ML17311A815

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Insp Repts 50-528/95-03,50-529/95-03 & 50-530/95-03 on 950115-0225.No Violations Noted.Major Areas Inspected: Announced Insp of Plant Status,Onsite Response to Events, Operational Safety Verification,Maint & Surveillance
ML17311A815
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 04/07/1995
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311A814 List:
References
50-528-95-03, 50-528-95-3, 50-529-95-03, 50-529-95-3, 50-530-95-03, 50-530-95-3, NUDOCS 9504250069
Download: ML17311A815 (54)


See also: IR 05000115/2002025

Text

ENCLOSURE

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/95-03

50-529/95-03

50-530/95-03

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating

Station,

Units 1,

2,

and

3

Inspection At;

Maricopa County, Arizona

Inspection

Conducted:

January

15 through February

25,

1995

Inspectors:

K. Johnston,

Senior Resident

Inspector

J.

Kramer,

Resident

Inspector

A. MacDougall, Resident

Inspector

B. Olson, Project Inspector

Approved:

owar

ong,

C ie

,

eactor

Jects

Branc

ate

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of plant

status,

onsite

response

to events,

operational

safety verification,

maintenance

and surveillance

observations,

onsite engineering,

refueling

operations,

maintenance

and engineering

followup, and,licensee

event reports.

Results

Units

1

2

and

3

~

Plant

0 erations

Inspectors

observed

mixed performance

in the area of plant operations.

Unit 2

operators

demonstrated

excellent performance,

with minor exceptions,

when

performing complex

and challenging

integrated

safeguards

testing

(Section

6. I).

However, Units

1

and

3 operators

did not demonstrate

a

questioning attitude

when they noted,

but failed to investigate,

off-normal

indications

in safety, injection line pressures

(Section 3.3).

In addition,

once the concern

had

been

addressed

in Unit 1, operations

management

did not

promptly investigate

the condition in Unit 3.

9504250069 9504i9

PDR

ADQCK 05000528

8

PDR

Ll

f

I

The inspectors

observed

a Nuclear Assurance

(NA) evaluator identify that

Unit 3 operators

did not implement

a procedure prerequisite

when starting

an

essential

cooling water

pump,

and the

NA evaluator

ensured that the finding

was documented,

reviewed,

and resolved

(Section 3.2).

~

Maintenance

While maintenance

craft continued to demonstrate

excellent work practices,

some of their work instructions

were poorly developed

and required significant

adjustment

in the Field.

As

an example,

work performed

on

a Unit 2 emergency

diesel

generator

was found to be good.

However,

associated

work instructions

were found to have weaknesses

such

as conflicting torque specifications,

duplicate gasket material,

and several

pages of nonapplicable

instructions

(Section 4.2).

Similar work instruction weaknesses

were identified'y an

NA

audit,

performed in November

1994.

The audit tied work instruction

inadequacies

to weak planner qualification and training (Section 5).

The

audit report

was found to be excellent,

identifying corrective actions

along

with the findings in a succinct style.

Weaknesses

were noted in the evaluation of main feedwater

pump reliability

which followed the failure of a governor control

speed

probe (Section 4. I).

These

weaknesses

also pointed to

a failure data trending data

base

which

lacked data for important-to-safety

systems.

Maintenance

management

acknowledged

that the feedwater

pump reliability evaluation

was weak

and

continued

improvements

need to be

made to the failure data trending program.

Inspectors

found that maintenance

personnel

conducting refueling activities

demonstrated

several

strengths,

including

a very good

knowledge of the job and

the equipment.

Licensee

engineering

demonstrated

excellent technical capabilities

and

a

strong questioning attitude in their resolution of discrepancies

they

identified in an analysis

performed

by

a vendor supporting

steam generator

modifications.

Engineering

management

took conservative

action to recommend

that the modifications,

which were

soon to be implemented,

be put on hold

(Section 7.1).

Inspectors

noted that longstanding

unresolved deficiencies

were receiving

greater attention.

Two issues

discussed

in the report involve plant

deficiencies

which had weak technical

reviews

and low priority for resolution.

One issue

involving essential

cooling water radiation monitors confirmed

previously identified weaknesses

in operability and safety evaluations,

timeliness of problem resolution,

and reportability (Section 7.2).

These

programs

have all received significant attention

in the past year.

In

addition, auxiliary feedwater modifications are being

implemented

which are

designed

to address

longstanding

condensation

drainage deficiencies

I

I

0'

~

~

(Section 3. 1).

Engineering

management

recognizes

that continued attention is

warranted

on these older issues.

~

Mana ement Oversi ht

Licensee

management

was responsive to weaknesses

identified in maintenance

instructions, failure data trending,

excess

use of overtime,

and engineering

issues.

Continued

assessment,

beyond the concerns

identified by the

inspectors,

was either being performed,

or was planned.

In addition,

NA was

demonstrating

a presence

in the field, asking probing questions,

and

addressing

significant issues.

Plant operators'ncorrect

assessment

of off-normal plant parameters

in the

safety injection system

and operations

management

slow resolution of the issue

indicated that continued attention

appears

warranted

in the area of operator

performance.

While engineering

management

has raised

the priority of resolving longstanding

plant deficiencies,

weaknesses

in the initial technical

reviews of

deficiencies

in the essential

cooling water system radiation monitors

and

auxiliary feedwater

condensate

drains indicate that continued attention is

warranted.

Summar

of Ins ection Findin s:

One unresolved

item was identified concerning

the operability and

reportability of the essential

cooling water system with nonseismically

qualified instrumentation

(Section 7.2)

~

Two violations were closed'Sections

9. 1 and

11. 1)

~

Three

Licensee

Event Reports

were closed

(Section

12).

Attachments:

1.

Persons

Contacted

and Exit Meeting

2.

Acronyms

1

I

)

i)f

/

I

ff

'

DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 began

the inspection period in a power ascension

to 100 percent

power

following the performance of a steam generator

chemistry hideout return test

and remained

at essentially

100 percent

power through the inspection period.

1.2

Unit 2

Unit

2 operated

at

100 percent

power during the first part of the inspection

period.

On February 3,

power was reduced

and the unit was taken offline in

preparation for the start of the fifth refueling outage.

On February

17,

during

a maintenance activity, startup strainers

were found in both

containment

spray

pump suction lines (discussed

in

NRC Special

Inspection

Report 529/95-08).

The unit ended the inspection

period with the core

offloaded.

1.3

Unit 3

Unit 3 began

the inspection

period at

100 percent

power and remained

at

essentially

100 percent

power through the inspection period.

2.

ONSITE RESPONSE

TO EVENTS

(93702)

2. 1

0 erations

Su

ort Buildin

Fire

Unit 3

On January

19,

1995,

a small fire broke out on the first floor of the Unit 3

operations

support building.

The fire, which started

in a battery storage

area,

was extinguished

by the automatic sprinkler system.

The storage

room

'contained

small

spare lead/acid

and nickel/cadmium batteries.

The onsite fire

department

responded

to the fire and ensured

the fire did not spread.

The

operations

support building is adjacent

to the Unit 3 control building and

houses site maintenance

and the

NRC resident inspectors'ffice.

The inspector

responded

to the control

room upon notification of the fire.

The inspector

noted that the reactor operators

were focused

on monitoring the

control board indications

and were not distracted

by the events of the fire.

The inspector

also observed site management

presence

in the control

room.

The

licensee

reviewed the emergency

plan classification

and determined that the

event did not warrant

an emergency classification

in that the fire did not

last longer than

10 minutes.

The inspector

agreed with the licensee's

determination.

The licensee

thought the fire may have

been

caused

by an employee laying

a

rubber apron across

the batteries

and causing

one of the batteries

with a

"maintenance

required tag" attached

with a fine wire to short circuit a

battery cell.

This may have

caused

the wire to get hot and start the apron

'

burning.

The inspector

concluded that the fire had

no impact

on Unit 3 plant

operations

or equipment

and the control

room personnel

responded

appropriately.

3 OPERATIONAL SAFETY VERIFICATION

(71707)

3. 1

Turbine-Driven Auxiliar

Feedwater

AFW

Pum

Drains Isolated

On January

25, during

a routine walkdown of the turbine-driven

AFW pump,

the

inspector

noted that the upstream

steam line drain isolation valve,

V-159,

and

the turbine trip and throttle valve below seat drain isolation valve,

V-161,

were closed.

The inspector also noted that there

was condensation

draining

out of the turbine casing drain

and the exhaust

stack drain line.

The

inspector

reasoned

that with the upstream drains isolated, all the 'condensate

in the steam

supply line had to drain through the

AFW pump turbine.

Additionally, there

was probably

some

amount of condensate

that remained

in

the upstream piping that would be forced through the turbine

when it was

started.

The inspector discussed

this configuration with the system engineer

to determine

why the drains

were isolated,

whether 'a

10 CFR 50.59 safety

evaluation

had

been

performed,

and if this configuration

had

an impact

on

AFW

pump operability.

The inspector

was informed that the drains

were isolated

in 1989 due to

a

concern with excess

flow check valves installed in the drain lines.

The

excess

flow check valves were designed

to stay

open during standby operation

to allow draining of the condensation.

When steam

was admitted to the

turbine,

they were

supposed

to close

and prevent

steam

from entering the

AFW

pump room.

The excess

flow check valves were also'sed

as the American

Society of Mechanical

Engineers

Boiler and Vessel

Code class

break between the

safety

and nonsafety

grade piping and were designed

to stop flow if the

nonsafety piping broke during

a design

bases

event.

In 1986, engineering

documented reliability problems with the excess

flow

check valves in several different systems

and

recommended

that the excess

flow

valves not

be relied

upon

as designed.

The evaluation

addressed

the impact

on

operability and the compensatory

measures

for each

system that

used the excess

flow check valves.

The evaluation

concluded that isolating the

AFW steam

supply upstream drains did not impact operability of the turbine since there

had not been

any performance

problems with turbine overspeeds

on startup

and

three of the five original drain paths

were still available.

The evaluation

did not recommend

any compensatory

measures

to periodically open the upstream

drains

and the drawings

were updated to show the isolation valves,

V-159 and

V-161,

as normally closed.

The inspector

reviewed the justification for

isolating the steam line drains

and agreed with the conclusion that the change

did not present

an operability concern.

In 1989, engineering

evaluated

the long term solution to the problem with the

AFW steam line drains.

Engineering

recommended

that the drains

be left

isolated

and administratively controlled to ensure

they remain closed.

Engineering

performed

a 50.59 evaluation

as part of this review and concluded

that the change did not create

a unreviewed safety question.

The inspector

reviewed the 50.59 evaluation

and noted that it did not include

a discussion

of the effect of the condensation

flowing through the turbine

and the

potential for turbine overspeed

events with the drains isolated.

The

inspector

noted that the initial evaluation

in l986 discussed

the potential

for turbine overspeeds

and that the turbine vendor technical

manual

did not

include any specific cautions or recommendations

for how much draining through

the turbine casing

was acceptable.

While the licensee

has experienced

overspeed trips due to condensation,

the condensation

in the turbine

was

considered

to have minimal impact.

The inspector

concluded that the decision to isolate the

AFW steam line drains

was

an example of a change

to the plant that

was performed outside the normal

design

change

process,

similar to changes

to the essential

cooling water

system discussed

in Section 7.2.

Although the drains

were isolated five years

ago,

the inspector

noted that the licensee

had not initiated actions at that

time to improve the steam line drains.

Prior to this inspection,

the licensee

had reevaluated

the steam line drains

as part of a reassessment

of AFW pump

performance

and

had initiated

a design

change to reroute the upstream drains

as part of a comprehensive

design

change to improve the reliability of the

turbine-driven

AFW pumps.

The design

change

was being

implemented

in the

current Unit 2 refueling outage

and

was

scheduled

for installation in the next

refueling outages

in Units I and 3.

The licensee

agreed that they should

have

addressed

the drainage configuration earlier.

The inspector

concluded that this issue

could have

been

addressed

earlier if

the licensee

agreed.

The inspector will review the effect of the design

change during future routine inspections.

As discussed

in Section 7.2, the

licensee

has

addressed

weaknesses

in the areas

of plant modifications,

50.59

reviews,

and engineering

follow through.

These actions

have

been

implemented

to prevent this type of issue

from recurring.

3.2

0 erator

Procedure

Usa

e

Unit 3

On February 8,'995,

the inspector

observed

control

room operators

perform

a

manual start of the essential

cooling water system.

In addition to the

inspector,

a nuclear

assurance

observer

monitored the evolution.

The

essential

cooling water

(EW) system operating

procedure

included

a

prerequisite

step that required operators

to direct

a radiation monitoring

technician to ensure that the

EW system radiation monitor was

on line.

The

reactor

operator

and control

room supervisor

noted that the monitor could not

be placed

on line based

on seismic

concerns

(see

Section 7.2).

They contacted

the radiation monitoring technician to perform sampling of the

EW system

and

continued with the procedures

The nuclear

assurance

observer

questioned

the operators

decision to continue

with the procedure without resolving the apparent

discrepancy with the

prerequisite

step

and initiated

a Condition Report/Disposition

Request

(CRDR)

to evaluate

the event.

The licensee

subsequently

revised the operating

i

0

that the change did not create

a unreviewed safety question.

The inspector

reviewed the 50.59 evaluation

and noted that it did not include

a discussion

of the effect of the condensation

flowing through the turbine

and the

potential for turbine overspeed

events with the drains isolated.

The

inspector

noted that the initial evaluation

in 1986 discussed

the potential

for turbine overspeeds

and that the turbine vendor technical

manual

did not

include

any specific cautions

or recommendations

for how much draining through

the turbine casing

was acceptable'hile

the licensee

has experienced

overspeed

trips due to condensation,

the condensation

in the turbine

was

considered

to have minimal impact.

The inspector

concluded that the decision to isolate the

AFW steam line drains

was

an example of a change

to the plant that was performed outside the normal

design

change

process,

similar to changes

to the essential

cooling water

system discussed

in Section 7.2.

Although the drains

were isolated five years

ago,

the inspector

noted that the licensee

had not initiated actions at that

time to improve the steam line drains.

Prior to this inspection,

the licensee

had reevaluated

the

steam line drains

as part of a reassessment

of AFW pump

performance

and

had initiated

a design

change to reroute the upstream drains

as part of a comprehensive

design

change to improve the reliability of the

turbine-driven.AFW pumps.

The design

change

was being

implemented

in the

current Unit

2 refueling outage

and

was scheduled for installation in the next

refueling outages

in Units I and 3.

The inspector

concluded that this issue

could have

been

addressed

earlier if

the licensee

agreed.

The inspector will review the effect of the design

change during future routine inspections.

As discussed

in Section 7.2, the

licensee

has

addressed

weaknesses

in the areas

of plant modifications,

50.59

reviews,

and engineering

follow through.

These

actions

have

been

implemented

to prevent this type of issue

from recurring.

3.2

0 erator Procedure

Usa

e - Unit 3

On February 8,

1995,

the inspector

observed control

room operators

perform

a

manual start of the essential

cooling water system.

In addition to the

inspector,'

nuclear

assurance

observer

monitored the evolution.

The

essential

cooling water

(EW) system operating

procedure

included

a

prerequisite

step that required operators

to direct

a radiation monitoring

technician to ensure that the

EW system radiation monitor was

on line.

The

reactor operator

and control

room supervisor

noted that the monitor could not

be placed

on line based

on seismic

concerns

(see Section 7..2).

They contacted

the radiation monitoring technician to perform sampling of the

EW system

and

continued with the procedure.

The nuclear

assurance

observer

questioned

the operators

decision to continue

with the procedure without resolving the apparent

discrepancy with the

prerequisite

step

and initiated

a Condition Report/Disposition

Request

(CRDR)

to evaluate

the event.

The licensee

subsequently

revised the operating

,

i

I

i

procedures

in all three units to direct the radiation monitoring technician to

perform specific actions if the radiation monitor could not to be placed in

service.

The inspector

noted that the

EW radiation monitors

had

been

removed

from

service

in April 1994,

and concluded that control

room personnel

in all three

units

had

been "operating

around" the prerequisite

step in the operating

procedure,

demonstrating

a lack of ownership of the procedure.

The inspector

noted the persistence

of the nuclear

assurance

observer to correct the

deficiency.

The inspector will evaluate

the final

CRDR recommendations

as

part of a routine inspection.

3.3

Safet

In 'ection

SI

Tank Drain and Fill Isolation Valve Leaka

e

On February

9, during

a routine tour of the Unit

1 control

room, the inspector

noted that the "B" train hot leg SI check valve leakage

pressure

indicator,

(PI) 391,

was reading

about

600 psi.

This gage is used to indicate

check valve leakage

from the reactor coolant

system hot leg through the

shutdown cooling suction line into the high pressure

safety injection (HPSI)

hot leg recirculation line.

The inspector

asked

the operators

why there

was

a

difference

between

the "A" train check valve leakage indicator PI-390, which

was reading less

than

50 psi,

and the "B" train indicator PI-391,

which was

reading close to safety injection tank (SIT) pressure.

The operators

told the inspector that running the

HPSI

pump during routine

surveillance tests

caused

pressure

to become

locked

between

the two hot leg

injection check valves.

The inspector

had previously questioned

operators

on

the difference

between

the readings of PI-390

and PI-391

and was given the

same explanation.

The inspector

asked

the operators

when the last

HPSI test

was performed

and

why PI-391

was reading the

same pressure

as

SIT pressure.

As

a result of the inspector's

questions,

operators

investigated

the situation

and determined that the

2B SIT drain

and fill isolation Valve SIB-641,

and the

HPSI fill isolation Valve SIB-322 were leaking past their seats.

The Unit

1 shift supervisor initiated work requests

for the leaking valves

and

called the system engineer to discuss operability of SI Valves

641

and 322.

The system engineer

stated that these

valves were not required to be zero

leakage

valves

and that the small leakage did not affect operability of the

SIT system.

The shift supervisor told the inspector that

an operability

determination

(OD) would be performed.

The inspector

agreed with the shift

supervisor's initial determination that the leaking valves did not create

an

immediate safety concern.

The inspector

noted similar differences

between

the pressure

readings for

PI-390

and PI-391 in Unit 3.

On February

14, the inspector

asked

the Unit 3

shift supervisor if he was

aware of the leaking

SI valve problem in Unit

1 and

evaluated

the condition in Unit 3.

The Unit 3 shift sunervisor

was not aware

of the problem

and

had not conducted

a review to determine

the extent of

leakage

in Unit 3.

(

The inspector

was informed that the Unit

1 shift supervisor

had sent the

information concerning

the leaking SI valves to the Unit 3 control

room on

February

10.

As

a result of the inspector's

questions,

the information from

Unit

1 was again provided to the Unit 3 control

room and

a troubleshooting

plan was developed

to determine

the source of the leakage

in Unit 3.

On

February

16, Unit 3 operators

gathered

information and determined that they

also

had

a leaking SIT drain

and fill isolation valve and

a leaking

HPSI fill

isolation valve.

On February

22, the inspector

reviewed the results of the test

conducted

in

Unit 3 and noticed that

an

OD for the leaking valves

had not been

performed.

The inspector

noted that although the SIT drain

and fill isolation valve

and

HPSI fill isolation valve were not required to be zero leakage

valves,

they

did receive

a safety injection actuation

signal to shut to maintain SIT

inventory in the event of a safety injection actuation

signal during SIT fill

or drain operations.

The inspector

questioned

the shift supervisor

about the

impact

on SIT integrity with the leaking valves

and whether

an

OD was

appropriate.

The shift supervisor told the inspector that the test data

had

been

forwarded to engineering

and that they did not think an

OD was required.

The inspector

then

informed the operations

department

leader

who agreed with

the inspector, that

an 00 was required.

On February

22, the system engineer

completed

a 'draft evaluation of the

condition in both Units

1

and 3,

The system engineer

determined that the SIT

system

was operable

because

the leakage,

in both cases,

was very small

(less

than 0. 1 gpm)

and the isolation valves

between

the SIT drain

and fill header

and the'reactor

drain tank and the refueling water tank were leak tight.

As

a

result,

the level in the SITs would stay constant

once the drain header

was

pressurized

through the leaking valves.

Additionally, system

alarms

would

alert the operators

to an increase

in boundary valve leakage if the condition

degraded.

The inspector

reviewed the design basis

manual,

the Updated Final

Safety Analysis Report,

and operating

procedures

.and

agreed with the

conclusion that the existing condition in Units

1 and

3 did not impact SIT

operability.

The inspector also noted that the system engineer

conducted

a

detailed,

thorough operability evaluation.

The inspector

had the following conclusions

concerning operator

performance

in

Units

1

and 3:

~

Control

room operators

did not question

an indicated discrepancy

in

control

board indication for safety-related

plant equipment.

The

operators

had developed

an assumption

which was not based

on fact.

While the condition was eventually determined to not be

safety-significant,

a more significant condition could have provided

similar indication.

Operations

management

did not aggressively

pursue identifying and

evaluating the condition in Unit 3.

l

,

At the exit meeting,

the Director of Operations

stated that operator

performance

did not meet his expectation

and that

he would reemphasize

the

importance of understanding

plant status,

particularly control

board

indications.

The inspector

concluded that these

actions

were appropriate.

4

MAINTENANCE OBSERVATIONS

(62703)

4. 1

Main Feedwater

MFW

Pum

S eed

Probe Failure

Unit

1

On January

21,

1995,

Speed

Probe

2 on the Unit

1

MFW Pump

A began to fail

intermittently,

The

Speed

Probe

2 failure did not impact the operation of the

HFW pump control

system,

since it acts

as

a backup input and is relied upon

only in the event of the failure of Speed

Probe

1.

However, the additional

failure of Speed

Probe

1 would result in the

MFW pump turbine governor valve

opening fully and causing

the

MFW pump to overspeed.

To repair the failed

speed

probe,

the

MFW pump would have to be removed

from service

and

power

reduced

to approximately

60 percent

power.

Plant operations

management,

with support

from maintenance

engineering,

decided to place the repair of the failed speed

probe

on hold for 10 weeks

until the start of the Unit

1 refueling outage

schedule.

The decision

involved

an evaluation of the risks of a power reduction late in core life,

the failure history of HFW speed

probes,

and the relatively short interval to

the outage.

The inspector

reviewed the failure history of the

speed

probes.

The data

was

provided

by maintenance

engineering with the support of system engineering,

and the maintenance

failure data trending group.

In general,

there

had

been

a

significant number of speed

probe failures in all three units.

However, the

inspector

found that the

MFW speed

probe failure history provided

by the

licensee

was inaccurate

and incomplete.

Although the data included several

HFW speed

probe failures,

the maintenance

engineer

noted that several

additional

speed

probe failures

had not been

picked

up in their data

search.

The inspector determined that analyses

to determine

a cause for the

speed

probe failures

had not been performed.

Additionally, the licensee

had not

identified

a mean time for speed

probe failure and noted that performing this

type of analysis

would be difficult.

The inspector

found that maintenance

had

not determined

the

age of the remaining

speed

probe in the Unit

1 "A" MFW pump

and considered

that this should

have

been

a key input to an analysis of MFW

pump reliability.

Maintenance

engineering

subsequently

determined that the

speed

probe

had

been installed in 1993.

The inspector discussed

the quality of the data with maintenance

failure data

trending

(FDT) personnel.

The licensee

recognized that

FDT historical

information, especially in balance of plant systems,

was weak.

In the case of

the

HFW speed

probes,

the

FDT program listed only three failures.

While a

significantly greater

number of failures were found in the maintenance

database,

these failures were listed under at least three different component

'

-10-

identifications.

Additionally, the maintenance

database

did not consistently

provide

an apparent

cause of failure.

The inspector discussed

the weaknesses

in the data provided to plant

operations

and the weaknesses

in the

FDT program with the Director of

Maintenance.

He concurred that the analysis

provided to plant operations

had

not met his expectations

and discussed it with his staff.

Additionally, he

recognized

the weaknesses

in the

FDT program

and the role that it would play

in the licensee's

implementation of the

10 CFR 50.65 maintenance

rule.

The

inspector

noted that

a weakness

in the

FDT program

had

been identified by the

licensee

previously

and

a maintenance

Level

1 action

had

been initiated to

improve the acquisition of data into FDT.

The inspector

found these

actions

to be appropriate.

4.2

Emer enc

Diesel

Generator

EDG

Work Order Deficiencies

Unit 2

On January

25, the inspector

observed

mechanical

maintenance

personnel

performing corrective maintenance

on the jacket water heater

pump

and the

prelube oil circulation

pump

on

EDG A in Unit 2.

Both of these

pumps

had

leaks

from the mechanical

seal

which were being replaced

as part of a

scheduled

online outage of the

EDG.

4.2. 1

Jacket

Water

(JW) Heater

Pump

The licensee

uses

model maintenance

instructions

(NI) for repetitive work to

establish

consistency

and to reduce

the

amount of prejob planning for routine

work.

The inspector

noted that the work order for reassembling

the

JW heater

pump was

an HI that

had

a step to torque the fasteners

using the general

torque specification

from the

EDG vendor technical

manual.

These

specifications

were" used if specific torque requirements

were not available.

However, the mechanic noticed that the section of the vendor technical

manual

for the

JW heater

pump included instructions to torque the fasteners

using

good mechanical

judgment.

Therefore,

the HI provided confusing guidance

on

the torque requirements

for the fasteners,

The mechanic

discussed

the situation with the

NA evaluator observing

the job

and decided to use the instructions

which specifically applied to the

JW

heater

pump (tighten the fasteners

using good mechanical

judgment).

The

NA

evaluator also noted that the HI specified

two different class

and item

numbers for the

pump suction gasket.

The

NA evaluator

suggested

that the

mechanic

discuss this problem with the

shop planner.

The inspector

observed

a questioning attitude

by the mechanic

and the

NA

evaluator

to find and solve the problem with the HI.

In spite of the

instruction deficiencies,

the mechanic

was able to eventually perform the work

appropriately.

However,

the inspector

was concerned

that these technical

errcrs

were not identified prior to sending

the paperwork to the field.

The

inspector discussed

this observation with the mechanical

maintenance

section

leader.

The inspector

asked

the section leader if he expected

the planner to

conduct

a technical

review of NIs prior to including it in a work package

sent

I

0

-11-

to the field.

The section leader stated that the planners

were tasked with .

reviewing the MIs when they

had time, but were not expected

to review each

package prior to sending

the work to the field.

As

a result,

the planners

were relying on feedback

from the field to correct technical

problems with the

work order.

The section leader

agreed

that reviewing the NIs needed

to be

a priority and

asked

the planner assigned

to his section to conduct

a technical

review of the

ten most used Hls.

In addition,

the planner

changed

the HI to reflect the

correct torque value

and gasket

class

and item number.

The inspector

noted

that weaknesses

in MI had

been identified by licensee

organizations

and

improvements

were in progress.

The inspector

concluded that the licensee's

initial corrective actions

were appropriate.

4.2.2

Pre-Lube Oil Circulation

Pump

The inspector

observed

the mechanics

performing work on the prelube oil

circulation

pump for

EDG A.

The inspector

reviewed the work order

and noted

that the objective of the work order

was to remove,

rebuild,

and replace

the

prelube oil circulation

pump using

a model

MI.

Because

the inspector

had

difficulty in following the HI, the inspector

asked for clarification of the

NI.

The mechanics

informed the inspector that they were only replacing the

pump mechanical

seal

and that most of the instructions

were unnecessary.

The inspector

observed

the remaining work on the

pump

and did not have

any

concerns

with the performance of the work in the field.

The inspector

noted

that the mechanics

were able to determine

the appropriate

steps

to be

performed.

However,

the inspector

was concerned

that the workers were

provided with a large

amount of unnecessary

instructions for the job they were

performing.

The inspector

noted that the mechanics

in the field had to mark

out eight of the ten

pages of work order instructions.

The inspector

was

concerned

that having

a complex work document

where

a simple document 'would

suffice may reinforce the tendency of the workers to not refer to the

instructions,

increasing

the chances

of a mistake.

The inspector

asked

the responsible

section leader

and department

leader if

the planner

should

have lined out the unused

steps prior to sending

the work

order to the field.

Neither individual expected

the planners

to remove

unnecessary

steps prior to sending

the work order to the field.

They felt

this type of review was too time consuming for the planners

and that the

workers in the field were able to do the review.

The inspector

reviewed the

work order

and noted that it would only have taken

about

5 minutes for the

planner to review the work order

and

remove the unnecessary

steps.

The inspector discussed

this issue with the Director of Maintenance

and

learned that it was his expectation that planners

delete

unnecessary

work

order instructions prior to sending

the package

to the field.

The licensee

had

a long term action to "sectionalize"

MIs so that only the applicable

portion of the NI would be produced for the work package.

The licensee

also

created

a

new NI for replacement

of the

pump mechanical

seals.

!

1

0

-12-

The inspector

concluded that each level of supervision

in the mechanical

maintenance

department,

from the team leader through the director of

maintenance,

had different expectations

for the level of prejob work order

review required.

The inspector

has identified previous

weaknesses

in the

quality of work instructions.

In addition,

an

NA audit found weaknesses

in

work instructions

and found problems

in planner qualification

and training.

At the exit meeting,

the Director of Maintenance

informed the inspector of an

effort by the maintenance

support group to improve planner qualification

training.

Maintenance

support also identified the problem with inconsistent

expectations

concerning

the responsibilities of planners.

At the

end of the

inspection

period maintenance

support

had completed its review but was still

developing

how to incorporate

management's

expectations

into the revised

training program.

The inspector will review the revised planner

qualifications

and the quality of work orders during future routine

inspections.

4.3

Motor-0 crated

Valve

MOV

Maintenance

and Testin

on Valve SIA-HV-696

Unit 2

On January

18,

1995,

the inspector

observed

portions of routine

MOV

maintenance

and testing

on shutdown cooling heat

exchanger outlet Valve SIA-

HV-696.

The inspector

noted that to perform the testing,

the valve motor was

operated

frequently

by technician.

During the testing,

the inspector

observed

that the motor casing

became

hot to the touch.

The valve took approximately

90 seconds

to travel its full stroke.

Additionally, in some instances,

the

valve motor was momentarily energized

or "jogged" several

times in succession

to position the valve for specific tests.

The inspector

was concerned

that

motor heating could lead to long-term motor winding degradation.

The inspector

asked

the

MOV technician if guidance

had

been provided

concerning

the potential for overheating

valve motors during testing.

The

technician

responded

that,

in general,

they feel the casing during testing

and

take

a break from testing

when the casing gets hot.

The inspector questioned

whether this general

guidance

was consistent

with

vendor recommendations.

The

MOV maintenance

engineering

section leader

showed

the inspector

a letter from the vendor,

Limitorque, to another utility

concerning jogging capabilities

as well as full load run times.

The guidance

provided

by the vendor

stated that the valve operator could

sustain

locked rotor current for up to

10 seconds.

The vendor noted that

a

motor starting event would produce

locked rotor current for less

than

1 second,

which would allow ten consecutive starts.

To account for variables,

the vendor

recommended

that these

motors

be limited to five consecutive

starts

with a cooling period of an hour or more between restarts.

The inspector

noted that this guidance

was more conservative

than the practice

observed

in the field, when the inspector

noted that in the span of

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> the

valve was fully stroked six times

and then jogged

up to six consecutive

times

I

,

j

)

-13-

at least twice.

The inspector discussed

this with the

MOV maintenance

engineering

supervisor.

He had reviewed the motor starting current traces

and

determined that Valve SIA-HV-696 achieved

locked rotor current for

0.25 seconds

each

time the valve was cycled.

According to vendor guidance,

this would allow up to 40 consecutive starts.

Based

on this data,

the section

leader

concluded that the motor had not been

damaged.

The inspector

found the

review to be acceptable.

The

MOV maintenance

engineering

section leader stated that additional training

covering the vendor recommendations

was provided to

MOV maintenance

technicians.

The training covered

the vendor's

recommendations,

and while it

did not endorse

the conservative

five start limit, it recommended

that caution

be applied.

The inspector

noted that the vendor's

guidance

was provided in September

1994,

and did not appear

to have

been provided to all licensees.

The

MOV

maintenance

engineering

section leader stated that while case-by-case

recommendations

had

been provided,

the vendor

had not provided consistent

generic guidance

to all facilities.

The section leader stated that

he would

pursue developing appropriate

generic

g'uidance for the evaluation of the

MOV

users

group.

These

recommendations

would then

be passed

to the vendor for

implementation.

The inspector

found these

actions to be appropriate

and will

follow the licensee's

actions during routine inspection.

4.4

Contamination

on Valve Stem

Unit 2

During

a routine tour of outage

work in the Unit 2 auxiliary building, the

inspector

noted

some boric acid contamination

on the valve stem of the "8" low

pressure

SI

pump miniflow valve.

The inspector

noted that the valve stem area

was not identified as

a contaminated

area.

The inspector

asked

the

technicians

working on the valve actuator if they informed

a radiological

protection

(RP) technician that the contaminated

area

needed

to be marked.

The technicians

stated that they were

aware of the contamination,

but did not

think it was necessary

to inform the

RP technician

and

have the area

marked.

The inspector

informed

an

RP technician of the situation

and the, contamination

was surveyed

and properly marked.

The inspector

concluded that although the technicians

were using good

RP

practices

to keep themselves

from getting contaminated,

they were not

sensitive of the

need to identify the contamination

to minimize the potential

for other workers to get contaminated.

The inspector discussed

this

observation with the valve services

section leader

who agreed that the

technicians

should

have

been sensitive to the broader

issue of identifying and

marking contaminated

areas.

The section leader stated that this observation

would be discussed

during industry events training.

The inspector

concluded

that these

actions

were appropriate.

4,

~

l

4.5

EDG Ins ection

Unit 2

On February

7, the inspector

observed

engineering

perform boroscope

inspections

of the Unit 2

EDG

8 as part of the

18 month

EDG inspection.

Based

on these

inspections,

engineers

recommended

that seven cylinder heads

be

removed

so that the cylinder liners

and pistons

could

be inspected.

The inspector

observed

the mechanical

maintenance

EDG team remove the cylinder

heads,

replace

several

liners

and pistons,

and reassemble

the affected

components.

The inspector

observed

excellent work practices

by the

EDG team

in the area of foreign material

exclusion control, identification and control

of removed parts,

cleanliness,

and work package

usage.

The inspector

also

observed

good communications

and

team work between

the maintenance

and

engineering

groups.

4.6

Other Maintenance

Observations

~

,

Uninterruptible

Power Supply for Emergency Lights for Safe

Shutdown

Monthly

PM

Unit 3

~

Nitrogen Supply Valve Replacement

for Steam Generator

Atmospheric

Dump

Valve Control

Unit 3

t

~

MOV Actuator Gear Replacement

- Unit 2

5

EFFECTIVENESS

OF LICENSEE EQUALITY ASSURANCE

(40500)

The inspector

reviewed

an audit performed

by the

NA - Maintenance

organization

of maintenance activities.

The audit was performed in November

1994.

The

inspector

noted that the audit identified weaknesses

in the quality of MI and

the training provided to those

who write the instructions,

The audit included

corrective actions to address

these

weaknesses.

As noted in this

and recent

inspection reports,

inspectors

identified similar weaknesses

in the quality of

MI.

The audit team also identified weaknesses

in the implementation of the

preventive maintenance

basis

program

and in the identification, evaluation,

and documentation

of 10 CFR Part 21 reportability and root cause of failure

analysis

requirements.

The audit also

assessed

the significance of the

findings and outlined corrective actions.

The inspector determined

the licensee's

audit was performed

by

a multi-

discipline team,

including individuals from the maintenance

organization.

The

inspector

noted that the audit report represented

a change

in format from

previous audit reports

in that it was focused

on inspection findings

and

captured

planned corrective actions.

While the overall length of the report

was substantially shorter

than previous audits, primarily since it did not

j

I

-15-

capture audit planning detail,

the inspector

found the audit findings were

presented

in an easy to follow format, allowing the reader to focus

on the

results.

6

SURVEILLANCE OBSERVATION

(61726)

6. 1

Inte rated

Safe

uards Testin

Unit 2

On February

6,

1995,

the inspector

observed

sections of Surveillance

Procedure

73ST-2DG02,

Class

lE Diesel

Generator

and Integrated

Safeguards

Surveillance

Test

Train B.

The inspector

noted that the test director

demonstrated

strong

knowledge of the test procedure

and expected

plant

response,

and that the control

room supervisor maintained

strong

command

and

control of the unit.

The inspector

noted

good communications

between

engineering,

operations,

and other members of the test

team during the

performance of the test.

The inspector

noted

some minor weaknesses.

Although independent

verifications

had

been

performed,

they had not been adequately

documented.

In addition, the

inspector

observed

several

instances

during the restoration of the plant

equipment

at the conclusion of the test where the operators

would manipulate

plant equipment,

but not announce

the expected

alarms to the crew before the

alarms occurred'he

inspector notified the shift supervisor of the

weaknesses

and the shift supervisor

subsequently

addressed

the weaknesses

to

the operating

crew during the next preevolution brief for safeguards

testing.

The inspector

concluded that the shift supervisor's

corrective actions

were

adequate

and that the overall performance of the integrated

safeguards

testing

was good.

6.2

Other Surveillance

Observations

~

Emergency

Safeguards

Features

Actuation System

Subgroup

Relay Testing

Unit

1

7

PLANT ENGINEERING

(37551)

7.1

Steam Generator Modifications Put

on Hold

On February

13,

1995,

the licensee

decided that modifications planned

on the

Unit 2 steam generators

would not be performed

as

scheduled

during the Unit 2

refueling outage.

Preparations

for the modifications, involving the extension

of the

steam generator

feed rings

and divider plate,

were underway

when the

modification was put on hold.

The licensee

made the decision to stop the

modification after they had identified weaknesses

in the modification

calculations

performed

by the vendor,

Combustion

Engineering.

The licensee

had found that the vendor

had not accurately

modeled the steam generator

geometry.

j

-16-

The inspector determined

the licensee

engineering

had aggressively

pursued

questions

developed

during their review of the modifications.

When answers

to

these

questions

demonstrated

weaknesses

in the vendor's analysis,

the licensee

lost confidence that

a definitive resolution could

be reached

by the

end of

the Unit

2 outage.

The inspector

noted the licensee's

decision to put the

modification on hold was conservative

and demonstrated

good quality

engineering.

As

a result of the weaknesses

in the vendor's

analyses

supporting the steam

generator modifications,

the licensee

plans to perform

an audit of the vendor.

In addition,

the licensee

put

on hold plans to install the

steam generator

modifications in the Unit I refueling outage,

scheduled

to begin

on April 1.

7.2

EW Radiation Monitors

As discussed

in Section 3.2 of this report,

in April l994, the licensee

had

taken'he

process

radiation monitors

(RU

2 and 3) for the

EW system out of

service

by closing the inlet and outlet isolation valves to establish

a

seismic/nonseismic

code break.

The inspector

reviewed this decision

and other

related activities concerning

EW system configuration control.

The inspector

found significant weaknesses

in the historical control of

EW system

configuration

as

we11

as

weakness

in how the

EW system configuration

was

controlled at the time of the inspection.

7.2. I

Ori inal

S stem Desi

n

The

EW system

includes

two closed cooling trains which are cooled

by the

ultimate heat sink spray

pond system,

The

EW system provides safety-related

cooling to the shutdown heat

exchangers

and the essential

chilled water heat

exchangers.

It also provides

backup cooling to other nonvital radioactive

systems

such

as spent fuel pool cooling

and the reactor coolant

pumps.

Normal

cooling to those

systems,

supplied

by the nuclear cooling water

system,

is

isolated

from the

EW system in an event.

Each

EW train was provided with a surge tank to allow for changes

in pressure.

Level transmitters

on the surge

tanks were provided to control solenoid

operated

valves

For makeup to the

EW system from the preferred

nonsafety-related

demineralized

water

and the backup safety-related

condensate

transfer

(CT) system.

Each train of the

CT system

was designed

to provide

approximately

50

gpm of makeup

from the condensate

storage

tank

(CST).

The

CT

system also

was designed

to provide makeup to the

EDG

JW cooling surge tank

and to the essential

chiller cooling system.

The

EW radiation monitors,

RU

2 and

RU 3 were installed in the

EW system to

meet

10 CFR Part 50, Appendix A, General

Design Criterion 44, cooling water

system requirements

for leakage detection.

The Updated

Final Safety Analysis

Report,

Section 9.2.2,

stated that to detect

leakage,

high and low level

alarms for the surge tank

and the radiation monitors provided leakage

detection.

The NRC's Safety Evaluation Report stated that each train of

EW

'

I

)

0

-17-

was provided with a "continually operating radiation monitor which alarms in

the control

room

.

RU

2 and

RU

3 were initially installed

as nonseismically qualified.

Flow

orifices in the inlet and outlets of the

RUs were used to reduce

EW system

leakage

in the event the

RUs failed following a seismic event.

A calculation

performed in 1984, prior to plant operations,

demonstrated

that worst case

leakage

through the

RUs would be

on the order of 12.5

gpm and, therefore,

within the capacity of CT makeup.

A similar calculation

had also

been

performed to demonstrate

that the failure oF nonseismic

pump discharge

pressure

instruments

would also

be within the capacity of CT system

makeup.

7.2.2

Historical Design

Changes

The inspector

found that the licensee

did not recognize,

until 1993, that the

operability oF the

EW system

depended

on the operability of the

CT system.

During this period,

the

CT system

was

removed

from service

and the

EW system

was not declared

inoperable.

Additionally, in 1992,

the licensee

disabled

the

ability of the

CT system to provide automatic

makeup to the

EW system.

According to the design

basis for the

EW system at the time, both trains of

EW

could have

become

inoperable within 7 minutes of a seismic event.

The licensee

then developed

a preliminary evaluation that the

EW system

would

have

remained intact following a seismic

event

and was not inoperable with CT

makeup unavailable.

However,

some

issues

are still unresolved.

Based

on the

significance of the issue,

the inspector

performed

a thorough review of the

design

change history for the

EW and

CT system

and noted weaknesses

in

operability and safety evaluations,

timely resolution of engineering

issues,

and reportability evaluations.

The following is

a summary of the significant evaluations

and resulting

system

changes

since

1992

on the

EW and

CT systems:

~

In 1992 the licensee

documented

a concern

in

CRDR 9-2-0122 regarding the

indicated level in the

CST versus

the minimum level referenced

in

Technical Specification (TS) 3.7. 1.3.

TS 3.7. 1.3 required that

CST

level

be

"

.

.

. at least

25 feet

(300,000 gallons)."

The licensee

determined that due to instrument

loop accuracies

and errors in the

assumption for the lower instrument tap,

a level of 29.5 feet

was

needed

to assure

a volume of 300,000 gallons.

The licensee

determined that

CST

levels

had

been routinely maintained

above 29.5 feet.

As corrective

actions,

administrative limits were placed to maintain

CST level

above

29.5 feet.

To resolve

CRDR 9-2-0122

and to reserve

CST volume for decay heat

removal,

the licensee

evaluated

the demands

placed

on

CST volume by

systems

supplied

by the

CT system.

In the review of the

EW system,

the

licensee

focused

on

a

1988 concern

regarding unreliable

excess

flow

(

l

l

l

I

-18-

check valves

used

as the seismic/nonseismic

code break point for

EW

surge

tank level instruments.

The review did not address

either the

system radiation monitors or the

pump discharge

pressure

instruments.

The evaluation

concluded that,

even with failed excess

flow check

valves,

the

EW system would not lose sufficient volume to impact

EW pump

net positive suction

head before operators

could take mitigating action.

In

a July

1992 resolution,

to preserve

CST volume, the licensee

decided

to isolate

CT makeup to the

EW system

by closing

a manual

valve.

In Hay 1993,

as part of the design

basis

review project,

the licensee

identified that the

RUs

and

pump discharge

PIs,

which were both not

seismically qualified, would provide

a worst case

leakage of 31.5

gpm

following a seismic event.

The immediate disposition of the evaluation

of this issue

CRDR 9-3-0422

was to isolate the

RUs

and PIs.

However,

within a few weeks,

engineering

reopened

the isolation to the

RUs based

on engineering

findings that the

RUs could probably

be seismically

qualified and that there

was

a low probability of an earthquake

in the

six months estimated for resolution.

The PIs remained isolated

and are

opened

only to support testing.

In April 1994,

the licensee initiated

CRDR 9-4-0271 to address

the

unresolved

seismic qualifications identified in

CRDR 9-3-0422.'ne

of

the immediate actions of the

CRDR was to isolate

RU

2 and

RU 3.

A

subsequent

review was initiated to either resolve the seismic

qualification of the

RUs or to abandon

them in place.

As compensatory

measures,

the licensee initiated routine sampling of the

EW system.

Disabling the

RUs was performed in accordance

with a

10 CFR 50.59 safety

evaluation.

The inspector

noted the following weaknesses

during this review of these

problem evaluations

and resolutions.

7.2.2.1

Operability and Safety Evaluation

Weaknesses

The inspector identified the following weaknesses

in the operability and

safety evaluations

that were performed:

k

The disposition of CRDR 9-2-0122 to isolate the automatic

CT makeup

failed to account for the original

EW system design

basis

which required

CT makeup.

Specifically, the evaluation did not consider the nonseismic

RUs

and PIs.

The decision to isolate automatic

CT makeup

was

a poor resolution for

the problem as identified in

CRDR 9-2-0122,

regardless

of engineering's

failure to consider

the nonseismic

RUs and PIs.

Since the calculations

demonstrated

that

CT makeup to the

EW system would have

had

no effect on

EW system operability and little impact

on

CST volume,

a better

resolution would have

been to leave the system aligned "as-is,"

'

f

-19-

The immediate disposition of CRDR 9-4-0271

was to isolate

RU 2 and

RU 3.

The change

was supported

by

a

10 CFR 50.59 evaluation

(94-0091).

The

evaluation

noted that manual

sampling would be initiated to detect

leakage of radioactive fluids into the

EW system.

However,

the

inspector

noted that the evaluation did not specifically address

the

replacement

of an automatic

system with a manual

system.

The inspector

considered

that

a thorough evaluation

would have

addressed

the frequency

of sampling

needed

to compensate

for an automatic

system

and the

availability of other leakage detection,

such

as the

EW surge tank level

instruments.

7.2.2.2

Operability Evaluations

At the

end of the inspection period,

the licensee

had not completed

an

evaluation to determine

whether the system would have

remained intact.

While

it appeared

that the

RUs could

be qualified in the "as-is" configuration,

modifications

had

been

performed to the PIs to be considered

seismically

qualified.

This would indicate that the PIs could have failed following a

seismic event.

The licensee,

during their reviews of both

CRDRs 9-3-0422

and 9-4-0271,

identified that the issue

was "potentially" reportable.

In a corrective

actions audit,

performed in December

1994,

NA identified that this was

one of

three

examples of issues

which had not received appropriate

followup

reportability reviews.

They noted that there

was

no tracking mechanism to

ensure that once the engineering

evaluation

was performed,

a final

reportability evaluation

was performed.

An action item was subsequently

opened

and

was being tracked.

The inspector

noted that,

as

a result of the

NA audit,

and findings associated

with a special

inspection

(NRC Inspection

Report 50-528/95-08;

50-529/95-08;

50-530/95-08),

the licensee

has initiated actions to improve reportability

training

and

enhance

the evaluation

process.

The inspector

considered

the

operability evaluation of this issue to be

an Unresolved

Item (530/9503-01).

7.2.2.3

Slow Resolution of Technical

Issues

CRDR 9-3-0422

was initiated May 1993,

and identified that the

RUs need to

either

be seismically qualified or abandoned

in place.

At the

end of the

inspection period,

22 months later, the licensee

had not resolved this issue.

Between

May 1993

and April 1994,

the licensee

operated with the

RUs in

service.

While the decision to valve the

RUs back into the system

was

consistent

with the guidance

provided in Generic Letter 91-18 regarding

ODs,

qualification should

have

been reestablished

in a timely manner.

The

inspector

found

11 months to be

an excessive

length of time to operate without

full qualification.

0,

1

~

-20-

The

RUs were

removed

from service

in April 1994.

The inspector

noted that

during the latter part of 1994

and early 1995,

engineering

made sporadic

progress

to resolve the qualification issue.

Although engineering

recommended

that the monitors

be abandoned,

operations

management

recommended

that they be

returned

to service.

While progress

appeared

to be

made

and

a March

1995 goal

was set,

the inspector considered

the eleven

months to be excessive

time to

resolve

the issues.

7.2.2.4

Licensee Corrective Actions

The inspector discussed

these

issues

with engineering

management.

As

a result

of the inspector's

review, the licensee initiated

a

CRDR to evaluate

the

issues

identified.

The inspector

noted that several

of the

key issues

, identified in this review had

been

addressed

to

some extent

by corrective

actions for similar issues.

~

In Nay 1994,

the licensee

implemented

an

OD proc'edure

implementing

the guidance

provided in

GL 91-18.

~

As previously noted,

the licensee

has initiated improvements

in

reportability assessments

through program enhancements

and

training.

In October

1994, the licensee

implemented training and procedure

improvements to address

weaknesses

in 10 CFR 50.59 evaluations.

In response

to several

issues

concerning timeliness

and thoroughness

of

engineering

resolution of plant deficiencies,

since August

1994,

engineering

management

has

implemented

a "Level 1" issue resolution

program,

and

has

conducted training

on the attributes of "Engineering

Excellence."

P

The inspector will review the licensee's

evaluation of this issue

and proposed

corrective actions

in a future inspection.

7.3

Current Confi uration

The inspector's

review of

EW issues

was initiated after

a weak procedure

step

was not properly followed by plant operators

(see

Section 3.2 of the report).

Theinspector

reviewed the plant configuration

and plant procedures

to

determine if there were other inconsistencies.

The inspector determined that

the control

room annunciator

response

procedure for a low surge tank level did

not indicate that automatic

makeup

from the

CT system

was disabled.

In

addition, it did not indicate

how to align the

CT system.

While the procedure

did reference

alternate

makeup

from the nonsafety-related

sources, it did not

identify the

CT system

as

a source.

t

The inspector

noted this weakness

to the system engineering

section leader.

The inspector also questioned

whether,

based

on the design basis

review

-21-

conducted after 1992,

whether it was still appropriate

to maintain the

CT

makeup isolation valve closed.

The section leader stated that this would be

reviewed

as part of the

CRDR initiated to review the

EW configuration issues.

8

PREPARATION

FOR REFUELING

(60705)

af REFUELING ACTIVITIES

(60710)

8.1

Refuelin

Activities Unit 2

On February

12,

1995,

the inspector monitored portions of the core offload

of Unit

2 from the refueling machine inside containment.

The inspector

noted

that the refueling senior reactor operator

(SRO)

was present

on the refueling

machine.

The inspector questioned

the

SRO about the refueling machine

operations

and

TS requirements

and determined that the

SRO had strong

knowledge of refueling activities.

The inspector

observed

good

and continuous

communications

between

the refueling

SRO

and the control

room.

The inspector

noted the foreign material

exclusion controls for re.ueling operations

were

adequate.

The inspector

concluded that the licensee

demonstrated

several

strengths

in the performance of the core offload.

9

FOLLOWUP OP ERATIONS

(92901)

9. 1

Closed

Violation 50-529 93-48-02:

Failure to Follow Procedures

for

Reactor Coolant

S stem

Hakeu

This violation involved the failure to return the reactor

makeup water

controller to automatic following a dilution evolution.

On November

23,

1993,

the inspector

noted that the reactor

makeup water controller was left in

manual

when the procedure directed

the operator to place the controller in

automatic following manual

operation.

The primary operator

subsequently

placed

the controller to automatic

when informed by the inspector.

As documented

in

NRC Inspection

Report 50-528/94-20;

50-529/94-20;

50-530/94-20,

the inspector

reviewed the licensee's

corrective actions

and

left this item open after finding that the licensee

had

made

a procedure

change for Unit 2 regarding the operation of the reactor

makeup water

controller,

but had not made similar changes

to procedures

in Units

1 and 3.

Subsequently,

the inspector

confirmed that the applicable

procedures

in

Units

1

and

3 had

been

changed

and closed this item.

10

FOLLOWUP - MAINTENANCE

(92902)

10. 1

Steam Generator

Nozzle

Dam Air Hoses

The inspector

reviewed

CRDR 9-4-0107 which indicated that fittings for steam

generator

nozzle

dam air hoses

were improperly procured.

The air hoses

were

used to inflate seals

in the nozzle

dams.

Specifically, the substitute

fittings were procured

as nonquality-related

items,

and their acceptability

was not evaluated

before use.

The nozzle

dams

were classified

as quality-

related

components.

l

-22-

Prior to the Palo Verde Unit 3 midcycle outage

which began

in November

1993,

contractor

personnel

noted that hose fittings for steam generator

nozzle

dams

were difficult to use.

A member of the licensee's

refueling services

group

found

a substitute fitting and contacted

a representative

from the nozzle

dam

manufacturer

regarding

the acceptability of the substitute fitting.

The

licensee

employee

took action to procure

new fittings after being told by the

manufacturer's

representative

that the substitute fitting was acceptable.

However,

a Material Engineering

Evaluation to justify the acceptability of the

new fitting was not performed.

The fittings were procured

as nonquality-

related

even

though the nozzles

dams

were classified

as quality-related.

Procedure

87DP-OMC09,

" Item Procurement

Specification Requirements,"

which

applies

to quality-related

components,

indicates that

a Material Engineering

Evaluation is to be performed to justify the acceptability of substitute

items.

The nozzle

dams,

with the substitute

hose fittings, were

used during the

Unit 3 midcycle outage.

The quality classification of the fittings was

questioned

in February

1994 during

a Unit 2 midcycle outage.

The licensee

promptly initiated the

CRDR and performed

a Material Engineering

Evaluation.

The licensee

determined that the substitute fittings were acceptable

for

continued

use.

In addition,

on February

24,

1994,

the nozzle

dam manufacturer

provided written confirmation that the substitute fittings were acceptable

for

use,

The safety significance of this issue is low in that the fittings were

determined

to be acceptable,

and the nozzle

dams were designed with multiple

inflatable seals,

including

a mechanical

seal, for redundancy.

The inspector

found that the licensee

thoroughly documented this issue

and took appropriate

corrective actions,

includi'ng counseling

the individual who procured

the

fittings.

In addition,

the inspector

reviewed the licensee's Bill of

Materials database

and determined that'he

parts for the air hose

assemblies,

including the substitute fittings, were classified

as quality-related.

11

FOLLOWUP ENGINEERING/TECHNICAL SUPPORT

(92903)

Il.l

Closed

Violation 50-528 93-40-06:

Overtime Limit Exceeded

This violation occurred

when

an individual exceeded

the work hour limitations

of the TS.

The inspector

also found that licensee

audit teams

had identified

other instances

where work hour limitations had

been

exceeded,

and the

inspector

concluded that additional

management

attention to this matter

was

warranted.

On November 3,

1993,

a stop work notice

was issued to departments

with

recurring problems

in exceeding

work hour limitations.

The stop work notice

prohibited the departments

from taking exceptions

to overtime limitations and

remained

in effect until the Director, guality Assurance

(now Nuclear

Assurance),

was satisfied that corrective action plans

were developed

to

address

the problem.

Corrective Action Report 93-0179

was issued for this

matter

and

was subsequently

superseded

by

CRDR 9-4-0070.

Initial corrective

I

I

l

~

e

~

-23-

actions

included:

adding overtime limitation requirements

to general

and

continuing employee training, revising the administrative

procedure for

overtime limitations,

and improving the computer

report which identifies

overtime violations.

The inspector

found that the licensee

continues

to implement corrective

actions for this issue

and that senior licensee

management

is involved in

determining corrective actions.

NA trends

the number instances

where overtime

limits have

been

exceeded,

and the inspector

found

a declining trend in these

events.

Additionally, the majority of these

occurrences

were later determined

to be invalid due to errors in entering data from time sheets.

Currently, the

licensee

plans to develop

a

new time sheet

to ensure

consistent

reporting of

overtime

and to improve employee

awareness

of work hours.

The inspector

concluded that the licensee

has placed sufficient priority on

this matter to allow closure of this item.

The inspector will review the

licensee's

continuing corrective actions

in

a future inspection.

12

ON-SITE REVIEM OF LICENSEE EVENT REPORTS

(LERs)

(92700)

12. 1

Closed

LER 529 94-01

Revision 0:

EDG and Attendant

E ui ment

~inn erabl e

This licensee identified event occurred

when operations

personnel

did not

declare

an

EDG inoperable after the circuit breaker for the diesel

generator

building essential

exhaust

fan was

opened during maintenance activities.

The

fan was attendant

equipment to support continued diesel

operation.

At the

time of the event,

the licensee

had not implemented

a written procedure for

ODs.

Shortly after this event,

the

NRC issued

a violation to the licensee for not

declaring the low pressure

safety injection system inoperable

when

a low

pressure

safety injection

pump breaker

was

opened during

a surveillance test

(NRC Inspection

Report 50-538/94-12;

50-529/94-12;

50-530/94-12).

This

occurrence

was similar to the event with the essential

exhaust

fan in that the

licensee

disabled

equipment

and planned for manual

actions to restore

the

equipment if it was needed for operation.

Corrective actions for the

LER included issuing

a night order to operations

personnel

which indicated that the

EDG is inoperable if the breaker for the

essential

exhaust

fan is opened.

Subsequently,

the licensee

implemented its

operability determination

procedure.

The inspector confirmed that copies of

the operability determination

procedure

were maintained

in each control

room.

The inspector

found that each unit's operability determination

logbook

included

a determination that the

EDG would be declared

inoperable if the

essential

exhaust

fan breaker

was

opened.

Also, the inspector

spoke with

control

room personnel

and found the personnel

to be familiar with the

operability determination

procedure,

when credit can

be taken for manual

~ gl

I

I

i

actions to restore

equipment,

and in particular, this event.

The inspector

concluded that the licensee's

corrective actions for this event were

appropriate.

l~

ATTACHMENT 1

1

Persons

Contacted

1. 1

Arizona Public Service

Com

an

R. Fullmer, Department

Leader,

Nuclear Assurance

D. Garchow, Director, Site Engineering

B. Grabo,

Section

Leader Compliance,

Nuclear Regulatory Affairs

M. Hodge,

Group Leader,

Design Engineering

W. Ide, Director, Operations

AD Krainik, Department

Leader,

Nuclear Regulatory Affairs

J.

Levine, Vice-President,

Nuclear Production

D. Mauldin, Director, Maintenance

C.

Seaman,

Director, Nuclear Assurance

W. Simko,

Department

Leader,

Nuclear Assurance

R. Stroud,

Regulatory Consultant,

Nuclear Regulatory Affairs

J. Velotta, Director, Training

1.2

NRC Personnel

K. Johnston,

Senior

Resident

Inspector

J.

Kramer,

Resident

Inspector

A. MacOougall,

Resident

Inspector

t

1.3

Others

R. Henry, Salt River Project Site Representative

All personnel

listed

above

attended

the exit meeting

held

on March 3,

1995.

2

EXIT MEETING

An exit meeting

was conducted

on March 3,

1995.

During this meeting,

the

inspectors

summarized

the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed

by,

the inspectors.

op

I

I

0

I

gO

ATTACHMENT 2

ACRONYMS

AFW

CRDR

CST

CT

EDG

EW

FDT

HPSI

JW

MFW

MI

MOV

NA

OD

PI

RP

SI

SIT

SRO

TS

auxiliary feedwater

Condition Report/Disposition

Request

condensate

storage

tank

condensate

transfer

emergency

diesel

generator

essential

cooling water

failure data trending

high pressure

safety injection

jacket water

main feedwater

I

maintenance

instruction

motor-operated

valve

Nuclear Assurance

operations

determination

pressure

instrumentation

radiological protection

safety injection

safety injection tank

senior reactor operator

Technical Specification

V

e

~l

,f,

I

I