performance

Ratin

3.

Category:

1

Recommendations

None

B. Radiolo ical Controls

~Anal sis

This functional area

addresses

those activities directly related to

radiological controls, radioactive waste

management,

environmental

monitoring, water chemistry,

and transportation of radioactive

material.

The radiation protection

(RP) program was effective in controlling

personnel

exposure to radioactive materials

and protecting the

health

and safety of plant personnel

and the public.

No internal or

external

exposures

in excess

of 10 CFR 20 limits occurred during the

assessment

period.

During the assessment

period, the licensee's

RP department

was

reorganized.

The restructuring established

the

ALARA and dosimetry

groups

as separate

entities,

reporting directly to the Health

Physics Supervisor,

and facilitated management

involvement in these

areas.

Adequate

numbers of qualified staff were available to

support both. routine

and outage activities...The technician training

program continued to be

a strength

as indicated

by comprehensive

job

performance

measures

for contractor technicians,

the inclusion of

integrated

mock-ups

and systems orientation in continuing training,

and licensee

support for National Registry of Radiation Protection

Technicians certification.

The Chemistry Department staff was well-

trained,

and staffing levels remained stable.

The

RP and chemistry self-assessment

programs

were generally

0

9'

proactive during the assessment

period.

Audits of both programs

were well-planned

and documented

with detailed information and

recommendations

to facilitate implementation of required corrective

actions.

In addition, the Radiological

Incident Report System

and

the recently-initiated Supervisory Surveillance

Program were used

effectively by the licensee to appropriately identify, trend,

and

correct health physics

problem areas.

Overall, the licensee

conti.nued to effectively manage collective

dose,

expending

approximately

419 person-rem during the assessment

period.

Collective doses for 1991

and

1992 were 938 and 325 person-

rem, respectively

(both under the estimated

person-rem

goals for the

periods).

For 1991, the majority of the dose

expended

was

associated

with the dual-unit outage

which included dose-intensive

work such

as resistance

temperature

detector

(RTD) removal.

For

1992, the dose primarily reflected operating conditions, with

approximately

64 outage

days.

The dose

was consistent with work

scope,

and the licensee

realized

a dose reduction from previous

assessment

periods, particularly with respect to dose during non-

outage conditions.

Efforts in ALARA during the assessment

period were effective in

reducing overall collective dose.

The licensee

realized significant

reduction in steam generator

channel

head

and reactor coolant system

loop piping dose rates

(by approximately

one half) due to the

effective implementation of a lithium/boron coordinated

chemistry

shutdown

program,

as well as reduced

dose rates

due to the removal

of the

RTDs during the previous

assessment

period.

The licensee's

improved performance of repetitive refueling tasks during the

1992

Unit 3 refueling outage resulted

in the completion of many tasks

with less

dose than their past best performance.

In particular, the

use of new reactor vessel

head tensioning

equipment

reduced

dose

considerably.

Other

ALARA efforts were undertaken

during this

assessment

period,

such

as the implementation of digital alarming

dosimeters,

to further reduce

doses.

I

The licensee's

radiation protection work planning

and program

implementation

were generally good;

however,

several

examples of

lack of attention to detail

as regards

procedural

compliance

were

identified during the review cycle.

These

included the failure to

conduct

ALARA pre-job briefings for workers in accordance

with

radiation work permit

(RWP)

and procedural

requirements;

the failure

to perform routine radiological

surveys consistent with procedural

requirements;-end

the failure -to adequately -leak test Iron-55 sealed

sources.

Corrective actions

associated

with these

areas

were

completed or in progress

at the end of the assessment

period.

Weaknesses

identified during the previous

assessment

period related

to the respiratory protection

program were corrected.

Continued

improvement

was noted in the licensee's

control of

contamination.

During the assessment

period, the licensee

decreased

contaminated

surface

area to an average of approximately

6110 square

feet,

approximately five percent of the radiation-controlled

area.

In addition,

personnel

contamination

events for 1992 were

approximately

66,

as

compared to a goal of 100, which was

a decrease

from previous years.

The licensee

continued to pursue

improvement

in laundry/protective clothing monitoring for further reduction in

personnel

contamination

events.

Overall,

improvements

were observed

in general

housekeeping

and radioactive material control,

particularly in,yard and radioactive material

storage

areas.

Plant water chemistry

was maintained within Technical Specification

(TS) limits and

an accurate

radiochemical

analysis

program continued

during the assessment

period.

Initiatives included the development

of methods to upgrade plant operations,

including the use of a

reverse

osmosis

process

to produce very high quality water for the

Mater Treatment

Plant for use in the primary and secondary plant.

During the assessment

period,

the licensee

took steps to correct

long-standing

problems with the operation of the secondary

system

polishers for removal of filterable solids.

Water chemistry

controls contributed to the fact that very few steam generator

tubes

have required plugging.

The radiochemical

analysis

program

effectiveness,

including sample collection

and analyses

accuracy,

was demonstrated

by overall

agreement

between results for analyses

conducted

using licensee

and the Region II mobile laboratory systems

during

a confirmatory measurements

inspection.

During the assessment

period, the liquid and gaseous

effluents

release

program was managed effectively.

Plant effluent releases

'ere

small fractions of their allowable regulatory limits, with no

unplanned

releases

reported.

Preparation

and recovery actions

regarding effluent control

and monitoring associated

with the August

24,

1992, hurricane

were timely, met

TS requirements,

and were

considered

appropriate.

These actions

included initially securing

all effluent release

pathways

and implementation of supplemental

monitoring as

a result of damage to the main stack

and radioactive

waste

(radwaste)

building ventilation systems

from the storm.

The licensee's

Radiological

Environmental

Monitoring Program

(REAP),

a program strength, verified that facility operations

resulted

in

minimal environmental

impact.

For the assessment

period,

measured

doses

and radionuclide concentrations

were significantly less than

TS reporting values or the specified lower limit of detection.

No

trends in the environmental

monitoring data were noted

compared to

previous

assessment

periods.

Accuracy of sample

analyses

was

confirmed--independently-

by -favorable-comparison

of licensee

analytical results with values for selected

environmental

samples

sent to the

NRC contractor laboratory.

Licensee

actions to restore

. the

REAP following the hurricane

were considered

timely and

appropriate.

With the exception of a July 9,

1992,

spent resin transfer spill

event,

improvements

in the processing,

storage,

and shipping of

radwaste

were noted during the assessment

period.

The resin spill

e

2.

contaminated

approximately

2000 square feet (ft~) of floor space

due

to the failure to follow procedures for equipment set-up

and

verification.

Poor housekeeping

in the area,

weak interfaces

between licensee

and vendor procedures,

and partially blocked floor

drains also contributed to the spill.

No concerns

were identified for shipping activities

and

improved

compliance with posting

and labeling requirements

were noted

as

compared to the previous

assessment

period.

Further,

management

commitments

and staff actions resulted

in a significant reduction of

contaminated

equipment

and dry active waste maintained onsite.

From

June

1992 through October

1992, the licensee effectively reduced

the

volume of radioactive

waste stored onsite

from 52,000 to 2,500 cubic

feet (ft ).

This reduction contributed to the lack of radioactive

waste

problems during Hurricane Andrew.

One violation was cited in the area of Radiological

Controls during

this assessment

period.

Performance

Ratin

3.

Category:

1

Recommendations

None

C. Haintenance

Surveillance

~Anal sis

This functional

area

addresses

activities related to equipment

condition, maintenance,

testing,

and surveillance.

In addition to

routine inspections,

a special

inspection of the motor operated

valve program

was conducted.

Although equipment failures continued to impact plant operations,

equipment reliability was improved over previous

SALP periods.

This

was evidenced

by reliable plant operation prior to the shutdown of

both units for Hurricane Andrew and by the fact that all necessary

equipment functioned

as required during the hurricane.

Additionally, unit availability was improved significantly over

previous

SALP periods.

During this assessment

period, there were

no

reactor trips due to maintenance. or surveillance

personnel

errors.

Equipment problems requiring plant shutdowns or power reductions

during this assessment

period included:

piping failures in the

turbine control oil system, oil leakage

from the

3B and

4C reactor

coolant

pumps,

and

a leaking weld joint on

a

4C steam generator

flow

transmitter.

The licensee

implemented

several

programs to improve equipment

reliability and reduce the impact of equipment malfunction

on plant

10

operation,

which resulted

in improved plant operations

as noted

above.

A procedure

was established

between

the Haintenance,

Engineering,

and Technical

Departments

to require

a root cause

analysis of equipment failures which recur following maintenance

action and/or engineering resolution.

Examples of specific issues

which were analyzed for root cause

and resolution during this period

include failures in the following systems:

residual

heat

removal

pump mechanical

seals,

area radiation monitoring system,

main

turbine control oil piping, spent fuel

pump shaft,

intermediate

range nuclear instrumentation,

turbine auxiliary oil pump,

and small

bore piping welds in the charging

system.

Also, the licensee's

aggressive

approach to a comprehensive

Generic Letter 89-10 Hotor

Operated

Valve program continued to improve equipment reliability.

Equipment availability was enhanced

by using

a quarterly schedule.

This method allowed each discipline to ensure that all necessary

maintenance

was performed

and coordinated

as

one equipment

outage.

This program also reduced

the number of hours safety-related

equipment

was in a Limiting Condition for Operation for planned

maintenance.

In addition, the quarterly schedule activities were

reviewed from a Probabilistic Risk Assessment

standpoint to evaluate

risk peaks

associated

with out-of-service

equipment.

The

Reliability Group of the Haintenance

Department started

a new

program in December

1992 to perform

a reliability-centered

maintenance

analysis

on

an entire system rather than just at the

component level.

The feedwater

system,

which was under review at

the end of this

SALP period,

was the first system

chosen

based

on

the number of corrective maintenance

manhours

expended

and the

potential reliability gains.

The licensee's

attention.to

reducing the backlog of corrective

maintenance

plant work orders

(PWOs), control

room deficiency tags,

and out-of-service control

room instruments

improved during this

period,

as all three indicators

reached all-time lows.

The non-

outage corrective maintenance

PMO backlog

was reduced

from 750 at

the end of the last

SALP cycle to approximately

425 at the end of

this cycle, which was significantly below the licensee's

goal of

700.

In addition, the ten oldest of these

PWOs for each maintenance

discipline were tracked at the daily

POD meeting,

which resulted in

completing the oldest

ones

(from 1986 to 1989).

The Haintenance

Department

continued to complete

more than

50X of the non-outage

corrective maintenance

PMOs within 3 months of initiation.

In

addition, the total

number of these

PWOs older than

12 months

was

reduced 'to 374 at the end of 1992, which was "well below the

licensee's

goal of 580.

Control

room deficiency tags

were reduced

from a low of 44 in the last

SALP period to

12 at the end of this

SALP period.

Out-of-service control

room instruments

were reduced

from a low of 28 in the last

SALP period to 5 at the end of this

SALP period.

In August 1992, licensee

management

established

a

dedicated

Haintenance/Engineering

task team

on

PWO reduction.

During the assessment

period,

the team processed

136

PWOs that were

previously

on hold for Engineering input.

In addition, the team

0

11

issued

nine standard

engineering specifications that allowed the

maintenance

disciplines to perform certain activities without

waiting for direct engineering

support.

The Maintenance

Department

continued to focus

on upgrading the

material condition of the facility.

During this

SALP period,

significant progress

was noted in this area

both prior to and after

Hurricane Andrew.

The formal weekly management

walkdowns with area

supervisors

continued to be effective.

Followup inspections

were

conducted to ensure that identified deficiencies

were either

promptly corrected

or entered into the plant work control system.

Improvement in the material condition was evident throughout the

plant.

The licensee

formalized

an insulation upgrade

program which

contributed to this improvement.

The Maintenance

Department

also

provided extensive

support to the licensee's

efforts on reducing the

amount of contaminated floor space.

Plant management

increased

emphasis

on reducing plant leaks

by establishing

a leak reduction

task force responsible for maintaining

a data

base of leaking

components

which resulted in a reduced

number of leaks.

This

program received direct management

attention

when it was discussed

at the daily

POD meeting.

equality of maintenance

work had

been

a problem in the last

SALP

period

and deficiencies

continued throughout this period.

However,

improvement

has

been noted.

A number of rework issues

were noted

during this assessment

period, including:

intake traveling screen

transmission

installed backwards,

charging

pump failures, electric

fire pump workmanship deficiencies,

and auxiliary feedwater

pump

B

vendor information deficiency.

In some cases,

Maintenance failed to

adequately prioritize work activities once identified.

Two recent

examples

included the failure to adequately

seal

the Unit 3

generator

housing (allowing water entry during heavy rains),

requiring

a shutdown of the unit and the failure to repair

a

corroded lube oil storage

tank pipe, resulting in subsequent

failure

and leakage of oil into the discharge

canal.

In addition, during

calibration of a refueling water storage

tank level transmitter,

a

maintenance

technician

removed the wrong unit, wrong train level

transmitter

from service.

The Maintenance

Department

implemented

several

actions to improve

the quality of work during this

SALP cycle.

The responsibilities

for the preparation,

review,

and revision of department

procedures

were returned to the Maintenance

Department

(as well as other

departments)

-from -a separate

procedures-group

to provide direct

ownership.

During critical maintenance activities, the Maintenance

Department

provided around-the-clock on-shift management

coverage.

The Department

also

implemented

a self-checking policy during this

cycle to enhance

the quality of work.

The routine preventive maintenance

(PM) program

was maintained

current

(except for approximately

one month immediately following

the hurricane) with an average of less than

10 overdue

PMs per

12

month.

The success

of the

PH program contributed to the previously

noted reduction in the corrective maintenance

PWO backlog.

The

licensee

began

an engineering

review of the

PH program to reverify

the basis for the existing program, delete

unnecessary

PHs,

add

PHs

where warranted,

and establish

the groundwork for implementation of

the

new

NRC Haintenance

Rule.

The first system

under review was the

chemical

and volume control system.

The

PH program continued to be

an asset

by identifying potential

problems prior to failure; for

example,

detecting

increasing vibrations of the

3B reactor coolant

pump.

The

pump motor and rotating assembly

were subsequently

replaced

during

a refueling outage.

Haintenance

Department overtime, training, staffing levels,

and

turnover rates

were adequate

throughout this assessment

period.

Overtime was reduced

from approximately

25X at the beginning of this

SALP period to 18X at the end.

The majority of the supervisors

completed

formal classroom training to help improve supervisory

performance.

Hock-up training (reactor coolant

pump seals,

conoseals,

and moisture separator

reheater

drain line repair)

and

vendor training for newly installed equipment

(HOVATS, Eagle

21,

and

the area radiation monitoring system) significantly improved the

quality and duration of critical maintenance activities

and also

contributed to reduced radiation doses for maintenance

personnel.

Training instructors

were used on-shift during the Unit 3 refueling

outage to both enhance

the technical

expertise

on shift and provide

current plant experience

to the instructors.

Staffing levels for

the four maintenance

disciplines were adequate.

Overall performance

in the surveillance

area

was adequate.

During

the previous

SALP period,

the licensee identified problems with

missed surveillances

due to surveillance

scheduling

and tracking.

The licensee

developed

a computerized

surveillance tracking program

for the tracking

and scheduling of all TS-required surveillances

with test intervals of one week or more.

Although this computerized

program was effective in eliminating missed TS-required

surveillances

which were caused

by tracking and scheduling errors,

the number of surveillance-related

problems attributed to other

causes

increased

since the last assessment

period.

During this asses'sment

period,

the licensee

issued

14 Licensee

Event

Reports

(LERs) regarding surveillance-related

problems.

These

problems

were caused

by a series of unrelated

personnel

errors

and

procedural

deficiencies.

Examples of .personnel

errors included

three-missed

ASHE Code. required tests,- two.missed

mode change

required tests,

and the failure of a vendor to test diesel

fuel oil

for sulfur content in accordance

with the method specified in the

TS. 'xamples of procedural

deficiencies

included

an inadequate

analog

channel

operating test of the overpressure

mitigation system;

failure to adequately recirculate the contents of the waste monitor

tank prior to sample acquisition;

inadvertent

automatic start of the

4B emergency diesel

generator;

and inadvertent de-energizing

of the

3A safeguards

bus.

The licensee's

corrective actions for these

13

2.

issues

resulted

in a decrease

in the number of surveillance-related

problems during the later part of this

SALP assessment

period

and

no

missed surveillances

have occurred since

September

1992.

During this period, there

was

one violation cited in the area of

Haintenance/Surveillance.

Performance

Ratin

3.

Category:

2

Trend:

Improving

Recommendations

None

D.

Emer enc

Pre aredness

~Anal sis

This functional

area

addresses

activities related to the

implementation of the Emergency

Plan

and procedures,

training of

onsite

and offsite emergency

response

organizations,

licensee

performance

during emergency

exercises

and actual

events,

maintenance

of facilities,

and staffing.

There were four actual

emergency

events:

one Alert (Hurricane Andrew) and three Notices of

Unusual

Events.

Overall, the emergency

preparedness

(EP) program received

strong

management

support,

thereby ensuring

a state of readiness

for

responding to emergencies.

For example,

the licensee

took actions

to improve activation

and staffing of the

Emergency Operations

Facility (EOF)

by assigning

several

members of the plant staff to

fill minimum required positions within the

EOF formerly filled by

corporate office personnel.

In addition, following Hurricane

Andrew, the allocation of resources

for restoration efforts to

ensure

a state of readiness

for the emergency

preparedness

program

was prompt and well organized.

The licensee

continued to maintain adequate

emergency

response

facilities (ERFs)

and equipment,

with appropriate

equipment

surveillance

and functional testing.

ERF communications

were

enhanced

by the utilization of video monitoring capability to

tr ansmit incident status

updates

from the Technical

Support Center

to the

Emergency Operations-Facility- and Operational

Support Center.

The licensee

continued to experience audibility problems with the

plant paging

system during the assessment

period.

Plant paging

problems

have

been identified by the licensee

and the

NRC for

several

years,

including during the

1991

emergency exercise.

Previous corrective actions

have not eliminated the problem.

During

the assessment

period,

the licensee identified additional corrective

actions for the paging problems that will be completed during the

14

next

SALP period.

The licensee's

performance during annual

exercises,

as well as

during an NRC-observed

simulator drill and interviews with response

personnel,

demonstrated

an emergency

response

organization that was

well trained

and prepared

to carry out the

Emergency

Plan

and

implementing procedures.

The licensee

demonstrated

an effective

response

capability during both the calendar year

1991

and

1992

exercises.

During these exercises,

the emergency classification

procedures

were effectively used to promptly and correctly classify

the scenario

accidents.

The response

organization

demonstrated

timely and effective communications with State

and local

authorities.

Accident mitigation information flow was effective

between

the

ERFs

and, with one exception,

the appropriate protective

action recommendations

(PARs) were

made for onsite personnel

and the

public.

The one exception resulted

in an exercise

weakness

due to

overly conservative

PARs based

on erroneous

data provided to the

EOF

by the engineering

accident

assessment

team.

The licensee's

critique was effective in the identification of the

PAR weakness

and

improvement items.

A computerized tracking system

was

implemented

for tracking exercise findings to resolution.

During the assessment

period,

observed

exercise

strengths

included

interface with State

and local officials;

ERF staffing;

emergency

classification; notification; Operational

Support Center operations

(team assembly,

briefings,

and deployment); facility status

boards;

and control

room staff responding

in the simulator.

The licensee

used the simulator during

an annual

exercise for the first time,

and

it performed well.

The exercise

scenarios

were detailed

and

posed

challenges

to the entire emergency organization.

However,

review of

the scenario

by the

NRC disclosed that the initiating conditions for

the graded exercise of 1991 contained similarities to that of the

previous year,

and the

1992 NRC-evaluated

exercise

contained similar

initiating events

as those of training exercises

conducted

during

April 1992.

The licensee

acknowledged

the exercise similarities and

committed to scenario

reviews to preclude recurrence.

Four emergency declarations

were

made during the

SALP period.

The

most significant event during the period was the Alert declaration

made

on August 24,

1992,

as

a result of Hurricane Andrew.

The

remaining events

were classified

as Notifications Of Unusual

Events

(NOUEs).

In each event, classifications

were correct

and timely.

With the exception of the Alert classification, notifications to

offsite authorities

were made"in accordance

with requirements.

During the hurricane,

the licensee's

communications

systems

became

disabled,

resulting in loss of the capability to notify offsite

authorities'onsequently,

the facility was unable to make the

notifications

as specified in 10 CFR Part 50.

After the hurricane,

the licensee

took prompt corrective actions to restore all

communications

systems.

Corrective actions

included

enhancements

as

well as replacements.

For example,

the previous

phone lines were

replaced with an underground fiber optic cable;

a microwave system

15

2.

was

added

as

a backup;

and two new radio systems

were installed with

replaceable

antennas.

In addition,

prompt actions

were taken to

repair and/or replace all sirens

used for alerting the public.

The

licensee

performed extremely well in hurricane-related

response

activities, including:

storm preparation; facility activations

(including decision-making

regarding relocation of ERFs); protection

of plant personnel

and the identification of potential safety

hazards;

approach to identification and resolution of issues

affecting onsite

and offsite emergency

preparedness;

and the prompt

well-organized restoration efforts (affected

ERFs,

communications,

staffing,

and offsite interface).

During the assessment

period,

one exercise

weakness

and

no cited

violations were identified in the Emergency

Preparedness

area.

Performance

Ratin

3.

Category:

1

Recommendations

None

E. ~Securit

~Anal sis

This functional

area

addresses

security activities associated

with

the plant's safety-related vital equipment

and the Fitness-For-Duty

program.

The site's security force was fully staffed to meet the licensee's

security manning

commitments of the Physical

Security Plan

and

continued to perform security functions very well.

The licensee's

security force was effectively managed,

well supervised,

and

had

very good procedures.

A thorough self-assessment

program concluded

that the Security Section

was well managed

and met the commitments

of the Physical

Security Plan

and procedures.

Security training was well planned

and executed.

The Meapons

gualification Program exceeded

the requirements

of the Security

Training and gualification Plan.

The progressive

security training

program

has contributed to outstanding

personnel

performance

in

daily-operations

and responses

to.contingency drills.. A major.

strength of'he training program was the continued joint tactical

response

training conducted with local law enforcement

agencies.

The most recent joint training culminated in a large-scale

contingency exercise

involving Federal,

State,

and local agencies

including maritime response

units.

Site management's

continued

support

was demonstrated

by funding and beginning construction of a

new firing range

and training facilities to replace facilities

destroyed

by the hurricane.

Additional management

support included

16

the availability of site personnel

and resources

to participate in

the joint contingency exercises

and the priority given to the

replacement

and repair of security

systems

and equipment

damaged

by

the hurricane.

During this assessment

period, the licensee

completed the major

upgrade of the security system that was ongoing during the previous

assessment

period.

The system

upgrade significantly improved

security program effectiveness

through

enhancement

of intrusion

detection

and assessment,

access

controls,

and operational

management

of the security force.

Completion of the security system

upgrade resulted in the, elimination of nine long-term compensatory

posts;

a significant savings in security manpower requirements.

Additional improvements

in the security system during the assessment

period included the addition of a video capture

system to the closed

circuit television

assessment

equipment

which greatly enhanced

the

ability of the alarm station operators

to assess

perimeter fence

alarms.

2.

The operational

capability and survivability of the upgraded

security

system

was severely tested

by Hurricane Andrew.

Although a

major portion of the system withstood the hurricane winds, security

system

components

and facilities sustained

considerable

damage,

necessitating

extensive

use of compensatory

measures.

The licensee

aggressively

responded

to the challenge to promptly restore

the

security

system to full operational

status.

Through the aggressive

rebuilding effort, which was 'strongly supported

by senior

management,

the licensee

restored

the physical security system to

'peration

and reduced

compensatory

measures

to a minimum within 28

days.

The licensee's

Fitness-For-Duty

program continued to be effective in

meeting the objectives of a drug-free workplace

and licensee

commitments relative to access

authorization

and the prevention of

the introduction of contraband

items into the protected

area.

Random testing for drugs

and alcohol

was conducted

in accordance

with procedural

requirements

and the confidentiality of test results

was assured.

Reportable

events

were thoroughly addressed

and

reported in a timely manner.

No violations were cited in the Security area during this assessment

period.

Performance

Ratin

'3.

Category:

1

Recommendations:

None

17

F.

En ineerin

Technical

Su

ort

~Anal sis

This functional area

addresses

activities associated

with the design

of plant modifications

and engineering

and technical

support for

operations,

maintenance,

outages,

and licensed operator training.

In addition to routine inspections,

four special

inspections

were

conducted:

Allegation Team Inspection,

Procurement

Engineering,

Structural

Design Audit, and Hurricane Andrew Recovery.

The licensee's

performance

in providing engineering

and technical

support

was good during this assessment

period, with some

improvements

noted over the previous period.

The engineering

and

technical

support groups generally took a proactive

approach to

resolving difficult engineering

problems.

Emergent

issues for both

operations

and maintenance

were generally aggressively identified

and resolved.

However,

weaknesses

continued

from the previous

SALP

period in contractor oversight

and the selection

and specification

of reliable plant equipment.

Weaknesses

were also identified in

other areas

including procedure

review, technical

communication,

and

plant drawings.

Notable actions

completed

by engineering

and technical

support

during the period included elimination of the drawing update

backlog

ahead of schedule,

issuance

of new computer-generated

piping and

instrumentation

drawings that superseded

existing plant operating

drawings,

reduction in the number of temporary

system alterations

(TSAs) from approximately

30 in the last

SALP period to 14,

and

successful

completion of the senior reactor operator certification

training by the engineering

manager

and the technical

support

manager.

Engineering

and technical

support for plant modifications was

generally good.

A documented

design

bases for Turkey Point Units 3

and

4 has

been developed

and the design

bases

documents

were updated

and programmatically controlled.

The quality and technical

content

of the modification packages

were good.

The Project'eview

Board effectively prioritized engineering

work.

High priority design

changes

and emerging technical

support

activities were documented

in the top 20 list for each unit, to be

worked during outages,

and the top 30 list to be worked while the

units were on-line.-

New work-items could only. be added

when

an item

was completed

on one of the above lists.

The result

was more active

engineering

involvement in providing timely day-to-day support to

the plant

and

a very low backlog of items

on hold for engineering

and techni'cal

support

by the end of the period.

For example,

the

backlog of Non-conformance

Reports

(NCRs) decreased

from 300 in 1990

to an average of less than

20 by the end of 1992 and,

as noted

previously, the backlog of TSAs decreased.

18

The licensee's

assessments

of Architect-Engineering

(AE) activities,

Plant Engineering

Group

(PEG) actions,

design reviews, guality

Assurance

(gA) audit support,

and the Technical Alert Program

(an

engineering

communication tool) were effective in identifying areas

for improvement within the design organization.

These efforts

demonstrated

the licensee's

ongoing proactive

approach

toward

enhancing

the quality "of engineering

support.

During this assessment

period, the licensee initiated several

actions to help improve performance

in the engineering

and technical

support area.

These actions included:

developing generic

engineering specifications to support routine repetitive

maintenance/construction

activities (i.e. temporary

lead shielding,

conduit routing, mounting standards,

etc.); involving the system

engineers

and the Probabilistic Risk Analysis

(PRA) Group in the

Maintenance

Department quarterly schedule of activities;

and issuing

a Nuclear Policy that restricted the use of unproven

or one-of-a-

kind designs

and required testing if proven

components

were not

available.

The plant-specific

PRA model for Turkey Point was applied to the

design control

and the preventive maintenance

programs during this

assessment

period.

PRA information was used for the evaluation of

plant modifications to the instrument air system.

Engineering

and technical

support staff provided excellent plant

support for the

damage appraisal,

recovery,

and restart efforts

foll.owing Hurricane Andrew.

The engineering

evaluations for the

fossil Unit

1 chimney demolition, the Unit 2 chimney condition,

and

the required plant change/modification

packages for the fire

protection

system recovery effort were timely and well done.

Other proactive actions in the Engineering/Technical

Support

area

included:

continuation of 100 percent

eddy current testing of all

steam generators

each

outage,

performance of a post-refueling

startup test program

on Unit 3 after the dual-unit outage

even

though

no refueling or core design

change

had occurred,

and

development of an outage

shutdown risk management

procedure that

controlled equipment to be taken out of service.

Meaknesses

in drawings

and operator training contributed to plant

events during this assessment

period.

For example,

an oil spill of

approximately

100 gallons

on the Unit 4 turbine deck was caused

by

an inadequate

clearance

attributed to the -lack. of plant operating

drawings

and insufficient operator training on the turbine bearing,

control,

and guarded oil systems.

Poor quality drawings contributed

to an inadequate

clearance

and the subsequent

spill of slightly

radioactive water in the auxiliary building.

A drawing error in the

fire protection

system

and discrepancies

in control of temporary

system alterations

and controlled diagrams

were also noted during

this period.

19

Weaknesses

in engineering

oversight of contractors

were noted both

early and late in the

SALP period.

The early event

was associated

with a Westinghouse

Eagle

21 system that replaced

several

Hagan

reactor protection

system

(RPS) racks.

Westinghouse

was contracted

to design, install, test,

and provide procedures

and training for

the Eagle

21 modification.

Due to inadequate

communications

and

followup, problems with discrepancies

in tuning constants

used to

process

excore detector signals for overtemperature

delta tempera-

ture

and overpower delta temperature

were identified during low

power physics testing.

Subsequently,

during Incore/Excore nuclear

detector calibration at

50X reactor

power, the range of adjustment

for the scaling factor for the overtemperature

delta temperature

setpoint

exceeded

the acceptance

capability of the Eagle

21

hardware.

Late in the

SALP period,

a licensee

investigation into an

unexpected

increase

in the local peaking factor and

a more positive

power distribution following a Unit 3 post-refueling startup

determined

the cause to be improperly manufactured

wet annular

burnable

absorbers

(WABAs).

The

WABA rod absorber centerlines

were

incorrectly positioned for both units.

There

was evidence of inadequate

procedure

review.

During the Unit

3 startup

from the dual-unit outage,

an operator

observed that

operating

procedures

permitted axial flux deviations outside the

target

band while at

100X reactor

power.

However,

TS did not permit

operation outside the target

band at or above

90X reactor

power.

The operators

realized this and reduced

power to less than

90X after

violating the

TS requirement while following the procedure.

Problems

were observed

in the engineering

selection

and

specification of reliable equipment.

There were problems with new

equipment installed during the dual-unit outage.

The

new emergency

diesel

generator

(EDG) air compressors

required engineering

redesign

to operate properly.

Also, the auto test feature

on the

new

safeguards

sequencer

failed and

a redesign

was required.

FPL

engineering

subsequently

completed

adequate

redesigns.

Effective licensed operator training was demonstrated

during this

assessment

period

by performance

on licensing examinations.

In

October

1992, initial examinations

were administered to eight

Reactor Operators

(ROs)

and nine Senior Reactor Operators

(SROs).

In April 1992, initial examinations

were administered

to three

ROs

and two SROs.

A 100X pass rate

was attained for both examinations.

Six of seven operator candidates

passed

the Generic

Fundamentals

Examination.

Requalification examinations. were administered

in

.

February

1992, to two,ROs

and eighteen

SROs.

Seventeen

SROs

and all

ROs passed

the examinations.

All five crews evaluated

passed

the

requalification simulator examinations.

Five violations were cited in the Engineering/Technical

Support

area

during this assessment

period.

20

2.

Performance

Ratin

3.

Category:

2

Trend:

Improving

Recommendations

None

G. Safet

Assessment

ualit

Verification

~nal sis

This functional

area

addresses

licensee

implementation of safety

policies; license

amendments,

exemptions,

and relief requests;

responses

to Generic Letters, Bulletins,

and Information Notices;

resolution of safety issues;

reviews of plant modifications

made

under

10 CFR 50.59; safety review committee activities;

and use of

feedback

from self-assessment

programs

and activities.

During this assessment

period, the licensee

demonstrated

a proactive

and conservative

approach to nuclear safety in preparing for and

coping with Hurricane Andrew.

Comprehensive

procedures,

early

severe

weather preparations,

and reinforcement training of reactor

operators

at the simulator for various accident

scenarios

as the

storm approached

were examples of good planning.

The licensee's

damage

assessment

and restart efforts following the storm were also

thorough,

demonstrating

technical capabilities

and commitment to

plant safety.

Licensee

corporate

management

maintained direct involvement with

plant status

by monthly status

meetings.

The meetings

were

beneficial in ensuring that issues

were forwarded to the appropriate

level of management

and in ensuring that assignees

of recommended

actions

were held accountable for their responses.

Increased

management

and supervisory

presence

in the field was also evidenced

by the stationing of managers

in the control

room during critical

plant evolutions

and by the development of. an off-hours tour program

for managers.

The licensee's

self-assessment

oversight groups,

including the Plant

Nuclear Safety Committee

(PNSC), the

Company Nuclear Review Board

(CNRB),

and the Independent

Safety Engineering

Group (ISEG),

performed well during this period.

The

PNSC provided

a

comprehensive

overview of plant performance

and effectively ensured

that matters

concerning nuclear safety were brought to the attention

of plant management.

The

CNRB effectively provided

a comprehensive

and independent

overview of plant performance

by experienced

personnel

with varied backgrounds.

CNRB members

attended

PNSC

meetings,

reviewed

NRC and equality Assurance

audit findings,

and

reported

on observations

during site tours.

Special

ISEG reviews

and

CNRB meetings

were conducted to assess

plant readiness

for

restart following Hurricane Andrew.

0

21

During this assessment

period, the licensee's

guality Department

audit program continued to be comprehensive

and effective in

identifying problems.

The guality Department

conducted

performance-

based

evaluations

which contributed to the facility's overall

assessment

efforts.

The group's audits identified several

issues of

non-compliance with NRC regulations

whi'ch were then promptly

corrected.

Examples

included the failure of a subcontractor

to test

diesel

fuel oil for sulphur content in accordance

with the test

method specified in the technical specifications,

the failure to

perform post-maintenance

testing of a component cooling water heat

exchanger drain valve and of the Unit 4 spent fuel pool purification

pump,

and the inadequate

line supervisory capability of the

intrusion detection

system.

In addition, investigations

were

initiated based

on reports of industry events

and resulted

in

findings related to deficiencies

in operator log-keeping.

As a

result,

the Operations

Department instituted

a monthly audit program

and the guality Department

began

random quarterly independent

audits

of log-keeping.

For major problems,

the guality Department

performed

independent

root cause

analyses

using management

oversight risk tree techniques.

The guality Department

also provided on-shift coverage

during major

plant evolutions, utilized outside technical

experts for audits in

the areas of environmental qualification and security to provide

current industry knowledge,

and performed post-Hurricane

Andrew

reviews in support of recovery

and restart activities.

In addition,

there

was

an improvement in the amount of time audit findings

'emained

open awaiting corrective action.

At the end of the

previous

SALP period, there were

no open findings older than

180

days, while at the end of the current

assessment

period, there were

no open audit findings older than

60 days.

This indicated

a

continued

improving trend in timeliness of correcting issues.

Event Review Team reports

and Nuclear Division Performance

Honitoring Hanagement

Information Reports

were reviewed at various

levels of management

for the effectiveness

of self-assessment

activities.

The Event Review Team reports identified several

areas

for improvement in plant procedures

and processes

based

on the root

cause

analysis of problems.

Some of the problems

analyzed

during

this assessment

period by the Event Review Team included the

auxiliary feedwater

pump outboard thrust bearing failure, the

3B

feedwater heater

tube failures,

an exciter field ground,

an

inadvertent safety injection during a containment isolation rack

surveillance,

and high sodium concentrations 'in the steam

generators.

Nuclear Division Performance

Honitoring Hanagement

Information Reports,

which were distributed to upper management

on

a

monthly basis,

were effective for monitoring plant performance,

defining corrective actions,

and tr acking

and trending nuclear

safety issues.

During this assessment

period, the licensee

took several initiatives

to help improve plant performance.

To strengthen

management

22

operating

knowledge, five managers

completed

a Senior Reactor

Operator certification class

which began in February

1992.

Another

group of managers

was scheduled

to attend this course later in 1993.

The Operations

Manager also attended

a five-week Senior Management

Course.

In addition, the

CNRB Chairman attended

a Senior Reactor

Operator certification class at St. Lucie.

To focus resources

and

efforts, the licensee initiated annual strategic

planning tasks with

assigned

task teams

and periodic progress

reviews during the monthly

status

meetings.

One of the

1992 tasks

involved developing

and

implementing

a new consolidated

reporting system to provide

a single

reporting process

by which conditions of concern to the plant staff

may be identified, evaluated,

analyzed,

and corrected.

This system

reduced

the number of different types of reporting systems

and

provided

a mechanism for all employees

to easily identify problems

to site management

for corrective actions.

Another 1992 task

involved the development

and implementation of a detailed quarterly

work schedule to improve maintenance

efficiency and equipment

reliability (See Section IV.C.).

The licensee's

submittals to the

NRC during the previous

SALP period

included

some which were not of good quality.

During this

assessment

period, the quality of the licensee's

submittals in

support of licensing activities was again mixed.

Many of these

submittals

were comprehensive,

timely, and reflected

a sound

understanding

and appreciation of the technical

issues,

regulatory

requirements

and the

NRC licensing processes.

For example,

three

requests

for temporary waivers of compliance

were comprehensive,

timely,

and well-supported.

During the recovery period following

Hurricane Andrew, the licensee

prepared

and submitted several

excellent

and timely safety evaluations

supporting activities

such

as the interim fire protection system,

demolition of the Unit

1

chimney,

and

an assessment

of the Unit 2 chimney condition.

Licensee

Event Reports

submitted during this period were generally

timely, well-written, and adequately

addressed

root causes

and

corrective actions.

On the other hand, there were

a number of licensing submittals

during the period which were inadequate.

For example,

a request for

a TS change to modify relays in the 480-volt degraded

voltage

protection

scheme

in the engineered

safety features

actuation

system

was deficient in scope

and justification and did not reflect

a sound

understanding

of the technical

issues.

The licensee's

evaluation in

support of a relief request to enable

a non-Code repair of a leaking

main -steam drain pipe did not properly consider the loads

on the

pipe necessary

to demonstrate

structural integrity.

The licensee

requested

and was granted interim approval of certain inservice

inspection testing relief requests,

but failed to follow up promptly

with revised

permanent relief requests.

When submitted,

the

permanent relief requests

were not adequate,

needed

several

iterations,

and required

a last-minute expedited staff review to

support the licensee's

schedule

needs.

23

No violations were cited in the Safety Assessment/Quality

Verification area during this assessment

period.

2.

Performance

Ratin

Category:

1

3.

Recommendations

None

V.

SUPPORTING

DATA

A. Licensee Activities

B.

Units 3 and

4 began this assessment

period in a dual-unit outage for

electrical

upgrades

and both units ended the period at power.

Unit 3 was placed

on line on October

1,

1991.

It remained

on line

for the remainder of the period, with the exception of one manual reactor trip, three

unplanned

shutdowns,

two other occasions

when the

unit was taken off line for maintenance,

and

a combined Hurricane

Andrew/refueling outage late in 1992.

Unit 3 availability for the

period was

74X.

Unit 4 was placed

on line on October 29,

1991.

It remained

on line

for the remainder of the period, with the exception of one automatic reactor trip, five unplanned

shutdowns,

three other occasions

when the

unit was taken off line for maintenance,

and

a Hurricane Andrew

outage late in 1992.

Unit 4 availability for the period was 83X.

The licensee's

Quality Department

was reorganized

in November

1991 with

Quality Assurance

and Quality Control

becoming

one organization

reporting to a Site Quality Hanager.

Reactor Tri

s

and

Un lanned

Shutdowns Un't Taken Off Line

Reactor Trips:

October 3,

1991:

Unit 3 was manually tripped in response

to a

mechanical failure of a piping nipple in the turbine control oil

system.

The unit was

down for 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />.

Narch 26,

1992:

- Unit -4 tripped automatically

due to a switch failure

during surveillance testing of containment isolation racks.

The unit

was

down for 39 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br />.

Unplanned

Reactor Shutdowns/Unit

Taken Off Line:

December

10,

1991:

Unit 4 was manually shut

down for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

due to

a load sequencer

failure.

The unit remained

down for an additional

165

hours to repair

a conoseal

leak.

Unit 4 was returned

on line on

'

December

18.

January

3,

1992:

Unit 3 was manually shut

down to repair

3B

RCP oil

leakage.

The unit was

down for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

January

28,

1992:

Unit 4 was manually shut

down for repairs to

a

leaking welded joint on

a flow transmitter

on the

4C steam generator.

The unit was

down for three days.

March 25,

1992:

Unit 4 was taken off line to correct

a turbine

generator exciter water intrusion problem.

The unit was off line for

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

April 27,

1992:

Unit 3 was manually shut

down to replace

the

3C

RCP

seal.

The unit was

down for 15 days

and was returned

on line on May

12,

1992.

May 7,

1992:

Unit 4 was taken off line due to steam generator

chemistry problems.

The unit was off line for eight hours.

August 23,

1992:

Unit 4 was manually shut

down for Hurricane Andrew.

The unit remained

down for post-hurricane

repairs for 37 days

and was

restarted

on September

29.

August 23,

1992:

Unit 3 was manually shut

down for Hurricane Andrew.

The unit remained

shut

down for post-hurricane

repairs

and

a refueling

outage.

The unit was

down for 102 days

and

was returned

on line on

December

3.

September

29,

1992:

Unit 4 was manually shut

down from Mode

2 in

response

to the identification of two missed

TS surveillances

and

problems with the

B AFW pump overspeed trip.

The unit was

down for

eight hours,

then restarted.

October

1,

1992:

Unit 4 was manually shut

down from 30K power - this

was

a voluntary licensee

action until

FEMA completed

an evaluation

of offsite state

and county emergency

preparedness.

The unit was

down

for 23 days

and

was restarted

on October 24.

December

4,

1992:

Unit 3 was taken off line for turbine overspeed

testing

and to correct

a main generator exciter fan problem.

The unit

was off line for two days.

January

7,"1993:

Unit 4 was taken off line to repack the

4A steam

generator

feed regulating valve.

The unit was off line for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

January

8,

1993:

Unit 3 was taken off line to repair

a steam leak on

a

3B moisture separator

reheater

drain line.

The unit was off line for

32 hours3.703704e-4 days <br />0.00889 hours <br />5.291005e-5 weeks <br />1.2176e-5 months <br />.

0'

25

C. Direct Ins ection

and

Review Activities

During the assessment

period,

35 routine

and

seven special

inspections

were performed at Turkey Point by the

NRC staff.

The special

inspections

were:

Allegation Team Inspection of Engineering Actions

Procurement

Engineering

Structural

Design Audit

MOV Program Inspection

Hurricane Andrew Recovery (three inspections)

D. Escalated

Enforcement Actions

l. Orders

None

2. Civil Penalties

None

E. Confirmator

Action Letters

None

F. Licensee

Conferences

During the

SALP period,

17 meetings

were held with the licensee

to

discuss

active licensing issues,

other issues of interest,

and licensee

self-assessments,

accomplishments,

and plans.

The subjects of the more

significant meetings

included:

October

15,

1991

January

9,

1992

April 3,

1992

July 9,

1992

Sept.

10,

1992

Sept.

22,

1992

November 2,

1992

November

16,

1992

Eagle

21 problems during Unit 3 startup

Engineering initiatives

New load sequencers

and instrumentation

setpoints

Proposed

temporary

non-Code repairs to main

steam drain line

Status of restoration of nuclear units

after Hurricane Andrew

Interim fire protection configuration; Unit

2 chimney evaluati'on,

and Unit 4 restart

plan after Hurricane Andrew

Licensee

self-assessment

presentation

Unit 3 restart

plan after Hurricane Andrew

and refueling

26

G.

icensin

Activities

During the assessment

period, the staff completed

51 licensing

activities, while 44 new ones

were opened.

Eight of the closed

items were

amendments

and the remainder

were multi-plant and other

regulatory activities, including

NRC Bulletins and Generic Letters.

H. Review of Licensee

Event

Re orts

For the assessment

period,

a total of 34

LERs were analyzed.

The

distribution of these

events

by cause,

as determined

by the

NRC staff,

is as follows:

Cause

1.

Component Failure

2. Design

3. Construction,

Fabrication,

or Installation

Unit 3 or Common

Unit 4

4. Personnel

Error

a. Operating Activity

b. Maintenance Activity

c. Test/Calibration Activity

d. Other

2

1

10

1

5. Other

ota

Note 1:

With regard to the area of "Personnel

Error," the

NRC

considers

lack of procedures,

inadequate

procedures,

and erroneous

procedures

to be classified

as personnel

error.

Note 2:

The "Other" category is comprised of LERs where there

was

a

spurious signal,

a totally unknown cause,

or an external

cause

such

as natural

phenomena.

Note 3:

In addition to the above,

one voluntary

LER was submitted,

which was not considered

in this report.

27

I. Enforcement Activit

unctsona

Area

o.

o

so atsons

1n

ac

ever>ty

eve

V

IV

III

II

I

Unit 3/Unit4

ant

peratlons

Radiological

Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

1/1

1/1

0/0

0/0

5/5

0/0

Net total

(each Violation counted

once)

12

~

'