ML17333A585

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Insp Repts 50-315/96-10 & 50-316/96-10 on 960805-29. Violations Noted.Major Area Inspected:Engineering Support of Facilities & Equipment
ML17333A585
Person / Time
Site: Cook  
Issue date: 09/27/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17333A583 List:
References
50-315-96-10, 50-316-96-10, NUDOCS 9610030336
Download: ML17333A585 (15)


See also: IR 05000315/1996010

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

Licenses

No:

50-315,

50-316

DPR-58,

DPR-74

Reports

No:

50-315/96010(DRS);

50-316/96010(DRS)

Licensee:

Indiana Michigan Power

Company

Facility:

Donald

C.

Cook Nuclear Generating

Plant

Location:

7700

Red Arrow Highway

Stevensville,

MI

49127

Dates:

August 5-29,

1996

Inspectors:

Approved by:

D. Butler, Reactor Inspector, RIII

R. Lerch, Reactor Inspector,

RIII

M. A. Ring, Chief

Lead Engineers

Branch

Division of Reactor Safety

Ins ection

Summar

Routine inspection of previously identified issues

from the Integrated

Performance

Assessment

Process

and other inspections.

One violation for lack

of test control

was identified for lack of surveillance testing of some

component cooling system flows.

One unresolved

item was initiated regarding

the appropriateness

of a revision to the Updated Final Safety Analysis Report.

96f0030336

960927

PDR

ADOCK 050003i5

8

PDR

O

M8.1

Miscellaneous

Maintenance

Issues

Closed

Violation 50-315 95014-01

DRP

The licensee

did not properly

train Instrument

and Control (IC) technicians

and provide adequate

calibration details in maintenance

procedure

No.

12

IHP 6030

IMP.014,

"Protective Relay Calibration."

In response,

the licensee requalified all of the

IC technicians that

calibrate protective relays.

In addition, the maintenance

procedure

was

revised with a note defining the relay pick-up current

as the point

where the continuity light "just flickers."

The inspectors

reviewed the

technician training records,

training lesson

plan No. IC-C-0720,

"Protective Relays," the maintenance

procedure,

and observed

two.

protective relay calibrations

in the field.

The inspectors

concluded

the licensee

had addressed

this violation in an acceptable

manner.

In

addit1on,

the

IC technicians

that performed the calibrations clearly

understood

proper protective relay calibration techniques.

This item is

considered

closed.

E2

E2.1

Engineering

Support of Facilities

and Equipment

Follow-u

of NRC Issues

Re ardin

Com onent Coolin

Water

CCW

S stem

Flow Balancin

'a

~

Ins ection

Sco

e

2.

In February

1996,

an Integrated

Performance

Assessment

Process

(IPAP)

inspection

team identified that the completed Unit

1

CCW flow balance

procedure,

1

EHP 4030 STP.248,

"Unit

1 Component

Cooling Water

Flow

Balance,"

completed

on September

28,

1995,

was inadequate

because:

Sample cooler flows were not met,

although objectives

were provided in

the procedure.

The objectives

were not acceptance

criteria, although

the flows were described

as the minimum required flows in the Updated

Final Safety Analysis Report

(UFSAR).

Cooling flow to the containment air recirculation fan was not verified

by the surveillance.

Additional details

on these

observations

may be found in Inspection

Reports

No. 50-315/316-96003

and

No. 50-315/316-96006

(Inspection

Follow-up Item (IFI) 96006-03).

The inspector

reviewed licensee

actions

taken since conclusion of the

IPAP inspection with regard to

CCW

surveillances

and discussed

the issues

with the licensee's

staff.

The

inspectors

also reviewed the

UFSAR revision dated July 1996

and

a safety

evaluation

performed regarding

the

CCW system description revision to

the

UFSAR.

2

Observations

and Findin

s

A Unit 2 flow balance surveillance,

2

EHP 4030 STP.248,

"CCW Flow

Balance,"

was started

in April and completed

Hay 1,

1996,

using

a

procedure similar to the one reviewed

by the

IPAP team.

No changes

in

response

to

NRC concerns

had

been

made;

however,

the

IPAP inspection

report

had not been received/reviewed

by the licensee.

The

IPAP report

was issued April 17,

1996.

Nonetheless,

inspector interviews with

members of the engineering staff indicated the requirement for the

surveillance

program to verify and maintain

system performance

in

accordance

with the

UFSAR was not well understood

or appreciated

by

several

members of the engineering staff.

A UFSAR revision dated July 6,

1996,

was submitted to the

NRC, which

revised Table 9.5-2,

making miscellaneous

header

flows (sample coolers,

thermal barriers,

seal injection,

and others) for information only

rather than minimum required flows.

The licensee

completed

a safety evaluation

dated July 31,

1996, to

evaluate

the July

UFSAR revision.

The position of the safety evaluation

was that only safe

shutdown cooling loads

needed

to have

minimum

requirements

specified.

Issues

such

as license

commitments

made to meet

Three Mile Island action items for post-accident

sample cooling, or the

importance of reactor coolant

pump thermal barrier cooling to potential

events

were not,addressed.

Given the importance of miscellaneous

header

cooling flows to plant operations,

the designation of flow information

as "for information only" could

be misleading.

Discussions

with the licensee

indicated that based

on recent

system flow

readings

and sampling

by the chemistry department,

the sample coolers

were useable

with reduced

coolant flow under normal conditions.

Additional cooling of samples

could

be obtained

by slowing the flow of

the sample

through the cooler.

Conclusions

The inspectors

identified the following issues:

The containment recirculation/hydrogen

skimmer fan cooling flow is not

verified by any surveillance.

The

CCW sample cooler flows were measured

by surveillances

1

EHP 4030

STP.248,

"Unit

1 Component

Cooling Water Flow Balance,"

completed

on

September

28,

1995,

and

2

EHP 4030 STP.248,

"CCW Flow Balance,"

completed

Nay 1,

1996,

but measurements

indicated they were less

than

required

by the test objectives

and the

UFSAR.

The chemistry staff

stated that samples

can

be adequately

cooled with existing flows;

however,

the ability to cool

samples

under accident conditions

was

undetermined

and

had not been evaluated.

When engineers

created

surveillance

procedure objectives

and accepted

surveillance

flow results

which were less

than the

UFSAR specified for

0

CCW flow to sample coolers,

they changed

the operation of the system

as

described

in the

UFSAR ~

Although the effects

appear

to have

been

minimal, they were not evaluated

and safety evaluations

were not

performed.

The inspectors

were concerned that it was not appropriate for the

UFSAR

revision to describe

the flow requirements

for the miscellaneous

header

as nominal

and for information only.

Issues

1 and

2 were examples of inadequate

test control.

The licensee

initiated condition report 96-1367 to track corrective actions for these

issues.

The failures to verify adequate

CCW flows through surveillances

were examples of a violation of 10 CFR 50, Appendix B, Criterion XI,

"Test Control" (50-315/316-96010-01).

Issue

3 was related to the

concerns of Issue

2.

E2.2

Issue

4 required further review by the

NRC to determine

the information

and level of detail

needed

in the

UFSAR.

This is an unresolved

item

(URI) pending further review by the

NRC (50-315/316-96010-02).

NRC Information Notice

IN 92-18:

Potential for Loss of Remote

Shutdown

Ca abilit

Durin

a Control

Room Fire

The

NRC notified the industry via IN 92-18 about

an unanalyzed

condition

regarding fire protection

and

a plant's safe

shutdown capability during

a control

room fire that forced reactor operators

to evacuate

the

control

room.

This fire location could cause

hot shorts,

such

as short

circuits between

motor operated

valve

(HOV) control circuit conductors

and their control

power source.

As a result,

spurious operation of

certain

MOVs may occur before the operators

shifted control of the

valves to the remote/alternate

shutdown panel.

Motor thermal

overload

protection

may be bypassed,

set high or set with a longer tripping time

to allow for additional

valve duty cycles and/or reversing of the

HOV

during stroking.

The

IN identified that

HOV torque

and limit switches

=would not electrically disconnect

the stroking valve, causing

mechanical

damage

to the valve and/or damaging

the motor due to the hot short

bypassing

the limit or torque switches.

Licensees

took credit for

manual manipulation of certain

HOVs in many of the Appendix

R safe

shutdown scenarios,

but in some instances,

did not consider the valves

could

be mechanically

damaged.

The licensee

provided the inspectors

a list of electrically operated

Appendix

R valves.

The D.

C. Cook'design

uses

a double break

scheme

around the valve open/close

contactor.

In most cases

this was provided

by both limit/torque switch contacts

and remote/alternate

transfer

switch contacts.

For the above,

two hot shorts of the correct polarity

and conductors

must occur to operate

a valve.

The inspectors

reviewed

the electrical

design of the Appendix

R valves for both units.

All the

valves incorporated

the double break design.

The inspectors

noted that

four steam generator

(SG) turbine driven auxiliary feedwater

pump

(TDAFP) feed valves

had

common relay contacts,

such

as relay 63Xl-SGlT

for the valve feeding

SG1, that could initiate valve operation

due to

one hot short.

However, the torque switch remained electrically

connected

and would prevent mechanical

damage to the valve.

The

emergency

remote

shutdown

procedure

had the operators electrically

disable the individual

TDAFP to

SG valve power supplies.

This would

effectively remove

any continuous

close signal

and permit manual

valve

manipulation.

In addition, only two SGs were required for an Appendix

R

scenario.

The probability of a single hot short

on more than

two TDAFP

feed valves

was extremely low.

The inspectors

concluded that

D.

C.

Cook

met the intent of the IN.

Susce tibilit of Ta lor MOD 30 Di ital Controllers to Electrostatic

Dischar

e

ESD

On March 17,

1996, the differential pressure controller for the Unit I

feedpump

(I-RU-05) failed without operator interaction

and resulted

in a

reactor trip.

Unit conditions were stabilized

and the controller was

replaced.

Initial investigations identified that the controller had

failed in the unconfigured state.

During this period,

several

other

controllers exhibited control

panel "flicker" when touched.

The

licensee's

root cause

analysis

determined that

ESD was causing

the

MOD

30 controller problems.

The licensee

concluded that controller circuit board static drain clips

were not properly oriented

and were not grounding the controller.

In

addition, the control

room humidity was very low and

had increased

ESD

buildup.

The licensee

had installed

ESD limiting carpeting.

Samples

were sent to the manufacturer to verify that the correct carpet

had

been

installed.

The test results

indicated that the installed carpet

was

ESD

limiting (l. I KV, step

and 0.9 KV, scuff).

In addition, the licensee

installed grounded static step-off pads in front of ESD sensitive

equipment.

The

MOD 30 manufacturer

performed

ESD sensitivity tests

on the failed

controller.

ESD levels to

3

KV were capable of inducing control

panel

"flicker."

The manufacturer installed

an additional

ground wire from

the module mounting case that increased

ESD tolerance to

7 KV.

The

extra ground wire has

been installed

on the feedpump controller at

D.

C.

Cook.

In addition, the manufacturer

has identified that the electrical

conductor ribbon strip that attached

to the membrane

keypad switch

control

panel

(face-plate)

was also susceptible

to

ESD.

The

manufacturer

was testing different face-plate modifications.

The

ESD

immunity has

been

increased

to

12

KV by insulating the ribbon strip.

Replacement

of the currently installed face-plates

was being reviewed

by

the licensee.

The licensee

has initiated other actions to improve

ESD immunity.

These

include control

room humidity monitoring

and improving control

room

humidifier operation.

The inspectors

concluded that the licensee

was

effectively addressing

ESD affects

on digital equipment.

Niscellaneous

Engineering

Issues

Closed

IFI 50-315 316-95005-05

DRP

During the past several

years,

numerous

Foxboro

N-2AO-V2H (V2H) voltage to current cards

have failed

due to design

and/or component related

weaknesses.

These

included

an

undersized circuit board fuse

and the encapsulated

(potted)

DC to

DC

converter

module.

The licensee

has worked closely with Foxboro to

resolve these

issues.

The resultant

design

changes

have replaced

the

fuse with a larger size

and

added additional

fuse protection.

The

DC to

DC converter

module

was completely redesigned

and installed

on all of

the safety related cards.

Only one

new card failure has occurred.

This

was attributed to

a card burn-in type failure.

The licensee

indicated that the

new

DC to

DC converter

module

had

a

manufacturing flaw.

Two surface

mount biasing resistors

were installed

at

a lower resistance

value than called for in the design.

Testing

has

demonstrated

that the lower resistor values

have slightly increased

the

module heat generation.

However,

module components

thermal

design

margin was high (= 50X) so that this flaw should not affect

functionality.

The licensee

indicated that card life testing will

continue to determine if the

mean time before failure of the cards

had

increased.

This item is considered

closed.

Closed

IFI 315 316-93012-Ola

and

c DRS:

The Systems

Based

Instrument

and Control Inspection

(SBICI) team determined that certain Westinghouse

WCAP-13055,

"Setpoint Methodology for Protection

Systems

D. C. Cook,

Unit 1," and

WCAP-13801,

"Setpoint Methodology for Protective Systems-

D.

C. Cook, Unit 2," protective action setpoints

did not include

an

environmental

allowance

(EA) term in diverse

secondary

(backup) trip

functions.

The trip functions of interest

included

SG water low level,

low-low level

and high-high level;

and main steam flow/feedwater flow

mismatch.

In response,

Region III requested

assistance

from the Office of Nuclear

Reactor Regulation

(NRR) to determine if backup trip functions were

required to include

an

EA term in the setpoint methodology.

NRR

reviewed the

above

backup trips and determined that the accident

analysis did not include

an

EA in the uncertainty calculations.

NRR

concluded that the licensee's

methodology concerning

EAs was consistent

with Westinghouse's

methodology

and

IEEE Standard

279; "Criteria for

Protective

Systems for Nuclear

Power Generating Stations."

This item is

considered

closed.

Closed

IF I 315 316-93012-Old

DRS:

The SBICI team noted that the

D.

C.

Cook design

used containment

pressure

to detect

a steam line break

inside containment rather than

steam line flow.

The team was concerned

that this design

was not meeting the intent of IEEE Standard

279-1968,

since containment

pressure

was not

a direct variable measurement

of this

accident condition,

In response,

Region III requested

assistance

from NRR to determine if

containment

pressure

was

an acceptable

variable to detect

a steam line

E8.4

break inside containment.

NRR reviewed

UFSAR Section 14.3.4,

"Containment Integrity Analysis,"

and concluded that the containment

pressure

variable

was the accepted

licensing basis for this accident

scenario.

This item is considered

closed.

Closed

IFI 315 316-93012-Ole

DRS:

The SBICI team noted that

Regulatory

Guide 1.97,

Category

1, condensate

storage

tank

(CST) level

instrument

loop accuracy calculation did not include

a seismic bias

error term.

In response,

the licensee

provided the Foxboro equipment qualification

reports for Model

N-E13DM and

E13DM pressure

transmitters.

The

qualification report

showed that the differential pressure

transmitters

would return within their. reference

accuracy following a seismic event.

NRR concluded that the licensee's

treatment of the

EAs for the

CST level

instrument

loop calculation

was acceptable.

This item is considered

closed.

E8.5

Closed

IFI 315 316-93012-Olf DRS:

The SBICI team noted that the

refueling water storage

tank

(RWST) level instrumentation

cables

were

routed through

a high energy line break

(HELB) area.

The D. C.

Cook

UFSAR indicated that the

RWST level channels

were

used to mitigate

an

SG

blow down event.

As such,

an

EA term should

be included for the cable

routed through the

HELB area.

In response,

the licensee

provided

NRR a calculation that included cable

insulation losses.

NRR reviewed the calculation

and concluded that the

licensee

had addressed

cable insulation losses

in an acceptable

manner.

This item is considered

closed.

E8.6

EB. 7

Closed

IFI 50-315 316-96006-03:

CCW flow balance

surveillances

did

not meet the

UFSAR.

This is'losed

to violation 50-315/316-96010-01

in

this report.

Closed

URI 50-315 96006-15 DRS:

NRC Inspection

Report

No. 50-

315/316-95010,

Section 3.5, identified that the Unit

1 west motor-driven

auxiliary feedwater

pump

(MDAFP) had

a history of instantaneous

relay

(PJC type) trips during Mode 4,

5 or 6 testing.

The testing took place

prior to entering

Mode 3.

The

MDAFP was required to be operable

in

Modes

1,

2 and 3.

In response,

the licensee

issued condition report

No. 95-1204 to address

this concern.

The licensee's

investigation identified that the

MDAFP

,instantaneous

relay (1-50-50N-TA2)

had insufficient margin for motor

starts during high voltage conditions

(4280 volts).

The safety

buses

were supplied

from the reserve auxiliary transformer

(RAT) during Modes

4, 5, or 6 testing.

Since Unit

1 was shut down,

house

loads

were at

a

minimum (< 2.5

MW) while operating plant loads

were typically 20.5 to

36

MW.

This resulted

in higher

bus voltage

due to

a lightly loaded

RAT.

Normal

Mode 1,

2 or 3 electrical

supply to the safety

buses

was from the

unit auxiliary tr'ansformers

that also

power the house loads.

During the

past year's

Mode 1,

2 or 3 operation,

the Unit

1 safety

bus high average

voltage

was about

4195 volts.

The Unit

1 west

pump has tripped four

times since

1987.

All of the trips occurred during Hode

5 or 6 testing

of the pump.

There

have

been over

a hundred successful

Unit

1 west

pump

starts

since

1987.

In addition, the Unit

1 east

and both Unit 2 MDAFPs

were successfully

started

during bus high voltage conditions.

The licensee

determined that the Unit

1 west

HDAFP current transformer

(CT) saturated

at

a higher value than the manufacturer's

saturation

curve.

Therefore,

the resultant

CT excitation voltage

change

was

greater for a given

CT current

change at the

PJC relay.

At higher motor

starting voltages,

an induction motor starting current will increase,

since electrically the motor appears

as

an

impedance

device.

This

generated

higher current flow to the

PJC relay and caused

the relay to

trip sooner.

The four HDAFP PJC relays

were set for a nominal primary current of 27

amperes.

Calculation

PS-4KV-001,

"4 KV Safety Hotor Electrical

Protection,"

developed

the setpoints

based

on

IEEE 242-1989

recommendations.

Although the setpoint margin was lowest for the

HDAFP

motors,

the results

were within the calculation acceptance

criteria.

The licensee

increased

the Unit

1 west

HDAFP setpoint to

a primary

current of 33 amperes

and

was reviewing the other

HDAFP setpoints.

In

addition, the licensee

indicated that additional

CT testing

was being

performed.

The licensee

revi'ewed all of the current

4

KV motor

protective setpoints

and concluded the calculation

had

been

performed

satisfactorily.

The inspectors

reviewed the

above information and

CT design standards,

and concluded that the licensee's

root cause determination

and

corrective actions

were reasonable.

In addition, the inspectors

concluded that the Unit

1 west

HDAFP was operable,

since safety

bus

voltage did not exceed

4280 volts during past

Mode 1,

2 or 3 operation.

This item is considered

closed.

V. Nana

ement Neetin

s

Exit Meeting

Summary

The inspectors

met with various licensee

representatives

on August 9,

1996,

and

summarized

the scope

and findings of the inspection

in the

electrical

and instrumentation

and control areas.

Inspectors

also

conducted

an exit meeting

by phone

on August 29,

1996,

and

summarized

the scope

and findings with regard to follow-up on component cooling

water flow balancing.'he

persons listed under the partial list of

persons

contacted

participated

in the telephone exit.

The licensee

did

not identify any of the documents

reviewed

by the

NRC as proprietary.

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

A. Blind, Site Vice President

K. Baker, Assistant

Plant Hanager

P. Schoepf,

Supervisor,

Safety-Related

Systems

J.

Kobyra, Hanager Nuclear Engineering

R. Ptacek,

Licensing

W. HcCrory,

System

Engineer

INSPECTION

PROCEDURES

USED

IP 37551

On-site Engineering

IP 62703

Haintenance

Observation

ITEHS OPENED,

CLOSED,

AND DISCUSSED

~0ened

50-315/316-96010-01

VIO

50-315/316-96010-02

URI

Closed

Lack of test control for CCW flow balance

FSAR

requirements.

Revision to the

FSAR changed

the minimum

required

CCW miscellaneous

flows to nominal

flows for information only.

50-315/95014-01

50-315/316-96005-05

50-315/316-96006-03

50-315/96006-15

VIO

IFI

IFI

URI

The licensee

did not properly train

IC

technicians

and provide adequate

calibration

details.

During the past several

years,

numerous

Foxboro

N-2AO-V2H (V2H) voltage to current cards

have

failed due to design and/or component related

weaknesses.

CCW flow balance

tracked

under

VIO

50-315/316-96010-01.

NRC Inspection

Report

No. 50-315/316/95010,

Section 3.5, identified that the Unit

1 west

HDAFP had

a history of instantaneous

relay

(PJC

type) trips during Hode 4,

5 or 6 testing.

315/316-93012-Ola

5 c

IFI

Certain Westinghouse

protective action setpoints

did not include

an

EA term in diverse

secondary

(backup) trip functions.

315/316-93012-01d

315/316-93012-Ole

315/316-93012-01f

IFI

IFI

IFI

The

D.

C.

Cook design

used containment

pressure

to detect

a steam line break inside containment

rather than

steam line flow.

II

The Regulatory

Guide 1.97,

Category

1,

CST level

instrument

loop accuracy calculation did not

include

a seismic bias error term.

The

RWST level instrumentation

cables

were

routed through

an

HELB area.

10

CCW

CST

CT

EA

ESD

HELB

IC

IFI

IN

IPAP

MDAFP

MOV

NRR

RAT

RWST

SBICI

SG

TDAFP

UFSAR

URI

VIO

LIST OF ACRONYMS USED

Component

Cooling Water

Condensate

Storage

Tank

Current Transformer

Environmental

Allowance

Electrostatic

Discharge

High Energy Line Break

Instrument

and Control

Inspection

Follow-Up Item

Information Notice

Integrated

Performance

Assessment

Process

Motor-Driven Auxiliary Feedwater

Pump

Motor Operated

Valve

Office of Nuclear Reactor Regulation

Reserve Auxiliary Transformer

Refueling Water Storage

Tank

Systems

Based

Instrument

and Control Inspection

Steam Generator

Turbine Driven Auxiliary Feedwater

Pump

Updated Final Safety Analysis Report

Unresolved

Item

Violation