ML17348A596

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Initial SALP Repts 50-250/90-26 & 50-251/90-26 for Aug 1989 - Jul 1990
ML17348A596
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/25/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17348A595 List:
References
50-250-90-26, 50-251-90-26, NUDOCS 9010160219
Download: ML17348A596 (39)


See also: IR 05000250/1990026

Text

ENCLOSURE

INITIAL SALP

BOARD REPORT

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE

INSPECTION

REPORT

NUMBER

50-250/90-26

AND 50-251/90-26

FLORIDA POWER

AND LIGHT

TURKEY POINT UNITS 3 AND 4

AUGUST 1,

1989 - JULY 31,

1990

TABLE OF

CONTENTS

~Pa

e

I ~ INTRO DUCT ION

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1

II. SUMMARY OF RESULTS ..........,,...,,...............,...,....

2

I II. CRITERIA ..............................'.................,...

3

IV. PERFORMANCE ANALYSIS

A.

B.

C.

D.

E.

F.

G.

Plant Operations .....................

Radiological Controls ................

Maintenance/Surveillance ...,..........

Emergency

Preparedness ...............

Security

& Safeguards ..............,.

Engineering/Technical

Support ........

Safety Assessment/equality

Verification

3

7

9

13

15

16

20

V. SUPPORTING

DATA

A.

Licensee Activitses ......................,...,

B.

Direct Inspection

and Review Activities ..'.....

C.

Escalated

Enforcement Actions ...........,.....

D.

Licensee

Conferences

Held During Appraisal

Peri

E.

Confirmatiog of Action Letters ................

F.

Reactor Trips ........;..................,....,

G.

Review of Licensee

Event Reports

and

10 CFR 21

H.

Licensing Activities ..........................

I.

Enforcement Activity ..........................

~

~ 4 ~ ~ ~ ~

od ....

~ ~

~ ~ ~ ~ ~ ~

Reports.

23

23

24

24

24

24

2627,

27

I.

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is an

integrated

NRC staff effort to collect available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

on the basis

of

this information.

The program is supplemental

to normal regulatory

processes

used to ensure

compliance with NRC rules

and regulations.

It

is intended to be sufficiently diagnostic to provide

a rational

basis for

allocation of NRC resources

and to provide meaningful

feedback to the

licensee's

management

regarding

the NRC's assessment

of their facility's

performance

in each functional area.

An NRC SALP Board,

composed of the staff members listed below, met on

September

6, 1990, to review the observations

and data

on performance,

and to assess

licensee

performance

in accordance

with Chapter

NRC-0156,

"Systematic Assessment

of Licensee

Performance."

The guidance

and

evaluation criteria are

summarized

in Section III of this report.

The

Board's findings and recommendations

were forwarded to the

NRC Regional

Administrator for approval

and issuance.

This report is the NRC's assessment

of the licensee's

safety performance

at Turkey Point Units

3 and 4, for the period August 1, 1989,

through

July 31,

1990.

The SALP Board for Turkey Point was

composed of:

L. A. Reyes, Director, Division of Reactor Projects

(DRP), Region II

(RII) (Chairman)

A. F. Gibson, Director, Division of Reactor Safety,

RII

J.

P. Stohr, Director, Division of Radiation Safety

and Safeguards,

RII

M. Y. Sinkule, Chief, Reactor Projects

Branch 2,

DRP, RII

R.

C. Butcher, Senior Resident

Inspector,

Turkey Point,

DRP, RII

H. H. Berkow, Director, Project Directorate II-2, Office of Nuclear

Reactor Regulation

(NRR)

G. Edison, Project Manager, Project Directorate II-2, NRR

Attendees

at

SALP Board Meeting:

R.

Y. Crlenjak, Chief, Project Section

2B,

DRP, RII

R.

P. Schin, Project Engineer,

Project Section

2B,

DRP, RII

K. D. Landis, Chief, Technical

Support Staff,

DRP, RII

II.

SUMMARY OF RESULTS

Turkey Point operated with improved performance

during the assessment.

period.

Management

continued to upgrade

the material condition of

jhst'ystems

and components

which resulted

in improved operating

times

wTK..

fewer failures

due to equipment malfunctions.

Significant improvemfwas

noted in the areas

of Security

and Safety Assessment/guality

Verifia5'an.

Improved performance

was also demonstrated

in the areas of RadiologM

Controls

and Maintenance/Surveillance.

Although there

was

a reduction in

personnel

errors in the Operations

area

over this

SALP period,

an iuxease

occurred

near the end of the period.

Additional attention

should

he

directed to this problem.

There

has

been considerable

improvement in the area of Security.

Gages

in management

made during this

and the prior assessment

period haveTad

to marked

improvement in this area.

Upgrading of the security traiexg

program

and enhanced

security communications capability were other

initiatives which have contributed to the overall

improvement.

ExtmPve

hardware modifications, currently in progress,

are expected

to resuifix

.

an excellent security complex.

The Safety Assessment/guality

Verification area

has also

shown not8h-

improvement.

Your ability and comnitment to determine "root cause"Xs

improved substantially,

to the point that repeat events/failures

wee;

minimized.

The preparation efforts, including self-assessments

con6zt'ed

by Regulatory

Compliance

and guality Assurance,

resulted

in positive

findings by the

NRC in several

team inspections

conducted

during

tha3LLP.

period.

The licensee's self-identification of NRC violations is

considered

a significant indicator of effectiveness

in this area.

'3heach

self-identified case,

prompt and thorough corrective actions

were tkh= hy

the licensee.

For licensing activities, significant improvement in%.

timeliness of submittals

and responses

to

NRC initiatives was notch

8oth the Radiological Controls

and Maintenance/Surveillance

areas

ha8

improved.

The area of Radiological Controls benefited

from the posture

efforts in reducing collective dose expenditure,

contaminated floorsym,

and personnel

contamination

events.

The positive achievements

in th:.

Maintenance/Surveillance

area resulted in improved plant and equipmaf

reliability.

Strengths

in this area

were:

personnel

staffing and nfzed,

turnover rates;

upgrading of the auxiliary building;

PWO backlog

reduction; preventive maintenance

program,

and

a reduction of contr8'toom

deficiency tags.

Although the licensee

has taken measures

to contr@:

rework PWO's, with noted improvements,

additional attention is warmed..

Improvement continues with no changes

in SALP ratings

over the previm

SALP period in the areas of Operations,

Emergency

Preparedness,

and

Engineering/Technical

Support.

Clearly all areas

have benefited bye

licensee's

commitment to improve and to make safe operation

a prio~

making conservative

choices

when necessary.

. Functional

Area

Facil it

Performance

Summar

Rating Last

Period

Rating This

Period

Plant Operations

(Operations

& Fire Protection)

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

En ineering/Technical

Support

Engineering, Training

& Outages)

Safety As'sessment/

guality Verification

(guality Programs

& Licensing)

III. CRITERIA

2

2

2

3 Improving

2

2 Improving

2 Improving

2

2 Improving

2

The evaluation criteria which were used,

as applicable, to assess

each

functional area

are described

in detail in NRC Manual Chapter 0516.

This

chapter is in the Public Document

Room files.

Therefore

these criteria

are not repeated

here, but will be presented

in detail at the public

meeting held with the licensee

management

on October 3, 1990.

However,

the

NRC is not limited to these criteria and others

may have

been

used,

where appropriate.

IV.

PERFORNNCE

ANALYSIS

A. ~10

l. ~Anal sis

This functional area

addresses

the control

room and performance of

activities directly related to operating the unit, as well as fire

protection.

These activities were viewed during routine and special

inspections

conducted

throughout the asessment

period.

8oth units have

been shut

down and started

up numerous

times during

the

SALP period.

Changes

in plant modes'and

power levels were

conducted

in a controlled

and professional

manner.

Several

times,

prompt actions

by the operators

stabilized the plants during

transient conditions.

There were two reactor trips on Unit 3 during

the

SALP period.

One was attributed to operator error while conduct-

ing a load reduction associated

with a condenser

tube leak

and the

other trip was associated

with an equipment

pr'oblem.

On Unit 4,

three of 'the four reactor trips resulted

from equipment

problems

and

one trip was attributed to operator error, during testing.

The

equipment

problems that caused

the trips were not repetitive

failures.

During the previous

SALP period,

two reactor trips

occurred, of which one was

due to operator error.

Overall, operator

performance

has

been satisfactory.

Personnel

errors,

inadequate

component labeling,

and improper

clearances

had contributed to

a number of events

during the previous

SALP period.

The licensee

has

taken actions to specifically address

each of the previous

problem areas.

In the area of component

labeling, the licensee

implemented

a program to include independent

verification of labeling

and improve the process

of identifying and

correcting in-plant labeling problems

by utilizing the system

engineers.

There

has

been

a substantial

increase

in labeling since

the previous

SALP.

The licensee's

changes

'in this program have

been

effective.

Ouring this

SALP period, there

has not been

an event

which has

had mislzbeling identified'as

the root cause.

Personnel

errors

were fewer than experienced

during the previous

SALP

period; however,

near the end of this

SALP period there were events

that indicated

a lack of attention to detail.

Ouring a four-day

period in May 1990,

one unit entered

mode

3 from mode

4 with a

containment isolation valve pinned

open in lieu of pinned closed

and

with both channels

of the Reactor

Vessel

Level monitoring system

inoperable,

and exceeded

an administrative limit of 380 degrees

F

with both safety injection (SI) system flowpaths locked closed.

Other events

appeared,to

be related to lapses

in the

command function

in the control

room; e.g., in May 1990, Unit 4 was inadvertently

tripped when an operator (with the plant supervisor's

concurrence)

pushed the manual reactor trip buttons in lieu of continuing the

reactor startup

as intended;

and in June,

1990, Unit 3 was

inadvertently tripped when

an operator pulled control rods to control

temperature

and failed to monitor reactor

power, resulting in a

reactor trip at

10K reactor

power.'o

increase

operator attention to detail, Operations

has

increased

its effort to understand

how different events

occur and to implement

corrective actions appropriate

to them.

One of these efforts has

been to conduct weekly open discussions

with the operating

crews

on

the events,

the root causes,

causal

contributors,

and actions'needed

to prevent

a similar occurrence

in the future.

These shift meetings

have helped to identify problem areas

so that they could be acted

on,

and

have provided personnel

with a better understanding

of the events

and management's

expectations

in similar situations.

As a result of

the discussions

and other corrective actions (i.e., procedure

changes,

self-check training,

and discipline) the operational

error

rate has

decreased

when compared to the

same time frame in 1989.

The

licensee

plans to provide additional

simulator training time for

operators

over the next year, including emphasis

on normal

evolutions.

Although the

number of events

associated

with clearance

problems

has

decreased

from the last

SALP period, errors involving clearances

were

associated

with two violations cited in the operations

area

and two

in the maintenance

area.

The licensee

has

performed

a review of

their clearance

process

and

as

a result is making changes.

These

changes

include developing simplified clearance

procedures

and

procedures

on handling equipment out of service,

and modifying the

work control measures.

Currently, these

clearance

program changes

are scheduled

to be in place prior to the November

1990 dual unit

outage.

The licensee

has

had problems with inadequate

implementation of

corrective actions for known problems.

During a design validation

inspection,

several

procedural

and equipment

problems

were

identified.

When the licensee's

completed corrective actions

were

inspected,

several

of the previously identified discrepancies still

existed.

In February,

1990,

a leak occurred in the Unit 3 spent fuel

pool

pump room and due to the floor drains

being partially plugged,

approximately

3 inches of water accumulated

in the spent fuel pool

pump room and the cask

wash area.

The spent fuel pool

pump room

floor drains were being periodically tested

but that testing

had not

been adequate.

The licensee

has since revised their method of floor

drain testing.

During the last

SALP period,

on January

20,

1989, the licensee

concluded

the "Management-On-Shift"

(MOS) program.

However, since

the termination of the

MOS program. and during the early part of the

SALP period, the licensee

continued to utilize non-licensee

observers

that were previously part of the

MOS program to obtain

an independent

assessment

of plant operations.

The independent

observer

coranents

were positive, indicating that operato'rs

displayed

a very positive

attitude toward their jobs

and management;

plant personnel

were

continuing to display

a sense

of pride

and ownership; significant

improvements

in cooperation

between

operations

and other departments

were observed;

overall

improvements

in the material condition of the

Auxiliary Suilding were noted;

and shift technical

advisors

were more

involved in shift activities,

such

as coordination of testing.

The

resident inspectors

have

made similar observations

during their

routine inspection activities.

The Operations

department

has

implemented

an in-depth plan-of-the-day

(POD) meeting,

and shift briefings are thorough

and professional.

Operations

explains the shift objectives

and asks

each

department

(chemistry, mechanical

maintenance,

etc.) their main objectives for

their shift.

Also, Operations

personnel briefly explain the status

of the plant in their area of responsibility.

Plant management,

during this

SALP period,

has taken

a conservative

approach

to plant operations.

The following examples

demonstrate

operational

conservatism:

On December

25,

1989, the licensee

took Unit 3 off line to

replace

corroded electrical

terminal blocks,

even

though the

system

demands

were high and temporary

power interruptions

resulted.

On March 25, 1990,

the licensee

stopped all outage

work on Unit

3 to review and walk down clearances

following an inadvertent

spill of water from the reactor water storage

tank.

In Hay,

1990, the licensee

discovered

a control oil leak

on

a

fitting of the left turbine stop valve.

The fitting could

possibly have

been tightened with the unit on line.

However,

the licensee

conservatively

decided to take the unit off line to

avoid risking a plant transient if the oil line failed during

tightening.

The

NRC had expressed

concern in previous

SALPs regarding the use of

excessive

operations staff overtime.

The overtime use

has

remained

at about the

same level

as in the previous

SALP period

(25 to 30 X)

due to outages

and

an aggressive

labeling program,

but was

substantially

reduced

near the end of the

SALP period.

The recent

qualification of two non-licensed

plant operator training classes

and

the planned staffing increases

from the operator license candidates,

presently in training should help control overtime."

Presently

there

are

52 operator license

candidates

in training, with 29 scheduled

to

take the NRCPtest in the first quarter of 1991.

Turnover rate of

on-shift licensed

operators

has

been

low compared to previous

SALP

periods, with 2 of 29 (6.8X) leaving Operations.

An Emergency Operating

Procedure

(EOP) inspection

was conducted

during this period.

The team, concluded that the licensee's

EOPs

adequately

covered the broad

range of accidents

and equipment

failures necessary for safe

shutdown of the units.

Prior to this

inspection,

the licensee

had initiated self audits of the

EOPs

and

made extensive

improvements

to the

EOPs

and the

EOP setpoint

document.

The licensee

committed to take corrective actions for

weaknesses

in Off Normal Operating

Procedures

and other deficiencies

identified by the

EOP

team

and by a Design Validation Inspection.

The inspection of the fire protection features, fire detection

systems

and the fire fighting equipment indicated that these features

were in a state of readiness.

Early in this

SALP period there

was

a

team inspection for conformance to 10 CFR 50, Appendix

R requirements

with no violations identified and late in the

SALP period there

was

a

second

inspection in the fire protection area with no findings.

The

team inspection report recognized that the self assessment

audit

conducted

by the licensee's

gA organization, with contractor

assistance,

was comprehensive

and ensured

the licensee that their

Appendix

R modification program

was satisfactory.

Six violations were cited in the Operations

area during this period.

2. ~Pf

2

Category:

2

3. Recomendations

An increase

in personnel

errors occurred during the final quarter of

this

SALP period.

Additional attention

by the licensee is

recomended

to ensure

that the

command function is maintained

and

attention to detail is enforced.

B. Radiolo ical Controls.

l. ~Anal sis

This functional area

addresses

those activities d;rectly related to

radiological controls

and primary/secondary

chemistry control,

as

viewed during routine inspections

conducted

throughout the inspection

period.

Radiation protection organization

and staffing were adequate

to

protect worker health

and safety.

Organizational

and technical

staffing upgrades,

the majority of which were completed early in the

SALP period, included having the

ALARA Supervisor report directly to

the Health Physics

(HP) Technical

Support Supervisor,

and the

addition of a specialist position to the ALARA group.

Also,

a

HP

Training. and Procedure

Coordinator

improved integration of Radiation

Protection

(RP) personnel

training and

enhanced

the ongoing procedure

development

and/or upgrades.

Overall, the

HP staff provided appropriate

coverage for routine

operations

and outage conditions.

During the

HP contractor

technician. strike,

management

properly trained

and utilized licensee

replacement staff to provide adequate

HP coverage for limited outage

activities.

Licensee

audits of RP activities were comprehensive,

thorough,

and

continued to strengthen

the health physics

program.

Two

RP issues

identified by licensee

audits were reviewed.

Significant technical

upgrades within the

RP program resulted

from the timeliness,

depth,

and

scope of the audits;

the significance of identified issues;

and

appropriateness

of corrective actions.

Procedure

and Radiation

Work Permit

(RWP) guidance for radiation

protection activities were technically sound.

Compliance with

established

procedures

was adequate,

with only two isolated

issues

regarding failure to follow procedures

identified.

One was

a

deficiency regarding maintenance

of Special

Nuclear Material

inventory records,

which was corrected imediately.

The other was

a

violation regarding the failure of selected

workers to follow RWP

requirements.

Licensee evaluation of this issue

and corrective

actions

were thorough

and appropriate

to prevent recurrence.

Overall, the licensee

continued to effectively manage

and

reduce

collective dose expenditure.

The facility's three-year

average

annual collective dose continued to decrease

from 475 to 399

person-rem

per reactor

from 1988 to 1989.

For July 31,

1990, the end

of the current

12 month

SALP cycle, the licensee

projected

a

collective dose of approximately 341.5 person-rem

per reactor

as

measured

by thermoluminescent

dosimeter

(TLD).

=This value represents

a decrease

from the previous

13 month

SALP period,

when collective

radiation

dose

was reported

as

430 person-rem

per reactor.

The

effective management

of dose expenditure

was demonstrated

by the

continued overall reduction

even with increased

routine maintenance

activities, which effectively reduced

source

terms.

Also, this

reduction

was achieved in spite of an unexpected

extension of the

Unit 3 outage to correct reactor

head 0-ring leaks

and also

an

unscheduled

outage to repair Unit 4 pressurizer

spray valves.

These

unplanned activities contributed approximately

76 person-rem

per

reactor to the total

TLD exposure

values,

as estimated

from

self-reading dosimetry.

Licensee

actions to reduce

the percentage

of contaminated floor space

within the radiologically controlled area

(RCA) were very effective.

Actions included

an aggressive

decontamination

program

and subsequent

resurfacing of selected

areas/rooms

within the

RCA, and the use of

catch containments

and prioritizing corrective

and preventative

valve

maintenance.

The licensee started

the

SALP period with 17 percent of

the floor space

(20,929

square feet) contaminated.

By November 1,

this was

reduced to 10 percent.

= This percentage

did increase

during

outages,

but was immediately reduced after outages.

As of July 30,

1990, the percentage

of contaminated floor space

during non-outage

conditions

was being maintained at approximately 8,900 square feet

(ft~), 7.5 percent.

A dramatic

improvement

was noted in the reduction of personnel

contamination

events

(PCEs) reported

between

1988 and

1989,

from 384

to approximately

168 respectively,

as

a result of,employee

awareness

and procedural

upgrades.

The licensee

reported

219

PCEs for .the

current evaluation period.

During the

HP contractor strike,

an

unexpected

increase

in the frequency of PCEs

was noted

and determined

to result from decreased

availability of clean laundry for workers.

Additional long-term improvements

including laundry monitoring

equipment

and procedure

upgrades

were being

implemented

to prevent

recurrence.

Solid radioactive

waste storage

and processing

were identified as

program areas

with deficiencies.

A violation was issued for failure

to maintain appropriate

posting

and labeling of a radioactive waste

storage

area.

In addition, problems with completing spent resin

transfer during waste processing

were noted during the review period.

A preliminary licensee

evaluation of the event indicated deficiencies

and concerns

in operations,

ALARA, and administrative

areas.

The

'reliminary evaluation

appeared

thorough

and proposed corrective

actions

adequate .to prevent recurrence.

Hanagement

support continued to be strong through continued

implementation of a management

control

system which helps to ensure

an aggressive

chemistry program.

The completeness

of documentation

of chemistry parameters

provided

a highly visible means of tracking

plant chemistry

and highlighting anomalies.

A confirmatory measurements

evaluation

was performed with beta

samples

sent to the licensee.

All analyses

(4) were in agreement.

The liquid and

gaseous

effluents

programs

were effective.

Only one

unplanned liquid release

was

made during the period.

Less

than

one

microcurie was released,

and

no dose 1'imits were exceeded.

The

licensee

took effective corrective action to prevent recurrence.

Radwaste

processing

had

been

a joint effort shared

between

Operations,

Health Physics,

and Chemistry groups, with Operations

administering

the vendor contracts.

With the appointment of a

Radwaste

Coordinator within the Chemistry Department,

reporting

directly to the Chemistry Supervisor,

Chemistry

assumed

administration of vendor contracts

in the Radwaste

area

and

respons>bility for overall coordination of the program.

The licensee

expects this organization

change to improve control

by focusing

program responsibility on one individual.

Two violations were cited in the Radiological Controls area

during

-this period.

2. Performance

Ratin

Category:

2

Trend:

Improving

3. Recomendations

The Board noted that there

has

been

a significant improvement in

radiological controls during the

SALP period.

The Board, a1so

recognized

that the licensee's

performance, at the end of the

SALP

period" was excellent.

After careful deliberation,

the Board

concluded that the appropriate

characterization

of performance

throughout the

SALP period was Category

2 Improving.

C. Maintenance/Surveillance

l. ~Anal sis

Routine

and special

inspections

during this assessment

period were

conducted

to evaluate

equipment condition and maintenance

activities

and to provide an overview of the maintenance

program.

The

NRC performed

a followup inspection to determine

the

effectiveness

of the licensee's

corrective actions for the findings

of the

NRC Maintenance

Team Inspection

(MTI) conducted

in the prior

SALP period.

The licensee. developed

and implemented corrective

actions to address all of the weaknesses

identified by the MTI.

.

Significant improvements

were observed

in all areas.

Management

involvement in implementing the improvements

was evident through

well-stated policies for control of corrective actions,

consistent

evidence of prior planning

and assignment

of priorities, and decision

making at

a level which ensured

adequate

management

review.

Personnel

are accountable

to plant management

for implementing

improvements

and their performance

was actively monitored.

Corporate

management

allocated significant resources

to the improvements

and

supported

plant management

in all their activities.

Improvements

noted included:

increased

and more effective guality Control staff;

10

hiring of permanent staff employees

to replace contract personnel

in

important maintenance

support functions;

development of engineering

support functions, especially

system

and reliability engineering;

ongoing equipment

upgrade

program,

which has

improved plant

and

equipment condition;

and

changes

to planning

and scheduling

activities, which have

reduced

maintenance

delays.

The tracking and scheduling of the surveillances

has

been effective;

no survei llances

exceeded

'the

TS grace period.

During the previous

SALP period weaknesses

were identified in the inservice testing

(IST)

program regarding root cause analysis

and corrective actions

pertaining to testing motor-operated

valves

(MOVs).

The licensee

has

resolved

these

problems.

Root cause

analysis

and corrective action

evaluations of MOV IST failures were timely and 'technically adequate.

Strengths

were identified in the area of leak rate testing pertaining

to trending of valve leakage data,

and testing of additional'pressure

isolation valves not required

by the Technical Specifications

(TS).

The licensee's

IST surveillance

procedures

were technically adequate

and in conformance with TS requirements.

Two instances

were

identified where insufficient briefing of personnel

for low power

physics testing resulted

in portions of tests

not being performed to

expectations.

Inservice test personnel

were knowledgeable of the

surveillances

they were following and routinely followed procedures.

During test performance, it was noted that test personnel

did not

always identify and correct the equipment

nomenclature

errors in test

procedures.

Overall, the licensee

conducted

surveillances

in a safe,

conservative

manner.

Licensee

management

has

made

improvements

in the areas of Maintenance

Department

personnel

staffing, turnover rates,

and overtime reduction

throughout this assessment

period.

Currently the staffing levels for

the four maintenance

disciplines

are consistent

with the licensee's

authorized levels.

Turnover rates

have steadily

improved since the

last SALP.

In addition, during this period,

no

ISC personnel

have

transferred

to the Operations

Department,

which in the past accounted

for the majority of the turnover rate of the

ISC specialists.

Maintenance

Department

management

has

remained stable

throughout this

period.

Over most of the

SALP period, overtime rates

have remained

above the licensee's

goal of 27 percent or less.

However, at the

end

of the

SALP cycle, the overtime rate

had

been

reduced to almost half

of the level experienced

in the first half of this cycle.

The

decrease

was

due to new controls implemented'by

the licensee at the

beginning of 1989, including pre-approval

of overtime by supervisors

and tracking of overtime.

The material condition of the plant has continued to improve during

this period.

In October l989, the licensee

implemented

a material

condition upgrade

plan requiring plant walkdowns

by a management

team.

The team then generates

a list of deficiencies

which are

corrected or tracked to be corrected

when plant conditions allow.

Some noted areas of improvement are:

upgrading of the auxiliary

building, including hallways, Unit 4

RHR pump room,

and Unit 3

charging

pump room; painting and lagging in the turbine plant area;

11

reduction in the total amount of contaminated

floor space;

overhaul

and repacking of a'significant

number of valves; reduction in the

number of control

room green tags;

and

a complete overhaul

and

material

upgrade of the cranking diesels

and switchgear.

The

licensee's

efforts in the material condition upgrade

have resulted

in

improved plant reliability and.availability.

This is evidenced

by

the facility being

on target at

52 days for their "unplanned

days off

line" for 1990.

Late in the last

SALP cycle the licensee

began tracking rework

PWOs

and established

a goal to have less

than

30 rework

PWOs per month by

the end of 1990.

Ouring the first quarter of 1990,

a downward trend

was noted indicating that the goal

was achievable.

However,

an

increase

in rework

PWOs occurred

near the end of the Unit 3 refueling

outage

as

systems

and components

were returned to service.

In an

effort to reduce

rework, the licensee

established

a rework

maintenance

engineer position within each

maintenance

department

discipline.

Their responsibility is to analyze

the cause for repeat

equipment

problems.

The licensee

has

made progress

in the

identification of recurring equipment failures

and provided adequate

corrective action.

For example,

the charging

pump oil pressure trip

switches

caused

numerous

spurious trips due to switch location

and

range.

These

were subsequently

replaced with a

new switch having

a

more appropriate

range

and relocated

to a low vibration area.

Since

these corrective actions

were taken there

have

been

no further

spurious trips due to this switch.

However, continuing rework

problems exist due to poor design,

poor workmanship/maintenance

practices,

and poor vendor supplied

components

and services.

The

charging

pumps

and the Ingersoll-Rand

spent fuel pool cooling

pumps

have

had failures

due to poor design.

Poor workmanship

has

resulted in failures of the feedwater heater

68 outlet valve,

deaerators

for the water storage

tanks,

and pressurizer

spray valves.

Finally, failures

due to poor vendor/contractor

supplied

components/services

include: reactor vessel

head 0-ring;

generator

hydrogen cooler gaskets;

turbine control wire; residual

heat

removal

pump mechanical

seals;

and atmospheric

steam

dump

valves.

Efforts continue to be directed in Plant Work Order

(PWO) backlog

reduction.

These resulted

in a positive reduction in the backlog

during the first part of the

SALP cycle.

However,

an upward trend

resulted

in about the

same total

as noted in the prior SALP period.

The increase

was

due largely to the

PWOs generated

for the licensee's

systematic material condition upgrade

program,

which was established

in October

1989,

and activities associated

with the Unit 3 refueling

outage.

The licensee

has established

a goal to reduce the backlog to

less

than

700

PWOs.

The licensee

has established

guidelines for

maintaining the percentage

of corrective maintenance

PWOs greater

than

90 days old at less

than

50%.

This target level has

been met

since the beginning of April 1990.

Although the current trend of

PWOs

may a'ppear high, it is

an

improvement

over the backlog noted in

prior SALP reports

and indicates

appropriate

management

involvement

in controlling and reducing

PWO backlog.

12

The licensee's

preventive maintenance

(PN) program continued to

improve throughout this cycle.

Although the

number of corrective

maintenance

(CN) work items

has

increased

due to the Unit 3 outage

and the plant's material

upgrade, program,

the

PN/PN+CN ratio has

shown

an improvinq trend throughout this

SALP period.

The ratio is

currently running at

59%, which is near the current goal of 60%.

The

total number of past

due

PMs which exceeded

their grace period

has

also decreased

during this period,

from 32 to less

than 20.

The

achievement

of this lower number is attributed to the licensee's

policy implemented in the last

SALP period to require management

approval for a

PM to exceed its grace period by 25K.

The licensee's

Analytical Based Predictive Maintenance

(ABPN) program

was

expanded

during this period with additional

personnel

being added

to the thermography

group,

increased capability to perform on-site

ferrography for the oil analysis

program,

and the addition of a new

Reliability Centered

Maintenance

(RCN) group consisting of four

maintenance

analyzers

and

a lead engineer.

The

RCN section selects

components for analysis

based

on impact on plant availability and

reliability. After the analysis is complete,

a package

is issued

recommending

program or equipment

changes

to improve reliability.

The group has

issued

packages

on the pressurizer

spray valves

and

condenser

tub'e cleaning

system

and is currently working on analysis

for the reactor coolant

pumps,

pressurizer

heaters/controls,

and the

control rod drive system.

The

ABPN group has continued to enhance

plant maintenance

throughout this period.

A few examples

include

identification of: air in-leakage

on the Unit 4 condenser;

the

location of coils with above-average

temperatures

in the reacto~

protection relays;

a defective

feed

pump rotor; excessive

vibration

in the

4B reactor coolant

pump;

and high vibration in 3C charging

pump f1ui d drive.

The increased

licensee attention to reduce

the large

number of

control

room deficiency tags

noted in the last

SALP cy'cle resulted in

continued to improvement throughout this assessment

period,

The

total number of deficiency tags

was reduced

by approximately half of

the level at the beginning of the

SALP period.

This is

a significant

reduction

compared to totals

noted in previous years.

The Plan-of-the-Day

(POD) continues

to be

a licensee

strength.

The

Operations

Department

has the necessary

control to assign priorities

for maintenance activities

and ensure that operational

concerns

are

addressed.

The

POD clearly identifies

and prioritizes work to be

accomplished,

support groups required,

clearances

required,

and

applicable Radiation

Work Permits.

During the last

SALP cycle, the

Planning

and Scheduling

Group

began tracking the effectiveness

of the

POD to identify all jobs not worked as scheduled,

along with the

reason for,the delay.

The licensee

has

a current target of 70

percent effectiveness

with a goal of 90 percent

by the end of 1991.

During this

SALP period the total effectiveness

has

averaged

around

80 percent.

13

2.

3.

Two violations were cited in the Maintenance/Surveillance

area

during

this period.

a

~fR

Category:

2

Trend:

Improving

Recomendations

None

D.

Emer enc

Pre aredness

l. ~Anal sis

This functional

area

includes evaluation of activities related to the

implementation of the Emergency

Plan

and procedures,

support

and

training of onsite

and offsite emergency

response

organizations,

and

licensee

performance

during emergency

exercises

and actual

events.

Performance

is also evaluated

in the areas

of and interactions

between onsite

and offsite emergency

response

organizations

during

exercises

and actual

events.

During the

SALP period one routine

inspection

and

one exercise evaluation

were performed.

Two Emergency

Plan changes

were reviewed.

During this period, the licensee

provided

good management

support to

the emergency

preparedness

(EP) program and maintained

adequate

staffing levels for responding to an emergency.

Support to the

EP

program

was evident from both corporate

and site management.

For

example, following the departure

of the site emergency

planning

coordinator,

corporate

management

provided

a corporate

emergency

planner to the site full time until the vacant position could be

filled.

Additionally, an emergency

planning consultant

was provided

to the site for calendar year

1990.

Site support to the program also

involved upgrading the emergency

response

coordinator to a

supervisory level reporting directly to the Operations

Superintendent.

Adequate staffing levels for responding

to an emergency

were also

demonstrated

during the November 30,

1989,

emergency exercise.

Emergency

preparedness

coordination

and support for coordination

was

good,

as reflected

by the detailed exercise

scenario

and effective

control observed

during the annual exercise.

The emergency

preparedness

training was effective,

as demonstrated

during exercise

observations

and inspection walk-throughs, with two noted exceptions.

The first training exception

was that the Emergency Coordinator

(EC)

did not know that the responsibility for emergency classification

remained with the

EC and did not transfer to the

EOF upon its

activation.

During the exercise,

the

EC recomended

rather than

declared

a General

Emergency

(GE) classification to the Recovery

Manager in the

EOF.

Despite this procedural error,

a

GE

classification

and the accompanying. required actions

were

accomplished

in a timely manner.

This exercise

weakness

was

14

corrected

during the period and verified during an inspection

walk-through.

The other exception

was the limited effectiveness

of

the Technical

Support Group

(TSG) in support of the Technical

Support

Center staff during the exercise.

This was

due to a lack of timely

and complete information flow to the

TSG.

The remainder of emergency

comunications within and

among the licensee's

emergency

response

facilities were effective during the exercise.

There were three

emergency declarations,

all Notifications of Unusual

Events

(NOUEs) during the rating period, although

one

on August 23,

1989 was later determined to have

been in error and was withdrawn.

On Oecember

18,

1989,

the licensee

declared

a

NOUE for having failed

on Oecember

1, 1989,

(17 days earlier) to establish fire protection

compensatory

measures

within the one-hour time limit specified

by

Technical Specifications.

The significance of this belated

declaration

was mitigated

by the fact that the applicable

emergency

action level

(EAL) for event classification

was conservative

compared

with NUREG-0654 guidance,

has since

been revised

such that the

occurrence

on December

1,

1989, would not now meet the

EAL for a

HOVE.

On. April 11,

1990,

a hydrogen explosion

and fire in the Unit 2

(fossil plant) turbine generator

was promptly classified

and required

offsite notifications were made.

Management

support to the emergency

preparedness

program was apparent

in the guality Assurance

program

and implementation of corrective

actions.

Both the corporate

and site audits reflected substantive

findings with complete

and timely corrective actions.

The licensee's

self-critique of their emergency

exercise

was detailed

and consistent

with regulatory requirements.

The licensee

continues to maintain adequate facilities and equipment

to respond to an emergency,

including the Technical

Support Center,

the Emergency Operations Facility and communications

equipment.

The

relocated

Operation Support Center

(OSC) provides

adequate

communication capabilities

and its larger size

was

an improvement

over the previous

OSC facility, as

noted in the annual

exercise.

The licensee

submitted

two revisions to the Turkey Point Plant

Emergency

Plan during this assessment

period.

The substantive

change

was

an extensive rewrite of the EALs.

The changes

were consistent

with existing guidance

and regulatory requirements

in most cases.

In

those

few instances

where the changes

appeared

to degrade

the plan,

the licensee

revised

them so

as not to decrease

the effectiveness

of

the plan.

One exercise

weakness

was identified during the period.

Category:

2

3. Recommendations

Hone

15

E. Securit

and Safe uards

l. ~Anal sis

This functional area

addresses

those se"urity activities related to

protection of plant vital systems

and equipment,

as viewed during

inspections

and observations

during the assessment

period.

Inspection of the security 'program during this assessment

period

confirmed continuing improvement in program effectiveness

and

performance.

The licensee

has

focused considerable attention,

including personnel

and funds, to assure

adequate

and timely

accomplishment of the programed

upgrade.

"State of the art"

equipment

has

been procured,

and improved facilities have

been

designed to house security systems

and components.

Included are

new

protected

and vi.tal area barriers,

intrusion detection

and access

control systems,

high mast security lighting, dual security

computers,

a dedicated

security diesel

generator

and

an Entry Control

Building with an associated

vehicle entrapment

area.

The

new

security hardware

exceeds

basic regulatory requirements.

Installation of the facilities and system

components

is in progress

and is generally

on schedule.

Construction of the Entry Control

Building and installation of high mast lighting has

been

completed.

Cable duct banks

and associated

electrical

terminal facilities are

largely complete.

Barrier foundations

and equipment supporting

structures

are under construction.

,These activities are scheduled

to

be completed

by late

December

1991.

During this assessment

period,

NRC review activities were concluded for the majority of the

site-initiated

changes

to the Turkey Point physical security program.

Two site visits were conducted

by NRC staff, in February

and June,

to

finalize long-standing

issues

related to vital equipment

identification and vital barriers.

The resolution of these

issues

and the anticipated final implementation will significantly improve

the total security program at Turkey Point.

Initiatives to improve personnel

management

and resource utilization

noted in the 'previous

SALP report are continuing

and

a marked

improvement

has

been noted.

Performance

improvement is evidenced

by

the decline in the

number of violations cited from a total of ten in

the previous

SALP period to one in the current assessment

period.

The one violation cited was for a failure to control safeguards

material

by the security force.

In addition, there

was

an event that

involved the failure to maintain control of a visitor by a

contractor.

The improvements

in adherence

to regulatory requirements

and security plan commitments is attributed to senior management

attention,

recruitment of qualified and experienced

security managers

and supervisors

and resulting

enhancement

of morale,

and performance

orientation of security shift personnel.

The current limiting factor

in the overall effectiveness

of the security program is the extensive

use of compensatory

measures

which are necessitated

by deficiencies

and operational

limit'ations of the old security systems

and

facilities now in use,

and the extensive

upgrade efforts ongoing.

nr

16

Considerable

improvement

has

been

made in the security training

ogram

as evidenced

by security shift personnel

performance

and the

reduction in the number of violations.

Improvement is attribute

i

d 'n

part to the assignment

of a proprietary training supervisor

and

increased

emphasis

and involvement by the security contractor

corporate

management.

The extent of improvement in training

effectiveness

was demonstrated

by the performance of personnel

during

response drill scenarios

and the various evaluation

and critique

methods

employed

by security managers

and supervisor s.

The submission of security plan revisions

and temporary

changes

to

accommodate

frequent

changes

resulting from the security program

upgrade activities

have

been timely with few provisions requiring

further discussion,

validation, or change.

The licensee

has established

an improved comounications capability,

both within the security organization

and in communicating reportable

events,

security concerns

and issues,

and other significant items of

interest to the

NRC.

The on-site comunications capability was

enhanced

by the use of a highly reliable radio-telephone

system.

The

capability of the system frequently provided for the receipt of

notification of an event

by Region II directly from the event scene

prior to notification through

normal reporting channels..

guality Assurance

audits of the security program

have

been helpful in

identifying deficiencies

and providing recommendations

for

improvements.

The licensee

has

a well-established

"Fitness

For Duty" program that

is managed

by the corporate security function.

An on-site manager is

responsible for all on-site

and related activities.

Although the

program was not formally inspected

during this assessment

period,

review indicated that the program

was providing adequate

results with

a minimum of problems.

One violation was cited in the Security and Safeguards

area during

this period.

I. ~II

Category:

2

Trend:

Improving

3. Recomendations:

None

F.

En ineerin /Technical

Su

ort

l. ~Anal

s is

The engineering'and

technical

support area

includes all activities

associated

with the design of plant modifications, engineering

and

technical

support for operations,

outages,

maintenance,

testing

and

17

4

survei

1 lance,

procurement,

and licensed

operator training.

These

activities were viewed during routine

and special

inspections

throughout

the assessment

period.

Overall, engineering

and technical

support

has

been effective during

'his

assessment

period with improvements

evident in the System

Engineering

and Licensed Operator Requalification Training

programs.'eficiencies

were identified related to comprehensiveness

of generic

application evaluations',

incorporation of design information into

plant procedures,

and technical

overview of contracted

engineering

services.

Engineering

has

demonstrated

effective technical

support during. this

evaluation period.

Engineering evaluations

to support Appendix

R

technical

issues

'were excellent.

Technical

information was well

maintained

and complete.

Engineering

implementation of R.G. 1.97,

Instrumentation to Assess

Plant

and Environs Conditions During and

Following an Accident, was timely, technically sound,

and thorough.

The root cause

analysis for Telemand

Relay failures

was

comprehensive.

The Operating

Experience

Feedback

(OEF) program

identified

a potential plant operability problem related to

recirculation

sump screens.

Further effective engineering activity

was demonstrated

by the Emergency

Power System

upgrade initiatives

progressing

on schedule

through this evaluation period.

Engineering

, interface with the

NRC on this activity was characterized

by sound

analyses

and timely response

to requests

for further information.

Engineering

involvement in these

issues

demonstrated

an improvement

in comnunications

between corporate

engineer ing and the plant.

Performance

has

been generally adequate

within engineering

program

activities.

Design change control

and implementation

has

been

adequate

overall

and demonstrated

improvements

in some areas.

Design

change

packages

generated

in the previous year have

improved with

respect to screening

and detailed requirements for post- modification

test'equirements.

Engineering

involvement in the Request for

Engineering Assistance

(REA) and Nonconformance

Reporting

(NCR)

programs

has

been effective.

The licensee

has contributed considerable

resources

to the

reconstitution

and verification of Design

Base

Documents

(DBD).

The

NRC Design Validation Inspection

(DVI) conducted

during this

assessment

period reviewed engineering

resource

improvements

resulting from this activity.

The system level

DBDs were well

assembled,

however the associated

Component

Design Requirements

(CDRs) contained

errors which could have infiltrated into the design

process

since the

CORs were approved for use.

The

CDRs were

developed

by a contractor

and

had not been verified by FPAL.

The

scope of the

DBD verification program was too limited in that it did

not address all of the Reactor Protection

System

(RPS) functional

characteristics

and the external

hazards

design

bases.

A positive

aspect of the

DBD activity was the establishment

of a Systematic

Design Investigation

(SDI) program to evaluate

the issues

that arose

during the reconstitution effort.

The SDI program was found

18

extremely beneficial, particularly with respect to its expansion

to

include technical

issues

beyond select

systems

concerns.

Although the

DVI determined that engineering

and technical

support

performance

on issues

and program activities was generally effective,

there were examples of less effective engineering

performance.

A

change

to Component

Cooling Water,(CCW) flow rates

was

made without

verifying adequate

flow rates for all accident conditions.

There

were several

examples of design information not being incorporated

into plant procedures;

e.g.

minimum

CCW flow for Emergency

Containment

Coolers

(ECC),

PORV opening time limits, and

ICW to TPCW

isolation valve test requirements.

Inadequate

technical

overview of contracted

engineering

services

contributed to deficiencies

in design calculations identified by the

NRC DVI inspection.

Calculations

associated

with the

CCW

modifications contained errors resulting in the erroneous

evaluation

of heat exchanger

and nozzle loads.

Additionally, pipe and support

calculations

did not account for required load

and stress

aspects.

In a letter dated January

12,

1990, the licensee

provided plans

and

schedules

for corrective actions in response

to the DVI.

The last

corrective action to be implemented,

modification of Unit 4

CCW surge

tank anchorages,

is scheduled

to be completed

by the end of the dual

unit outage in 1991.

There were examples of inadequate

or incomplete generic application

reviews for specific plant issues.

Although the

OEF program

was

proactive in the identification of the recirculation

sump screen

issue,

the engineering applicability review for the operating unit

was not considered until prompted

by the

NRC.

Following

identification of Westinghouse

OT-2 switch deficiencies

on the Safety

Injection System,

the generic applicability review was delayed until

generic implications were raised

by other utilities.

Subsequent

review identified additional plant applications.

Engineering

evaluatio'n of the Fire Protection

Suppression

System operability due

to excessive

system

leakage

did not assess

the impact of excessive

leakage

preventing repairs to the system.

The performance

deficiencies

addressed

in the previous

paragraphs

do not indicate

major programmatic failures;

however they do indicate areas of

engineering

performance requiring increased

attention.

A comprehensive

Drawing Update

Program initiated 'in the previous

assessment

period was effective in reducing the backlog of drawing

changes,

however additional

drawing deficiencies

were identified in

this assessment

period.

The backlog

was reduced

from 28,000

outstanding

changes

in early 1989 to approximately 15,000.

Present

deficiencies

include existing drawings which are sometimes difficult

to read.

Several

NRC inspections

identified inaccurate

drawings

as

a

weakness

including: as-built conditions did not match drawings for

cable routing and piping supports,

Residual

Heat Removal

System

drawings did not accurately reflect Reactor Coolant System interface,

19

and there were

no drawings for the'containment

recirculation

sump

screens.

During the previous

SALP period, weaknesses

were identified in the

procurement of parts

needed for equipment maintenance.

Improvements

were

made during this period,

such as:

parts

issues

being included

in daily

POD meetings,

assignment

of additional

maintenance

and parts

personnel

to identify and expedite parts

needed for the refueling

outage,

supplementing

the engineering staff to reduce

procurement

backlog,

and

use of blanket purchase

orders for routinely used parts.

In addition, the responsibility for materials

management for the

nuclear units

was separated

from the fossil units

and included in the

new nuclear division.

As

a result,

the average

parts reorder time

was

reduced substantially,

from 111.5 days to 76.4 days,

and

engineering

procurement

backlog

was reduced

sharply,

from 740 items

to the current goal of around

200 items.

However, opportunity for

improvement in parts

procurement

remains,

as indicated

by the

increase

in the

number of corrective maintenance

PWOs awaiting parts

from 115 at the start of the

SALP period to 170 at the end of the

period.

r

Technical

support for the Unit 3 outage

was effective.

Outage

management

was upgraded to provide full shift coverage at

a

management

level capable of redirecting resources

to support outage

activities.

Consultants

were contracted

to assist in pre-outage

planning.

Prior to the Unit 3 outage,

Unit 4 entered

an outage to

correct conditions which could result in Unit 4 shutdown during the

Unit 3 refueling outage.

Preparation for the upcoming'ual unit

outage included contracting

personnel

experienced

in nuclear

outage

activities to overview the outage

program.

Additional outage support

actions

were the establishment

of a Plant Nuclear Safety Subcomaittee

to focus

on outage activities,

and

a configuration control

team to

coordinate modification activities.

System Engineering

program

improvements

have contributed to increased

effectiveness

of the system engineering

organization.

Program

improvements initiated included:

formal documentation of

responsibility,

increased

system walkdowns, increase

in staff size,

and

a training program with increased

emphasis

on system design

training.

Examples of improved system engineering

effectiveness

were

demonstrated

by problems identified by system engineers,

including:

CCW system design flow discrepancies,

CCW system misalignment,

and

misposition of a Safety Injection System valve.

NRC inspections

identified an increased

contribution of system engineering to plant

technical

support in the areas of maintenance

and operations.

System

engineers

have contributed to a reduction in LCO hours

by

improvements

in the

CCW system chemical injection system

and

increased availability of the Emergency Diesel Generators.

The licensee

has

taken actions which have resulted in improvements in

the requalification training program.

Improvements

include increased

management

involvement in the requalification training program

and

increased

simulator time for requalification trainees.

Management

20

routinely observes

simulator examinations

and critiques.

Periodic

feedback

sessions

between

management,

operations,

and training

personnel

address

requalification training issues.

Average simulator

time for requalification individuals increased

to greater

than

90

hours versus

an average

of 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> in the last

SALP period.

The

licensee

plans to reduce contract training staff by replacement

with

permanent

FPL staff from the licensed

operator class presently in

training.

The effectiveness

of training program

improvements

was demonstrated

by the

1990 requalification examination results.

Four of four ROs

and

10 of 12

SROs

passed

requalification examinations.

The

NRC rated

the licensee requalification program

as satisfactory

based

on this

87.5 percent

pass rate.

This program

had

been rated

as

unsatisfactory

since March,

1986.

Other examples of,effective

licensed

operator training activity include

a

100 per cent

pass rate

for 9 SRO upgrade

examination candidates

and

31

NRC Generic

Fundamentals

Examination candidates.

One violation was cited in the Engineering/Technical

Support

area

during this period.

2. Performance

Ratin

Category:

2

3. Recormendations

None

G. Safet

Assessment/ ualit

Verification

l. ~Anal sis

The assessment

of this functional

area is based

on

a review of

licensee

implementation of safety policies; activities related to

license

amendments,

exemptions,

and relief requests;

responses

to

Generic Letters, Bulletins,

and Information Notices; resolution of

safety issues

(10 CFR 50.59 reviews); safety review committee

activities;

and use of feedback

from self-assessment

programs

and

activities.

These activities were viewed during routine

and special

inspections

and comunications

throughout the assessment

period.

The licensee

was responsive

in supporting the numerous

NRC team

inspections

(See section V.B).

In all the areas

inspected,

the

licensee's

performance

was found to exceed regulatory requirements.

Special

mention was

made of the licensee's

successful

preparation

efforts, which included self-assessments

conducted

by QA and use of

outside contractor specialists

where appropriate.

The licensee

also

supported

several

large management

meetings

w'ith the

NRC at the site

to discuss

progress

in a wide range of issues.

In addition, the

licensee

briefed

NRC personnel

on the planning

and scheduling

progress for the dual unit outage

scheduled

to start late in 1990.

21

These meetings

required significant resources

by the licensee

and the

presentations

were substantive,

well prepared,

and helpful.

The licensee

has

taken corrective actions in response

to the

Independent

Management Appraisal

(IMA), which was performed to comply

with NRC Order'EA-87-85,

dated

October

19,

1987.

Positive personnel,

program,

and attitude

changes

have occurred

since the

IMA results

were issued.

The changes

included defining the educational,

experience,

and performance

requirements for 35 identified positions

noted in the

IHA report; approving written job descriptions;

and

filling those positions with qualified personnel.

Also, the licensee

has

suspended

their

management

development rotation program.

This

decision

was

made to maintain

a stable organization,

to develop

teamwork

and accountabil,ity,

and to ensure that managers

take

a

long-term view of the performance of their organizations.

Management

has

become

more directly involved in plant operations,

by:

monthly

evaluation of performance

indicators against site goals,

communicating established

goals to plant personnel

through monthly

meetings,

and increasing

management

presence

in the field.

This

management

involvement has

been

augmented

by operators

and system

engineers

being directed to identify deficient plant conditions,

and

the establishment

of a planning

and scheduling

group within the

Operations

Department.

The results of these efforts have

been

an

increased

awareness

in personal

accountability,

a downward trend in

the

PMO backlog,

and

an improved material condition of the plant.

.In

- addition,

new controls

on the commitment tracking process

have

reduced

the

number of overdue

comnitments

and

have

improved

comnunications

between

the licensee

and the

NRC.

The licensee

recently upgraded their employee

concern

program.

It is

now called the Speakout

Program

and

became effective on April 2,

1990.

The Speakout

manager is located in the Juno

Beach office and

reports directly to the Vice President

for Nuclear Assurance.

The

Turkey Point Speakout

supervisor

answers directly to the corporate

manager.

A special

team inspection of the Speakout

Program found

that the program was effective in identifying and resolving employee

concerns

and

had strong management

support.

The Speakout

Program is

a significant improvement over the previous

employee

concern

program.

The licensee

has self-identified

14 violations of NRC requirements

during this

SALP period.

In each case,

prompt and thorough

corrective actions

were taken

and,

as

a result,

these violations were

not cited by the

NRC.

In addition, self-assessment

activities were

carried out to review implementation of commitments to the

NRC

resulting from the Independent

Management Appraisal,

NRC maintenance

and fire protection

team inspections,'he

earlier Management-on-Shift

(MOS) program,

and several

other 'activities.

The Regulatory

Compliance section

has performed or participated in audits in

radiation protection, chemistry,

emergency

operating

procedures,

emergency

preparedness,

and fire protection/Appendix

R.

These audits

resulted

in positive

NRC inspection findings.

Vertical slice audits

have.-been

performed in the In-Service Inspection

and Hotor Operated

Valve programs.

The Performance

Monitoring section

has initiated

22

concerns

in several

areas

where subsequent

NRC inspections identified

similar concerns;

i.e.,

a concern regarding

the readiness

of a

hydrogen

recombiner

system

was identified prior to an

NRC inspection

of the

same area,

questioning

the adequacy of the flood protection

program

was initiated by gA, and the adequacy, of clearance

orders

and

work contr'ols

had also

been identified as

a concern

by the licensee.

The quality of LERs and special

reports

was generally good.

The

reports

were well written and provided adequate

information to

describe

the major aspects

of the events,

and they generally included

thorough analysis

and identification of the root causes

of the

events.

Three exceptions

were noted.

LER 250/90-011,

concerning

a

reactor trip on

a steam generator

high-high water level

due to

failure of a feedwater valve controller hand/auto station, did not

address

the potential effect of the post-trip cooldown at core end of

life when the shutdown margin would be most limiting.

LER 250/89-018,

regarding

a potential single failure design deficiency

discussed

in the Engineering/Technical

Support area, is another

example of an inadequate

analysis.

Also,

a special

report dated

June

19, )990, regarding Unit 3 standby feedwater

pump unavailability, did

not adequately

address

safety significance,

root cause,

corrective

actions,

or previous occurrences.

A high percentage

(65%) of the

34

LERs was attributed to personnel

errors

(see section V.G.).

Operational

personnel

errors

are discussed

further in the Operations

area.

During this evaluation

period there were two major licensing review

activities,

and

a number of generic

issues

and

NRC Bulletins were

resolved

and closed.

No emergency

Technical Specifications

(TS) were

requested.

Throughout the period, the licensee

showed significant

improvement in the timeliness of submittals

and responses

to

NRC

initiatives.

One major licensing review activity which has

been

ongoing is the conversion to Standard

Technical Specifications.

The

licensee

provided the necessary

resources

and timely,'igh quality

responses

to questions

to permit the

NRC staff to complete its

No

Significant Hazards

Evaluation

and its Safety Evaluation.

Another

major licensing review activity has

been

the Emergency

Power System

(EPS)

enhancement

effort.

At significant cost,

FPL is making

a major

safety improvement at the plant by upgrading

the emergency

power

system,

including the addition of two emergency diesel

generators,

an

extra station battery,

and two battery chargers.

During the

NRC

staff's review of these modifications

and associated

TS, the licensee

provided high quality responses

to questions

in a timely manner.

In the area of coomunications with NRC headquarters

staff, there were

a few minor problems associated

with the organizational shift of

licensing responsibility from corporate

headquarters

to the site.

However, since then improvement

has occurred.

The two violations cited in this area

involved the closure of a

Non-conformance

Report prior to completion of required actions,

and

failure to take corrective action in response

to electrical terminal

block corrosion that had

been previously identified.

23

2. Performance

Ratin

Category:

1

3. Recommendations

None

V.

SUPPORTING

DATA

A. Licensee Activities

Units

3 and

4 began

the assessment

period at power operation.

Unit 3

operated

very well with only two short interruptions until it

was shut

down on February 4,

1990, for a refueling outage.

The unit

restarted

again in early June

and

was at full power at the

end of the

period.

Unit 3 experienced

a relatively high availability of about

62K, considering

the four-month refueling outage.'nit

4 operated

throughout the period, but suffered

a number of brief shutdowns

and

interruptions of operations

due to equipment failures

and operational

problems.

Availability for Unit 4 was about

76%.

At the end of the

assessment

period, Unit 4 had

been shut

down for two weeks to repair

pressurizer

spray valves

and

RCS leaks.

A sumnary of the reactor trips

and unplanned

shutdowns for both units is in paragraph

F of this

section.

The licensee

made

one request for TS relief.

In May, 1990, the 48

Intake Cooling Water

( ICW) Pump experienced

low flow problems.

Aware

that replacing the

ICW pump within the

TS allowable time would be

difficult, the licensee briefed the

NRC on the technical

issues

and

requested

a Temporary Waiver of Compliance in a timely manner.

During this

SALP period,

FPL made significant organizational

changes,

creating

a separate

nuclear division and staffing it with

experienced

people.

8. Direct Inspection

and Review Activities

During the assessment

period,

32 routine, eight special,

and

no reactive

inspections

were performed, at Turkey Point by the

NRC staff.

Additionally, in October,

1989,

a team from NRR visited the

FPL Juno

Beach offices to review the licensee's

station blackout proposal.

The

special

inspections

included:

Fire Protection

and

10 CFR 50 Appendix

R safe

shutdown

requirements

Observation of operators

in simulator

and control

room

Performance

Enhancement

Program

Independent

Management

Assessment

followup

Maintenance

Team Inspection followup

Emergency Operating

Procedures

~ I

~ ~

t

24

Design Validation

Regulatory

Guide 1.97,

Instrumentation for Accident Conditions

C. Escalated

Enforcement Actions

1. Orders

None

2. Civil Penalties

None

D. Licensee

Conferences

Held During Appraisal

Period

August 21,

1989

-

Meeting held at

NRC headquarters

to discuss

the

Technical Specifications

revision project.

September

19,

1989

-

Heeting held at Turkey Point to discuss

management

issues,

engineering,

maintenance,

training,

and security.

November 1,

1989

-

Meeting held at

NRC headquarters

to discuss

calculation method for irradiation damage

function, Regulatory

Guide 1.99,

Rev. 2.

December

6,

1989

-

Meeting held at

NRC headquarters

to discuss

FPL's Probabilistic Risk Assessment.

January

9,

1990

-

Meeting held at Turkey Point to discuss

management

issues,

engineering,

maintenance,

training,

and security.

April 9-11,

1990

-

Meeting held at

NRC headquarters

to discuss

FPL's

Emergency

Power Systems

Enhancement

project.

May 16,

1990

-

Heeting held at Turkey Point 'to discuss

the dual

unit outage

and other programmatic

issues.

July 17,

1990

-

Meeting held at

NRC headquarters

to discuss

licensee's

proposed controls

and approach for

assuring

plant safety during the upcoming dual

unit outage.

July 26,

1990

-

Meeting held at RII office to discuss

the

licensee's

assessment

of their performance.

E. Confirmation of Action Letters

None

F. Reactor Trips and Unplanned

Shutdowns

~

~

t

25

Unit 3 experienced

three

unplanned

manual

shutdowns,

was manually taken

off line once,'and

had

two unplanned reactor trips during this

evaluation period.

Unit 4 experienced

six unplanned

manual

shutdowns,

was manually taken off line twice,

and

had four. unplanned

reactor trips

during this evaluation period.

The unplanned trips, taking the unit

off line, and shutdowns

are listed below.

l. Unit 3

Reactor Trips

June

9, 1990:

The unit tripped from 26K power on steam generator

high level

due to a feedwater

valve controller problem.

June

15,

1990:

The unit tripped from 10K power during shutdown

due

to personnel

error in pulling rods to control reactor coolant

temperature

with the turbine tripped.

Unplanned

Reactor

Shutdowns / Offline

August 7,

1989:

The unit was shut

down due to high steam generator

conducti Iity from condenser

tube leaks.

December

25,

1989:

The unit was taken off line to facilitate

corrective actions for MSIV solenoid

power electrical junction box

terminal strip corrosion

problems.

Hay 27,

1990:

The unit was shut

down to correct problems with new

atmospheric

dump valves failing to actuate

properly.

June

4, 1990:

The unit was shut

down due to continued

problems with

atmospheric

dump valves failing to actuate

properly.

2. Unit 4

Reactor Trips

September

15,

1989:

The unit was manually tripped from 100" power

following a transient

caused

by the left turbine stop valve

inadvertently closing due to an oil leak.

December

23,

1989:

The unit tripped from 94K power when the 4A main

steam isolation valve spuriously closed

due to electrical junction

box terminal strip corrosion.

April 9, 1990:

The. unit tripped from 100K power due to the failure

of an underfrequency

relay in the 48 4KV bus which tripped the

4B and

4C reactor coolant

pumps

on

a false underfrequency

signal.

May 26, 1990:

The unit was inadvertently manually tripped from

approximately ll power due to personnel

error. when the reactor

operator

pushed

the reactor trip pushbuttons

in lieu of continuing

the reactor startup

as

planned.

~

I'J

~ 0

26

Unplanned

Reactor

Shutdowns/Of fline

August 16;

1989:

The unit was shut

down to correct gasket

installation problems with the main generator

hydrogen coolers.

September

6,

1989:

The unit was taken off line to correct main

condenser

tube leaks.

October

19,

1989:

The unit was shut

down to repair leaks in the

turbine control oil system.

January

9, 1990:

The unit was shut

down to correct

a reactor coolant

pump vibration problem.

May 18,

1990:

The unit was taken off line to correct

problems with

t'urbine control oil leaks.

May 20,

1990:

The unit was shut

down to facilitate cleanup of

turbine oil which became

contaminated

following an auxiliary oil pump

failure.

N

July 17,

1990:

The unit was shut

down to correct pressurizer

spray

valve leakage

problems.

G. Review of Licensee

Event Reports

During the assessment

period,

a total of 34

LERs were analyzed.

The

distribution of these

events

by cause,

as determined

by the

NRC staff,

is as follows:

Cause

Component Failure

Design

Construction,

Fabrication,

or Installation

Unit 3 or Conmon

Unit 4.

Personnel

Error

- Operating Activity

- Maintenance Activity

- Test/Calibration Activity

- Other

8'

2

0

Other

ota

Note 1:

With regard to the area of "Personnel

Error," the

NRC

considers

lack of procedures,

inadequate

procedures,

and erroneous

procedures

to be classified

as personnel

error.

27

Note 2:

The "Other" category is comprised of LERs where there

was

a

spurious

signal or

a totally unknown cause.

H. Licensing Activities

During the assessment

period the staff completed

seven licensing

actions.

Also, .a total of 36 multiplant actions for the

two units were closed.

I. Enforcement Activity

Functional

Area

No. of

eviat>ons

and Vio ations in

Each Severity Level

Dev.

V

IV

III II

I

Unit 3/Unit4

Plant

perat>ons

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

6

2/0

2/2

0/0

1/1

1/1

2/2