ML17345A314
| ML17345A314 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 07/28/1988 |
| From: | Brewer D, Crlenjak R, Mcelhinney T, Schnebli G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17345A312 | List: |
| References | |
| 50-250-88-14, 50-251-88-14, NUDOCS 8808150008 | |
| Download: ML17345A314 (33) | |
See also: IR 05000250/1988014
Text
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UNITED STATES
NUCLEAR R EGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-250/88-14
and 50-251/88-14
Licensee:
Florida Power and Light Company
9250 West Flagler Street
Miami, FL
33102
Docket Nos.:
50-250
and 50-251
Facility Name:
Turkey Point
3 and
4
License Nos.:
and
Inspection
Conducted:
June 3-25,
1988
Inspectors:
D.
R. Brewer, Senior
Re 'dent Inspector
T.
F. McElhinney, Reside
Inspector
4-~
Le
G. A. Schn~bli,
Residen
nspector
Approved by:
R.
V. Crlenjak, Section
Chi f
Division of Reactor Projects
7 g8F
D te Signed
Date Si
ned
Date Si
ned
~ zs)e~
Date Signed
SUMMARY
Scope:
This routine,
unannounced
inspection
entailed direct inspection at
the site,
including backshift inspection,
in the areas
of annual
and
monthly
survei llances,
maintenance
observations
and
reviews,
engineered
safety
features,
operational
safety,
facility
modifications
and plant events.
Results:
One violation of
Appendix B, was identified.
Failure to
control materials
used in safety related
systems,
in that
some
fittings used
in the Intake Cooling Water
( ICW) system
were
steel
in lieu of stainless
steel,
(250,251/88-14-01)
(paragraph
5).
Two Inspector
Followup Items
( IFIs) were
identified: evaluate
the
root cause
of using
a
20
ampere
breaker
instead
of the required
30
ampere
breaker
in the alternate
power
supply to the
rod position
indicator
(RPI)
system
(IFI 250,251/88-14-02)
(paragraph
5);
and
evaluate
the basis for selecting
maximum stroke
times for the
Power
Operated Relief Valves (PORVs),
( IFI 250,251/88-14-03)
(paragraph 8).
8808l50008
880729
ADOCK 05000250
9
REPORT DETAILS
Persons
Contacted
Licensee
Employees
- J. S.
Odom, Site Vice President
- J .
E. Cross,
Plant Manager-Nuclear
- L. W. Pearce,
Operations
Superintendent
- J. A. Labarraque,
Senior Technical Advisor
- F. H. Southworth,
Technical
Department
Supervisor
J.
W. Kappes,
Maintenance
Superintendent
- T. A. Finn, Training Supervisor
J.
D. Webb, Operations - Maintenance
Coordinator
W.
R. Williams, Assistant Superintendent
Planned
Maintenance
D. Tomaszewski,
Instrument
and Control Department
Supervisor
J.
C. Strong,
Mechanical
Department Supervisor
L.
W. Bladow, Quality Assurance
(QA) Superintendent
- J .
W Anderson, Quality Assurance
Super visor
- D. A Chancy,
Engineering
Manager
- R. J. Earl, Quality Control
(QC) Supervisor
- B. A. Abrishami,
System
Performance
Supervisor
R.
G.
Mende, Operations
Supervisor
J. Arias, Regulation
and Compliance Supervisor
V. A. Kaminskas,
Reactor
Engineering
Supervisor
- R. D. Hart, Regulation
and Compliance
Engineer
"G. Solomon,
Regulation
and Compliance
Engineer
S. Hale, Engineering Project Supervisor
Other
licensee
employees
contacted
included
construction
craftsmen,
engineers,
technicians,
operators,
mechanics,
and electricians.
- Attended exit interview on June. 29,
1988.
Note:
An alphabetical
tabulation of acronyms
used in this report is
listed in paragraph
11.
Followup on Items of Noncompliance
(92702)
A review
was
conducted
of the following noncompliances
to assure
that
corrective actions were adequately
implemented
and resulted
in conformance
with regulatory
requirements.
Verification of corrective
action
was
achieved
through
record
reviews,
observation,
and
discussions
with
licensee
personnel.
Licensee
correspondence
was evaluated
to ensure
that
the
responses
were timely and that corrective actions
were
implemented
within the time periods specified in the reply.
On
August
18,
1986,
the
NRC issued
a Confirmatory Order
and Notice of
Violation and Proposed
Imposition of Civil Penalties
related to Inspection
Reports
250,251/85-32,
250,251/85-40,
250,251/86-02,
250,251/86-11,
and
250,251/86-26.
This enforcement
action combined violations and unresolved
items discussed
in these
inspection
reports.
To ensure
that all of the
inspection
findings presented
in these
reports
have
been
addressed,
this
section
of the
report
presents
closeout
of the
violations
as
they
originally appeared
in the inspection reports.
It should
be
noted that additional
examples
of Escalated
Enforcement
Action
86-20,
Item
I
(86-26-05)
and
Item
IV (86-26-09)
have
been
identified,
which
may indicate
continued
weaknesses
in the
licensee's
implementation
of
the
Plant
Change
Modification
(PC/M)
program.
Additional corrective
actions
in the
area of PC/M program implementation
will be tracked
in conjunction with the violations
issued
by Inspection
Report 250,251/87-54.
Escalated
Enforcement
Action
(EA) 86-20-I:
Failure
to Correctly
Translate
Design
Inputs
into
Operating
Procedures;
Failure
to
Correctly Translate
Design Inputs into Drawings; Failure to Translate
Appropriate Quality Standards
into Procedures
or Drawings; Failure to
Correctly Translate
Design Inputs into System Descriptions
and Design
Basis
Documents;
Failure
to
Impose
Appropriate
Design
Control
Measures;
and Failure to Adequately
Document
Assumptions
and Design
Inputs
in Calculations.
This
EA originated
from violation
250,
251/86-26-05,
which
encompassed
previously
identified
unresolved
items
250,251/85-40-04;
250,251/85-40-05;
250,251/85-40-06;
250,
251/85-40-09;
250,251/85-40-14;
250,251/85-40-22;
250,251/85-40-26;
250,251/85-40-32;
and items associated
with paragraphs
12
and
15 of
Inspection
Report 85-40.
Item
EA 86-20,
EA 86"20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86"20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86-20,
EA 86-20,
I.A.1
I.A.2
I.A.3
I.A.4
I.A.5
I.B
I.C.1
I.C.2
I.D.1
I.D.2
I.D.3
I.D.4
I.ED
I.F
Status
closed
closed
closed
closed
closed
closed
closed
closed
closed
closed
closed
closed
closed
closed
The basis for closure of each
item is discussed
below.
(Cl osed)
EA 86-20,
I.A.1:
Failure
to Establish
Adequate
Design
Control.
Inspection
Report 250,251/85-40
delineated
a failure by the licensee
to establish
adequate
design
control
measures.
Specifically,
the
licensee
failed
to
revise
off-normal
operating
procedure
(ONOP)
0208. 11,
Annunciator List
Panel
I - Station
Service,
following
completion of
PC/M 80-117.
ONOP
0208. 11
had
not
been
revised
to
include appropriate
operator
action in the event of a
low pressure
alarm
on the nitrogen backup
system.
This error
was apparently
due
to a breakdown in the plant change modification program.
Recent
modifications for the
backup
supply.
system
were
installed under
PC/M 85-175,
Change
Request
No.
2, Nitrogen Station
Additions and Relocation
Unit 3, dated
March
19,
1987,
and
PC/M
85-176,
Change
Request
No.
4,
Station
Additions
and
Relocation - Unit 4, dated
March 19,
1987.
The licensee
has revised
ONOP 0208. 11, dated
March 28,
1988, to reflect current setpoints
and
required
operator
action.
Upon receipt
of
a valid low pressure
alarm, the operators
are directed to valve in additional bottles of
and valve out the nitrogen bottles previously in operation.
The directions also specify the time frame within which the operator
must
take
action
to
ensure
a
continued
supply of nitrogen for
operation of the auxiliary feedwater
(AFW) control valves.
The inspector
reviewed administrative
procedure
(AP) 0190. 15, Plant
Changes
and
Modifications,
dated
June
14,
1988.
This
procedure
provides
specific
guidance
to
the
appropriate
plant
department
coordinator
and
requires
that training briefs,
and
operating
and
maintenance
procedure
revisions,
be
prepared
and
completed prior to
the turnover of
a
PC/M to the plant operating staff.
This item is
closed,
and also closes part of violation 250,251/86-26-05.
(Closed)
EA 86-20, I.A.2: Lack of Operator Training and Inadequacies
of Emergency
Operating
Procedure
(EOP) for the
Rupture of
a
Steam
Generator
Tube.
Inspection
Report
250,251/85-40
identified
a
safety
concern
pertaining to the ability of licensed operators
to isolate
steam flow
paths
from
a faulted
steam
generator
in the event of tube rupture.
During the inspection, it was determined that
AFW steam
supply valves
could not
be remotely
shut with an
AFW initiation signal
present.
These valves
were designed
to cycle
open during the event,
even if
the control
room hand switches
were held in the closed position.
The
licensee
failed to recognize this design
feature
and therefore
had
not
supplied
adequate
procedures
or sufficient training
on
an
alternate
means
of isolation
.
This issue
was significant in that
without an alternate
means
of isolation,
an unnecessary
radioactive
release
could have occurred following a steam generator
tube rupture
In response
to this item,
the current revision of
EOP 3/4-EOP-E.3,
Steam
Generator
Tube
Rupture,
dated
March 25,
1988,
addresses
the
inability to close,
from the control
room,
the
steam
supply motor
operated
valve
(MOV) from the
ruptured
steam
generator.
If the
reactor
control operator
(RCO) is unable
to close
the
steam
supply
MOV from the cont~ol
room,
the
EOP directs
the
RCO to dispatch
an
equipment operator to locally open the
steam
supply
MOV breaker
and
then manually close the valve. If the
steam
supply
MOV can
be closed
from the
control
room,
the
EOP directs
the
RCO
to
dispatch
an
equipment operator to locally open the
steam
supply
MOV breaker.
The
licensee
has
determined
that if the
steam
supply
MOV can
be
closed
from the control
room, that the equipment operator
should also
verify the valve is in the closed position after opening
the
steam
supply
NQV breaker.
The licensee
has
issued
night orders
informing
the operating staff of this additional
information and
has committed
to formally incorporate
the verification of the valve position after
opening the
steam
supply breaker in EOP-E.3
by October
1,
1988.
This
item is closed,
and also closes part of violation 250,251/86-26-05.
(Closed)
EA 86-20, I.A.3: Inadequate
Operator Training and Incorrect
Procedural
Information.
Inspection
Report 250,251/85-40 identified
a failure by the licensee
to provide licensed operators
with training that 'specifies
the time
available
to
the
RCOs
to
take
action
following
a
low pressure
alarm.
The
value
provided
to the
operators
in training
differed
from that specified
in operations
procedures
and
in the
system description.
As
noted
in item I.A.1, the licensee
has
issued
PC/Ms85-175
and
85-176, to provide enhanced
system operability.
Review of the system
description,
training materials,
drawings,
and
procedures
indicates
setpoint
agreement
with the
PC/M.
AP 0190. 15 assigns
responsibility
for plant design
and control,
and maintenance
of design
documents,
to
the
power plant
engineer.
In addition
to the
requirements
of
0190. 15,
the
1 i cen see
uti l izes
JPE-gI
3. 1,
Contr ol
of
Desi gn
Performed
by JPE,
dated June
23,
1987, to ensure that
PC/Ms generated
by
the
licensee's
Power
Plant
Engineering
Department
adequately
control
the
design
efforts for structures,
systems
and
components
important to nuclear
safety.
This item is closed,
and also closes
part of violation 250,2Sl/86-26-0S.
(Closed)
EA 86-20, I.A.4: Failure to Provide Adequate
Procedures
Inspection
Report
250,251/85-40
delineated
the
failure
by
the
licensee
to
provide
adequate
emergency
operating
procedures.
Specifically,
emergency
operating
procedures
did not give sufficient
guidance
to assure
that the required
AFW flow is supplied to each
unit within three minutes,
in the event of a two unit trip with only
one
AFW pump available.
To resolve this concern,
the licensee
has included specific direction
in 3/4-EOP-ECA 0.0,
Loss of All A.C. Power,
dated April 16,
1987.
A
caution statement
has
been included to direct operations that, in the
event both units require
AFW under natural circulation conditions
and
trai n
1
of
AFW i s
inoperabl e,
within
3
minutes
the
AFW f1 ow
controllers
should
be placed
in manual
and adjusted
to
300
gpm per
unit.
Licensed Operator Instructor
Lesson
Plan
No. 0063-0L, Appendix
00,
ECA 0.0,
dated July 9,
1986, requires
the instructor to discuss
the basis for all cautions
and notes in the procedure.
Additionally,
the
lesson
plan
handouts
provide
an
explanation
of the setpoints
provided in the procedure.
This item is closed,
and also closes part
of violation 250,251/86-26-05.
(Closed)
EA 86-20,
I.A.5: Failure to Provide
Adequate
Procedures
Covering
a Safety Related Activity.
Inspection
Report 250,251/85-40 delineated
a fai lure by the licensee
to provide
adequate
procedures
to cover
safety related activities.
Specifically, procedures
did not specify. local operation of'rain
2
of AFW when 'the main control
room is inaccessible
and only the
B AFW
pump is available.
Additionally, instructions
were not provided
on
how to locally reset
and restart
a tripped
AFW pump.
To
resolve
these
concerns
the
licensee
has
revised
O-ONOP-103,
Control
Room Inaccessibility,
dated July 18,
1987,
to direct local
operation
of the
AFW system,
provide provisions for operation
of
train
1 or
2 of
AFW and
provide
instruction
on
the
process
for
resetting
and
restarting
a
tripped
pump.
Additionally,
Inspection
Report
250,251/87-07
documented
observations
of
a walk
through
of
the
aforementioned
procedure.
Several
areas
of
improvement
were
noted including reset of
a tripped
pump
and
local
operation
of the
AFW system.
This item is closed,
and also
closes part of violation 250,251/86-26-05.
(Closed)
EA 86-20, I.B: Failure to Correctly Translate
Design Inputs
into Plant Drawings.
Inspection
Report 250,251/85-40
documents
the licensee's
failure to
correctly translate
design inputs into plant drawings.
Specifically,
the nitrogen
backup
system
drawings incorrectly identified pressure
control valves
as being set at
55 psig versus
the correct value of 80
psig.
The setpoint
change
was brought about during implementation of
the
PC/M.
To resolve this
concern
the licensee
has
revised
Instrument
Index
Sheet,
5610-M311,
Pressure
Controllers,
dated
September
18,
1986 and
Piping
and Instrument
drawing
5610-M339, Auxiliary Feedwater,
Main
Steam Isolation Valve,
and Pressurizer
Backup
Supply
Systems,
dated April 26,
1988.
These revisions correctly reflect the
value of 80 psig for the nitrogen pressure
control valves.
As noted
in item I.A.3 above,
the
power
plant
engineer
is
responsible
for
plant design
and control,
and the maintenance
of design
documents.
This
item is
closed,
and
also
closes
part
of violation
250,
251/86-26-05.
(Closed)
86-20,
I.C.1-2:
Failure
to
Correctly
Translate
Appropriate Quality Standards
into Procedures
or Drawings.
Inspection
Report 250,251/85-40
delineated
a failure by the licensee
to properly co'ntrol
design
changes
in that required
changes
to the
licensee's Q-list were not completed following completion of a
PC/M.
This error resulted
in components
of the nitrogen backup
system not
being maintained
commensurate
with their function.
To
resolve
this
concern,
the
licensee
has
in
place
Quality
Instruction
JPE-QI
2.7,
Nuclear
Plant Q-List,
dated
November
30,
1987,
which sets
forth the requirements
that the Q-list be revised
for impact from:
(1)
PC/Ms;
(2)
New or revised
drawings
resulting
from plant design
changes,
plant modifications, resolution of nonconformances,
and drawing
discrepancy
resolution;
(3)
Technical Specification
(TS) changes;
and
(4)
Correspondence
between
the licensee
and the
NRC.
Review of the Q-List for'tems85-176
revealed
the
correct
classification.
Purchase
orders
materials
were
purchased
to the
item
is
closed,
and
also
250,251/86-26-05.
associated
with
PC/Ms85-175
and
incorporation
of
the
safety
were also
reviewed to ensure
that
appropriate
classifications.
This
closes
part
of
violation
(Closed)
EA 86-20, I.C.2: Safety Related Application.
Inspection
Report
250,251/85-40
delineated
the
failure
by
the
licensee
to
provide
the
required
protection
against
commo'n
mode
failure for the nitrogen
backup
low pressure
alarm.
To resolve this issue,
the
licensee
has
completed
PC/Ms85-176
and
85-175,
which installed
safety
grade
pressure
switches
along with
supporting
equipment
and
instrumentation.
Review
of
drawing
5610-E-27,
SH.34,
Elementary
Diagram
N2 Backup Supply Stations
1 & 4,
Low Pressure
Alarms, dated January
1,
1988,
and associated
referenced
drawings,
confirmed
the
changes
and the protection
against
common
mode failure for the nitrogen
backup
low pressure
alarm.
This item
is closed,
and also closes part of violation 250,251/86-26-05.
(Closed)
EA 86-20,
I.D.1-4:
Failure to Correctly Translate
Design
Inputs into System Descriptions or Design Basis
Documents.
Inspection
Report
250,251/85-40
documents
the licensee's
failure to
correctly translate
design
inputs into the
system
description
or
design basis
documents.
I
Review of System Description
No. 0709117, Auxiliary Feedwater
System,
dated
April 22,
1988,
reflects
the
correct
incorporation
of the
backup
operating
pressure
of
80 psig,
container
backup
low pressure
alarm setpoint of 650 psig, accurate
description
of the train configuration
and
the
time associated
with operator
action
in order to preclude
loss of the nitrogen
backup.
As noted
above,
the licensee
has
adequate
procedures
in place
to ensure
that
the appropriate
plant documentation
is updated
when
PC/Ms are issued.
This
item is
closed,
and
also
closes
part
of violation
250,
251/86-26-05.
(Closed)
EA 86-20,
I.E:
Failure to Evaluate
the
Impact of Design
Changes
on the
AFW System.
Inspection
Report
250,251/85-40
delineated
the licensee's
failure to
evaluate
the
impact of design
changes
on the nitrogen
consumption
rate
by the
AFW flow control valves
and the time period allowed for
operators
to valve in additional nitrogen bottles.
To
resolve
this
item,
the
licensee
has
developed
operational
surveillance
procedure
3/4-0SP-075.3,
System
Low
Pressure
Alarm Setpoint,
dated
May 5,
1988, 3/4-0SP-075.6,
Auxiliary
Train
1
Backup Nitrogen Test,
dated
March
28,
1988
and
3/4-0SP-075.7,
Train
2
Backup
Nitrogen Test,
dated
March
28,
1988.
These
procedures
provide for the
dynamic
testing
of the nitrogen
consumption
rate
and the low pressure
alarm
setpoint for both trains
1
and
2 of the
AFW backup
system
flow control
valves.
This
item
is
closed,
and
also
closes
part of violation 250,251/86-26-05.
(Closed)
EA 86-20, I.F:
Failure to Adequately
Document Assumptions
and Design Inputs in Calculations for Plant Modifications.
Inspection
Report
250,251/85-40
documents 'the licensee's
failure to
adequately
document
assumptions
and
design
inputs
in calculations
used for plant modifications.
To
resolve
this
item,
the
licensee
has
in
place
Administative
Procedure
JPE-AP3.9,
Calculation Standard
Format, dated
September
10,
1986,
which
requires
that calculation
packages
be
completed
and
assumptions
be
clearly
stated
such
that
no
additional
verbal
explanation
is required,
and that all basic data
and assumptions
be
provided with references
or basic
discussions.
Additionally, the
pagination/revision
scheme
for the calculation
package facilitates
a
cursory review for original order, missing or out of sequence
pages,
and the correct revision of each
page.
This item is closed,
and also
closes part of violation 250,251/86-26-05.
Escalated
Enforcement
Action (EA) 86-20-IV:
Failure to Establish or
Implement Adequate
Procedures,
and to Properly Control the Revision
and Distribution of Safety-Related
Procedures.
This
EA originated
from violation
250,
251/86-26-09,
which
encompassed
previously
identified unresolved
items 250,251/85-40-03,
250,251/85-40-17,
and
250,251/85-40-20.
Status
Item
EA 86-20,
IV.A.1
EA 86-20,
IV.A.2
EA 86-20,
IV.B
closed
closed
cl osed
The basis for closure of each
item is discussed
below.
(Closed)
86-20,
IV.A.1:
Failure
to
Establish
Procedures
Specifying Independent
Verification for Safety Related
Systems.
Inspection
Report
250,251/85-40
delineated
the licensee'
fai lure to
provide
and implement adequate
procedures
to ensure that independent
verification was performed
and documented
on the return to service of
instrumentation vital to the operation of the auxiliary feedwater
and
backup nitrogen
systems.
The licensee
has in place
O-ADM-031, Independent Verification, dated
April
26,
1988,
which
specifies
the
overall
plant
policy for
independent verification and delineates
those safety related
systems
which require
independent
verification,
including
the
AFW system.
This
item is
closed,
and
also
closes
part
of violation
250,
251/86-26-09.
(Cl osed)
EA 86-20,
IV.A.2:
Fai 1 ure
by the
P 1 ant
Nuc1 ear
Sa fety
Committee
to
Review
Nuclear
Safety-Related
Temporary
System
Alterati on s.
Inspection
Report
250,251/85-40
delineated
the
licensee's
Plant
Nuclear Safety Committee'
(PNSC) failure to review Temporary
System
Alterations
(TSAs)
3-84-11-75,
3/4-85-8-75,
3/4-84-99-75,
and
3/4-84-100-75 within fourteen
days of the
Plant
Supervisor-Nuclear
approval date.
The inspector
reviewed current
TSAs to confirm review by the
PNSC
within the required
time frame.
No discrepancies
were identified.
The inspector's
review of O-ADM-503, Control
and
Use of Temporary
System Alterations, dated June 2,
1988,
noted that
TSAs for inservice
equipment
may be installed without prior PNSC approval,
based
on the
determination
by the Shift Technical Advisor and the Plant Supervisor
Nuclear that
the
TSA is identical
or similar to
one previously
installed.
(TSAs installed
under this
method
are still required to
be
reviewed
by
the
PNSC within the
required
time
frame).
The
procedure,
however,
does not provide guidance
on the determination of
identical
or similar.
To rectify this situation,
the licensee
has
committed to remove the possibility of TSA installation
based
on
an
identical
or
similar determination
from the
procedure
currently
10
undergoing
revision.
This item is closed,
and also
closes
part of
viol ati on 250,251/86-26-09.
(Closed)
EA 86-20,
IY.B:
Failure to Ensure that
a Safety-Related
Procedure
was Properly Controlled
Inspection
Report 250,251/85-40
delineated
the licensee'
failure to
ensure
that
a safety-related
procedure
was
approved
for release
by
authorized
personnel
and
appropriately
distributed
prior to
the
cancellation of the previous procedure.
Review of ADM-0109. 1,
Preparation,
Revision,
Approval,
and
Use of
Procedures,
dated
dune
7,
1988,
indicates
that the licensee
has
in
place
adequate
controls
to
ensure
that
related
procedures
and
commitments
are
addressed
prior to the
issuance
of new or revised
procedures.
This item is closed,
and also closes part of violation
250,251/86-26-09.
3.
Followup
on
Unresolved
Items
(URIs),
Inspector
Followup
Items (IFIs),
Inspection
and
Enforcement
(IE)
Information
Notices, IE
Bulletins
(information only), IE Circulars
and
NRC Requests
(92701).
(Cl osed)
IFI
250,251/88-11-03
pertains
to
the
resolution
of
the
differences
in
documentation
associated
with the
ICW
assembly
material.
It has
been
determined
that the
requirements
of
Appendix
B, Criterion III were violated
in that
a
change
to
a design
specification
was
made
without
appropriate
review
and
evaluation.
Corrective action will be tracked
along with violation 250,251/88-14-01,
which is di scussed
in paragraph
5 of this report.
This IFI is closed.
(Closed)
250,251/85-40-29:
Inspector
Concerns
Pertaining
to
the
Sizing of Motor Thermal Overload Relays
(REF. 87-32,
paragraph 5.g).
Inspection
Report
250,251/85-40
delineated
a concern
pertaining to the
apparent
difference
between
the
manufacturer's
recommended
thermal
overload
size
and the size
chosen
by the licensee
to satisfy Regulatory
Guide
1. 106,
Thermal
Overload
Protection
for
Electric
Motors
on
Motor-Operated
Valves.
The licensee's
Power Plant Engineering
group has completed preparation
and
departmental
approval of Standard
No. E-3.20,
Motor Operated
Valve Thermal
Overload
Heater
Relay Selection
Criteria.
The licensee's
integrated
schedule
projects that the review of all safety related
motor operated
valve thermal
overload relays in accordance
with the selection criteria to
will be completed
by November
1988. This review will include the issuance
of the
appropriate
PC/Ms
as
necessary
to correct
design deficiencies.
This item is closed.
(Closed)
IFI
250,251/85-40-38:
Inspector
Concerns
Pertaining
to
Licensee's
Fail
Safe
Testing
of the Auxiliary Feedwater
Flow Control
Valves
(REF. 87-32,
paragraph 5.j).
Inspection
Report 250,251/85-40
delineated
a concern
over the licensee's
method of fail safe testing the
AFW flow control valves.
The
inspector
reviewed
OP
0209.1,
Valve
Exercising
Procedure,
dated
Nay 19,
1988;
3/4-OSP-075. 1,
Auxi 1 iary
Train
1
Oper abi 1 ity
Verification, dated
February
16,
1988;
drawing 5610-T-E-4061,
sheet
4,
Pumps
Steam
Supply
Systems,
dated
November 28,
1987;
and drawing 5610-T-E-4062,
sheet
3,
Steam
Generator Auxiliary Feedwater
Supply Systems,
dated
November 28,
1987;
and confirmed that the
AFW flow
control
valves
are
tested
in
a fail
safe
manner
in accordance
with
licensee
commitments.
This item is closed.
(Cl osed)
250,251/86-18-13:
Inspector
Concerns
Pertaining
to
the
Licensee's
Loss of DC Power Procedure
(REF. 87-32,
paragraph
5.o).
Inspection
Report 250,251/86-18
noted that the licensee's
Phase
I review
identified the absence
of a loss of
DC power procedure.
Additionally, the
Institute of Nuclear
Power Operations
issued Significant Operating
Event
Reports
(SOER)
81-15
and 83-5,
which document
industry events
involving
the failure of various aspects
of a plant's
DC power system.
Currently
the
licensee's
engineering
department
has -forwarded to the
Procedure
Upgrade
Program
(PUP)
group the engineering
evaluation
on the
loss
of
bus
study.
The engineering
study analyzed
the
independent
failure of each vital
DC bus
and
addressed
the
recommendations
of the
The
study
addressed
recommendations
by identifying all
equipment
powered
from each vital
DC bus,
the fai lure
mode
on
a loss of
power,
and analysis
of the
systems
required for safe
shutdown for each
vital
DC bus failure.
The
PUP group will address
the study's findings via the generation
of four
off-normal
operating
procedures,
O-ONOP-003.14,
.15,
.16,
and
.17,
to
fully address
potential
loss of
bus
scenarios.
Issuance
of these
procedures
is scheduled for October
1988. This item is closed.
(Open)
IFI 250,251/87-07-03:
Generation
of Electrical
Breaker Setpoint
Document
(REF. 87-32,
paragraph
5.u)
Inspection
Report
250,251/87-07
documents
the
l icensee'
request
for
engineering
assistance
for the
development
and
issuance
of
a breaker
setpoint document.
This item was
issued
in conjunction with the closure
of URI 86-37-01
and IFI 85-22-11,
which pertained to the establishment
of
DC feedbreaker
and inverter input breaker trip setpoint
settings'he
licensee's
integrated
schedule
currently projects modification 0618,
Add to Breaker List Breaker Trip Setpoints,
to start in June
1989 with
completion for December
1989.
An additional
aspect
of the
licensee's
electrical coordination documentation
includes modification 1254,
Add Fuse
Specifications
to Breaker List and Drawings,
scheduled
to start
in June
1989
and be completed in January
1990.
12
This item will remain
open
pending completion of a breaker trip setpoint
and fuse specification
document.
Monthly and Annual Surveillance
Observation
(61726/61700)
The
inspectors
. observed
TS required
surveillance
testing
and verified:
that
the test
procedure
conformed to the requirements
of the
TS; that
testing
was
performed
in accordance
with adequate
procedures;
that test
instrumentation
was calibrated;
that limiting conditions for operation
(LCO) were met; that test results
met acceptance
criteria requirements
and
were
reviewed
by personnel
other than the individual directing the test;
that deficiencies
were identified,
as
appropriate,
and
were
properly
reviewed
and resolved
by management
personnel;
and that system restoration
was adequate.
For completed tests,
the inspectors
verified that testing
frequencies
were met and tests
were performed by qualified individuals.
The
inspections
witnessed/reviewed
portions
of
the
following test
activities:
4-SMI-041. 16
TAVG/Delta T Protection
Channels
Periodic Test
4-0SP-072.2
Main
Steam
Isolation
Valve
Backup
Periodic Test
No violations/deviations
were identified in the areas
inspected.
Maintenance
Observations
(62703/62700)
Station
mainten'ance
activities of safety related
systems
and
components
were
observed
and
reviewed
to ascertain
that
they
were
conducted
in
accordance
with approved
procedures,
regulatory guides,
industry codes
and
standards,
and in conformance with TS.
The following items
were considered
during this review,
as appropriate:
That
LCOs were met while components
or systems
were
removed
from service;
that approvals
were obtained prior to initiating work; that activities
were
accomplished
using
approved
procedures
and
were
inspected
as
applicable;
that procedures
used
were
adequate
to control the activity;
that
troubleshooting
activities
were
controlled
and
repair
records
accurately
reflected
the maintenance
performed; that functional testing
and/or
calibrations
were
performed
prior to returning
components
or
systems
to service; that
QC records
were maintained; that activities were
accomplished
by qualified personnel;
that parts
and materials
used
were
properly certified; that radiological controls were properly implemented;
that
QC hold points
were established
and
observed,
where required; that
fire prevention controls
were
implemented;. that outside
contractor
force
activities were controlled in accordance
with the approved
QA program;
and
that housekeeping
was actively pursued.
13
The
inspectors
witnessed/reviewed
portions of the following maintenance
activities in progress:
Repairs to
ICW Pump
3A and
3C Discharge
Pressure
Gauge Fittings.
Troubleshooting
Unit 3 Rod Position Indicator Alternate
Power Supply
Breaker
(LP 317-18).
Troubleshooting Unit 3,
3B Main Steam Isolation Valve Nitrogen Backup
Regulator Failure.
a.
ICW Pipe Fitting Design
Change
IFI 250,251/88-11-03,
identified conflicting requirements
in licensee
design specifications for ICW gauge
assembly fittings. The licensee's
original
and current design specifications,
5610-M-50 and 5177-PS-11,
require the
use of stainless
steel fittings for ICW gauge
assemblies.
However,
Non-conformance
Report
dated
March 5,
1986,
was
issued
to document
the
use of nonconforming
ICW pump discharge
pressure
and
piping.
Attachment
D to
the
NCR,
drawing
5610-J-155-P10,
note
12, allowed the
use of carbon
steel
for piping
between
the
root valve
and
the
main
for gauge
PI-3-1452.
Discussions with the licensee
indicated that the drawing in the
documented
the "as-found" condition of the
ICW gauges
and associated
piping,
and
erroneously
allowed
the
use
of carbon
steel
in this
portion of the system.
In addition,
the licensee
could not determine
when
the
nonconforming
material
was
installed
or
whether
any
engineering
evaluation
occurred prior to the material substitution.
10 CFR 50, 'Appendix B, Criterion III, as
implemented
by the approved
Power
and
Light
Company
Topical
Quality Assurance
Report
(FPLTQAR) 1-76A, Revision
11, Topical Quality Requirement
(TQR) 3.0,
Revision 5, requires that design
changes
be subject to design control
measures
commensurate
with those applied to the original design,
and
that these
design control measures
assure
that applicable
regulatory
requirements
and
the
design
basis
are correctly translated
into
specifications,
drawings,
procedures
and instructions.
FPLTQAR 1-76A,
Appendix
C,
Revision
7 specifically
commits,
with
exceptions
not
relevant
here,
to
American
National
Standards
Institute
(ANSI) N45.2. 11-1974,
Quality Assurance
Requirements
for
the
Design of Nuclear
Power Plants,
and to Regulatory
Guide 1.64,
Revision 2, Quality Assurance
Requirements
for the Design of Nuclear
Power Plants,
which endorses
specifies that
documented
procedures
shall
be
provided
for design
changes
to approved
design
documents
which assure
that the impact of
the change is carefully considered,
required actions
documented,
and
information
concerning
the
change
is transmitted
to all affected
persons
and
organizations.
These
changes
must
be justified
and
subjected
to control measures
commensurate
with those applied to the
original design.
14
Contrary to the above,
on March 5,
1986,
a change
was
made to the
ICW
design
specifications
through
the
resolution
of
non-conformance
report 86-112,
attachment
D, drawing
5610-J-155-P10,
note
12,
which
allowed the
use of carbon
steel
pipe fitting between
the root valve
and
the
main
for pressure
PI-3-1452.
The
increased
susceptibility of the
steel
to .corrosion
was
not carefully
considered
or
justified
through
an
engineering
evaluation.
Subsequently,
on April 27,
1988,
the fitting failed due to salt water
induced
corrosive
wear.
This resulted
in the
3A
ICW
pump
being
placed
out of service.
The failure to
meet
the
requirements
of
10 CFR 50, Appendix
B is
a violation (250,251/88-14-01).
b.
Rod Position Indication (RPI) Alternate
Power Supply Breaker Sizing
'I
~
I
On June
17,
1988,
at
1446, with Unit 3 at
100% power,
the breaker
supplying alternate
power to the
RPI circuitry tripped,
causing
a
loss of all
RPI for the unit.
The licensee
was performing Section
6. 5 of
3-PMI-028. 2,
Axial
Flux
Rod
Deviation
and
Rod
Position
Indication Monthly Test,
which allows power to the
RPI to be shifted
to the alternate
power
supply in lieu of the
RPI inverter.
After the
alternate
power
supply
was lost,
power
was
restored
to the
circuitry through the normal inverter.
This situation again occurred
at
0125
on
June
19,
1988,
when
the
procedure
was reinitiated
to
complete the testing.
The breaker
was reclosed
and the procedure
was
completed satisfactorily.
Troubleshooting
was initiated to determine
the
cause
of the
inadvertent
tripping of the
RPI alternate
power
supply breaker
(BKR LP 317-18).
Initial inspection
revealed that the
breaker
was
rated
at
20
amperes
and
load for the circuit was
approximately
21-22
amperes.
PC/M 82-121,
which installed
the
alternate
power supply,
indicated that the breaker
had
a
30
ampere
rating.
The licensee
obtained
a gL-1 replacement
breaker,
rated at
30 amperes,
and installed it in BKR LP 317 at position
18.
Initial
indication was that
PC/M 82-121
may have
been
inadequate
in that it
did not require replacing
the existing
20
ampere
breaker with the
required
30 ampere
breaker.
However, the inspectors
and the licensee
are still researching
the issue.
It will be addressed
in the next
report.
This issue is identified as
an inspector followup item (IFI
250,251/88-14-02).
6.
Operati ona1
Safety Verificati on (71707)
~
~
The inspectors
observed control
room operations,
reviewed applicable logs,
conducted
discussions
with control
room
operators,
observed
shift
turnovers
and
confirmed operability of instrumentation.
The inspectors
verified the operability of selected
emergency
systems,
verified that
maintenance
work orders
had
been
submitted
as required
and that followup
and prioritization of work was
accomplished.
The
inspectors
reviewed
tagout
records,
verified compliance with TS
LCOs and verified the return
to service of affected
components.
15
By observation
and direct interviews,
verification
was
made
that
the
physical security plan was being implemented.
Plant
housekeeping/cleanliness
conditions
and
implementation
of
radiological controls were observed.
Tours of the intake structure
and diesel, auxiliary, control
and turbine
buildings were
conducted
to observe
plant equipment conditions including
potential fire hazards,
fluid leaks
and excessive
vibrations.
The
inspectors
walked
down accessible
portions of the following safety
related
systems
to verify operability
and proper valve/switch alignment:
A and
Control
Room Vertical Panels
and Safeguards
Racks
Intake Cooling Water Structure
4160 Volt Buses
and
480 Volt Load and Motor Control Centers
Unit 3 and
Platforms
Unit 3 and
4 Condensate
Storage
Tank Area
Area
Unit 3 and
4 Main Steam Platforms
No violations/deviations
were identified in the areas
inspected.
~
~
7.
Physical Security (71881)
Station security activities were observed
during this inspection period to
ascertain
that
they
were
conducted
in
compliance
with the
approved
Physical
Security Plan
(PSP).
The following attributes
were
considered
during these
observations,
as
appropriate:
that the minimum number of armed guards is
on site for each
shift; that
search
equipment
such
as x-ray machines,
metal detectors
and
explosives detectors
are operational;
that the protected
area
(PA) barrier
is well maintained
and is not compromised
by erosion,
opening in the fence
or walls, or proximity of vehicles or other objects that could be used to
scale
the barrier;
that illumination in the
PA is
adequate
to allow
patrolling guards
to observe
the
area
at night
and
permit the
use
of
closed circuit monitor s by alarm station
operators;
that the vital area
(VA) barriers
are well maintained;
that persons
granted
access
to the site
are
badged
to indicate whether
they
have
unescorted
or escorted
access
authorization; that there are
no obstructions
in the isolation
zone that
could
conceal
an
individual
attempting
an
unauthorized
entry
or
interference
with the detection/assessment
system;
and that
when
search
equipment
or alarm
systems
are inoperable,
or when there is
a breach of
the
PA or
VA barrier,
the licensee
implements
appropriate
compensatory
measures.
No violations/deviations
were identified in the areas
inspected.
16
8.
Reactor
Vessel
Pressure
Transient Protection (TI 2500/19)
The
purpose
of this
inspection
was
to verify that
the
licensee
has
implemented
commitments contained
in correspondence
related
to Unresolved
Safety
Issue
A-26,
and the
safety evaluation
reports
concerning
reactor
vessel
pressure
transient protection.
The
items to
be verified have
been divided into several
areas:
design;
administrative
controls
and
procedures;
training
and
equipment
modification; and surveillance;
and are discussed
below.
a
~
Design
PC/M
75-81,
entitled Nil Ductility Transition
Temperature
(NDTT)
Contr ol,
was
impl emented
on January
6,
1978 for Unit
3
and
on
November
9,
1977 for Unit
4.
This
PC/M modified
PORV control
circuits to provide low pressure relief settings.
The setpoint of 415
psig for low temperature
operation
(below 300F)
is designed to
keep
the primary loop pressure
below the Appendix
G limits.
The following
PC/Ms were
subsequently
implemented
to
meet
the additional
design
requi rements:
PC/M 78-27,28,
Overpressure
Mitigation System
(OMS)
Permissive
Status
Panel
Light
and
Interlocks;
PC/M
78-16,17,
Pressurizer
PORV's
Backup
N-2 Supply;
and
PC/M 78-23,24,
OMS Test Switch and Relabel
OMS Components.
These
modifications
are
discussed
further in the following sections.
The pressurizer
are
spring-loaded-closed.
Air is required to
open the valves
and is supplied
by instrument air.
In the event of a
loss of instrument air,
a
backup
(N-2) system is provided
which will supply
enough
N-2 for
a
minimum of ten
minutes
of
operation.
Drawing 5610-M-339
shows
the
N-2 backup
system provided
for each
PORV.
Each
PORV has
two redundant
solenoid valves which are
energized
in order to
open
the
These
solenoid
valves fail
closed
on
a loss of power.
However,
each solenoid is powered off the
125 volt vital
DC supply.
Therefore
on
a loss of offsite power, the
station batteries will be available to allow the operation
of the
PORV.
Drawing 5610-E-25,
sheet
64,
shows
the wiring configuration
and power supply for the
There are two PORVs
and their associated
block valves which are
shown
on drawing 5610-T-E-4501.
If one
PORV is inoperable,
the remaining
PORV is capable of relieving the
RCS to prevent exceeding
Appendix
G
limits. If the
PORV fails in the
open position, its associated
block
valve
can
be closed to isolate
the
PORV to terminate
the pressure
Drawings
5610-E-855
and
5610-E-25,
sheet
27,
show the
wiring configuration
for
the
motor
operated
block
valve.
By
referencing
the breaker list, the inspector verified that the block
valves
were
powered
from
a separate
vital power source.
The block
valves
are
powered
from the vital portion of the
3B and
4B motor
control
centers
(MCC) for Unit
3
and
4 respectively.
Each
block
valve fails
as is.
The failure of one block valve will not affect
17
the operability of the associated
PORV, therefore it would not create
a pressure
Each
PORV is opened
by the energization
of two solenoid valves which
realign to allow instrument air or N-2 to flow to the
PORV actuator.
These
solenoids
are
redundant
such
that
the fai lure of
one will
prevent the
PORV from opening.
If the
PORV was
open
and the solenoid
valve failed,
the
PORV would fail closed.
However,
the remaining
PORV would not be affected
and could be used to mitigate the pressure
Drawing 5610-T-D-16A shows the control
system for the
OMS.
Each
has
its
own
switch
installed
on
the
main
control
board.
The
operator
can enable/disable
the
OMS by selecting
"LO Pressure
OPS" or
"Normal
OPS",
respectively.
The
setpoint
pressure
and
actual
pressure
are
derived
from
redundant
temperature
and
pressure
transmitters.
456,
which is the
primary
OMS channel,
uses
temperature
element
(TE)
430B
and
pressure
transmitter
(PT)
403.
PORV 455C, the backup
OMS channel,
uses
TE-423B and PT-405.
The
licensee's
Appendix
G curve
used
for overpressure
analysis
shows the limit at 100F to be
510 psig.
In conjunction with
the Nuclear
Steam Supply
System
vendor,
the
PORV setpoint
overshoot
was determined
to
be
78 psig.
With
a relief setpoint of 415 psig,
the final pressure
of 493 psig is reached
for the worst
case
mass,
input transient.
This setpoint is acceptable
since it will keep the
pressure
below the Appendix
G limit of 510 psig.
The limiting heat
input cases
calculations
also
show
a maximum pressure
below
that allowed by Appendix
G limits.
The inspector
reviewed
the licensee's
safety evaluations
which were
completed for each
PC/M associated
with the
OMS.
All the information
was complete.
Administrative Control
and Procedures.
No procedure exists to specifically minimize the time the reactor is
in a water-solid condition.
However,
when operating
in a water-solid
condition,
precautions
are
taken to minimize the possibility of
a
pressure
some of which are discussed
below.
To minimize the possibility of
a
pressure
while in
a
water-solid condition, Operating
Procedure
OP-041.1, entitled Reactor
Coolant
Pump,
specifies
that
when the
RCS is solid,
a
RCP shall not
be started if the
steam
generator
blowdown temperature
exceeds
the
RCS temperature
by 10F.
This will prevent the Appendix
G limits for
the heat input case
from being exceeded.
General
Operation
Procedure
(GOP) 305, entitled
Hot Standby to Cold
Shutdown,
contains
instructions
to isolate
the hot leg and cold leg
safety
injection
valves
prior to
cooling
the
below
380F.
18
Attachment
1 to this procedure
also requires
the operators
to sign
off that the safety injection valves
are
closed
and their breakers
are locked open,
and to isolate the pressurizer
heaters
to reduce
the
possibility of a pressure
The operators
are alerted
to the automatic
operation
of the
OMS by
provided
on vertical
panel
A in the control
room.
In
response
to the annunciators,
the operators
refer to
ONOP
0208.3,
entitled Annunciator List - Panel
A, Reactor Coolant.
GOP 305,
step
5. 11, directs the operator to establish
and verify OMS
operation.
This is accomplished
by performing OP-041.4,
Overpressure
Mitigation
System.
Section
5. 1
of this
procedure
contains
the
instructions for verifying the
OMS setpoint
and that the
open
as indicated
on the appropriate
305,
Attachment
1, lists the
components
for the cold
shutdown
clearance
tagging
requirements.
The
inspectors
reviewed
selected
completed
procedures
to verify that the
attachment
was being signed
off as complete
as the units were brought to cold shutdown.
503,
step
5. 16,
has
the
operators
align the
OMS for normal
pressure
operation
per
entitled
Pressurizer
Operation.
Section
5.2
of thi s
procedure
contains
the
steps
necessary
to
transfer the
OMS to normal operation.
GOP 305,
step 5.12.1,
specifies that if a pressurizer
bubble is to be
maintained,
the pressurizer
heaters
and/or sprays
are to
be
used to
maintain pressurizer
pressure
in the range of 325 to 375 psig.
There
are
no specific procedures
for performing this evolution.
Tut key
Point
TS,
Section
3. 15,
specifies
that
with
the
temperature
less
than or equal
to
275F with
RCS pressure
boundary
integrity established,
two
PORVs shall
be operable with a setpoint of
415 psig k 15 psig.
The inspectors verified that the plant installed
system,
along with the
appropriate
procedural
guidance,
exist to
ensure that the
TS requirements
are being followed.
Training and Equipment Modifications,
The inspectors
reviewed
Lesson
Plan
No. 6902009, entitled Pressurizer
and Relief System.
This training is designed
for licensed
operator
candidates,
and contains
a description of the
OMS and the operational
characteristics.
The license
candidates
must
also
perform various
evolutions
under
the
guidance
of
a
licensed
operator.
These
evolutions include testing of the
OMS and aligning the
OMS for normal
and low pressure
operations.
The inspectors
also questioned
selected
RCOs
concerning
the
operation
of the
and
the
causes
and
prevention of pressure
All of the operators
interviewed
were knowledgeable
of the
OMS operation
and the necessary
precautions
to be taken to prevent pressure
19
Turkey Point Administrative Procedure
(AP), 0190.15 entitled Plant
Changes/Modifications
(PC/M), is used to control the review, approval
and
implementation
of PC/Ms.
Section
8. 1 contains
instructions for
the
preparation
of the
PC/M which
includes
preparing
a
safety
evaluation
report
in accordance
with
to
review
any
unreviewed
safety
questions.
This
procedure
also
requires
the
Startup
Department
to perform functional
tests
after
the
PC/M is
completed.
AP 0190.22,
entitled
Changes,
Tests
and
Experiments,
provides
guidance for preparation
of the safety evaluation
report.
These
admini strative controls provide
an effective method to resolve
any unresolved
safety issue during any
PC/M,
and also to ensure that
functional testing is performed after completion of the modification.
In the
example
given for the modifications of the solenoid
valves,
the
PC/N would be developed
and the post modification testing
would
be
performed
under
the administrative
controls to ensure
that the
equipment
is still in its design
basis.
If maintenance
were to
be
performed
on
the
sol enoi d
val ves,
0190. 28,
enti tled
Post
Maintenance
Testing,
would govern.
Appendix
E to this
procedure
provides specific guidance for post-maintenance
test requirements
for
This will also ensure that the design basis of the
system is being maintained.
Drawing
5610-T-D-16B
shows
the
provided for the
ONS.
The
has
an annunciator
that will alert
the
operator
that
pressure
is approaching
the
OMS setpoint.
This will alarm at
400
.
psig
when the
OMS mode switch is in low pressure
operations
and
the
PORV control switch is in automatic.
The
inspectors
reviewed
the initial test
data
obtained
after the
installation of the
backup
N-2 system
under
PC/M 78-16
and 78-17.
This
data
indicates
that
the
system
design
allows the
PORV to
be
opened
for
at
least
ten
minutes
using
the
backup
N-2
system.
entitled
Overpressure
Mitigating System
Backup
Leak and Functional Test, is performed periodically to ensure
the N-2
Backup System
can perform its intended function.
Surveillance
The
PORV electronics
and setpoints
are verified each time before the
OMS is aligned for low pressure
operations
per
entitled
Overpressure
Mitigation System.
The inspectors
reviewed the stroke
times for the Units 3
and
4
PORVs dating
from May 1984 through
May
1988.
These tests
were
performed in accordance
with the licensee's
Inservice Test (IST) Program.
The
IST requirement
for each
PORV is
to fully stroke
within
15
seconds.
The
stroke -times
reviewed
indicate
an average
opening time as fol.lows:
20
Valve
seconds
PCV"3-456
PCV-3"455C
PCV-4-456
PCV-4-455C
4.25
3.67
2.76
2. 41.
These
average
stroke
times
are
well
below
the
15
second
criterion.
However,
in an
NRC safety evaluation report
(SER) issued
on March 14,
1980,
supporting license
amendment
numbers
55/47 for the
OMS,
a relief valve
opening
time of 2.0
seconds
was
assumed
in
calculating the setpoint overshoot for the mass input case.
The heat
input case
assumed
a relief valve opening time of three
seconds.
The
on the average,
are not meeting the design
basis
indicated
in the
~
This discrepancy
is being
reviewed
by the
licensee
and will be tracked
as IFI 250, 251/88-14-03.
e.
Summary.
The inspectors
completed
a review of the
OMS design
and installation
for Turkey Point Units
3 5 4.
TI 2500/19 is closed.
However,
as
described
in paragraph
8.d.
above,
the
adequacy
of
PORV stroke
time
testing
remains
a
followup
item
pending
further
review
and
evaluation.
No violations/deviations
were identified in the areas
inspected.
9.
Plant Events
(93702)
The following plant events
were reviewed to determine facility status
and
the
need for further
followup action.
Plant
parameters
were evaluated
during transient
response.
The significance of the event
was evaluated
along with the
performance
of the
appropriate
safety
systems
and
the
actions
taken
by the
licensee.
The
inspectors
verified that
required
notifications were
made to the
NRC.
Evaluations
were performed relative
to the
need for additional
NRC response
to the event.
Additionally, the
following issues
were
examined,
as
appropriate:
details
regarding
the
cause of the event;
event chronology; safety
system performance;
licensee
compliance
with approved
procedures;
radiological
consequences,
if any;
and
proposed
corrective actions.
The licensee
plans
to
issue
Licensee
Event Reports
(LERs)
on
each
event within 30 days following the date of
occurrence.
On June
15,
1988, at 0835, with Unit 3 at
100% power,
excessive
noise
and
high bearing temperatures
were noted from the main generator air side seal
oil pump.
Unit power
was
reduced
to about
95% and the subject
pump
was
replaced.
The unit was returned to
100% power at 1600
on the
same day.
On June
15,
1988,
at
1654, with both units at
100% power,
the licensee
reported
a significant event in that the
Emergency
Notification System
(ENS)
phone
was
out of service.
The licensee
contacted
the telephone
21
company to effect repairs
and the
ENS phone
was placed
back in service
on
June
16,
1988, at 1520.
Exit Interview
The
inspection
scope
and
findings
were
summarized
during
management
interviews held throughout the reporting period with the Plant Manager
Nuclear
and selected
members of his staff.
An exit meeting
was conducted
on June
29,
1988.
The areas
requiring management
attention
were reviewed.
No proprietary
information
was
provided
to the
inspectors
during
the
reporting period.
Item Number
Descri tion and
Reference'50,
251/88-14-01
250,
251/88-14-02
Violation - Failure to control materials
used in
safety related
systems,
paragraph
5.
IFI - Evaluate
the
root
cause
of using
a
20
ampere
breaker instead of the required
30
ampere
breaker
in the alternate
power supply to the
system,
paragraph
5.
250,
251/88-14-03
IFI
Evaluate
the
basis
for selecting
maximum
stroke times for the
paragraph
8.
Acronyms and Abbreviations
ADM
a.m.
ANSI
CFR
FPLTQAR
gpm
ICW
IFI
LCO
LER
Administrative
ante meridiem
American National Standards
Institute
Administrative Procedures
Code of Federal
Regulations
Escalated
Enforcement Action
Emergency
Contingency Action
Emergency Notification System
Emergency Operating
Procedures
Florida Power
8 Light
Florida Power
8 Light Company Topical
Final Safety Analysis Report
General
Operating
Procedure
gallons per minute
Intake Cooling Water
Inspection
and Enforcement
Inspector
Followup Item
Inservice Test
Limiting Condition for Operation
Licensee
Event Report
Motor Control Center
Motor Operated
Valve
Quality Assurance
Report
22
NRC
N-2
ONOP
PC/M
p.m.
PNSC
Psi9
PUP
RCO
TQR
TS
Non-conformance
Report
Nil Ductility Transition Temperature
Nuclear
Regulatory
Commission
Overpressure
Mitigation System
Off Normal Operating
Procedure
Protected
Area
Plant
Change Modification
post meridiem
Plant Nuclear Safety Committee
Power Operated Relief Valve
pounds per square
inch gage
Physical
Security Plan
Procedure
Upgrade
Program
Quality Assurance
Quality Control
Reactor Control Operator
Rod Position Indicator
Safety Evaluation
Report
Significant Operating
Event Report
Senior Reactor Operator
Temperature
Element
Topical Quality Requirement
Technical Specification
Temporary
System Alterations
Unresolved
Item
Vital Area
0