ML17328A779

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SALP Repts 50-315/90-01 & 50-316/90-01 for Jul 1989 to Aug 1990
ML17328A779
Person / Time
Site: Cook  
Issue date: 11/15/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17328A778 List:
References
50-315-90-01, 50-315-90-1, 50-316-90-01, 50-316-90-1, NUDOCS 9011200209
Download: ML17328A779 (39)


See also: IR 05000315/1990001

Text

SALP

9

INITIALSALP

REPORT

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE

Inspection

Report

No. 50-315/90-01;

50-316/90-01

Indiana Michigan Power

Company

Donald

C.

Cook Nuclear Plant

July 1,

1989,

through August 31,

1990

TABLE OF

CONTENTS

~Pe

e No.

I.

INTRODUCTION ...

II.

SUMMARY OF RESULTS

.

verview ..............

0

III. CRITERIA

.

IV.

PERFORMANCE ANALYSIS ..

A.

Plant Operations ...

B.

Radiological Controls ..

C.

Maintenance/Surveillance '.

D.

Emergency

Preparedness .............

13

E

Security

.

F.

Engineering/Technical

Support .....................

G.

Safety Assessment/guality

Verification

17

19

V.

SUPPORTING

DATA AND SUMMARIES

23

A.

Licensee Activities ...............

23

B.

Inspection Activities ..

C.

Escalated

Enforcement Actions ..................

~ ..

26

D.

Confirmatory Action Letters

(CALs)

26

ED

Review of Licensee

Event Reports .............

26

I ~

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is an

integrated

NRC staff effort to collect available observations

and data

on

a periodic basis

and to evaluate

licensee

performance

on the basis

of this information.

The program is, supplemental

to normal regulatory

processes

used to ensure

compliance with NRC rules

and regulations.

It

is intended to be sufficiently diagnostic to provide

a rational basis for

allocating

NRC resources

and to provide meaningful

feedback to the licensee's

management

regarding

the NRC's assessment

of the facility's performance

in each functional area.

An NRC SALP Board,

composed of the staff members listed below,

met on

October

26 and 31,

1990, to review the observations

and data

on performance,

and to assess

licensee

performance

in accordance

with the guidance in

NRC

Manual Chapter

0516., "Systematic

Assessment

of Licensee

Performance."

The

guidance

and evaluation criteria are

summarized

in Section III of this

report.

The Board's findings,and

recommendations

were forwarded to the

NRC Regional Administrator for approval

and issuance.

This report is the

NRC's assessment

of the licensee's

safety performance

at D.

C.

Cook Nuclear Plant for the period July 1,

1989,

through

August 31,

1990.

The

SALP Board for D.

C.

Cook Nuclear Plant was

composed of the following

individuals:

Board Chairman

H. J. Miller, SALP Board Chairman, Director, Division of Reactor

Safety

(DRS)

Board Members

E.

G. Greenman,

Director, Division of Reactor Projects

(DRP)

R.

C. Pierson,

Project Directorate, Office of Nuclear Reactor Regulations/

Project Directorate

(NRR/PD) III-I

W. L. Axelson,

Deputy Director, Division of Radiation Safety

and

Safeguards

B. Clayton, Chief, Reactor Projects

Branch 2,

DRP

T.

G. Colburn, Senior Project Manager,

NRR/PD III-I

B. L. Jorgensen,

Senior Resident

Inspector,

DRP

Other Attendees

at the

SALP Board Meetin

A. B.

C. J.

M. A.

G.

C.

B..L.

J.

R.

M.

C.

Davis, Regional Administrator,

Region III

Paperiello,

Deputy Regional Administrtor, Region III

Ring, Chief, Engineering

Branch,

DRS

Wright, Chief, Operations

Branch,

DRS

Burgess,

Chief, Reactor Projects

Section

2A,

DRP

Creed,

Chief, Safeguards

Section,

DRSS

Schumacher,

Chief, Radiological Controls

and Chemistry Section,

DRSS

I&

Other Attendees

at the

SALP Board Meetin

con't.

W.

G. Snell, Chief,

Emergency

Planning Section,

DRSS

J.

A. Isom, Senior Resident

Inspector,

DRP

D.

G. Passehl,

Resident

Inspector,

DRP

E.

R. Schweibinz,

Senior Project Engineer,

DRP

P.

S. Koltay,

NRR, SIB

M. L. Dapas,

NRR

C. A. Carpenter,

NRR

M. L. McCormick-Barger,

Reactor Engineer,

DRP

F. A. Maura,

Reactor Inspector,

DRS

Z. Falevits,

Reactor Inspector,

DRS

J.

M. Ulie, Reactor Inspector,

DRS

C.

F. Gill, Senior Reactor

Programs Specialist,

DRSS

J.

A. Gavula,

Reactor Inspector,

DRS

II.

SUMMARY OF RESULTS

Overview

The licensee's

was acceptable

effectiveness,

improvement in

overall performance

level during this assessment

period

in all areas.

The degree of management

attention

and

however,

ranged

from commendable

in

some areas

to needing

others'he

licensee

generally

conformed to its

own standards,

which were appropriately

directed to the needed

assurance

of safe performance.

In a couple of

areas,

however,

there

was

a lack of progress

in achieving resolution of

identified weaknesses.

Management

appeared

proactive

and effective in meeting high standards

of

performance

in operations,

emergency

preparedness,

and security,

and

consistently

demonstrated

a conservative

operating philosophy..

Tolerance

of prolonged

weaknesses

in maintenance

and in engineering/technical

support

was noted.

Over the period,

some

improvements

were noted in maintenance

support

systems

and in plant housekeeping

and material condition.

Additional

planned

changes, if well implemented,

should result in an overall

improvement

in the of quality of the management

and implementation of maintenance.

Weaknesses

in engineering/technical

support adversely affected

capabilities in other areas,

especially

maintenance,

and

some were long

standing.

There is reason for concern

about the adequacy

of design

development,

and implementation

and control of modifications.

This is

based

on identified instances

of failure to achieve

compliance for such

issues

as Appendix

R design

requirements,

problems with design

verification, and continued identification of design calculation errors.

Material

and personnel

resources

were generally

adequate

in all areas.

Organizational

changes

and adjustments

in resource

allocations

were

made

in some areas

which appeared

appropriate

to address

some previous problems.

These

had not yet had significant effects at the end of the assessment

period.

The performance

ratings during the previous

assessment

period and

this assessment

period according to functional areas

are given below:

Functional

Area

Rating Last

Period

Rating This

Period

Trend

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Security

Engineering/Technical

Support

Safety Assessment/equality

Verification

1

2

2

1

2

.2

2

~

1

2~ 3A'

1

3

2

improving"

  • Rating changed

from a

2 to a

3 improving by Regional Administrator

III. CRITERIA

Licensee

performance is assessed

in selected

functional areas.

Functional

areas

normally represent

areas

significant, to nuclear safety

and the

environment.

Some functional areas

may not be assessed

because

of little

or no li'censee activities or lack of meaningful observations.

Special

areas

may be added to highlight significant observations.

The following evaluation criteria were

used to assess

each functional

area:

l.

Assurance of quality, including management

involvement

and control;

2.

Approach to the identification and resolution of technical

issues

from a safety standpoint;

3.

Enforcement history;

4.

Operational. events (including response

to, analyses

of, reporting

of, and corrective actions for);

5.

Staffing (including management);

and

6.

Effectiveness

of training and qualification program.

However, the

NRC is not limited to these criteria and others

may have

been

used where appropriate.

On the basis of the

NRC assessment,

each functional

area evaluated is

rated according to four performance

categories.

The definitions of

these

performance

categories

are

as follows:

~Cate or

1:

Licensee

management

attention to and involvement in nuclear

safety or safeguards

activities resulted

in a superior

level of performance.

NRC will consider

reduced levels of inspection effort.

~Cate

or

2:

Licensee

management

attention to and involvement in nucle'ar

safety'or

safeguards

activities resulted

in a good level of performance.

NRC will consider maintaining

normal levels of inspection effort.

~

Cate<aCor

3:

Licensee

management

attention

to and involvement in nuclear

safety or safeguards

activities resulted in an acceptable

level of

performance;

however,

because

of the NRC's concern that

a decrease.

in

performance

may approach or reach

an unacceptable

level,

NRC will

consider

increased

levels of inspection effort.

~Cate

or

N:

Insufficient information exists to support

an assessment

of licensee

performance.

These

cases

would include instances

in which

a r'ating could not be developed

because

of insufficient licensee

activity or insufficient

NRC inspection.

The

SALP Report

may include

an appraisal

of the performance

trend in a

functional area for use

as

a predictive indicator.

Licensee

performance

during the assessment

period should

be examined to determine whether

a

trend exists.

Normally, this performance

trend should only be used if

a definite trend is discernible.

The trend, if used,

is definedas:

~lm rovin

Licensee

performance

was determined to be improving during

the assessment

period.

~Dec111fnin

Licensee

performance

was determined

to be declining during

the assessment

period,

and the licensee

had not taken meaningful

steps to

address this pattern.

IV.

PERFORMANCE ANALYSIS

A.

Plant 0 erations

1.

A~nal sis

Evaluati'on of this functional

area

was based

on the results of

12 routine inspections

and

1 special

(augmented

team)

inspection

by resident

and regional

inspectors.

Enforcement history in this functional

area

was comparable

to

that of the previous

assessment

period.

One violation involved

an equipment configuration control problem,

one involved

multiple failures to document shift turnover log reviews

as

required

by procedures,

and one involved the failure of a

non-licensed

equipment operator'to

perform and to document

required

rounds.

The licensee

took strong disciplinary action

against

the equipment operator for his misconduct

and applied

a

programmatic

approach to ensure that other equipment operators

clearly understood their assignments

and were performing and

documenting

them completely.

The violations were not repetitive

or otherwise greatly significant from a programmatic

or safety

standpoint.

The number of events that required submittal of licensee

event

reports

(LERs) continued to decline in this functional area.

One

LER corresponded

to the violation involving configuration

control, another

was

a voluntary report of an operator

equipment

manipulation error,

and

a few more involved fire protection

program activities, typically incomplete implementation of

required compensatory

measures.

This last category

appeared

slightly improved in that fewer events

occurred

compared to the

previous

assessment,

but events

were clustered

in the middle of

the current period.

In responding

to these

events,

management

,appeared

properly focused

on the

need to reduce

the administrative

burden

on plant operators,

rather

than

make it more complex,

so

that operators

could concentrate

on monitoring the reactor

and

its associated

safety

systems.

Only two reactor trips occurred in the entire period,

both

on

Unit 2.

This performance

compares

favorably to the four Unit 1

trips and two Uni't 2 trip signals

(no rod motion) that occurred

during the previous

assessment

period.

Both current reactor

trips were caused

by random equipment failures.

Both units operated

almost continuously throughout the

SALP

period,

except for a scheduled

Unit 2 refueling outage

in the

last

2 months.

Still, operators

were occasionally challenged

to respond to plant transients.

These

included both Unit 2

reactor trips,

one of which was corhplicated

by a significant

loss of control

room instrumentation

from the initiating event.

By following procedures

and taking appropriate actions,

operators

safely recovered

from this event. despite

the complications.

Other transients

included

a substantial

Unit

1 power reduction

to re-isolate

the ice condenser,

a Unit 2 thimble tube leak,

and

a couple of "Unusual

Event" conditions

caused

by electrical

faults.

Operators

also

responded

well (conservatively

and

without any error) to these

events.

Likewise, routine plant

startups

and shutdowns,

though few, were all completed

uneventfully.

On the other hand,

although equipment configuration

control errors were rare

and only once approached

the level that

calls for mandatory

LER reporting,

some lesser errors did occur

late in the period.

These

included making different components

in opposite trains concurrently inoperable,

contrary to the

licensee's

administrative control practices;

mispositioning

a

diesel

control air dryer valve; installing locks

on essential

service water valves in a way that did not prohibit valve

operation;

and starting

a recirculation fan instead of a recombiner.

The licensee

documented

each of these

occurrences

for detailed

corrective action review,

and in several

cases,

applied the

Human Performance

Evaluation

System

(HPES) to ensure

consistency

and thoroughness

in assessing

root cause.

5

Operations

Department

management

was actively involved in the

assurance

of quality of performance

in this functional area.

This was evident in mariagement's

consistent,

safety-conservative

operating philosophy in dealing with issues,

in their swift,

strong action to deal with an auxiliary operator

who was delinquent

in performing his duties,

and in their continued insistence

on

a high standard of formality and decorum in control

room

operations

and communications.

The licensee's

command

and

control during plant manipulations

were uniformly excellent.

The plant manager

continued

a policy of being personally present

in the control

room for significant scheduled

evolutions,

whatever the day or hour.

The time spent

by corporate

management

onsite,

including direct

observation

and assessment'in

the control

room,

was substantially

increased

during this appraisal

period.

The Vice

President-Nuclear

was normally at the plant at least

one day

each

week.

This executive

was present

on both occasions

when

electrical faults caused

"Unusual

Event" condit'ions

and was able

to personally

observe

the response

of his staff to these

events.

Licensee

management

kept abreast of plant operating

parameters

and trends,

both by direct observation

and by monitoring systems

of data collection

and reports.

The licensee's

approach to the resolution of technical

issues

from a safety standpoint related to operations

remained

sound

and conservative.

When questions

arose

concerning

the status of

post-maintenance

testing

on check valves

one day after

the

Unit

1 startup

from refueling (a few days into this assessment

period), operators

immediately returned the unit to Mode

5 while

the situation

was studied

and rectified.

Established

policy to

limit interactions with safety

components

(inspections,

tests,

repairs, etc.) to

a single train served to unburden shift

personnel

from having to make frequent interpretations

of

operability interfaces

and implications.

Likewise, continued

progress

on the computerized

"clearance

permit" system

served

to reduce

the potential for error inherent in developing

clearances

on

an ad hoc basis.

One apparent

counter-example

to

the general

tendency to expeditiously

move to

a conservative

plant mode to resolve questions

occurred.

This involved a

delayed decision to take Unit 2 to Mode

5 in January

1990 when

problems

were encountered

with the performance of the main steam

isolation valves.

During the delay,

however,

the operability

of these

valves

was repeatedly

demonstrated

while. the problem

(condensate

collection in the operating cylinder) was studied.

Throughout the

SALP period,

housekeeping

and the material

condition of the plant improved, but did not achieve

exceptionally

good levels.

Plant lighting was poor early in

the period but improved with an upgrade

program the licensee

started

in late

1989.

Some

examples of poorly lighted areas

remained

through the

end of the period.

The licensee

had an ample operating staff, with licensed

personnel

assigned

to operating shifts well in excess

of the requirements

of Technical Specifications.

The Operations

Department

made

very limited use of overtime.

A five-shift rotation

was used,

with a new schedule

of 12-hour shifts being

implemented in the

middle of the assessment

period (February

1990) after more than

80 percent of the affected staff vote'd to endorse this schedule.

The licensee carefully prepared for the transition to 12-hour

shifts,

and potential

problems (overtime scheduling

and control,

"shiftwise" frequency for activities, etc.) were averted.

Further,

the licensee

conducted

continuing assessments

to

determine whether personnel

exhibited

any loss of alertness

late

in the extended shifts.

The licensee

found no such indications.

The training and qualifications

programs for personnel

performing

in this functional

area

appeared

to be effective and to contribute

to hi'gh-quality performance.

Unit

1 operated this cycle and

utilized

a reduced

primary coolant

system pressure/temperature

with no associated

problems.

Likewise,

as previously noted,

the

licensee

conducted

scheduled

plant evolutions including startups,

shutdowns,

and major power-level

changes without

a single

significant operational

error.

Personnel

made

few errors,

but

as previously noted,

personnel

did make. some errors in equipment

.

configuration control.

One

such error resulted in one of the

violations, which was also

a subject of a management

meeting

between

NRC Region III staff and the licensee early in the

assessment

period.

Through the middle of the period,

configuration control appeared

to be excellent.

Then, late in

the period,

a few more errors of minor significance occurred.

During this assessment

period, the plant control-room simulator

and

a number of operating,

off-normal,

and emergency

procedures

for the plant were exercised

by an

NRC inspection

team.

The

inspectors

found the procedures

generally effective and free of

significant flaws.

The simulator remained

a major, asset

in the

overall training and qualification of the staff.

2.

Performance

Ratin

The licensee's

performance is rated Category 1'n this area.

The licensee'

performance'as

rated Category

1 during the

previous

assessment

period.

3.

Recommendations

None.

B.

Radiolo ical Controls

l.

~Anal sis

Evaluation of this functional area

was based

on the results

of seven

inspections

by regional

inspectors

and observations

by resident inspectors.

Enforcement-related

performance

in this area

was good.

One

Severity Level IV violation was identified.

Although this

violation did not constitute

a programmatic

breakdown

in licensee

radiological controls, it involved a weakness

in pre-job planning

and the licensee's

review of a contracted

safety valve testing

job which caused

a minor injury, hot particle spread,

and

personnel

and area contaminations.

Staffing, training,

and qualifications were generally

good.

The staff turnover rate for RP was very low; thus, the experience

level increased.

However, the turnover rate for chemistry

technicians

was high.

The licensee

continued to reduce its

dependence

on contract

RP technicians.

The assignment

of an

ALARA (as

low as reasonably

achievable)

representative

to the

planning/scheduling

staff was

an improvement.

J Overall,

managem'ent's

involvement in ensuring quality showed

significant improvement in the support of radiological controls

at the plant manager

level during the

second half of the assessment

period.

The licensee

has

improved the

Use of the radiological

awareness

reporting

system to record,

investigate,

and initiate

c'orrective action

on radiological

problems identified by station

personnel

and has initiated an aggressive

program for hot

particle

and contamination

controls

The licensee is continuing

to make progress

on actions to address

weaknesses

identified in

the maintenance

team inspection

as evidenced

by improved

integration of ALARA/RP controls into the maintenance

process.

An exception

appeared

to be the safety valve testing work

previously noted.

Management

weakness

was also noted in the

event involving low-level iodine exposure

to a number of workers

in containment that resulted

from poor communication

between

the

~ operations

and radiation protection groups.

This was

a recurrent

problem,

also

noted in the previous

assessment

period.

This

poor communication

also

appeared. to be

a factor in the

somewhat

fragmented responsibility for oversight of releases

through the

turbine building sump.

Management

has

supported

a good water

chemistry program that conforms to industry guidelines,

and its

monitoring of secondary

water chemistry

and data handling

has

improved.

The licensee

addressed

most of the inspection

concerns identified

during this period,

as evidenced

by the implementation of the

valve recovery

program to reduce

leaking valves,

making

'perational

a second whole-body counter,'pgrading

methods of

counting

and documenting

smear surveys,

improving laboratory

quality assurance/quality

control (gA/gC) and chemistry parameter

trend charts, initiating a training program for long-term

contract radiation protection technicians,

and addressing

concerns

related .to personnel

contamination

events originating

at the upper

and lower containment exit control

points'he

licensee's

approach to the identification and resolution

of technical

issues

was generally

good.

Personnel

contamination

events

(PCEs)

were occurring at

a significantly lower rate in

1990 compared with 1989.

A high percentage

of PCEs appeared

to

involve hot particles,

but this may be

a result of the licensee's

improved hot particle identification program.

The licensee

also

significantly reduced

contaminated

areas.

The total station

dose in 1989 was 534 person-rem,

indicating adequate

performance.

Reported liquid and gaseous

radioactiv'e effluents were well

within Technical Specification limits, and

a downward trend in

the generation

of solid radwaste

was evident,

No transportation

events

were identified.

Inspectors

noted performance

weaknesses

were evident in the events that involved the containment

iodine

exposures

and the safety valve test.

The licensee's

performance

in the nonradiological

confirmatory

measurements

program was good, with 27 agreements

in 33

comparisons.

After instrument recalibration, this figure

improved to 32 agreements

in 33 comparisons.

The licensee's

performance

in the radiological confirmatory measurements

program was fair, with only 63 agreements

in 85 comparisons.

.Eighteen of the disagreements

were caused

by the insensitivity

of -the licensee's

counting

systems

which resulted

in failure to

identify the radionuclides.

The licensee

installed

a new,

improved system,

which should

be operational

early in the next

assessment

period.

Split samples of liquid radwaste

analyzed

by

a licensee contractor

agreed

in all five comparisons.

The

Radiological

Environmental Monitoring Program

(REMP) appeared

to

be operating

in accordance

with regulatory requirements.,

and-

equipment

was well- maintained.

However,, the licensee's

uncertain

knowledge regarding the

use of the local groundwater aquifer for

drinking water was

a weakness.

2.

Performance

Ratin

The licensee's

performance is rated Category

2 in this area.

The licensee's

performance

was rated Category

2 in the previous

assessment

period.

3.

Recommendations

None.

C.

Maintenance/Surveillance

l.

A~nal sis

Evaluation of this functional

area

was based

on the results of

12 routine inspections

performed

by resident

inspectors

and

5

routine or special

inspections

by regional

inspectors,

including

a December

1989 maintenance

team inspection.

Two Level

IV violations were issued during the assessment

period

compared to eight during the previous period.

One violation was

for failing to take required

compensatory

action for a

surveillance test failure.

The second

involved multiple examples

of failing to follow procedures;

one of the examples specifically

tl

involved maintenance activities and two examples

involved

surveillance activities.

Mhile the violations were not of

major safety significance,

occasional

examples of procedural

violations were also noted during the previous

SALP period.

Furthermore,

during

a Safety System Functional

Inspection

(SSFI)

conducted

near the

end of the

SALP per'iod, failures to follow

procedures

in 'maintenance

and surveillance

were again observed.

The number of events in this functional area,

requiring submittal

of LERs,-decreased

slightly during the appraisal

period.

During

the current period,

a few of the

LERs were caused

by equipment

problems;

some were caused

by procedure deficiencies,

and the

remainder resulted

from human errors.

As'during the previous

period, essentially all of the reportable

events

involved

surveillance testing.

The current events

were not repetitive

and lacked generic or programmatic implications.

Further,

none

of the events

in this functional area

had major safety

significance.

In the first half of the assessment

period,

management

involvement

in maintenance'as

noted

as weak;

however,

improvements

were noted

in the latter part of the period.

The maintenance

program contained

a number of programmatic

weaknesses

as noted in the following examples.

The preventive

"maintenance

program focused principally on equipment

covered

by the technical specifications;

only limited consideration

was given to vendor recommendations

for plant equipment.

Significantly greater

maintenance effort was given to corrective

maintenance

rather than

maintenance

to prevent

or reduce

equipment fai lures.

At the time of the maintenance

team

inspection,

the absence

of an integrated

approach to planning,

scheduling,

and coordination for corrective

and preventive

maintenance

was

a contributor to. unnecessary

equipment

downtime

and

a large backlog of non-outage

corrective maintenance

job

orders.

Adding to this problem,

planners

and schedulers

did not

have formal job descriptions

and were not thoroughly trained in

their tasks.

There were also

examples of work histories

that were poorly recorded

on job orders,

which detracted

from

the ability to accurately trend problems

and develop

good root

cause

analysis of component failures'lso,

post maintenance

test requirements

were not always sufficiently specific

or detailed.

In December

1989, there

were

a significant

number of steam,

water and oil leaks noted in the plant

during the maintenance

team inspection.

For example,

there

were

numerous

packing leaks; oil, fuel

and water leaks were

noted

on the emergency diesel

generators

and

a large

number of

minor fluid leaks were noted in the auxiliary building.

Some of the leaks involved contaminated

water;

however,

plastic containments

were in place to contain the leaks

and

minimize radiological problems.'n

the latter part of

the appraisal

period,

some

improvements

were noted in the plant

material condition as well as maintenance

support

systems

such

as uniform setting of priorities and centralizing

preventive

maintenance activities.

10

Examples of positive management

involvement included incorporating

industry experience

with check valve problems into applicable

maintenance

procedures,

conducting

a broad outage job order

review when

one job was found that lacked

a post maintenance

test,

and performing

a generic

review of implications of "Bellevilie"

washer decompression

in some motor operated

valve applications.

The quality of surveillance

procedures

remained

good,

and

developed

maintenance

procedures

were adequate

in most cases.

The surveillance

program which verified component availability

was performed in a timely manner with good procedural

control.

Findings

showed

a high degree of reliability for safety related

equipment.

However,

maintenance

jobs were frequently performed

without detailed

procedures.

The licensee

continued to rely on

first line supervisors

to provide additional

needed details

for

a given job rather than providing formal procedures

or

instructions to include these details.

The lack of maintenance

procedures

occasional,ly resulted in poor,

incomplete,

or

incorrect work.

A specific example

involved the charging

pump

seal

replacement.

For maintenance activities conducted late in the appraisal

period,

some jobs

showed evidence of improved planning;

however,

there

was also

some evidence of poor planning

and scheduling of

electrical

maintenance activities.

There were cases

when

personnel

failed to adhere to procedures,

or excessive liberties

were taken with procedural

intent as noted in the violations.

Late in the appraisal

period the licensee

placed

an increased

emphasis

on improving compliance to maintenance

and test

procedures;

however,

there were still instances

of weak

maintenance

procedures.

The licensee's

approach to resolution of technical

issues

from a

safety standpoint

was of mixed quality.

When the licensee

recognized

or believed that

an issue

had potential

safety

significance,

a conservative

approach

was generally taken.

Examples include (1) the approach to the incore tube thinning

problem, (2) development of effective preventive maintenance

for

vital instrument electrical

power supplies,

and (3) performance of

special

main

steam isolation valve monitoring processes

to ensure

timely identification of potential degradation.

Conversely,

the licensee

sometimes

did not initially respond

with a broad or conser'vative

approach.

Examples of this include

the failure to recognize

the implications of the main steam

isolation valve test failures of June

1989

and January

1990,

and questionable justification for short-duration

Type

C pressure

drop tests'he

licensee

changed its approach

on each of these

items

upon questioning

by NRC.

Because

the main steam isolation

valve test results

were not given adequate

attention,

the

cause-effect

relationship

between

dump valve leakage

and poor

main

steam isolation valve performance

was not recognized

and

known dump valve leaks

had low priority for repair.. There were

li

S

also

a few instances

of rework because initial repair attempts

were unsuccessful,

and the licensee

did not always thoroughly

investigate

the root cause of equipment failures.

Staffing in this functional

area

was generally adequate.

However, the license relied heavily on contracted

workers to

perform substantial

amounts of less 'complex maintenance

work.

This caused

or contributed to work schedule

coordination

problems

and to

some instances

of job-related

paper work duplication

and

confusion regarding work status.

An example of this problem

involved the work on the breaker for the emergency

incoming feed

for emergency diesel

generator

2AB.

There were occasional

examples of 'poor work practices

by both plant and contractor

personnel.

For example,

undocumented

temporary repairs

were

installed, incorrect torque values

were used,

post-work area

inspections

were omitted and areas

were left dirty, and

some

detailed procedural

controls (including administrative controls)

were not followed.

A licensee

sponsored

staffing study

recommended

converting

some

contract workers to permanent

maintenance

workers.

The degree

to which this recommendation will be implemented,

and the

schedule,

were not immediately established

but remained

in

development at the close of the assessment

period.

Overtime was

'enerally

well controlled

and not excessive.

NRC guidelines for

control of overtime were rarely approached.

Mhen brief instances

of demand for high overtime arose,

they were properly reviewed

and approved.

The licensee's

training and qualification programs resulted

in

a force of knowledgeable

site workers for the performance of

maintenance

and surveillance tasks.

Overall the skill level of

plant craft personnel

was very good.

Expertise of other staff

(e.g.,

schedulers,

supervisors)

.was adequate.

Mhile chronic programmatic

weaknesses

were noted in the

maintenance

area early in the appraisal

period,

the licensee

planned

several

maintenance

improvement initiatives.

However,

implementation of the licensee's

planned

program

improvements,

including the aspects

of the reliability centered

maintenance

effort, have

been

slow, deliberate

and have not yet been fully

effective at improving the maintenance

process.

2.

Performance

Ratin

Licensee

performance is rated Category W3" with an improving

trend in this functional area.

The previous rating was

Category

2.

  • Rating changed

by the Regional Administrator from a Category

2 to

a

Category

3 with an improving trend.

.12

n

3.

Recomendations

Accelerated

implemeptation of all maintenance

improvement

programs

and increased

RIII inspection after 9-12 months.

D.

Emer

enc

Pre aredness

1.

~Anal sis

Evaluatiop of this functional

area

was based

on three

inspections

by regional

inspectors

and observations

made

by

resident

inspectors.

Enforcement-related

performance

remained excellent.

No violations

were identified during this assessment

period or the previous

period.

Management's

involvement in assuring quality continued to be

very good.

Corporate staff members

are assioned

to conduct

in-depth quarterly internal audits of selected

program areas.

Management's

support of the emergency

preparedness

program was

excellent,

and program requirements

have

become part

of= the

normal plant survei llances

and operations.

Program

enhancements

by the licensee

during this assessment

period included (1) the

implementation of monthly drills, (2) creation of a permanent

scenario

development

committee,

(3) agreements

with a second

hospital to provide medical

support facilities,

and (4) several

additions

and upgrades

to emergency

response facilities and

equipment.

Staffing of the emergency

response

organization

(ERO) was

excellent throughout this assessment

period.

The licensee

maintained

a roster of qualified personnel

available to fill

all

key positions in the

ERO.

The ability of licensee

personnel

to respond

was well demonstrated

by their timely response

and

activation of emergency

response facilities during the

May 24,

1990, "Alert" declaration.

The emergency

plan training program

was good.

The program

provides extensive initial training and has established

practical

factors demonstrations

required,

which includes completion of

position-specific "qualification cards" for all

ERO members.

Periodic participation of

ERO member s in drills or exerci ses is

also required.

These

requirements

have

been

met for all

ERO

members.

Inspectors

found that annual retraining requirements

were less clearly defined

and identified

some ambiguity between

program areas.

The licensee initiated immediate actions to

clarify the ambiguity between initial and annual training

programs

and to clearly define emergency

preparedness

retraining

requirements.

They also

have

an aggressive

schedule

to completely

review all emergency

response

training and to resolve

any

identified concerns.

13

The l.icensee's

resolution of technical

issues

from a safety

stand-point

was excellent

and consistently conservative.

In

response

to emergency

plan activations,

the licensee

conducted

post-activation

reviews for each event to identify areas that

could be improved.

Items identified through these

reviews

of real events,

as well as critiques of drills and exercises,

internal

and external

audits,

and inspections,

were effectively

tracked

and appropriately

resolved

by the licensee

in a timely

manner.

The licensee's

response

to operational

events

was excellent.

A

total of eight events

were classified

and reported pursuant to

10 CFR 50.72 as

emergency

plan "Unusual Events."

One event

involving an explosion

and fire in the plant switchyard

on

May 24,

1990,

was upgraded

to an "Alert" when the licensee

decided to reduce Unit 1 power output to minimize the risk of a

plant transient during necessary

switching.

Each event

was

correctly classified in a timely manner.

Appropriate

notifications to the State.,

counties,

and the

NRC were

made

within the required time limit for each event.

The licensee

effectively utilized the emergency

response facilities,

procedures,

and organization to evaluate

plant conditions

and

anticipated actions to successfully mitigate the consequences

of

the

May 24,

1990,

"Alert".'he

licensee

kept its emergency

plan

and implementing procedures

current by conducting appropriate

periodic reviews.

When

necessary,

the licensee

made revisions in a timely manner

and

appropriately distributed the revisions.

Emergency

response

facilities and equipment

have

been well maintained

and are

inventoried,

inspected,

response

checked,

and tested for

operability, in accordance

with a well-defined surveillance

program.

The licensee

demonstrated

an excellent

emergency

response

capability in both emergency

exercises

evaluated

during

this assessment

period.

Inspectors

identifi'ed no exercise

weaknesses.

The licensee

greatly improved exercise

realism by

including the

use of a plant simulator with the

1989 exercise.

The

1990 exercise

was consider'ed

complex

and particularly

challenging

since it was conducted off hours,

was initiated at

0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />,

and was not announced

to station

employees

or State

and county participants.

2.

Performance

Ratin

The licensee's

performance is rated

a Category

1 in this area.

The licensee's

performance

was rated

a Category

1 during the

previous

assessment

period.

3.

Recommendations

None.

~Securit

1.

~Anal sis

Evaluation of this functional area

was based

on the results of

four inspections

conducted

by regional'nspectors

and

'bservations

made

by the resident

inspectors.

Enforcement-related

performance

improved during this assessment

period

and is considered

excellent. 'nspectors

identified no

violations during thi s assessment

period while they identified

four violations during the previous period.

Management's

involvement in assuring quality was excellent.

Senior management

aggressively

supported security initiatives as

evidenced

by (1) upgrades

of the security

system,

(2) reduction

in personnel

errors involving security,

(3) ample allocations of

both personnel

and equipment resources,

(4) extensive

management

overviey and thorough planning,

and (5) self-audits

and

surveillances

by quality assurance

and security personnel.

The

high level of security awareness

that exists within the plant

work .force contributed to

a positive attitude towards security

and

a reduction, i'n errors.

1

The licensee's

approach

to th'e identification and resolution of

technical

issues

was excellent.

The licensee

upgraded or

replaced

equipment before it reached

the end of its lifespan.

The licensee's

program included upgrades

such

as (1) the purchase

and installation of new state-of-the-art

closed circuit television

(CCTV) cameras,

including switching units

and replacement

of

existing cabling with fiber optics; (2) implementation of a

new

radio communication

system;

(3) upgrading of perimeter intrusion

detection

system (IDS); and (4) installation of a "video capture"

assessment

system to aid in perimeter

alarm assessment.

In

addition, the licensee

developed

a 5-year security equipment

replacement

plan to assist

in continuous

upgrading of security

equipment,

taking into consideration

maintenance

requirements

and performance capabilities of the current equipment.

This

plan will also

be used

as

a guide for replacement

and budgeting

for new equipment

before the equipment

reaches

the

end of its

lifespan.

These proactive efforts by the licensee

have reduced

the

number of false or nuisance

alarms

and

have greatly increased

the reliability of the detection

system

and assessment

capabilities.

The technical

coordination

and working

cooperation

between

the security

and the maintenance

work units

was excellent.

The overall'effectiveness

of the

security-related

equipment

was attributed to diligent and

competent technical

maintenance

support.

However, inspectors

raised

a concern

about the timely repair of security lighting.

Although lighting requirements

were maintained,

some security

lights were not repaired

in a timely manner

and

no preventive

maintenance

program existed for security lighting.

15

The licensee's

attention to security issues

is excellent.

Security

and site 'management

aggressively

pursue

and evaluate

all issues that can strengthen

the security program.

This is

evidenced

by the involvement

and support of site management

to

significantly reduce

personnel

errors involving badge control

and unsecured

security doors.

The decline in personnel

errors

in security 'procedures

is the result of careful tracking and

trending by management

of not only the

number of incidents,

but

of the individuals involved, their employer,

and the responsible

department

head or contractor representative.

Individuals

responsible

for each event,

as well as their respective

supervisors

and department

heads,

are held personally accountable.

In

addition, .the licensee

analyzes

each

event for root cause

by

taking into consideration

human factors

and equipment.

The licensee's

security staffing and other staff,.resources

dedicated to'he security organization

were ample

and

effectively utilized.

This was demonstrated

by the licensee's

internal security force structure that effectively blends

the

utility and contractor organization into elements that are

each

responsible

for implementing specialized

portions of the

security program,

including portions of the fitness for duty

(FFD) program.

These

elements

operate

independently

but are

monitored by security management

personnel

who coordinate

the

effectiveness

of the overall security program.

The close

and

effective liaison established

between

the security contractor

and the licensee's

security managers

is

a major strength of the

program.

guality assurance

audits of the security program

make

a positive contribution to the security organization's

overall performance.

The audits are aggressive,

detailed,

broad

in scope,

and well documented.

As a result of management/employee

relations

programs,

the security force turnover rate for 1990 is

only about

3 percent,

which is the lowest rate yet achieved.

The licensee's

program for reporting required security events

and keeping the

NRC informed of security-related

issues

was

excellent.

Required reports

were accurate

and timely.

The

licensee's

program for logging security events

uses

appropriate

regulatory guidance,

was implemented

in a conservative

manner,

and ensured

good monitoring of potential

equipment

problems.

Security-related

records

were complete, well maintained,

and

readi ly'vai 1 abl e.

The training and qualification program for the security

organization

was generally

good and is well implemented.

The

licensee

has

completed,

a 2-year project of revising the

program to reflect up-to-date

industry guidelines.

Although

security is not subject to industry accreditation,

the licensee

undertook the revision to make security training methods

and

documentation

as consistent

as possible with other plant

department training methodology

and to provide

a more effective

means of conducting

and do'cumenting qualification of personnel.

16

f

The licensee's

fitness for duty program

was upgraded

and

implemented during this assessment

period in accordance

with 10.

CFR Part

26.

The licensee's

program

was

implemented

2 months

ahead of the required January

3,

1990,

implementation date.

2.

Performance

Ratin

H

The licensee's

performance

was rated Category

1 in this area.

The licensee's

performance

was rated Category

2 in the previous

assessment

period.

3.

Recommendations

None.

En ineerin /Technical

Su

ort

1.

~Anal sis

Evaluation of this functional

area

was based

on two routine

inspections,

one special

inspection,,

and

one team inspection

by

regional inspectors,

several

inspections

by resident

inspectors,

one

enforcement

conference,

a safety

system functional inspection

(SSFI)

team inspection,

and interactions

between

the licensee

and the staff of the Office of Nuclear Reactor Regulation

(NRR).

Enforcement history consisted

of five Level IV violations

reflecting the weaknesses

identified by several

inspectors

throughout this assessment

period.

There were few reportable

events

d'uring this assessment

period:

Among events that did not reach the requirement for reporting,

however,

were two cases

which indicated that the licensee

did

not always deal with matters of .lesser

significance

as effectively

as reportable matters.

Management's

involvement in ensuring quality in this functional

area continued to be of a mixed nature.

On the negative

side,

the licensee

had not effectively dealt with certain

problem

areas.

One area

was the lack of proper engineering

involvement

in activities as evidenced

by the interruption of on-going

activities during the replacement of control

room instrumentation

distribution 125-amp inverter breakers

due to breaker

incompatibility and wiring drawing deficiencies,

and the

inadequate

testing of the diesel

generator

undervoltage

relays,

due to inadequate

procedure

guidance

and test equipment.

A

further weakness

was the continuing identification of calculational

and design verification errors.

For example,

a pipe support

where the engineer initially failed to account for bending

in a pin,

and

a pipe support evaluation

where the most critical

load directions

were not considered.

Although subsequent

analysis

demonstrated

the loads to be acceptable,

the failure to

perform

a proper evaluation

demonstrated

a lack of attention to

detail.

Similar findings in the

ar ea of attention to detail

17

were noted by the

SSFI

team inspection late in the assessment

period.

Numerous deficiencies

existed in the plant's fire protection

safe

shutdown

program.

These deficiencies

(inadequate

emergency

lighting evaluation

and inadequate

design control) continued to

exist even after

a number of years of program development

and

were identified by a licensee

audit conducted in preparation for

the

NRC team inspection of safe

shutdown capabilities.

Additional

items identified by the

NRC ( shortly after the

SALP assessment

period ended)

and not identified by the licensee

included

inadequate shift staffing procedure

regarding

minimum staffing

to perform post fire safe

shutdown procedures,

human factors

problems

in procedures,

and the potential

loss of both

units'ontrol

room

HVAC systems.

Cumulatively, the deficiencies

indicated

an inadequate

assessment

of applicable

Appendix

R

requirements,

and

a lack of attention to details

Positive

management

influences,

in response

to

NRC concerns

in

the last assessment

period,

were evident in the continued

implementation of organizational

changes at the corporate

level to

create

an engineering division dedicated to the

D.

C.

Cook plant,

stationing of several

additional corporate

engineering

personnel

on

site,

and the implementation of an independent

audit of the design

change

and control program.

Nevertheless,

the evidence indicates

that it is too early to determine

the effectiveness

of these

programs.

Other initiatives included taking an industry leadership

role in

designing

and seismically testing "temporary" scaffolding,

installing on-line steel alloy verification equipment,

equipment

environmental qualification, the prioritization and scheduling

of work, and the implementation of the requalification program,

where

a marked

improvement

was noted over the

SALP 7 assessment

period.

In the area of Appendix R, strengths

included the

reorganization

of the

Emergency

Remote

Shutdown

(ERS) procedures,

the

use of the

ERS procedure

status

check sheets,

and the fire

protection engineering

analysis related to fire detection,

suppression,

and fire barriers.

Engineering

and technical

support of licensing actions

was of

mixed quality, with the inaccurate

or incomplete submittals to

the

NRC appearing

to be caused

by a breakdown in communication

between

the licensee's

corporate

engineering

personnel

and the

site staff.

The licensee's

approach

to the identification and resolution of

technical

issues

from a safety standpoint

has

been of mixed

quality.

A conservative

emphasis

on safety

was evident in the

licensee's

approach to such issues

as

a potential

adverse

performance

trend for diaphragm-type

valves in heat-traced

systems,

a repetitive nonessential

service water

(NESW) seal

failure phenomenon,

the potential for inadvertent

moderator

dilution inherent in the chemical

and volume control

system

(CVCS) crosstie modification,

and

a "hydraulic lock" condition

discovered

in manipulation of NESM isolation valves.

18

'nstances

occurred,

however,

in which the licensee failed to

identify the problem or appeared,

at least initially, to misjudge

or underestimate

the 'technical

or safety implications of issues.

Examples

included the susceptibility of the auxiliary feedwater

system to deadheading

one train by a

common miniflow line, the

implications of the main steam isolation valve performance

change,

the discrepancies

between

the size

and setpoints of the

thermal

overload trip devices in safety-related

motor circuits,

and the applicability of Regulatory

Guide 1.97 to power supply

separation

for the wide-range

steam generator

level instruments.

However, the licensee

generally responded

appropriately

when

issues

such

as these

were presented.

Staffing for engineering

and technic~1

support

was ample,

pnd

personnel

were adequately qualified.

The licensee's ability to

apply these

resources

effectively, however,

remained

somewhat in

question.

During this assessment

period,

the licensee

implemented

initiatives involving corporate

engineering

support reorganization

and onsite implementation of a system engineer

program.

Both

initiatives appear to have long-range

promise,

but short-term

effects were not remarkable

and were partially offset by early

communication

and coordination hurdles inherent in the nature of the

changes

themselves.

Training and qualification program activities were generally

adequate.

The licensee

implements

a defined training program

across multiple disciplines,

including technical staff training.

The licensee's

requalification program was effective in preparing

the operators for the NRC-administered

examinations.

However, for

initial examinations,

the program

showed weaknesses

in the

simulator training of new operators.

This weakness

was reflected

in a low passing

rate

(59 percent) for the first examination

using the plant specific simulator.

Improvements

in the training

program, especially in the exercise of the emergency

operating

procedures,

resulted in an 89 percent passing

rate late in the

assessment

period.

2.

Performance

Ratin

The licensee's

performance

is rated Category

3 in this area.

The

licensee's

performance

was rated Category

2 in the previous

assessment

period.

3.

Recommendations

Design control

needs

improvement

as does support to

maintenance.

Region III needs to increase

inspection.

G.

Safet

Assessment/

ualit

Verification

l.

~Anal sis

This functional area

was evaluated

based

on results of twelve

inspections

by the resident

inspectors

and several

inspections

19

n

by regional

inspectors.

In addition, the

ARC staff's reviews of

licensee

submittals

and requests

for amendments

to the operating

licenses

were considered.

The enforcement history in this functional

area consisted

of one

Severity Level III violation and four 'Severi-ty Level

IV violations.

This is an increase

in enforcement activity compared to the two

Level IV violations noted in the previous

assessment.

The Level

III violation involved the long-term conditional inoperability

of the Unit 2 turbine-driven auxiliary feedwater

pump, for which

a $75,000 civil penalty was

imposed.

The violations all involved

inadequate

or untimely corrective actions for identified problems.

They were otherwise dissimilar,

and

none appeared

programmatic

in nature.

The Level III violation involved

a program deficiency

which no longer existed during the current assessment

period.

The only LERs in this area

were related to three of the

violations.

, The involvement of the licensee's

management

in assuring quality in

this functional

area

was mixed.

On the positive side,

an

organizational

change

elevated

the plant's Safety

and Assessment

Department

so that it reported directly to the plant manager.

The plant's

senior

managers

stayed well informed about

activities'nd

results

by monitoring performance

information and by active

participation in both the Problem Assessment

Group

(PAG) reviews

and the Plant Nuclear Safety

Review Committee

(PNSRC) activities.

The information derived in these

evaluations

and reviews appeared

to be appropriately applied in nearly all cases.

The occasional

recurrence

of a previously identified problem was

an exception.

Management

coptinued to support various self-improvement

initiatives, several

of which were carried

over from the previous

appraisal

period, including: (I). computerization of long-range

planning processes

and of an integrated

information management

program; (2) broadening of the Quality Maintenance

Team program;

and, (3) retaining of technical consultants

for critical self-

assessments.

One example of the latter initiative was the audit

by CYGNA Energy Services of design practices for the Cook plant.

The lengthy duration of some of these

self-improvement

programs

raised questions

about the amount of resources

and management

commitment applied to bring them to completion.

Management

took

strong steps to "reclaim" the auxiliary building after problems

were identified with material condition and storage of extraneous

materials.

The licensee

continued to operate

a large-volume low-threshold

corrective action program, with a focus

on timely classification

and segregation

of potentially significant items for higher-level

review.

The program retained

a focus

on the potential for

repetitive problems

and was sensitive to identification of

possible

adverse

trends.

In the Appendix

R area,

however,

the deficiencies identified during the most recent

NRC inspection

(conducted shortly after the

SALP assessment

period ended)

were

similar to

some

1982 Appendix

R post-fire safe

shutdown inspection

'20

findings.

For events potentially involving personnel

error, the

licensee

used the

Human Performance

Evaluation

System

(HPES) to

evaluate

selected

items.

However, the reviews were not always

completed in a timely manner

because

the position of HPES

Coordinator

was temporarily vacant

on two occasions.

Further,

management

did not follow HPES reviews closely

and was unaware

that

some reviews

remained

"open" for more than

a year.

One problem which the licensee

apparently did not adequately

address

involved design calculation deficiencies.

Even though

problems

were recognized

by the licensee

as early as

1987,

the

licensee did not initiate prompt corrective actions

nor thoroughly

apply additional

adequate

verifications of design calculations

during the current assessment

period.

As

a consequence,

some

design assumptions,

references,

and calculations

contained

avoidable errors.

It was noted that calculations

performed

later in the assessment

period did not contain errors similar to

those

noted at the beginning of'he period.

However,

implementation

of the verification process

remained

incomplete.

Further,

a

maintenance

self-assessment

from early

1988 contained

about

70

recommendations

for enhancements

or corrective actions.

Followup

on about half of these

was later judged to be incomplete

because

management

had chosen

not to implement them.

However, early in

the current appraisal,

the licensee

reversed this decision

and

undertook the actions

recommended.

The Quality Assurance

audit organization onsite

responded

to the

identified issue of maintenance

programmatic

weaknesses,

but was

not proactive in initially identifying problems.

Management

supported

QA by increasing

the surveillance of main'tenance

activities, in the latter half of the period.

The licensee

provided the quality control group with newly purchased

equipment,

and the training to operate it properly, for screening metal/alloy

components

during receipt inspection to detect potential

counterfeits.

Audit and surveillance activities by both the

QA and

QC groups

were independent

and technically oriented.

Technical expertise

in review of issues

was apparent

in the following activities:

(1) the

QA group identified incomplete "half-loop" training

coverage for maintenance

workers; (2) the Safety

and Assessment

group identified a potential

adverse

trend in fuse control; (3)

the

QA group noted

a lack of independent

substantiation

of

personnel

security background

checks

by one contractor;

and, (4)

the

QC group displayed

a conservative,

inquisitive attitude

,about

any anomalous

results

in alloy parts testing.

Early in

the assessment

period, neither

the

QA group nor the

QC group.

were programatically involved in the assessment

of work in

progress.

Work verification was being accomplished

instead

by a

"peer inspection"

program.

Inspectors

considered

administrative controls for this program

vague,

lacking sufficiently detailed

guidance

and acceptance

criteria to ensure effectiveness.

Additionally, the "peer

inspection" process

doesn't

provide the

same data for evaluation

21

that- would normally be available

from a guality Control Inspection

surveillance.

As a result,

the opportunity. for identification

of declining performance

trends

may not reach

management's

attention for implementation of appropriate

corrective action,

However,

no cases

of ineffective verification were

'noted.

During the assessment

period the overall quality of licensing

submittals

improved.

The sa'fety evaluations

supporting

the

license

amendments

almost always addressed

the criteria of

10 CFR 50.92 in sufficient detail.

The quality of licensing

submittals could be improved further by greater attention to

detai l.

A number of license

amendments

contained

minor editorial

errors.

The licensee

usually approached

resolution of technical

issues

in this functional area

from a conservative

safety standpoint.

At times,

the licensee's

proactive pursuit of issues

led to

prevention of problems or questions

which affected other licensees

as

was the case in their safety review under

10 CFR 50.59 to

address

a

new technique to test main

steam safety valves at

power.

The quality assurance

that the licensee

applied to the

ATMS (anticipated transient without scram) mitigating system

actuation circuitry (AMSAC) modification generally

met or

exceeded

the supplemental

gA guidance

given in Generic Letter 85-06.

On the other hand,

the licensee's

actions for NRC

Bulletin 85-03, involving motor operated

valve problems

appeared

designed

to meet

minimum requirements.

Thus,

most valves

remained

untested

against

the criteria of the Bulletin.

Information on technical

issues

was not always adequately

di sseminated

within the licensee's

organization.

As a result,

the corporate

Nuclear Safety

and Licensing group, which is the

designated

point of contact

on issues

for the

NRC Office of

Nuclear Reactor Regulation,

lacked current information on

some

relatively significant events at the plant.

In one case,

the

corporate licensing staff appeared

to have information (concerning

main steam

stop valve stroke timing problems)

which differed

from that at the plant site

~

Staffing remained sufficient and stable

in this functional area.

The onsite review committee

was properly staffed

and functioned

well. It included both strong

management

and strong technical

involvement.

The offsite review committee

was not evaluated.

Training and qualification of personnel

appeared

to be

a positive

factor in the identification and resolution of potential

problems

in this functional area.

Personnel

assigned

to quality

verification responsibilities

including craft personnel,

typically

possessed

technical

expertise

in the activity being examined.

Findings, therefore,

were usually founded

on technical merits.

22

A

2.

Performance

Ratin

The licensee's

performance

is rated Category 2"'in this area.

The licensee's

performance

was rated Category

2 during the

previous

assessment

period.

3.

Recommendations

None.-

V.

SUPPORTING -DATA AND SUMMARIES

A.,Licensee Activities

Unit

1

Throughout most of the assessment

period, Unit

1 of the

D.C.

Cook plant operated routinely at 100-percent

power.

The

assessment

period began at the

end of a refueling outage.

During the rest'f the assessment

period, Unit

1 shut

down only

once for a

3 day ice condenser

surveillance

in March 1990.

Unit

1 did not experience

any reactor trips during this

period.

No engineered

safety feature

(ESF) actuations

were

reported during the assessment

period.

There were

no

significant outages,

and only two events

occurred during

the assessment

period

as

summarized

below.

Unit

1 Si nificant Outa

es

and Events

/

On May 8,

1990,

a containment recirculation fan was

inadvertently started

which caused

the lower ice condenser

inlet doors to open,

and ice bed temperatures

increased

above

the technical

specification limit.

The reactor

power was

subsequently

reduced to 8 percent to allow personnel

entry to.

close the doors manually.

On May 24,

1990,

a fire and explosion occurred in the Unit 1,345KV

switchyard.

Power

was reduced to 62 percent to allow a breaker

to be removed

from service, as

a result of insulator

damage

and

an oil leak on

a transformer.

2.

Unit 2

Throughout most of the assessment

period;

D.C.

Cook, Unit 2,

operated routinely at 100-.percent

power and shut

down for

a refueling outage

on June

30,

1990.

The unit was shut

down for'

planned

3 day ice condenser

surveillance

in January

1990,

and remained

shut

down

an additional

16 days for repairs to the

steam generator

stop valves.

Unit 2 experienced

two reactor trips during the assessment

period.

Both trips resulted

from electronic

equipment

23

1

4'1

failures.

One enginee'red

safety feature

(ESF) actuation

was

reported. during the assessment

period.

Unit 2 Si nificant Outa

es

and Events

a.

The first Unit 2 reactor trip occurred

on August 14,

1989,

following 'a severe

undervoltage

condition

on the 120-volt

Control

Room Instrumentation Distribution Panel

No.

4 (GRID

IV).

The undervoltage condition, which occurred

when the

GRID IV input was transferred

from the non-Class

lE

alternate

supply to the normal Class

1E supply through

a

failed switching circuit, also resulted in a partial loss

of indication and control

used for post-trip recovery

(e.g., all wide-range

steam generator

level indication and

condenser

steam

dump control).

b.

On January

6,

1990, Unit 2 entered

into a planned

Mode

3

outage for ice condenser

surveillances.

During

steam generator

stop valve testing

on January

8,

1990,

stop valve closure times

on, three of the four stop valves

exceeded

the Technical Specification limit of 5 seconds.

The licensee

continued to test the valve's in Mode

3 until

January

11,

1990,

when the unit was placed in cold shutdown

in order to repair the valves.

The unit was placed

back in

service

on January

25,

1990.

On June ll, 1990,

a second

reactor trip was caused

by

a negative flux rate signal.

Although the licensee

was

unable to determine

the root cause of this signal,

a single

phase of the power supply to one group of rods

was found

electrically "open."

d.

On July 19,

1990, during

a refueling outage,

a fatal

accident occurred

near

an energized

4KV feeder.

A worker

was electrocuted,

and

a flash fire seriously burned the

three other

workers present.

B.

Ins ection Activities

Thirty-two inspection reports

are discussed

in this

SALP report

(July 1,

1989, through August 31,

1990)

and are listed below under

"Inspection Data."

Table

1 lists the violations by functional area

and severity levels.

Significant inspection activities are listed

below under "Special

Inspection

Summary."

l.

Ins ection Data

a.

Unit

1

Docket No. 50-315

Inspection

Reports

Nos.

89-21 through 89-23,

89-25

through 89-34,

90-02,

90-03,

90-05 through 90-08,

90-10

through 90-17,

90-19 through 90-21,

and 90-201

b.

Unit 2

Docket No. 50-316

Inspection

Reports

Nos.

89-21 through 89-23,

89-25

through 89-34,

90-02 through 90-08,

90-10 through 90-17,

90-19 through 90-21,

and 90-201

Table

1

Number of Violations in Each Severit 'evel

Functional

Areas

Unit

1

III

IV

V

Unit 2

III

IV

V

Common

III

IV

V

A.

Plant Operations

B.

Radiological

Controls

C.

Maintenance/Surveillance

D.

Emergency

Preparedness

ED

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/

guality Verification

TOTALS

2 ~

S ecial

Ins ection

Summar

1

1

1

4

3

10

a.

During August

15 through

18,

1989,

a special

Augmented

Inspection

Tea'm (AIT) conducted

a review of the

ci rcumstances 'surrounding

the Unit 2 reactor trip as

a

result of the undervoltage

condition

on the Control

Room

Instrumentation

Panel

(GRID) (Inspection

Report

Nos.50-315/89-25;50-316/89-25).

During December

4 through 22,

1989,

a special, Maintenance

Team Inspection

(MTI) was conducted

(Inspection

Report

Nos. 50-315/89-31;

50"316/89-31)

.

c.

During April 2.through 6,

1990, the annual

emergency

preparedness

exercise

was conducted

(Inspection

Report

Nos. 50-315/90-03;

50-316/90-04).

d.

e.

During March

13 through August 22,

1990,

a special

maintenance

inspection

was conducted

to assess

improvements

in maintenance

(Inspection

Report

Nos. 50-315/90-07;

50-316/90-07) .

During June

11-22 and July 9-13,

1990,

a Safety

System

Functional

Inspection

was conducted (Inspection

Report

Nos.50-315/90"201;

50"316/90-201).

25

C.

Escalated

Enforcement Actions

2.

On January

4,

1990,

an enforcement

conference

was held regarding

the violation of TS for the failure to ensure operability of the

turbine-driven auxiliary feedwater

pump for Unit 2 (Enforcement

Case

No. EA-89-252, Inspection

Report

No. 50-316/90-03).

A

Severity

Level III violation was issued

and

a $75,000 civil

penalty

was imposed.

On February

27,

1990,

'an enforcement

conference

was held

regarding

Main Steam

Stop Valve operability (Inspection

Report

Nos. 50-315/90-08;

50-316/90-08).

A Severity

Level IV

violation was i ssued with no civil penalty.

D.

Confirmator

Action Letters

None.

E.

Review 'of Licensee

Event

Re orts

Collectively,

26

LERs were issued during this assessment

in

accordance

with NUREG-1022 guidelines.

These

LERs are addressed

in,this

SALP 9 report.

Unit 1-LER Nos.

89009 through 89015

and

90001 through

90004

Unit 2-LER Nos.

89011 through 89019

and 90001'through

90007

~Note

No. 69016

was oot used)

Table

2 shows

LER cause

areas for Unit

1 and Unit 2.

Tabl e

2

Number of LERs b

Cause

Cause

Area

'Unit

1

Unit 2

Personnel

Errors

Design Deficiencies

External

Causes

Procedure

Inadequacies

Equipment/Component

Other/Unknown

7

1

0

3

0

0

TOTALS

15

'26

Table

3 shows

a comparison of LER causes

for SALP 8 and

SALP

9.'able

3

Cause

Area

Personnel

Errors

Design Deficiencies

External

Causes

Procedure

Inadequacies

Equipment/Component

Other/Unknown

TOTALS

FREQUENCY (LERs per month)

  • Includes three voluntary

LERs

"*Includes one voluntary

LER

SALP 8

(16 Months)

16 (41.0%)

1 (2.6%)

0 (0.0%)

5 (12.8%)

12 (30.8%)

~512. 8%

39" (100%)

2.4

SALP 9

(14 Months)

11 (42.3%)

2 (7.7%)

0 (0.0%)

7 (26.9%)

6 (23.1%)

~00. 0%L

26"" (100%)

1.9

NOTE:

This information is derived from a review of LERs performed

by

the

NRC staff and the cause

may not completely correspond

to the

causes

assigned

by the licensee.

27