ML17312B129

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Insp Repts 50-528/96-16,50-529/96-16 & 50-530/96-16 on 961006-1116.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML17312B129
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 12/05/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312B127 List:
References
50-528-96-16, 50-529-96-16, 50-530-96-16, NUDOCS 9612110028
Download: ML17312B129 (30)


See also: IR 05000528/1996016

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

'ocket

Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By;

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/96-1 6

50-529/96-1 6

50-530/96-1 6

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

October 6 through November 16, 1996

K. Johnston,

Senior Resident Inspector

J. Kramer, Resident Inspector

D, Garcia, Resident Inspector

D, Carter, Resident Inspector

Dennis F. Kirsch, Chief, Reactor Projects Branch F

ATTACHMENT: Supplemental

Information

'P612f i0028 961205

PDR

ADQCK 05000528

G

PDR

~ ~

l

I

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report 50-528/96-16; 50-529/96-16; 50-530/96-16

~Oerations

~

A loss of the operating instrument air (IA) compressor occurred in Unit 1, while it

was in Mode 6, as a result of an incomplete review of work by the work control

senior reactor operator (SRO).

Operations personnel

responded

appropriately to the

event; however, operations

personnel

exhibited weakness

in attention to detail in

that the shift supervisor did not ensure that the event was properly documented

in

control room logbooks or the corrective action programs (Section 01.1).

~

Refueling personnel demonstrated

good communications

and a formal

safety-conscience

approach when performing refueling operations.

The refueling

senior reactor operator (LSRO) directing the core load during its latter stages

used

improved monitoring equipment

and handling techniques.

Operations showed good

judgement in stopping upper guide structure (UGS) installation operations when

LPSI flow indications could not be verified (Section 01.2).

~

The Unit 1 operations midloop team did not ensure proper completion of all

prerequisites

prior to initiating the drain down of the reactor coolant system

(RCS)

to reduced inventory. After it was identified that the lineup was incorrect, auxiliary

operators

(AOs) (initial positioner and verifier) reperforming the valve lineup failed to

identify an incorrectly positioned valve.

This is a violation of requirements to follow

procedures.

Both of these issues are repeat events from previous violations of the

same procedure.

The resolution of the draining discrepancies

by the operators

and

subsequent

management

response

was very good (Section 04.1).

Maintenance

~

Maintenance work observed was well performed.

Technicians were experienced

and knowledgeable of their assigned tasks and demonstrated

good communications

between work groups.

Additionally, maintenance

personnel exhibited strong

knowledge of the reactor vessel multistud tensioner and stud insertion process

(Section M1.1).

~En ineerin

~

Licensee Event Report (LER) 528/95007, Revision 1, was incomplete in that it did

not address

significant aspects of problems with letdown isolation valves which

individually could not have isolated full RCS pressure,

Additionally, the initial LER

and first revision did not fully address the safety implications of the as-found

condition of these valves (Section E8.3).

~

An unresolved

item was identified concerning the degraded

flexible covers for the

reactor coolant pump lubrication oil collection system (Section F2.1).

e

~ 4

Re ort Details

Summar

of Plant Status

Unit 1 began this inspection period defueled.

On October 29, following completion of a

39 day refueling outage, the unit commenced

a reactor startup and power ascension.

On

November 6, the unit reduced power from 90 to 25 percent to repair a steam leak

downstream of a main turbine control valve.

Following the repair, the unit returned to

100 percent power and remained there for the duration of the inspection period.

Units 2 and 3 operated at essentially 100 percent power for the duration of the inspection

period.

I. 0 erations

01

Conduct of Operations

01.1

Loss of IA Com ressor

B Unit 1

ao

Ins ection Sco

e 71707

The inspector observed operations'esponse

to the loss of IA Compressor

B, a

nonsafety related component,

which resulted from a unexpected

power loss during

a maintenance

activity. The inspector discussed

the event with the shift supervisor,

operations director, unit department

leader, and electrical maintenance

department

leader.

b.

Observations

and Findin s

On September 29, electrical maintenance

technicians obtained approval from the

work control senior reactor operator (SRO) to perform work on the 480 volt Circuit

Breaker NHNM0219 using Work Order (WO) 770890.

The electrical maintenance

technicians de-energized

Circuit Breaker NHNM0219, which removed power to

Distribution Panel NHN-D02. One load supplied by Distribution Panel NHN-D02 was

control power for IA Compressor

B. IA Compressor

B was in operation with IA

Compressors

A and C in standby.

After control power was removed, IA

Compressor

B tripped and IA Compressor A and C both started.

IA Compressor A

subsequently

tripped on low oil pressure.

An AO responded to the area and

restarted

IA Compressor A.

The inspector, who was in the control room at the time the event occurred,

observed that control room personnel took appropriate actions to restore an

IA compressor to service.

The event did not have a significant impact on the plant,

which was in Mode 6 at the time.

The shift supervisor briefed the entire operations crew and the site shift manager on

the initial lessons

learned from the event.

The shift supervisor stated that the work

control SRO failed to perform a proper review of WO 770890, by not evaluating

-2-

electrical prints to determine which loads would be affected by de-energizing

Circuit

Breaker NHNM0219.

On October 3, the inspector noted that the event had not been documented

in

either the unit or the control room logbooks and it had been not documented

in the

licensee's corrective action program in that a condition report/disposition request

(CRDR) had not been initiated.

The inspector discussed

concerns that the details of

the event had not been documented

in the control room logbooks or captured by

the corrective action program with the unit department

leader.

The unit department

leader did state that he had been independently tracking this issue; however, he

agreed that the shift supervisor should have ensured it was adequately

addressed

without his involvement.

The inspector noted that once the inspector identified concerns were brought to the

attention of management they were appropriately addressed.

C.

Conclusions

A loss of the operating IA compressor occurred as a result of an incomplete review

of work by the work control SRO.

Operations personnel

responded

appropriately to

the event; however, operations

personnel exhibited weakness

in attention to detail

in that the shift supervisor did not ensure that the event was properly documented

in control room logbooks or the corrective action program.

01.2

Fuel Movement UGS Installation

Unit 1

Ins ection Sco

e 71707 and 60710

The inspector observed refueling operations

and the installation of the UGS using

the following procedures:

78OP-9FX01, Refueling Machine Operations

40OP-9PC02,

Section 9.0, Filling and Draining the Refueling Pool Using the

CS, LPSI and HPSI Pumps

40OP-9ZZ12, Mode 6 Operations

31MT-9RC33, Reactor Vessel UGS Removal and Installation

b.

Observations

and Findin s

On October 16, 1996, the inspector observed

Unit 1 refueling operations.

The

LSRO directed all fuel transfers from the refueling bridge.

Allfuel movement was

coordinated with the control room and logged in accordance

with

-3-

Procedure 72IC-9RX03, "Core Reloading."

Good communications were observed

between the LSRO, the fuel pool bridge crane operator,

and the control room.

The inspector observed the latter portions of the fuel load.

It was during this stage

in fuel loading during the 1995 Unit 1 refueling outage that a fuel assembly was not

properly positioned on the core support plate.

The licensee attributed this, in part,

to weaknesses

in their fighting and ability to use video cameras

as the vessel was

filled. The inspector observed that, during this core load, the licensee had

implemented corrective actions which enabled them to,more closely monitor the

latter portion of core load.

Additionally, the LSRO used proper techniques to verify

the last fuel assemblies

were properly set.

The inspector observed proper radiological protection practices while the camera

cabling was removed from the refueling pool and proper foreign material control

inventory practices.

The inspector also observed

good use of safety harnesses

for

personnel frequenting the refueling cavity and while walking across the bridge

crane.

On October 17, the inspector observed the lifting, transfer, and insertion of the UGS

into the reactor vessel.

The licensee demonstrated

good communications

and

oversight in the movement of the UGS.

Radiation protection personnel continuously

monitored and kept operators informed of dose rates in manned areas,

The

licensee's

use of remote underwater cameras greatly aided the alignment and

insertion of the UGS into the reactor vessel.

After the UGS was lowered into the vessel the inspector observed the licensee

unlatch all the control element assembly self-latching mechanisms

in preparation for

lowering the control element assembly support plate.

During this time, the control

room was lining up the LPSI system to lower refueling pool water level.

The control

room informed the LSRO of LPSI flow problems and UGS installation was halted.

Control room personnel

concluded

LPSI flow detector SIN-Fl-300 was not providing

reliable information.

The licensee corrected the flow indication problem prior to

resuming the UGS installation.

The inspector determined this action to be

appropriate.

Conclusions

Refueling personnel demonstrated

good communications

and a formal

safety-conscience

approach when performing refueling operations.

The LSRO

directing the core load during its latter stages

used improved monitoring equipment

and handling techniques.

Operations showed good judgement in stopping UGS

installation operations when LPSI flow indications could not be verified.

-4

04

Operator Knowledge and Performance

04.1

RCS Reduced Inventor

and Midloo

0 erations

Unit 1

a.

Ins ection Sco

e 71707

On October 20, 1996, in the process of reducing the RCS level for midloop

operations,

operators identified that their drain path was not properly established.

In addition, during a subsequent

valve lineup walkdown, AOs failed to identify that

a valve, required to be open, was locked closed.

The inspector reviewed the

licensee's

response

to these problems,

b.

Observations

and Findin s

Missed Prere

uisite for Drain Ali nment

On October 20, 1996, shortly after they initiated draining the RCS, the operations

midloop team did not receive the expected

level change for the refueling water

tank (RWT) and identified an unexpected

level change

in the holdup tank (HUT).

The midloop team subsequently

identified that Appendix Q of

Procedure 400P-9ZZ16, "RCS Drain Operations," did not reflect current plant

configuration in that three valves were not in their correct lineup to align the drain

path to the RWT.

The licensee investigation determined that the following sequence

of events

contributed to the valve lineup problem.

On October 17, following core reload, the

oncoming control room night shift continued the drain of the refueling cavity to the

RWT, an activity that was initiated on day shift. Concurrent with cavity drain

operation, the crew lowered the reactor vessel level approximately 2 inches in

accordance with Procedure 40OP-9ZZ16, "RCS Drain Operations."

Operators

had

changed the drain path, documented

in Appendix Q to the procedure, to drain the

RCS to HUT. Subsequently,

the operators misplaced the paperwork for the revised

Appendix Q lineup, and, therefore, the revised lineup did not replace

a previously

existing Appendix Q lineup, which showed the drain path established to the RWT.

The operators completed both drain evolutions at approximately 11:30 pm.

The licensee determined that during the draining evolutions on October 17, the

midloop control room supervisor

(CRS) was preparing for the upcoming drain to

midloop and was not directly involved with the crew's activities.

However, the

midloop CRS was peripherally aware that the crew had performed

a drain of the

RCS to the RWT. The next day, the midloop team was temporarily disbanded

due

to outage delays that affected the midloop schedule.

On October 19, the midloop team reconvened

for night shift and prepared to drain

the RCS to reduced inventory condition by draining the RCS to the RWT. The

midloop team did not reperform Appendix Q because they were confident that they

-5-

had an established

drain path to the RWT based

on the completed Appendix Q

demonstrating

a drain path to the RWT and the midloop CRS's previous

understanding

of draining operations to the RWT on October 17.

The team

subsequently

performed

a drain of the RCS in preparation to enter a reduced

inventory condition.

After draining approximately

1 ft of level from the RCS, the

midloop CRS identified that there was a slight level increase

in the HUT rather than

the RWT. The midloop team halted further drain operations until an investigation

was completed,

k'he

licensee's investigation determined that the midloop CRS failed to ensure the

drain path was aligned in accordance

with Appendix Q prior to draining the RCS.

The inspector concluded that the failure of the CRS to perform the prerequisites was

a violation for failure to follow Procedure 40OP-9ZZ16.

The inspector noted that the midloop CRS did not ensure completion of Appendix Q

and relied on communications that were overheard when reviewing paperwork.

The

inspector determined that this event was similar to a midloop event on

November 28, 1994, where the CRS relied on discussions

between the control

room staff and assumed that makeup flow path alignments had been performed.

This event was identified as a failure to follow procedure violation in NRC Inspection

Report 50-530/94038.

The inspector concluded that it was reasonable

to expect

that the corrective actions taken following the November 1994 event should have

prevented the October 1996 event.

Inade

uate Valve Positionin

and Verification

After the midloop team initially halted the RCS drain on October 20, the midloop

CRS dispatched two AOs to perform and independently verify the Appendix Q valve

alignment.

The AOs identified two open valves that Appendix Q required to be

closed and, subsequently,

closed the valves.

These actions isolated the drain path

to the HUT. However, the AOs did not identify that locked closed

Valve CHN-V495, which established

a drain path to the RWT, was required to be

open.

The midloop crew recognized that diverting letdown water from the volume control

tank would provide a performance verification of the drain path alignment without

reducing RCS level. The crew initiated a divert and noted that the drain path was

still not properly aligned.

The midloop CRS informed the AOs of the problem and

directed them to recheck the Appendix Q valve lineup.

The AOs subsequently

identified that Valve CHN-V495 was locked closed and opened the valve to align

the drain path.

The failure of the AOs to place Valve CHN-V495 in the open

position is the second example of the failure to follow Procedure 40OP-9ZZ16.

The inspector noted that on October 17, 1995, Unit 3 operations

personnel

attempted to lower the RCS level by draining to the RWT. Operators were unable to

drain the RCS and, subsequently,

discovered that Valve CHN-V495 was closed.

-6-

The licensee had identified that AOs failed to initially position and independently

verify the position of Valve CHN-V495. This event was documented

as a noncited

procedure violation in NRC Inspection Report 50-528,529,530/95018.

The

inspector concluded that it was reasonable

to expect that the corrective actions for

the October 1995 event should have prevented this October 1996 event.

The two failures of the operations staff to follow procedure

is a violation of

Technical Specification (TS) 6.8.1 (50-528/96016-01).

Problem Resolution

After the midloop team identified Valve CHN-V495 had been mispositioned, they

suspended

the performance of the reduced inventory preparations to reperform all

drain down prerequisites

and evaluate the events.

The licensee subsequently

recommenced

the drain down evolution and completed the midloop operations

without incident. 'In addition, the licensee initiated CRDRs and human performance

evaluations to assess

personnel performance issues.

The inspector found that the midloop teams had been prompt in identifying that the

lineup had not been properly established.

In addition, once the initial walkdown

was completed, the midloop team's actions to test the lineup demonstrated

conservative action.

The licensee's evaluation of the event was questioning

and

thorough.

C.

Conclusions

-The midloop team did not ensure proper completion of all prerequisites

prior to

initiating the drain down of the RCS to reduced inventory.

After it was identified

that the lineup was incorrect, AOs (initial positioner and verifier) reperforming the

valve lineup failed to identify an incorrectly positioned valve.

Both of these issues

are repeat events from previous violations of the same procedure.

The resolution of

the draining discrepancies

by the operators

and subsequent

management

response

was very good.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

Violation 50-529 96005-01:

failure of a reactor o erator to follow a

rocedure

in reali nin

ower sources

and

Closed

LER 50-529 96002:

ina

ro riate work

ractice results in an en ineered safet

feature actuation of the

Train B emer

enc

diesel

enerator.

This event was discussed

in Inspection Report 50-528,529,530/96-05.

The

inspector verified the corrective actions described

in the licensee's

response

letter,

dated May 22, 1996, to be reasonable

and complete.

In addition, no new issues

were revealed

in the LER.

-7-

08.2

Closed

Violation 50-530 95025-02:

failure to follow the prescribed operability

evaluation.

This violation concerned

an incident where an operability detern ination

had not been performed by operations

personnel when credit for manual actions

were taken to compensate

for a degraded

condition found on the Unit 3 Essential

Chiller 8 as determined

by engineering

personnel.

The inspector verified the corrective actions described

in the licensee's

response

letter dated March 25, 1996, to be reasonable

and complete.

II. Maintenance

NI1

Conduct of Maintenance

M1,1

General Comments

on Maintenance Activities

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

e

WO 752667:

replace gasket on 1B Emergency

Diesel Generator

B fuel oil

discharge filter (Unit 1)

~

WO 770205:

replace manifold on Emergency Diesel Generator

B (Unit 1)

~

WO 771959:

evaluate/test

reactor coolant pump rotorbars (Unit 3)

~

31MT-9RC30: reactor vessel head removal and installation (Unit 1)

b.

Observations

and Findin s

The inspectors found the work performed under these activities to be professional

and thorough.

All work observed was performed with the work package present

and in active use.

Technicians were experienced

and knowledgeable

of their

assigned tasks and demonstrated

good communications

between work groups.

The

inspector concluded that maintenance

personnel

exhibited strong knowledge of the

reactor vessel multistud tensioner and stud insertion process.

M1.2

General Comments on Surveillance

Activities

a.

Ins ection Sco

e 61726

The inspectors observed

all or portions of the following surveillance activities:

~

33ST-9HJ01:

control room air handling unit airflow capacity and

pressurization test (Unit 1)

-8-

~

739T-9AF02:

auxiliary feedwater pump A inservice test (Unit 2)

The inspectors found these surveillances were performed acceptably and as

specified by applicable procedures.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Leakin

Bod -to-Bonnet Seal on Shutdown Coolin

Isolation Valve SIB-652

Unit 1

a.

Ins ection Sco

e 62707

During restart activities in Unit 1, the licensee discovered that shutdown cooling

isolation Valve SIB-652, the first of two isolation valves for the RCS, had a leaking

body-to-bonnet

seal.

In response to the licensee's

decision to not repair the valve

prior to restart, the inspector reviewed the basis for this decision and reviewed

work performed on the valve during the outage.

Two conference

calls were held

with the licensee involving the NRC's Region IV office and the NRR projects,

manager.

b.

Observations

and findin s

During the refueling outage, the licensee installed modifications to Valves SIB-652

and SIA-651 to provide pressure relief in these double wedge gate valve bonnets to

prevent the development of pressure

locking under design basis accident conditions.

To accomplish this modification, the licensee had to disassemble

the valves and

subsequently

replace the body-to-bonnet

seal during valve reassembly.

The seal

installed was prepared with a surface of silver, which was designed to improve

valve sealing.

The modification was done with the core off loaded and the

shutdown cooling loops drained.

During the subsequent

flood up, the licensee

observed that the seal leaked.

They concluded that the leakage was not

unexpected

since, in their experience,

the valve seals tended to seal better as RCS

pressure

increased.

However, in Mode', with the RCS at normal operating temperature

and pressure,

the valve was found to leak at approximately 0.08 gallons per minute (gpm).

Maintenance

engineering

evaluated

and allowed mechanics to increase

body-to-bonnet

bolt torque.

This activity did not decrease

the leakrate.

Maintenance

engineering

also allowed mechanics to use the manual handwheel

on

the actuator to apply additional seating pressure to establish

a better seal at the

upstream valve seat.

They stipulated that the seating pressure

be relieved to the

original seating force.

This activity reduced the body-to-bonnet

leak to around 0.03

gpm.

-9-

Licensee engineering

subsequently

performed an evaluation which concluded that

this amount of leakage was acceptable for the duration of the operating cycle.

The

licensee evaluated;

The susceptibility to corrosion of valve components

exposed to the boric

acid environment.

The I(censee found that under the environmental

conditions, the valve components,

which were mostly stainless steel with a

few carbon steel components,

would not be subject to significant corrosion.

The exposure of the system piping to thermal stratification.

They determined

that existing evaluations remained valid as long as the leak remained below

0.1 gpm.

The ability to monitor the teak.

They installed a video camera to allow

control room operators to monitor the general condition of the leak.

In

addition, they planned to enter containment twice per week to measure

system leakage and assess

valve condition.

The licensee constructed

a stainless steel drip catch with a hose draining through a

floor drain to the containment sump. At the end of the inspection period, the

licensee was evaluating additional actions that could reduce leakage,

After roughly

'two weeks at full power, the leak rate had decreased

slightly.

The inspector reviewed the licensee's evaluation of continued operations with the

leak and found that it adequately

addressed

the technical issues of boric acid and

thermal stratification exposure.

Additionally, the evaluations to support the

activities performed to reduce the leak were appropriately reviewed.

The inspector

found that the installed drip catch was well constructed

and performed as designed.

The licensee's monitoring activities to date have demonstrated

concern for changes

in leak rate.

C.

Conclusion

The licensee has performed adequate

actions to address

a leaking body-to-bonnet

seal in a reactor coolant pressure

boundary valve.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

Closed

Violation 529 95010-01:

use of an uncalibrated boronometer.

LER 529/94008, submitted on February 7, 1995, identified that Unit 2 operators

had used an uncalibrated boronometer to comply with the compensatory

action

requirements of TS 3.1.2.7, which applied when a startup channel was out of

service.

The inspector reviewed the LER and the associated

CRDRs and found

weaknesses

in the evaluation of the cause of this event and with the corrective

actions.

Inspection Report 50-529/95010 included a Notice of Violation (NOV) for

failure to use a properly calibrated instrument to meet TS requirements.

Although

-10-

licensee identified, the violation was cited because the licensee had not

implemented adequate

corrective actions.

The licensee responded

to the NOV in a letter dated July 27, 1995.

They stated

that corrective actions would be implemented to:

Revise procedures for controlling preventive maintenance

and preventive

maintenance

activities to require notification of the shift supervisor when a

preventive maintenance

task is waived.

Revise procedures to require notification of the shift technical advisor or

other appropriate

engineering

personnel when out-of-tolerance results are

found during surveillance testing.

Require the shift technical advisor or appropriate engineer to perform a

documented

evaluation of the significance of the problem or deficiency and

ensure that when appropriate

a corrective action document

is generated.

Issue a night order to all three units outlining the actions to be taken if the

boronometer

is not available, including initiating a "control room discrepancy

log" entry to make the status of the boronometer obvious to control room

personnel.

Review the event in the operator training.

The inspector reviewed the corrective actions described

in the licensee's

response

and found them to appropriately address the cause of the violation.

In particular,

the corrective actions to highlight deficiencies with an operations impact to

operators

addressed

the cause of this event.

The inspector noted that operators

have done a more thorough job of highlighting deficiencies with controlled

temporary notes and control room discrepancy

log entries.

M8.2

Closed

LER 50-529 95006:

failure to perform TS surveillance

requirement 4.5.2.e.4, inspection of all emergency core cooling systems outside

containment

and verify total leakage

is less than

1 gpm.

The inspectors

documented

the event and initial licensee response

in NRC Inspection Report 50-

528,529,530/95-14.

The licensee initiated an investigation to identify the cause

and corrective actions

for the event.

The licensee noted that sections of the surveillance were performed

in two midcycle outages

and documented

as full performance

on the surveillance

test package review sheets

(STPRS) although the test log clearly indicated only

partial performance.

The licensee identified that the cause of the event included

both procedure

and personnel

weaknesses.

-1 1-

The licensee revised the STPRS forms and provided training to operations

and

maintenance

personnel,

on the revised form, in industry events training.

In

October 1995, the test program users group performed

a human factors review of

the revised STPRS form, concluded that the STPRS form was less than adequate,

and identified further enhancements

to the form.

In February 1996, the licensee

performed an assessment

of the effectiveness of the corrective actions similar to

the initial investigation and concluded that the corrective actions were effective.

The failure to perform the surveillance requirement is a violation of the TS.

The

inspector reviewed condition report/disposition request

(CRDR) 2-5-0252 and found

the licensee's investigation to be thorough and their corrective actions to be

thorough.

This licensee-identified

issue is being treated as a noncited violation

consistent with Section Vll of the NRC Enforcement Polic

(50-529/96016-02).

III. En ineerin

E8

Miscellaneous Engineering Issues (92903)

E8.1

Closed

LER 50-529 95001;

TS 3.0.3 entry until TS limiting condition for

operation

(LCO) 3.4.9 Action B was met by isolating the Charging Pump A, On

April 12, 1995, Unit 3 was in Mode

1 operating at approximately 100 percent

power when an AO identified a leak through

a cracked weld in the piping system

near the Charging Pump A suction drain valve.

Control Room personnel

entered

TS

LCO 3.0.3 following a determination that Action B for TS LCO 3.4.9 could not be

met.

Within nine minutes, operations isolated the Charging Pump A which

established

compliance with TS LCO 3.4.9 Action B, and exited TS LCO 3.0.3.

The licensee determined that this was an isolated failure which had resulted from a

defective weld, most likely from original fabrication," They concluded that the failure

was accelerated

because

of material fatigue as a result of the vibration of the

charging pump suction line. The licensee performed walkdowns of the remaining

charging pumps in Units 1, 2, and 3 and did not identify any additional material

nonconformance

or leakage.

On April 18, 1995 the Unit 3 Charging Pump A was

repaired and returned to service.

The inspector found the licensee's

response

to

this event to be appropriate.

E8.2

Closed

Violation 50-528 95025-03:

failure to leak test the essential chiller

system.

This violation addressed

the licensee's failure to establish testing required

to demonstrate that the essential chilled water system could perform satisfactorily

in that they had not identified and performed tests incorporating the requirements

and acceptance

limits for the allowable system leakage.

-1 2-

The inspector reviewed the licensee's response'to

the violation dated March 25,

1996.

The licensee discussed

the following corrective actions:

~

Engineering revised the calculation which established

the maximum allowed

system leakage.

These changes

were reflected in the associated

design

basis manual.

~

Operator rounds were revised to provide leakage measurements

and the

results were to be reviewed by engineering.

~

Maintenance

personnel were briefed on the importance of observed

leaks on

the chiller and the chilled water pump.

In addition, the licensee stated in the NOV response that they had established

a

June 30, 1996, schedule for completion of the design basis project for the heating,

ventilation, and air conditioning systems.

The inspector reviewed the licensee's

planned coriective actions and determined

that they addressed

the weaknesses

identified. The inspector reviewed revisions to

the calculation for acceptable

leak rate and the procedure to test for leakage and

found that they established

a reasonable

leak rate and an acceptable

method to test

for this leakage.

The inspector noted that the CRDR also included actions to have

maintenance

perform weekly checks of the essential chiller pumps for leakage and

found this action to be prudent.

E8.3

0 en

LER 50-528 95007

Revision 1: adverse affect of low bench set on Fisher

air o crated letdown containment isolation valves

Observations

and Findin s

In September

1994, as documented

in NRC Inspection Report

50-528;529;530/94031,

the inspector noted that Unit 1 Valve CHB-515, the

.

letdown to regenerative

heat exchanger isolation valve, had a caution tag indicating

that the valve leaked at a rate of 41 gpm when closed at normal operating pressure

and could not be used to isolate the letdown line. Although this condition had

existed since late 1992, the inspector identified that the licensee had not performed

an adequate

review of the deficiency and had missed an opportunity to fix the valve

during a 1993 refueling outage.

Subsequently,

the licensee performed an

operability determination and concluded that, in its existing condition, the valve

could perform its design functions.

The inspector subsequently

identified that the

valve was required to close as part of the licensee's control room fire mitigation

strategy and initiated Unresolved Item 528/9431-01.

The licensee took

compensatory

actions to provide additional fire mitigation strategies,

reperformed

the operability determination and determined that the valve could perform its design

functions.

This action was documented

in LER 528/94009, issued on March 2,

1995.

The licensee submitted

LER 528/95007 (dated June 9, 1995) and

-13-

LER 528/95007, Revision

1 (dated April 6, 1996), to document that a design

deficiency had contributed to the problems with Valve CHB-515, that this was

applicable to downstream letdown line containment isolation Valves CHA-516 and

CHB-523, and that it had impacted

a number of design basis functions of these

valves.

The inspector reviewed LER 528/95007, Revision 1, and associated

evaluations

and calculations.

The three letdown isolation valves are air to open, spring to close, 2-inch globe

valves.

The seating force of the spring, established

during a bench set, should be a

function of the spring force necessary to close the valve against system pressure

and friction forces and the air pressure

available for the air operator.

The licensee

identified, in LER 95007, Revision 1, that the letdown valve operators were

undersized for their application and that this was attributed to the absence

of a

detailed design basis for these air operated valves.

Valve service engineering determined that in order to close under design basis

conditions, the letdown isolation valves required

a bench set of at least 38 pounds

per square inch gage (psig).

The valves, as originally procured and installed, were

provided a bench set of between 22 and 38 psig,

The licensee determined that the

Nuclear Steam Supply System vendor had procured the valves and had not

established

an adequate

design basis for the air operated valves.

The licensee

initiated the following corrective actions:

~

Evaluations were performed for all air-operated valves of a similar design.

Valve services engineering

calculated appropriate

bench set requirements for

each of the valves and determined that all these valves had been set

appropriately.

~

The air operators for all of the letdown isolation valves were replaced during

the past round of refueling outages.

~

Valve services engineering

established

an air-operated valve program to

establish air operator valve setpoint, diagnostic testing, maintenance,

and

testing programs.

The licensee planned to implement this program for

air-operated valves in priority systems.

The inspector noted that in addition to having procured undersized

valve operators,

licensee as-found test results on all nine letdown isolation valves were below the

22 psig originally specified as the minimum for the valves.

The as-found bench sets

for the valves were between 10 and 20.6 psig.

The as-found results were not

addressed

in either LER 50-528/94009 or LER 50-528/95007,

Revision 1.

In

addition, the licensee had not evaluated this problem in any of the CRDRs

associated

with this issue.

The inspector discussed

this issue with maintenance

personnel.

They determined

that the set point changes

probably were the result of not ensuring that the valve

-14-

stroke length was maintained when the actuator and valve stem were recoupled

following maintenance

activities.

Routine activities which would have required

decoupling the valve stem from the actuator included valve repacking and actuator

diaphragm replacement.

They also determined that vendor instructions should have

been adequate to ensure that valves were properly reassembled.

Independent

of

this issue, the licensee's

air operated valve program has been improved to ensure

that these valves are properly set up and that design bench sets are maintained.

Conse

uences of Leakin

Letdown Isolation Valve:

In LER 528/95007, Revision 1, the licensee determined that the following design

basis functions were impacted by low letdown isolation valves bench sets:

~

The containment isolation function of Valves CHA-516 and CHB-523

~

The mitigation of a letdown line break outside containment (functions of

Valves CHB-515 and CHA-516) as described

in the Updated Final Safety

Analysis Report (UFSAR) Chapter 15

The isolation of a high energy line break of the letdown line break in the

auxiliary building (function of Valves CHB-515 and CHA-516)

1

The isolation of the letdown line for reactor coolant inventory control for

10 CFR Part 50, Appendix R, fire scenarios

(all three valves)

~

The isolation of letdown upon the receipt of a safety injection actuation

signal (Valves CHB-515 and CHA-516).

LER 528/95007, Revision 1, documented

the analysis performed by the licensee to

determine the impact of having a bench set as low as 22 psig on each of these

functions.

The analysis concluded that there would be adequate

isolation for all

scenarios

as long as two letdown isolation valves close.

Additionally, for the,

letdown line break scenarios

in which only one valve could be credited, the licensee

determined that offsite dose, auxiliary building environment,

and loss of RCS

inventory would be increased,

but within design basis limits.

The inspector noted that the evaluation in LER 528/95007, Revision 1, did not

consider the as-found valve bench sets which would have resulted in greater

leakage in the case where only one valve was available to close.

However, portions

of this evaluation were performed in Calculations 13-MA-CH-954 13-NC-ZY-249.

As discussed

in the LER, the letdown valves, with a minimum bench set of 22 psi,

would have to be closed with a differential pressure

across the valve of 1878 psi,

which would be achieved 27 minutes into the event.

According to

Calculation 13-MA-CH-954, the lowest as-found valve would not have fully closed

until the differential pressure

across the valve was 1120 psi approximately 85

minutes into the event.

The LER indicated that the resultant thyroid dose at the

-15-

exclusionary boundary would be 7.2 rem, while Calculation 13-NC-ZY-249 found

the dose to be 21.45 rem.

The LER also stated that only one valve could have been assumed to close for some

fires outside the control room.

Although the LER described compensatory

measures

that were put into place until the air-operated

valves could be replaced, it did not

describe the consequences

of having only one valve closed.

After questioned

by the inspector concerning the as-found data, the licensee

performed an evaluation to determine the impact of the as-found bench sets on their

ability to achieve safe shutdown.

The licensee informed the inspector that they

determined that they could have achieved safe shutdown with the as-found bench

sets despite calculated valve leakage.

In response to these findings, the licensee proposed to submit a second revision to

LER 528/95007.

This item willremain open pending review of the revised LER.

b.

Conclusions

LER 528/95007, Revision 1,,was incomplete in that it did not address significant

aspects of problems with letdown isolation valves which individually could not have

isolated full RCS pressure.

Additionally, the initial LER and the first revision did not

fully address the safety implications of the as-found condition of these valves.

EBA

Closed

Violation 50-530 95025-01:

failure to identify significant changes

in chiller

refrigerant as a condition adverse to quality. This violation involved maintenance

personnel correcting a deficiency in essential chiller refrigerant levels identified by

the inspector without documenting the problem as required by the corrective action

program.

The licensee missed opportunities for determining the potential impact on

system performance

and operability.

The inspector verified the corrective actions described

in the licensee's

response

letter dated, March 25, 1996.

The inspector reviewed the evaluation response to

CRDR 9-6-0135 that was initiated to addresses

the weaknesses

identified by the

NRC, and found it acceptable.

In addition to a self-assessment

that was performed

by engineering

personnel, the licensee contracted

an independent

assessment

to

compare their chiller performance

issues to current industry standards.

The

inspector determined that the licensee took appropriate actions to address the

violation.

E8.5

Closed

Ins ection Followu

Item 50-530 96012-02:

departure from nucleate

boiling ratio (DNBR) uncertainties,

This item was opened pending the licensee's

completion of corrective actions concerning core operating limit supervisory system

addressable

constant change

and reportability of the DNBR uncertainty issue.

-16-

The nuclear fuels director issued

a memorandum to all nuclear fuels management

personnel emphasizing management's

expectations that all changes

require an

independent

review and section leader review prior to implementation.

In addition,

the licensee discussed

their expectations with all nuclear fuels management

personnel.

On October 18, Combustion Engineering issued 10 CFR Part 21

notification alerting the industry of the potential nonconservatism

in the DNBR limits

previously identified by the licensee.

E8.6

Closed

Followu

Item 50-528 95016-02:

history of ground fault relay failures.

This followup item concerned

a history of failures of General Electric ground fault

relays (GFRs) in safety and nonsafety related 480 volt motor control center

breakers.

The licensee had evaluated

GFR failures in a CRDR written in 1994.

In

Inspection Report 50-528,529,530/95016,

the inspector identified the following

concerns

regarding the licensee's

actions in response to the failures:

An analysis of the failure rates for these GFRs had not been performed.

The licensee had developed

a schedule for the replacement of GFRs which, if

they failed, could place the plants in a TS action statement.

However, the

licensee had not applied risk insights nor enlisted significant operation and

engineering support in assessing

what additional GFRs needed to be

replaced.

At the time of the inspection, none of the GFRs had been replaced according

to the schedule that was established to close the 1994 CRDR.

The licensee initiated CRDR 9-5-1021 to address the inspector's concerns.

The

licensee concluded

in their evaluation of the CRDR that the frequency of GFR

failures matched the vendor's expected failure rate.

Additionally, the licensee found

, that there was no trend to the GFR failure rate.

Based on this analyses, the licensee

determined that a root cause of failure evaluation, which would have been difficult

for this solid state device,'as not warranted.

The licensee did assess

the additional contribution of the GFR failure data on

probabilistic risk assessment

conclusions.

For purposes of the evaluation, the

licensee established that a contribution to core damage frequency of greater than

10'ere candidates for replacement,

The inspector noted that in the past year the

licensee has improved the failure data collection process

and questioned

whether

this may have had an impact on any failure rate calculations,

The inspector

reviewed the failure data for GFRs over the past year and found that the failure rate

was consistent with previous data.

The inspector reviewed work history over the past year and determined that, as of

November, 1996, the licensee had replaced

61 of 66 GFRs in safety-related

applications.

Additionally, the licensee had established

a plan to replace the General

Electric GFRs in nonsafety-related

breakers which could initiate a plant transient.

-17-

The inspector determined that the licensee had taken adequate

actions in response

to this issue.

IV. Plant Su

ort

F2

Status of Fire Protection Facilities and Equipment

F2.1

Reactor Coolant Pum

RCP

Lubrication Oil Collection S stem

Unit 1

a.

Ins ection Sco

e 71750

On October 25, the inspector performed a walkdown of the Unit 1 RCP oil collection

system and reviewed the licensee's commitment to comply with Section III.O of

Appendix R to 10 CFR Part 50.

b.

Observations

and Findin s

The inspector observed that the Unit 1 RCP oil collection system contained the

required oil collection devices as indicated in the UFSAR. The system contained

one welded high pressure

pipe connection on each RCP that did not have a

protection device around it; however, the licensee was not required to have the

welded connection protected.

During the walkdown with the system engineer, the inspector noted that the

condition of the flexible covers (silicon treated glass cloth shields) for the RCP oil lift

system were tom and improperly secured.

The licensee initiated a work request to evaluate and repair the flexible covers on all

four RCPs,

The licensee subsequently

replaced two of the covers, repaired the

remaining two covers, and ensured

all the Unit 1 covers were properly fastened.

In

addition, the licensee performed 31FT-9RC01

"RCP Lubrication Oil Collection

System Inspection," to reverify the status of the complete oil collection system prior

to entering Mode 4.

On October 21, four days prior to the inspector's walkdowns, maintenance

personnel

had performed 31FT-9RC01

as a prerequisite for mode change.

The

procedure included an inspection of the covers and maintenance

personnel,

performing this inspection, concluded that the covers were in good condition and

properly installed.

The licensee initiated CRDR 9-6-1247 to evaluate the flexible cover deficiencies.

The licensee planned to evaluate whether the flexible cover condition existed during

the initial performance of 31FT-9RC01 and why they were determined acceptable,

to develop

a basis for acceptability for future performance of 31FT-9RC01, and to

assess

human performance

and procedural adequacy.

In addition, the licensee

-18-

planned to evaluate the transportability of the as-found condition of flexible covers

to Units 2 and 3.

The inspector will review the licensee's

evaluation, conclusions,

and corrective

actions during'

future inspection (Unresolved Item 528/96016-03).

F8

Miscellaneous Fire Protection Issues

F8,1

RCP Lubrication Oil Collection S stern

Unit 1

a.

Ins ection Sco

e 71750

The inspector performed

a walkdown of the RCP oil collection system and reviewed

the applicable sections of the design basis manual for the fire protection system

pertaining to RCP oil collection.

'b.

Observations

and Findin s

The inspector noted that each of the two tanks in the oil collection system is

capable of holding 110 percent of the lubrication oil from two RCPs.

The inspector

noted that the tanks were equipped with a local gage glass level indication and

were not equipped with a remote level indication or level alarm.

During the walkdown, the inspector identified a potential condition where the RCP

lubrication oil collection system tanks would not be capable of collecting and

holding the lubrication oil from two RCPs.

It appeared that if nuclear cooling water

supplied to the RCP developed

a leak it could be captured by the oil collection

system, fillthe collection tank, and, therefore, not provide the necessary

capacity

for the collection of RCP oil. The inspector noted that there was a flange

connection

in the nuclear cooling water line within the area of the RCP oil collection

system.

Since the tank level has no alarm capability and level can only be checked

from inside containment,

a loss in collection tank capacity could go undetected.

The licensee initiated a CRDR to evaluate the inspector's concern.

The inspector

will review the licensee's evaluation and conclusions during a future inspection

(Inspection Followup Item 528/96016-04).

V. Mana ement IVleetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the conclusion of the inspection on November 13, 1996.

The licensee

acknowledged

the findings presented.

-1 9-

The inspectors

asked the licensee whether any material examined during the

inspection should be considered

proprietary.

No proprietary information was

identified.

e

SUPPLEMENTAL INFORMATION

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Flood, Department Leader, System Engineering

R. Fullmer, Director, Nuclear Assurance

J. Hesser, Director, Design Engineering

W. Ide, Vice President,

Engineering

D. Kanitz, Engineer, Nuclear Regulatory Affairs

A. Krainik, Department Leader, Nuclear Regulatory Affairs

D. Mauldin, Director, Maintenance

R. Myrick, Department Leader, Mechanical Maintenance

G. Overbeck, Vice President,

Nuclear Operations

F. Riedel, Department Leader, Operations

C. Seaman,

Director, Emergency Services

M. Shee, Director, Radiation Protection

D. Smith, Director, Operations

J. Taylor, Department Leader, Operations

M. Windsor, Section Leader, Mechanical Maintenance

Engineering

C. Zell, Department Leader, Operations

INSPECTION PROCEDURES USED

71707

60710

92901

62707

61726

92902

92903

71750

Plant Operations

Refueling Activities

Followup- Plant Operations

Maintenance Observations

Surveillance Observations

Followup-Maintenance

Followup-Engineering

Plant Support Activities

II

(

1

(

I

ITEMS OPENED

CLOSED AND DISCUSSED

~Oen ed

50-528/9601 6-01

VIO

failure to follow RCS drain down procedure

line up

requirements

50-528/96016-03

URI

degraded

RCP oil collection system

50-528/9601 6-04

IFI

potential for nonsafety-related

nuclear cooling water to leak

into RCP oil collection system

Closed

50-529/96005-01

VIO

failure of a reactor operator to follow a procedure

in

realigning power sources

50-529/96002

LER

inappropriate work practice results in an engineered

safety

feature actuation of the Train B emergency diesel generator

50-530/95025-02

VIO

529/95010-01

VIO

50-529/95001

LER

failure to follow the prescribed operability evaluation

use of an uncalibrated boronometer.

TS 3.0.3 entry until TS LCO 3.4.9 Action B was met by

isolating the A charging pump.

50-528/95025-03

VIO

failure to leak test the essential chiller system

50-530/95025-01

VIO

50-528/9501 6-02

IFI

50-530/9601 2-02

IFI

failure to identify significant changes

in chiller refrigerant as

a condition adverse to quality

history of GFR failures

DNBR uncertainties

50-529/95006

LER

failure to perform TS surveillance requirement 4.5.2.e.4

50-529/96016-02

NCV

failure to perform TS surveillance requirement 4.5.2.e 4

Discussed

50-528/95007

LER

adverse affect of low bench set on Fisher air operated

letdown/containment

isolation valves

(

4

~ ~

LIST OF ACRONYMS USED

AO

CRDR

CRS

DNBR

GFR

gpm

HPSI

HUT

IA

LCO

LER

LPSI

LSRO

NOV

pslg

RCP

RCS

RWT

SRO

STPRS

TS

UFSAR

UGS

WO

auxiliary operator

condition report/disposition request

control room supervisor

departure from nucleate boiling ratio

ground fault relay

gallons per minute

high pressure safety injection

holdup tank

instrument air

limiting condition for operation

licensee event report

low pressure safety injection

refueling senior reactor operator

Notice of Violation

pound per square inch gage

reactor coolant pump

reactor coolant system

refueling water tank

senior reactor operator

surveillance test package review sheets

Technical Specifications

Updated Final Safety Analysis Report

upper guide structure

work order

1

E

qr

vl

I