ML17325B386

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Insp Repts 50-315/89-31 & 50-316/89-31 on 891204-08 & 18-22. Violations Noted.Major Areas Inspected:Maint,Engineering, Inservice Testing,Support of Maint & Related Mgt Activities
ML17325B386
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/01/1990
From: Dey M, Falevits Z, Giitter J, Hart K, Jablonski F, Mendez R, Passehl D, Paul R, Ramsey C, Tella T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17325B381 List:
References
50-315-89-31, 50-316-89-31, NUDOCS 9003140288
Download: ML17325B386 (44)


See also: IR 05000315/1989031

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION III

Report

No:

50-315/89031;

50-316/89031

Docket No:

50-315;

50-316

Licensee:

Indiana Michigan Power

Company

1 Riverside

Plaza

Columbus,

OH 43216

License

No:

DPR-58;

DPR-74

Facility Name:

D.

C.

Cook Nuclear Power Station,

Units

1 5 2

Inspection At:

Bridgman,

MI 49106

Inspection

Conduc

d:

December

4 through 8,

Inspectors:

Z.

alevits,

TeaWLeader

7-

w.( gp;p~

~D.

se

and

December

18 through 22,

1989

3-j- 9'o

Date

3- -90

Date

Date

5-j- 4'a

Date

j~ Qo

Date

Date

Contractor:

R.

Paul

~'~8 p

aw8k+

T. Fredette

Date

Date/- 90

Date

Approved By

Maintenance

5 Outage Section

8-/- ~rO

Date

Ins ection

Summar

Ins ection

on December

4 throu

h 8 and

December

18 throu

h 22

1989

Re ort No.

50"315/89031'0 "316/89031

DRS

9003140288

90030i

PDR

ADOCK 05000315

Q

PNU

in-service testing,

support of maintenance,

and related

management activities.

The inspection

was conducted utilizing Temporary Instruction 2515/97,

the

attached

Maintenance

Inspection Tree,

and selected

portions of Inspection

Modules

62700,

62702,

62704,

62705,

and 92701 to ascertain

whether maintenance

was

effectively accomplished

and assessed

by the licensee.

Results:

Based

on the items inspected

during the time frame that the inspection

was conducted overall performance

in maintenance

was considered

satisfactory.

However,

based

on the deficiencies

noted, significant management

involvement and

improvements

in the maintenance

process

was warranted.

A synopsis

of the overall

implementation of the maintenance

program is provided in Section 3.0 of the

report.

There were four violations: failure to follow procedures,

with seven

examples;

failure to provide adequate

and timely corrective action, with two

examples; failure to adequately

document traceabi lity of materials or components;

and failure to provide adequate

test instrumentation

and testing methodology.

Section

CONTENTS

~pa

e

1.0

2.0

2.1

2.1.1

2.1.2

2.2

2.3

2.3.1

2.3.2

2.3.2.1

2.3.2.2

2.3.2.3

2.3.3

2.3.4

2.3.4.1

2.3.4.2

2.4

2.4.1

2.4.2

2.4.2.1

2.4.2.2

2.4.2.3

2.4.3

2.4.4

2.5

2.6

2.6.1

2.6.2

2.6.3

2.6.4

2.7

2.7.1

2.8

2.8.1

2.8.2

2.9

2.9.1

2.9.2

2.9.2.1

2.9.2.2

2.9.3

3.0

3.1

3.1.1

3.1.2

Maintenance..

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13

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~ 15

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17

19

19

20

20

20

21

21

25

...26

27

formation

28

~ .....29

30

30

31

31

31

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~ 33

33

34

34

34

34

35

35

35

36

36

36

37

37

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~ 37

Persons

Contacted.

Introduction to the Evaluation

and Assessment

of

Performance

Data

and System Selection

Historic Data.

System Selection.

Description of Maintenance

Philosophy

Observation of Current Plant Conditions

and

Ongoing Work Activities.

Current Material Condition

.

Ongoing Work Activities

Ongoing Electrical Maintenance

Ongoing Mechanical

Maintenance.

Ongoing Instrument

and Control Maintenance

Radiological Controls

Maintenance Facilities, Material Control,

and

Control of Tools and Measuring

Equipment

Facilities.

Material

and Test

Equipment Control

Review and Evaluation of Maintenance

Accomplished

Backlog Assessment

and Evaluation.

Review and Evaluation of Completed Maintenance.

Past Electrical Maintenance

Past Mechanical

Maintenance.

Past Instrument

and Control Maintenance.

Vendor Manual Control

Application of NRC Notices,

Generic

and Vendor In

Letters.

Maintenance

Work Control

Engineering

and Technical

Support of Maintenance.

Corporate

and Site Engineering.

System

Engineers

Performance

Engineering

Equipment Failure Analysis

Maintenance

and Support Personnel

Control.

Training and gualifications

Valve Testing.

MOVATS Testing Program..

SOER 86.03

Check Valve Failures

Review of Licensee's

Assessment

of Maintenance.

Audits and Surveillance

Review of Maintenance

Self-Assessment.

Maintenance Self Assessment

guality Teams..

Effectiveness

of Corrective Action.

Synopsis

Overall Plant Performance

(Direct Measures).

Historic Data.

Plant Walkdowns

3.2

3.2.1

3.2.2

3.2.3

3.3

3.3.1

3.3.2

3.3.3

3.3.4

4.0

Management

Support of Maintnance.

Management

Commitment

and Involvement.

Management

Organization

and Administration.

Technical

Support

Implementation of Maintenance

Work Control

Plant Maintenance

Organization.

Maintenance Facilities,

Equipment

and Material Control

Personnel

Control.

Exit Meeting.

.

37

37

37

38

..

38

38

....

39

.40

.40

Appendix A:

Acronyms

DETAILS

1.0

Princi al Persons

Contacted

American Electric Power Service

Cor oration

D. Williams, Jr., Senior Executive Vice President,

Engineering

and

Construction

  • M. Alexich, Vice President,

Nuclear Operations

"T. Argenta, Assistant Vice President,

Nuclear Engineering

Indiana

and Michi an Electric

Com an

"A. Blind, Plant Manager

T. Bestrom,

General

Supervisor,

Production Control

"S. Brewer,

Manager,

Nuclear Safety

and Licensing

P. Carteaux,

Gneral Supervisor,

Mechanical

and Welding

R. Hunsicker, Electrical Supervisor

  • J. Kurgan,

Manager,

Nuclear Operations

and Support

"S. Klementowiscz,

Manager,

Radiological

Support

"F. Pisarsky,

General

Supervisor,

Mechanical

and Welding

U.S. Nuclear

Re viator

Commission

"H. J. Miller, Director, Division of Reactor Safety

"B. Burgess,

Section Chief, Division of Reactor Projects

"M. Caruso,

Acting Chief, Performance

and guality Evaluation,

Nuclear Reactor Regulation

"Z. Falevits,

Team Leader,

Division of Reactor Safety

"J. Giitter, Licensing Project Manager,

Nuclear Reactor Regulation

"F. Jablonski,

Section Chief, Division of Reactor Safety

"B. Jorgensen,

Senior Resident

Inspector

"R. Mendez, Assistant

Team Leader, Division of Reactor Safety

"D. Passehl,

Resident

Inspector

"Denotes those present at the exit on January

18,

1990.

Other licensee

personnel

were contacted

as

a matter, of routine during the

inspection.

2.0

Introduction to the Evaluation

and Assessment

of Maintenance

An announced

NRC team inspection of maintenance

was conducted during normal

plant operations

at the Donald

C.

Cook Nuclear

Power Plant during the period

of December

4-8 and 18-22,

1989.

The inspection

was conducted

to evaluate

the

extent that

a maintenance

program

had

been developed

and

implemented.

Three

major areas

were evaluated:

(1) overall plant performance

as affected

by

maintenance;

(2) management

support of maintenance;

and (3) maintenance

implementation.

This inspection

was based

on the guidance

provided in

NRC

Temporary Instruction 2515/97;

"Maintenance Inspection,"

and Drawing 425767-C,

"Maintenance

Inspection Tree."

The drawing, which is attached

to this report,

was used

as

a visual aid during the exit meeting to depict the results of the

inspection.'cronyms

used in this report are defined in Appendix A.

Results of this inspection

were derived from data obtained

by observation of

current plant conditions

and work in progress,

by review of completed work,

and by evaluation of the licensee's

attempt at self assessment

of maintenance

and correction of weaknesses.

Major areas of interest

included electrical,

mechanical,

instrument

and control

and the support

areas cf radiological

control, engineering,

quality control, training, procurement,

and

operations'roblems

identified by the inspectors

were evaluated for effect on Technical

Specification operability and technical

or managerial

weakness.

2.1

Performance

Data

and

S stem Selection

2.1.1

Historic Data

The inspectors

considered

the latest Systematic

Assessment

of Licensee

Performance

(SALP) report and completed

NRC inspection reports.

Primarily, the

inspectors

were sensitive to technical

and managerial

problems that appeared

to

be maintenance

related.

Results of this review indicated that there were poten-

tial weaknesses

with the preventive maintenance

(PM) program,

motor-operated

valves

(MOVs), parts

and material controls, trending, root cause analysis,

and

engineering

involvement.

The inspectors

reviewed plant operations

history data for 1989, to assess

the

license's

performance

in meeting established

goals.

Results follow:

The non-outage

backlog of corrective maintennace

job orders for both units

was

1772; the goal

was 850.

Forced outage

rate for Unit

1 was

1.64/> and for Unit 2 was

1.57/>,

the goal

was less

than

4/o.

Two unplanned

reactor trips occurred

on Unit

1 and'4

on Unit 2; the goal

was less

than

one per unit.

Two of the six trips were attributed to INC,

two to operational

errors,

and two to equipment failures.

Two engineered

safety features

(ESF) actuations

occurred

on Unit

1 and

one

on Unit 2;

a goal

was not established.

No unplanned

safety

system actuations

occurred;

the goal

was zero.

Thirty-two licensee

event reports

(LERs) were issued;

the goal

was 24.

During 1988 and

1989 through the inspection date,

54

LERs were submitted

with 25 attributed to maintenance/surveillance

problems.

Equivalent availability for Unit

1 was 69.3X and for Unit 2, 74.4%; the

goal for Unit 1 was 705 and for Unit 2, 80K.

Cumulative whole body dose for 1989 for both units was

508 (TLD) man-rem;

the goal

was 487.7

(SRD) man-rem.

Although the goal

was not met, the dose

for 1989 was considerably

below the industry average

of 732 man-rem for a

2 unit site

~

Some goals

had been established

to determine if maintenance

was accompli shed

including

maintenance

backlog

and control

room instrument job orders.

However,

the licensee

had not established

goals for measuring effectiveness

of maintenance

such

as the

number of limiting conditions for operations

due to equipment

problems,

the number of power reductions

due to equipment

problems;

percent of

rework,

and failed surveillances.

2.1.2

S stem Selection

The systems

and components

selected for this inspection

were based

on the

probability risk assessment

(PRA) study furnished to the team by the Reliability

Applications Section of the Office of Nuclear

Reactor Regulation

and review of

LERs, Deviation Reports,

Nuclear Power Reliability Data System

(NPRDS)

and

discussions

with the senior resident

inspector.

The systems

selected

were the

Auxiliary Feedwater

System

(AFW), Emergency Diesel Generators

(EDG), and Station

Air Compressors

(CAS).

2.2

Descri tion of Maintenance

Philoso

h

The inspectors

reviewed plant policy statements,

administrative

procedures,

organization charts,

established

goals,

and documents that described

improvement

programs for the maintenance

process.

Very limited maintenance

improvement

programs

were initiated in the la'st several

years.

An organizational

change

took place at the Donald

C.

Cook site

on November I, 1989,

to enhance

outage

and maintenance

management.

The major affect of the reorganization

was combining

the maintenance

group

and the

IKC group into one maintenance

department.

Some

confusion existed

among the maintenance

personnel,

which was

compounded

because

the organization

and individual responsibilities

had not been

documented.

Inter-

views and discussions

with maintenance

personnel

indicated that authority,

responsibilities,

accountability

and interfacing of the various plant groups

involved in maintenance

was not formalized or clearly defined.

Although in one

department,

each

group maintained

independent

internal instructions

and procedures.

Maintenance policies existed only for the instrument

and controls (I&C) group.

Departmental

goals did not exist for any of the maintenance

groups

and station

goals relative to maintenance

were not aggressively

pursued,

consequently,

most

were not achieved in 1989.

The maintenance

philosophy appeared

to be mainly compliance oriented with little

consideration for an effective proactive process.

Maintenance

was primarily based

on Technical Specification

requirements

and

some vendor manual

recommendations;

however, only 893 of 6800 vendor manuals

had been

reviewed

and approved.

The inspectors

could not determine if the licensee's

maintenance

program was

appropriately

balanced with corrective maintenance

(CM) and preventive mainten-

ance

(PM) because

a formal

PM program

had not been established

and the licensee

did not adopt or track established

industry guidelines for maintaining

a ratio

between

CM and

PM.

The licensee's

predictive maintenance

program was at the

early stages

of implementation in the areas of vibration analysis

and oil sampling.

Thermography

was in the planning staoes

with implementation

planned for sometime

in 1990.

Formal

procedures. did not exist for the predictive maintenance

programs

and trending of results

was not started.

On the positive side,

the licensee

recently initiated

a reliability centered

maintenance

(RCM) pilot program.

RCM is

a concept that is gaining increased

attention throughout the nuclear industry as

a means to systematically

examine

the basis for PM programs

and establish

a more rational

approach to

PM.

An

overall objective of the

RCM program was to completely evaluate current

PM

practices.

Other

RCM objectives

include:

reduce

the amount of CM; establish

PM

frequencies

based

on historical data

and

sound engineering

judgement; redirect

time directed

PM tasks to condition monitored/diagnostic

type

PM tasks;

evaluate

vendor

recommended

PM tasks;

and optimize plant resources

in implementing

an

effective

PM program.

The licensee

has taken credit for the

RCM program

as

a

means to eventually integrate

the existing

PM practices

into a single

PM program

which is based

on

a well documented

and systematic

approach.

This program is

considered

a strength.

The licensee

included three

systems

in the

RCM pilot program:

Feedwater,

Auxiliary Feedwater,

and Service Water.

The

RCM program staff consisted

of four

contractors,

three

system engineers

and

an

RCM Project Manager.

The licensee

recently initiated the system engineering

program to support the

RCM project,

however,

formal procedures

to govern the program, responsibilities,

and qualifi-

cations requirements

did not exist.

A systems

engineer

was assigned

to each

system currently being assessed

in the

RCM pilot program.

The licensee

also initiated

a Level III Probali stic Risk Assessment

(PRA) in

response

to Generic Letter 88-20.

The licensee

planned to incorporate

PRA

results into the

RCM program.

Component

and safety

system important measures

will be compared to

RCM results to ensure that important failure modes

have

been

identified and addressed

and that

a particular safety

system received

the

appropriate

degree of attention.

The

PRA also

has applications

to corrective

maintenance.

Importance

measures

for systems

and components

might be used

as

a basis for pr ioritizing the safety significance

and order of performing

corrective maintenance

job orders.

Implementation of PRA techniques will

provide useful

feedback applicable to the maintenance

program

and was considered

a strength.

The plant manager recently established

a monitoring system to better

manage

and

measure

maintenance

effectiveness.

A matrix was developed that related major

topics to key attributes of the maintenance

area,

including criteria from NRC

and other established

industry maintenance

related documents'n

addition,

findings and observations

of NRC inspections,

SALP reports,

and other assessments

will be compiled into each major topical areas.

Each of the topical

areas will

be assigned

to

a responsible

licensee

individual to develop

an action plan to

improve performance,

to develop

a system for measurement

and monitoring,

and

develop appropriate

reporting criteria.

In addition, goals

and objectives will

be established

for each of the topical areas

to improve performance

at the

Donald

C.

Cook plant.

It was too early to assess

program implementation

and

results;

however,

the program itself was considered

a strength.

2.3

Observations

of Current Plant Conditions

and

On oin

Work Activities

2.3. 1

Current Material Condition

The inspectors

performed general

plant as well as selected

system

and component

walkdowns to assess

the general

and specific material condition of the plant to

verify that job orders

had been initiated for identified equipment

problems,

and to evaluate

housekeeping.

The selected

systems

were identified in Section

2.1.2 of this report.

Walkdowns included

an assessment

of the buildings,

components,

and

systems for

proper identification and tagging, accessibility, fire and security door

integrity, scaffolding, radiological controls,

and any unusual

conditions.

Unusual conditions included but were not limited to water, oil, or other

liquids on the floor or equipment;

indications of leakage

through ceiling, walls

or floors; loose insulation; corrosion;

excessive

noise;

unusual

temperatures;

and abnormal ventilation and lighting.

Both units were in operation

and subject

to operating

pressures,

flows, and temperatures.

Two obvious problems

from the walkdown inspections

were the significant number

water,

o" oi> >eeks

<rom the

AFM and

DG systems,

and the lack of

consistency

in tagging deficiencies

in the plant.

Tagging of deficiencies

was

not specifically required,

which resulted

in a lack of consistency.

As a

result,

many deficiencies

were noted,

but not tagged.

Also, several

tags were

found for which a job order did not exist or the job order was completed,

indicati ng

a weakness

in the link between deficiency .identification and wor k

accomplisnmeni.

A number oi the leaks

had already

been identified by plant

personnel,

were tagged,

and

some utilized a temporary arrangement

to catch

and

redirect the leakage to an appropriate drain.

Specific observations

included:

Identification of components

and equipment

was generally

good and was

located

on or near the equipment.

Color coding by a uniquely colored band

around the identification marking was considered

a strength.

Oil was leaking from some

EDG fuel oil transfer

pump regulator

caps

and

buckets

were placed

under the caps to collect the oil; there were numerous

packing leaks

and excessive oil was leaking through the diesel

mounting

bolts; fuel was leaking through

some of the diesel

fuel injectors;

in

addition, water

leaks were noted by the

EDG jacket water

pump.

In a

letter dated

September

29,

1989,

"Emergency

DG Reliability Status

Report,"

it was stated that analyses

of the diesel jacket water by the plant

laboratory indicated that there

was

some difficulty maintaining the proper

level of corrosion inhibitor due to leakage

from the jacket water

pump

packing.

The licensee

issued job orders

on December

1,

1989, to resolve

these

problems.

Numerous

packing leaks were observed

coming from the

AFM pumps.

Two of the

six pumps

had excessive

leaks but

a job order

had not been written to

correct the problem, which is discussed

at length in Section 2.3.2.2.

The

team also observed

a large

number of system fluid leaks

and approximately

400 catch basins for controlling those that were contaminated.

The licensee

stated

in the ore-exit

on January

12,

1990, that 207 of the leaking valves

had open job orders for repair,

as well as the numerous

steam

and other

liquid leaks noted by the team in the rest of the plant.

Several

safety valves were observed that were excessively

corroded,

incorrectly fitted, or leaking.

In particular,

safety valve SV-71 of the

Component Cooling Mater System,

located

on the Spent

Fuel Pit Heat Exchanger,

was leaking excessively

and did not have

a job oder tag.

The matter of

safety valves is discussed

at length in Section 2.6.4.

Calibration sticker information was inconsistent

for several

instruments

observed

throughout 'the plant.

Non-safety related

instruments

and

indicators

had calibration stickers that were either marked "N/A", were

illegible or were past

due for calibration.

Some calibration stickers

were

blank.

Additionally, containment control air ring header

pressure

indicator,

1-XPI-185,

was off scale high and was overdue for calibration by ten months.

The inspectors

were informed that calibration sticker information for

balance of plant (BOP)

and non-safety related

instruments

would be eliminated

by the conversion

process

to

a

new Instrument

Data System (IDS). The calibra-

tion stickers

would show reference

to IDS information instead of a calibration

due date.

The conversion

process

to the

new IDS program

was on-going at the

time of the walkdown.

An oil pool existed

on the east

end foundation of the east

main feed

pump

turbine; valve

1-DRY-331 had

a significant body to bonnet leak;

and there

was

a significant amount of oil on the base of plant air compressor

2-0ME-41.

Water

seepage

was observed

coming from the walls below grade level of the

screen

wash

pump room.

Mineral deposits

on the walls indicated that the

water seepage

occurred over

a fairly long period of time.

Corrosion

was

noted

on valve 1-BD-142, which became

apparent

when the lagging

had been

removed for work on an adjacent

valve.

The problem of external

corrosion

occurring beneath

lagging should receive additional attention.

Numerous platforms were observed

throughout the plant with vertical ladders

that provided access.

In many instances,

the safety chains installed at

the top of the ladders

were not in use,

which presented

a personnel

safety

hazard.

Ten temporary structures,

material

storage

cages,

were identified by the

licensee

in the Auxiliary Building that

had been in place approximately

three to six years.

The licensee

could not demonstrate'hat

the structures

were analyzed for seismic

impact

on safety related

equipment.

Based

on the

results of plant walkdowns of the ten areas

of concern,

the licensee deter-

mined that three of the structures

posed

a threat to safety related

equipment

during

a seismic

event,

and were therefore dismantled

and

removed.

The

licensee

determined that

a possible threat existed to safety related or

important to safety equipment at the 609'valuation.

Condition Report

(CR)

12-12-89-2014

was issued to review the conditions for possible

upgrading,

replacement

or removal of the temporary structures.

Nine tags

from equipment in the diesel

generator

room and

a switchgear

room

were selected

by the inspectors

to evaluate

the effectiveness

of the licensee's

deficiency identification program.

Open job orders existed for three of

the tags.

For six of the tags,

the work was completed

or cancelled

and

the job orders

were closed.

However, tags

B016950,

B016832,

BQ12209,

B017240,

029643

and

15119

had not been

removed

as required

by procedure

PMI-2290, "Job Orders",

Revision 8, Section 4.4.8.

This requires that

upon

completion of the physical

work required by the job order,

the individual(s)

responsible

for performing the work shall

ensure that all appropriate

follow-up actions are completed.

Section 4.4.8.3 requires that job order

tags

be removed

and discarded

and the appropriate

box on page

2 of the

job order form shall

be marked.

The inspectors

noted that for sev'eral

of

the job orders this section

had

been

marked but the job order tag was

physically hanging

on the equipment.

Additionally, for job order

15119

the explanation for not discarding

the job order tag was that the tag

could not be located.

However, the inspectors

located this tag during

a

walkdown on the Unit 2 diesel

generator

room.

The licensee

appeared

to

have

an excessive

number of tags

hanging

on equipment,

although job orders

were completed or cancelled.

This failure to follow procedures

is an

example of a violation of 10 CFR 50, Appendix B, Criterion

V (50-315/89031-01A;

50-316/89031-01A).

2.3.2

On oin

Work Activities

The inspectors

observed

routine ongoing work in electrical,

I&C, and mechanical

maintenance

areas.

The inspector s selected

these activities from the plan of

the day listing, work assignments

in individual maintenance

shops,

and through

discussions

with individual foremen.

Where possible,

safety significant

activities were chosen for review.

Since both units were in operation,

the

inspectors

could not observe

many safety related maintenance activities;

most

activities observed

were routine

and surveillance activities.

Maintenance activities were witnessed/observed

to determine if those activities

were performed in accordance

with required administrative

and technical

require-

ments.

Work activities were assessed

in the following areas:

work control

and

planning;

management

presence,

involvement,

and knowledge; quality control

(gC)

presence

and involvement; health physics

(HP) support

and hazards;

procedures

available,

adequate,

and used;

personnel

trained

and qualified; materials avail-

able,

adequate

and used;

meausri ng and test

equipment

(MME) and tools proper,

calibrated," and used;

post maintenance

testing

(PMT) acceptance

criteria,

and

performed

as specified.

2.3.2. 1

On oin

Electrical Maintenance

Electrical maintenance

has only recently

been established

as

a maintenance

function

of IEC.

Previously, electrical

maintenance

was integrated with mechanical

main-

tenance.

Established

electrical

safety related

PM requirements

was limited to

circuit breaker

and motor lubrications, battery maintenance/inspections

and

emergency lighting maintenance.

Formal

PM for pump electric motors,

valve actuator

motors

and G.E.

HFA relays

was not established.

Predictive electrical

maintenance

appeared

to have

been limited to occassional

thermographics

on safety related

components.

PM on

BOP components

was limited to required turbine generator

maintenance.

There was

no established

predictive electrical

maintenance

program

for BOP components.

The inspectors

observed

portions of four routine electrical

maintenance activities

as discussed

below.

In addition, detailed observations

were

made of thermal

overloads installed in various motor control centers

(MCC).

8043635

RFC 2900

RFC 1482

Perform

PM on hyrdrogen

recombiner

2-HRI power supply

Pull cables for radiation monitors

Splice copper to aluminum cables

2THP 6030 IMP.250

Calibrate

4kV ESS bus undervoltage

relays

Based

on the observation

of activities

and review of past maintenance,

the

inspectors

concluded that electrical

maintenance activities in the pertinent

areas

described

in Section 2.3.2 were satisfactorily accomplished

by mainten-

ance personnel.

Concerns

were identified with the narrow scope of electrical

PM program, traceability of cables

and aluminum splice kits, absence

of gC hold

points

and evidence of "peer" inspection,

inadequate

test equipment

and method-

ology for testing undervoltage

relays,

and improper installation of thermal

,overloads

in various

MCCs.

B043635 - The inspectors

noted excessive

dust. in both the hydrogen

recombiner

transformers

and power supplies during

a walkdown of the licensee's

switch-

gear rooms.

These

components

were not included in the

PM program.

The

licensee

subsequently

issued

a job order to perform

PM which was completed

on December

7,

1989.

RFC-1482 - The inspectors

observed

several

splices in the

MCC compartments.

Many of the splices

were performed in accordance

with RFC-1482,

which

terminated approximately

40 safety related

power feeds to motors.

A copper

extension

piece

was spliced to the field routed power aluminum cable that

supplies

power to the individual motors.

The engineering

department deter-

mined that termination of the aluminum cable to copper

connections

at the

motor starter in the

MCC compartment

was unacceptable,

therefore

the metal

sleeves

were used to splice the copper

and aluminum cables.

The design

change

package

did not contain information about the type of sleeve,

the

material of the sleeve,

or the type of splice or anti-oxidizing agent which

is

common

when aluminum and copper are spliced.

Engineering

Design Speci-

fication (EDS) 608,

Revision

1, stated that aluminum sleeves

were of an

electro tin plated finish and specified

approved joint compounds.

However,

the design

change

package

made

no reference

to the type of sleeve

used.

The licensee

stated that the sleeves

were obtained

from stock including the

cable extension

pieces

and cable.

The licensee

could not provide documen-

tation regardi ng the traceabi lity of the cable or aluminum sleeve

because

the information was not written or documented

in the design

package

or other

quality documents

related to RFC-1482.

10 CFR 50, Appendix B, Criterion VIII requires that the licensee establish

measures

for the identification and control of materials,

parts

and

components.

Criterion VII further states that measures

shall

assure

that

identification of the item is maintained

by part numbers or serial

number

either

on the item,

as required throughout fabrication, erection, installa-

tion, and use of the item.

Failure of the licensee

to establish

documented

traceabi lity of the cable extension

pieces

and the aluminum splice kits is

a violation to

10 CFR 50, Appendix B, Criterion VIII (50-315/89031-02;

50-316/89031-02).

RFC 2900 - The inspectors

observed

the installation of a cable

from an area

radiation monitor to a control panel

in the auxiliary building.

The

completed work package

was only partially filled out and

many of the steps

were not filled out. In addition,

no gC inspections

or gC hold points were

established.

The licensee

used

a peer inspection

process

that consisted

of

a qualified maintenance

worker that accompanies

the maintenance

personnel

and verifies

gC inspection

hold points.

The inspectors

observed

several

maintenance

and surveillance activities

and

none involved

a

gC type inspec-

tion; however,

none of the maintenance activities had

gC inspection

hold

points established.

Inspection of maintenance activities was practically

non existent.

The inspectors

concluded that the licensee's

program for peer

type maintenance

inspections

was vague

and suffered

from lack of guidance

and acceptance

criteria.

10

The cable pulling procedure for safety related

components

had two gC

inspection hold points neither of'hich addressed

segregation

of power,

control,

and instrumentation

cables;

separation

of redundant

Class

1E

cables

and non-safety related cables;

maximum allowable cable pull tension

and the sidewall pressure

factor acceptance

criteria; or the allowable

minimum bend radius.

The inspector

noted that procedure

12

MHP 5021.082.005,

"Removal

and Installation of Power

and Instrumentation

and Control Cable",

Revision 8, was

one of the the few procedures

that included

gC inspection

hold points.

2 THP 6030 IMP.250 - The inspectors

observed

portions of the monthly 4kV

diesel start

and essential

bus undervoltage

relay calibration surveillance

performed

under procedure

2 THP 6030 IMP.250,

"4kV Diesel Start,

4kV ESS

Bus Undervoltage

Relay Calibration," Revision

7 and required

by Technical

Specification Section

3'.2,

Engineered

Safety Feature Actuation System

Instrumentation.

The inspectors verified that the voltmeter used

by the

technicians

was in calibration

and the type required

by procedure.

Technicians

indicated that the acceptance

criteria for the undervoltage

relay dropout

was 90.3 to 91.8 volts, which was consistent with the Technical

Specification

4kV Bus loss of voltage values.

The 'inspectors

noted that the

increment the analog

type voltmeter could indicate

was to the nearest volt,

that is,

90,

91 or 92, making the measurement

to the nearest

one-tenth of a

volt unlikely since there are

no division markings

between

the numbers.

The

inspectors

noted that the technicians

interpolated results while the volt-

meter's

indicator

was in motion, that is, in the increasing

or decreasing

direction and documented

the results in tenths of a volt.

The as-left drop

out voltage value of relay 27-3721C

was 91.2 volts and the pick-up voltage

was 100.2.

In addition,

the inspectors verified records for the voltmeter used in

calibrating the relays.

Procedure

2THP 6030

IMP.250 stated

in Section 3.0,

Equipment Required, that testing

personnel

shall

use

a Westinghouse

type

PA-161 analog voltmeter, or equivalent, with equal

or better accuracy

and

adequate

range to measure

the desired

parameter.

The accuracy of the PA-161

was

+1/o of full scale,

150 volts or +1.5 volts.

The tolerance of +1.5 volts

was the entire range or band of the Technical Specification

acceptenance

criteria drop out voltage from 90.3 volts to 91.8*volts and regardless

of

where -the drop out voltage occurred the accuracy of the test results

were

questionable.

Furthermore,

the technicians

used

a cumbersome

technique for

obtaining data that involved use of hand signals

by two technicians

to

transmit

messages

to indicate the moment the relay dropped out to

a third

technician.

The third technician,

who was not within sight of the first

technician,

adjusted

the input voltage

and responded

to the second

technician's

signal.

The inspectors

noted that the licensee

found the following four diesel start

relays out of calibration:

27-1T21B,

27-1T21C,

27-3T21C

and 27-3T21D.

In

addition,

a 4kV undervoltage

relay 27-T21A-1 was also found out of calibra-

tion.

The inspectors

determined that these relays

have continuously

been

found out of calibration by the licensee.

Due to problems with the diesel

start relays the licensee

has

increased

the surveillance

frequency

from every

refueling outage to a monthly schedule.

The licensee

issued

CR 8.9-1352 to

document

the out of calibration relays

and was in the process

of issuing

an

LER.

11

The current testing

method

and testing

equipment did not appear

adequate

to measure with sufficient accuracy

the required Technical Specification

surveillance

parameters.

10 CFR 50, Appendix B, Criterion XI, test control,

states

that

a test program shall

be established

to assure

that all testing

required to demonstrate

that structures,

systems

and components will perform

satisfactorily in service is identified and performed in accordance

with

written test requirements

and acceptable

limits contained

in applicable

design design

documents.

In addition, Criterion XI further states

that the

test procedures

shall

assure

that adequate

test instrumentation is available

and used.

Failure to provide adequate

test methodology

and instrumentation

is

a violation of 10 CFR 50, Appendix B, Criterion XI (50-315/89031-03;

50-316/89031-03).

During field observation

and review of MCC compartments

associated

with

the

EDG the inspectors

noted that thermal

overloads

could be placed in one

of two positions,

which was in accordance

with the vendor manual.

The

inspectors

compared field thermal

overload size

and orientation data

with the engineering

data provided by the licensee for 20 motors.

Ten

thermal

overload sizes did not match the licensee's

design information.

In addition,

the licensee

found that"nameplate

motor data verified in the

field did not match the drawing data.

The full load

amps

(FLA) rating of

several

motors

was compared to the design drawings.

Six did not match the

drawings.

The discrepancies

included safety

and non-safety-related

loads.

The inspectors

noted that the thermal overloads installed in MCC compart-

ments

1-ABD-A-2E and

1-ABD-B-1C for the

EDG starting air compressors

were

three sizes

too large,

which would result in the air compressor

motor

operating

in an overloaded condition for an extended

period of time.

An

RFC was prepared

to have the devices

replaced.

In addition, the

inspectors

noted that five other non-safety-related

loads still had the

incorrect thermal overload size regardless

of which FLA was used,

as found

or as noted

on the drawings.

The licensee

indicated that the correct

thermal

overload would be replaced for the above loads

and that the drawings

would be updated to reflect the correct

FLA.

The inspectors

also noted the incorrect setting of thermal

overloads

in

MCC compartment

1-E2C-C-R2D,

which feeds

RHR loop isolation valve ICM-111.

RFC 12-2180 required that the thermal overload heater

be installed

and set

at the low trip current rating instead of the high trip current rating as

found.

The as-found position of the, thermal

overload heaters

was not

required to be documented

when the heaters

were removed during maintenance

because

this was considered "skill of the craft".

The licensee

stated that

if a question

arose

about the position of the heater,

the electrician would

obtain the nameplate

FLA and look up the

MCC vendor manual to determine

the

correct position.

Based

on the above discussion this explanation did not

appear

probable.

The licensee

agreed that the heater in

MCC 1-E2C-C-R2D

was incorrectly installed.

Failure to comply with the requirements

of RFC

12-2180

was considered

a violation of 10 CFR 50, Appendix B, Criterion

V

(50-315/89031-01B;

50-316/89031-01B).

The inspectors

determined that in. 1989

numerous

CRs

and at least

32 Problem

Reports

(PR)

had been written about inconsistencies

between

various design

drawings

and the actual field configuration.

For example

on December

10,

12

1989,

CR 89-2085

documented that flow diagram OP-2-511B-14 did not match

actual field conditions.

On February 2,

1989,

PR 89-220,

documented

that

an inconsistency

existed

between

various wiring prints in the

number desig-

nated for the terminal that was assigned

to another terminal.

On June

16,

1989,

PR 89-580 documented that

an unidentified jumper wire was found

installed in the terminal

bus for VFS-7 while troubleshooting chiller P7

tripping problems.

This jumper would have prevented

the chiller from

tripping on low flow.

The jumper was placed

by maintenance

to jumper

a

faulty switch rather than having it repaired.

In addition, the

IKC super-

visor indicated in the

PR that in the past there

had

been similar jumpers

identified.

On August 23,

1989,

PR 89-969 documented that, contrary to

PMI 2030, drawings maintained

by the maintenance

department did not reflect

the latest revision of drawings listed in the master drawing index.

The inspectors

observed

portions of Emergency

Diesel Generator

Sub Panel

DGAB and 600 Vac Auxiliary Bus 21A MCC2-ABD-A9ESS and identified several

wiring discrepancies.

Subsequent

investigation

by the licensee

determined

that wiring diagrams

PS2-94205-0

and PS2-92320-1

were not in conformance

with field installation.

CRs 89-2055

and 89-2056 were initiated to revise

the drawings.

The inspectors

determined that procedure

PMI-2030 "Document

Control," Revision

10,

was inadequate

because it failed to include the

requirements

that Master Drawing Indexes

be reviewed

by intended

users for

the latest

as built drawings located in the plant master file, which was

denoted

by an asterisk

in the Master Drawing Index.

The inspectors

also

determined that drawings issued

by the document control center

were not

the latest

as built drawings partially because

personnel

were not aware of

the requirements

denoted

by the asterisk

in the Master Drawing Index.

The

inspectors

concluded that management

attention

was weak in the area of

identifying and correcting as-built discrepancies.

Inadequate

procedures

is an example of a violation of 10 CFR 50, Appendix B, Criterion

V

(50-315/89031-01C;

50-316/89031-01C).

2.3.2.2

On oin

Mechanical

Maintenance

The inspectors

observed

portions of 18 mechanical

maintenance activities

as discussed

below:

A001682

A001845

A002213

A007539

A008991

A013632

A014194

A019318

Repair auxiliary building snubbers

Repair

steam leak on valve 1-RCA-1036

Maintenance of reheater

drain control valve I-MLC-401

Change oil in

DG starting air compressor

I-QT-142-CDI

Replace

the backwash

nozzles

in traveling screen

1-3

Repack strainer of south miscellaneous

cooling water

pump

Investigate

and correct problem in the acid

sump

pump

Repair valve 1-DRV-350

13

A017539

A18578

B000265

8000425

B015829

B017262

8017133

B017427

B017 540

Lubricate

AFW and

EDG air compressor

Replace

north misc sealing

and cooling water

pump

Maintenance of drain control valve 2-MRV-470

Temporary

steam leak repair

using Furmanite

compound

Repair Unit 2 main turbine oil coolers

Weld on piping and fittings around 2-B-323

Replace

mechanical

seals

on motor driven

AFW pump

Replace

DG starting air compressor

2-gT-142-CD2.

Maintenance of north essential

service water

(NESW)

pump

in-board mechanical

seal

8018578

Repair south lube oil coolers

17688

Replace

mechanical

seals

on

NESW pump

Based

on the observation of activities

and review of past maintenance,

the

inspectors

concluded that mechanical

maintenance activities in the pertinent

areas

described

in Section 2.3.2 were satisfactorily accomplished

by maintenance

personnel.

Concerns

were identified with misapplication of a thread sealant,

lack of safety precautions

in procedures,

undocumented

amounts of lubrication

used,

use of replacement

parts without engineering

review and lack of acceptance

criteria for pump packing leakoff.

A008991 - The workers

used

a thread sealant to install the

new nozzles

in

the screen

wash

system.

The job order and procedure did not address

the

use of Loctite or any other thread sealant

in the performance of this

maintenance.

A014194 - This job required the workers to wear rubber coveralls,

boots

and

a face shield while working in the acid storage

room.

The area also

required monitoring the atmosphere

for sufficient levels of oxygen.

While

the workers were cognizant of these

precautions

and took appropriate

action,

the job order

and work procedure

contained

no mention of these

measures.

A017539 - The inspectors

observed that routine

PM action

was accomplished

in accordance

with the job order and the applicable lubrication cards.

The

lubrication cards

provided the greasing

locations

and the type of lubricant

to be used,

but provided

no information about the quantity to be used.

The

lubrication card provided

a blank space for the quantity required,

but none

of the cards specified

a quantity.

The lubrication cards for all the

DG

starting air compressors

and the

AFW pumps were also examined

and found to

have

no information provided for the quantity of lubricant required.

B000265 - The repair of valve 2-MRV-470 included replacement

of the

stem.

The specified part No.

1V389035162

was actually incorrect for the required

14

replacement

stem

and

a plug assembly.

Another stem part

No.

1K586935162,

slightly longer than the original'art,

was used for the repair of valve

2-MRV-470.

The replacement

part, class

23, standard,

was not reviewed by

engineering prior to its use for its suitability in this application

because

engineering

evaluations

were only performed

on class

30 safety-

related parts.

B017133 - During a walkdown of the Unit

1 and Unit 2 AFW pump rooms,

the

inspectors

noted that three of the six

AFW pumps appeared

to be leaking

through the

pump packing.

The job order identified excessive

leakage

through the inboard

and outboard

mechanical

seals,

the probable

cause

being

worn seals.

No other job orders

were written for the two remaining

AFW

pumps,

which also appeared

to be excessively

leaking.

Although

a job order

had been

issued

the licensee

explained that

a certain

amount of leakage

through the packing

was acceptable

per the vendor instructions,

but the

leakage

was not quantified.

The inspectors

reviewed the

AFW pump vendor

manual

and verified that the instructions require

a small

amount of leakage

for lubrication of the packing.

The manual further stated that shutting off

leakage

from the packing will result in burned packing,

scored shaft sleeves

and possible rotor seizure.

Moreover, the vendor manual

required that the

leakage

be controlled by making adjustments

of the gland nuts following the

startup of the

pump.

The inspector discussed

this last requirement

with two

cognizant maintenance

engineers;

both agreed that the only acceptable

method

for adjusting

pump packing is when the

pump is running.

The inspector

noted

that this requirement

was not specifically incorporated

into the motor driven

AFW pump maintenance

procedure

and not included in the turbine driven

AFW

pump maintenance

and procedure.

In addition,

the

pump manufacturer's,

"Pump

Operators'ata"

manual,

Second Edition on page

108, required the operator

to watch the packing carefully when starting

up.

The manual

stated that at

the first sign of heating,

the

pump should

be shut

down to allow the packing

to cool

and that several

pump starts

may be necessary

before the leakage

breaks

through

and the packing

box runs cool.

Additionally, Procedure

12MHP5021.056.002,

"Repair Procedure

for Turbine Auxiliary Feed

Pump,"

Revision 4,

made

no mention of any adjustment

to the packing before or

after the

pump was started.

The licensee

indicated that the procedure

would be revised

to incorporate

the acceptance

criteria.

Failure of the

licensee

to include qualitative acceptance

criteria in their repair

procedure is

an example of a violation of 10 CFR 50, Appendix B, Criterion

V (50-315/89031-01D;

50-316/89031-01D).

2.3.2.3

On oin

Instrumentation

and Control Maintenance

The inspector

observed

portions of seven

I&C maintenance activities as discussed

below.

A014129

Investigate/repair

U-1 pressurizer

heater

fan

failure

A014255

B017523

B043570

Repair

S/G

12 and

13 blowdown sample flow alarms

Repair turbine thrust bearing

lube oil gage

Power

steam generator

level transmitter

from a

separate

source

15

1

THP 4030 STP.411

2 THP 4030

STP. 510

Solid state protection

system logic and reactor

trip breaker train "B" surveillance

(Unit 1)

Solid state protection

system logic and reactor

trip breaker train "A" surveillance (Unit 2)

12

THP 6030

IMP.014

Calibrate

2 AB EDG protective relays

Based

on the observation of these activities the inspectors

concluded that

I&C

maintenance activities in the pertinent

areas

described

in Section 2.3.2 were

accomplished

by skilled, knowledgeable

and conscientious

personnel.

However,

concerns

in the areas

of poor work techniques

on

BOP equipment,

hand agitation

of instruments,

tools beyond calibration date,

improper method

used for

calculating

response

time, failure to have procedures

"in hand,"

and improper

technique

used to clean

and test relays were identified during observation of

the following work:

A014129 - During replacement

of an

SCR fan electronic "paddle" switch, the

inspectors

noted that the technician

soldering the switch .into place did

not exercise

any standard

techniques for electronic soldering.

The solder

joints were not cleaned,

and the switch had to be forced into position

because

the

SCR fan circuit wiring was too large

for the switch's pierced

solder terminals.

It appeared

that

no job briefing had been

conducted

regarding

the size of the

SCR fan wire compared to the replacement

switch.

This activity exemplified the fact that non-safety related

maintenance

jobs

did not receive the

same attention to detai

1

and emphasis

on job planning

as safety related

and Technical Specification work items.

A014255

Steam generators

12

and

13 blowdown sample

low flow alarms did

not operate

when

removed

from service

because

the flow meter indicators

were "stuck" at .3

GPM.

A non-licensed

operator

"tapped" the meter face-

plate,

which caused

the meter indication to drop to 0

GPM and the alarms

operated.

The flow meters

were declared

inoperable.

These

instruments

were Tech Spec related

and

CR 1-12-89-2004

was prepared

by the licensee.

After discussion with both the operator

and

an

IKC maintenance

supervisor,

the inspectors

determined that the "tapping"-of these particular instruments

was

an isolated

case.

The inspectors

discussed

with the licensee

the

negative

aspects

of agitating electrical/electronic

instruments.

B043570

The inspectors

observed

two crimpers in a technician's

work cart

beyond the calibration due dates.

The technician

was aware of that fact.

One crimper

ECO-002

had

a calibration due date of September

2,

1989,

and

the other,

ECOH-1 had

a due date of September

9,

1989.

Although, the work

was non-safety-related,

the attitude of the worker was disturbing because

of the the potential for using the tools when performing either safety

related or non-safety-related

work.

This appeared

to be

an isolated

case.

As discussed

in Section 2.3.4.2, overall control of tools was good.

1

THP 4030 STP.411 - A technician incorrectly calculated

Reactor Trip

Breaker

time response

from a strip chart recorder trace.

The technician

used the time response

from the trace "trailing" step instead of the

"leading" step.

The procedure

included

an attachment that illustrated

the

proper method to determine

time response

for the breaker,

but this aid was

16

not utilized by the technician until prompted

by the

IKC supervisor

at the

job site.

A review of previous

t'ime response

calculations for this

surveillance

indicated that the calculations

were correct.

2 THP 4030 STP.510 - Paragraph

7.2 of STP.510 surveillance

required

an

operator to manually "rack-in" Reactor Trip Bypass

Breaker "A" to the

"TEST" position and subsequently

to the

"OPERATE" position as

a prelude to

testing

the "A" Train Reactor Trip Breaker.

The operator

was observed

racking in the bypass

breaker without the use of "double-asterisked"

('":)

Procedure

12-OHP 4021.082.018

"Racking In and Out Reactor Trip, Reactor

Trip Bypass,

and

MG Set Output Breakers,"

Revision 2, which was required

to be "in-hand" when performing this evolution, but was not at the job

site.

The licensee

prepared

Problem Report 89-1349 to document the

discrepancy.

Upon further review it was noted that

a reactor trip had

occurred in the past during performance of the

same activity when the

wrong breaker

was "racked".

Failure to follow procedures

is an example of

a violation of 10 CFR 50, Appendix B, Criterion

V

(50-315/89031-01F;

316/89031-01F).

Procedure

STP.510

was also deficient from a

human factors standpoint

in

that

a technician

was required to manually hold

a Shunt Block pushbutton

inside

an energized electrical cubicle for approximately five minutes

( steps

7.3. 14 and 7.3. 19).

During tni s evolution, the technician did not

take appropriate electrical

precautions

such

as

removal of hand jewelry.

12-THP 6030

IMP.014

During inspection of a Time Overcurrent

(IAC) Relay,

the inspectors

observed

a maintenance

technician cleaning

the relay drag

magnet

and disk with the adhesive

portion of a calibration sticker.

Step

8. 1.2-2 of Procedure

IMP.014 "Protective

Relay Calibration", Revision 8,

specified the use of black electrical

tape

when cleaning

IAC relay

mechanisms.

Failure to follow procedures

is

an example of a violation of

10 CFR 50, Appendix B, Criterion

V (50-315/89031-01E;

50-315/89031-01E).

The inspectors

observed

a technician

perform

a cursory inspection of the

relay wiring terminations

and

use

a screwdriver

to tighten terminations

on

the instantaneous

overcurrent

type

PJC relay.

The relay inspection portion

of the procedure

for IAC or

PJC relays contained

no details

on tools or

techniques

to be employed

when checking relay wiring terminations

and hard-

ware for tightness

such

as torque requirements.

Additionally, documentation

concerning

the "as found" condition of relays during inspection

such

as

dirt, debris,

or corrosion,

was inadequate.

The data

sheet

contained

space

for the technician to enter

comments

on the results of relay inspections,

but nothing was documented.

The inspectors

concluded that inconsistencies

existed

in the conduct

and documentation

of electrical

equipment inspections.

A review of the licensee's

NPRDS report revealed

several

instances

of

equipment

problems related to dirt and foreign matter inside electrical

devices

and enclosures.

2.3.3

Radiolo ical Controls

Maintenance

work was observed

in contaminated

and radiation areas

as were

movements of tools/equipment

to and from these

areas;

interactions of workers

with radiological protection personnel

were also observed.

Cleanliness

and

17

housekeeping

appeared

generally

good.

Radiological controls,

posting,

and

labeling were good.

Radiation protect'ion job coverage

and As

Low As is

Reasonably

Achievable

(ALARA) support for major maintenance activities were

considered

strengths.

Through observations

of work in the planning

and implementation

phase,

and

discussions

with licensee

personnel,

the inspectors

determined that radiological

controls were integrated into the maintenance

process.

The ALARA staff appeared

to implement effective

ALARA oversight of maintenance

activities.

The

ALARA staff had good management

support.

Communications

and

the working relationship

between

the maintenance

planning department

had improved.

The ALARA staff attended certain planning meetings,

reviewed engineering

designed

work modifications

and maintenance

work packages

that involved dose producing

jobs, administered

the shielding program,

conducted

pr'e and post-job surveys,

and

wrote the Radiation Work Permits

(RWPs).

In most cases

there

appeared

to be

sufficient lead time to perform ALARA reviews;

Proposed facility changes

are

reviewed by the

ALARA staff.

The licensee

was developing job history files,

a photo library of equipment,

and

dose

saving documentation

to factor lessons

learned into the planning process.

A computer

program will be installed in 1990 that

will provide maintenance

job

planners with historical maintenance

data.

Oose

savings

were achieved

through

use of portable venting systems,

flushing

of valves

and lines, training,

and

use of previous lessons

learned.

Audits by the onsite

QA organization,

an outside audit,

and the corporate office

of the radiation program were performed.

Findings of a recent audit performed

of radiation protection activities were reviewed; identified problems

were

adequately

addressed.

For non-emergent

work, monitoring to support

RWP issuance,

RWP job coverage,

and

use of dosimetry

appeared

good.

Coordination

and data

exchange

between

health

physics

and mechanical

maintenance

for high dose or dose rate jobs was improving.

RWPs were adequately

developed

and detailed.

In most cases sufficient advanced

notice was given to the radiation protection department

so that adequate

radiological controls are

implemented.

Weaknesses

in this area

were also identified as follows:

Sufficient communication,

planning

and adequate

advanced

notice to

HP was

weak for emergent

and unplanned

outage work.

Although this weaknes's

can

cause overall

ALARA pre-job planning

and radiation

surveys to be degraded,

the inspectors

found no evidence that sufficient radiological controls were

not implemented for this type of work.

Frequently,

scheduled

RWP work was not performed

as

scheduled

and resurveys

were performed before the work began.

Resurvey work causes

unnecessary

radiation exposure.

Work activities in the

same

area or on the

same

equipment especially during

18

an outage

were not coordinated so.that

resurveying

and duplication of work

could be reduced.

Work packages

did not always contain sufficient tools/equipment

for work

in radiologically significant areas.

Work packages

should

have sufficient

detail to prevent workers from spending

unnecessary

time in dose rate areas.

Identified outage

work was not always well planned in advance

of scheduling.

There

appeared

to be

a problem with a significant number of outage jobs that

were scheduled

at the

end of the Unit 1 outage

which were insufficiently

planned.

This weakness

caused

unnecessary

personnel

exposure.

There were

a high number of workers assigned

to radiation producing jobs.

Unplanned

outage work performed without sufficient planning

and

communication

led to unnecessary

radiation dose

and inefficient work.

The licensee

maintained

reasonably

low personal

doses.

The total person-rem

for 1989 was 508; the industry average for a

2 unit site was 732,

however,

improvement in outage planning/scheduling

would further reduce station dose.

2.3.4

Maintenance Facilities

Material Contorl

and Control of Tools and

Measurin

E ui ment

The inspectors

reviewed the licensee's

activities in the areas

of facilities,

equipment

and material control to assess

support given to the maintenance

process.

Interviews were conducted with various maintenance

management

and

craft personnel

to determine

the policies, goals,

and objectives;

and follow-up

observations

were performed to determine

the extent to which the plant practices,

procedures,

equipment,

and layout supported

the maintenance

process.

2.3.4. 1

Facilities

The inspectors

observed

the licensee's

mechanical

workshop facilities, tool rooms,

mechanic's

work areas,

and supervisor's

offices.

All the mechanical

supervisors

had offices close to the office of other maintenance

management.

The licensee

had

good work shop facilities, tool rooms

and other work areas

in close proximity.

Other facilities included welding areas,

a sand blasting area,

and

a carpenter

shop for packaging

'equipment to be shipped to outside vendors.

The electrical

maintenance

shop

was being remodeled.

Few provisions were

made

to provide adequate

work space for the craft while the

shop

was being remodeled.

An untagged

spare

breaker

was placed

on

a bench

and breaker

parts were lying on

the floor.

The inspectors

noted that the "Hot Tool Room," located in the Auxiliary Building,

had

a list of hot tools contained there,

and maintained control of the tools

issued or received.

No evidence of contamination of plant areas

or personnel

due to the lack of positive control of hot tools was noted during the inspection.

IKC maintenance facilities were adequate.

The instrument maintenance

workshop

was located adjacent to the turbine bui lding close to the control

room and

auxiliary electrical

areas.

The

IKC superintendent,

supervisors

planners

and

coordinators officer's were located adjacent

to or in close proximity to the

maintenance

shop area.

19

".3.'.2

Material

and Test

E ui ment Control

The inspectors

evaluated

material

storage,

spare parts control,

and measuring

and test equipment

(METE) control.

Weaknesses

were identified with parts

control, procurement,

engineering

involvement,

and planning.

The warehouse facility included both level

A and

B storage

space.

Access to

the warehouse

was controlled,

environmental

controls were adequate,

and

housekeeping

was good.

Controls for consummable

materials

such

as solvents

and

cleaners,

thinners,

paint lubricants,

and gasket materials

were adequate.

A

separate

section

was established

for flammable materials

and those that

required special

handling

such

as hazardous

materials.

The inspectors

determined that the design

change

program did not consider

spare parts

when

a modification to equipment is performed,

which ultimately

results

in lack of spare parts

when equipment fails to perform as designed.

The inspectors

reviewed

a printout of open non-outage

job orders

on hold

for parts.

The sample

indicated that

none

had

a high priority or safety

significance.

k

The work package

completed

by the planner for job order B000265, repair of

valve 2-MRV-470, included

a computer printout from the equipment data

base

which indicated that the required part,

a valve stem,

was available

in

storage;

in fact, three were indicated but only one was needed.

However,

incorrect parts were stored

in

a designated

bin due to

a purchasing error

that caused

the incorrect parts to be ordered.

The mechanic

suspended

work

to search for a substitute part,

found one,

and ultimately completed the

job; however,

actual

use of the substitute part was not documented

and the

substitution

was not evaluated

by engineering.

Even though this was

a

BOP

activity, parts control, procurement,

and engineering

involvement were

considered

weak.

Also, as discussed

in Section 2.5,

a potential

generic

weakness

exists with planning because

of an inaccurate

equipment data

base

for establishing. the number

and types of parts in stock.

Control of METE was satisfactory.

Defective or "calibration due" instruments

were segregated

from those in calibration

and acceptable

for use.

Procedures

were developed for the issue,

return,

and recall of MME.

The individual

checking out an instrument;

the work order,

procedure,

or location used;

date

out,

and date returned

were recorded for permanent

records.

Storage of ready

for issue

MME was considered

excellent.

= Inventories were conducted of all

"ready for issue"

METE twice a day.

MTE issued

from the central

equipment tool room,

such as,

torque wrenches

and

dial indicators,

was accounted for by personnel

in the issue

room, with ultimate

control of calibration status

maintained

by the

METE lab.

The

METE lab was

maintained

by six full-time technicians qualified in metrology.

These technicians

conducted calibrations of all on-site

M&TE except the calibration standards,

which

were sent off-site for calibration.

All calibration records

were traceable

to

national

standards.

2.4

Review and Evaluation of Maintenance

Accom lished

2.4. I

Backlo

Assessment

and Evaluation

20

The inspectors

reviewed the amount of work accomplished

compared

to the amount

of work scheduled.

Emphasis

was placed

on work that could affect the operability

safety-related

equipment or equipment

considered

important to safety,

which

included

some balance of plant components.

Maintenance

work backlogs

were

evaluated for cause

and impact

on safety.

A coordinated effort did not exist to identify and track the overall

CM

and

PM backlog.

Periodic reports of backlogs

were issued to management

but the items were not prioritized, separated

by outage or non-outage,

nor

broken

down by

CM or PM.

Work backlogs

were separately

kept by the

maintenance

and

IKC groups.

The total backlog varied between

900 and

1200

throughout

1989 with CM at 88K and

PM at 12K.

At the time of the inspection,

an estimated

1400 job orders

were open for

more than

90 days

and

500 were open for over one year.

With the current

maintenance

staff, the backlog of 1400 job orders would take approximately

four months to complete,

which is higher than the three

month industry

average.

Forty-five job orders classified "expedite" or "important" were

backlogged greater

than

90 days.

Several

delays were attributed to non-

availability of parts or jobs awaiting parts.

Although the parts backlog

was large, operability was not affected.

In the mechanical

and welding

areas,

the backlogs

have steadily declined during the past five months.

About 10'" of the backlog

was attributed to administrative

review and closeout.

2.4.2

Review and Evaluation of Com leted Maintenance

The inspectors

selected

the equipment

and systems identified in Section 3.1.2

of this r'eport for further review.

The purpose of this review was to determine

if specified electrical,

mechanical,

and

IEC maintenance

on those selected

systems/

components

was accomplished

as required.

This review included application of

risk-based priority to the performance

and extent of maintenance;

evaluation to

determine

the extent that

RCM was factored into the established

maintenance

process;

evaluation of the extent that vendor manual

recommendations,

IE

Bulletins ( IEB), IE Notices (IEN), Significant Operating

Experience

Record

(SOERs),

and other outside

source

information was utilized; evaluation of the

extent that maintenance

histories,

NPRDS, information,

LERs, negative trends,

rework, extended

time for outage,

frequency of maintenance,

and results of

diagnostic

examinations

were analyzed

for trends

and root causes

for modifica-

tion of the

PM process

to preclude

recur rence of equipment or component failures;

evaluation of completed

JOs for use of qualified personnel,

proper prioritization,

adequate

work instructions, guality Control (gC) involvement, quality of documen-

tation of machinery history, description of problems

and resolutions,

and post

maintenance

testing; evaluation of work procedures

for inclusion of gC hold points,

acceptance

criteria,

ease of use,

and general

conformance

to NUREG/CR-1369.

2.4.2.1

Past Electrical Maintenance

The inspectors

reviewed

19 completed work packages

and

4 procedures

for the

attributes

included in paragraph

2.4.2.

A008279

Measure

the

1AB diesel

generator

and exciter air gas

A012225

Diesel would not maintain

speed

21

A013949

Auxiliary Building Ventilation System tripped

A014428

Locate

DC ground

B006652

Repair computer inverter backup voltage transformer

B012654

Locate

DC ground

1243

2289

4596

Clean, calibrate,

and inspect circuit breakers

Clean, calibrate,

and inspect circuit breakers

Clean, calibrate,

and inspect circuit breakers

020909

Clean

and inspect circuit breaker

21

PHC 4

706162

East

RHR pump breaker would not close

718266

Locate

DC ground

718613

Clean, calibrate,

and inspect circuit breakers

739183

S/G stop valve stuck in test position

91740

Clean, calibrate,

and inspect circuit breakers

MHI-7090

"Maintenance

Department

Inspection

Hold Point

Program,"

Revision

0

PMI-2010

"Plant Manager

and Department

Head Instruction,

Procedures

and Index, Revision

17

RFC 12-2982

Adjust setpoints

of safety related

pump motor

overcurrent relays

RFC 12-3008

Complete modifications for the miscordination

discrepancies

12

MHP 5021.056.002,

"Repair Procedure for Auxiliary Feed

Pump,"

Revision

4

h

12

MHP 5021.082.001,

"Inspection

and Repair of 4kV Circuit Breakers,"

Revision

7

12

MHP 5021.082.003,

"Inspection

and Repair of ITE Type K1600 and

K1600S

600

V Power Circuit Breaker," Revision

4

12

MHP 5021.082.006,

"Power Cable Termination

and Splicing," Revision

6

The work packages

reviewed were generally satisfactory.

Concerns

were identified

with inadequate

action to correct breaker failures,

use of copper to aluminum

splices,

inadequate

review of procedures,

and inadequate

control of fuses.

The

method for responding

to and locating dc grounds

was considered

a strength.

22

1243,

2289,

4596,

91740,

718613,

RFC 12-2982

and

FRC 12-30008 - These

items

included concerns

with possible relay coordination

problems.

Based

on

review of the referenced

documents,

the inspector

concluded that adjustments

made to safety related

pump motor overcurrent relays were not required to

be modified because

of the miscoordination discrepancies.

There were

instances

where fuses in the

250 Vdc distribution system did not have the

optimal 2/1 ratio,

however,

the inspector did not identify any instances

wnere tnis had

been

a problem.

Proper circuit breaker

and relay coordination

was maintained

through continuing design

review and control of relay setpoint

sheets.

Procedures

for calibration of relays

and circuit breakers

did not

include reference

to relay coordination

because

the subject is beyond the

scope of those

type procedures.

The licensee

recognized that relay

coordination

was important and that if not properly maintained,

a single

electrical fault could disable

power to one or both trains of safety related

equipment.

A014428,

B012654

and 716826

The licensee

implemented

a process

for locating

ground faults

on battery circuits by use of "D.C. Scout" instrumentation that

superimposes

an

ac signal

on individual battery circuits and indicates

the

faulted circuit by measuring

the lowest resistance

to ground and the highest

pulse magnitude.

During the past year the licensee

had issued

three job

orders to initiate action to locate ground faults.

The inspectors

noted

that in one instance

location of the ground took approximately

two hours,

which was in sharp contrast to the previous practice of operating

several

weeks with a

known ground

on the dc system.

The licensee's

process

for the

prompt location of grounds

was

a strength.

A013949 - On September

9,

1989,

the auxiliary building ventilation system

1-HV-AS-1 motor breaker tripped after five minutes of operation

because

one of the three connections

to the motor had disintegrated.

According to

job order A013949,

the wrong type and size of lugs"were

used to connect

the 'motor leads.

The lugs were too large for the wire and copper materials

were directly connected

to aluminum.

Consequently,

this caused

the

connections

to loosen,

which caused

the overheating

and subsequent

failure

of the motor.

Copper to aluminum connections

are not good practice

because

of the situation just described.

There are

numerous installations of this

type throughout the Donald C.

Cook Plant that have

been there

since the

plant was constructed;

however, significant problems

have not been reported.

706162 - On February 8,

1989,

scheduled

maintenance

was performed

on Brown

Boveri Type 5HK250 4kV Breaker T-1106.

During post maintenance

tests,

the

breaker

would not close

because

the operating

linkage would not reset

due

to hardening of the linkage grease.

Problem Report No.89-150 stated that

the grease

used

was believed to be of a type which would not require

replacement.

On February

27,

1989,

another

type 5HK250 4kV Breaker, T-llD4,

failed to close during

a test because

the linkage failed to reset.

Problem

Report

No.89-245 stated that the cause of the failure was

a build up of

old grease

and dirt in the breaker's

operating linkage.

The problem report

was reviewed

by Plant Assessment

Group (PAG) on March 17,

1989,

and deter-

mined the failure to be insignificant:

Prior to the

PAG review, the licensee

had notified the manufacturer of the failure of the closing mechanisms

in two

Type 5HK250 circuit breakers.

The licensee

requested

assistance

from the

vendor,

who on March 3,

1989,

issued

a

10 CFR Part 21 Report.

The report

was based

on the investigation

by the manufacturer

who determined that the

23

cause of the breaker failures was aging, dirt contamination

and hardening

of the grease

used for lubrication of the breaker's

closing mechanism.

The

breakers

were

17 years old and the closing mechanism

had never

been lubricated

because

of the licensee'

interpretation of the vendor manual,

which is

described

below.

Vendor

manual

1B6. 1.2.7-1,

under the "Lubrication" section for the

5HK250

circuit breakers,

states

in part,

"The circuit breaker requires

no lube ica-

tion during its normal service life.

However, if the grease

should

become

contaminated

or if parts are replaced,

any relubrication should

be done with

NO-OX-1D or ANDEROL grease

as applicable."

The licensee

mistakenly applied

the first statement

of the recommendation

without considering

the

second

statement.

In the

10 CFR Part 21 Report,

the vendor states

in part,

"Both

of these

statements

on lubrication must be considered

together.

The

second

statement

concerning

contamination

or parts

replacement

means that period-

ically, at least

when parts are replaced,

relubrication is required.

Also

dependent

upon the cleanliness

of the environment,

periodic checks for

contaminants

should be performed."

The Brown Boveri representative,

subsequently,

recommended

a procedure for cleaning

and lubricating the

closing mechanism

in order to provide for proper functioning of the breaker.

In an attachment

to problem report 89-245,

the licensee

committed to

revising

the maintenance

procedure

to include cleaning

and l,ubrication of

tne breaker closing mecnani sm on

a periodic basis.

Even though the licensee

was

aware of the problem,

no apparent

action

was

taken

and

seven additional

breakers failed to close

due to hardening of the

linkage grease

as follows:

Problem

Re ort

89-250

89-325

89-325

89-439

89-439

89-439

89-537

~Com anent

East

RHR Pump

East Motor Driven AFW Pump

West Motor Driven AFW Pump

Heater Drain

Pump Supply

1B2

Reserve

Feed to Aux Trans

1B5

Heater Drain

Pump

1D2

'mergency

Power

Feed to TllD

Date of

Concurrence

3/1/89

3/17/89

4/7/89

4/11/89

4/11/89

4/12/89

4/26/89

Problem Report 89-250 evaluated

by the plant Assessment

Group Committee

(PAG) on March 23,

1989, stated

in part, "All indicators point to this

being

an isolated incident.

No specific preventive

measures

are indicated."

Subsequently,

seven other breakers failed to close during testing

due to

binding of the operating linkage.

Failure to take prompt corrective action

is considered

another

example of a violation of 10 CFR 50, Appendix B,

Criterion XVI (50-315/89031-04A;

50-316/89031-04A)

.

Procedure

PMI-2010, "Plant Manager

and Department

Head Instructions,

Procedures

and Index", Revision

17, Periodic

Review 3.14, Section 3.14.1

states

in part, that "All effective instructions

and procedures

shall

be

reviewed

no less frequently than

once every two years.

Several

procedures

had not been

reviewed during the previous

two years,

including:

PMI 405,

MHI 2070,

MHI 7090,

12

THP 6030 IMP.071,

and

12

THP IMP.062.

As a result,

24

the procedures

were not updated to reflect feedback

and changes

to

PM

activities.

This failure to follow procedures

is

an example

.",

a v'ola+i

n

of 10 CFR 50, Appendix B, Criterion

V (50-315/89031-01G;

50-316/89031-01G).

2.4.2.2

Past

Mechanical

Maintenance

The inspectors

reviewed

13 completed

mechanical

work packages

and

9 procedures

for the attributes

included in Paragraph

2.4.2.

The inspectors

noted that in

most cases,

the work packages

indicated that prior approvals for the work were

obtained,

some hold points were noted,

necessary

procedures

were included

and

the calibration status of the

M&TE was noted.

The maintenance

problems

and

resolutions

were documented.

The procedures

were reviewed for completeness,

necessary

approvals,

adequacy

of work instructions,

user friendliness,

inclusion

of (jC hold points

and acceptance

criteria.

The following work packages

and

procedures

were reviewed:

A003612

A004018

A007755

A008177

A010634

A014421

B003137

016548

028121

039847

710327

723568

723762

Test set point of 1-SV-78-AB2 on Unit

1

AB DG

Rep'air of governor linkage of Unit

1 AB DG

Repair fuel injector on Unit

1

DG AB

Replace

governor

on Unit 1

CD DG

Disassemble

and inspect

check valve 1-FW-132-2

Test set point of valve 2-SV-78-AB2 on Unit 2 AB DG

Repair contorl valve 2-MRV-487

Annual

PM on control air dryer

Repair safety valve

on air receiver of AB DG

Clean

and inspect

2 AB starting air receiver tanks

Replace Unit 2 TDAFP governor valve bonnett

Annual

PM on Unit 1 control air compressor

Replace

bearing

housing

on

MD AFP

12

MHP 4030.STP.046,

"Emergency Diesel Generator

System

18 Month

Inspection",

Revision

1

12

MHP 5021.001.013,

"Fisher Type 7600 Series Butterfly Valves",

Revision

1

12

MHP 5021.002.001,

"Disassembly,

Inspection,

Repair

and Reassembly

of Reactor Coolant Pump", Revision

3

12

MHP 5021.016.001,

"Maintenance

and Repair Procedure for Component

Cooling Water Pump", Revision

2

12

MHP 5021.032.008,

"Emergency Diesel Generator Starting Air Compressor

Starting Air Compressor

Removal

and Installation", Revision

2

12

MHP 5021.032.012,

"Disassembly

and Reassembly

of Emergency Diesel

Engine

and Generator",

Revision

1

12

MHP 5021.032.022,

"Emergency Diesel

Engine Cylinder Head Inlet and

Exhanust 'Valve Inspection

and Repair", Revision

1

12

MHP 5021.032.037,

"Emergency Diesel

Engine Woodward Governor

Removal

and Installation", Revision

0

25

12

THP 6030. IMP.030, "Air Operated

Valve Check Out Procedure",

Revision

4

The work packages

were generally satisfactory.

Concerns

were identified with

documenting

nonconforming conditions,

a procurement

problem that caused

reuse

of defective

equipment,

and failure of MSIVs to meet acceptance

criteria for

closure time.

016548 - The work package for the annual

PM maintenance

of Unit 2 control

air dryer system did not include any procedures

for the maintenance

activities to be performed.

The mechanic

noted that none of the

54 filters

was installed in the six header filters. It was not clear from the record

how long the filters were missing.

A deviation report was not written by

the mechanic,

the work package

did not include any root cause for the

missing filters, and

no special

notation

was included to draw attention of

the planners or management.

723762 - The bearing

housing

purchased

for the Unit

1 East Motor Driven

Auxiliary Feed

Pump,

was unsuitable

and

had to be returned.

The licensee

used

the old bearing

housing.

A010634 - The work package for disassembly

and inspection of check valve

1-FM-132-2 did not include any acceptance

criteria for the torquing of the

cover nuts.

However, the package

did include

a sheet indicating the torque

used

and was signed

by the mechanic

and the

gC inspector.

MSIV Stroke Testing

On January

23,

1990, the licensee

stroke tested Unit 2

MSIV 2-2MRV-210 during the refueling outage.

The Technical Specification

required closure in five seconds;

however,

the valve took over six seconds.

During this test major steam flashing

and splashing

occurred at the

2-MRV-212 dump valve.

The

dump valve leaked

and caused

water to accumulate

on the MSIV, which consequently

caused

the MSIV to close

beyond the

acceptance

limit.

Only valve 2-MRV-212 appeared

to be leaking;

however,

the inspector determined that

on Unit

1 six of the eight

dump valves

had

leaks but only two had job order tags.

A review of past

MSIV slow stroke

times indicated that leaking

dump valves

was the likely cause.

Inadequate

maintenance

procedures

for the

non safety related

dump valve appeared

to

have resulted

in the poor maintenance

and performance of the MSIVs.

For

more information, refer to

NRC Report Nos. 50-315/90005;

50-316/90005.

2.4.2.3

Past Instrumentation

and Control Maintenance

The inspectors

reviewed past

I&C maintenance activities and procedures

for the

attributes described

in Paragraph

2.4.2.

The

ILC maintenance

philosophy

had

recently

been

expanded

to include

some concepts of RCM.

The inspector also

noted

a program unique only to I&C Department.

Procedure

IMP.347 "Job Order

Trend Evaluation Program",

Revision

0,

1989, provided

a method to identify and

disposition multiple instrument failures over

a period of one,

two, or three

years;

however,

actual

trending of failures was considered

slow.

Of 13

instruments

meeting the multiple failure criteria in May 1989, only 4 Trend

Reports

had been evaluated at the time of the inspection.

The

I&C job order

data

base identified 12 other instruments that met the multiple failure criteria

in October

1989, but no evaluations

had

been

done.

Various technicians

and

support

personnel

throughout the

I&C Department

conducted

evaluations

of Trend

26

Reports which appeared

to be the cause of of slowness

in evaluating trend reports.

A dedicated

engineer

had not been

assigned

to the

18C staff.

The inspectors

determined that

I&C maintenance

was primarily basea

on Tecnnical

Specification requirements

and vendor manual

recommendations.

Selected

vendor

source

documents

were reviewed to determine if requirements

specified were

incorporated into appropriate

maintenance

procedures.

The source

documents

reviewed were:

SS2200-761

Dynalco Corp.

Speed Transmitter,

Model

SS2000

No. 320-1382

Airpax Electronics

Overspeed

Device

GEH-2024A

G.E. Multicontact Auxiliary Relay,

Type HFA51

GEI-28803B

G.E.

Instantaneous

Overcurrent

Relay,

Type PJCllXl

GEH-1753F

G.E.

Time Overcurrent

Relay,

Type

IAC51A

The inspectors verified that vendor recommendations

were adequately

addressed

in appropriate calibration procedures

except that maintenance

on

HFA relays

was "replace

as fail."

PM was not done although the vendor specified contact

cleaning

as

a maintenance

item.

The inspectors

reviewed

12 corrective maintenance

job orders

completed

over the

past year for quality and completeness

of documentation

for work history, failure

analysis

and post-maintenance

testing.

The inspectors

determined that attention

to detail

was weak

on job order documentation,

which is also discussed

in

Section 2.5.

The following concerns

were identified:

"Scope of Work" documentation

for all

12 Job Orders

reviewed was limited

to "Repair as necessary"

or "Repair and recalibrate".

Post-maintenance

testing documentation

was non-specific or

non-descriptive.

Of the

12 Job Orders

reviewed,

5 listed

post-maintenance

tests

as "tested for satisfactory operation."

Cause of Failure

on

4 of the

12 Job Orders

was not documented.

The "Tech Spec Related?"

block on

4 of the

12 Job Orders

was checked

incorrectly.

Recent job orders

reviewed reflected

an increased

management

awareness

about the

importance of job order documentation.

All of the more recent job orders

were

complete,

concise,

and descriptive

and documented

"causes

of failure."

2.4.3

Vendor Manual Control

Control

and validation of vendor technical

manuals

was weak.

A limited number

of vendor manuals

were reviewed to determine

the optimum

PM frequency for

components

essential

to safe

and reliable plant operation.

All new safety

related

vendor manuals

received at the site were sent to the corporate office

for review and approval.

The

new non-safety-related

vendor manuals

were

reviewed

by plant engineers

or maintenance

personnel.

The manuals

were being

27

sent to the corporate office at

a rate of approximately

50 manuals

per month

for review.

Az. znaz raze,

the ieview would not be completed for nine years.

Out of 6800 vendor manuals,

only 893 were reviewed

and approved at the time of

this inspection

including only 629 safety related

manuals.

The licensee

did not

know the exact

number of safety

and non-safety related

manuals.

The quality of

the current vendor manuals

was poor.

For example,

the

ESW pump vendor manual

(VICS 385) contained six pages of handwritten instructions

on

pump disassembly

and removal.

The manual

review sheet

acknowledged

the additional

pages

but

contained

no validation or justification to support the change to the technical

manual.

It appeared

that the additional

pages

were written by a maintenance

technician

based

on experience

in removing the

pump.

This additional information

was very useful,

but not formally controlled to show the source

document

and

the approval

of such information for use in the plant;

The vendor manuals

had

not been

adequately

reviewed

and released

for use

by maintenance

and other

station staff.

There were two controlling procedures

developed to control this

area:

Donald C.

Cook procedure

12

PMP 2030 VICS.001 - "Control of Vendor

Documents",

Revision

2;

and

AEPSC procedure

5.6 - "Vendor Information control

System

(VICS) for the Donald

C.

Cook Nuclear Plant", Revision

1

~

Based

on the findings noted

above,

the inspectors

concluded that systematic

evaluation of the vendor recommendations

and its incorporation into the

PM

process

was weak.

2.4.4

A

lication of NRC Notices

Generic

and Vendor Information Letter s

The inspectors

reviewed select

instances

of important nuclear industry

events with potential applicability to Donald

C.

Cook in the mechanical

area,

to see

how effectively such information was disseminated

and evaluated.

Incoming information was screened

by plant shift technical

advisors

(STAs),

and then routed to appropriate

departments.

The system

proved effective

in July 1988,

when

a steam

leak developed in an extraction

steam line from

a high pressure

turbine at another

Region III utility.

The licensee

examined similar systems

and found appreciable

pipe thinning in an area

thought to have

low probability of erosion failure.

The affected sections

of pipe were replaced

and have

been included in future evaluations

as part

of the erosion/corrosion

program.

The Erosion/Corrosion

Inspection

Program,

outlined in procedure

MHI-5022 provided effective guidance to evaluate

degradations

in pipe wall thickness

in areas

suspected

of high potential

for erosion/corrosion.

The program

has only been in place since October

1989

so results could not be observed.

Although this program only addressed

piping, the concepts

involved provide the beginning of a plant aging program.

Information regarding industry initiatives in the electrical

area

was not

,

always

communicated

to the appropriate

levels of the maintenance

staff.

For example,

plant maintenance

personnel

interviewed by the inspection

team

had

no knowledge of Information Notice Nos. 83-19

and 88-69,

and G.E.

Service Information Letter No. 44, Supplement

4, regarding the type

HFA

relays potential for binding of the moveable contact fingers.

NRC Information Notices

Nos. 83-19,

88-69 and

GE Service Information Letter

No. 44,

Supplement

4, advised all licensee's

of the

need to ensure that

appropriate

plant personnel

were aware of the potential for binding of the

moveable contact fingers of all

HFA relays manufactured

by G.E.

and the

need for periodic verification of the relay wipe and gap settings.

Although

28

these

systems

are not classified

as Class

lE or safety-related, it was

considered

a weakness

that the licensee

has not given appropriate

conside-

ration to the possible

adverse effect on safety.

The licensee

indicated

that

a

PM program was being developed for these relays.

To the best of the

inspector's

knowledge,

none of these

type relays

had failed at Donald C.

Cook.

PM had not been

performed

on non-latching type G.E.

HFA relays in Class

1E

safety related applications,

the licensee'

Failure Data

Base

and various

drawings indicated that G.E

HFA non-latching type relays

were installed in

the emergency diesel

generator

starting air system,

the containment

ice

condenser refrigeration

system,

and the auxiliary feedwater

system initiation

logic.

All molded case circuit breakers

were not inspected,

maintained

and tested

as specified

in

NRC Generic Letter 81-12.

However,

18 month

PM was

performed

on

some safety related

and containment penetration

molded case

circuit breakers

in accordance

with procedure

Ho.

12

MHP 5021.082.017,

which satisfied the criteria of the generic letter.

To the best of the

inspectors

knowledge,

there

have not been

any molded case circuit breaker

failure.

2.5

Maintenance

Work Control

The inspector

reviewed several

maintenance

records

and job orders to evaluate

the effectiveness

of the maintenance

work control process

to assure

that plant

safety, operability,

and reliability were mainta',ned.

Areas evaluated

were

procedures

for planning

and scheduling,

control of maintenance

job orders,

prioritization and scheduling of work, control of backlog,

and post maintenance

testing.

Results follow.

The maintenance

process

begins with identification of the

need to perform

maintenance

and continues

to post maintenance

testing,

review,

and documen-

tation of actions.

Work controls were delineated

in procedure

PMI-2290,

"Job Order," Revision 8, which described

how to complete

a job order form;

however,

formal procedures

did not exist for the remaining processes.

Procedure

PMI-2290 required that all jobs be planned but only general

guidelines

were provided, although

numerous

informal memoranda

were

available for use

by the planners

and schedulers;

the procedure

was

silent about the scheduling

process.

Planners

and schedulers

lacked job descriptions.

Among other tasks,

planners identified the required work procedures,

spare parts,

and post

maintenance

tests;

however,

formal training had not been provided to

either planners

or schedulers

in the respective

processes.

Interviews with planners

and schedulers

indicated that there

was

no

integrated

approach

to work planning,

scheduling,

and coordination in

the maintenance

organization.

Planners utilized an equipment data base, Facility Data

Base

System

(FDBS).

The

FDBS included data

such

as

component

names,

identification numbers,

locations,

manufacturers,

serial

numbers,

reference.-drawings,

applicable

procedures

and technical

specification,

vendor manuals,

parts data,

and

more.

These

data

were controlled and verified by the records

management

29

group;

however,

a formal feedback

system

from field users

was not in place

to assure

continued accuracy of the data,

which were frequently used for

job planning.

Maintenance

personnel

stated that retrieval

time was slow for computerized

data,

the data

base

and history were incomprehensive,

erroneous,

and

ineffective for use in planning activities.

0

Pre-job planning

was done only on major jobs.

Planners

rarely reviewed

previous job orders or researched

similar component failure records to

evaluate

the extent of a problem or for potential

common

mode failure.

This

probably occurred

because

completed job orders

lacked adequate

descriptions

of the problems,

the work done or the possible

cause,

even though

each job

order required the recording of such information.

Usually the job order

had

marked "not applicable" in,the

space

provided for stating the reason for the

work.

Only 2 of 40 job orders

reviewed

by the inspectors

had reasons

stated

for the work.

This weakness

affects planning

and determination of root cause

analysis,

and trending of failures.

This is also discussed

in Section

2.4.2.3.

Results of completed

maintenance activities

such

as problems encountered,

possible

cause of the problem, or actual

man-hours

expended

were not normally

fed back to the planning

and scheduling

departments,

nor to engineering for

needed

adjustments

of the

PM program to preclude

recurrence

of component

failures.

Scheduling

and coordination

had not been established

for CM,

PM, and

survei llance activities

on the

same piece of equipment,

which resulted

in

an increased

amount of equipment

downtime.

For example:

PR-89-195 stated

that the job order

had to be returned

because

design drawings were not

included in the work package;

PR-89-569

documented

the lack of coordination

of activities

on the

same piece of equipment

between construction

and main-

tenance

departments

that resulted

in workers receiving unnecessary

increased

exposure

to radiation;

PR-89-639

documented

that the maintenance

department

submitted

a clearance

to tag out components for maintenance

already completed,

which resulted

in unnecessary

removal of equipment

from service

by operations

and "standing alarms" in the control

room for six days.

Both planning

and scheduling activities were considered

weak.

2.6.

En ineerin

and Technical

Su

ort of Maintenance

2.6.1.

Cor orate

and Site

En ineerin

Engineering

support to plant maintenance

came

from the corporate office and the

plant engineering staff.

Three corporate divisions, nuclear operations,

nuclear

plant engineering,

and electrical

systems,

supported

the plant.

The Nuclear

Engineering Division (NED) consisted

of four sections

including mechanical

and

chemical

engineers.

The Maintenance

Department at the plant had three mechanical

engineers,

one electrical

engineer but no IKC engineer,

and

had to heavily depend

on the plant performance 'engineers

and the corporate office for engineering

support.

30

Maintenance

engineers

were primarily involved in plant modifications

and procedure

revisions applicable to

a specific area of expertise.

Maintenance

engineers

had

job descriptions

that defined responsibilities

which did not include involvment

in routine review of job orders unless specifically requested;

therefore

only

obvious generic

problems would be identified.

2.6.2

S stem

En ineers

The "System Engineer" concept

was relatively new and only three engineers

had

been assigned

system responsibilities.

The average

longevity on the job was

about

two months.

The system engineering

program

was defined in an interface

agreement

between

the corporate office and the plant;

however, plant procedures

had not been

developed

to implement the program.

Draft position descriptions

were developed for the three

grades

of system engineers.

One

system engineer

indicated that

he followed the system's

operation

and was informed of major

events,

but did not receive

any completed job orders for review and evaluation

of equipment failure trends.

2.6.3

Performance

En ineerin

Performance

engineers

evaluated

performance

in the areas of thermogoraphy

and

included vibration analysis for equipment

such

as

pumps,

fans,

and air compressors.

Results of the vibration monitoring were reported

to station

management if

problems occurred;

however,

no trending of the vibration monitoring results

was

performed

on individual equipment.

Thermography

equipment

was purchased

about

a

year ago.

Five persons

were trained in its use;

however,

procedures

have not

been developed for implementing thermography

techniques

including the equipment

on which thermography

could be effectively utilized.

2.6.4

E ui ment Failure Anal si s

The inspectors

evaluated

the reporting of equipment failures to the Nuclear Plant

Reliability Data

System

(NPRDS)

and related

correspondence

which indicated that

reporting of fai lures to the

NPRDS

had

been satisfactory.

The use of NPRDS and other data

and information were reviewed to determi ne if

root causes

of failures and any necessary

corrective actions

were taken.

There

were

no formal programs

in place to address

concerns

associated

with plant aging

although

based

on

NPRDS data

some of the elements

may exist.

The cause

codes

used to identify the reason for component/equipment

failures does

however include

a category labelled "normal wear/aging".

The licensee

also

has

a formal program

established

to trend

and track pipe wall erosion

and corrosion which is described

in Section 2.4.4.

A review of all job orders closed out in the past year both

maintenance

and

IKC, which were attributed to "normal wear/aging" indicated that

many jobs received that cause

code

when the other choices did not fit or when

little or no root cause

investigation

was done.

It seemed

to be used

as

a default

value for

a cause

code

and as

such provided little value in determining the

characteristics

of plant aging at the facility.

Component Failure Analysis Reports

(CFAR) derived from NPRDS data for

Unit

1 and

2 for the 18-month period from December

1987 through

May 1989

were reviewed.

Several

components,

about

10 categories,

had significantly

higher failure rates

than the industry average.

For example,

the failure

31

rate of safety valves

exceeded

the industry average

by a factor of about

4.

Failure categories

were listed as failure to open within acceptable

ranges

or failure to reseat.

There

have

been

39 such failures at Donald

C.

Cook since

March 1986,

and several

valves

have repeatedly failed by

this mechanism.

The cause of failure to reseat

provided in the

NPRDS were

attributed to dirt, wearout,

or unknown causes.

Specific observations

of

safety valves are described

in Section 2.3. 1.

A root cause of these

problems

was not given.

Several

individuals were interviewed to determine

the analyses

conducted

and corrective actions

taken to address

the problem.

The

NPRDS supervisor

stated that the

CFARS were sent to various department

managers

who were

responsible

for taking appropriate corrective action.

The maintenance

department

manager

stated that the'orporate

nuclear engineering

department

was responsible for determining corrective actions,

and stated that

NED had

advised

the plant that the events

were isolated

and

a detailed investigation

of the problem was not necessary.

NED engineers

were interviewed but were

not aware of the

CFARS.

The inspectors

reviewed various

memoranda

about

this subject

between

the plant and corporate office and noted that there

was poor communication

between

the plant and corporate

technical

support;

in January

1987

a superficial investigation of the problem was done

by

engineering;

there

was

no specific analysis of the root cause of the

failures;

and

no corrective actions

were initiated or planned to address

the problem.

The ISI section supervisor

stated that

a preventive mainten-

ance

program for the safety valves did not exist and

had not been established

as

a result of budget

constraints'ased

on the above,

the inspector concluded that response

by the licensee

to this problem was not effective.

A detailed

study was not conducted

to

investigate

an obvious negative

trend and determine

the root cause of the

failures including failure mode

and appropriatness

of application.

During the review of NPRDS data,

CRs,

and

PRs for 1989, the inspectors

noted

that numerous entries identified an adverse

trend concerning installation

and control of fuses.

For example

in April 1989,

PR-470 documented

that 400A

fuses

were installed in batter charger

1AB1+2 and

1CD1+2

DC transfer cabinet

but drawings specified

300A.

In May 1989,

PR 89-406 documented that load was

shed

on bus

T11A and TllB due to inadvertent

removal of fuses during perfor-

mance of maintenance activities, which resulted

in a total loss of the West

RHR pump.

In May 1989,

PR 89-572,

documented that heat trace circuits had

20A fuses installed, while design drawings specified

15A fuses.

In August

1989,

PR-872

documented that fuses installed in Unit 1

CRCD Circuit ¹7 were

40A fuses

instead of the

35A called for by the drawing.

Finally, in December

1989,

PR-89-1342

documented

that fuses installed in HCC 2-AN A compartment

3D were

SA while the drawing specified

10A.

On July 21,

1989,

PR 89-907

was prepared after

a review of PRs by Shift

Technical Advisor personnel

identified numerous

problems with fuses or

breakers.

Four of the

PRs were written between April and July 1989'he

licensee

stated

in

PR 89-907 that "Identification of fuse/breaker

related

Problem Reports within a 22 month period of time created

the perception of

a possible

adverse trend."

PR 89-907 was closed,

but at least

two additional

PRs,89-872

and 89-1392 were written to document the installation of

incorrect fuses'he

inspectors

concluded that the licensee failed to

32

2.7

perform an adequate

root cause

analysis

and therefore did not correct the

cause

of the misapplication

and use of incorrect fuses.

Maintenance

and

Su

ort Personnel

Control

The inspectors

reviewed the licensee's

staffing control

and staffing needs.

Inspection activities included interviews with plant personnel,

training facility

observations,

in plant observations,

and review of documentation.

The licensee's

maintenance

department

had recently

been reorganized

to integrate

the

I&C department with the previous

complement of mechanical

and electrical

personnel

that formed the'lant maintenance

department.

Under the

new organiza-

tion,

I&C and electrical

departments

were combined to form an Instrumentation

and Electrical

( I&E) department,

which consisted of ILC technicians

and

15

electricians,

with 2 supervisors.

Electrical maintenance,

such

as relays

and

switchgear,

was performed

by I&C technicians

rather

than electricians,

as

was

the case prior to the reorganization.

One supervisor

and six electricans

were

scheduled

exclusively to MOVATS testing,

leaving

one supervisor

and remaining

electricans

to perform electrical

maintenance

tasks.

According to the licensee,

the electrical

maintenance

scope will expand to include preventive

and predictive

maintenance

on additional safety related

and

80P componets.

However, the

capability of the electrical

maintenance

staff to implement

such

an expansion

had not been evaluated

by the licensee.

Although maintenance

staffing appeared

adequate

at the time of the inspection, it was not clear that sufficient

resources

would be available in the future.

2.7. 1

Trainin

and

uglification

The inspectors

reviewed maintenance

training programs

in the welding, electrical,

mechanical

and instrumentation

and controls areas.

Detailed lesson

plans

on

several

topics

as well as the training records for maintenance

personnel,

including

a supervisor,

were also reviewed.

The records

adequately

reflected

sufficient training for the tasks that were observed.

Training for planners

and schedulers

was not provided.

Due to the large

number of fluid system leaks, training conducted

in the areas

of torque requirements

and flange

makeup were reviewed.

The lesson

plans

contained sufficient depth

and detail in these

areas.

The mechanical

maintenance

continuing training program also contains specific information about check valve

problems which includes

INPO

SOER 86-03.

The training program provided

an integral part of the qualification system

used

for maintenance

personnel.

Formal training requirements

as well as on-the-job

training evolutions were documented

in an individual's qualifica ion matrix.

In discussions

with a maintenance

supervisor,

the inspector determined that the

qualification matrix was

used to assign

individuals to specific tasks,

but no

requirement

existed to ensure that qualified personnel

were used for all tasks.

In this area, all the necessary

elements

appeared

to be in place

such that

a

plant administrative

procedure

which provided guidance

and direction

on training,

qualification and the assignment

of qualified personnel

to maintenance

tasks

would provide

an effective system.

The established

training program for

maintenance

personnel

was considered

a strength.

33

2.8

2.8.1

MOVATS Testin

Pro

ram

Inspection

Report

No. 50-315/316/89-028

documented

the results of the NRC's

inspection

of the

licensee

'

MOVATS testing results to ensure operability

of critical safety related motor-operated

valves

(MOVs).

The scope of the

testing

was limited to 35 critical safety related valves in each un'rid

some additional

problem safety related

and

non safety related valves.

Testing

was performed

on Unit

1 during the Unit

1

1987 outage,

on Unit 2

during the Unit 2 1988 outage

and

some testing

was performed

on certain

valves in 1989 in accordance

with the procedures

which incorporate

the test

criteria of Bulletin 85-03 .

While the testing

per formed sati si fed the

criteria of Bulletin 85-03, the testing

was limited to a small

sample of

i3Vs.

Of approximately

500

MOVs in each unit, 250 are safety related.

Of

1000

MOVs in both units, the licensee

estimated that approximately

100 have

been tested

using the criteria of Bulletin 85-03.

Prior to 1987, there

was

no test program for MOVs.

MOVs were repaired

on

an

as

needed

basis.

PM No.

12

MHP 5030.012.001,

"Preventive Maintenance

Requirements,"

and the preleminary draft "Motor Operated

Valve Program"

dated June

1988, required that 33<< (42 valves of which 50~ must be

environmentally qualified equipment) of safety related

MOVs have

PM

performed every refueling outage

including inspection

and cleaning of

electrical

components,

checking lubricants,

and the torque switch smooth

operation,

cleaning

and lubricating valve stems,

lubricating upper bearings

and repacking

the valve stuffing box, if required,

and setting torque

switches

and limit switches.

This program

was still in the rough draft

stage

and

had not been formally implemented.

According to the licensee,

evaluation is ongoing of long term

MOV testing

programs at other utilities as well as evaluation of the results of

preleminary testing

performed in accordance

with the criteria of Bulletin 85-03.

Additionally, the licensee

indicated that the formalized long term

program will incorporate

the testing criteria of NRC Generic Letter No.

89-10 and

be expanded

to include all safety related

MOVs.

2.8.2

SOER 86-03 Check Valve Failures

The inspectors

evaluated actions

taken in response

to

SOER 86-03 regarding

check valves failures.

A program was established

on August 30,

1988, to

implement the recommendations

of the

SOER.

There are

440 total check

valves:

10 per unit are

examined

under the

IST program and

an additional

23 are

examined for each refueling outage.

Procedure,

12

THP 5070 ISI.003,

"Disassembly

and Visual Examination of Check Valves per

SOER 86-03 Require-

ments",

Revision

0,

was issued at the time of the inspection.

During the

Unit 1 outage

in 1989,

29 valves were examined for the

SOER 86-03.

Most

of the check valves were found to be in good condition;

however, four

exhibited minor pitting; one indicated erosion/corrosion;

and one with a

centerline split disc

had

a loose spring,

an eroded

stem hinge,

and

a

damaged

rubber seat insert.

All the valves were repaired to operable

condition.

2.9

Review of Licensee's

Assessment

of Maintenance

34

2.9.1

Audits and Surveillance

The inspection

team reviewed

samples of maintenance

related

gA survei llances

and audits.

gA findings were

made

known to managment.

While the technical

content

appeared

to be appropriate,

the

scope of the audits did not address

significant aspects

as follows:

None of the survei llances

under

PMI 5020 "Maintenance Policy" appeared

to

address

various electrical

maintenance

program content

and implementation

deficiencies that were identified by the inspection

team.

Surveillance

Report No.

12-89-134 failed to address

appropriate criteria

for 4KV circuit breaker relay calibration, in that the circuit breaker/fuse

coordination setpoints

as specified in the licensee's

coordination

study

were not verified.

None of the surveillances

under

PMI 6010 "Radiation Protection

and

Monitoring'-'ppeared

to address

approximate

395 piping leaks in the Auxiliary Building

in accordance

with Regulatory

Guides

1.21

and 4.1.

Reg Guides

1.21

and 4.1

require the gA program include measures

to survey possible radiological

exposures.

gA audits of the

PM program were performed in 1987

and

1988 but non'e

was

scheduled

or performed in 1989.

The inspectors

determined that lead

gA auditor qualifications were established

in accordance

with ANSI 45-2. 12 and specified in the licensee's

gualification

and Certification Procedure

No. 2. 1 for quality assurance

personnel.

2'.2

Review of Maintenance Self Assessment

2.9.2.1

Maintenance

Self Assessment

The inspectors

reviewed the report of the licensee's

self assessment

of

maintenance

performed

by corporate

and site personnel

in February

1988,

when

71

findings and recommendations

were identified.

Based

on reviews

and comparisons

with other industry self assessments

of maintenance

and the results of this

inspection

the inspectors

concluded that the licensee's

self assessment

was

performance

based

and effective in identifying maintenance

problems

and

concerns.

However,

gA did not utilize the .report. results to develop checklists

as part of audit plans for verification of corrective action.

At different

times subsequent

to the assessment

in February

1988,

36 of the

71 findings and

recommendations

had

been investigated

and closed;

however,

in December

1989,

19

of the 36 were reopened

because

of inadequate

corrective action.

Many of the

items have

remained

open for two years,

which indicated

poor management effort

to address

the concerns.

Furthermore,

target dates

have not yet been set to

correct the assessment

findings, which was considered

a significant weakness.

During this inspection

a large

number of previously identified weaknesses

were

still evident,

which indicated that corrective actions to address

most of the

deficiencies

was untimely and noncomprehensive.

For example:

(1) scope of the

PM program was minimal and not well defined,

formalized or integrated;

(2)

recurring maintenance

problems

were not trended

and analyzed;

(3) maintenance

history data

were incomplete

and erroneous;

(4) rework was not tracked or

35

analyzed for root cause;

(5) responsibility and authority of each maintenance

group was not delineated;

and (6) various computerized

forms of maintenance

data

lacked coordination.

In July 1987,

the licensee

established

the concept of "Quality Teams"

(QTs), to

give maintenance

workers

and other personnel

an opportunity to identify and

solve maintenance

work related

problems.

As stated

in the

QT Implementation

Plan,

a "vital support function" needed for the success

of the

QT program was

communication

between

the

QTs and management

"to ensure that team generated

solutions

are aggressively

addressed"

.

The inspectors

obtained

a lengthy list

of jobs performed in 1988 and

1989 by maintenance

workers that outlines problems

encounx,crea

and suggested

solutions.

Some

foremen associated

with ihe jobs were

interviewed to get

an assessment

of QT effectiveness.

Many foremen indicated

there

was

a profound lack of management

feedback to

QT suggestions

and

recommended

improvement

based

on field experience.

Most suggestions

received

no response.

One example

requested

an investigation into using qualified flexible conduit for

electrical

connection to the containment

sump

pumps,

which are

removed every

outage

and require

numerous determinations.

The suggestion

affected

wear

on the

cable

ends,

time and consequently

man-rem exposure.

2.9.3

Effectiveness

of Corrective Action

The inspectors

evaluated

the effectiveness

of licensee's

corrective action to

correct deficiencies

noted during

a maintenane

assessment

conducted at Donald C.

Cook by an outside organization

in April 1988.

The inspectors

determined that

many of the corrective actions

taken

have

been

inadequate

in identifying the

cause

and resolving the problem.

For example,

the plant continues

to have

a

problem with a significant number of system leaks.

In addition,

36 of the

71

findings and recommendations

resulting from the February

1988 maintenance

self

assessment

had to be reopened

in December

1989 due to inadequate

corrective

action.

Contributing to this weakness

in corrective action is the lack of a

formal program to direct or implement root cause analysis,

which is addressed

in Procedure

PMI-7030, "Condition Reports

and Plant Reporting."

Problem reports

require

an investigation

and determination of root cause,

but in cases

where

a

problem report is not initiated,

a root cause

analysis will probably not

be done.

As

a positive note,

formal training sessions

were conducted

on root cause

analysis

by

a contractor

and were presented

to 44 plant personnel

in September

1988.

The fact that many of these

problems

remained

uncorrected

at the time of this

inspection reflects

a significant weakness

in the corrective action

system.

While numerous

plans

and proposals exist that address

the eventual

solution to

many of these

concerns,

the long-standing

nature of most of these

problems is

cause for concern.

Failure to take prompt and adequate

corrective action to

identified deficiencies is considered

a violation of 10 CFR 50, Appendix B,

Criterion XVI (50-315/89031-04B;

50-316/89031-04B)

.

3:0

Syyno sis

This synopsis highlights the inspection findings in terms that are meant to be

representative

of the presentation

tree that is attached

to this report.

A (+)

means that the area is good or has potential to be so;

a (-) means that the

area is weak or not fully developed.

Unmarked areas

are factual but were not

a (+) or (-).

36

3.1

Overall Plant Performance

3.1.1

Historic Data

(+)

The forced outage rate

was less

than half the established

goal; there

were

zero safety

system actuations,

the plant manager recently established

a system

to measure

and

manage

maintenance

effectiveness.

(-)

Operating records

since January

1989, indicated that the

number of

unplanned

reactor trips was exceeded

on both units; three of the six reactor

trips appeared

to be maintenance

related;

the

number of LERs was more than

twice the established

goal;

24 of the

54

LERs were attributed to maintenance/

surveillance

problems; unit availability was not met for either unit.

(Unit

1 = 69.3//70/o; Unit 2 = 74.4/>/80%)

3.1.2

Plant Walkdowns

(+)

Equipment

was well identified with color coding around the identification

number

.

(-)

Material condition was poor for a plant in operation:

there were

a

significant number of steam,

water, or oil leaks

from the

AFW and

DG systems,

and

numerous

safety valves;

there

were over 400 catch basins to control leaks

some of which were contaminated;

tagging of deficiencies

was not specifically

required therefore tagging

was inconsistent;

many deficiencies

were not tagged

and

some tagged

items lacked job orders therefore

may never

be repaired;

as-built drawing discrepancies

wer e noted

by the

team and the licensee.

3.2

Mana ement

Su

ort of Maintenance

3.2. 1

Mana ement

Commitment

and Involvement

(+)

The

1988 self assessment

was performance

based

and effective in identifying

maintenance

problems

and concerns.

(-)

Root causes

were not assessed

and corrective action

was not taken to preclude

and correct

several

programmatic

problems identified in 1988 during

a self

assessment

of maintenance

and recurring

problems with 4kV electrical circuit

breakers;

a significantly high number of safety -valve failures, four times the

industry average,

was reported to the corporate

nuclear engineering

department

but

a detailed

study was not conducted to investigate

an obvious negative trend

and determine

the root cause;

there

was

no feedback

from management

to guality

Team suggestions.

3.2.2

Mana ement

Or anization

and Administration

(+)

A RCM pilot program was recently initiated that eventually will be integrated

with the recently initiated

PRA, and ultimately integrated with existing

PM

practices;

system engineers

are utilized to support the project.

(-)

A corporate

manager exists for the plant maintenance

division of fossil plants

but none was established

for the Donald

C.

Cook Nuclear Plant; only limited goals

were established

for maintenance

in 1989

and

none for 1990; maintenance

policies

did not exist for mechanical

and electrical

groups;

the

I&C and electrical-

37

mechanical

maintenance

groups were compartmentalized

instead of being integrated;

the job order prioritization system

was not uniform for all maitnenance

groups.

(-)

The recent reorganization left maintenance

personnel

confused

about authority,

responsibilities,

accountability

and interfacing because

these acti vities were

not formalized nor clearly defined for the various plant groups involved in

maintenance.

(-)

Maintenance

was primarily based

on Technical Specification requirements

and

vendor recommendations;

systematic

evaluation of vendor recommendations

and

incorporation into the

PM process

was weak; only 893 of 6800 vendor manuals

had

been

reviewed.

3.2.3

Technical

Su

ort

(+)

Whole body radiation dose

was considerably

below the industry average

but

station

goals

were not met; radiation protection job coverage

and

ALARA support

for major maintenance activitie were considered

strengths.

(+)

A unique

system,

"dc scout,"

was effectively used to identify the location

of grounds

on dc battery

systems.

(-)

Poor communication existed

between plant and corporate technical

support

staffs;

corporate usually determined corrective actions with minimum plant

engineering

input.

The system engineer

concept

was not fully developed;

implementing procedures

were not established;

vendor manuals

were not reviewed for QC inspection or

PM

requirements;

completed

work requests

were not reviewed for trending or failure

analysis.

(-)

Technical

support

was weak

on corrective action for recurring problems;

engineering

support in the areas

of root cause,

failure analysis,

and post

maintenance

testing

was also weak; engineering

was not involved in resolution

of discrepancies

noted between

sizes

and set points of thermal

overload

installations; efforts were minimal in the areas

of predictive maintenance;

handling of generic industry information from outside

sources

was weak in the

electrical

area

and mixed in the mechanical

area.

Response

to Bulletin 85-03

MOV common

mode failures

was

slow and only met minimum requirements;

only

100 of approximately

1000

MOVs were tested

using criteria from Bulletin 85-03.

(-)

QC "peer inspection"

was considered

ineffective, vague,

and lacking in

guidance or acceptance

criteria.

(At Donald

C.

Cook a "peer inspection"

program

has

been

developed to supplant conventional

QC inspection.)

3.3

Im lementation of Maintenance

3.3. 1

Work Control

(-)

Work histories in the form of documented

work activities

on job orders

was

weak: descriptions of work scope

were typically repair

as necessary,

or repair

and recalibrate;

post maintenance

testing

was neither descriptive

nor specific;

causes

of failure were not included; planning

and determination of trends

and

root causes

was severely

hampered.

Recent job orders indicated considerable

improvement.

38

(-)

Planning

and scheduling

were weak: work planners

and schedulers

lacked job

descriptions

and did not receive specific training in those

processes;

an

inta.'

.;

"'"==.". ';

planning,

scheduling,

and coordination did not exist for

scheduling

and coordination of CM,

PM,

and surveillance

activities which

contributed to increased

equipment

downtime.

Retrieval of computerized

data

used

for planning

was slow and the data were not comprehensive

and

sometimes

erroneous'-)

Planning,

communication,

and advanced

notice of HP was weak for emergency

and unplanned

outage

work.

= Mork was not well coordinated

or planned:

required

tools

and equipment,. were not specified,

and

a high number of workers were

assigned

to radiation producing jobs; frequently work schedules

were not followed

and required radiation resurveys.

All of these

shortcomings

have the potential

to cause

unnecessary

increased

radiation exposure.

(-)

The backlog of non-outage

CM job orders at 1772 was excessive

and more than

twice that planned.

A goal

had not been established

for maintaining

a ratio

between

PM and

CM; the total backlog for 1989 ranged

between

900 and

1200 with

CM at 88K and

PM at 12K.

(-)

Maintenance

procedures

did not include vendor

recommended

maintenance;

procedures

were technically weak and did not adequately

consider

human factors;

for the most part

gC inspection

hold points did not exist.

(-)

In several

instances,

activities were not accomplished

in accordance

with

procedures,

instructions,

or drawings.

As a result the following kinds of

problems

were identified:

equipment

was in indeterminate

status;

thermal

overload heaters

were incorrectly sized or adjusted; field verifications were

done with outdated drawings;

AFW pump vendor requirements

were not included in

maintenance

procedures;

relay contacts

were incorrectly cleaned;

a potential

reactor trip was created

by operations

personnel

not having

a required

procedures;

maintenance

procedures

were not periodically reviewed to assure

that

PM aspects

of components

were updated

based

on results of current

operating conditions.

3.3.2

Plant Maintenance

Or anization

(-)

Mechanical

maintenance

was poor in several

instances

as evidenced

by MSIV

failure to meet acceptance

criteria for closure time; misapplication of bolt

thread sealant;

procedures

lacked safety precautions

and acceptance

criteria

for torque values of cover bolts for a check valve and

AFW pump packing leakoff;

amounts of lubrication used were not documented for various pieces of equipment;

54 filters were missing from an air dryer but

a deviation report was not

prepared;

and the scope of MOV testing

was narrow.

(-)

Electrical maintenance

was poor in several

instances

as evidenced

by:

narrow scope of PM, G.

E.

HFA relays

wer e notably missing from the program;

information regarding industry initiatives was not always

communicated

to

appropriate

levels of the electrical

maintenanace

staff, for example,

informa-

tion about

HFA auxiliary relays;

fuses

were inadequately controlled;

equipment

accuracy

and technique

were inadequate

for the testing of the

under voltage

relays that actuate

the emergency diesel

generator.

(-)

I&C maintenance

was poor in some instances

as evidenced

by:

poor work

techniques

on

BOP equipment,

hand agitation of instruments,

tools beyond

39

calibration

due date,

and improper method

used to calculate

response

time;

evaluations

were not made of instruments with multiple failures.

(-)

Trending of vibration monitoring results

was not performed

on individual

equipment

and procedures

had not been

developed for implementation of thermo-

graphy techniques;

effects of component

aging were not formally analyzed; it

was noted that the cause

code

"normal wear/aging"

was often listed

on job orders

but it was by default and

no apparent

analysis

was done.

3.3.3

Maintenance Facilities

E ui ment and Material Control

(+)

Control of MME was satisfactory,

defective tool were segregated

from those

in calibration.

(-)

Spare parts were

sometimes

unavailable

because

some design

packages

did not

always

make

such

a consideration;

procurement,

parts control

and substitution,

and engineering

involvement in these

processes

was weak;

AFW pump parts

had to

be reused,

and parts for repair of valves were substituted

by maintenance

person-

nel without engineering

review; traceability was not maintained for materials

and

components

used in safety-related

motor control centers.

3.3.4

Personnel

Control

(+)

The established

training program for maintenance

personnel

as considered

a strength;

formal training sessions

were conducted

on root cause analysis

by

a contractor

and were presented

to 44 plant personnel

in September

1988.

(-)

Resources

did not appear sufficient to address

weaknesses

in the technical

support

area that required engineering

expertise,

reduction of the large

number

of parts

on back order,

and establishment

and implementation of an effective

PM

program.

The inspectors

met with licensee

representatives

(denoted

in Paragraph

1) on

January

18,

1990, at the Donald

C.

Cook Power Plant

and summarized

the purpose,

scope,

and findings of the inspection.

The inspectors

discussed

the likely

informational content of the inspection report with regard to documents

or

processes

reviewed

by the inspectors

during the, inspection.

The licensee did

not identify any such documents

or processes

as proprietary.

40

AC

AEPSC

AFW

ALARA

BOP

CM

CR

GRID

DC

ECCS

EDG

EPRI

ESF

FDBS

FLA

FSAR

GE

GE SIL

HP

HVAC

IKC

IEB

IEN

INPO

ISI/IST

JO

K

KV

LER

MCC

MOV

MB(TE

NPRDS

NRC

NUMARC

OOS

PAG

PM

PMT

PR

PRA

QA

QC

RCA

RCM

RFC

RWP

SALP

SOER

SSFI

TS

UV

V

'PPENDIX A

Alternating Current

American Electrical

Power Service

Company

Aux'.liary Feedwater

System

As

Low As Reasonably

Achievable

Balance of Plant

Corrective Maintenance

Condition Report

Control

Room Instrument Distribution

Director Current

Emergency

Core Cooling System

Emergency Diesel Generator

Electrical

Power Research Institute

Engineered

Safety

Feature

Facility Data

Base

Full Load Amps

Final Safety Analysis Report

General Electric

General Electric Service Information Letter

Health Physics

Heating, Ventilation and Air Conditioning

Instrument

and Control

IE Bulletin

IE Notice

Institute for Nuclear

Power Operations

Inservice Inspection/Inservice

Testing

Job Order

Kilo

Kilo Volt

Licensee

Event Reports

Motor Control Center

Motor Operated

Valve

Measuring

and Test Equipment

Nuclear

Power Reliability Data System

Nuclear Regulatory

Commission

Nuclear Utility Management

and

Human Resource

Committee

Out of Service

Plant Assessment

Group

Preventive

Maintenance

Post Maintenance

Testing

Problem Report

Probabilistic Risk Assessment

Quality Assurance

Quality Control

Root Cause Analysis

Reliability Centered

Maintenance

Request for Change

Radiation

Work Permit

Systematic

Assessment

of Licensee

Performance

Significant Operating

Experience

Report

Safety

System Functional

Inspection

Technical Specification

Undervoltage

Volt

I

~ ~

wT laX5