ML17345A289

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Insp Repts 50-250/88-11 & 50-251/88-11 on 880425-0603. Violation Noted:Fuel Oil Suction Valve Closed.Major Areas Inspected:Annual & Monthly Surveillance,Maint Observations & Operational Safety
ML17345A289
Person / Time
Site: Turkey Point  
Issue date: 06/29/1988
From: Brewer D, Crlenjak R, Mcelhinney T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17345A288 List:
References
50-250-88-11, 50-251-88-11, NUDOCS 8807260336
Download: ML17345A289 (32)


See also: IR 05000250/1988011

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-250/88-11

and 50-251/88-11

Licensee:

Florida Power and Light Company

9250 West Flagl er Street

Miami, FL

'33102

Docket Nos.:

50-250

and

50.-251

Facility Name:

Turkey Point

3 and

4

License

No s.:

DPR-31

and

DP R-41

0

Inspection

Conducted'.

April 25,

1988 through June

3,

1988

Inspectors:

D.

R. Brewer, Senior Resident

I

pector

T.

F. McElh'qney, Resident

Inspe tor

r

G.

A

chne li, Resident

Inspector

Approved by:

V.

C len

, Secti

n Chief

Division o

Reactor Projects

Date

igned

Date Signed

6

D te Signed

Date Signed

SUMMARY

Scope:

This routine,

unannounced

inspection

entailed direct inspection

at

the site,

including backshift

inspection,

in the

areas

of annual

and

monthly

surveillance,

maintenance

observations

and

reviews,

engineered

safety

features,

operational

safety, facility modifica-

tions, plant physical

security

and plant events.

0

Results:

One

violation

of

TS 6.8. 1

was

identified.

Failure

to follow

procedure,

in that Diesel

Fuels Oil Tank suction valve 003 was found

locked closed

when required to be locked open,

(50-250,251/88-11-02)

(paragraph

6).

One

Unresolved

Item

was

identified,

Evaluate

licensee's

method of testing

check valves to meet the requirements

of

ASME Boile~

and

Pressure

Vessel

Code,

Section

XI, (50-250,251/88-

11-01)

(paragraph

3).

One Inspector

Followup Item was identified,

Resolution of the differences

in documentation

associated

with the

Intake

Cooling

Water

gauge

assembly's

materials,

(50-250,251/88-

11-03) (paragraph

9).

SB072*0336 880707

PDR

ADOCK 05000250

6

PNU'

REPORT DETAILS

Persons

Contacted

Licensee

Employees

F

AJ

T

J

D

J

  • R.

R.

"R.

RG

S.

  • J

AE

AG

~R.

J.

Dager,

Vice President

S.

Odom, Site Vice President

E. Cross,

Plant Manager-Nuclear

J.

Baker, Plant Manager-Nuclear

(Acting)

W. Pearce,

Operations

Superintendent

H. Southworth,

Technical

Department

Supervisor

W. Kappes,

Maintenance

Superintendent

A. Finn, Training Supervisor

D. Webb, Operations - Maintenance

Coordinator

Tomaszewski,

Instrument

and Control

(18C) Department

Supervisor

C. Strong,

Mechanical

Maintenance

Department

Supervisor

W. Bladow, Quality Assurance

(QA) Superintendent

J. Earl, Quality Control

(QC) Supervisor

A. Abrishami,

System

Performance

Supervisor

.G.

Mende, Operations

Supervisor

Arias, Regulation

and Compliance Supervisor

D. Hart, Licensing Engineer

Salamon,

Regulation

and Compliance

Engineer

Hale, Engineering Project Supervisor

Abbatiello,

QA Performance

Monitoring Supervisor

D. Evans,

Document Control Supervisor

A. Suarez,'echnical

Department

Engineer

M. Smith, Services

Manager-Nuclear

L. Fritchley, Assistant Training Supervisor

Other licensee

employees

contacted

included construction

craftsmen,

engineers,

technicians,

operators,

mechanics,

and electricians.

"Attended exit interview on June 8,

1988.

Note:

An alphabetical

tabulation of acronyms

used in this report is

listed in paragraph

12.

Unresolved

Items (URI)

Unresolved

items

are

matters

about

which

more

information is required

to determine

whether

they are acceptable

or

may

involve violations of

requirements

or deviations

from commitments.

One

unresolved

item

was

identified in this report;

"Evaluate

licensee's

method of testing

check

valves to meet

the requirements

of ASME Code,

Section

XI" (URI 250,251/

88-11-Ol)(paragraph

3) .

3.

Monthly and Annual Surveillance

Observation

(61726/61700)

The

inspectors

observed

TS required

surveillance

testing

and verified

that:

the test procedure

conformed to the requirements

of the

TS, testing

was performed in accordance

with adequate

procedures,

that test instrumen-

tation

was calibrated,

Limiting Conditions for Operation

( LCO) were met,

test results

met acceptance

criteria requirements

and

were

reviewed

by

personnel

other than

th'e "individual 'directing the test, deficiencies

were

identified,

as appropriate,

and were. properly

reviewed

and

resolved

by

management

and

system restoration

was adequate.

For completed tests,

the

inspectors

verified that testing

frequencies

were

met

and

tests

were

performed

by qualified individuals.

The

inspectors

witnessed/reviewed

portions

of

the

following test

activities:

4-0SP-041.18

3-OSP-049.

1

O-OSP-023.1

O-OSP-022.5

3" PMI-071.1,

2,3,4

Reactor Coolant System

Pressure

Boundry Check Valves

Leak Test,

Reactor Protection

System

Logic Test,

"A" Diesel Generator Operability Test,

Emergency Diesel

Generators

Starting Air Valves

Operability Test,

and

Steam Generator

Level Protection

Instrumentation

Channel Calibration.

On

May 25,

1988,

while operating

in mode 3, the licensee

declared Unit 4

Reactor

Coolant

System

(RCS)

pressure

boundary

isolation

check

valves

4-876

A,

B

and

C out of service

because

leakage

tests

performed

as

required

by

TS

3. 16 indicated

the potential for leakage 'greater

than 5.0

gallons

per

minute

(gpm).

On

two

occasions,

surveillance

procedure

4-OSP-041. 18,

entitled

RCS

Pressure

Boundary

Check

Valves

Leak Test,

revision dated

May 12,

1988,

had

been

unsuccessfully

implemented.

The

observed

discrepancy

included

an inability to establish

a differential

pressure

(dp) across

the check valve seating

surface.

This condition

was

thought to be indicative of a leaking valve.

The decision to declare

the

valves

out of service

was

made

by the Plant Supervisor-Nuclear

and

was

conservative.

After six hours;

a cooldown

was initiated in accordance

with TS 3. 16.4.

Since this shutdown

was required

by the

TS,

a Notice of

Unusual

Event was

made

as required

by 10 CFR 50.72(b)( 1)(i)(A).

Three explanations

existed for the

observed inability to establish

a

dp

across

the check valves.

- A check valve could

be

damaged,

a check valve

could

be stuck

open or the valve design could require

a significant drop

in

upstream

pressure

to terminate

leakage

by firmly compressing

the

seating

surfaces.

The. licensee

staff

favored

the latter possibility

because

procedure

4-OSP-041. 18

had

previously

been

implemented

without

incident

but

had

recently

been

rewritten

to

use

a

slower

method

of

upstream

depressurization.

The initial

use

of the rewritten

procedure

failed to establish

a differential pressure.-

Consequently,

the procedure

twas

revised to utilize

a larger depressurization'rain

path.

However,

prior to

implementing

the

revised

procedure it was

noted

that

a

dp

developed

across

the valve,

apparently

without the

use

of

any depres-

surization

technique.

Leak tightness

checks

were successfully

completed

and

the unit was

returned

to

power

on

May 28,

1988.

The satisfactory

leakage

rates verified that

no check valve seat

was damaged.

The licensee

did not 'evaluate

how the 'check valves

became firmly seated.

Consequently,

the

NRC inspectors

questioned

whether

the observed

phenomenon

was due to

valve design

or valve binding.

On June

7,

1988,

valve vendor

represen-

tatives

confirmed

that

seat

dp

design

could

have

precluded

initial

attempts to establish

dp across

the valves.

On that date,

the

power level

of the

reactor

precluded

additional

testing

to determine

whether valve

binding

had existed.

Clearly,

any binding that

may

have

occurred

must

have

been

minor because

the valves

were

observed

to seat without overt

operator

action.

Nevertheless,

the

inspectors

conducted

a

review of

previous

check valve stroke tests

to verify that valve binding was not

a

significant concern.

Check valves

4-876 A,

B and

C are required to be tested

in accordance

with

the American Society of Mechanical

Engineers

(ASME) Boiler and

Pressure

Vessel

Code,

Section XI, Division 1, Subsection

IWV, 1980, Edition through

Winter

1981 Addenda;

IWV-3520, Tests for Check Valves.

The code requires

that

check valves

be exercised

at least

every

three

months,

except

as

provided

by IWV-3522, Exercising Procedure.

IWV-3522 specifies,

in part,

that:

Check valves

shall

be exercised

to the position required to fulfill

their function unless

such operation

is not practical

during plant

operation.

If only limited operation

is practical,

during plant

operation

the check valve shall

be part-stroke

exercised

during plant

operation

and full-stroke exercised

during cold

shutdown.

Valves

that cannot bemxercised

during plant operation

shall

be specifically

identified by the

Owner

and shall

be full-stroke exercised

during

cold shutdowns,

Full-stroke exerci sing during cold shutdowns

for all

valves not full-stroke exercised

during plant operation

shall

be

on

a

frequency

determined

by the intervals

between

shutdowns

as follows:

for intervals

of three

months

or

longer,

exercise

during

each

shutdown;

for -intervals

of

less

than

three

months,

full-stroke

exercise

is not required

unless

three

months

have

passed

since

the

last

shutdown axercise.

Additionally, for normally closed

check valves

such

as 4-876 A,

B and

C,

IWY-3522 specifies,

in part, that:

Valves that

are

normally closed

during plant

operation

and

whose

function is to

open

on reversal

of pressure

differential shall

be

tested

by proving that the disk moves

promptly

away

from the

seat

when

the closing pressure

di-fferential'is

removed

and flow through

the valve is. initiated, or when

a mechanical

opening force is applied

to the disk.

Confirmation that the disk moves

away

from the

seat

shall

be by visual observation,

by electrical

signal initiated by

a

position indicating device,

by observation of substantially

free flow

through the valve

as indicated

by appropriate

pressure

indications in

the

system,

or by other positive means.

This test:may

be

made with

or without flow through the va'lve.

Check valves

4-876A,

B and

C are tested

in accordance

with Appendix

B of

Operating

Procedure

(OP)

0209. 1, entitled

Valve Exercising

Procedure,

revision dated

Nay 19,

1988.

An Inservice

Test

(IST) relief request

has

been filed with the

Commission,

in accordance

with

10 CFR 50.55a,

to

require valve testing during cold

shutdown

conditions

rather

than during

normal

operations

The valves

can

not

be tested

during

normal

operation

because

the

Residual

Heat

Removal

(RHR)

pumps

do not develop sufficient

discharge

head

to establish

a flow path

through

the valves at elevated

primary pressure.

The test

procedure

directs

the full flow from two

RHR pumps through the

check

valves.

Valve

4-876A is isolated

from 4-876B

and

C

such that

approximately

5000

gpm pass

through

the valve.

The piping configuration

is

such that valves

4-876B

and

C can

not

be isolated

from each

other.

Consequently,

valves

4-876B

and

C

are

tested

simultaneously

and

about

5000

gpm is

assumed

to

pass

through

the

two

valves.

However,

the

licensee's

procedure

does

not verify how the total

flow is split.

Since

all

5000

gpm

passes

easily

through

a single valve,

the test

does

not

demonstrate

that

both

valves

4-876B

and

C

are

unobstructed.

This

deficiency

appears

to violate

code

requirements

in that

valves

4-876B

and

C can

not

be determined

to have

been full-stroke tested

during the

performance

of Appendix

B of

OP

0209. 1.

There is

no confirmation that

both .check valve disks

move promptly

away

from their

seats

when flow is

initiated.

A brief review of plant procedures

and piping confagurations

has

revealed

that this deficiency applies

to Units 3 and

4. It appears

that

check

valves

3/4-8760

and

E,

located

in the alternate

low head

injection line,

may be susceptible

to the

same lack of definitive testing.

Also check valves 3/4-874A and B, located in the hot leg injection lines,

are incompletely tested

based

on existing procedures.

The licensee

has

not previously

sought

a relief request relative to this

testing

problem.

Consequently, it appears

that the Section

XI- code test

requirements

have

not

been

adequately

implemented.

The

licensee

is

evaluating

the effect of these

discrepancies

on

the

operating

units.

Preliminary

evaluations,

performed

by

the

Mestinghouse

Corporation,

indicate that the licensee's

test

methods

for valves

876A,

B and

C are

sufficient to

guarantee

that

adequate

flow will reach

the

core

for

accident

mitigation

purposes.

However,

the

number

and location of all

valves

which

are

not definitively full-stroke

tested

have

not

been

determined.

Consequently,

this issue will be identified as

URI 250,251/

88-11-01,

pending additional

licensee

research

and

NRC followup evalua-

tion.

No violations or deviations

were identified in the areas

inspected.

4.

Maintenance

Observations

(62703/62700)

Station

maintenance

activities of safety related

systems

and

components

were

observed

and

reviewed

to ascertain

that

they

were

conducted

in

accordance

with approved

procedures,

regulatory guides,

industry 'codes

and

standards,

and in conformance'with= TS.

The following items

were

considered

during this review,

as appropriate:

LCOs

were

met while

components

or

systems

were

removed

from service;

approvals

were obtained prior to initiating work; activities

were

accom-

plished

using

approved

procedures

and

were

inspected

as

applicable;

procedures

used

were

adequate

to control

the activity; troubleshooting

activities

were controlled

and repair records

accurately

reflected

the

maintenance

performed;

functional

testing

and/or

calibrations 'ere

performed prior to returning

components

or systems

to service;

gC records

were maintained; activities

were accomplished

by qualified personnel;

that

parts

and materials

used

were

proper ly certified; radiological

controls

were

properly'mplemented;

that

gC

hold

points

were

established

and

observed

where

required;

fire prevention

controls

were

implemented;

outside contractor force activities were controlled in accordance

with the

approved

gA program;

and housekeeping

was actively pursued.

The

inspectors

witnessed/reviewed

portions of the following maintenance

activities in progress:

Installation of the Amertap

System for Unit 4 Intake Cooling Mater/

Component Cooling Water

( ICW/CCW) Heat Exchangers,

Repair/Modification of Unit 4 Containment

Purge Valves,

Repairs to

ICW Pump

3A Gauge Bushing,

Troubleshooting

MOV-4-750 Failure to Open,

Troubleshooting

MOV-4-865 Failure to Operate,

and

Troubleshooting Unit 3 R-11 Spurious Isolation Signals,

and

Containment

Purge Valve Stroke Testing.

On

May 9,

1988, with Unit 4 in Mode 5,

the outboard

containment

purge

exhaust

valve (POV-2602)

was stroke tested

in accordance

with

OP 0209. 1,

entitled

Valve Exercising

Procedure.

Appendix

B of this procedure lists

the valves that are tested during cooldown and/or cold shutdown.

POV-2602

stroke test requires that the valve be verified to close within 5 seconds.

4

The stroke

time recorded

on

May 9,

1988,

was

6.93

seconds.

Plant

Mork

Request

MA880509195444

was -issued

and

troubleshooting

Has

commenced.

Troubleshooting

included lubricating the actuator

shaft

and valve

stem,

and rebuilding the actuator.

The post maintenance

stroke times were also

unsatisfactory.

On

May 13,

1988,

the licensee

formed

an

Event

Response

Team

(ERT

no.88-008)

to investigate

the

problem.

Based

on, the data

obtained through research

and analysis,

the

ERT was able to formulate root

causes.

The primary root 'cause -identifi'ed'as 'that there

was insufficient

capacity to vent the POV-4-2602 actuator.

Contributing to this condition

was

the

implementation

of Plant

Change/Modifications

(PC/M)

to

the

actuator

and instrument air lines over the past eight years.

These

changes

are listed below:

PC/M 79-129,

dated

January

28,

1980,

added air regulators

to

limit valve opening to 50 degrees.

PC/M 81-07, dated

March 4,

1982,

removed the air regulators

and

added

mechanical

hardstops

to further limit supply valves to 33

degrees

and the exhaust

valves to 30 degrees

open.

PC/M 87-406,

dated

December

21,

1987,

changed

solenoid valves

on

POV-4-2690

and POV-4-2602 which involved a change

from 1/2 inch

. carbon

steel

piping to

1/2

inch thick-walled tubing for the

instrument air lines.

This reduced

the internal diameter of the

exhaust line.

The altered

stroke of the actuator

and the unregulated

supply of instru-

ment air contributed to the slower closing times.

A -review of the Unit 3

and

4 containment

purge exhaust

valves closure

time history revealed

the

following:

Valve

Avera

e Closure

Time

POV-3"2602

POV-3-2603

POV-4"2602

POV"4"2603

4.58

seconds

3.46

seconds

4.40

seconds

4.54

seconds

In order to decrease

the stroke

times

on the Unit 4 exhaust

valves,

the

licensee

implemented

PC/M 88-158.

The

PC/M increased

the

size

of the

tubing

from 1/2 inch to

1 inch

on the vent side of the solenoid valves.

The 1/2 inch check valves in the air line were replaced with

1 inch check

valves.

Also the existing needle

valves in the instrument air system were

relocated

upstream of the solenoid valves to limit valve

opening

rate to

no greater

than

3 inches

per

second.

The solenoid valve tubing arrange-

ment,

was

changed

to allow simultaneous

venting of the

solenoid valves.

The licensee

had

noted

a concern with the previous series

solenoid valve

arrangement.

A failure

of

the

upstream

solenoid

could

prevent

the

downstream

solenoid

from venting properly,

thus. preve'nting

the

purge

exhaust

valve

from closing. " The-'new parallel

'-venting

path

allows

the

purge

valve to

be closed

in less

than

5 seconds

with the failure of one

solenoid.

During the

ERT investigation,

a concern

was rai sed with the

method =of testing

the

purge

valves.

The licensee

discovered

that the

stroke times varied depending

on

how long the operator

kept the valve open

prior to initiating closure.

The licensee 'test results,

on

POV-4-2602,

were as follows:

Wait Duration

Closure

Time

2 second

15 second

20 second

5 minute

>5 minute

3.32

seconds

4.89

seconds

5. 10 seconds

5. 15 seconds

5. 16 seconds

. The licensee

determined that there

was

a high probability that the valves

could exceed their maximum closure

times due to the inconsistencies

in the

test

method.

Therefore,

on

May 16,

1988,

the Unit 3 containment

purge

valves

were

de-energized

and

declared

out of service.

The

licensee

determined that the test results for all air operated

valves

may have

been

affected

by time sensitive test methods.

All Unit 4 containment integrity

valves

were

subsequently

tested

satisfactorily utilizing a three

minute

pre-test

condition wait period.

The three

minute period

was conserva-

tively established

by the licensee

based

on test

data

collected.

The

Unit 3 containment integrity valves'losure

time histories

were reviewed

to verify there

were

no valves close to their maximum stroke time.

There

was

evidence

of

slow closure

time for

CV-3-519A (Primary

. Water

to

Pressurizer

Relief

Tank

and

Reactor

Coolant

Pumps),

therefore,

the

licensee

stroke

tested this valve waiting three

minutes

in the pre-test

position.

This test

was satisfactory.

The remaining Unit

3 valves

were

not tested

as

the unit is at

100xo power.

In order to ensure full air

pressure

is applied

to the actuator

prior to stroking

in the

closed

position,

the licensee

made

a revi sion to

OP 0209. 1 to have the operator

wait three minutes before closing any air operated

valve.

No violations or deviations

were identified in the areas

inspected.

5.

Engineered

Safety Features

Walkdown (71710)

The inspectors

performed

an inspection

designed

to verify the operability

of the Unit 3 and

4 Emergency

Diesel Generators.

This was accomplished

by

performing

a complete

walkdown of all accessible

equipment.

The following

criteria were used,

as appropriate,

during this inspection:

b.

System

lineup procedures

match plant drawings

and

as built configu-

ration.

Housekeeping

was

adequate

and appropriate

levels of cleanliness

are

being maintained.

8

c.

Valves in the

system

are correctly installed

and do not exhibit signs

~

of gross

packing leakage,

bent

stems,

missing

handwheels

or improper

labeling.

d.

Hangers

and supports

are

made

up properly and aligned correctly.

e.

Valves in the flow paths

are in correct position

as required

by the

applicable

procedures

with power

avai lable,

and valves

were locked/

lock wired as required.

f.

Local

and

remote position indications were compared

and remote instru-

mentation

was functional.

g.

Major system

components

are properly labeled.

The inspectors

reviewed

the following documents

during the course of the

inspection:

O-OP-023,

Emergency

Diesel

Generator

Operating

Procedure;

Operating

Diagram for Diesel

Generators

"A" and "B", S610-T-E-4S36,

sheets

1

and

2

t

No violations or deviations

were identified within the areas

inspected.

6.

Operational

Safety Verification (71707)

The inspectors

observed

control

room operations,

reviewed applicable

logs,

conducted

discussions

with control

room operators,

observed shift turn-

overs

and

confirmed operability of

instrumentation.

The

inspectors

verified the operability . of selected

emergency

systems,

verified that

maintenance

work orders

had

been

submitted

as required

and that followup

and prioritization of work was

accomplished.

The

inspectors

reviewed

tagout records,

veri Red compliance with TS

LCOs

and verified the return

to service of affected

components.

Plant

housekeeping/cleanliness

conditions

and

implementation

of radio-

logical controls were observed.

Tours of the intake structure

and diesel, auxiliary, control

and turbine

buildings

were

conducted

to observe

plant

equipment conditions including

potential fire hazards,

fluid leaks

and excessive

vibrations.

The

inspectors

walked

down accessible

portions of the following safety

related

systems

to verify operability

and proper valve/switch alignment:

A and

B Emergency

Diesel Generators

Control

Room Vertical Panels

and Safeguards

Racks

Intake Cooling Mater Structure

4160 Volt Buses

and

480 Volt Load and Motor Control Centers

Unit 3 and

4 Feedwater

Platforms

Unit 3 and

4 Condensate

Storage

Tank'Area

Auxiliary Feedwater

Area

Unit 3 and

4 Main Steam Platforms

Control of Technical Specification

Books

On

May 1,

1988,

the" plant 'staff

made

a partial distribution of

TS

amendment

number 130/124.

The

TS change

increased

the

amount of time

a

Component

Cooling Mater

(CCW) heat

exchanger

could remain

out of

service

The

Amendment

was

sent

to

only

about

half

of

the

individuals maintaining controlled copies of the

TS books.

Normally,

the

change

wouTd

have

been

simultaneously

issued

to all holders of

controlled

TS.

A partial

site distribution

was

made

to expedite

incorporation

of the

new requirements.

The site distribution

was

to

be

promptly followed by

a

corporate

office initiated complete

distribution.

The partial distribution

included

essential

watch-

station

personnel

such

as Control

Room Operators,

Nuclear Operators,

Turbine

Operators

and

the Shift Technical

Advisor.

Some

support

groups,

such

as the Technical

and guality Assurance

Departments,

were

not issued

the Amendment.

Partial

distribution

of the

Amendment

created

the potential

for

confusion

in that

not all

controlled

TS contained

identical

CCW

system requirements.

This concern

was discussed

with senior licensee

Supervisors

who specified that the distribution of TS changes

would

always

be complete for future Amendments.

Change

130/124

was

issued

to all holders of controlled

TS on

May 6,

1988.

On

May 5,

1988,

during

a page verification of selected

TS books, it

was

determined

that controlled

copy

number

17,

assigned

to

the

Nuclear Operator's

workstation,

was not up to date.

Several

changes

had been

added to the book without subsequent

removal

of the

super-

seded

pages.

Some of the

superseded

pages

were quite old.

Addi-

tionally,

many sections

were

not in numerical

order

and

some

pages

were missing

from the book.

These

discrepancies

were

brought

to

the attention

of the

Plant

Supervisor-Nuclear

and corrective

action

was initiated.

The Opera-

tions

Department

maintains

four additional

controlled

copies of the

TS.

These

were audited

by the licensee

and additional

discrepancies

were identified and corrected.

However,

even

though all Operations

Department

TS books

had discrepancies,

no audit

was initiated for

'ooks

held by other Departments.

In early

June,

NRC inspectors

audited

two additional

controlled

copies

of TS.

No discrepancies

were identified

in the

book held

by the

IKC Department.

Numerous

discrepancies,

similar

to

those

mentioned

above,

were identified in controlled

copy

number

57,

held

by the Mechanical

Maintenance

Department.

10

The

need for

a comprehensive

assessment

of the status of controlled

books,

such

as the

TS and the

Updated

Final Safety'nalysis

Report,

was discussed

at the exit meeting.

The licensee

committed to develop

a program to ensure

that controlled copies

of important plant books

are

periodically verified against

the current list of effective

pages.

b.

Diesel

Fuel Oil System Misalignment '

On

May 31,

1988,

during the

performance

of

OP 4304.4,

Diesel

Oil

Transfer

System

Periodic

Test

of

Pumps,

test

personnel

noted

inadequate

discharge

pressure

on "A" diesel

fue1 oil transfer

pump.

An operator

checked

the valve line-up for this test

and

$ound the

main diesel oil suction valve,70-003,

locked closed.

This valve is

normally locked

open.

The operator

immediately notified the control

room and the valve was repositioned

and locked in the

open position.

The licensee

then

made'a

significant event notification per

10 CFR 50.72(b)(2)(iii)(D).

This event is further discussed

in

paragraph

9.

The following chronology

documents

those

occasions

when plant

personnel'recently

performed tests

and alignments

of the

fuel oil

system.

05/22/88

1715

0-ADM-205 (Administrative Control of Valves,

Locks,

and

Switches)

completed,

valve

70-003

verified locked open.

05/24/88

0106

0-0SP-023.6

(Diesel Generator

System

Flowpath

Verification)

completed

satisfactorily,

valve

70-003 verified locked open.

05/24/88

0308

05/28/88

0308

0-OSP-023.

1 (Diesel Generator Operability Test)

completed satisfactorily

on "A" EDG.

O-OSP-022.6

(Diesel

Fuel Oil Storage

Tank

Accumulated

Water

Removal)

completed

satis-

factorilyy.

05/29/88

1700

NC-103 (Diesel

Fuel Oil Inventory, Receiving

Shipments

and

Periodic

Sampling)

Step

8.3.4

(Main Diesel

Storage

T'ank) sampling completed.

05/31/88

1445

.

Valve 70-003 discovered

locked closed.

Discussions

were conducted with the individuals performing the above

evolutions

and it was determined

that the valve

was

locked closed

upon completion of the the diesel oil periodic

sampling

on

May 29,

1988,

at

1700.

A chemistry'echnician

stated

that

prior

to

performing

the

sampling

of the diesel

fuel oil storage

tank,

he

11

reviewed Nuclear Chemistry procedure

NC-103 and found it difficult to

understand.

He then'equested

another technician'o* help him sample

the tank.

During the sampling evolution,

a copy of the procedure

was

not taken

to the

sample

location.

The

sampling

procedure,

section

8.3 '

of NC-103, directs that the

sample valve 70-004

be unlocked

and

opened

to obtain

the

required

sample,

then to close

and lock the

sample

valve.

These

steps

were

accomplished

by

the

technician

requested 'to help in the evolution.

The other" technician

thought

he

also

needed

to

open

the

main

suction

valve

(70-003)

to obtain

a

sample.

The valve is clearly labeled

as

a locked

open

valve.

He

unlocked

and thought

he opened

the

70-003

valve

and

upon completion

of sampling, fully closed

and locked the valve.

Positioning of valve

70-003 is not required or addressed

by NC-103.

Due to the fact that

the technician

thought

he initially needed

to open

valve

70-003 to

obtain his

sample

and that

he obtained valve movement

when attempting

to open the valve,

the Chemistry

and Operations

Supervisors

conducted

further interviews with the

individual.

His recollection

of the

event

was that

he

was

unable

to recall

the initial valve position

either by stem position or the

number of turns

taken

to operate

the

valve.

He indicated that

some degree of motion in the

open direction

was obtained,

maybe 3-5 turns.

However,

he was not sure.

The valve,

when properly positioned

should

be off the backseat with some motion

in the

open direction available,

about

1/2 to

1-1/2 turns.

Full

closure of this valve requires

about

14 full turns

on the handwheel.

Based

on the discussion

above,

the licensee

concluded that the 70-003

valve

was already

open

when the technician

thought

he opened it and

that the initial movement of the valve

he obtained

was

due to the

number of turns the valve was off the back seat.

The configuration of the Diesel

Fuel Oil Supply System at the site is

as follows:

Each diesel

engine

has its own 4000 gallon day tank separated

by

a concrete

wall from the tank of the other

engine.

Each

tank

gravity feeds

through

a solenoid valve to its associated

diesel

generator

skid mounted

(275 gallon) fuel tank.

A solenoid valve

is provided with

a

manual

bypass

valve

and associated

piping.

This

arrangement

provides alternative capability to fill each

skid tank should

the

solenoid

close

due to loss

of power or

valve malfunction.

The two da'y tanks are'upplied

by one

common

storage

tank having

a capacity of 64,000 gallons.

This tank has

sufficient storage

capacity

to permit

one diesel

generator

set

to operate

at the

"168 Hour Rating" for 7 or more

days.

An

alternate fill connection

to

each

Diesel

Oil Day Tank suitable

for tie-in from a mobile tank unit is provided.

Alternate fill

lines provide

an alternate fill path

should

the

normal

supply

via the Diesel Oil Transfer

Pumps

become

unavailable.

Transfer

12

of fuel oil from the storage

tank to the day tanks to maintain

level is accompli-shed-automatically

by one'of two electric motor

driven

transfer

pumps.

The

70-003

valve

i s

in the

common

suction line from the

common storage

tank to the

two day tanks

via their

respective

transfer.

pumps.

As

noted,

there

are

alternate

means to provide

a supply of fuel oil to the diesels.

The consequences

of having the

70-'003 valve shut would be that

when

the

day tank level

dropped

and automatically

started

the

respective

transfer

pump

to refill the

day

tank

from

the

storage

tank,

no transfer of fuel oil would take

place,

as

the

suction valve was shut.

The licensee

estimated

that the diesels

would run about 8-10 hours with only the 4000 gallon day tank as

a supply.

Identification of the

lowering day tank level would

be possible after the receipt of a low level alarm.

Thus, there

would have

been

time to determine

the problem and correct it or

provide another

means

to supply fuel to the engine.

However,

this

would require

operator

action rather

than

the automatic

initiation

as

designed.

The

licensee

is

evaluating if the

diesel oil transfer

pumps would have

been

damaged

while running

with the suction

val.ve closed.

Nuclear

Chemistry

Procedure

NC-103, entitled

Diesel

Fuel

Oil

Inventory,

Receiving

Shipments

and Periodic

Sampling,

revision

dated April 14,

1988, directs in section 8.3:4, that only 70-004

valve be operated

to obtain

a sample.

Contrary

to

the

above,

on

May 29,

1988,

valve

70-003

was

closed

during the

performance

of this procedure.

The failure

to follow procedure

NC-103 is

a violation (250,251/88-11-02).

7.

Medical

Emergency Drill

The

licensee

conducted

a

medical

emergency drill on

May

24,

1988,

to

demonstrate

the

effectiveness

of

recently

implemented

training

and

equipment

enhancements

identified as

weaknesses

during the

NRC Emergency

Response

Facilities

Appraisal,

February

22-25,

1988,

(IR 50-250,251/

88-01).

The drill simulated

a

contaminated

injured

man in the Radiation

Waste

Building.

Upon discovery',

the

proper notifications

were

made

and

the

victim was attended to.

Communications

between

responsible

personnel

were

good,

as were contamination controls to prevent

the

spread

of contamina-

tion outside

established

boundaries.

The victim's injuries were-promptly

assessed

and treated.

No deficiencies

requiring

long-term

corrective

actions

were identified.

Minor deficiencies

identified

were

discussed

with drill participants

and resolved at

a critique following the drill.

8.

Physical

Secur ity

(71881)

Station security activities were

observed

during this inspection

period

to. ascertain

that

they

were

conducted

in compliance with the

approved

Physical

Security Plan

(PSP).

13

The fol lowing attr ibutes

were

considered

during

these

observation,

as

appropriate: 'he'inimum

number af

armed -guards

is

on 'site for each

shift;

search

equipment

such

as

x-ray

machines,

metal

detectors

and

explosives

detectors

are

operational;

the

Protected

Area

(PA)

bar rier

is well maintained

and is not compromised

by erosion,

opening in the fence

or walls, or proximity of vehicles

or other objects that could

be

used

to scale

the barrier; illumination in the

PA is adequate

to allow patrol-

ling guards

to observe

th'e

area 'at night and permit the

use of closed

circuit monitors

by alarm station operators;

the vital area

(VA) barriers

are

well maintained;

persons

granted

access

to the site

are

badged

to

indicate whether

they

have

unescorted

or escorted

access

authorization;

there

are

no obstructions

in the isolation

zone that could conceal

an

individual attempting

an unauthorized

entry or interfere with the detec-

tion/assessment

system;

and

when

search

equipment

or alarm

systems

are

inoperable,

or when there is

a breach of the

PA or

VA barrier,

the licen-

see

implements appropriate

compensatory

measures.

No violations or deviations

were identified within the areas

inspected.

Plant Events

(93702)

The following plant events

were reviewed to determine facility status

and

the

need for further followup action.

Plant

parameters

were

evaluated

during transient

response.

The significance

of the event

was evaluated

along with the

performance

of the

appropriate

safety

systems

and

the

actions

taken

by the

licensee.

The

inspectors

verified that

required

notifications were

made

to. the

NRC.

Evaluations

were

performed

r elative

to the

need for additional

NRC response

to the event.

Additionally, the

following issues.

were

examined,

as

appropriate:

details'egarding

the

cause

of the event;

event chronology;

safety

system performance;

licensee

compliance with approved

procedures;

radiological

consequences,

if any;

and proposed corrective actions.

The licensee

plans to issue

LERs

on each

event within 30 days following the date of occurrence.

On Apri 1 27,

1988,

at

0927,

with Unit 3 at

100% power,

the

3A Intake

Cooling Water

( ICW) pump was stopped

and declared

out of service

(OOS) due

to

a discharge

pressure

gauge

piping failure.

The

3A

ICW pump receives

its emergency

power

from the

A Emergency

Diesel Generator

(EDG) and the

3B

and

3C

ICW pumps receive their emergency

power from the

B

EDG, which was

OOS

for scheduled

preventive

maintenance.

When

the

3A

ICW

pump

was

declared

OOS, the

3B and

3C

ICW pumps

became technically

OOS in accordance

with TS 3.0.5,

even though they continued to operate.

With more than

one

ICW pump

OOS, the unit entered

TS 3.0. 1.

At 1045

on April 27,

1988,

the

B

EOG was returned

to service

thus

the

3B and

3C

ICW pumps

also

became

operable.

The unit then exited

TS 3.0. 1,

and entered

TS 3.4.5.b.2,

which

permits

one

ICW pump to

be

OOS for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The pressure

gauge piping

was repaired

and the

3A

ICW

pump

was

returned

to service

at

1209

on

April 27,

1988.

The unit exited

TS 3.4.b.2

at that time.

The

cause of

14

the

failure

of

the

3A

ICW

pump

discharge

pressure

gauge

piping

was

corrosion of the coupling which attaches

the pressure

gauge

piping to the

ICM discharge

pipe.

The corrosion

was

due to

a leak

and

the

use of

a

carbon

steel

instead

of

a stainless

steel

coupling.

The initial inspec-

tion into the reason

carbon steel fittings existed in

a

sea

water

system

indicated that the fittings in question

should

have

been

constructed

of

stainless

steel.

This is identified in the licensee's

original specifi-

cations,

5610-M-50,

a'nd

the

current

specifications,

5177-PS-ll,

for

fittings in the

Intake

Cooling

Mater

System.

However,

the

licensee

recently provided the inspector

a copy of NCR 86-112,

dated

March 5,

1986,

requesting

information on the proper valve, fitting, and piping arrange-

ment for the discharge

pressure

gauges

on the

ICW pumps.

Attachment

D to

the

NCR includes

a diagram of the subject

gauge

assembly

and allows for

the

use of carbon

steel fittings in certain applications for these

gauge

assemblies.

Based

on

the differences

in the

documentation

associated

with the

gauge

assemblies,

this item will be addressed

in the next report

after further information

has

been

obtained.

This is identified

as IFI

50-250,251/88-11-03.

On April 28,

1988, Unit 4 was shut

down due to

a noted increase

in

RCS leak

rate.

The increased

leak rate

was identified as

coming from pressurizer

spray valve

455B

and

was approximately

3. 15 gallons

per minute.

The

TS

limit is

10 gallons per minute.

Subsequent

investigation

revealed that the

bellows internal

to the valve

had failed and was replaced.

The unit was

returned to power on May 28,

1988,

upon completion of various maintenance

items.

On

May 6,

1988, at 0225,

the licensee

declared

an Unusual

Event due to a

security

guard reportedly

being

shot at while

on routine patrol

in the

owner controlled

area.

The

FBI and Metro-Dade

Police

were called in to

assist

with the

investigation

and

the

licensee

terminated

the

Unusual

Event at 1047 that

same day.

The security guard later recanted

his story

that

he

was

shot at by one of three

intruders

in the

owner controlled

area.

He stated that

upon being confronted

by the individuals,

he shot at

their feet to scare

them away.

He then

shot at his

own truck and in the

trees

and fabricated

a story.

He was fearful of losing his job because

he

didn't follow company

procedures

relative to the

use of his weapon.

The

security guard

has

subsequently

resigned

from duty.

No

LER is required to

document this event.

On

May 13,

1988,

the licensee

made'

notification of a significant event

to the

NRC.

During the

design

basis

reconstitution

review of the

RHR

System,

the

licensee

identified

a

situation

where

insufficient

Net

Positive

Suction

Head

(NPSH) for the

RHR,

CS and

HHSI pumps could occur.

Valve 3/4-887

was being maintained

in the 30o'ocked

open position.

This

valve provides

a flowpath from the

RHR pump discharge. to the

CS and

HHSI

pumps during the

post-LOCA recirculation

from the containment

sump.

Plant

engineering

department

determined that insufficient

NPSH would not result

if valve 3/4-887

was being maintained

open

such that the flow through the

valve would be equal to or greater

than

3750

gpm.

The licensee

indicated

that this valve was being maintained

30% since pre-operational

testing but

15

could not obtajn

a positive correlation

between

the valve position

as

a

result of the pre-operational

testing

and the previous

30io valve posi tion.

The valve was locked to 100 percent

open

upon identification of this concern.

Further

investigation

by

the

licensee

revealed

that insufficient

NPSH

would not result with the valve 30:.'pen.

On

May 25,

1988,

the licensee

made

a notification of a significant event

to the

NRC.

With Unit 4 in Mode 3, 'testing 'of pressure

boundary isolation

valves

4-876 A, B, and

C indicated

a possible

leakage

problem.

The plant

entered

an

LCO in accordance

with TS 3. 16 and

commenced

a unit cooldown at

0915.

The valves were subsequently

retested

and declared

back in service

at 2330

on May 25,

1988. This item is discussed

further in paragraph

3.

On May 28,

1988, during routine verification of the Unit 3

PRMS R-11 high

level trip setpoint,

actuation

of the relay for containment

and control

room ventilation isolation occurred.

The actuation

was generated

when the

"High Level

Setpoint"

pushbutton

was

depressed

to verify the setpoint.

The instrument

drawer

was declared

out of service

and

a work order

was

generated

to 'troubleshoot

the

problem.

The

failure

could

not

be

duplicated

during troubleshooting

in the

shop

by

I&C technicians.

The

drawer

was returned for "indication only" at the request

of operations

department,

on

May 29,

1988,

in order

to monitor containment activity

levels

due to

a

suspected

Reactor Coolant

Pump

(RCP) seal

problem

on

RCP

3A.

On

May 30,

1988,

the

drawer

caused

the

same isolation

signal

when

depressing

the

pushbutton

to verify the setpoint.

The drawer

was

then

replaced

with

a

new

drawer

on

June

2,

1988.

The old

drawer will be

shipped to the vendor to determine

the cause of the spurious trip signals.

On May 31,

1988, during the performance

of OP 4304.4,

Diesel Oil transfer

System Periodic Test of Pumps,

test

personnel

noted

inadequate

discharge

pressure

on "A" diesel

fuel oil transfer

pump.

An operator

checked

the

valve line-up for this test

and found the main diesel .oil suction valve,70-003,

locked closed.

This valve is normally locked open.

The operator

immediately notified the control

room and

the valve

was repositioned

and

locked in the

open position.

The licensee

then

made

a significant event

notification

per

10 CFR 50.72(b)(2)(iii)(D).

This

event

is further

discussed

in paragraph

6.

Onsite

Followup and In-Office Review of Nonroutine Events

(92700/92712)

The

Licensee

Event

Reports

(LERs)

discussed

below

were

reviewed

and

closed.

The inspectors verified that reporting requirements

had been

met,

root

cause

analysis

was

performed,

corrective

actions

appeared

appro-

priate,

and generic applicability had

been considered.

Additionally, the

inspectors

verified that the licensee

had reviewed

each event, corrective

t

16

actions

were

implemented,

responsibility for corrective actions not fully

completed

was clearly assigned,

safety'uestions

had

been

evaluated

and

resolved,

and

violations

of regulations

or

TS

conditions

had

been

identified.

(Closed)

LER 251/87-23, entitled Process

Radiation Monitor Trends

High Due

to

Jammed

Paper

Drive Causing

Control

Room Ventilation

and

Containment

Vent Isolation.

The licensee

replaced

the paper

and readjusted

the paper

drive tension.

The paper drive units were subsequently

overhauled

and, at

present,

new drive units

are

on order from the vendor.

LER 251/87-23 is

closed.

(Closed)

LER 250/87-03, entitled Reactor Trip During Load Reduction

Oue to

Low Pressurizer

Pressure.

The unit trip occurred

during

a rapid load

reduction that

was being

performed

due to

a turbine plant cooling water

leak in the main generator exciter

and the resultant

ground.

The trip was

caused

by an excessive

cooldown due to emergency boration during the load

reduction.

The licensee

implemented

a

new procedure

to provide instruc-

tions for

a rapid load reduction

(3/4-ONOP-100)

and included

a simulator

scenario

in the operator training program.

LER 250/87-03 is closed.

11.

Exit Interview

The

inspection

scope

and

findings

were

summarized

during

management

interviews held throughout the reporting period with the Plant

Manager

Nuclear

and selected

members of his staff.

An exit meeting

was conducted

on June 8,

1988.

The areas

requiring management, attention

were

reviewed.

No proprietary

information

was

provided

to the

inspectors

during

the

reporting period.

Unresolved

Item 50-250,251/88-11-01,

Evaluate

licensee's

method of

testing

check

valves

to

meet

the requirements

of ASME Boiler and

Pressure

Vessel

Code,

Section XI.

Violation 50-250,251/88-11-02,

Failure to follow procedure,

in that

the diesel

fuel oil tank suction

valve

003

was

found locked closed

when required to be locked open.

Inspector

Followup

Item

50-250,251/88-11-03,

Resolution

of

the

differences

in documentation

associated

with th'e intake cooling water

gauge

assembly materials.

12.

Acronyms and Abbreviations

AOM

a.m.

ANSI

AP

Administrative

ante meridiem

American National

Standards

Institute

Administrative Procedures

'

17

ASME

CCW

CFR

CS

dp

EDG

ENS

ERT

FBI

FPL

FSAR

gpm

HHSI

I &C

ICM

IFI

IST

LCO

LER

LIV

LOCA

MOV

MP

NCR

NPSH

NRC

ONOP

OOS

OP

OTSC

PA

PC/M

p.m.

PNSC

PSN

PSP

QA

QC

RCO

RCP

RCS

RHR

SRO

TS

TSA

URI

VA

American Society of Mechanical

Engineers

Component

Cooling Mater

Code of Federal

Regulations

Containment

Spray

Differential Pressure

EDG

Emergency

Diesel Generator

Emergency Notification System

Event Response

Team

Federal

Bureau of Investigation

Florida Power 5 Light

Final Safety Analysis Report

Gallons

Per Minut'e

High Head Safety Injection

Instrumentation

and Control

Intake Cooling Mater

Inspector

Followup Item

Inservice Test

Limiting Condition for Operation

Licensee

Event Report

Licensee Identified Violation

Loss of Coolant Accident

Moter Operated

Valve

Maintenance

Procedure

Non-conformance

Report

Net Positive Suction

Head

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Out of Service

Operating

Procedure

On The Spot Change

Protected

Area

Plant Change/Modification

post meridiem

Plant Nuclear Safety Committee

Plant Supervisor

Nuclear

Physical

Security Plan

Quality Assurance

Quality Control

Reactor Control Operator

Reactor Coolant

Pump

Reactor

Coolant System

Residual

Heat

Removal

Senior Reactor

Operator

Technical Specification

Temporary

System Alternative

Unresolved

Item

Vital Area