ML17347B258
| ML17347B258 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 07/28/1989 |
| From: | Butcher R, Crlenjak R, Mcelhinney T, Schnebli G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17347B256 | List: |
| References | |
| 50-250-89-27, 50-251-89-27, NUDOCS 8908180037 | |
| Download: ML17347B258 (36) | |
See also: IR 05000250/1989027
Text
~p,S RECy
(4
Pp
Cy
0O
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTAST., N.W.
ATLANTAIGEORGIA 30323
Report Nos.:
50-250/89-27
and 50-251/89-27
Licensee:
Power
and Light Company
9250 West Flagler Street
Miami,
FL
33102
Docket Nos.:
50-250
and 50-251
Facility Name:
Turkey Point
3 and
4
License Nos.:
and
Inspection
Conducte
ay
- June
30,
1989
Inspec
~c.P
R.
C.
che
,
nio
Resident
Inspector
T.
F.
Mc
n
y,
eside
Inspector
G. A.
S
bli, Reside
Inspector
Approved by:
R.
.
C
enjak,
S
ion Chi
Division of Reactor Projects
7- Zc-
-89'ate
Signed
7'- zc A
Date Signed
7- zc
-Zci'ate
Signed
te
gned
SUMMARY
Scope:
This routine resident
inspector
inspection entailed direct inspection at the
site
in the
areas
of monthly surveillance
observations,
monthly maintenance
observations,
engineered
safety features
walkdowns, operational
safety,
plant
events,
Unit
3 startup
from an
outage,
Unit 4 startup
from refueling,
and
installation
and testing of modifications.
Results;
Both Units
3 and
4 were taken critical and put on line during this inspection
period.
Also, Unit 4
was
taken off line,
due to
a
TPCW leak wetting the
generator
and
then
returned
to
power.
All manipulations
were
accomplished
in
a deliberate
and controlled
manner.
Operations
exhibited
a
professional
attitude in controlling the operation of the plant.
Two violations were identified:
PORV opening
time exceeded
the
OMS safety evaluation limit of 2 seconds.
(Paragraph
2)
8908i 80037 890803
ADOCK 05000250
8
PNU
Installation of an erroneous
label
p'1ate
on the Unit 3 safety injection
bl ock switch.
(Para'gr aph 9)
One non-cited violation was identified which involved failure to identify an
outstanding
clearance
affecting auxiliary" feedwater flow to the
C
steam
generator.
(Paragraph
2)
One
Inspector
Followup
Item was identified regarding
minor procedural
and
drawing discrepancies.
(Paragraph
8)
REPORT
DETAILS
Persons
Contacted
Licensee
Employees
J.
W Anderson, guality Assurance
Supervisor
J. Arias, Assistant
to,. Plant Manager
- L. W. Bladow, Plant guality Assurance
Superintendent
- J.
E. Cross,
Plant Manager-Nuclear
- T. A. Dillard, Maintenance
Manager
- R. J. Earl, guality Control Supervisor
T. A. Finn, Training Supervisor
S. T. Hale, Engineering Project Supervisor
- K. N. Harris, Vice President
- D. W. Herrin, Regulatory
Compliance
Engineer
- J. P. Hendrickson,
Reactor
Engineer
- R. J. Gianfrencesco,
Maintenance
Superintendent
V. A. Kaminskas,
Technical
Department Supervisor
J.
A. Labarraque,,
Senior Technical Advisor
- E. Lyons, Acting Regulatory
and Compliance Supervisor
- F. G. Mahler, Services
Manager
R.
G.
Mende, Operations
Supervisor
- L. W. Pearce,
Operations
Superintendent
J.
C. Strong,
Mechanical
Department Supervisor
J.
D. Webb, Operations - Maintenance
Coordinator
- A. J. Zielonka, Site Engineering
Group Supervisor
Other
licensee
employees
contacted
included
construction
craftsman,
engineers,
technicians,
operators,
mechanics,
and electricians.
- Attended exit interview on June
30,
1989
Note:
An Alphabetical Tabulation of acronyms
used in this report is
listed in paragraph
13.
Actions on Previous
Inspection
Findings
(92702)
A review
was
conducted
of the following noncompliances
to assure
that
corrective actions
were adequately
implemented
and resulted
in conformance
with regulatory
requirements.
Verification of corrective
action
was
achieved
through record reviews, observation
and discussions
with licensee
personnel.
Licensee
correspondence
was
evaluated
to ensure
that
the
responses
were timely and that corrective actions
were implemented within
the time periods specified in the reply.
(Closed)
50-250,251/87-44-02,
Review
Revisions
to
AP 0103.2
as
Required
by
NRC and the Licensee's.MOS
Program.
The required
changes
were
made to the subject
procedure
and the requirements
of the
MOS program have
been lifted after
NRC review.
This item is closed.
(Closed)
URI 50-250,251/88-26-01,
Review Licensee's
Evaluation of the
Effect of
PORV Opening
Time on the Operability of the
OMS During Previous
Shutdowns;
The licensee
issued
a safety evaluation,
JPN-PTN-SEMJ-88-076,
revision 1,
on February
17,
1989, which analyzed
the
PORV maximum stroke
times.
This evaluation
concluded that with a tested
stroke time less
than
or equal
to 3.45 seconds,
one
PORV can safely mitigate the most limiting
pressure
A review of the licensee's
IST Program for the
revealed
that the opening stroke times
exceeded
the 3.45
second limit on
numerous
occasions.
Therefore, if the plant experienced
the most limiting
pressure
and
the
PORV opening
times
were greater
than
3.45
seconds,
the
Appendix
G limits would
have
been
exceeded.
Appendix
8, Criterion III, as
implemented
by the
approved
Florida Power and Light Company Topical Quality Assurance
Report
(FPLTQAR)
1-76A,
Revision
11, Topical Quality Requirement
(TQR) 3.0,
Revision 7,
requires that measures
be established
to assure
that applicable regulatory
requirements
and
the
design
basis
are
correctly
translated
into
specifications,
drawings,
procedures,
and instructions.
Contrary to the above,
the 2.0 second
PORV opening
time specified in the
Overpressure
Mitigating System,
Safety Evaluation
Report dated
March 14,
1980,
was
not incorporated
into the licensee's
IST Program.
Instead,
a
non-conservative
acceptance
criteria of 15.0 seconds
was used.
This could
have resulted
in the Unit 3 and
4
PORVs being unable to mitigate the most
limiting design
basis
for
low
temperature
overpressure
protection,
had this transient
occurred.
This condition
existed
on
several
occasions
from
May 1984
through
June
1988.
This
item is
identified
as
Violation 50-250,251/89-27-01.
Therefore,
URI 50-250,
251/88-26-01
is closed.
(Closed)
URI 50-250,251/89-24-04,
Determine
the
Cause
of Inadequate
Clearance
Control during
AFW Testing.
With Unit 3 in Mode
5 and Unit 4 'in Mode 2, the licensee
declared
the Unit
4 Train
1
AFW out-of-service.
The licensee
had determined that instrument
air supply check valves
(4-40-813
and 815) for flow control valves
(FCV)
4-2817
and
4-2818,
respectively,
were
backleaking.
Technical Specification 3.18 specifies
that in Modes 1,
2 or 3, with one of the two
required
independent
AFW trains inoperable,
either restore
the inoperable
train to an operable status'within
72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />,
or place the affected unit(s)
in at least
hot standby within the next six hours
and in hot shutdown
within the following six hours.
Since Unit 4 was in Mode 2, it entered
the
TS 72-hour Action Statement.
The licensee
repaired
the valves
and
commenced
testing later that night.
The test
was
completed;
however,
FCV 4-2818 did not pass
the test.
I&C worked on the valve and
on May 22,
1989, the Unit 4 Train
1
AFW operability test
was performed again.
During
the test,
operators
noted that the
was not receiving
flow.
The operators
secured
from the test.
Investigation of this event revealed
that stop valve (4-20-341) to steam
generator
C
from the
pump
was
closed
under
clearance
order
4-89-05-149,
thus
preventing
the
C steam
generator
from receiving
feed
flow during the
performance
of surveillance
procedure
4-0SP-075.1,'AFW
Train
1 Operability Verification.
Review by the licensee
revealed
that
the Train
1
AFW control valve 4-2818
was listed in the
Equipment
Out of
Service
Log sheet.
Also another
clearance
existed at this time for the
Train
1
AFW flow control valve filters and
instrument air check valves
(clearance
number 4-89-05-154).
When the operators
were verifying proper
AFW system
alignment prior to testing, this clearance
was lifted.
How-
ever,
the operators
did not identify the other
remaining
clearance
on
Train 1'FW.
The test
was
subsequently
performed sucessfully
and
train
1
was
returned
to serv'ice
prior to the expiration of the 72-hour
Action Statement.
3.
The root
cause
was attributed to personnel
error
and is considered
an
isolated event.
The licensee
counseled
the operator regarding
the circum-
stances
of this event.
TS 6.8. 1 requires
that written procedures
and
administrative
policies shall
be established,
implemented
and maintained
that meet or exceed
the requirements
and recommendations
of Section
5. 1 of
ANSI
N18. 7-1972.
ANSI
N18. 7-1972,
Sec tion
5.1. 2,
speci fi es
that
procedures
shall
be followed.
Surveillance
Procedure
4-OSP-075. 1,
Train
1 Operability Verification, dated
March
29,
1989,
Section
3.2,
required
that
the
AFW system
be aligned
in normal
standby
service
per
Operating
Procedure
4-0P-075, Auxiliary Feedwater
System.
Attachment
1
to
Operation
Procedure
4-0P-075,
dated
March 24,
1989,
requires
that
valve
4-20-341
be
locked
open for normal
AFW system
operation.
Contrary to the above,
valve 4-20-341
was found closed during
the
performance
of 4-OSP-075.
1 on
May 22,
1989, which prevented
AFW flow
to the
C steam
generator.
However, this violation is not being cited
because
criteria specified
in Section
V.A of the
NRC Enforcement
Policy
were satisfied.
This
item is identified
as
Non-Cited Violatiop
(NCV)
50-250,251/89-27-02.
Followup on Inspector
Followup Items (92701).
(Closed)
IFI 50-250,251/89-24-05,
Resolution of the Failure. of MOV-4-751.
This item is discussed
in detail in paragraph.6.a.
This item is closed.
4.'nsite
Followup
and In-Office Review of Written Reports
of Nonroutine
Events
and
10 CFR Part 21 reviews
(92700/90712/90713).
The Licensee
Event
Reports
(LERs)
and
10 CFR Part 21 Reports
discussed
below were
reviewed
and closed.
The inspectors
verified that reporting
requirements
had
been
met, root cause
analysis
was performed,
corrective
actions
appeared
appropriate,
and
generic
applicability
had
been
considered.
Additionally, the inspectors
verified that the licensee
had
reviewed
each
event,
corrective actions
were
implemented,
responsibility
for corrective actions
not fully completed
was clearly assigned,
safety
questions
had
been
evaluated
and resolved,
and violations of regulations
or
TS conditions
had
been identified.
When applicable,
the criteria of
10 CFR 2, Appendix C, were applied.
(Closed)
LER 50-250/86-41,
Pumps
Not in Operation
as
Required
by
Techni ca 1
Speci ficati ons.
The
inspectors
revi ewed
the
compl eted
corrective actions
and found them acceptable.
This item is closed.
(Closed)
LER 50-250/87-23,
Safety Injection
and
Reactor Trip due to
a
Failed
High Steam
Flow Instrument.
The corrective actions
taken,
as
a
result of this event,
were reviewed
and found to be adequate.
This item
is closed.
(Ref. Inspection
Report 50-250/87-39)
(Closed)
LER 50-250/87-33,
Reactor
Trip During Controlled
Shutdown
When
Source
Range
High Neutron
Flux Trip Unblocked.
The inspectors
reviewed
the completed corrective actions
and found them acceptable.
This item is
closed.
(Ref. Inspection
Report 50-250/87-51)
(Closed)
LER 50-250/88-09,
guality Assurance
Discovered
Missed Technical
Specification
Surveillances
for Station Battery Pilot Cell
Rotation
and
Fuel Oil Sampling Analysis.
The inspectors
reviewed
the
completed
corrective actions for these
items
and found
them acceptable.
This item
is closed.
(Closed)
LER 50-250/88-22,
Diesel
Generators
Due to Planned
Maintenance
and
Fuel Filter Flow Restriction.
The inspectors
opened
Inspector
Followup Item 50-250/88-30-01
to track the licensee's
corrective
actions.
This item is closed.
(Closed)
LER 50-251/87-13,
Failure of the
480 Volt Undervoltage
Relay.
The corrective actions required,
as
a result of the failure, were reviewed
and found to be adequate.
This item is closed.
(Closed)
LER 50-251/87-'6,
Failure of 4A ICW Pump Causing
Auto Start of 4C
ICW Pump.
The corrective actions
taken,
as
a result of the failure, were
reviewed
and found to be adequate.
This item is closed.
(Closed)
LER 50-251/87-26,
Auto Start of 4B
CCW Pump when Returning
4C
Pump to Service.
The corrective actions required, for this event,
were
reviewed
and found to be adequate.
This item is closed.
(Closed)
LER 50-251/87-27,
Failure to Estimate
Steam
Generator
Blowdown
Flow Rate.
The corrective actions specified in this
LER were reviewed
and
found to be adequate.
This item is closed.
(Closed)
P2185-01,
" Potential
Problem
with
Pipe
Clamps
during
Installation.
Licensee
review of the subject
pipe clamps identified and
determined
that
they
were
purchased
for the
St.
Lucie Plant
and
no
purchase
orders for Turkey Point could be located.
However, the licensee
stated
that current
procedures
regarding
visual
examination
were
sufficient to detect this problem and discrepancies
would be corrected,
as
required.
This item is closed.
Monthly Surveillance
Observations
(61726)
The
inspectors
observed
TS required surveillance
testing
and verified,
that the test
procedures
conformed to the requirements
of the TS, testing
was performed'n
accordance
with these
procedures,
and that the test
instrumentation
required to perform the tests
was calibrated.
In addition,
the
inspectors
verified that
the test results
met acceptance
criteria
requirements,
were
properly
reviewed
by
personnel
other
than
those
directing
the test,
deficiencies
identified were properly reviewed
and
resolved
by management
personnel
and that system restoration
was adequate.
For completed tests,
the inspectors verified that testing frequencies
were
met and tests
were performed
by qualified individuals.
The
inspectors
witnessed/reviewed
portions
of
the
following test
activities:
0-0SP-16.26,
Electric Driven Fire
Pump Operability Test.
O-NCZP-030,
Component
Cooling Water Sampling.
4-0SP-200.3,
Section 7.2,
Main Turbine Trips Test.
4-OSP-089. 1, Turbine Generator
Trip Test.
O-OSP-062.2,
3B Safety Injection
Pump Inservice Test.
3-0SP-075.2,
Train
2 Operability
Verification.
OP-4004.2,
Safeguard
Relay Rack Train A,
B - Periodic Test
on
Unit 4.
3-SMI-071.5,
Protection
Set III (gR-18) Analog
Channel
Test.
0-OSP-023. 1, Diesel
Generator Operability Test.
On June
24,
1989,
the operators
performed 3-0SP-075.2,
to test the Unit 3
AFW System Train 2.
- The
B and
C AFW pumps are normally aligned for Train
2 Service.
The
B
AFW pump was tested satisfactorily,
however, during the
C
pump test,
the governor oil level
was low in the sightglass.
Further
investigation
revealed
an oil leak existed
at
a governor
housing
plug.
The
C
AFW pump was declared
OOS due to the oil leak.
Unit 3 was in Mode
2
at the time
and
was
preparing
to
go
on line.
Technical
Specification
3. 18, Auxiliary Feedwater
System
requires
that
two trains of
AFW be
while in Modes 1,,
2 or 3.
This section
also allows the third
AFW pump to be
00S for 30 days
and that
TS 3.0.4 is not applicable to the
third
pump (i.e.,
Unit
3
could
change
modes
with the third
pump
Since
the
A and
B
pumps
were aligned to train
1
and
2,
respectively,
the provisions of TS 3. 18 were met.
Unit 3 was
placed
on
line later
that
day.
The
C AFW
pump
was
repaired
and
tested
satisfactorily
on June
27,
1989,
which
ended= the Limiting Condition for
Operation
(LCO).
0
Most of the surveillances
witnessed
during this inspection
period
were
conducted
to support
the Units
3
and
4 startups.
The inspectors
noted
that test
personnel
performed
the tests
in
a controlled,
deliberate
manner.
The tests
were completed without major discrepancies,
and minor
discrepancies
were adequately
resolved
in accordance
with administrative
controls.
No violations or deviations
were identified in the areas
inspected.
6.
Monthly Maintenance
Observations
(62703)
Station
maintenance
activities
on safety related
systems
and
components
were
observed
and
reviewed
to ascertain
that
they were
conducted
in
accordance
with approved
procedures,
regulatory guides,
industry codes
and
standards,
and in conformance with 'TS.
The following items
were considered
during this review,
as appropriate:
That
LCOs were met while components
or systems
were removed
from service;
=
approvals
were
obtained
prior to initiating work; activities
were
accomplished
using
approved
procedures
and were inspected
as applicable;
procedures
used
were
adequate
to control
the activity; troubleshooting
activities
were controlled
and repair
records
accurately
reflected
the
maintenance
performed;
functional
testing
and/or
calibrations
were
performed prior to returning
components
or'ystems
to service;
gC records
were maintained;
activities
were
accomplished
by qualified personnel;
parts
and materials
used
were properly certified; radiological controls
were properly
implemented;
gC hold points
were established
and observed
where
required;
fire prevention
controls
were
implemented;
outside
contractor
force activities
were
controlled
in
accordance
with the
approved
gA program;
and that housekeeping
was actively pursued.
The
inspectors
witnessed/reviewed
portions of the following maintenance
activities in progress:
Troubleshooting
Cranking Diesel
No. 2.
Would not synchronize
on
line.
Repair
of MOV-3-750,
MOV-3-751,
MOV-4-750
and
MOV-4-751 to
eliminate pressure
binding.
(See discussion
below).
Repair of CV-3-2821 for excessive
seat
leakage.
Repair of Unit 4 Flux Mapper Assemblies.
Repair of Unit 4 High Pressure
Turbine Cylinder Heating
Steam
Leak.
Replacement
of 3A RHR Pump Mechanical
Seal.
The modifications to MOV-750 and
751
on Units
3 and
4 were previously
discussed
in Inspection
Report
50-250,251/89-24
and identified
as
IFI
89-24-05.
The
licensee
performed
testing
on
the Unit 4 valves
and
determined that. the binding of the valves
was
caused
by pressure
trapped
between
the
discs
of the
valve.
The testing
was
accomplished
by
increasing
the pressure
between
the valve discs using
a test
pump and then
performing
MOVATS testing
on the actuator
which showed that
as
pressure
was
increased
between
the discs,
the pull out torque
or thrust
also
increased.
This
phenomenon
was previously discussed
in
which
was
evaluated
by the licensee
and
EBASCO in several
letters
and
documents
(JPE-PTP0-87-836,
PTP-87-120,
JPE-PTPO-87-1521
and
REA-TPN-85-39) in mid 1987.
The correspondence
identified the valves
in
the plant,
that could
be subjected
to thermal
or pressure
binding
and
provided
several
methods
to correct
the
problem, if required.
The
licensee
concluded,
in JPE-PTP0-87-1521,
that the identified valves did
not present
an operability concern.
Their conclusion is based
on existing
plant
procedures
that demonstrate
valve operability
by periodic cycling
and
a lack of reported failures
due to thermal or pressure
binding.
Since
this fai lure
was directly attributed
to pressure
binding,
the licensee
implemented
PC/M 89-373 for Unit 4 and
PC/M 89-375 for Unit 3.
These
PC/Ms installed
bonnet equalizing
lines
from the bonnets
of MOV-750 and
751 for both units
through
the existing
packing leak-off lines to
a
connection
upstream of the subject valve.
This would allow any pressure
trapped
between
the discs
to
be vented to the upstream
side of the valve
and thus eliminate the effects of pressure
binding.
Testing
was conducted
after installation .of the
PC/Ms
which verified the modification did
eliminate
the
pressure
binding effect experienced
in these
valves.
The
licensee
also
evaluated
the other valves identified
as
a result of the
and
determined
that
due
to lack of failure history
and
valve
application
that
no further corrective action
was required at present.
The
residents
discussed
this
issue
with the
Region
and
due
to the
potential
generic
application
the
Region is currently considering
the
issuance
of an Information Notice.
The licensee notified the industry of
the failure
and
cause
via Operating
Plant
Experience
Report,
OE 3376,
dated
June 2,
1989.
No violations or deviations
were identified in the areas
inspected.
Operational
Safety Verification (71707)
The inspectors
observed
control
room operations,
reviewed applicable logs,
conducted
discussions
with control
room
operators,
observed
shift
turnovers
and confirmed operability of instrumentation.
The inspectors
verified the operability of selected
emergency
systems,
verified that
maintenance
work orders
had
been submitted
as required
and that followup
and prioritization of work was
accomplished.
The inspectors
reviewed
tagout records,
verified compliance with TS
LCOs
and verified the return
to service of affected
components.
In addition,
by observation
and direct interviews, the inspectors verified
that the physical security plan was being implemented.
Plant
housekeeping
and implementation
of radiological controls were'lso
observed.
The inspectors
found the cleanliness
conditions in the plant
and the implementation of radiological controls to be satisfactory.
Tours of the intake structure
and diesel, auxiliary, control
and turbine
buildings
were
conducted
by the
inspectors
to observe
plant equipment
conditions
including potential fire hazards,
fluid leaks
and excessive
vibrations.
The inspectors
walked
down accessible
portions of the following safety
related
systems
to verify operability and proper valve/switch alignment:
A and
B Emergency
Diesel
Generators
Control
Room Vertical Panels
and Safeguards
Racks
Intake Cooling Water Structure
'160
Volt Buses
and
480 Volt Load and Motor Control Centers
Unit 3 and
Platforms
Unit 3 and
4 Condensate
Storage
Tank Area
Area
Unit 3 and
4 Main Steam Platforms
Auxiliary Building
The inspectors
also
reviewed
the licensee's
administrative
program for
ensuring
that
a
licensed
operator
that fails
his
requalification
examination
is
removed
from licensed
duties.
Administrative Procedure
0301,
Licensed
Operator
Requalification
Program,
provides
for the
administrative
controls in this area.
Step 8.4.2.2.
requires
that
any
individual that fails
the requalification
examination
be
placed
in
a
remedial training program until the responsible
supervisors
are satisfied
that
the
individual
is
again
proficient.
Proficiency
shall
be
demonstrated
by passing
another
examination.
When an individual fails the
examination,
the Training Department
sends
a memorandum to the Operations
Supervisor
informing
him that
the
individual failed to
complete
the
requalification requirements
and is to be relieved of all licensed duties
effective immediately.
At this time the individual is removed
from the
watch bill and is not allowed to assume
the watch until requalification
requirements
have
been
successfully
met.
When the individual is again
deemed proficient the Training'epartment
sends
another
memorandum to the
'Operations
Supervisor
informing him that the individual
may again
assume
licensed duties.
At this time the individual is placed
back
on the watch
bill.
In this inspection
the inspectors
reviewed
AP 0301,
memorandum
removing
and
reinstating
individuals,
and
held
discussions
with
responsible
Training
and Operations
Department
personnel.
In the past,
the
inspectors
have
personally
witnessed
the
removal
of
a
licensed
individual
from licensed
duties
due to failure of 'a requalification
examination.
~
No violations or deviations
were identified in the areas
inspected.
Installation
and Testing of Modifications (37828)
a 0
The
inspectors
reviewed
PC/M 88-535,
Pressurizer
PORY Air a'nd
Nitrogen Supply Tubing Enhancement,
Revision 4, Supplement
3.
Recent
PORV stroke
time measurements
had revealed
that opening times, for
both instrument air and nitrogen
sources,
were
not within the
two
second
opening
time requirement
stated
in the
OMS design analysis.
This
issue
was
discussed
in Inspection
Report
88-26
and is being
followed up as Violation 50-250,251/89-27-01
as noted in paragraph
2
of .this report.
The inspectors
observed
the installation of various
components
and
determined
that
proper
preoperational
testing
was
performed.
The
preoperational
test procedures
were reviewed for proper setpoints
and
to insure that test results
met the test criteria.
The modification
package
and
procedures
were controlled
in accordance
with licensee
administrative
procedures.
Drawings
were
updated
to reflect the
modification except
as noted:
4-0P-041.2,
Pressurizer
Operation,
dated
5/10/89,
attachment
2,
page
4 of 4, lists
4-40-240
and
4-40-250 nitrogen cylinder
isolation
valves
as
open.
Drawing
5610-M-339,
Auxiliary
MSIV and
Pressurizer
PORY Nitrogen
Backup
Supply
Systems,
Revision 39,
does
not show the noted valves.
4-0SP-041.4,
Overpressure
Mitigating System Nitrogen Backup Leak
and Functional Test,
dated 5/2/89, refers to valves
4-40-240
and
4-40-250.
These
valves,
as
noted
above,
are
not
shown
on
drawing 5610-M-339.
b.
The
inspectors
reviewed
PC/M 88-245,
Main
Steam
Isolation
Valve
(MSIV) Air Accumulator
System,
revision dated October
13,
1988.
The
purpose
of this modification
was to provide safety
related air
capable
of closing
each
MSIV in five seconds
or less.
This modification ensured
that the
MSIV can
be maintained
closed for
one
hour before operator
action outside
the control
room would
be
required.
The inspectors
witnessed
various
stages
of installation
and testing
to verify that the appropriate
work controls
were
being followed.
The following preoperational
tests
were witnessed/reviewed
by the
inspectors:
POP
0800.212,
Unit 4
MSIV Air Accumulator
Backup
System
Cold
Test.
POP
0800.213,
Unit 4
MSIV Air Accumulator
Backup
System
Hot
Test.
The inspectors
performed
a walkdown of the
system
using appropriate
drawings
and procedures
to verify that:
Major system
components
were properly labeled.
10
Instrumentation
was properly installed, functional,
and process
parameter
values
normal.
Valves in the
system
were aligned in the correct position for
normal operation.
Drawings
and
procedures
reflected
the
proper
system
configuration.
The documentation
reviewed included:
4-0P-072,,Main
Steam
System,
dated April 28.
1989.
4-0P-013,
Instrument Air System,
dated April 6,
1989.
Drawing
5610-M-735,
MSIV Air Operator
and Air Accumulator
Back-up System
POV-4-2604,2605,2606,
Unit 4, Revision 0.
Drawing
5610-T.-E-4061,
Sheet
5,
MSIV Air Operator
and Air
Accumulator Back-up System.POV-4-2604,
2605,
2606,
Revision 0.
The inspectors
noted the following discrepancy:
4-0P-013,
Attachment
1,
page
58,
had the operator verify the
position of valve 4-40-2166,
Instrument Air to MSIY POV-4-2604,
2605,
and
2606 Isolation,
two times.
One time to verify the
valve to
be
open,
the other to verify the valve closed.
The
normal
system alignment required the valve to be open.
c.
The inspectors
reviewed
the Unit 4 High'ensity
Spent
Fuel
Rack
Project,
as outlined in Procedure
No. FPL-0113-P-l,
Revision
1.
The
following procedures
were reviewed:
FPL-0113-P-l,
Rev.
1
Project
Administrative
Procedure
for
High Density
Spent
Fuel
Rack Project
(HDSFRP).
FPL-0113-P-2,
Rev.
1
Rack removal for HDSFRP.
FPL-0113-P-4,
Rev.
1
Hydrolasing for HDSFRP.
FPL-0113-P-5,
Rev.
1
Underwater
Vacuuming for
HDSFRP.
FPL-0113-P-7,
Rev.
1
Drag Test for HDSFRP.
FPL-0113-P-8,
Rev.
1
Housekeeping
Procedure for HDSFRP.
Topics for possible
enhancements
to the
procedures
were discussed
wi,th appropriate
licensing personnel.
t
11
The inspectors
observed
various
rack manipulations
both outside
and
inside the Spent
Fuel Building.
On June
19,
1989, while the licensee
was
attempting
to lower old rack
No. 3, to the ground,
the nylon
strap rigging failed and the rack dropped
a small distance
to the
ground.
Personnel
in the
area
immediately
secured
the operation,
sealed
the
area off and took prompt actions
to survey the area for
any possible
contamination.
There
was
no contamination,
or injuries
due to the
dropped
rack.
The licensee
immediately
began
a lessons
learned
review and
by the
end of the week were ready to make their
recommendations
to management
to preclude similar incidents.
During
the inspectors
observations,
various incidents of lack of attention
to detail
were
noted to the licensee.
The licensee
took positive
steps
to prevent recurrence.
By the end of June
23,
1989,
old rack
No.
3 was
boxed
and
on
a flat bed truck ready for shipment.
Old rack
No.
4 was
moved into old rack No.
3 position in the Spent
Fuel Pool,
ready to be hydrolased
and removed.
New rack No.
4 has
been
Dry Drag
tested
and the rigging installed,
ready to
be put in the pool.
The
inspectors
also
reviewed
various
Daily Project Status
Reports,
as
required
by Project Administrative Procedure,
FPL-0113-P-1.
Correction of the
noted discrepancies
in items
8a.
and
b.
above
by the
licensee will be followed as Inspector
Followup Item 50-250,251/89-27-03.
No violations or deviations
were identified.
9.
Followup on Onsite
Events
(93702)
The following plant events
were reviewed to determine facility status
and
the
need for further followup action.
Plant parameters
were evaluated
and
the significance of the event
was evaluated
along with the performance
of
the appropriate
safety
systems
and the actions
taken
by the licensee.
The
inspectors
verified that required notifications
were
made
to the
NRC.
Evaluations
were
performed
relative
to the
need for additional
NRC
response
to the event.
Additionally, the following issues
were examined,
as
appropriate:
details
regarding
the
cause
of the
event;
event
chronology;
safety
system
performance;
licensee
compliance with approved
procedures;
radiological
consequences,
if any;
and
proposed
corrective
actions.
On June
12,
1989, with Unit 3 in Mode 5,
leakage
was
noted during
system fill and vent.
Investigation
by the licensee
revealed
RVS-200,
Reactor
Coolant Vent System drain valve,
was approximately
one half turn
open.
This valve was required to be closed during the fill and vent.
The
valve had
a hose attached
which ran to
a floor drain.
The. floor drain
had
overflowed.
The valve
was
closed
and the fill and vent
was completed.
The
licensee
could not determine
how the valve
was
opened.
The site
guality Assurance
Performance
Monitoring Section
reviewed the incident and
issued
a
summary
on
June
20,
1989,
(gAO-PTN-89-993).
The corrective
actions
for this event
were to change
the fi11
and vent
procedures
to
include verification of valve
RYS-200 to be closed if it is not used
as
a
vent path.
Also,
a verification of blank flanges
and caps
was being
added
12
to post alignment checks.
This step
was already in the process
of being
incorporated
at the time'f this event.
This
was part of corrective
actions
to
a similar event for Unit
4
on
March 9,
1989.
This event
.resulted
in
a Violation 50-250,251/89-12-03.
This item is still open
and
the completed corrective actions will be reviewed to determine if they are
adequate
to prevent recurrence.
On June
16,
1989, at
11: 15 a.m., with Unit 3 in Mode 5; PRMS rack 66 was
de-energized
causing
process
radiation
monitors
R-11
and
R-12 to trip
resulting
in
Containment
Isolation
on Unit
3
and
the
Control
Room
Ventilation System to automatically shif't to the Recirculation
Mode.
All
equipment
functioned
as
required
and
the licensee
notified the
NRC in
accordance
with
The
event
occurred
when
ILC
personnel
were troubleshooting
the pressurizer
safety
valve acoustical
monitoring circuitry using
an oscilloscope.
The oscilloscope
was plugged
into
a vital
AC outlet in the bottom of rack
67 and
when the
scope
was
turned
on it caused
breaker
3P08-19 to trip which de-energized
R-Il and
R-12.
The licensee
is taking the following actions to prevent recurrence;
( 1) clearly identify, by labeling, all vital AC power feeds
and electrical
receptacles;
(2) install protective
covers
over the vital
AC receptacles
(3) require
personnel
to obtain
permission
from control
room personnel
prior to
using
unidentified
power
feeds
and electrical
receptacles;
(4) determine if the electrical
loading
on the breaker
is close to its
trip setpoint
as
the oscilloscope
only
draws
about
two
amps
and
was
checked to be functioning properly.
On
June
16,
1989, at 9:49 p.m., with Unit
3 in
Mode 5,
an inadvertent
Train "B" safeguards
actuation
occurred while re-energizing
the safeguards
relay
racks
after
maintenance
in
accordance
with
3-ONOP-049.
All
equipment
functioned
as
expected
and
was verified using
3-EOP-E.O.
The
licensee notified the
NRC of the event
as required
Initial troubleshooting
indicated
the pushbutton for relay 3SIB-2, manual
safety injection block pushbutton,
failed to remain inserted
which caused
the actuation
when the pushbutton
was released.
The
ISC Department
found
a
cracked
wafer in the contact
block which
was
replaced.
On
June
17,
1989, at 4: 13 p.m.,
the
same
event occurred while re-energizing
the Train
"A" safeguards
relay racks.
Again, all equipment
functioned
as expected
and
the
NRC
was notified.
Licensee
investigation
into the occurrence
indicated
the
Block Switch
was mislabeled
in that the "Block" and
"Unblock" positions were reversed.
The licensee
obtained
a picture of the
switch and the general
area of that portion of the control
room panel that
clearly
shows
the
switch labeling opposite
to that at present.
The
picture
was
made in March of 1989 by simulator personnel
for training and
simulator validation use,
which indicated
the labeling
had
been
changed
between
March
and
June of this year.
The licensee's
investigation into
the
issue
identified that the
person installing the
new label
did not
verify that the switch positions
were the
same
as the positions
on the
label
to
be
removed.
requires
that written procedures
and
administrative
policies shall
be established,
implemented
and maintained
that meet or exceed
the requirements
and recommendations
of Appendix
A of
USNRC Regulatory
Guide 1.33
and Sections
5. 1 and 5.3 of ANSI N18.7-1972.
13
O-ADM-209, Equipment
Tagging
and Labeling, provides the responsibilities,
precautions,
limitations
and instructional
guidance for establishing
and
maintaining
an accurate,
complete
and effective plant tagging
program.
Contrary to the above,
engraved
label
plates
were replaced
on the Unit 3
Safety
Injection
Block
Switch without following the
requirements
of
O-ADM-209, resulting in two separate
safeguard
actuations within a
24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
period.
This is identified as Violation 50-250,251/89-27-04.
On June
17,
1989, with Unit 4 at approximately
30% power, the
RCO received
a
Generator
Field
Brush
Contact
Failure/Ground
alarm.
Inspection of the generator exciter revealed
a Turbine Plant Cooling- Water,
(TPCW) leak.
The leak
was located
on
a copper tubing drain line from the
D air cooler.
The
operators
commenced
a
load reduction at
5:32 a.m.
and
took
the unit off line at
5:52 a.m..
The
licensee
determined
that the tubing failure was
due to the tube vibrating against
the clamps.
The defective tubing was replaced
and
a protective sleeve
was
installed to protect the tube.
The Unit 3 exciter cooler drain lines are
stainless
steel,
therefore,
they
are
less
susceptible
to this failure
mode.
The
licensee
plans
to replace
the
copper tubing with stainless
steel
during
an outage of sufficient duration.
The licensee
dried and
tested
the exciter.
Unit 4 was returned to service
on June
18,
1989.
10.
Followup on Licensee
Employee
Concerns
(RII-88-A-0066)
The
inspectors-
reviewed
the following licensee
employee
concerns
which
resulted
from
NRC interviews.
The concerns
are described
below with their
disposition.
a
~
A
concern
was
raised
involving configuration
of electrical
cannisters.
Each cannister
has
a nitrogen fill line
which is provided to maint'ain the cannister
from 15 to 19 psig.
The
cannisters
are
pressurized
with nitrogen
to verify cannister
integrity for the
LLRT and the ILRT, and also to maintain
a moisture
free environment.
On June ll, 1986,
NCR 86-293
was written.
The
problem described
was that the
used
to monitor the cannister
nitrogen pressure
did not appear
on any prints or on the g-list.
The
NCR disposition
stated
that the
could
be
used
as is.
The
cannisters
are
checked
by the Electrical
Maintenance
Department
during quarterly preventive
maintenance
per
MI 51003
and
51004 for
Units
3 and 4, respectively.
If the pressure
is found less
than
15
psig,
the Technical
Department
is notified to implement repair
and
perform
a
LLRT. The
are not calibrated
since
the pressure
is
checked
during the
LLRT with calibrated
The
NCR also stated
that
the cannisters
are
provided with an isolation valve located
between
the cannister
and pressure
This valve is maintained
closed except
when monitoring nitrogen pressures.
The inspectors
walked
down electrical
for Units
3 and
4
using
drawing
5610-E-54A-1,
sheet
1, revision
1.
The inspectors
noted that the drawing did not match
the field installation in that
14
the
isolation valve
was
not included
on the drawing.
The
inspectors
brought this discrepancy
to the Engineering
Department's
attention.
The licensee
subsequently
performed
a
walkdown which
generated
NCR 89-0237,
on
June
12,
1989.
Another discrepancy
was
identified in that the drawing specified pressure
have
a range
of 0-100 psig.
The installed
have
a range of 0-30 psig.
This
item is being adequately
addressed
by., the licensee.
A concern
was raised
involving excessive
hum in NIMS.
This item
was submitted
to the licensees
on March 30,
1989.
The
NIMS was
installed in May 1984
and
June
1985 for Units
4 and
3 respectively..
Shortly after installing both Units,
NIMS developed
a 120 Hertz noise
contamination.
The systems
were still operable
and could detect
a
2
foot-pound
impact at
3 feet
as originally designed.
The
vendor
suggested
that the noise
contamination
could
be
removed
by lifting
the shield connection of any noisy channel
in the control
room NIMS
rack,
In
October
1986,
a
REA
was
generated
to
address
the
noise
contamination
in both units.
The
REA recognized
that the noise
was
caused
by shield connections
being grounded
on both the control
room
and containment
side of the system.
In August
1987,
the Unit 3 loop ground
was
removed
permanently
by
lifting the shielded
connections
in the containment
and relanding the
control
room connections.
In March 1989,
the
NIMS vendor performed
a system operability check
and
a
system calibration
on Unit 4.
The vendor also
reviewed
the
licensee's
NIMS procedures
to insure
that
the
system
was
being
operated
and maintained
to conform with the original design.
The
Unit 4 loop ground
was
removed
in April of
1989
by lifting the
containment
connections
and
by
relanding
the
control
room
connections.
Subsequent
investigations
revealed
cracked
glass
insulators
on the
accelerometers.
This condition
caused
a ground in the containment
and with the control
room side
grounded,
noise
was still present.
Therefore,
the containment
side will be grounded
and the control
room
connections will be lifted to remove the ground loop.
The incorporation of vendor
recommendations
into plant procedures
and
the
elimination of noise
contamination
should
ensure
reliable
operation
of the
NIMS.
This
concern
was
adequately
addressed
according to
ADM -002,
Employee
Concerns
Reporting
System
Program.
A concern
was raised
that the
PAHMS did not work properly.
This
concern
was submitted to the licensee's
on March 30,
1989.
The
licensee
formed
a task
team in November
1988 to address
the numerous
LCO hours
due to
PAHMS inoperability.
Discussions
with the equipment
vendor
have
led to corrections
and clarifications
to
OP 0204.2,
15
d.
Periodic
Tests,
Checks,
and
Operating
Evolutions.
The licensee
expects
these corrections'o
reduce
the
number of out of service
hours
on
PAKMS.
Additionally, I&C and the task
team are monitoring
the
performance
of
PAHMS and further corrective
actions will be
initiated, if necessary.
The inspectors
found that this
item was
addressed
satisfactorily by ADM 002.
A concern
was
raised
that
the
PASS did not work properly.
This
concern
was submitted to the licensee's
on March 30,
1989.
The
licensee
responded
that
since
the
was
installed
in
1980,
numerous
design
and operational
problems
have
been encountered.
One
by one,
the problems
have
and continue to be corrected.
The chloride
analyzer is the last non-functional
analyzer.
The licensee
plans to
issue
a design
package
which will replace
the chloride analyzer
in
1989.
In the meantime,
the
sample
cask is available for offsite
reactor
coolant chloride analysis.
However,
PASS reliability is
still being evaluated.
Items targeted for further evaluation
include
the oxygen analyzer,
hydrogen analyzer,
flow instruments
and tempera-
ture instruments.
The
PASS is considered
operational
in accordance
with
NRC
requirements.
The
PASS modifications
and
operational
testing is
an ongoing
NRC concern
which is discussed
in Inspection
Report
50-250,251/88-29.
The inspectors, found that this
employee
concern
was addressed
in accordance
with ADM-002.
e.
A concern
was raised that
due to deficient procedures
and drawings,
availability of the
Halon Fire Suppression
System
was questionable.
This concern
was submitted
to the licensee's
on March 30,
1989.
The trip energy
source for the release
valves is provided
by
a pair
of nitrogen bottles.
Adequate
pressure
is monitored
by
pressure
switches
mounted
on
each bottle.
These
pressure
switches
are calibrated
by the vendor..
One of the problems
noted
was that
during
bottle
replacement
the
pressure
switch
is
decalibrated.
The licensee
determined,
by checking bottle pressures,
that
an operability problem did not exist.
However,
a
REA is being
developed
to resolve
the calibration concern.
The inspectors
found
that
this
employee
concern
was
addressed
by the
licensee
in
accordance
with ADM-002.
A concern
was raised
involving inadequate
reactor trip relay timing
tests.
This
concern
was
submitted
to the licensee's
and
adequately
addressed
in accordance
with ADM-002.
This concern
was
also
discussed
in
NRC Inspection
Report 50-250,254/89-06,
paragraph
5.
ll.
Generic Letter 88-17 (TI 2515/101)
This TI addresses
the licensee's
short-term
program entitled "Expeditious
Actions" for the
Loss of Decay
Heat
Removal
issue
discussed
The licensee
responded
to the
NRC recommended
expeditious
actions
in letter
dated
January
3,
1989.
The
licensee
implemented
the
recommendations
of the
Generic
Letter
in
procedure
16
3/4-0P-041.9,
Reduced
Inventory Operations,
which provides instruct'ional
'uidance
for operation of the unit when
RCS level is lower than three feet
below the reactor
vessel
flange with irradiated fuel in the vessel.
The
review of this TI, to assure
the licensee
actions
to prevent
and, if
necessary,
respond
to loss of decay
heat
removal
during operations
with
the
RCS partially drained,
consisted of the following:
a
~
General
b.
The
licensee
completed its response
to the expeditious
actions
in
licensee
letter L-88-559,
dated
January
3,
1989.
The
inspectors
reviewed the subject
response
for implementation
by discussions
with
responsible
licensee
personnel
in operations
and training, review of
the implementing procedure
(3/4-0P-041.9)
and referenced
procedures,
and
a visual
inspection
of the
components
or systems
required for
this
mode of operation.
Training
Turkey Point currently provides training
on
RCS midloop operations
and
recovery
from loss of
RHR for licensed
operators.
Training
topics
presented
since
the fourth quarter of 1988 were
the Diablo
Canyon event,
related
events,
lessons
learned,
the implications of
the
event
and
loss
of
RHR off normal
procedure.
In addition,
licensed operators
received simulator training concerning
loss of RHR
flow at midnozzle
operation.
Prior to operating
in
a
reduced
inventory condition,
Turkey Point will provide training on operation
in a reduced
inventory condition with irradiated fuel in the reactor
vessel.
Procedure
3/4-0P-41.9
requires
that operating
shifts
be
briefed prior to and
as part of shift turnover when operating
the
in
a reduced
inventory condition.
This briefing shall
include what
equipment,
indications,
and actions
are required to monitor
and
RHR parameters
during reduced
inventory operation
and recovery from
loss of
RHR.
Available sources
of
makeup water shall
also
be
discussed.
The inspectors
reviewed
the training briefs discussing
RCS Mid-Loop Operations,
the Diablo Canyon event,
related industry
events
and
the
simulator
training
program for loss
of
Flow/Cooling.
Procedure
3/4-0P-041.9
contains
prerequisites
for
conducting shift briefings
and
documentation
of attendance
and
content
of the briefing prior to entering
a
reduced
inventory
condition.
c ~
Containment
Closure
Procedure
3/4-0P-041.9
contains
the
requirements
for containment
closure to be established
prior to entering
a reduced
RCS inventory
condition.
Certain
exceptions
are
allowed
by step
3. 16.4 provided
the following requirements
of step 4. 13 are met.
(1)
Containment
closure is not necessary if the Reactor
Vessel
and
surrounding
pool contain
no irradiated fuel.
17
(2)
Containment
including the
equipment
hatch,
may
remain
open
provided closure
is
assured
within two hours of
initial loss of Decay Heat Removal.
(3) If openings totaling greater
than
one
square
inch exist in the
cold legs,
reactor
coolant
pump
connections
to the cold leg
water
space,
or crossover
pipes
of, the
RCS,
then
containment
closure
must be. reasonably
assured
within 30 minutes of initial
loss of Decay Heat Removal.
(4) If a vent path is provided
by removal of the pressurizer
manway.
or
a
S/G
manway,
then
the
30 minute
time requirement
may
be
increased
to two hours.
(5)
Containment
closure activities are to
be initiated upon loss of
RHR for greater
than five minutes
per 3/4-0NOP-050,
Loss of RHR.
(6)
Once containment closure activities are initiated due to loss of
Decay Heat
Removal,
they may not be terminated until controlled
and stable
Decay Heat
Removal
has
been restored
and the
RCS has
been returned to
a controlled
and stable condition.
d.
Temperature
Indication
The existing core exit thermocouples
meet this requirement
when the
reactor
vessel
head
is located
on top of'he reactor
vessel.
the
do not currently provide
an alarm function,
however,
Turkey Point will evaluate
the feasibility of providing this
function.
If an alarm function is not available,
two independent
channels
will
be
monitored
and
recorded
every
15 minutes
when
operating
in
a reduced
inventory condition.
If an alarm function is
available,
two independent
channels will be monitored
and recorded
every
hour
by
an operator
in the control
room while operating
in a
reduced
RCS inventory condition.
The inspectors verified that these
requirements
are
included
in the licensee's
procedure
3/4-0P-041.9,
steps
3.11,
3.17,
4.14,
4.15,
5.2.2.2,
and
Attachment
2 require
logging of the temperatures.
e.
RCS Water Level Indication
Turkey Point currently
has
two methods of RCS level indication.
One
is
a
pressure
transmitter
which provides
level indication to the
control
room.
The other is
a tygon hose located inside containment,
and vented to the pressurizer.
Both indicators
are connected
to the
RCS at the "A" loop intermediate
leg drain.
FPL's engineering
group
has
developed
a correlation
graph
between
indicated intermediate
leg
level
and
actual
hot leg level for use
during
reduced
inventory
conditions.
When in
a
reduced
RCS inventory condition,
the level
transmitter will be monitored
and
recorded
every
15 minutes until
alarm functions
can
be provided.
When alarm functions are provided,
the level transmitter will be monitored
and recorded
every hour.
The
18
licensee will monitor the tygon
hose
and record
the level every
15
minutes
when 'RCS is'in
a reduced
inventory condition.
The operator
monitoring the
hose will be in communication with and report
each reading'to
the control
room.
These
requirements
are included in
the licensee's
operating
procedure
3/4-0P-041.9,
steps
3. 12,
3. 13.
4.2,
4.10,
4.14,
4.15,
5.1.1.4,
5.1.2.3,
5.2.2.1,
5.2.2.2,
and
Attachment 2, which requires
logging of level indications.
RCS Perturbations
Procedure
3/4-0P-041.9 "includes
a
'general
precaution
in step
4.12
that states:
"When
RCS water level is lower than three feet below the .Reactor
Vessel
Flange, all activities
which
may cause
perturbation of
the
RCS water level including the manipulation of systems
that
maintain the
RCS in a stable condition should
be prohibited."
In addition,
Enclosure
1
to
the
procedure
provides
a list of
activities that are
undesirable
during reduced
inventory conditions
as
they
may cause
RCS perturbation.
Step
5. 1.2.8 of the procedure
requires verification that
these activities
are
not in progress
or
will not cause
perturbations
prior to reducing
RCS inventory.
RCS Inventory
As
a prerequisite
to entering
a
reduced
RCS inventory condition,
procedure
3/4-0P-041.9
requires
that at least
one
high pressure
safety injection
pump is available
and capable of taking suction from
the
and
providing injection to the
hot
and cold legs.
In
addition,
the procedure
requires
that two charging
pumps
are avail-
able
and
capable
of taking
suction
from the
and
providing
injection to the
RCS.
Guidance for operation of these
systems
during
loss
of
are
contained
in existing
off-normal
procedure,
3/4-0NOP-050,
Loss of RHR.
Hot Leg Flow Paths
At this time,
Turkey Point
does
not
use
nozzle
dams.
However,
procedure
3/4-0P-041.9
requires that
a vent path
be provided whenever
an opening of one square
inch or greater exists in the cold leg, the
RCPs or the intermediate
leg.
Until further analysis
is performed,
this vent will consist
of either the pressurizer
manway,
a
steam
generator
hot leg manway or a steam generator
cold leg manway.
These
requirements
are contained
in procedure
steps
4.16 and 4.17.
Loop Stop Valves
Loop stop valves
are not installed in the
RCS loops at Turkey Point
Units
3 and 4.
19
The inspectors
consider
the licensee's
response
to the Generic Letter and
the implementation of the response
in training, equipment,
and procedures
to be adequate
and satisfy the requirements
of the TI.
This TI is closed.
No violations or deviations
were identified in the areas
inspected.
12.
Exit Interview (30703)
The
inspection
scope
and findings
were
summarized
during
management
interviews held throughout
the reporting period with the Plant Manager-
Nuclear
and selected
members of his staff.
An exit meeting
was conducted
on June
30,
1989.
The areas
requiring management
attention were reviewed.
No proprietary
information
was
provided
to the
inspectors
during the
reporting period.
The inspectors
had the following findings:
Item Number
Descri tion and Reference
50-250,251/89-27-01
50-250,251/89-27-02
50-250,251/89-27-03
50-250,251/89-27-04
13.
and Abbreviations
Violation -
PORV opening
time exceeded
the
OMS safety evaluation limits of 2 seconds,
Paragraph
2
Non-Cited Violation - Failure
to identify
outstanding
clearance
affecting
the
flow to the
C
steam
generator,
Paragraph
2
IFI - Correction of minor procedural
and
drawing discrepancies,
Paragraph
8
Violation - Installation of erroneous
label
plates
on the Unit 3 safety injection block
switch, Paragraph
9
ADM
ANSI
CCTY
CFR
DP
ERT
Alternating Current
Administrative
American National
Standards
Institute
Administrative Procedures
American Society of Mechanical
Engineers
Component Cooling Water
Closed Circuit Television
Code of Federal
Regulations
Containment
Spray
Differential Pressure
Employee
Concerns
Program
Emergency
Diesel
Generator
Emergency Notification System
Event Response
Team
20
FPLTQR
HDSFRP
ICW
IEB
IFI
LCO
LER
LIV
MI
MIMS
MOVATS
NRC
ONOP
00S
OP
OTSC
PAHMS
PC/M
PNSC
REA
RCO
T AVG
TQR
TS
Power
& Light
Power
8 Light Topical Quality Assurance
Report
Final Safety Analysis Report
High Density Spent
Fuel
Rack Project
High Head Safety Injection
Intake Cooling Water
Inspection
and Enforcement Bulletin
Inspector
Followup Item
Integrated
Leak Rate Test
Inservice Testing
Limiting Condition for Operation
Licensee
Event Report
Licensee Identified Violation
Local
Leak Rate Test
Loss of Coolant Accident
Maintenance
Instruction
Metal
Impact Monitoring System
Motor Operated
Valve Analysis
and Test
System
Maintenance
Procedure
Non-conformance
Report
Net Positive Suction
Head
Nuclear Regulatory
Commission
Overpressure
Mitigating System
'ff Normal Operating
Procedure
Out of Service
Operating
Procedure
On the Spot
Change
Protected
Area
Post Accident Hydrogen Monitoring System
Post Accident Sampling
System
Plant Change/Modification
Plant Nuclear Safety Committee
Power Operated Relief Valve
Plant Supervisor Nuclear
Physical
Security Procedures
Quality Assurance
Quality Control
Request for Engineering Assistance
Reactor Control Operator
Pump
System
Residual
Heat
Removal
Refueling Water Storage
Tank
Senior Reactor Operator
Average Reactor Coolant Temperature
Topical Quality Requirement
Technical Specification
Temporary System Alteration
Unresolved
Item