ML17310B147
| ML17310B147 | |
| Person / Time | |
|---|---|
| Site: | Palo Verde |
| Issue date: | 03/15/1994 |
| From: | Wong H NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| To: | |
| Shared Package | |
| ML17310B145 | List: |
| References | |
| 50-528-94-02, 50-528-94-2, 50-529-94-02, 50-529-94-2, 50-530-94-02, 50-530-94-2, NUDOCS 9403310071 | |
| Download: ML17310B147 (62) | |
See also: IR 05000528/1994002
Text
APPENDIX B
U. S.
NUCLEAR REGULATORY COMMISSION
REGION
V
Inspection
Report:
50-528/94-02
50-529/94-02
50-530/94-02
.
Operating Licenses:
NPF-51
Licensee:
Arizona Public Service
Company
P. 0.
Box 53999, Station
9082
Phoenix,
AZ 85072-3999
Facility Name:
Inspection At:
Palo Verde Nuclear Generating Station
Units 1, 2,
and
3
Maricopa County, Arizona
Inspection
Conducted:
January ll through February
14,
1994
K. Johnston,
Senior Resident
Inspector
H.
F} eeman,
Resident
Inspector
J.
Kramer,
Resident
Inspector
A; MacDougall, Resident
Inspector
B. Olson, Project Inspector
J. Winton, Intern
Approved By:
ong,
C se
Reactor
Projects
Branch II
> i<fp
ate
Soigne
Ins ection
Summar
Areas
Ins ected
Units
1
2
and
3
Routine,
announced,
resident
inspection
of:
~
Plant events
(inspection procedure
93702)
~
Plant activities
and operational
safety verifications
(71707)
~
Maintenance activities
(62703)
~
Surveillance activities
Units
1 and
2 (61726)
~
Diesel
Generator
problems
(61726,
62703,
71707)
snspectson,
chemical cleaning,
and tube plugging (62700,
42700,
37703,
73753,
62703,
92701)
Review of Employee
Concerns
Program
(92720)
94033i007i 9403i6
ADOCK 05000528
8
)
Training and gualification Effectiveness
(41500)
Follow-up on corrective actions for Violations (92702)
Follow-up of previously identified items
(92701)
Follow-up of Licensee
Event Reports
(92700,
90712)
Results
Units
1
2
and
3
Strengths:
Plant management
responded swiftly to inspector-identified
concerns
regarding worker performance
in the radiological controlled area
(RCA).
Comprehensive
corrective actions
were initiated following the initial
notification of the issues to first-line supervisors
(Sections
3.1
and
4.2).
Unit
1 operations
personnel
thoroughly reviewed
a plant protection
system circuit problem, demonstrating
a questioning attitude throughout
the review (Section 5.2).
Weaknesses:
A Unit 2 contract
employee
removed his security badge
and dosimetry
and
placed it on
a nearby transformer while working inside the protected
area
and within the
RCA (Section 3. 1).
In addition, the inspectors
found that plant personnel
did not consistently display their security
badges
and dosimetry
as required
by plant procedures
(Section 3.2).
Maintenance
personnel
demonstrated
poor radiological practices
while
working on
a main turbine control valve (Section 4.2).
~
The inspectors
observed
several
examples of poor plant material
condition
and in several
of these
instances
the deficiencies
had not
been previously identified by the licensee
(Sections
3.3
and 6.5).
~
Engineering
was slow to evaluate
the cause of cracks
observed
in the
valve bodies of two Unit 2 containment isolation valves
(Section 4.3).
~
The removal
from service of a emergency diesel
generator jacket water
system automatic valve without a documented
review, despite
the fact
that its function was described
in detail in the
FSAR, indicated that
the licensee's
review of degraded
plant conditions
was weak (Section
6.4).
Summary of Inspection
Findings:
~
Violation 50-529/94-02-01
was identified (Section 3. 1)
~
Follow-up items 50-529/94-02-02
and 50-528/94-02-03
were opened
(Section
3.3.1)
l
Violations 50-529/93-04-02,
50-529/93-35-02,
and 50-529/93-40-4
were
closed
(Section 10).
~
Follow-up items 50-530/93-11-5
and 50-529/93-55-01
were closed
(Section
11).
~
Licensee
event reports
50-530/93-03
(Section
12)
and 50-528/93-04,
revision
1 (Section 13), were closed.
Attachment:
Persons
Contacted
and Exit Heeting
f
DETAILS
1
PLANT STATUS
1.1
Unit
1
Unit
1 operated
throughout the inspection period at essentially
85K'ower.
On
January
17,
1994, Unit
1 experienced
a 250 megawatt
load shed
due to the
in southern California.
The steam
bypass
control
system
responded
to maintain plant power and all systems
responded
normally during the event.
On January
26,
1994, the licensee
determined that three of the four
atmospheric
dump valve
(ADV) linear variable differential transformers
(LVDT)
had
been in-service longer than their qualified life.
The licensee
determined
that the failure of the
LVDT would not affect the operation of the
ADV or
prevent operators
from determining the position of the ADV.
The licensee
documented their evaluation in a justification for continued operation.
At
the
end of the inspection period,
one of the three
LVDTs had
been replaced.
On February
7,
1994,
the licensee
detected
small
amounts of radioactive
tritium in the secondary
system.
On February 8,
1994, the licensee
installed
anion resin paper in the Steam Generator
No.
2 downcomer
sample line and
measured
small
amounts of radioactive iodine which confirmed
a very small
primary-to-secondary
leak.
Based
on the tritium levels in the steam
generators,
the leak rate
was less
than
1 gallon per day
(GPD).
At the
end of
the inspection period, the licensee
was closely monitoring the tritium levels
and the leak rate was.staying
constant
at less than
1
GPD.
1.2
Unit 2
Unit 2 began the inspection period in Node
5 starting
a mid-cycle steam
generator
tube
eddy current inspection
and chemical
cleaning outage.
The
licensee
reduced
the reactor coolant system level to mid-loop to facilitate
the installation of steam generator
nozzle
dams in preparation for eddy
current testing of the steam generator
tubes.
The
RCS level
was then raised
to a level just below the reactor vessel
and remained there throughout
the inspection period.
The licensee
completed
chemical
cleaning of the steam
generator
during the outage
(see Section 7.2).
The licensee
had completed
eddy current testing of steam generator
2-1
and was continuing
to test
2-2 at the
end of the period
(see Section
7. 1).
The
licensee
had identified
a significant number of axial crack indications in
2-2.
1.3
Unit 3
Unit '3 operated
throughout the inspection period at essentially
85 percent
power.
On January
19,
1994,
the licensee
gagged
closed
safety valve which had developed
a small seat leak.
Gagging
one safety valve
reduced
the Technical Specification
maximum allowable reactor
power to 98.2
percent.
I
t
l
1
J
ONSITE RESPONSE
TO EVENTS (93702)
2. 1
Hain Steam Isolation Valve Fast Closure
Unit
1
On January
20,
1994, during
a surveillance test to partial stroke the Hain
Steam Isolation Valves (HSIV), HSIV-170 fast-stroked full closed
and
immediately fast-stroked full open.
The plant responded
as follows:
~
Reactor coolant temperature
increased
about
one degree.
~
Primary system pressure
did not change.
~
The affected
pressure
increased
about
20 psig.
The licensee
declared
the "A" train of the hydraulic system for HSIV-170
HSIV-170 remained
since the "8" train of the hydraulic
system
was still available to operate
the valve.
The licensee
determined
the
cause of the event
was
a failure of the "C" solenoid valve in the "A" train.
This aligned hydraulic accumulator,
instead of the hydraulic pump, to the HSIV
operator
and fast-closed
the valve.
The solenoid valve was replaced
and
a
partial stroke test
was satisfactorily completed.
The inspector
reviewed the licensee's
troubleshooting of HSIV-170 and
concluded that the licensee's
response
to this event
was appropriate.
3
OPERATIONAL SAFETY VERIFICATION (71707)
The inspectors
performed this inspection to ensure that the licensee
operated
the facility safely
and in conformance with license
and regulatory
requirements
and that the licensee's
management
control
systems effectively
discharged
the licensee's
responsibilities for safe operation.
The methods
used to perform this inspection
included direct observation of
activities
and equipment,
observation of control
room operations,
tours of the
facility, interviews
and discussions
with licensee
personnel,
independent
verification of safety
system status
and Technical Specifications limiting
conditions for operation, verification of corrective 'actions,
and review of
facility records.
3. 1
Worker Removed Dosimetr
and Securit
Bad
e in Radiolo ical Controls
Area Protected
Area
Unit 2
On January
25,
1994, the inspector noted that
an individual was working inside
the protected
area
and within the radiological controlled area
(RCA) and was
not wearing his automated
controlled access
device
(ACAD) or dosimetry.
The
individual was
a contract worker involved in steam generator
chemical
cleaning
operations
(see Section 7.1).
The inspector
observed that the
ACAD and
dosimetry
was
on top of a nearby transformer,
approximately five feet from the
worker.
When the worker noticed the inspector looking at the
ACAD and
dosimetry
on the transformer,
he properly attached it to his body.
The worker
was working in the
pump trailer used for steam generator
chemical
cleaning.
The radiation levels in the trailer were subject to change
due to various
chemical
solutions
being
pumped through the trailer.
The inspector notified
l
t
l
the worker's supervisor of this observation.
The supervisor
subsequently
informed radiation protection
(RP)
and security.
Procedure
Revision 2, "Radiation Exposure
and Access Control,"
Step 3.2.3, states,
in part, that personnel will be issued dosimetry which
shall
be worn at all times within the
RCA.
Step 3.2.4.1 states,
in part, that
dosimetry shall normally be worn on the front of the body between the thigh
and head,
unless directed otherwise
by RP.
Procedure
20AC-OSK04, Revision 9,
"Protected/Vital
Area Personnel
Access Control," Step 3.2. 1, states,
in part,
that
ACADs shall
be displayed
by all .individuals while inside Protected/Vital
areas
and shall
be positioned
on the front of the outermost
garment,
between
the neck
and the waist,
photograph
side out.
The failure of the employee to
follow procedures
is
a violation of Technical Specification 6.8.1 (Violation
50-529/94-02-01).
The licensee initiated Condition Report/Disposition
Request
(CRDR) 2-4-0041 to
evaluate this problem.
The licensee
also performed
an exposure
evaluation of
the worker.
The worker's
TLD was read
and the area
he had worked in was
surveyed.
Based
on the survey,
a maximum unmonitored
exposure of 0.003
mrem
could have
been received
by worker.
The
RP Department
denied the employee
further access
to the
RCA.
In addition, the Security Department
performed
a
check to verify that unauthorized
use of the worker's
ACAD had not occurred
and that the
ACAD had not left the worker's sight.
The Security Department
also
removed the employee's
unescorted
access
to the protected
area.
Further,
the contractor for chemical
cleaning held training for all of its employees
to
re-emphasize
the licensee's
expectations
in security, radiation protection,
and job performance.
The inspector
noted that the licensee's
response
to this event
was thorough.
In particular,
the inspector noted that the licensee
took prompt action to
assess
the incident
and took action when it was brought to the attention of
first line supervision
by the inspector.
3.2
Dosimetr
Securit
Bad
e Placement
On February
7,
1994, the inspector
observed
a licensee
maintenance
individual
entering the Unit 3 radiologically controlled area
(RCA) wearing the
dosimetry/security
badge (i.e.,
ACAD) hanging off the right front pant's
pocket.
The dosimetry at Palo Verde is attached
to the security badge.
The
individual moved the
badge to the torso after the inspector questioned
a
radiation protection technician whether this was the correct location for the
dosimetry.
Later, the inspector
noted that there were other personnel
wearing
their dosimetry in similar locations inside the
RCA.
As noted in Section 3. 1 of this report,
the licensee
procedures
required that
dosimetry shall normally be worn on the front of the body between
the thigh
and
head
unless
otherwise specified
by Radiation Protection
(RP).
The
licensee's
procedure for personnel
access
control required that the security
badge
be displayed
on the front of the outermost
garment,
between
the neck and
'the waist.
Additionally, the procedure
required that all personnel
report any
unbadged
personnel
in the protected/vital
area.
Although the badge location
probably did not affect the measured
whole body dose reading in these
cases,
s
I
I
I
.
)
the inspector
noted that the improper location of the badge
could hamper
proper identification by security.
The licensee
acknowledged
the problem
and committed to have all managers
and
supervisors
review with their employees
the proper location for the dosimetry
and security badge.
Additionally, the licensee
noted that they would review
the differences
in the requirements for security
badge
placement
and dosimetry
placement to determine if a change
was needed.
Finally, the licensee
committed to review employee training/retraining to determine if the location
was properly defined.
The inspector .considered
these corrective actions to be
adequate.
3.3
Plant Material Condition
3.3.1 Unit 2 Hi
h Pressure
Safet
In 'ection
Pum
During a routine plant tour, the inspector
observed that large boric acid
formations
had formed at both ends of the
2A pump.
The acid formation
was apparently
due to pump seal
leakage.
The licensee
responded
by issuing
a
work order
and
had the
pump cleaned.
The licensee
stated that the seals
were
scheduled for replacement
in the next refueling outage
and every subsequent
third refueling outage.
The inspector reviewed the Updated Final Safety Analysis Report
(UFSAR)
and
determined that Section 6.3. 1.3.N.l.a states,
in part, that the maximum HPSI
pump seal
leakage
allowed is 100 cc/hr.
Although unable to determine
the
extent of the
pump seal
leakage
since the
pump was in standby
mode,
the
inspector
noted that the licensee
had performed the Technical Specification
surveillance
inspection of emergency
core cooling system
(ECCS) leakage
(TS 4.4.5.2. 1) during the refueling outage in August 1993.
The purpose of this
test
was to verify that there
was less
than
1 gallon per minute leakage of the
ECCS equipment outside containment providing long-term,
post loss-of-coolant-
accident recirculation.
The seals
had
no identified leakage during the
performance of this test.
Based
on the observation of a number of other boric acid leaks in
pumps
and valves
and the fact that the licensee
did not attempt to quantify leaks
as
they developed,
the inspector questioned
the basis of the
UFSAR pump seal
leakage
requirement
and whether the
TS surveillance
was adequate
to verify
compliance with the requirement.
The inspector will review the licensee's
response
to these
questions
during
a future inspection
(Followup item 50-
529/94-02-02).
3.3.2 Unit
1 Malkdown
During
a routine tour of Unit 1, the inspector identified
a small
steam leak
from a drain valve in the supply line to the steam-driven,
pump
and packing leaks from both condensate
transfer
pumps.
The inspector
reported
these conditions to the shift supervisor
who was not aware of the
deficiencies.
Unit
1 mechanical
maintenance
personnel
evaluated
the
conditions
and determined that the steam leak was unisolable
and that
a leak
repair
had
been previously attempted.
A new work order was written to attempt
1
1
another leak repair.
The inspector noted that
a work order
had
been
previously written to adjust the packing
on one of the condensate
transfer
pumps.
However, the other packing leak had not been identified and
a work
order was written to repack the
pump.
At the
end of the inspection period,
the packing
was replaced
and the steam leak and packing adjustment
on the
other
pump were included in the 12-week work schedule.
3.3.3 Conclusions
In addition to the conditions discussed
in the above sections,
the inspectors
noted several
other minor material condition problems during routine
walkdowns,
such
as boric acid leaks in pump
and valve packings
and lube oil
leaks
on pump bearings.
Upon followup, the inspectors
found that several
of
these conditions
had not been previously identified by the licensee.
The
inspectors
noted that the licensee
does not require that maintenance
tags
be
placed
on equipment
when
a maintenance
request
has
been initiated.
As
a
result, it is not obvious to plant personnel
who observe plant deficiencies
whether
a deficiency
has
been previously identified.
Because of this,
personnel
would need to verify whether the deficiency had already
been
identified and, if not, initiate documentation
of the problem.
The additional
verification work could
be
an obstacle for plant personnel
to identify new
plant problems.
The inspectors
discussed
these
observations
at the exit meeting.
The licensee
management
noted that significant efforts had
been
made in the
1990
1991
time frame to improve the plant's material condition.
Nevertheless,
they
conceded that progress
may have slowed
and committed to review their plant
material condition program.
4
MAINTENANCE OBSERVATIONS (62703)
During the inspection period, the inspectors
observed
and reviewed the
selected
maintenance
and activities listed below to verify compliance with
regulatory requirements
and licensee
procedures,
required quality control
department
involvement,
proper use of safety tags,
proper equipment
alignment
and
use of jumpers,
personnel
qualifications,
appropriate radiation worker
practices,
calibrated test instruments,
and proper post-maintenance
testing.
Specifically, the inspectors
witnessed
portions of the following maintenance
activities:
4.1
Atmos heric
Dum
Valve Positioners
Unit
1
On February 3,
1994, the inspector
observed
the calibration of the air
positioner for atmospheric
dump valve
(ADV) 178.
The inspector
reviewed the
maintenance
procedure,
discussed
the history of ADV maintenance
problems with
the system engineer,
and noted the steps
operators
took to declare
ADV-178
operable following maintenance.
The inspector
noted that the licensee
has
had several
problems with early
failures of the
ADV positioners
since
1992.
Plant engineering
conducted
a
thorough evaluation of positioner failures in 1992
and
1993.
These
evaluations
provided
sound
recommendations
to improve the reliability of the
I
'
I
I
positioner.
The inspector also noted that the
ADV calibration procedure
incorporated
vendor recommendations
and adequately
demonstrated
the
performance of the
new positioner.
However, surveillance test
(ST) 41ST-
1SG05,
"ADV Nitrogen Accumulator Drop Test,"
has not been consistently
performed
as
a retest to ensure operability of the
ADV.
4. 1. 1 Histor
of Positioner Maintenance
On January
3,
1994, operators
performed
a nitrogen system pressure
drop test
on ADV-178.
The positioner leak rate
was measured
at 0.9 standard
cubic feet
per minute (scfm).
This was higher than the normal leak rate of 0.6 scfm
(some
amount of leakage
through the positioner is required for the positioner
to function).
The licensee
determined that if the positioner leakage
increased
to about
1.0 scfm, the overall nitrogen
system would probably not
meet the pressure
drop test requirements.
On January
21 the licensee
replaced
the positioner
and performed successful
pressure
drop
and functional tests.
On January
30, operators
performed
a functional test of ADV-178 and
discovered that it failed the 30 percent
open response
time requirements.
The
licensee
determined that ADV-178 failed this test
due to excessive
positioner
leakage.
CRDR 1-4-0038
was written to determine
the cause of the January
30
failure of the positioner.
On February 3, the licensee
replaced
the positioner for ADV-178 with a newer
model.
The manufacturer
redesigned
the internals of the positioner to provide
more surface
area to "grip" the diaphragm.
The positioner for ADV-178 was the
first of 12
ADV positioners on-site to be replaced with the
newer
model.
The
licensee
planned to replace the older style positioners with the
new models
when they fail or when they reach the
end of their qualified life.
4. 1.2 Performance of A
ro riate Retest
On February 3, the shift supervisor declared
ADV-178 operable after the
technicians
successfully
completed the positioner calibration.
During the
final review of the work order,
the shift supervisor
recognized that
surveillance test
"ADV Nitrogen Accumulator Drop Test," should
have
been performed prior to declaring
ADV-178 operable.
The drop test
had
not been listed in the retest portion of the work package.
The drop test
was
immediately performed
and satisfactorily completed.
The licensee
determined that 41ST-1SG05
was not consistently
used
as
a retest
to ensure operability of the ADV.
At the conclusion of the inspection,
the
licensee
was conducting
a review to determine whether the retest
was required
and the significance of not performing the test.
CRDR 1-4-044
was initiated
to evaluate
the condition.
The inspector will review the results of the'CRDR
in a future inspection report (Followup item 50-528/94-02-03).
4.2
CV-3
Assembl
and Restoration
Unit 2
0
On February
4,
1994, the inspector
observed
contract'maintenance
employees
performing work on
Portions of the Unit 2
secondary
systems
were being controlled
as radiologically contaminated
areas
1
J
0,
1
,I
!
~
i
I
1
0
as
a result of the
1993 steam generator
tube rupture event.
The inspector
oted the following weaknesses
in the worker's radiation protection practices:
Upon the inspector arrival in the work area,
the foreman reached
across
the radiological controlled area
(RCA) boundary
and offered to shake the
hand of the inspector.
The inspector verified that the foreman
had
been
instructed during general
employee training that reaching
across
an
boundary
was not
an acceptable
radiological practice.
~
An employee,
while working in
a, radiologically contaminated
area,
retrieved
a tool that
had
been
dropped
across
the contaminated
boundary
without ensuring that radiation protection
(RP)
had
been notified and
without ensuring that radiological conditions
had not changed.
Coincidentally,
an
RP technician,
who had just arrived at the job site,
observed
the workers retrieve the tool.
The technician
surveyed the
area
where the tool
had been
and determined that there
had
been
no
spread of contamination.
The inspector brought these
observations
to the attention of the
a Unit 2
maintenance
foreman.
In response,
the licensee
held
a stand-down
meeting
on
February 7, with all site mechanical
personnel
assigned
to the turbine deck.
The briefing included
a representative
from RP who discussed
radiological
work
rules
and
how to treat radiation boundaries.
In addition, licensee
management
detailed their expectations
regarding radiological work practices.
A second
- tand-down
and briefing was held for the remainder of the crew that
came of
shift on February 9.
Additionally, the licensee
planned to conduct detailed,
pre-job briefings prior to performing activities inside contaminated
areas
or
when work activities require personnel
to be
on both sides of radiological
boundaries.
The inspector
noted that the increased
attention given to radiological work
practices
on the turbine deck
and concluded that the licensee's
corrective
actions
were appropriate.
4.3
S stem
Sam le Line Isolation Valves With Internal
Cracks
Unit 2
On January
27,
1994, Unit 2 maintenance
workers identified cracking in the
valve bodies of two reactor coolant
system
(RCS)
sample line valves.
The two
valves,
SSAUV-203 and
SSBUV-200, were the containment isolation valves for the
RCS loop
1 hot leg sample line.
Maintenance
workers
had
been inspecting the
valves to determine
the cause of seat leakage.
The cracks
were internal to
the valve body and circumscribed
the seat
area.
However, it did not appear
that the cracking could have
caused
the seat
leakage.
The licensee
determined that there were
a total of six containment isolation
valves in each unit which are similarly-designed
and in similar service
conditions.
The licensee visually inspected
the inside of a third Unit 2
valve and did not observe
cracks.
A licensee
review of the past maintenance
history on these
eighteen
valves
and the industry history, did not identify
other examples of cracking problems.
0
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The licensee
developed
an action plan to (1) remove
SSAUV-203 and
send it to a
laboratory for fracture
mode analysis;
(2) remove
SSBUV-200
and conduct on-
site ultrasonic testing
(UT); and,
(3) cut SSBUV-200 into quarters
and perform
visual
and microscopic examinations
following the ultrasonic testing.
The
licensee initially planned to
UT the
15 valves that had not been visually
i'nspected.
However,
when they performed the
UT of SSBUV-200, they were not
able to characterize
the extent of the cracking.
As
a result, they determined
that
UT of the remaining
15 valves would not provide useful information.
By February
14,
SSAUV-203 had not been delivered for inspection to the
independent
laboratory.
The licensee
had decided not to perform destructive
examination of SSBUV-200 until the other valve had
been delivered.
As
a
result,
the cause of the cracking
had not been determined.
The inspector
noted at the exit meeting that while the initial action plan was well
developed,
the progress of this investigation
had
been slow.
Licensee
management
concurred with this assessment
and noted that the valve had
subsequently
been delivered
and that they expected
a more timely resolution of
the issue.
5
SURVEILLANCE OBSERVATION (61726)
The inspectors
reviewed this area to ascertain
that the licensee
conducts
surveillance of safety-significant
systems
and components
in accordance
with
Technical Specifications
and approved
procedures.
5.1
Reactor Protection
S stem
Res
onse
Time Testin
Unit 2.
On February 3,
1994, the inspector
observed
portions of surveillance test
(ST)
"RPS Matrix Relays to Reactor Trip Response
Time Testing," in
Unit 2.
For most of the plant protection
system
(PPS)
instruments,
Technical Specification (TS) 3.3. 1 requires that the total channel
response
time to be
less
than
1. 15 seconds.
TS 4.3.1.3 also requires that
one channel
of each
function be tested
at least
once every
18 months.
The total response
time is measured
in the following three steps:
~
Procedure
measured
the process
equipment
response
time [i.e.,
the time from the process transmitter (e.g. pressurizer
pressure)
to the
PPS cabinet].
~
Procedure
measured
the
PPS cabinet
response
time (i.e., the
time from the
PPS cabinet to the matrix relays).
~
Procedure
measured
the response
time from the matrix relays
to the reactor trip breaker opening.
The inspector
concluded that the these surveillance
procedures
adequately
demonstrated
that the overall response
time requirements
of TS 4.3. 1.3 were
satisfied.
Additionally, the inspector
rioted that procedure
was
well written and that the technicians
used
good communications
during the
performance of 36ST-9SB44.
11
I
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I
The inspector reviewed the data collected during the performance of 36ST-9SB41
completed
on Harch 26,
1993;
completed
on August 16,
1993;
and
during the inspector's
observation of 36ST-9SB44
on February 3,
1994.
In
addition, the inspector reviewed calculation
13-JC-SB-02 to determine the
basis for the acceptance
criteria provided in these surveillance tests.
The
purpose of this review was to verify that the overall time response
of the "B"
channel
high and low pressurizer'pressure
trips were within the
TS requirement
of 1. 15 seconds.
Based
on these
reviews the inspector
concluded that, the
TS requirement to
verify the "B" channel
pressurizer
pressure
high and low trip response
time
was satisfied;
the "B" channel
was tested within the 18-month period specified
in TS 4.3. 1.3; the overall process
response
time was satisfied
by meeting the
acceptance
criteria for each portion of the test;
and the calculation for the
acceptance
criteria contained
a large margin of safety
and the actual
response
times were well within the
TS requirement.
5.2
Plant Protection
S stem Functional
Test
Unit
1
On February
9,
1994, during the performance of surveillance test
"Plant Protection
System
(PPS)
Functional Test-Reactor
Protection
System/Engineered
Safety Features
Actuation System
(ESFAS) Logic," the
technicians identified
a problem which they believed to be in the test
circuit.
The inspector
observed that the technicians
immediately notified the
shift supervisor
and documented
the problem in the test log.
The shift
supervisor
and shift technical
advisor reviewed the test logic diagrams
and
agreed that the most likely cause of the problem was with the test circuit.
However, the shift supervisor
continued to question the technicians
and
contacted
the
I&C supervisor
and system engineer to ensure
a proper evaluation
was performed.
The system engineer
also thought the problem was in the test
logic portion of the circuit.
The
same step
was repeated
5 times
and the
proper response
was obtained.
The remaining portions of 36ST-9SB04
were
satisfactorily completed.
The licensee initiated
CRDR 1-4-0060 to trend the
spurious test circuit anomaly.
The inspector
concluded that the problem was appropriately
documented
and
that'he
shift supervisor aggressively
evaluated
the problem to ensure that the
performance of the
RPS was not affected.
6
DIESEL GENERATOR CONDITION AND TESTING (61726,
62703,
71707)
During the inspection period, the licensee
experienced
unanticipated trips of
an emergency diesel
generator
(EDG) in all three units.
Each of the trips
resulted
from a non-safety related
problem.
In each
case,
the inspectors
assessed
the licensee's
review and plans for corrective actions.
In addition,
this section discusses
a degraded
condition in the Unit
1 "B" EDG jacket water
system that was not thoroughly evaluated
by the licensee.
6. 1
Unit
1
Diesel
Generator
Reverse
Power Tri
Durin
Shutdown
Se
uence
I'n
January
25,
1994,
a reverse
power trip of the Unit
1 "B" EDG occurred while
operators
were securing the
EDG per procedure
"Emergency Diesel
12
!
I
Generator
B."
The
EDG was running to perform the weekly Technical
Specification surveillance test.
The inspector
concluded that the operator
correctly followed the procedure for securing
the
EDG.
Despite
weaknesses
in
the procedure
and
a lack of sensitivity by the operator concerning
the
potential for a reverse
power trip contributed to the event,
the inspector
c'oncluded that the licensee's
corrective actions
were appropriate.
Procedure
410P-1DG02 directed the operator to lower the generator
output to
less than 0. 1 megawatts
(HW), and then
open the generator
output breaker.
The
operator
lowered power to approximately 0. 1
MW and turned to discuss
the
evolution with a trainee.
When
he turned to trip the output breaker,
the
wattmeter still indicated 0. 1
HW and the
EDG tripped automatically
on reverse
power.
The licensee
inspected
the "B" EDG output breaker
and found no damage to the
breaker or the generator.
An evaluation of the event
was conducted
and
documented
in Condition Report/Disposition
Request
(CRDR) 1-4-0023.
The
licensee
concluded that the following factors
caused
the reserve
power
condition:
~
The operating
procedure directs the
EDG to be unloaded to 0. 1
HW, but
the megawatt meter is calibrated to only +/- 0.2
HW.
Operators
were not aware,
and
had not been trained, that the megawatt
meter in the control
room would show
a positive indication in a reserve
power condition.
The operator delayed tripping the output breaker;
however, there
are
no
precautions
in the procedure to ensure that the output breaker is
immediately opened after the load is reduced to 0.1
HW
Unit
1 operations
management
issued
a night order emphasizing
the need to
immediately trip the output breaker
when the
EDG is unloaded.
The night order
also discussed
the expected
response
of the megawatt meter during
a reverse
power condition.
In addition,
an Instruction
Change
Request
was initiated to
change
the
EDG operating
procedures
in all three units to lower the generator
output to 0.3
HW before opening the output breaker.
The inspector
concluded
that these
actions
appeared
to be appropriate.
6.2
Unit 2
Diesel
Generator Tri s
Due to Control Air S stem Problems
On January
30,
1994, the Unit 2 "B" EDG tripped after
10 seconds
of the
cooldown cycle of a surveillance test.
The licensee
reviewed the trip and
determined that it resulted
from the failure of a check valve in the
pneumatic,
non-safety related,
control air system.
The control air system
provides protective trips to the
EDG governor during maintenance
runs;
however,
these trips are
bypassed
during
a safety start.
The licensee
subsequently
repaired the check valve.
On January
31,
1994, during the post-maintenance
start of the "B" EDG, the
fuel racks closed before the
EDG reached
rated
speed,
and the diesel
13
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I
subsequently
tripped
on under-frequency.
Although the problem appeared
to be
caused
by the control air system,
the licensee
could not identify the
component
which caused
the failure. It appeared
that
a control air system
solenoid allowed the air to pass
through to the fuel racks and'close
them.
During an emergency
run of the diesel,
two emergency
solenoids
in series
would
have prevented
the trip by preventing the fuel racks'from closing.
The licensee restarted
the
EDG on February
1,
1994, with instrumentation
installed for troubleshooting.
However, the cause of the earlier trip was not
determined.
The licensee
determined 'that
a diesel start failure,. as defined
in the Technical Specifications,
had not occurred since the diesel
would have
started if required during an emergency.
The inspector
agreed with the
licensee
and concluded that
a start failure had not occurred during the
January
31,
1994, start of the
EDG.
6.3
Unit 3
Diesel
Generator
Overs
eed Tri
Durin
Shutdown
Se
uence
On January
26,
1994, the Unit 3
EDG "A" tripped
on overspeed
during
a post
maintenance
retest.
The diesel
was being retested
following planned
maintenance
and tripped immediately after the operator
depressed
the manual
shutdown button.
Depressing
the manual
shutdown button disengages
the
electrical
governor
and engine
speed
control is taken over by the mechanical
governor.
Engineering
and maintenance
troubleshooting
determined that the
mechanical
governor had'not controlled properly and that the problem was
- probably caused
by air in the governor's hydraulic control lines.
The oil in
'he
governor
had
been
changed previously as part of the planned
maintenance.
The licensee restarted
the
EDG, cycled the speed setting
on the manual
governor several
times,
and then performed
a normal
shutdown.
The inspector
compared
the procedure for changing the governor oil with the
vendor technical
manual.
The inspector concluded that the technical
manual
did not specify
how to change
the governor oil to ensure that the hydraulic
lines were not air bound.
The licensee
informed the inspector that they
intended to incorporate
the cycling of the mechanical
governor
speed control
into the oil change
procedure to prevent future problems with the governor.
The inspector
concluded that this action was appropriate.
6.4
Unit
1
Diesel
Generator Jacket
Water
Ex ansion
Tank Automatic Hake-u
Ca abilit
Disabled Without A
ro riate Review
During a system walkdown of the Unit
1 "B" EDG, the inspector noted that the
jacket water make-up
combined-header
stop valve,
1PDGBV013,
was shut.
There
was
a caution tag
on the valve 'indicating that the valve was closed
due to
leakage
past the solenoid-operated,
auto make-up valve.
With the jacket water
make-up valve closed,
the jacket water expansion
tank level could not be
controlled automatically.
The ability to automatically control level
was
described
in the Updated Final Safety Analysis Report
(UFSAR).
The inspector
reviewed the licensee's
work control processes
to determine
whether the licensee
had conducted
an operability evaluation of this
condition.
The inspector
found that the licensee
had not considered
the
automatic function described
in the
In addition, the licensee's
14
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C
screening
process for conducting operability evaluations of degraded
conditions
was narrowly focused
and did not include conditions
where automatic
functions described
in the current licensing basis
were removed.
The inspector
was concerned that the failure to include
an evaluation of the
r'emoval of automatic functions in the operability screen
process
was
a
significant weakness,
in that safety significant design
changes
to the plant
could be inadvertently performed without an appropriate operability
evaluation.
As discussed
which distributed
NRC
Inspection
Manual
9900, "Operability", it is important to evaluate
the
physical differences
between
the automatic
and manual
actions to ensure
the
change
does not alter the licensing basis for the plant.
Nevertheless,
the
inspector considered
that the safety, significance of this particular condition
was low because
the
EDG automatic jacket water make-up function was designed
as
an operator
convenience
and
was not needed to ensure
the proper operation
of the
EDG.
6.4. 1
De raded
Nonconformin
Condition
The inspector determined that the leaking jacket water auto make-up valve was
a degraded
condition
and reviewed the licensee's
program requirements
for
degraded
conditions described
in procedure
"Control of Degraded
and Nonconforming Material."
This document stated that
a work request
(WR) or
Condition Report/Disposition
Request
(CRDR) should
be used to report
a
degraded
condition.
The inspector
noted that
was written on
December
10,
1993,
which was the
same date that the auto make-up valve was
found leaking
and caution tagged.
The
WR was subsequently
canceled
on
December
15,
1993,
by the work planner.
The work planner
had initiated
CRDR
1-3-0208 in Narch
1993
based
on repeated
problems with the make-up valve
leaking.
The planner decided to defer the maintenance
and leave the jacket
water auto make-up valve isolated until engineering
completed this evaluation
(the action was
due in April 1994).
The inspector
concluded that the degraded
condition of the auto make-up valve was appropriately reported
and documented.
6.4.2
0 erabilit
Evaluation
The inspector
noted that Appendix
D to procedure
"Work Initiation,"
contained
a potential
impact screening
step
used to determine if a
MR required
additional
review by the shift supervisor.
Although the impact screening for
the jacket water auto make-up valve
WR was conducted
by an operations
evaluator
and
was not forwarded to the shift supervisor for an operability
determination,
the inspector
concluded that the operability decision
was
consistent
with the screening criteria.
The inspector further concluded that the guidelines for screening
WRs for
operability concerns
were narrow.
The guidelines'addressed
only those
situations
where Technical Specifications
(TS)
and associated
Limiting
Conditions for Operations
(LCOs) were obviously impacted
by
a degraded
condition.
In the case of the auto make-up valve, the evaluator
decided that
the loss of the automatic
make-up capability for the jacket water expansion
tank did not impact the operability of the
EDG.
This decision
was apparently
15
I
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1
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i
based
on isolating the jacket water auto make-up valve in the past
due to
similar problems with the valve leaking.
The inspector discussed
the design basis for the auto make-up capability with
the system engineers.
In July 1993,'during the evaluation of CRDR 1-3-0208,
the .system engineer
documented that the function of the automatic jacket water
make-up
system
was for operator
convenience
and not for design safety or to
minimize the impact of any postulated jacket water system failures.
When the
auto make-up valve was shut in December
1993, the operations
evaluator
was not
aware of the function of the valve described
in the
CRDR evaluation.
The
inspector
concluded that removing the automatic jacket water make-up
system
did not adversely affect the operation of the
EDG.
6.4.3 Licensee Actions
0
The inspector discussed
the weaknesses
in the operability guidelines with
licensee
management..
The licensee
had formed
a review group to develop
more
comprehensive
guidelines for operability determinations
based
on previous
NRC
concerns
(see
NRC Inspection
Report 50-528/93-12,
Paragraphs
13
and 17.b.).
At the exit meeting,
licensee
management
recognized that this issue
demonstrated
a vulnerability in their degraded
condition review process
and
indicated that the lessons
learned
would be factored into their operability
determination guideline development.
The inspector will continue to follow
the licensee's
progress
in this area during routine inspection.
6.5
Conclusions
At the exit meeting,
the inspector noted that while the problems resulting in
unanticipated
EDG trips and the degraded
condition of the jacket water system
in Unit
1 did not appear to be safety significant, they may be precursors
of
degrading
EDG condition.
In addition, the inspector
noted that
each of the
EDGs appeared
to have
numerous
minor lube oil, fuel oil, and air system leaks.
The inspector recognized
a licensee
management initiative to assess
the
trips to determine if there were
common problems which could affect
reliability.
Licensee
management
noted that in recent years there
had
been
increased
emphasis
in reducing
EDG out-of-service times.
This may have raised
the threshold for correcting minor system problems.
They stated that
an
assessment
of EDG maintenance
practices
and their affect of EDG reliability
would be performed.
7
STEAN GENERATOR INSPECTION,
CLEANING AND PLUGGING
7. 1
Edd
Current Testin
73753
7. 1. 1 Back round
and Pur ose
During this inspection,
the licensee
conducted
extensive
eddy current
inspections of the Unit 2 steam generators.
The licensee's
inspections
were
being performed to comply with commitments
made in their letter to the
NRC,
dated July 18,
1993.
The purpose of this inspection
was to determine if the
licensee
and licensee
contractors
had
been performing inspections,
data
0
16
analysis,
and inspection
scope
changes
in accordance
with licensee
procedures
and commitments.
7.1.2 Procedures
The inspector reviewed licensee
procedure
Eddy
Current Examinations,"
Revision
10, dated January
12,
1994.
The procedure
was
reviewed to determine if requirements
for bobbin coil and motorized-rotating
pancake coil
(HRPC) eddy current data analysis
and evaluation
had
been
defined.
The inspector
reviewed the .procedure
to assess
the licensee's
criteria for equipment calibration
and bobbin coil and
HRPC data discrepancy
resolution.
The procedure
was also reviewed to determine if the flaw
indications,
which were expected
by the licensee
in certain
areas of the steam
generator,
had
been identified.
The inspector
found that specific requirements
for bobbin coil and motorized-
rotating pancake coil eddy current data analysis
.and discrepancy resolution
had been
adequately
defined in the procedure.
The inspector also found that
equipment calibration
and particular types of flaw indications for each
section of each
area
had
been
adequately
defined in the
procedure.
The inspector
concluded that licensee
procedure
73TI-9RC01 included
requirements for bobbin coil
and motorized-rotating
pancake coil
(HRPC) eddy
current data analysis
and evaluation.
The inspector concluded that the
procedure
also included equipment calibration criteria,
bobbin coil and
HRPC
data discrepancy resolution criteria,
and descriptions of particular flaw
indications expected to be found in certain
areas of the steam generator
tubes.
7.1.4 Observations
The inspector
observed
licensee activities at four HRPC and two bobbin coil
data acquisition stations to determine if the licensee
had
been performing
and
recording data in accordance
with licensee
procedures.
The inspector also
reviewed
equipment calibration records.
The inspector
found
that the licensee
had
been performing the bobbin coil and
HRPC eddy current
tube examinations
in accordance
with licensee
procedure.
The
inspector also found that the licensee
had
been recording data
on approved
data sheets
and that eddy current inspection
equipment calibrations
had
been
performed
and were being checked
in accordance
with procedure.
The inspector also observed activities at four data analysis stations.
The
inspector
found that each of the four stations
had
a current technique
sheet.
The inspector noted that the eddy current operator
was utilizing frequencies
and mixes specified
on the technique
sheet for eddy current testing analysis
.in accordance
with procedure
Therefore,
the inspector
concluded
that licensee
personnel
had
been performing steam generator
tube eddy current
inspections,
data recording,
and data analysis
in accordance
with licensee
procedures.
17
I
Cal ibrati on
On January
31,
1994, during the licensee's
gA review of eddy current testing
work, the licensee identified that
4 of 36 eddy current calibration groups
exceeded
the four-hour limit for calibration verification.
This is
a
requirement of Procedure
Paragraph
8.3.3.
The licensee's
root-
cause
analysis identified several
reasons
that the calibrations
were not done:
~
In some cases,
the operator
was not examining
any tubes
when the four-
hour calibration requirement
was required.
In some cases,
the operator
was performing activities without problems
and simply lost track of the time requirement.
There
was
no mechanism
established
to remind the operator
when the 4-hour limit was
approaching.
In some cases,
as the four-hour limit approached,
the operator
had
problems getting the calibration completed.
The inspector noted that
calibration can often
be difficult to obtain.
The licensee's
corrective actions
included conducting
a stand-down
meeting of
eddy current personnel,
the use of a preset timing device to alert the
operator
when the four-hour time period is going to expire,
and having the
primary and secondary
data analysts
make
a report noting the beginning
calibration time and the ending calibration time.
This finding was licensee-
identified and appropriate corrective actions
were taken.
Stuck
HRPC Probe
During this inspection period,
a
HRPC probe
became
lodged in
tube.
This probe
was removed
by running another
probe in from the cold leg
and dislodging the struck'probe.
The root cause of this incident was that the
operator
was given
an incorrect tube number.
The programmer incorrectly
entered
the tube number, resulting in the acquisition operator probing the
. wrong tube.
The operator
was moving the
HRPC probe quickly to the desired
elevation;
however,
the probe
was inserted into the tube's
U-bend well before
that desired level (for the correct tube)
because
he was provided with the
wrong tube number.
As
a result,
the probe
became
lodged in the U-bend.
The licensee's
root-cause
evaluation identified human error in two areas.
First, the programmer entered
the wrong tube number,
and second
the person
responsible for checking that tube list against
the original list, failed to
note that
an incorrect tube
number
had
been entered.
Corrective actions
taken
included writing a procedure for programming
special
interest tubes,
such
as
this one.
Personnel
in data
management
had
a stand
down meeting to address
attention to details
and review the procedures for programming tubes.
7. 1.3
Sam lin
Hethodolo
and
Ex ansion Criteria
The inspector reviewed the licensee's
Unit 2 steam generator
sampling
methodology inspection plan.
The inspection plan was reviewed to determine if
18
e
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I
)
the licensee
included inspection
expansion criteria, historical
steam
generator
data from licensee
inspections
and other utilities, and loose part
monitoring.
The inspector
found that the licensee's
Unit 2 steam generator
(SG) sampling
plan included criteria for expanding the inspection
scope.
The inspector
noted that the licensee's
inspection
plan included:
~
a full tube length bobbin coil inspection of 4200 of the approximately
12,000 tubes
in the two Unit 2 steam generators,
an
MRPC inspection at the top of the tubesheet for 2283 (in
SG 2-1)
and
2203 (in
SG 2-2) of the hot leg tubes,
and
approximately
1800 tubes in the upper bundle area (in the arc of
interest that analysis
indicates to be most susceptible
to free span
cracking)
from the first vertical support to the
08H support.
The inspector also found that the licensee's
inspection
plan included previous
tubing indications
found in Palo Verde steam generators
and problems
identified by other utilities, vendors,
and the
NRC.
The inspector
concluded that the sampling methodology
used to develop the
inspection
plan included the areas
necessary
to provide information needed to
ascertain
the condition of the steam generators
tubes.
The inspector
found
the sample
expansion criteria used to be satisfactory.
7.1.5 Ins ector
and Anal st's
uglification
The inspector
reviewed licensee qualification and certification requirements
for steam generator
eddy current inspectors
and data analysts.
Licensee
requirements
for steam generator
eddy current inspectors
were included in
licensee
procedure
The inspector reviewed approximately thirty eddy current
and analysis
personnel
qualifications.
The inspector found that licensee
and contractor
personnel
qualification and certification records
were up-to-date
and that the
inspectors
or analysts
were qualified in accordance
with licensee
procedure
The inspector also found that the licensee
and contractor
inspectors
were certified level I, II, or III in accordance
with American
Society for Nondestructive
Testing Standard
SNT-TC-IA.
7.2
Chemical
Cleanin
- Unit 2
37703
42700
62700
The inspector
reviewed the licensee's
preparations
for chemical
cleaning the
secondary
sides of the Unit 2 steam generators.
The primary purpose of the
chemical
cleaning
was to remove
tube deposits that could
become initiation sites for intergranular stress
corrosion cracking.
During
previous
eddy current testing of Unit 2 steam generators,
the licensee
observed
axial cracks in steam generator
tubes at locations where deposits
19
~
~
,l
'
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l
existed.
The licensee
contracted
with
BSW Nuclear Technologies
(BWNT) to
perform the chemical
cleaning operation.
The chemical
cleaning
process
used different solvents to remove magnetite
and
copper deposits
from the steam generator
internal surfaces.
The generic
process
solvents
were developed
by the Electric Power Research
Institute
and
the Steam Generator
Owners
Group
(EPRI/SGOG),
and the process
had
been
previously used at other nuclear facilities.
7.2. 1
Process
uglification
The inspector reviewed portions of ABB Combustion
Engineering
and
BWNT reports
which evaluated
steam generator materials,
determined corrosion allowances for
materials in contact with solvents,
and described
laboratory tests to
determine
the effectiveness
of the solutions for dissolving deposits.
Samples
of tubes previously removed
from Unit 2 Steam Generator
2-2 were
used in
portions of the laboratory tests.
As a result of the laboratory tests,
BWNT
modified the generic
EPRI/SGOG process to apply to Palo Verde Unit 2
conditions.
The inspector discussed
the qualification of the process
with
licensee
and
BWNT representatives.
The reports
provided
a detailed
background
of the process qualification and the individuals appeared
to be very
knowledgeable of corrosion allowances,
susceptible
materials,
and process
qualification testing.
The inspector
also reviewed
two 10 CFR 50.59 evaluations
prepared
by the
licensee for.the cleaning evolution.
One of the evaluations
indicated that
there
was
no plausible accident
which would result in the simultaneous failure
of more than
one chemical
container
and that
a spill of 55 gallons of ammonium
hydroxide
(one container)
would not affect control
room habitability.
During
discussions
with BWNT personnel,
the inspector learned that
up to four
containers
of ammonium hydroxide could
be moved at one time using
a forklift.
The inspector
commented to the licensee that moving four containers
at one
time could result in dropping
and failure of the containers,
which was not
reviewed in the
IO CFR 50.59 evaluation.
The licensee
subsequently
determined
that failure of four ammonium hydroxide containers
would not affect control
room habitability.
7.2.2
Process
Im lementation
BWNT supplied the equipment for performing the process,
and the inspector
walked
down the majority of the equipment which was located outside of
containment
in the radioactive
waste yard.
The inspector
observed that the
equipment
was in good condition,
components
were labeled,
and there
were
no
indications of leaks
from components that would carry chemical
solvents.
The
inspector
found that
BWNT equipment operators
and process
engineers
were
familiar with the operation of the equipment
and were familiar with the
overall process.
The inspector
observed
portions of pre-cleaning
system operational
testing
which was performed to verify equipment operation
and to ensure that
procedures
were appropriate.
The inspector
considered that the pre-cleaning
operational
testing
was beneficial in ensur'ing
successful
performance of the
20
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I
evolution.
The inspector reviewed portions of various procedures
used for the
evolution
and found the procedures
to be appropriately detailed.
The
procedures
had
been
approved
by the licensee,
and procedure
changes
were
made
in accordance
licensee
requirements.
The inspector discussed
the implementation of the process with various
licensee
organizations
including Operations,
guality Control, Radiation
Protection,
Chemistry, Fire Protection,
and guality Assurance.
The inspector
found that the organizations
were adequately
involved in preparing for the
process;
however, it appeared
that the licensee's
project manager
was not
receiving all of the comments or concerns
generated
by the organizations.
The
licensee
intended to conduct pre-evolution briefings for all involved
organizations
and
based
on comments
from the inspector,
the licensee
intended
to make procedure
changes
to ensure that licensee
organizations
were involved
in concurring to start the process.
7.2.
The inspector
observed that chemical spill kits, showers,
and
eyewash
stations
were staged
at various locations
and that
BWNT personnel
appeared
to be
knowledgeable of chemical
hazards.
The inspector discussed
contingencies
with
personnel
from the Palo Verde Fire Department
and found that personnel
had
been trained to respond to spills or a fire.
The inspector
found that
procedures
contained
contingency actions if chemistry results or corrosion
rates
were not in expected
parameters.
Licensee representatives
were assigned
to work with the
BWNT personnel
during
the evolution to provide coordination with licensee
organizations for both
normal or abnormal
operations,
and the inspector
found these
personnel
to be
knowledgeable of the process
and their assigned
duties.
The inspector
discussed
contingencies
for handling contaminated
solutions with
licensee
Radiation Protection
personnel
and with BWNT chemists.
The inspector
found that while licensee
personnel
expected
the solvents to become
contaminated
as
a result of the previous Unit 2 steam generator
tube rupture,
the
BWNT personnel
did not expect contaminated
solvents
based
on past
experience
at other facilities.
The inspector
commented that the expectations
of the licensee
and the contractor
appeared
to differ and that additional
coordination
may be needed to ensure that the contractor would be prepared
to
implement contingencies
imposed
by Radiation Protection.
As
a result,
the
licensee
revised the Radiation
Exposure
Permit for the process,
specified
Radiation Protection expectations,
assigned
additional technicians
to the job,
and worked with contractor personnel
to ensure that licensee
expectations
were
understood.
7.2.4 Chemical
Cleanin
Performance
The inspector
observed
portions of the chemical
cleaning operations
and
closely followed the licensee's
progress.
Overall, the inspector
observed
good operations
practices
and noted
good communications
between
BWNT and the
licensee.
However, the inspector
noted that
some activities
had not been
adequately controlled.
For example,
21
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l
During the transfer of equipment inside containment
from Steam Generator
2-1 to the Steam Generator
2-2,
one person
was sprayed with chemical
solution
on his clothing and another
person
was sprayed
in the face.
The leaking connection
was immediately reconnected
and the leak stopped.
The person
sprayed in the face
used the eye wash station to rinse his
face.
Both individuals exited containment,
and showered.
Neither
individual experienced
side effects from the solution.
The licensee re-
briefed all chemical
cleaning personnel
on the requirement to wear face
shields
and proper protective clothing when working with chemical
cleaning
systems.
Subsequently,
BWNT used
a large catch basis to
collect possible
leakage
and provided coverage
over connection
being
opened to reduce the possibility of spray.
~
On February ll, a spill of water and corrosion products occurred outside
the Unit 2 containment
hatch
when operators
aligned
a sludge lancing
tank to the chemical
cleaning
system.
The spill had resulted
from the
improper manipulation of one of the sludge lancing system valves.
The
BWNT operator did not have specific instructions to manipulate
the valve
and
was not cognizant of the system configuration.
The licensee
initiated procedure
changes
to ensure that sludge lancing valves are not
re-positioned
unless directed
by a supervisor.
~
The licensee fire captain,
the leader of the hazardous
material
response
team,
was called to respond to the February ll spill.
He had difficulty
determining
who was the
BWNT contact at the scene
and it took several
minutes for the captain to find the
BWNT contact.
As corrective action,
BWNT established
that the person in charge of the chemical
cleaning
operation
would be required to identify himself to the fire captain
upon
arrival of the hazardous
material
response
team.
(Note:
The spill that
occurred
on February
11 was subsequently
determined
not to be
a
hazardous
material.)
In addition, the inspector
noted that the licensee
responded
appropriately to
level indication problems
observed
during the chemical
cleaning.
The steam
generator
2-2 level
gage
was blown down with nitrogen several
times in
attempts to achieve
an accurate
level indication.
BWNT operators
monitored
the
amount of solution
pumped into the steam generator
and compared this with
the indicated level
and used the lower of the two indications
as the level.
This conservative
action ensured that the unanalyzed
metal portions of the
would not be exposed to cleaning chemicals.
Subsequently,
operators
determined that the top portion of the tube bundle
had not been
cleaned.
As
a result, the cleaning process
was increased
by 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />
so that
the top of the tube bundle could be cleaned.
To resolve the level inaccuracy
problems,
the licensee
planned to use the six-inch hand hole
as
a tap for an
attachment for the level instrument in the upcoming Unit 3 steam generator
chemical
cleaning.
The inspector
concluded that the licensee
response
to the events that occurred
during the chemical
cleaning of the steam generators
was adequate.
, 22
l
l
7.2.5 Results
Chemical
cleaning
removed approximately
5600 pounds of material
from Steam
Generator
(SG) 2-1
and approximately
5000 pounds of material
from SG 2-2.
The
bulk of the material
removed
was iron.
Other material
removed included
and small
and chromium.
Sludge
lancing subsequently
removed approximately
400 pounds of material
from SG 2-1
and approximately
500 pounds of material
from SG 2-2.
The licensee
found that the. levels
of. chromium in the corrosion products
removed resulted in the classification of the material
as mixed waste
(both
hazardous
and radioactive waste).
At the end of the inspection period,
the
licensee
was evaluating the waste to determine
the actions
necessary
for its
disposal.
The photographs
of the
SG tubes
were taken before
and after
cleaning.
The licensee
determined that chemical
cleaning successfully
removed
deposits
on the steam generator
tube surfaces:
The axial crack indications from eddy current testing
more prevalent after the chemical
cleaning.
2-1
had
no
appreciable
difference in the before
and after results of the
ECT.
At the
end
of the inspection period,
the licensee
and the
NRC's Office of Nuclear Reactor
Regulation
(NRR) were reviewing these results.
7.3.
Oconee
Tube Plu
in
Problems
The inspector
reviewed the possibility of a plug installation error occurring
at Palo Verde similar to the
one that caused
14 plugs to become dislodged
from
at Oconee Unit 3 in South Carolina.
The dislodged
plugs
were discovered
during
a refueling outage that
commenced
on January
2,
1994.
These plugs
had
been improperly installed during the August
1992 outage
by the
same contractor that performed the tube plugging at Palo Verde.
The contractor explained to the inspector that the plug-rolling tool
used at
Oconee
was
an older model than the one used at Palo Verde.
This tool used
a
flow verification assembly to monitor the air flow and air pressure
delivered
to the air motor which was
used to roll the plugs.
When the proper
amount of
air flow and air pressure
were reached,
the assembly
would stop the air flow.
However, this method did not measure
the actual
torque applied to the plug,
nor could it detect
problems in the rolling process
such
as
a misaligned tool.
The contractor
uses
the Delta roll expansion tool at Palo Verde.
The Delta
roll tool provides
an on-line feedback of the installation torque.
The
contractor developed
a torque trace
method using the Delta tool called
a "roll
energy" verification.
The roll energy verification integrated
the area
under
the torque verses
time curve which was proportional to the work applied to the
plug.
Because
the work applied to the plug was proportional to plug wall
thinning, it could
be used to determine
how well the plug was secured to the
tube.
Additionally, this method could reveal
improper lubrication, tool
alignment
and other problems
by changes
in the shape of the curve
and the
amount of time required to roll the plug.
The inspector
concluded that this
23
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i
method provided appropriate
assurances
that the plugs were adequately
secured
to the tubes.
8
REVIEM OF
EMPLOYEE CONCERNS
PROGRAM (92720)
As of January
26,
1994, the following statistics
were noted with regard to the
ECP files initiated by the licensee
during the last four years:
1991
1992
1993
1994
Number of ECP concerns
submitted:
Number of submitters:
Number of anonymous .submitters:
Number of concerns
assigned
outside
ECP:
Average length of time to close file (weeks):
Longest period file was
open
(weeks):
Number of concerns
substantiated:
Number of files remaining
open:
129
251
199
94
144
133
12
17
14
92
136
113
5
15
12
19
80
42
22
42
23
0
20
41
The inspector
reviewed the licensee's
ECP procedures,
a random selection of
ECP files closed within the last several
months,
and interviewed several
licensee
employees
who had submitted
ECP concerns.
The inspector
noted that
the licensee
has recently initiated
a comprehensive effort to reduce the
backlog of open
ECP files.
The inspector
noted the following concerns
in that
regard:
The licensee's
ECP procedure
(60AC-OQQ22) requires that
an
ECP file be
initiated for every concern received
by the
ECP group.
Historically,
this has resulted in a large
number of files being opened
and
independently
investigated
by the
ECP group which were not related to
nuclear safety,
which would more appropriately
be handled
by another
group.
The licensee
has
implemented
a program of screening
concerns
received
by the
ECP group,
and making
a determination
as to whether to
initiate an
ECP file or to refer the concern to another licensee
organization for resolution.
However, this
new screening
program
and
associated
new "initial contact form" has not been incorporated into the
ECP procedure.
As
a result the criteria for initiating an
ECP file are
not clearly or consistently defined,
nor are the bases for such
determinations
clearly or consistently
documented
or retrievable.
In one
instance,
the inspector noted that
a concern
received
on October
1,
1993,
involving inadequate
pre-maintenance
tailboard meetings
and poor ALARA,
appeared
to warrant opening of an
ECP file.
Hany
ECP files have
been closed without
a final closure letter being sent
to the concerned
employee,
as required
by the licensee's
ECP procedure.
ECP file 93-130-01,
which involved potential discrimination,
was closed
on the basis that the concerned
employee
requested
that the concern
be
withdrawn.
Based
on
a review of the employee's
concerns
and discussion
with the employee,
the inspector
concluded that the licensee failed to
properly resolve this concern.
As
a result,
the licensee
missed
a
l
significant opportunity to reenforce its stated
commitment to a timely
and discrimination-free resolution of employee
concerns.
In particular,
the involved employee stated that
he would not use the licensee's
program in the future because
he was convinced that licensee
managers
had
conducted
a "witch hunt" to identi.fy him as the alleger.
The employee
had only withdrawn his employee
concern
on the basis that
he had already
gone to his manager
and identified himself as the alleger.
The concerned
employee told the inspector that none of the managers
in the employee's
reporting chain or from the
ECP group had ever sat
down with him to
resolve his discrimination concern.
This failure has the potential to
created
a "chilling effect" that is likely to reach further than the
involved individual, since
he continues to interface with other licensee
employees
with the belief that
he was not properly treated.
~
The licensee
has
a long history of a high volume of both technical
and
discrimination concerns
coming into its
ECP program,
as well as having
the highest incidence in Region
V of substantiated,
employee
discrimination concerns
submitted to the
NRC and the Department of Labor.
~
ECP files involving substantiated
concerns
did not consistently
document
or reference
documents for tracking corrective action followup (e.g. file
93-010-01,
and 93-109-05).,
In the instance of file 93-109-05, it was not
clearly documented that the licensee
had thoroughly evaluated
the impact
of failed snubbers.
t
The licensee
acknowledged
the inspectors
comments
and stated that actions
would be taken to correct the problems
noted
by the inspector.
9
TRAINING AND QUALIFICATION EFFECTIVENESS
(41500)
In late
1993, the
NRC was
made
aware of concerns that the operators
at Palo
Verde could be reluctant to take actions in the simulator because
adverse
actions
would be taken against
them if they misdiagnosed
a problem.
In order
to address
this concern,
.an
NRC inspector interviewed five reactor operators
and five senior reactor operators
on January
26,
1994.
Four individuals were
from Unit 1, two from Unit 2,
and four from Unit 3.
Eight individuals clearly stated that they would always take appropriate
actions in the simulator or in the plant and that they were not influenced
by
a fear of adverse
actions if they misdiagnosed
a problem.
They all stated
they would take the correct actions.
One of the eight stated that
he
had
been
challenged
by personnel
from another facility concerning
"malicious
compliance" during the Palo Verde steam generator
tube rupture event,
but
clearly stated to that individual and to the ins'pector that
no "malicious
compliance"
was intended or occurred.
One individual stated
he would not hesitate
to take the correct actions,
both
in the simulator
and in the plant, but that requirements
for strict adherence
to procedures
in the past
had caused
him some fear.
He went on to state that
the manner in which the steam generator
tube rupture event
was dealt with by
procedures
was slow.
The operators
knew they had
tube
25
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J
rupture
and what they had to do, but were frustrated
by the plant procedures.
Although there
were
no safety implications, the delays
complicated
recovery
and cost the utility a lot of money.
The individual indicated that the
facility now recognizes
these
problems
and it appears
they are
headed
in the
correct direction (i.e., to give operators
reasonable flexibility). Starting
last year senior
management
has repeatedly
asked for operators'nputs
and
these
issues
have
been identified.
Regarding the delays complicating the recovery from the steam generator
tube
rupture,
the inspector
observed that, since the steam generator
tube rupture
event the facility has provided additional
guidance
and training to ensure
operators
can complete appropriate
emergency
steps early.
In October
1993,
the facility also committed to the
NRC to completely review and revise the
emergency
procedures
to make them more usable for the operators.
The.
inspector
concluded that these
two corrective actions
adequately
resolved the
operator's
concern.
One other operator stated that
he would make the best decision
he could and
follow through regardless
of what others
would do to him.
He did not have
any
specific problems in mind, but was concerned
about the constant
emphasis
on
accidents
and training far beyond the design-basis
events described
in the
Final Safety Analysis Report.
He felt that operators
may cause
problems
because
they were looking too hard for problems during
an uncomplicated trip
when there
were no problems.
The inspector discussed this issue with the operator,
but did not identify any
significant safety concerns.
The inspector
agreed that the scenarios
used for
training or testing
are often beyond the plant design basis,
but this provides
a safety margin for operators,
training,
and plant procedures.
The operator
did identify two procedure
steps
in emergency operating
procedures
which, to
be useful,
almost always
had to be completed early.
These
step directed the
sampling of the steam generators,
and restoration of power to non-vital
480
Volt AC busses.
The inspector
found that the planned revision of the
licensee's
emergency
operating
procedures
should help this problem,
and that
operators
had
been trained to complete steps early when necessary.
The
inspector
concluded that there
was
no need to correct existing training.
The inspector determined that all the individuals interviewed understood
the
facility policy for following procedures
and were confident they were
implementing these
procedures.
The operators
did not identify any safety
problems
and were aware of the emergency
p'rovisions of 10 CFR 50.54(x).
At the conclusion of the inspection the inspector discussed
the findings with
the Manager of Operations
Training
and the Vice President,
Nuclear Generation
to ensure
they were aware of the issues
raised
by the operators.
26
'
10
FOLLOWUP
ON CORRECTIVE ACTIONS FOR VIOLATIONS (92702)
10. 1
Closed
Violation 50-529 93-04-02: Fire Protection Test Procedure
not Followed
Unit 2
This violation was issued after
a fire protection technician failed to perform
a surveillance test in accordance
with the procedure.
The technician
performed procedure
steps out-of-order, did not establish
and maintain
communications,
and signed off restoration
steps prior to completing the
procedure.
The licensee
reviewed the incident
and determined that the violation was
caused
by personnel
error.
The technician believed that the requirement to
perform steps sequentially
was general
guidance
and that steps
could
be
performed in a different sequence if the objectives of the test
were still
being met.
The licensee
counseled
the technician regarding procedural
compliance.
Additionally, the licensee
briefed the entire fire department
on
the incident
and the need for procedural
compliance.
The inspector
concluded
that these
steps
were appropriate for this violation.
10.2
Closed
Violation 50-529 93-35-02: Failure of Offsite Safet
Review
Grou
to Review Abnormal Indication
Unit 2
This violation was issued
because
the Offsite Safety
Review Group
(OSRC)
failed to review abnormal
indications obtained during the third Unit 2
refueling outage in 1991.
The licensee
had discovered
one axial mid-span
crack and six axial cracks at the first. tube support.
Technical Specification 6.5.3.4f required the
OSRC (formerly the Nuclear Safety Group) to review
abnormalities
or deviations
from normal.
The inspector
reviewed the
licensee's
response
to the violation and determined that they were
appropriate.
The licensee
acknowledged that the abnormal
indications should
have
been
reviewed
by the
OSRC.
Following the tube rupture in Unit 2, the licensee
formed
task force, consisting of senior managers
and
engineers,
to evaluate
the failure.
The licensee
intended to develop the task
force into a permanent
group whose mission
was to identify and predict failure
modes
and determine
and implement strategies
to minimize steam generator
problems.
The licensee
stated that steam generator
group would make
a
presentation
to the
OSRC if steam generator testing revealed
a significant
deviation or abnormality, or the necessity for a reduced operating cycle.
The inspector
concluded that the licensee's
level of management
involvement in
the site's
and the formation of a permanent
group should ensure that future steam generator
problems
are addressed
by the
appropriate
level of management.
10.3
Closed
Violation 50-529 93-40-04: Surveillance Test
Administrative Procedure
Not Followed
Unit 2
This item involved operations
personnel
in Unit 2 not following the
administrative controls for surveillance testing documentation.
Specifically,
27
'
t
contrary to the administrative
procedure
governing surveillance testing,
operators
did not mark
a step unsatisfactory
during the performance of a
charging
pump surveillance or make
a test log entry documenting the problem.
The item also noted that the Unit
1 Operations
personnel
did not understand
when the administrative requirements for surveillance tests
were applicable.
This had resulted in a previous violation (Violation 50-528/93-26-01).
The inspector
reviewed the licensee's
response
to the previous violation in
NRC Inspection
Report 93-43
and noted that the licensee's
corrective actions
included forming a focus group to improve the overall surveillance testing
administrative procedure.
The inspector
noted that
an extensive revision to
the surveillance testing administrative
procedure
was issued in December
1993.
The inspector
reviewed the revision
and noted that Step 3.6.1 stated that
"...any failed step or out of tolerance
data shall
be identified by circling
the initialled space
or data entry."
The step also
has specific instructions
for notifying the operation's shift supervisor,
making
a test log entry,
and
initiating a work order or CRDR.
The inspector concluded that the revision to
the procedure clarified management's
expectations
for documenting
problems
during surveillance tests.
The inspector also noted
examples
in the field
(see Section 5.2 of this inspection report) where problems
noted during
surveillance tests
were properly documented.
11
FOLLOWUP (92701)
Closed
Ins ection Followu
Item 50-530 93-11-05:
Ma ne-Blast
Breaker
Ino erabilit
Close Latch
S rin
Interference
This item involved the inoperability of a safety-related
(GE)
Magne-Blast breaker
due to interference of the close-latch
spring with the
close-latch monitoring switch.
This item was left open to review the
licensee's
actions regarding
several
recommendations
listed in Condition
Report/Disposition
Request
(CRDR) 3-3-0152.
The licensee's first recommendation
was to issue
a plant change
request to
annunciate
any failure of the breaker closing springs to charge in the control
room.
Plant engineering initiated Plant
Change
Request
PCR 93-13-PB-001 in
July 1993.
The
PCR was approved
by the plant modification committee
on
January
24,
1994.
The modification will be prioritized and scheduled for
installation.
The licensee's
second
recommendation
was to issue
an engineering
evaluation
request
(EER) to permit the use of torsion type close latch springs
on
Magne-Blast Breakers.
EER 93-PB-004
was written to allow using the torsion
springs
as
a design equivalent
change
and directed the replacement
of the
older style springs during scheduled
breaker overhauls.
The licensee's
third recommendation
was for the licensee to obtain service
advice letters
(SALs)
and other information regarding the spring changes
from
the vendor,
The licensee
determined that
GE had not
issued
any SALs concerning
the new-style, close-latch
springs or any problems
with the springs that would prevent the charging of the closing springs.
28
I
I
The licensee's
last recommendation
was to revise all the applicable
maintenance
and surveillance
procedures
to ensure there
was sufficient
clearance
between
the spring
and the closing mechanism.
The inspector reviewed-
the overhaul
procedures
for the various types of GE magne-blast
breakers
(32HT-9ZZ37 through 32HT-9ZZ39)
and noted that steps
were included to ensure
a
minimum of 1/8-inch clearance
existed
between the spring
and the closing
mechanism.
On January
4,
1994,
NRC Information Notice 94-02 was issued describing this
event
and the potential
impact
on breaker operation.
The inspector
concluded
that the licensee's
recommended
corrective actions
were appropriately
implemented.
11.2
Closed
Ins ection Followu
Item 50-529 93-55-01:
Reactor
Coolant
S stem Flow Anomal
This followup item involved
a review of the licensee's
analysis of reactor
coolant system
(RCS) flow anomalies.
On the evening of January
6,
1994, with
Unit 2 at 85 percent
power, operators
noted that
RCS flow had dropped
approximately
2 percent
over the previous
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />,
as indicated
by the flow
instruments for all four reactor
coolant
pumps
(RCPs).
The operators
also
noted increases
in the differential pressure
across
the
(approximately
2
percent)
and across
the core (approximately
1 percent),
and increases
in
amperes
(approximately
5 percent) for all four RCPs.
These
RCS parameters
appeared
to have gradually changed
over
a 12-hour period
and then stabilized.
Reactor
power
and the
RCS hot leg and cold leg temperatures
did not change
appreciably.
The licensee
concluded that change in
RCS flow resulted
from the build-up of a
thin, rough layer of corrosion products
on the fuel rods.
The deposit of
corrosion products
appeared
to result from the planned reduction of RCS
lithium concentrations.
This reduced
pH and apparently
caused
corrosion
products in colder parts of the system to go into solution
and plate out on
the relatively hotter fuel rods.
The licensee
calculated that
a layer of
corrosion products
approximately 0.0003
inches thick could result in the flow
decrease
observed.
Prior to the flow anomaly,
operators
had
been reducing
concentration
in preparation for the mid-cycle outage.
This process
is used
to initiate a "crud burst" during
RCS cooldown that allows operators
to remove
RCS corrosion products through the chemical. and volume control system.
This
reduces
the radiation levels in the
RCS, particularly the steam generator
bowls.
The licensee
concluded that they had maintained
RCS chemistry within
industry established
guidelines.
However, the
which is proportional to boron concentration,
was high since the Unit was
early in its operating cycle.
Therefore,
the net change in lithium
concentration
and,
subsequently
RCS pH,
was. significantly greater
than
has
been typically experienced
during
a plant shutdown at the end of an operating
cycle.
The licensee
concluded that the change in
RCS flow did not impact plant
safety.
Throughout the anomaly,
core flow remained
above design flow as well
29
~ g
'
0
l
I
f
1
!
l
as Technical Specifications
minimum flow requirements
(95 percent of design
flow).
Additionally, the licensee
determined that core physics
parameters
had
not been affected.
The licensee
expects that normal
RCS chemistry controls
following plant restart will remove the layer of corrosion products
from the
fuel rods
and that
RCS flows should return to normal.
The licensee
discussed their analysis with the resident inspectors
and the
staffs of Region
V, and the
NRC's Offices of Nuclear Reactor Regulation,
and
Analysis
E Evaluation of Operational
Data during
a conference call
on
January
31,
1994.
Their analysis
was determined to be acceptable.
12
ONSITE REVIEW OF LICENSEE EVENT REPORTS
(92700)
12. 1
Closed
Licensee
Event
Re ort 50-530 93-03
Revision 0:
Emer enc
Diesel
Generator
Unable to Start
and
Run in the Manual Test
Mode
This
LER reported
an event where the "B" EDG in Unit 3 was not capable of
being manually started
from the control
room from July 3-10,
1993.
As
a
result,
the licensee
determined that the
EDG was inoperable
since the
Technical Specifications
(TS) requirement to start the
EDB in the manual test
mode could not have
been
performed during this period.
The inspector
conducted
a review of the event to determine the safety significance of not
being able to manually start the
EDG from the control
room.
The manual test
method of starting the
EDG is primarily used to verify the
engine is functional following maintenance
on the
EDG.
When the
EDG is
started in this mode, additional protective
shutdowns
are provided in case the
maintenance
introduced
a condition adverse to the safe operation of the
EDB.
The inspector determined that the
EDB could have
been started
manually using
the simulated loss of offsite power
(LOOP)
and simulated
emergency
safeguards
features
(ESF)
manual start buttons at the local
EDG control panel.
These
methods of starting are
used to test the design features
described
in the
safety analysis for the
EDB to start
on
a
Additionally, the
EDB was able to automatically start in the event of an
actual
LOOP or
ESF actuation.
The inspector
concluded that the safety significance of this event
was low
since the
EDG would have automatically started
as designed
and also could have
been manually started
from the local control panel.
13
IN OFFICE REVIEM OF LICENSE EVENT REPORTS
(90712)
LER 50-528/93-04,
Revision
1,
"ASHE Section
XI Testing of Charging
Pumps not
in Compliance with Code Requirements"
was closed
based on'n-office review.
30
'
l
ATTACHMENT
1
PERSONS
CONTACTED,
Arizona Public Service
Com an
- R. Adney,
- K. Akers,
- W. Chapin,
- R. Cherba,
R. Flood,
- R. Fountain,
- B. Grabo,
- W. Ide,
- J. Levine,
D. Hauldin,
J. Minnicks,
J.
Ong,
- G. Overbeck,
F. Riedel,
P. Rail,
- K. Roberson,
D. Robertson,
- C. Russo,
- J. Scott,
- C. Seaman,
H. Searcy,
- H. Shea,
- R. Stevens,
R. Stroud,
P. Wiley,
Others
Plant Manager,
Unit 3
guality Assurance
Manager,
Refueling
and Maintenance
Services
Manager, guality Audits
Plant Manager,
Unit 2
Supervisor,
guality Audits and Monitoring
Supervisor,
Nuclear Regulatory Affairs
Plant Manager,
Unit
1
Vice President,
Nuclear Production
Director, Site Maintenance
and Modifications
Manager,
ECP Program
ECP Investigator
Director, Site Technical
Support
Manager,
Operations,
Unit
1
ECP Investigator
Senior Engineer,
Nuclear Regulatory Affairs
ECP Investigator
Manager, guality'ontrol
Assistant
Plant Manager,
Unit 3
Director, guality Assurance
and Control
ECP Investigator
Manager',
Radiation Protection
Director, Nuclear Regulatory
8 Industry Affairs
ECP Investigator
'anager,
Operations,
Unit 2
- R. Henry,
- P. Luther,
Site Representative,
Salt River Project
Site Representative,
Public Services
Denotes
personnel
in attendance
at the Exit meeting held with the
NRC
resident
inspectors
on February
16,
1994.
2
EXIT MEETING
An exit meeting
was conducted
on February
16,
1994.
During this meeting,
the
inspectors
summarized
the scope
and findings of the report.
The licensee
acknowledged
the inspection findings documented
in this report.
The
inspectors
acknowledged that the licensee
had provided various proprietary
chemical
cleaning reports for NRC review.
The proprietary
information was subsequently
returned to the licensee.
31
C
1
P