ML17311B130

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Insp Repts 50-528/95-14,50-529/95-14 & 50-530/95-14 on 950702-0813.Violations Noted.Major Areas Inspected:Onsite Response to Plant Events,Operational Safety,Maint & Surveillance Activities & Onsite Engineering
ML17311B130
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 08/24/1995
From: Huey F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311B128 List:
References
50-528-95-14, 50-529-95-14, 50-530-95-14, NUDOCS 9509010070
Download: ML17311B130 (42)


See also: IR 05000528/1995014

Text

ENCLOSURE 2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/95-14

50-529/95-14

50-530/95-14

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating Station,

Units 1, 2,

and

3

Inspection At:

Maricopa County,

AZ

Inspection

Conducted:

July

2 through August

13,

1995

Inspectors:

K. Johnston,

Senior Resident

Inspector

0. Garcia,

Resident

Inspector

A. MacDougall,

Resident

Inspector

J.

Kramer, Resident

Inspector

Approved:

Huey,

cting

C ie

,

eactor

ProJects

B

0 te

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of 'onsite

response

to plant events,

operational

safety,

maintenance

and surveillance

activities, onsite engineering,

plant support activities,

and followup items.

Results

Units

1

2

and

3

~0e rat i one

During the period, operations

performance

weaknesses

of varying significance

were observed.

These

issues,

identified below,

appear contrary to the

improvement noted in operations

performance

since the

end of 1994.

~

Operator

performance

weaknesses

during

an electrical

bus realignment

contributed to

a Unit 2 reactor trip (Section

2. 1).

9509010070

950828

PDR

ADOCK 05000528

PDR

Operator

performance

weaknesses

resulted

in two Unit

1 auxiliary

feedwater

system trains being simultaneously

inoperable for over five

hours

(Section 2.5).

Operators failed to properly evaluate

and resolve

an observed

estimated

critical rod position discrepancy prior to continuing with a reactor

startup.

The

NRC inspector later determined that the discrepancy

was

the result of a calculational error (Section 3.4).

~

Operators failed to properly evaluate

and correct the cause of a control

room annunciator until questioned

by the

NRC inspector

(Section

3. 1).

Maintenance

Surveillance

~

Maintenance

personnel

responded

appropriately to

an inspector identified

loose motor operated

valve motor end cap bolt, performing

a thorough

inspection

and evaluation

(Section 4.2).

En ine'erin

and Technical

Su

ort

System engineers

and plant operators

responded

appropriately to

a

containment

spray waterhammer

in Unit 2, performing thorough evaluation

and testing to determine

the cause of the problem (Section 6. I).

lant

Su

ort

~

Licensee

radwaste

personnel

used

undersized

rigging, which had

been

improperly stored

and inspected,

to lift a loaded radioactive resin

container,

resulting in failure of the rigging and dropping of the

container.

The licensee

had identified previous

weaknesses

in the

control

and

use of rigging equipment

by radwaste

workers,

however,

subsequent

corrective actions

were inadequate

(Section 2.2).

Mana ement

Involvement

and Oversi ht

~

Management

Response

Team evaluation of the cause of a feedwater control

system problem, following a Unit 2 reactor trip, was flawed

and too

quickly settled

on

an incorrect failure mechanism

(Section

2. 1).

~

The decision

making process for performing

an equalizing

charge

on newly

installed Unit 2 vital batteries,

in response

to observed specific

gravity variations,

did not appear

to have received

appropriate

management

attention

and review (Section 3.3).

Summar

of Ins ection Findin s:

~

One violation was identified involving the failure to follow rigging

procedures

used in the handling of radioactive

waste

(Section 2.2).

,$

r

I

(

j

One unresolved

item was identified concerning

the removal

from service

of two trains of auxiliary feedwater

(Section 2.5).

~

One

open item was identified concerning vital battery specific gravity

variations

(Section 3.3).

~

Two violations were closed

(Sections

7. 1

and 8. 1),

~

Two Licensee

Event Reports

were closed

(Section 9).

Attachments:

1.

Persons

Contacted

and Exit Meeting

2.

List of Acronyms

(I

l

I

DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 started

and

ended

the inspection period at essentially

100 percent

power with no significant events

1.2

Unit 2

Unit 2 began

the inspection period at

100 percent

power.

On July 17, the unit

experienced

a reactor trip on low steam generator

(SG) level

(Section

2. 1).

On July 18, the unit commenced

a startup

and subsequently

increased

power to

100 percent.

The unit operated

throughout the remainder of the inspection

period at essentially

100 percent

power.

1.3

Unit 3

Unit 3 operated

throughout the inspection period at essentially

100 percent

power with no significant events.

2. 1

Reactor Tri

- Unit 2

On July 17, the unit tripped from 100 percent

power due to low SG level,

The

low SG level occurred after power was momentarily lost to the feedwater

control

system

(FWCS)

and the main feedwater

pumps ran back to minimum speed.

Prior to the reactor trip, the licensee

was performing scheduled

maintenance

on the normal

power supply to NAN-S05 (13.8

Kv nonclass

switchgear),

which

required operators

to energize

NAN-S05 from its alternate

source.

The control

room

(CR) operator

attempted

to transfer

NAN-S05 to its alternate

source

using

CR switches

which closed the alternate

supply breaker

and opened

the normal

supply breaker.

Although the transfer properly occurred,

the breaker

indications in the

CR did not change (e.g.,

the normal

supply breaker

indicated closed

and the alternate

breaker indicated

open),

and the operator

concluded that the breakers

had not changed position.

An auxiliary operator

(AO) was dispatched

to investigate

the problem.

Since

the

CR operator believed that the alternate

supply breaker

was

open

and could

close unexpectedly,

creating

a potential safety problem for the responding

AO,

he placed the alternate

supply breaker switch back into the

open position.

This caused

the alternate

supply breaker,

which was closed

and supplying

bus

power, to open, resulting in a loss of power to the

FWCS.

Prior to plant restart,

the reactor trip was reviewed

by

a management

response

team

(MRT).

The

NRT concluded that the loss of power to the

FWCS had resulted

i

I

i'

Il f

'

f

0

from failure of the system to fast transfer to its alternate

power source.

When the problem could not

be reproduced

during troubleshooting,

a

FWCS.

control circuit card

was determined

to be the most likely component to have

failed,

and

was replaced.

Subsequent

to the plant restart,

further licensee

review identified that the

FWCS fast transfer

had actually responded

as

designed,

but apparently

was not fast

enough to preclude the observed

transient.

Licensee

management

concluded that the

MRT had

been too quick to

conclude that the

FWCS fast transfer

had not performed

as designed

when, in

fact, the root problem appeared

to involve

a design deficiency.

The licensee initiated

an incident investigation

team to review the unit trip.

The licensee

determined that two plant hardware

issues

contributed to the

event.

They determined that the design of the

FWCS power supply should

be

modified to ensure

a bumpless transfer to

a backup source.

Additionally,

prior to the event,

the plant multiplexer had failed in

a configuration that

froze the switchyard breaker indications without the

CR operator's

knowledge.

The licensee

also identified operator

performance

weaknesses.

When the

operator

noted that the breaker indication did not match the switch position,

there

was other control

board indication available that would have indicated

that the transfer

had taken place.

Additionally, when attempting to restore

the breaker

alignment to its initial configuration,

the operator did not

operate

switches

in the appropriate

sequence

to ensure

a make-before-break

transfer.

The inspector

agreed with licensee

concerns

regarding

equipment

performance,

CR personnel

performance,

and the

MRT evaluation.

The inspector will follow

the licensee

corrective actions

as part of the Licensee

Event Report

(LER)

review.

2.2

Radioactive

Waste Container

Dro

ed

Unit 3

On July 21, while lifting a high integrity container

(HIC) loaded with spent

resin,

the rigging failed, allowing the

HIC to drop approximately

7 feet onto

the ground.

The HIC's highest contact

dose rates

were

70 Rem/hr

on the side

and

100 Rem/hr

on top.

The HIC was designed

and tested to survive

a 30-foot

drop with a full load,

and remained intact

and apparently

undamaged.

The

licensee

took appropriate

actions following the event to complete the

transfer.

Additionally, the licensee initiated

an incident investigation to

review the event.

The licensee

determined that inappropriate rigging practices

were the primary

cause of the event.

Additionally, the inspector

noted

examples of procedural

noncompliance,

ineffective oversight

by both radiation protection supervision

and nuclear

assurance,

a lack of awareness

and sensitivity to previous rigging

concerns,

and questions

concerning rigging qualifications

and training.

,

I

0

2.2.1

HIC Transfer

The HIC was initially moved from a high level storage

area to a transfer

shield

on

a trailer in the radwaste truck bay.

After the trailer was

relocated

to the radwaste yard,

the

HIC was to be moved from the transfer

shield

on the trailer into a storage

shield in the radwaste yard.

The first movement

was performed successfully.

A remote grappling device

was

used

as the primary method of rigging.

In preparation for the

second

movement,

the remote grappling device malfunctioned

and

a decision

was

made

by

radiation protection

management

to use

an alternate

rigging method.

The

alternate

rigging method involved use of a nylon sling that

had

been

attached

to the

HIC in 1993.

The nylon sling was inspected

by the rigger and

used to lift the HIC.

During

the transfer,

the nylon sling failed and the

HIC dropped

approximately

7 feet

onto the asphalt

in the upright position.

2.2.2

Rigging Inspection

The licensee

subsequently

determined that the load rating of the nylon sling

was less

than the load of the HIC.

The nylon sling had

been attached

by the

licensee

to wire ropes installed

on the

HIC at the request of the burial site.

The burial site planned to use the nylon sling only to attach

the wire ropes

to

a crane

hook.

The licensee

had not intended or designed

the sling to lift

the HIC.

The licensee

determined that the rigger had not verified the load capacity of

the nylon sling.

In fact,

a cloth tag

on the sling which provided the load

rating of the sling was illegible, apparently

due to age

and exposure.

Plant

Procedure

30DP-9HPII, "Field Use of Rigging," Step 3.5.3.2 required that the

rigging equipment

have

a capacity that exceeded

the weight of the load.

The

nylon sling was rated for 3800 lbs maximum load.

The gross weight of the

HIC

was

5615 lbs.

In addition,

the licensee's

rigging program required that rigging equipment

be

inspected yearly and that

a color code tag indicating the year of inspection

be attached

to nylon slings'he

involved nylon sling had not received

an

annual

inspection

nor was it color coded.

However, the rigging program also

allowed field inspection of rigging which had not received

an annual

inspection.

The rigger for the

HIC lift stated that

he

had performed

an

inspection to comply with this requirement prior to the lift.

However,

the

licensee

determined that the rigger had not performed this inspection

properly,

in that

he

had failed to inspect the entire sling.

The inspector

subsequently

determined that the rigger had not received

the training

necessary

to perform the inspection,

and

had not documented

the inspection

prior to using the sling.

'

'

The failure to use

a nylon sling rated for the lift and the failure to perform

an adequate

inspection

were failures to follow procedures

required

by

Technical Specifications

(Violation 530/9514-01).

2.2.3

Previous

Rigging Concerns

The inspector

reviewed

a sample of Nuclear Assurance

Evaluation

Reports

and

condition report/disposition

requests

(CRDR) that were written within the past

year concerning rigging.

The inspector

noted several

examples of rigging

concerns

that were identified, evaluated

and corrected.

As documented

in

ER 95-0556,

Nuclear Assurance

Plant Support identified that

rigging used for a filter change

out in Unit 2 was not in compliance with

Plant Procedure

30DP-9MP11,

"Field Use of Rigging."

The annual

inspection

documentation

did not exist nor was the rigging equipment properly color

coded.

Corrective actions

included the performance of an annual

inspection

with documentation for the rigging equipment

used for filter change

outs in

all units.

As documented

in ER-95-0050,

Nuclear Assurance

Plant Support identified that

the annual

inspection of the rigging equipment

used for fuel receipt in Unit 2

had not been properly performed.

One of the corrective actions to

CRDR 920683

included daily and documented

annual

inspection of rigging equipment.

A

decision

was

made to wait until fuel receipt activities were complete prior to

implementing the

new procedure

requirement.

The inspector

found that these

problems

were similar in nature to the problems

that resulted

in the drop of the

HIC and that it would be reasonable

to expect

that corrective actions for these

problems

should

have prevented

the rigging

failure.

However, it appeared

that the corrective actions did not adequately

communicate

the significance of the use of deficient rigging material,

particularly nylon slings which had not been properly stored or inspected.

2.2.4

Management

Oversight

A prejob briefing was performed for the

HIC transfer with representatives

from

operations,

radiation protection,

security

and Nuclear Assurance

present.

In

addition,

both the radiation protection supervisor

and

a member of Nuclear

Assurance

were present

at the work site prior to the lift, yet neither

questioned

the adequacy

of the inspection of the nylon sling.

The inspector

noted that this did not meet licensee

management

expectations.

2.2.5

qualifications

and Training

The inspector

reviewed the training records for the rigger and the crane

operator

and found that both were qualified.

The HIC transfer

was considered

a "High Hazard Lift" by the rigging procedure.

As corrective action for

previous rigging issues,

the licensee developed'raining

for "Heavy and High

Hazard Rigging" with the expectation that, after September

1995, all high

hazard liFts would be performed

by riggers

who had received

the training.

ii

Although the rigger was qualified for all lifts in 1990,

he had not received

the

new enhanced

"Heavy and High Hazard Rigging" training.

2.2.6

Corrective Actions

The inspector

reviewed the findings of the incident investigation

and found

the review to be thorough

and self critical.

The investigation indicated

significant management

concern

and involvement.

The incident investigation

team initiated the following immediate corrective actions:

~

A news flash was issued to all site personnel

describing

the event

and subsequent

interim corrective actions.

In addition,

the'essons

learned

from the event

were discussed

in safety meetings

with employees.

~

Only personnel

who had completed

the classroom portion of the

"Heavy and High Hazard Rigging" training were allowed to perform

lifts greater

than

6000 pounds or "High Hazard Lifts".

Riggers

were required to read

and fully understand;

Procedures

30DP-9MPll, Revision

1, "Field Use of Rigging";

and

30AC-OMP13, Revision 4,

"PVNGS Rigging Control."

The inspector

found these

actions to be appropriate.

However,

the inspector

observed

that

some riggers did not appear to have

'a clear understanding

of

rigging requirements.

On August

1, the inspector

observed

a radiation

protection technician

challenge

the qualifications of mechanical

maintenance

technicians

who were proceeding

to the location of a lift they had

been 'tasked

to perform.

The technicians

were unsure if they were qualified to perform the

task

and were

asked to verify their qualification.

After discussions

with

their supervisor, it was determined that they were qualified to perform the

task.

The inspector

concluded that the radiation protection technician's

questioning

was

a positive step for ensuring

proper rigging.

However, the inspecto'r

concluded that the riggers

should

have

been

knowledgeable

of their

qualifications before preceding

to the job site, especially

in light of recent

rigging issues.

In response

to this concern,

maintenance

management

took

further action to communicate

expectations

to riggers.

2.3

Offsite Volta e Dro

to Less

Than

524

Kv

On July 29, the offsite power grid dropped

below 524

Kv for approximately

10

seconds

when

a 30 MVar capacitor

bank north of Phoenix shorted to ground.

Voltage

on site,

normally controlled at approximately

530 Kv, dropped to

a low

of 523.6

Kv.

The licensee

considers

that both offsite sources

are inoperable

if switchyard voltage is below 524 Kv.

The three

Palo Verde units experienced

load swings in response

to the transient.

After the initial voltage drop, the

l

grid voltage raised

to

a high of 537.7

Kv and stabilized within 6 minutes at

532 Kv.

The system dispatcher for Arizona Public Service did not identify that system

voltage

had dropped

below the minimum of 524

Kv until

a review of alarms

was

performed several

hours after the system

had recovered stability.

The system

dispatcher notified the Unit

1

CR.

The Unit

1 shift supervisor

(SS) declared

that Technical Specification (TS) 3.0.3

was entered for the brief period

when

grid voltage

was below 524 Kv.

The licensee

planned to submit

an

LER on the

issue.

The inspector will review the

LER in a future report.

2.4

Both Trains of Low Pressure

Safet

In 'ection Briefl

Ino erable

Unit

1

On July,

27, Unit

1 operators

entered

TS 3.0.3 for seven

minutes

when both low

pressure

safety injection (LPSI) trains were declared

inoperable.

The

licensee

had

been in

a Train

8 outage for the emergency diesel

generator.

During the Train

B outage,

operators

elected to perform

a surveillance test

(ST)

on the Train

B high pressure

safety injection (HPSI)

pump.

During the

test,

a closed

HPSI injection valve leaked

and pressurized

the cold leg

1A

safety injection header,

which is also fed by Train

A LPSI.

The licensee

had

determined that the

LPSI injection valves

may become

pressure

bound

and fail

closed if downstream

pressure

exceeds

1635 psig.

This determination

was

reflected

in the annunciator

response

procedures

for the safety injection

header

pressure

alarms.

The annunciator

response

procedure

required operators

to depressurize

the header

by opening

a drain path to the reactor drain tank.

This was performed

and the train was declared

operable.

The licensee

planned to submit

an

LER for the event.

The inspector will

review the licensee's

evaluation of the cause of the event

as well

as

corrective actions during

a future inspection.

2.5

Two Trains of AFW Ino erable - Unit

1

On August 9, Unit

1 operators

inadvertently

removed

two AFW trains from

service without entering

the appropriate

TS action statement.

At 6 a.m.,

night shift operators

removed the Train

A Spray

Pond

(SP)

from service for

scheduled

maintenance.

This required that the Train A essential

chiller (EC),

cooled

by the

SP through the essential

cooling water system,

be declared

inoperable.

The Train A

EC provided

room cooling to several vital systems,

including the Train

A turbine driven

AFW pump.

According to procedures

for

the cascading

of TS requirements,

operators

declared

the Train A AFW pump

inoperable

and logged entry of action

(a) of TS 3.7. 1.2, which allowed the

pump to be out of service for a maximum of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

At 9: 15 a.m.,

day shift operators

removed the Train

N AFW pump,

a motor driven

pump powered

by the Train

A emergency

diesel

generator,

from service to

perform

a minor modification on the motor breaker.

Operators failed to

recognize that the Train

A AFW pump was inoperable,

and logged that action (a)

of TS 3.7. 1.2 .was entered.

Operators

should

have

been

knowledgeable of the

Train A AFW pump inoperability and recognized that removing the Train

N AFW

li'

-10-

pump placed

the unit into TS 3.7. 1.2, action (b), which required operators

to

restore

one

pump or be in hot standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

The licen'see

completed

work on the Train

A SP

and racked the

pump motor

breaker into position

by 3:00 p.m.,

making the Train

A SP available.

However,

a functional test for the Train A SP

pump breaker

was not performed

on Train A

SP until 3:23 p.m.

Operators

did not discover that both trains

were

inoperable until the night shift had returned

and maintenance

personnel

informed them that the Train

N AFW pump could

be returned to service.

The licensee initiated

an event investigation,

which was underway at the

end

of the inspection period.

At the

end of the inspection period,

the licensee

had determined that the out of service time for two trains of AFW was

between

9: 15 a.m.

and

3 p.m.,

a period of 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />,

45 minutes.

The licensee

preliminarily concluded that since the

TS action requirement to shutdown

within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

had not been

exceeded,

an

LER was not required.

The inspector

did not consider

the Train

A AFW pump to be operable until 3:23 p.m.,

and

considered

this to be

an unresolved

item (URI), pending review of the

licensee's

formal evaluation of the event

(URI 528/9514-02).

2.6

Hissed Surveillance for Emer enc

Core Coolin

S stem

Leaka

e

Unit 2

On July 13, during preparation for an internal audit of TS, the licensee

noted

that emergency

core cooling system

(ECCS)

TS surveillance

requirement

3/4.5.2.e.4

was not performed within the prescribed

18 month periodicity.

The

surveillance

required

an inspection of all

ECCS piping outside of containment

which is in contact with the. recirculation

sump,

and verify that total

measured

leakage is less

than

1 gpm.

The licensee

developed

a temporary

procedure to perform the system leak test in Node one,

performed the

procedure,

and verified acceptable

leakage within the

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> allowed

by

TS 4.0.3.

The licensee initiated

a

CRDR and

an investigation

team to evaluate

the cause

of the event.

The inspector

noted

a good response

by licensee

personnel

to

verify acceptable

leakage

upon discovery of the missed surveillance.

The

inspector will review the licensee's

corrective actions

as part of the

LER

review.

3 OPERATIONAL SAFETY VERIFICATION

(71707)

3. 1

Fuel Buildin

Hi

h Tem erature

Annunciator - Unit 3

On July 11, while performing

a

CR walkdown, the inspector

noted that the "Fuel

Building HVAC SYS TRBL" annunciator

window was illuminated.

The annunciator

identified that the normal

exhaust

plenum temperature

was high.

The inspector

questioned

the control

room supervisor

(CRS),

who stated that this particular

annunciator

often

came in as

a result of high outside temperatures.

The

temperature

sensor for this annunciator

was located

under

a sheet

metal duct

on top of the fuel building roof.

The inspector

asked

the

CRS if the actual

room temperature

of the fuel

building had reached

the high alarm setpoint of 99

F.

The

CRS did not know,

but was confident that there were

no further actions required

by operators

in

accordance

with the alarm response

procedure.

Subsequent

to this discussion,

the

CRS directed

a nuclear operator to measure

actual

room temperature

of the fuel building.

The actual

room temperature

was

91'F

and

a work request

was generated

to recalibrate

the temperature

indicator.

After further licensee

followup,

a decision

was

made to cancel

the

work request

and perform

a site modification to change

the location

and type

of temperature

sensor

used for fuel building temperature.

This site

modification had

been previously performed in Units

1

and 2, but had

been

postponed for Unit 3,

as low priority.

The inspector

concluded that

had operators

been appropriately inquisitive

about the spurious

annunciator,

more timely corrective actions

may have

resulted,

without the

need for NRC prompting.

The Unit 3 Operations

Department

Leader agreed,

and noted that operator

response

to the annunciator

had not met management

expectations.

3.2

Containment

S ra

Header

Leaka

e

Unit 3

For the past several

months,

Unit 3 operators

have

been trying to identify the

location of a small leak from the containment

spray header.

Approximately

every

3 weeks,

operators

have

had to refill the containment

spray header with

demineralized

water to clear the containment

spray header

low level alarm.

Several

containment entries .have established

the leak to be approximately

3 to

4 drops per minute.

On July 25, the inspector

noted that the licensee

had not documented

investigation'ctivities

in

a work order or CRDR.

The inspector

concluded

that,

although operators

and engineers

were actively pursuing the problem,

documentation

of the efforts was appropriate.

The inspector discussed

this

concern with the Unit 3 Operations

Department

Leader,

who concurred,

and

a

CRDR was subsequently

initiated.

3.3

Vital Batter

Hi

h Electrol te Levels

Unit 2

On August 2, the inspector

noted that

10 cells in the Channel

D vital battery

had

a level approximately

1/2 inch above the maximum level indication mark.

The inspector determined that the Channel

D battery

had

been placed

on

an

equalizing

charge to counter diverging specific gravities.

The inspector

discussed

the observation of increased

level with the electrical

maintenance

engineer,

who noted that the electrolyte levels

had risen

due to gas

from

electrolysis

being captured

under the battery plates.

The engineer

examined

the battery

and noted that approximately

16 cells

had exceeded

the

TS

surveillance limit of 1/4 inch above the

maximum level indication provided in

TS 4.8.2. l.a, Category

A.

i

I

4

I

~ ~

-12-

The

TS requires that if the Category

A limits are exceeded,

the batteries

must

be verified to be within the Category

B limits within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The

Category

B limits require that electrolyte levels

do not overflow the battery.

In response

to the inspector's

observation,

the licensee

entered

the

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

surveillance

requirement

to verify Category

B limits.

The licensee

developed

work orders

and verified the proper levels for all cells

on site,

and

specifically verified that all Channel

0 cells were within the

TS 4.8.2. I.a

Category

B limits.

The licensee initiated

a

CRDR to evaluate

the elevated

cell levels.

The licensee

determined that,

on August I, the Unit 2

SS

had also noted that

several

cell levels in the Channel

D battery were high.

The

SS

had discussed

the observation

with electrical technicians,

who had informed the

SS that the

level

increase

was

due to the equalizing charge.

The inspector

noted that

more than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

had elapsed

between

the

SS observations

and the

verification performed in response

to the inspector raising the

same question.

The inspector

asked if this constituted

a missed

TS surveillance.

The licensee

subsequently

determined that the elevated electrolyte levels did

not affect the operability of the battery.

Further,

the licensee

determined

that the level limits were not intended to apply when

a battery

was being

equalized.

The licensee

concluded that it had not been

necessary

to perform

the category

B surveillance

requirements

and that they

had not violated the

TS.

Although the licensee's

conclusion

appeared

reasonable,

the inspector

noted

that this was the first, time. that the licensee

had performed

an equalizing

charge

on the newly installed

AT&T batteries.

The inspector considered

that

the diverging Channel

0 cell specific gravities

and the need for an equalizing

charge did not appear to have received

appropriate

management

attention

and

review.

Licensee

management

concurred,

and noted that

had the equalizing

charge

been

adequately

reviewed,

the applicability of cell level limits could

have

been

addressed

prior to the charge.

Furthermore,

the licensee

noted that

the Channel

0 battery

was

made

up of cells from several

manufacturing strings,

which accounted

for the variation in specific gravity of the battery.

They

found that all the cells with high electrolyte levels were from the

same

string,

and that these cells

had started with a higher specific gravity and

voltage level.

As

a result,

the licensee

concluded that more electrolysis

developed

in these cells.

They also noted that the cells with lower specific

gravities

were from a different string.

Based

on discussions

with the battery

manufacturer,

the licensee

concluded that

a 72-hour equalizing

charge

may be

insufficient to eliminate cell specific gravity variations,

and intends to

conduct further equalizing charges

on the battery.

The inspector

concluded that the licensee

had not appropriately

addressed

questions

involving AT&T battery cell electrolyte level until prompted

by the

NRC inspector.

Furthermore,

although the inspector

agreed with the licensee's

conclusion that the batteries

remain operable,

prompt further evaluation'of

the cause

and correction of cell specific gravity variations

appeared

to be

warranted.

This is

an open item

( Inspector

Followup Item 528/9514-03).

i'

I

-13-

3.4

Estimated Critical Position Durin

Reactor Startu

- Unit 2

On July 18, the licensee

performed

a reactor startup following a trip of the

unit on the previous day.

Operators

performed the initial "pul'I to

criticality" of the reactor

and subsequently

stopped after the reactor

engineer

and shift technical

advisor

(STA) calculated

two successive

ACPs that

were more than

500 percent millirho (PCM) below the estimated critical rod

position

(ECRP).

Operators

subsequently

inserted all the full length

regulating control element

assemblies,

as directed

by procedure.

The licensee

performed another calculation of the

ECRP,

and borated

the

reactor coolant

system

(RCS) to the

new estimated critical boron concentration

(ECBC).

The

SS conferred with the

STA and reactor engineer

and concluded that

the reason for the initial ACPs being more than

500

PCM below the

ECRP was due

to the decay of Xenon

and boron concentration

being low in the allowable band.

The

SS then

commenced

another reactor startup.

The inspector

reviewed the two

ECBCs used to perform the reactor startups.

The inspector

noted that the data

and calculations

used

in the

ECBCs were

accurate,

and concluded that the licensee

had correctly performed the

ECBCs.

The inspector

noted that the changes

in reactivity in the

ECBCs were

due to

the decay of Xenon.

The licensee

compensated

for the 300

PCM decrease

in

Xenon

by adding

300

PCM of boron.

Since the reactivity conditions in the core

for both startups

were nearly identical,

the inspector

concluded that the

licensee

had performed the second reactor startup without completely resolving

the reactivity discrepancy

observed

during the first startup.

The inspector

reviewed the

1/M plots performed

by the reactor engineer

and the

STA.

The inspector

noted that the

1/M plot performed

by the

STA contained

an

error,

in that,

the reactivity information was not plotted correctly.

This

error appeared

to have resulted

in one of the two ACPs that were more than

500

PCM below the

ECRP.

The inspector discussed

this finding with the reactor

engineer,

who agreed that the calculation

appeared

to be in error.

The

licensee

noted,

however, that the point was within 5

PCM of the value

calculated

by the reactor engineer.

Additionally, at the point the

calculations

were made,

the

ACPs

had not begun to converge

on the

ECRP.

The

inspector

agreed with the licensee that the calculation error was not obvious.

The inspector also reviewed the

ACP data table

and noted that the licensee

had

not documented

an independent

review of the

1/M plot as required

by procedure.

The inspector discussed

this observation with the licensee.

The licensee

noted that the

STA had performed

an independent

1/H plot, meeting the intent

of the procedure,

but agreed that this independent

action

had not been

appropriately

documented

on the

ACP data table.

The licensee

subsequently

initiated

a

CRDR to evaluate

the startup

and

a

CRDR

to evaluate

the failure to properly document

the independent

review of the

1/M

plot.

At the exit meeting,

licensee

management

emphasized its expectation

that

a more rigorous evaluation of the startup

should

have

been

performed.

~ ~

-14-

The inspector will evaluate

the licensee

c'orrective actions

as part of routine

inspection.

4

MAINTENANCE OBSERVATIONS

(62703)

4. 1

Atmos heric

Dum

Valve Interaction with Plant Protection

S stem

Unit 3

0

On July 12, the inspector

observed

instrumentation

and controls technicians

perform post-modification testing

on atmospheric

dump valve

(ADV) 179.

Site

Modification 03-SM-SG-016

was initiated to assure

that control for the

ADV was

retained

in the

CR in the event that power to the remote

shutdown

hand

indicating controllers

was lost then regained.

As part of the postmaintenance

test,

a nuclear operator

performed

a partial

stroke of the

ADV from the remote

shutdown

room.

During this test, pretrip

and trip lights were received

on the Plant Protection

System

Channel

C.

The

CR operators verified that these

were indicating lights only and that

no

actual pretrips or trips had

been received.

ADV 184 was partially stroked

from the remote

shutdown

room,

and the

same

lights were received

in the

CR.

ADV 184

had not been modified with the

new

controller.

The handswitch

from the

CR was taken to the open permissive

then

to normal position.

The Plant Protection

System trip and pretrip lights did

not

come in, but the Control

Element Assembly

C and Core Protection Calculator

fail lights came in.

The reactor operator verified that

a fail condition did not exist.

The

additional tests

provided assurance

that the site modification was not

a

contributor to the failing lights.

A CRDR was initiated to determine

the

cause of these

indicating lights.

The postmaintenance

test for the

ADV 179 was completed satisfactorily.

The

inspector

noted

good communications

between

licensee

personnel

in the field

and in the

CR.

The inspector

noted that operators

had properly responded

to

the indication

and

had taken appropriate

action to address

the problem.

4.2

Motor End

Ca

Bolts Loose - Unit 3

On July 20, the inspector

observed that

one of four motor end bell bolts was

visibly loose

on SIA-HV306 "LPSI-SD Cooling

HX A Bypass Valve."

The inspector

informed the Maintenance

Valve Services

section leader of the problem.

Valve

Services

issued

a work order to investigate

and correct the problem.

Although

Valve Services

could not find the cause of the bolt being loose,

the inspector

noted the aggressive effort performed to investigate

the cause of the problem.

The licensee

had performed

comprehensive

inspections, of similar valves in all

units

and

had conducted

appropriate

reviews of the as-found condition.

The

inspector

agreed with the licensee that the valve was operable with one bolt

loose

and concluded that the licensee

investigation of the problem was

appropriate.

-15-

4.3

Other Maintenance Activities Observed

The inspector

observed

portions

oF the maintenance

activities noted

below.

The activities observed

were performed appropriately.

~

Charging

pump

A Unit 3

fire Protection Modification of Control Cabinet for Control Building

Battery

Rooms

Unit

1

5

SURVEILLANCE OBSERVATION

(61726)

5. 1

Main Steam Isolation Valve Stroke Test

Unit 3

On July 12,

1995,

the inspector

observed

the licensee

perform portions of a

partial stroke test of the Unit 3 main steam isolation valves

(MSIVs) in

accordance

with 43ST-3SG01,

Revision 6,

"MSIVs Surveillance 4.7. 1.5."

When

the operator

placed

the

CR handswitch for MSIV SGE-UV-170 Train

A to the

exercise position,

the blue exercise light immediately illuminated.

Normally

the blue light does

not

come in until the valve has

reached

the

10 percent

closed position.

The

AO observing

the test at the valve did not observe

any valve motion.

The

reactor operator

stopped

and informed supervision.

The system engineer

was

contacted.

After some discussion

and evaluation,

the

AO was directed to reset

the exercise limit switch.

After the limit switch was reset,

the blue

exercise light extinguished.,

The reactor operator re-performed that portion

of the test

and the valve responded

as expected.

The

same

sequence

of events

was experienced

during the test of the Train

B handswitch.

A CRDR was initiated

and work requests

were written to repair the limit

switches.

The inspector

questioned

the significance of the exercise limit

switch

on the operability of the MSIV.

The

SS stated that the exercise limit

switch had

no affect on the safety related fast close function and, therefore,

did not impact the ability of the

MSIV to close

when required.

As

a

conservative

measure

an operability determination

was initiated.

The inspector

reviewed the surveillance testing requirements

and determined

that the operators

responded

appropriately.

On July 31, the inspector

observed

the licensee

perform sections of

73ST-9SG01,

"MSIV's Inservice Test," in Unit 2.

The inspector

noted that

operators

adequately

performed the procedure

in the

CR and in the field.

5.2

Other Surveillance

Observations

The inspector

observed

portions of the

ST activity noted below.

The

activities observed

were performed appropriately.

S

~ ~

-16-

~

Procedure

32FT-9(D02 Exide Emergency Lighting System,

8 Hour

Verification Testing for 1,2,3E(DNN02 - Unit 2

6

ONSITE ENGINEERING (37551)

6.1

Water

Hammer Durin

Containment

S ra

Pum

Start - Unit 2

On July 21, operators

noted

an abnormal

noise in the containment

spray

(CS)

system during performance of a

ST in Unit 2.

The operators

noted that the

noise occurred during the initial start of the

CS pump.

Operators

indicated

that the noise quickly subsided

and the

pump continued to run smoothly.

Operators

discussed

the observation with engineering.

The licensee

issued

an

operability determination

indicating that the

CS system

remained

operable.

The inspector

agreed with the licensee operability assessment.

The licensee initiated

an evaluation to determine

the cause of the problem.

The licensee

attached

accelerometers

to several

sections of the piping,

performed

system walkdowns,

vented the system in several

locations,

and re-

performed the test.

Engineering

determined that the cause of the problem was

incomplete venting of the system during the past refueling outage.

Upon

further inspection,

the licensee

noted that

one of the

CS trains in Unit

1

experienced

similar characteristics

when vented.

The licensee

intends to

evaluate

the optimum venting process

to alleviate this problem.

The inspector

concluded that engineering's

evaluation

was thorough,

and will monitor the

change

in the system venting process

as part of routine inspection.

6.2

Main Steam

Sam le Line Weld Crack Unit 3

On July 23,

1995,

an auxiliary operator identified

a small leak on Main Steam

Sample Isolation Valve SGN-V053 to the Unit 3

SG

1 Main Steam Line 2.

Engineering

was contacted

and

a

CRDR was initiated.

After testing

and

evaluation

by engineering, it was determined that the crack

may have resulted

from main

steam. line vibration.

Following last year's

implementation of RCS hotleg temperature

reductions

on

Unit 3, operators

began to hear

a loud humming noise in the turbine building

and the main steam support structure.

Engineering

performed extensive

vibration data collection

and analysis to determine

the source of the noise.

Prior to the cracking of the

sample line, they had not been

able to identify

the source of the noise.

They determined that the highest

measured

vibrations

were not of sufficient energy to damage plant equipment.

They continued to

trend the noise

and did not identify significant change

over time.

After the crack developed,

the licensee

noted that the sample line protruded

into the steam line to provide

a mixed sample.'hey

subsequently

determined

that the vibration was centralized

around

a thermowell located

on Main Steam

Line 2, near the turbine stop valve,

and just upstream of the

sample line.

The licensee

speculated

that

a vortex created

by the

steam

on the thermowell

,

1

i

t

I

l

f

-17-

created

a humming noise.

The location of this thermowell

and its proximity to

the

sample line was unique to Hain Steam Line

2 in Unit 3.

The licensee

determined that the vibration was not of sufficient magnitude to

have

caused

the sample line weld to crack.

They speculated

that there

was

a

preexisting

weld defect

and planned to perform further inspection of the weld

during the Unit 3 refueling outage.

As an interim action to reduce stress

to

the

sample line valve,

a clamp was installed.

Operations

and engineering

personnel

planned to monitor the valve until it can

be replaced

during the

outage.

The inspector

concluded that engineering

personnel

had aggressively

pursued

the vibration and noise problem.

The inspector

noted that the identification

of the leaking sample line by the auxiliary operator

was

a good example of

operator

awareness.

Plans to resolve the vibrat-ion and noise problem are

scheduled

during the next refueling outage.

7

FOLLOWUP HAINTENANCE (92902)

7. 1

Violation 530 9431-08

CLOSED

Im ro er Tor uin

of Essential

Chiller

Hotor Terminal

Fasteners

This violation involved maintenance

on the Train

B

EC in Unit 3 to install

a

new motor terminal

adapter.

During maintenance,

the technicians

tightened

the

adapter

fasteners

using personal

judgement rather than the required torque

values

in the vendor technical

manual.

The inspector

was concerned

that the work order instructions did not clearly

reference

the required torque values.

The licensee

determined that the cause

of the violation was cognitive personnel

error on the part of the maintenance

technician for failing to use the implementing references

specified in the

work order for torquing the adapter

fasteners.

However,

the licensee

acknowledged that the work order was deficient in that the correct section for

the vendor technical

manual

was not referenced

in the instructions to install

the motor terminal

arrangement kit.

The licensee

briefed all the heating, ventilation,

and air conditioning

technicians

on conduct of maintenance

expectations

and developed

a model work

procedure for all preventativ'e

and corrective maintenance

on the essential

chillers.

The inspector

reviewed the model work order

and noted that the licensee

had

developed

an appendix that gave instructions for installation of the motor

terminal

adapters

and that the appropriate

torque specifications

had

been

incorporated

into these instructions.

The inspector

concluded that the

licensee

had significantly improved the instructions for working on the

essential

chillers,

'I

t

i,l

,,'

-18-

8

FOLLOWUP ENGINEERING/TECHNICAL SUPPORT

(92903)

8. 1

Violation 529 9508-01

CLOSED

Failure to Identif

Startu

Strainer

Installed in the Containment

S ra

S stem

On February

17,

1995,

the licensee

discovered

startup strainers

in the Unit 2

containment

spray

system which should

have

been

removed prior to initial plant

startup.

A special

inspection

was conducted

and

a violation was issued

in

NRC

Inspection

Report 50-528/95-08

concerning

the licensee's

failure to identify

startup strainers prior to February

17.

The licensee

completed

an

investigation of the event

on March

10 and concluded that the primary cause

was personnel

inattention to detail

and lack of follow up for issue closure.

The licensee

also concluded that personnel

failed to aggressively

review

industry notifications which highlighted the potential

problems with startup

strainers.

Inspection

Report 50-528/95-08

noted that the weaknesses

in the licensee's

corrective action program

and review of industry events contributed to the

licensee's

failure to identify the startup strainers.

The inspector

reviewed

corrective action Audit 95-008,

conducted

in the

end of April to assess

the

effectiveness

of the licensee's

changes

to the corrective action program

implemented

in August of 1994.

The audit team concluded that although the licensee's

corrective action

program

was being effectively implemented,

problems with the adequacy

of root

cause

determinations

continued to compromise

the process'pecifically,

the

licensee

determined that three out of eight significant

CRDR root cause

evaluations

reviewed

were unsatisfactory.

The licensee

determined that interim corrective actions to strengthen

root

cause

evaluations after

a previous audit were ineffective.

The licensee

initiated

CRDR 9-5-f214 to document the problems with root cause

evaluations

and the Executive Vice President,

Nuclear assigned

a Level

1 action to the

Nuclear Assurance

Director to address

the deficiencies

in the corrective

action program.

The inspector

noted that

Phase III of the Level

1 actions

was

to include program changes

to strengthen

root cause

evaluations,

and

was

scheduled

for completion

by April of 1996.

The audit team also concluded that Industry Operating

Experiences

were being

evaluated

in a timely manner

and corrective actions

appeared

to be effective

at preventing similar occurrences.

The inspector previously noted that the

licensee

had conducted

appropriate

reviews of Information Notices 94-60

on

operation with inoperable

main steam safety valves,

and 94-82

on essential

chiller operation during low temperature

operations,

and agreed with the audit

team's

conclusion.

The inspector

concluded that the licensee

had conducted

a thorough

and

critical assessment

of the corrective action program.

The inspector

also

r~

,

1

i

~

-19-

noted that the corrective action program

was included

on the Nuclear Assurance

"top ten issues" list,

and that licensee

management

was appropriately

focused

on improving the effectiveness

of the corrective action program.

The

inspectors will continue to monitor the effectiveness

of the corrective action

program during future routine inspections.

8. 1.2

Other Corrective Actions

The inspector verified that the system engineering third quarter industry

events training included

a briefing on the startup strainer event.

'The

inspector also noted that the licensee

had included guidance

on

how to

identify temporary startup devices during system

walkdowns in the system

engineering

procedure.

The licensee

had also completed

system

walkdowns for

systems

important to safety and,production.

The licensee

planned to complete

walkdowns of other systems

by the

end of 1995.

The inspector verified that the licensee

had

removed all of the startup

strainers

from the piping and instrumentation

drawings.

The inspector also

noted that the licensee

had reduced

the total

number of incorporable

changes

by 50 percent

and reduced

the backlog of drawing changes

(those greater

than

45 days old) by 65 percent.

The licensee's

goal

was to incorporate all

drawing changes within 30 days.

The inspector

concluded that the licensee

had completed all the corrective

actions

committed to during the startup strainer 'special

inspection.

9

IN OFFICE REVIEW OF LERs

(90712)

The inspectors

reviewed the following licensee

event reports

and found that

they included appropriate

root cause

evaluations

and corrective actions to

prevent recurrence:

LER 529/95-03:

TS 3.0.3 Entry For Loss of Both Trains of Essential

Cooling Water

and Hydrogen

Recombiners

LER 529/95-02:

TS 3.0.3 Entry Due to Loss of Charging

Pumps

and Boration

Flowpaths

v'

l

1

t

1

Persons

Contacted

ATTACHMENT 1

1. 1

Arizona Public Service

Com an

  • H. Anderson III, Senior Engineer,

Nuclear Fuels

Management

J. Bailey, Vice President,

Nuclear'Engineering

  • M. Burns,

Department

Leader,

Nuclear Engineering

Design

  • C. Emmett,

Media Consultant,

Strategic

Communications

  • R. Fullmer,

Department

Leader,

Nuclear Assurance

  • D. Garchow, Director, Engineering
  • B. Grabo,

Section

Leader Compliance,

Nuclear Regulatory Affairs

  • V. Huntsman,

Department

Leader,

Radiation Protection

  • W. Ide, Director, Operations
  • A. Krainik, Department

Leader,

Nuclear Regulatory Affairs

  • D. Lamontague,

Senior Consultant,

Licensing,

Nuclear Regulatory Affairs

  • J

~ Levine, Vice-President,

Nuclear Production

  • D. Mauldin, Director, Maintenance

M. Shea,

Director, Radiation Protection

  • J. Steward,

Department

Leader,

Radiation Protection

  • W. Stewart,

Executive Vice-President,

Nuclear

  • R. Stroud,

Regulatory Consultant,

Nuclear Regulatory Affairs

J. Taylor, Unit

1 Operations

Department

Leader

  • R. Taylor, Acting Unit

2 Operations

Department

Leaders

1.2

NRC Personnel

  • K. Johnston,

Senior Resident

Inspector

  • D. Garcia,

Resident

Inspector

  • J. Kramer,

Resident

Inspector

1.3

Others

  • F. Gowers, Site Representative,

El

Paso Electric

  • B. Drost,

E&0 Committee

Member, Salt River Project

  • Denotes those present

at the exit interview meeting held

on August ll, 1995.

The inspector

also held discussions

with and observed

the actions of other

members of the licensee's

staff during the course of the inspection.

2

EXIT MEETING

An exit meeting

was conducted

on August 11,

1995.

During this meeting,

the

inspectors

summarized

the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

1

t

e

i

i

ATTACHMENT 2

LIST OF

ACRONYMS

ACP

ADV

AFW

AO

APS

CS

CR

CRDR

CRS

EC

ECBC

ECRP

FWCS

gpm

HIC

HPSI

Kv

LER

LPSI

MRT

NRC

NRR

PDR

PVNGS

RCS

SG

SP

SS

ST

STA

TS

URI

anticipated critical position

atmospheric

dump valve

auxiliary feedwater

auxiliary operator

Arizona Public Service

containment

spray

control

room

condition report/disposition

request

control

room supervisor

essential

chiller

estimated critical boron concentration

estimated critical rod position

feedwater control

system

gallons per minute

high integrity container

high pressure

safety injection

Kilovolt

Licensee

Event Report

low pressure

safety injection

management

response

team

Nuclear Regulatory

Commission

Office of Nuclear Reactor Regulation

Public Document

Room

Palo Verde Nuclear Generating

Station

reactor coolant

system

steam generator

spray

pond

shift supervisor

surveillance test

shift technical

advisor

Technical Specification

Unresolved

Item

~

~