ML17326B204

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Insp Repts 50-315/86-04 & 50-316/86-04 on 860121-0218. Violations Noted Re Failure to Properly Review & Control Procedure Changes & Failure to Meet Requirements of Tech Spec for Compensatory Sampling W/Equipment Inoperable
ML17326B204
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/25/1986
From: Hehl C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17326B205 List:
References
50-315-86-04, 50-315-86-4, 50-316-86-04, 50-316-86-4, NUDOCS 8603310069
Download: ML17326B204 (28)


See also: IR 05000315/1986004

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports

No. 50-315/86004(DRP);

50-316/86004(DRP)

Docket Nos

~ 50-315;

50-316

Licenses

No.

DPR-58;

DPR-74

Licensee:

American Electric Power Service Corporation

Indiana

and Michigan Electric Company

1 Riverside

Plaza

Columbus,

OH

43216

Facility Name:

Donald

C.

Cook Nuclear

Power Plant, Units 1 and

2

Inspection At:

Donald

C.

Cook Site,

Bridgman,

MI

Inspection

Conducted:

January

21,

1986 through February 18,

1986

Inspectors:

B.

L. Jorgensen

J.

K. Heller

C.

L. Molfsen

ED

R.

Swanson

Approved By:

Proje

Chief

s Section

2A

Date

Ins ection

Summar

Ins ection

on Januar

21

1986 throu

h Februar

18

1986

Re orts

No.

50-315/86004(DRP

. 50-316/86004

DRP

licensee

actions

on previously identified items; operational

safety verification;

reactor trip/safety system challenge

review; surveillance;

reportable

events;

and independent

inspection activities.

The inspection involved a total of 256

inspector-hours

by four NRC inspectors

including 20 inspector-hours

during

offshift.

Results:

Of the six areas

inspected,

no violations or deviations

were identified

in four areas.

The two violations (Level IV - failure to properly review and

control procedure

changes,

Paragraph

2.c;

Level

V - failure to meet requirements

of Technical Specification for compensatory

sampling with equipment inoperable,

Paragraph

6) were identified with one in each of the remaining areas.

DETAILS

1.

Persons

Contacted

M.

AB

"A.

  • J

K.

  • J
  • L
  • L

C

D.

M.

D

"R.

T.

G. Smith, Jr., Plant Manager

Svensson,

Assistant Plant Manager

Blind, Assistant Plant'anager

Kriesel, Technical

Superintendent-Physical

Sciences

Allard, Maintenance

Superintendent

Baker, Operations

Superintendent

Stietzel, guality'ontrol Superintendent

Mathias, Administrative Superintendent

Gibson,

Technical

Superintendent-Engineering

Murphy, Operations-Production

Supervisor

Draper,

Operations

Procedure

Coordinator

Horvath, guality Assurance

Supervisor

McAlhany, guality Assurance

(AEPSC)

Sims, Shift Technical Advisor

Postlewait,

Performance

Supervising

Engineer

The inspector also contacted

a number of other licensee

and contract

employees

and informally interviewed operations,

maintenance,

and

technical

personnel.

"Denotes personnel

attending exit interview February 19, 1986.

~

~

2.

Licensee Actions on Previousl

Identified Items

a 0

(Open) Unresolved

Item (315/85028-01;

316/85028-01);

apparent

failure to perform surveillance testing at the required frequency

and failure to perform adequate

surveillance testing.

This item has

three attributes,

each of which has

been determined to represent

a

Violation.

First,

as described

in Paragraph

3. a. of the referenced

Report, various

CHANNEL FUNCTIONAL TESTS required to be performed

each

month were, prior to August 1985, being performed only once

each

two months.

Second,

as described

in Paragraph

3.c. of the

referenced

report,

a motor-driven auxiliary feedwater

pump loss of

voltage relay required to be tested

each refueling had, prior to

August 1985,

never

been tested.

Third, as described

in Paragraph

3. d.

of the referenced

Report,

selected

CHANNEL CALIBRATIONS (defined

as

requiring inclusion of the sensor)

had, prior to August 1985,

been

performed excluding the sensor.

These matters

have

been discussed

with the licensee

during meetings with the

NRC Region III staff;

specifically during an Enforcement

Conference

held on November 13,

1985.

They remain under evaluation for appropriate

enforcement action,

including potential

escalated

enforcement.

Though

no Notice of

Violation concerning these

matters is being issued with this report

decisions

concerning application of proper enforcement

sanctions

are

pending.

The licensee

is being officially notified in writing via

the transmittal letter for this report that the items are considered

Violations. In the future this item will be tracked

as Violation

(315/85028-01;

316/85028-01).

0

T

'I

T

UI '

b.

C.

(Open) Unresolved

Item (315/85028-02;

316/85028-02):

failure to

conduct

a channel

functional test following a channel calibration.

NRC has not determined if this matter is a Violation.

NRC will

correspond with the licensee

concerning this item at a later date.

(Closed)

Unresolved

Item (315/85028-03;

316/85028-03):

apparent failure

to provide adequate

reviews

and controls

on temporary procedure

changes.

This item has also

been determined to be

a Violation, as discussed

previously with the licensee.

A Notice of Violation concerning this

item is being issued with this report.

A brief review of the facts is

appropriate.

During conduct of the inspection

documented

under Reports

No. 315/85028;

316/85028 the inspectors

observed

a procedure

in use

which had apparently

been altered

by a pen

and ink change.

Following

up this observation,

a large

number of similar procedures

(Control

and

Instrument group test procedures)

were reviewed from the files.

Though

the sample

was large, it constituted only a fraction of the total

number of procedures

of this type.

A total of eleven procedures

were

found which had been altered;

however, required review and approval for

such alterations

had not been applied.

Technical Specifications

(both

Units) Paragraphs

6.8.2

and 6.8.3 require prior review and approval of

all procedure

changes;

with permanent

changes

reviewed

and approved

by

the Plant Nuclear Safety Review Committee

(PNSRC)

and the Plant Manager;

and temporary

changes

(not altering the intent of the procedure)

requiring approval of two members of the management staff including one

Senior

Reactor

Operator license holder.

Subsequent

PNSRC and Plant

Manager approval of temporary

changes

must follow within 14 days.

In

the examples identified by the inspectors,

neither type of review and

approval

process

had been performed.

Subsequent

to this finding, as

stated in the licensee's

letter of November 27,

1985 and as described

in Inspection

Reports

No. 315/85041(DRP);

316/85041(DRP),

the licensee

performed

a comprehensive

review of all procedures

of the subject type,

identified and evaluated

each instance potentially involving a

previously unreviewed

and unapproved revision to such procedures,

and

documented

the requisite review and approval

as

needed.

No examples

were identified which appeared likely to have caused

incorrect procedure

performance

or invalid data.

Preventive actions

have included

conversations

with the personnel

apparently

involved in the procedure

alterations.

The discussions

focused

on

a Plant Manager letter dated

September

16,

1985 to all supervisors,

addressing

the

use of required

controls

when making changes

to procedures.

Since actions to correct

and to prevent recurrence

of this Violation have already

been completed,

the licensee will not be required to respond to the Notice of Violation

issued

herewith.

The inspector

has

no further questions

concerning

this matter at this time (Violation 315/86004-01;

316/86004-01).

Four violations and

no deviations

were identified.

'I

C

I

v

0 erational

Safet

Verification

The inspector

observed control

room operation including manning, shift

turnover,

approved procedures

and Limiting Condition for Operation

(LCO)

adherence,

and reviewed applicable

logs and conducted

discussions

with

control

room operators

during the inspection period.

Observations

of the

.control

room monitors, indicators,

and recorders

were

made to verify the

operability of emergency

systems,

radiation monitoring systems,

and nuclear

and reactor protection systems,

as applicable.

Reviews of surveillance,

equipment condition,

and tagout logs were conducted.

Proper return to

service of selected

components

was veri'fied.

Tours of the auxiliary

building, turbine building, and screenhouse

were

made to observe

accessible

equipment conditions, including fluid leaks, potential fire hazards,

and

control of activities in progress.

Unit 1 operated routinely at approximately

90 percent

power throughout the

inspection period.

The inspector performed

a walkdown and review of

accessible

portions of the Unit 1 "E" (East)

Containment

Spray System

(CTS)

using licensee

drawing OP-1-5144-6

and procedure

1-OHP 4021.009.001

"Placing Containment

Spray in Standby

Readiness".

Correct .flowpath valve

positions were verifi'ed, and

no condition was noted which degraded

the

system'or its major components.

It was not possible to verify the correct

(closed) position of valve 1-IMO-210 (an automatic

opening

pump discharge

valve) using the local dial indicator at the valve.

Control

room

indication established

the valve was correctly position'ed.

Discussion with

the licensee

suggested

the local indicator's

not heavily relied upon to

ascertain

valve position.

Nevertheless,

a Job Order was initiated to

adjust the dial to the correct

onscale

reading.

- Based

on a Unit 2 event

(discussed

below) involving valve identification tag interference with

proper valve operation for a small

manual valve, the walkdown specifically

focused

on potential additional

examples

where

an identification tag was

positioned

so as to create possible indication.

No examples

were noted in

this small sampling.

Unit 2 operated at approximately

80 percent

power throughout the inspection

period with three exceptions.

A Unit trip on February 1,

1986 is discussed

in Paragraph

4 below.

The two other events

both involved .licensee

initiation of plant shutdown pursuant to Technical Specifications

because

the Boron Injection Tank (BIT) boron concentration

became diluted below the

required 20,000 parts per million (ppm).

The first event occurred

February 7, 1986.

Operators

acquiring routine shift readings

noted

a level

increase

in the "S" (South) Boric Acid Storage

Tank (BAST), which was in

service recirculating the BIT.

A special

boron sampling

was requested

which showed at l2:05 p.m. that the BIT had been diluted to 17,331

ppm.

Recirculation

was switched to the "M" (Middle) BAST.,

a resample

called for,

and

a Unit shutdown

commenced.

By 1:40 p.m.

resampling results

demonstrated

the BIT concentration

was back in specification

and the

shutdown

was terminated.

Subsequent

investigation of a suspect pair of

cross-tie

valves

from the primary water system disclosed

one of the valves

had a damaged

internal

diaphragm which apparently permitted the leakage

and

resultant dilution.

The primary water system

had been in service to dilute

the primary coolant system in support of the ongoing power increase after

recovery from the reactor trip a week earlier.

0

II',

i

f

t

l

l

I

Five days later,

on February 12,

1986

a second dilution of the Unit 2 BIT

occurred.

In this event,

the BIT had been taken off "M" BAST recirculation

to permit alignment of the still-diluted "S" BAST through part of the

shared piping.

The "S" BAST was intended to be

pumped

down to a holding

tank to make

room for the addition of sufficient highly concentrated

boric

acid to return that tank to specification.

When the "M" BAST level

increased

(as observed

in the Unit 1 control

room, which has the only level

indication on this "shared" tank)

a special

boron sample

was again

requested

which, at 4:48 p.m.,

showed boron concentration

to be 19,047

ppm.

Since it was believed the dilution path must be directly through the BIT

(which later proved the case)

the BIT was immediately restored to

recirculation via the "M" BAST (which had not diluted significantly) and

resampling called for while a shutdown

was begun.

By 5:55 p.m. the

resample

analysis

showed the BIT back in specification.

The shutdown

was

terminated.

Investigation of this problem found a small

(one inch) manual

isolation valve separating

the "S" BAST from the BIT had not been fully

closed

because

the handwheel

had 'tightened

down on a small ball-chain

attaching the valve identification tag to the valve, instead of tightening

into the valve seat.

Some discussions

among the inspector

and licensee

personnel

concerning this event suggest

the following: first, the valve in

question

was not the sole isolation valve available

and dual isolation

could have

been established;

second,

changing

"M" BAST level could have

been

noted sooner

had Unit 2 communicated

more clearly or forcefully than

it did to Unit 1 that changing tank leve~l could indicate

a problem and;

third, the tag interference is not necessarily

indicative of a generic

problem because it involved a small manually operated

valve on an insulated

and heat-traced

pipe run (the insulation obscuring the valve stem)

and the

"old style" plastic identification tag;attached

with a ball-chain.

The

licensee is engaged

in placing new, color coded metallic permanent

identification tags

on plant components.

Guidance already in existence for

such permanent

tag placement

should, for a valve of this type, result in

attachment to the pipe rather than around the valve stem.

In fact, prior

to the conclusion of this inspection

a permanent

tag had been

made

and

placed at the valve in question

and the old tag and chain removed.

In each of the above instances,

the licensee's

actions

were in compliance

with requirements.

The previous Inspection Report

(No. 315/85041(DRP);

316/85041(DRP))

discusses

some

need for improved clarity in the way the licensee controls

the turbine driven auxiliary feedwater

pump speed controller setting.

The

instructions

given in various procedures

were at odds with each other.

During this inspection,

the licensee

completed procedure

change

sheets

to

applicable procedures

such that these contradictions

are

removed.

He has

chosen to control this parameter via an information tag placed at the

controller indicating the correct setting

as established

by monthly testing.

Proper controller position will be verified each shift.

The inspector

has

no further questions

or concerns

in this area.

Finally, the inspector discussed shift staffing,

and the licensee's

capabilities for maintaining and/or augmenting shift crews

as necessary

when considering

severe

inclement weather, with licensee

operations

management staff.

They appeared

both sensitive to and prepared for

weather

emergencies

insofar as maintaining adequate shift crews

was

concerned.

0

J

II I

'

Pl

1

5

v

0 'o

violations or deviations

were identified.

Reactor Tri s - Safet

S stem Challen

e Review

t t

The following event was reviewed by the resident inspectors

to determine:

the significance of the event;

the performance of safety systems;

immediate

actions

taken

by the licensee;

radiological

consequences;

and corrective

actions

taken.

Unit 2 tripped from about

80 percent

power at 8: 11 a.m.

on February 1,

1986

as

a consequence

of a main generator "unit differential" trip.

The

generator differential trip was apparently

caused

in turn by protective

relay response

to a faulting condition on the

2CD auxiliary transformer,

which was providing station power back off the main generator.

Plant

response

to the trip, including fast-transfer of station loads to startup

power,

was normal.

A fire ensued

on the

2CD transformer at a failed bushing atop the unit, and

the bus ducting system

drew considerable

smoke into the adjacent turbine

building, making the magnitude

and location of the fire uncertain at first.

An "Unusual

Event" was declared at 8: 15 a.m.

due to the fire, which was

subsequently

extinguished

by 8:27 a.m.

The "Unusual

Event" was secured at

9:03 a.m.

Licensee

response

to and management

of the fire situation are

subject to further review at

a later date

by specialists

from NRC

Region III, and will not be addressed

fur ther here.

Response

of the plant,,

as noted above,

was normal; although operators

continued running the

turbine driven auxiliary "feedwater

pump longer than needed

(perhaps

due to

focus

on the incoming reports relating to the fire) and cooldown proceeded

to 532 degrees

versus

a normal hot standby of 547 degrees

(and pressure

was

around 2,000 psig) before the

pump was secured.

Following applicable post-trip reviews

and required authorizations

the

Unit 2 reactor

was again taken critical late

on February 3, 1986.

In the

interim, early on February 3, the initial approach to criticality was not

proceeding

per expectations

established

by an estimated critical position

(ECP) calculation.

Extrapolations

during the approach

suggested

the

ECP,

plus

a 500

pcm target band,

was going to be exceeded.

The approach

was

terminated, all control banks re-inserted,

and a review initiated to

determine

what happened.

An NRC Region III inspector

specializing in

reactor physics

was onsite performing an inspection in that area,

arrangements

were

made for the specialist to review this matter as well.

That review was documented

in IE Inspection

Reports

No. 315/86005(DRS);

316/86005(DRS).

5.

No violations or deviations

were identified.

Surveillance

The inspector

reviewed Technical Specifications

required surveillance

testing

as described

below and verified that testing was performed in

accordance

with adequate

procedures,

that test instrumentation

was

calibrated, that limiting conditions for operation

were met, that removal

1

'

4

and restoration of the affected

components

were properly accomplished,

that

test results

conformed. with Technical Specifications

and procedure

requirements

and were reviewed by personnel

other than the individual

directing the test,

and that deficiencies identified during the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

Performance

of all or parts of the following tests

was observed:

""1 THP 4030 STP.013

"Pressurizer

Pressure

Protection

Set III"

    • 1 THP 4030 STP.014

"Pressurizer

Pressure

Protection Set IV"

""1 THP 4030 STP.005

"Over Temperature

and Over Power Protection

Set II Surveillance Test (Monthly)"

"*1 THP 6030

IMP.095

"OT/T-avg Protection

Set II Calibration"

The test designated

IMP.095 was required for recalibration of two R/E

converters

which were determined to be out of specification during initial

performance of STP.005.

The test designated

STP.005

was then repeated

(this retest

was specifically observed)

and all "as left" values

appeared

to be in specification.

For the following tests,

the inspector

reviewed the test procedures

and/or

completed test data for the more recent test performances:

~*1 OHP 4030 STP.007E

"East Containment

Spray System Operability

Test"

    • 1 OHP 4030

STP.007W

"West Containment

Spray System Operability

Test"

~*1 THP 4030 STP.205A

    • 1 THP 4030

STP.205B

""1 THP 4030 STP.217A

"Engineered

Safeguards

Features

Time

Response

Test - Train A"

"Engineered

Safeguards

Features

Time

Response

Test - Train B"

"Diesel Generator

Load Shedding

and

Performance

Test - Train A"

    • 1 THP 4030 STP.217B

"Diesel Generator

Load Shedding

and

Performance

Test - Train B"

The inspector

reviewed the technical

content of STP.007E

and

STP.007W (both

were Revision

1 with change

sheets

1,

2 and

3 incorporated)

and found that

the procedures

appear to demonstrate

the operability of the Containment

Spray

and Spray Additive Systems

in accordance

with the appropriate

monthly

Technical Specification surveillance

requirements.

However, the inspector

questions if the cycling of l-IM0-212, "1E CTS

Pump Eductor Supply Valve"

and 1-IMO-222 "1W CTS Pump Eductor Supply Valve" meets the intent of ASME

Boiler and Pressure

Vessel

Code,

Section XI.

The sequencing of STP.007E

/'I

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and STP.007W is such that valves

1-IMO-212 and I-IMO-222 are cycled

(closed-opened-closed)

before the valves are stroke-timed in the open

position.

The inspector discussed

this with the Operations

Superintendent

and the Operations

Procedure

Coordinator.

The Operations

Procedure

Coordinator agreed to review this item and make the appropriate

revisions

to STP.007.

This is an Open Item pending the Operations

Coordinator review

(Open Item 315/86004-02).

Technical Specification

3. 3. 2.1 at Table 3. 3-5 specifies

an Engineered

Safety Feature

(ESF) response

time of less

than or equal to 45 seconds

for the Containment

Spray System.

STP.205A and STP.205B at Step 6.6 '

of

attachment

4 implements this requirement.

The inspector

reviewed these

procedures

and found that parallel

spray

pump discharge

valves

(two per

pump) have

an allowable

ESF response

time of less

than or equal to 60

seconds.

This time is footnoted by reference

to Attachment

3 of STP.205A

or B, explaining why the response

time is increased

from 45 seconds

to 60

seconds.

Basically, attachment

3 explains that if the valves are

open at

least

20 percent,

the system resistance

is negligible and the spray system

will be capable of performing its safety function.

The attachment

does not

state

how many seconds. it takes for the valve(s) to reach

20 percent

open.

The inspector discussed this with the Technical Superintendent-

Engineering,

who initiated an evaluation to show the valves are at least

20

percent

open in less than 45 seconds.

An analysis that shows

20 percent

open will provide negligible flow resistance will be included.

Pending

further

NRC review of this matter, this is considered

an Open Item

(315/86004-03).

The inspector

reviewed completed Attachment

4 to STP.205B

(performed

November 1985)

and STP.205A (performed October 1983).

The following were

found.

a e

b.

STP.205B listed an

ESF response

time of 60.2 seconds

for IMO-220 and

documented

"Attachment

3 states

that valves must be 20 percent

open

within 60 seconds"

which is an incorrect interpretation of

Attachment 3.

The acceptance

criterion

was less

than or equal to 60

seconds.

The significance of the additional 0.2 seconds

is unclear.

However, this should

be resolved

when

Open Item 315/86004-03 is

resolved.

l

STP.205B includes the diesel

generator start time and load sequencing

time to determine

ESF response

time,

and states

these

times can

be

obtained

from STP.2178.

The inspector

reviewed

STP.217B

(performed

June

16, 1985)

and found that the timing graphs,

which used

a

multi-pen recorder,

did n'ot have

a "key" for deciphering which pen

tracks what component.

With the assistance

of a Performance

Engineer

the key was found in an uncontrolled location.

The Performance

Engineer

committed to incorporate

the

key into STP.217B.

The

inspector

reviewed

a sample of other procedures

that used multi-pen

recorders

and found that the completed procedures

adequately

identified components.

This was discussed

at the exit interview with

the inspector stressing,

and the licensee

agreeing,

that completed

documentation

should stand alone.

C.

STP.205A documented

"N/A" for the requirement to include the load

sequencing

time when determining the lE Containment

Spray

Pump

ESF

response

time.

This appears

to be in error.

The inspector discussed

this with the Performance

Supervisor concerning

how a demonstration

of

compliance to an overall time limit requirement

can

be made without

one of the time constituents.

He agreed to verify the response

time,

including sequencer

loading time, met the 45 second

requirement.

This

is considered

an Open Item (Open Item 315/86004-04).

No violations deviations

were identified.

Three

open items were

identified.

Re ortable

Events

Through direct observation,

discussions

with licensee

personnel,

and review

of records,

the following Licensee

Event Reports

(LERs) were reviewed.

The

review addressed

compliance to reporting requirements

and,

as applicable,

accomplishment

of immediate corrective action.

If indicated "closed", the

review showed appropriate corrective action to prevent recurrence

had been

accomplished

in accordance

with applicable

requirements.

Unit 1

(Closed)

RO 315/85005-00:

incorrect iodine sample

medium.

The plant had

been using silver zeolite cartridges for iodine collection/analysis

since

June

1982, contrary to Technical Specification 3.11.2. 1 Table 4. 11-2, which

specifies

a charcoal

medium for iodine collection in the auxiliary building

vent system,

and gland exhaust

system.

The iodine collection medium was

changed

back to a charcoal

cartridge

on February 5,

1985 and will be used

until a Technical Specification

change

can

be made to allow for the use of

the more accurate silver zeolite cartridge.

Application for this change is

included in a letter, dated January

21,

1986

(AEP:NRC:0956A) written to the

Office of Nuclear Reactor

Regulation.

(Closed)

RO 315/85019-00

and 315/85019-01:

low ice condenser

basket weights.

An April 1985 surveillance indicated that several

ice condenser

ice basket

weights were low.

The ice inventory in the ice condenser

was below the

Limiting Condition for Operation

(LCO) in Technical Specification 3.6.5. l.d,

for the minimum average

ice weight (1220 lb/basket) of sample

baskets

from

each row/group.

An extensive

ice replenishment

program was completed

during the Unit 1 1985 outage;

the surveillance,

12

THP 4030 STP.211,

"Ice

Condenser

Basket Weighing," was completed three times satisfactorily in

1985 after the replenishment.

In addition, Unit 2 satisfactorily completed

an ice basket weighing surveillance in August 1985 and plans

a

replenishment

program for 540 baskets

for the 1986 outage

which begins in

February

1986.

(Closed)

RO 315/85026-00:

ESF actuation-safety

injection.

The signal

occurred

due to one channel

of pressurizer

pressure

in test concurrent with

loss of the block signal

on another

channel

when the vital instrument

bus

Control

Room Instrument Distribution (GRID) was momentarily deenergized.

To prevent recurrence

the licensee

has

added

a precaution to the vital

I

I

lf

'-'

r

f!

1

tl

'

IC

instrument

bus power supply transfer

procedure

(OHP 4021.082.008)

that

advises

the operator to evaluate

the status

of protection channels prior

to power transfer.'-'-

The licensee

has,implemented'-a

design

change in Unit 1

to replace the

CRID inverters

(DC-01-2766)

and plans to complete the Unit 2

design

change during the 1986 outage.

The

new design

power supply can

be

transferred without deenergizing

CRIDS.

(Closed)

RO 315/85031-00

and 315/85031-01

(Applies to both Units):

incorrect calibration of residual

heat flow instrumentation.

The licensee

discovered

a combination of factors

had led to instrumentation for RHR hot

leg process

flow and

RHR cooldown flow being inaccurate.

The indicated

flow exceeded

the actual flow, such that use of the flow indication to show

compliance to requirements

for minimum flow through the reactor coolant

system,

is suspect.

At an indicated 3,000

gpm (corresponding

to the

minimum flow requirement)

actual

flow could have

been

as

low as 2,026

gpm.

The licensee's

supplemental

report dated

September

9,

1985 contains

analyses

demonstrating

2,000

gpm is adequate

flow for decay heat

removal

and to avoid boron stratjfication.

One of the subject instruments

(per

Unit) feeds

a low flow alarm which would warn plant operators

of loss of

flow, so actions could be taken to protect the associated

pump and to

establish

an alternate

flow path.

The alarm setpoint (intended for

2,000

gpm) could have

been set

as

low as

675

gpm.

Considering

independent

means to identify loss of flow and the substantial

time (at least

one hour)

permitted to correct

such loss,

accuracy of the alarm setpoint is not

considered critical.

At the time of the discovery of this matter in early July,

1985 the

inspector briefly reviewed the circumstances

with licensee

personnel.

Replacement

of erroneously

drawn meter faces

(considered

the primary

deficiency - see

IE Inspection

Reports

No. 50-315/85020(DRP);

50-316/85020(DRP)

Paragraph 3.c.)

was specifically verified at that time

as immediate corrective action.

Subsequent

reviews indicate all the

instruments

affected (three per Unit) were identified in the licensee's

search f'r additional

examples,

and

no other examples

were 'found in

independent

reviews by the resident inspectors.

Prevention

should

be

assured

by revision of the associated

calibration procedures,

which is

complete,

now that correctly drawn permanent

meter faces

are installed.

Though uncertain, it is likely the licensee

operated

both Units at various

times with (unknowingly) less than the required flow, in violation of

Technical Specifications.

In such

an event,

the violation would be of the

kind (identified, 'reported

and corrected

by the licensee,

small safety

significance

and unrelated to a previous similar violation) for which NRC,

under its enforcement policy as stated in 10 CFR Part 2, Appendix C, does

not usually issue

a Notice of Violation, and

no Notice of Violation is

being issued in this case.

(Closed)

RO 315/85034-00:

breach of containment integrity during refueling.

Both airlock doors were momentarily opened simultaneously

during refueling,

identifying a malfunctioning latching mechanism.

The mechanism

was

repaired within about five hours,

during which time no further simultaneous

openings

occurred.

10

j

t

~

v c

r

l

C

tl

(Closed)

RO 315/85035-00:

reactor coolant system

boron concentration

below

2,000

ppm during refueling (two occasions

about

30 ppm below).

The fuel

vendor evaluated

minimum boron concentration

necessary

to maintain shutdown

margin at 1565

ppm, well below the concentrations

observed

in this event.

No positive identification could be

made of the source of dilute water,

despite

an investigation of various possibilities.

The licensee

believes,

since strict control of boron concentration

above 2,000

ppm was not required

during the full core offload preceding this event, that stagnant

RCS volumes

(e.g. in idle legs)

mixed back into the system following reload

and

establishment

of varying residual

heat

removal flow paths.

This

possibility has

been

addressed

by a Standing Order to maintain 2,000

ppm

throughout the systems

even during periods

when there is no fuel in the

reactor vessel.

(Closed)

RO 315/85037-00:

ESF actuations

during cold shutdown.

Two events

occurred

as

a consequence

of modifications to the plant permitted only

during cold shutdown.

They are considered

minor events with respect

both

to safety significance

and to the question whether they may have merited

some effort in an attempt to avoid them.

Their reportabi lity is based

(correctly)

on the understanding

~an

ESF actuation

not "preplanned"

must

be reported.

The licensee

categorized

these

items

as not "preplanned"

due

to the absence

of a specific prior notification to the operators that an

actuation

was imminent.

(Closed)

RO 315/85039-00

(applies to both Units):

surveillance

performed

on wrong fire water ring header valve.

This item is similar to

RO 315/84025-00

discussed

in IE Inspection

Reports

No. 50-315/84023(DRP);

50-316/84025(DRP)

in that it involves discovery,

due to flow print verifi-

cation activities mandated

by the licensee's

Regulatory Performance

Improvement

Program, that a valve other than that intended

had been

subjected

to testing

due to flow print error.

The error was corrected.

(Closed)

RO 315/85040-00

(applies to both Units):

potential for RHR flow

below limits.

In review of

RO 315/85031-00

discussed

above involving RHR

flow instrument calibration, the licensee

recognized

RHR flow paths

are

available

and used which are not equipped with a low flow alarm.

Though

the license condition which prompted installation of the existing alarms

no longer exists,

the need to promptly identify loss of RHR flow remains

whatever the system alignment,

and written instructions to the operators

establishing

frequency for and documentation

on flow verification have

been issued.

(Closed)

RO 315/85044-00:

ESF actuation during cold shutdown.

As with

RO 315/85037-00

discussed

above,

these

were trivial (but reportable)

events

related to installation of a design

change permissible only with the plant

in cold shutdown.

(Closed)

RO 315/85052-00:

an

ESF actuation in the form of a containment

purge isolation

~si nal

(no purge

was in progress

so

no actual isolation

occurred)

was caused

by component failure in the Critical Control

Room

Power

(CCRP) inverter.

Damaged

and questionable

components within the

inverter were replaced

and normal electrical

lineups restored.

(Closed)

RO 315/85054-00:

an

ESF actuation in the form of a turbine trip

~si nal (the plant was in NDDE 3 with the turbine not in service)

was caused

by steam generator hi-hi level.

Level was being maintained

above the high

deviation alarm point of 50 percent level (at about

60 percent) to perform

a calibration procedure.

Temperature

changes

and feedwater

leakby increased

level to the 68 percent "trip" setpoint undetected

by the operator,

who was

involved in shift turnover.

Though this specific event lacked safety sig-

nificance, operator attentiveness

is highly important and was specifically

addressed

with the operator involved.

Job Orders to investigate

apparent

feedwater isolation valve leakage

were written.

n

(Closed)

RO 315/85057-00

and 315/85057-01:

an

ESF actuation in the form of

a reactor trip ~si nal (the plant was in NODE 3 with the control

rods

inserted

and the reactor trip breakers

open)

was caused

by simultaneous

de-energization

of two power range nuclear instruments to install

a design

change.

Though this specific example

lacked safety significance, it

occurred

because

the Unit Supervisor

and the, instrument technicians

involved

did not recognize

the activity could best

be accomplished

one channel at a

time.

(Closed)

RO 315/85059-00:

an

ESF actuation in the form of a reactor trip

~si nal (plant in NODE 3, trip breakers

open)

was caused

by a technician

lifting the wrong leads while performing instrument checks.

(Closed)

RO 315/85060-00:

an

ESF actuation in the form of an actual safety

injection and main steam isolation (plant in MODE 3, trip breakers

open)

was caused

by simultaneous

conduct of unrelated activities;

one of which

created

indicated high steam line flow while the other created

low-low

average

temperature.

The following Unit 2 item is discussed

here for continuity:

(Closed)

RO 316/85037-00:

an

ESF actuation in the form of a reactor trip

from about 81 percent

power resulted

from isolation for maintenance

of a

safety instrument channel

also being used for control circuit input without

transferring control to the alternate

channel.

Each of the three items immediately above

have in common that they were

avoidable

had plant personnel

exercised

greater foresight in conduct of

activities.

The licensee

has

been requested

to specifically address

NRC

concern in this area,

in writing, in response

to IE Inspection

Reports

No. 50-315/85036(DRP);

50-316/85036(DRP).

(Closed)

RO 315/85063-00:

inoperable

main steam flow transmitters.

Two

transmitters failed independently

but simultaneously,

indicating no steam

flow during a power increase.

License action requirements

were met, the

instruments

were repaired

and recalibrated,

respectively,

and returned to

service.

12

(Closed)

RO 315/85068-00:

an

ESF actuation in the form of a main steam line

isolation (plant in MODE 3) was caused

by performance of a surveillance with

temperature

below 541 degrees.

Reportability was

based solely on the lack

of prior notification to control

room operators that the actuation would

occur,

such that so far as they were concerned, it was unanticipated.

It

was considered

minor similar to

RO 315/85037-00

discussed

above.

Unit 2

(Open)

RO 316/83014-00:

Steam Generator

No.

23 Main Steam Isolation

Valves

Dump Valve, MRV-232, removed for repair.

The repair of MRV-232

placed

No.

3 Steam Generator

Stop Valve in a a less conservative

configuration than required

by Technical Specification 3.7.2.5,

however the

redundant

dump valve,

MRV-231 remained operable,

action requirements

were

.met,

and the valve',was

returned to service within, four hours.

The inspector

reviewed several,Job

Order packages'regarding

similar 'repairs to both Units

and found that three valves out of sixteen

needed repetitive repairs.

The

preventive

maintenance

program

was discussed

with plant personnel.

The

Preventive

Maintenance

(PM) procedure

for, the maintenance

department

(MHI 5030) included extensive

information on items scheduled

and frequency

of preventive maintenance,

and

has recently been

updated to reference

the

documentation

which resulted in an item being included in the Preventive

Maintenance

schedule.

However, the inspector is leaving this item open

until further details

on the preventive maintenance

program can

be reviewed.

(Closed)

RO 316/85014-00:

an, ESF actuation in the form of a safety

injection ~si nal (plant in MODE 5) was caused

by a momentary voltage drop

to two Control

Room Instrument Distribution (GRID) buses

when

a reactor

coolant

pump was started

from the

same

power source.

The CRID electrical

alignment was unique to an ongoing design

change

and would not have

been

permitted in other

MODES.

(Closed)

RO 316/85016-00:

missing seismic restraints.

In review of I. E.

Information Notice 85-45

and preparations

to address

questions/concerns

relating to seismic design of selected

Westinghouse

Incore Flux Mapping

Systems

(FMS), the licensee

discovered restraint devices specified in the

original design were never installed

on the

FMS frame.

This circumstance

was unique to Unit 2,

and was expeditiously corrected, prior to .startup

from the then existing shutdown.

(Closed)

RO 316/85018-00:

an

ESF actuation in the form of a reactor trip

~si nal (plant

in,.MODE 3, but reactor trip breakers

closed)

was

caused

by

conduct of routine instrument checks

not normally performed with the trip

breakers

closed.

This event

has

no safety significance but is another

example of an "avoidable" actuation.

Note: the following four items are grouped together

due to the

interrelationship

among them; although all apply to both Units, two

were identified first and assigned

by the licensee to the Docket for

each Unit.

13

A

ll

t

N

l

ll

L,B

1

1

(Open)

RO 316/85021-00

(applies to both Units):

failure to perform certain

instrument

channel

functional tests at the required frequency.

This matter

was originally identified in part by the

NRC and was described in the

associated

IE Inspection

Report as

an Unresolved

Item (No. 315/85028-01;

316/85028-01).

NRC has subsequently

determined this matter to be a

Violation, has

met with the licensee to discuss it, and is continuing an

evaluation relating to the choice of appropriate potential

enforcement

action.

Pending

such determination,

no Notice of Violation is being issued.

(Open)

RO 315/85043-00

and 315/85043-01

(applies to both Units): failure to

include primary sensors

in channel calibrations.

As with the above item,

NRC originally identified this item in part,

has

documented it within the

same Unresolved

Item (No 315/85028-01;

316/85028-01)

and

has since

determined it to represent

a Violation for which appropriate

enforcement

action is yet to be determined.

(Closed)

RO 315/85047-00

and 315/85049-00

(applies to both Units):

failure

to perform instrument surveillance at the required frequency.

These matters

were identified by the licensee

in performance of reviews stipulated in a

Confirmation of Action Letter (CAL) dated August 30,

1985 which was based

on the

NRC findings discussed

above.

In that appropriate

enforcement action

is being developed

concerning the similar NRC-identified matters,

no Notice

of Violation is deemed

necessary

concerning these

items identified, reported

and corrected

by the licensee

pursuant to the

CAL based

on the

NRC items.

(Closed)

RO 316/85025-00

(applies to both Units):

inadequate

control to

assure

required surveillance

completed.

This matter

was also identified,

reported

and corrected

by the licensee

pursuant to the evaluations

performed

to implement the

CAL discussed

immediately above.

(Closed)

RO 316/85012-00

and 316/85043-00:

failure to complete

compensatory

sampling within required time interval.

Each of these

events

involved late

collection of "grab" samples of the Unit 2 auxiliary building ventilation

gaseous

effluent with the automatic

sampling equipment inoperable.

Unit 2

Technical Specification 3.3.3. 10 requires

the effluent monitoring instrumen-

tation be

OPERABLE as

shown in Table 3.3-13, which lists the Unit vent noble

gas activity monitor as Item 3.a, specifying the minimum operable

channels

permissible

as

one channel.

Pursuant to Specification 3.3.3. 10, with less

than the minimum number of channels

OPERABLE, the licensee

must take the

ACTION shown in Table 3.3-13,

which is ACTION 28 in the case of the vent

gaseous

monitor.

ACTION 28 permits continued operation for up to 30 days

provided grab samples

are taken at least

once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

The first event

occurred

June 3,

1985 when

a sample required

by 5:00 a.m.

was not collected

until 5:30 a.m..

The second

event occurred

December

27,

1985 when

a sample

required

by 4:55 a.m.

was not collected until 7: 18 a.m..

In accordance

with NRC enforcement policy concerning licensee-identified violation which

should

have

been prevented

.by corrective action for previous similar

problems,

a Notice of Violation is being issued for the second

(December

27)

occurrence

(Violation 316/85004-02).

Five violations and

no deviations

were identified.

Each of the violations

were initially identified by the licensee.

One Notice of Violation is

being issued.

14

7.

Inde endent Ins ection Activities

a 0

b.

On February 4,

1986 the licensee

discovered

the Technical

Specification surveillance

"grace period" for performing

CHANNEL

CALIBRATIONS on the post-accident

monitoring instrumentation of

Table 4.3-10 (Unit 2) was about to expire.

The instruments

in this

Table were overlooked in the licensee's

request for a one-time

extension of the surveillance interval (for instrumentation

which

would otherwise

be "overdue") to February

28,

1986.

Thus, with no

time available to process

a Technical Specification

change

request,

the licensee properly declared

the instrumentation in question to be

"inoperable" effective that day.

This places

the Unit 2 plant in a

30 day Limiting Condition for Operation

(LCO); however,

since

operation

beyond February

28 is already prohibited (relates to

electrical

equipment environmental qualification issues)

the subject

LCO will not affect plant operation.

The instrumentation in question

remains functional

and is operating normally.

The following procedures

(main Control

Room copies)

were reviewed

for clarity, technical

content,

consistency,

and appropriate

administrative controls:

1 OHP 4024. 105

"Annunciator No.

5 Response

Containment

Spray"

U-1

2

OHP 4024.205

"Annunciator No.

5 Response

Containment

Spray" U-2

These procedures

are currently a combination of recently re-typed

(perhaps

word processor

based)

pages - each

page typically addresses

response

to a single alarm "window" on the panel - and what appear to

be repeatedly

photocopied

pages.

Several of the pages

in each

procedure suffer from poor legibility.

The Unit .1 procedure currently

has

seven effective change

sheets,

while the Unit 2 procedure

has only

three.

Finally, an obvious typographical error (e. g., high spent fuel

pool temperature

alarm setpoint at 18025 degrees)

on "drop 28" of the

Unit 1 procedure

had been corrected to 125 degrees

(handwritten

"correction").

The corresponding

Unit 2 setpoint

was identified as

124 degrees.

Alarms on another panel

(each Unit) also covering fuel

pool high temperature

- and there is but one pool - identify the alarm

setpoint

as

125 degrees.

Each of these

minor matters

was discussed

with the procedure co-ordinator

who is taking action to address

them.

The inspector specifically checked procedure

cross-references

to

Technical Specifications for accuracy

and found all were accurate.

C.

Observations

were

made involving plant personnel

access

controls

utilizing newly-arrived and more modern automated

metal detection

equipment at the main access

control point.

The new equipment

appeared

substantially .superior to that it replaced.

d.

Preliminary conduit layout work to support planned 'implementation,

during the upcoming Unit 2 outage,, of RFC 2808,

(replacement

of

control

room instrument distribution panels),utilizing'Job

Order

43573,

was briefly observed.

'o

violations or deviation were identified.

15

~ '

J

(

II

I

'1

4

n

U

g

~0en Items

Open Items are matters

which have

been discussed

with the licensee,

which

will be reviewed further by the inspector,

and which involve some action

on the part of the

NRC or licensee

or both.

Open Items disclosed during

the inspection are discussed

in Paragraph

5.

e

Mana ement Interview

K

4

1

I

The inspector

met with the licensee

representatives

(denoted in Paragraph

l.a above) following completion of the inspection

on February 19,

1986.

The inspection

summarized

the scope

and findings of, the inspection

as

described in these details.

a.

The two apparent Violations were specifically discussed,

including

corrective actions for the first Violation as

a basis for not

requiring a written response

(Paragraphs

2.c.

and 6.).

b.

The inspector advised the licensee that certain items identified as

Unresolved

items in Inspection

Reports

No. 50-31585028;

316/85028 are

now to be classified

as Violations.

NRC will correspond further

with the licensee

concerning

these matters at a 'future date

(Paragraphs

2.a.

and 2.b.).

The inspector also discussed

the likely informational content of the

report with respect to documents

or processes

reviewed.

The licensee

was

afforded the opportunity to identify any such document/processes

which

might be proprietary,

and

none were

so designated.