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LER-1980-010, /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired |
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| 2441980010R03 - NRC Website |
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4 U. S. NUCLEAR REGULATORYCOMMISSION 80-010/03L-0 LICENSEE EVENT REPORT (CAR 1275)
QI (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 6 Qs
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1 QE~QE LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 NRC FC 366 I7.77) system.
This constitutes a degradation of a system designed to contain radioactive
~O3 material.
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Residual heat removal operation was continued through 6
a lternate discharge to RCS, and at lea st one steam generator wa s available CONTROL BLOCK:
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LICENSEE CODE 14 15 CON'T
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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO
~o2 During a unit'hutdown a pinhole leak tva s found in the weld of a thermowell on the RHR
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CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE F
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.
CODE TYPE NO.
Q17 REPoRT ~80
+
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0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB.
SUPPLIER MANUFACTURER
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S Q 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 5
The initial weld was of poor quality and is believed to be the reason for the leak.
The weld was repaired to current standards.
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80 80 80 45 80 80 80 NRC USE ONLY 68 69 80 Ts oN E 3 1 5 5 2 4 4 4 4 6, ext ~ 2 1 4 S. M. Spector NAME OF PREPARER 7
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FACILITY
~30 METHOD OF STATUS
% POWER OTHERSTATUS ~
DISCOVERY DISCOVERY DESCRIPTION Q32
~75 X
Q25 ~00 0
Q25 Crevice cleaninp
~AQOT Durinq operational tour 7
8 9
10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY~
LOCATIONOF RELEASE Q 6
~Z Q33
~ZQ34 NA NA 7
8 9
10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39
~00 0
QET Qss NA 7
8 9
11 12 13 PERSONNEL INJURIES 7
8 9
11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
~ZQ42 NA 7
8 9
10
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| 05000244/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000244/LER-1980-001-03, /03L-0:on 800118,while Performing PT-12.1, Emergency Generator 1A Would Not Accept Nameplate Steady Load Rating.Caused by Adjusting Governor Setting to Incorrect Value Indicated on Dynotape Sticker Setting Mod | /03L-0:on 800118,while Performing PT-12.1, Emergency Generator 1A Would Not Accept Nameplate Steady Load Rating.Caused by Adjusting Governor Setting to Incorrect Value Indicated on Dynotape Sticker Setting Mod | | | 05000244/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000244/LER-1980-002-03, /03L-0:on 800331,during Review of Special Instructions,Discovered That Time from Previous Boron Concentration Sample Exceeded 75 Days.Caused by Inadequate Guidance for Bimonthly Sampling Schedule.Schedule Changed | /03L-0:on 800331,during Review of Special Instructions,Discovered That Time from Previous Boron Concentration Sample Exceeded 75 Days.Caused by Inadequate Guidance for Bimonthly Sampling Schedule.Schedule Changed | | | 05000244/LER-1980-003-01, /01T-0:on 800414,during Steam Generator Inservice Insp,One Tube in a Steam Generator & 34 Tubes in B Generator Showed Pluggable Indications.Probably Caused by Concentration of Caustics in Crevices | /01T-0:on 800414,during Steam Generator Inservice Insp,One Tube in a Steam Generator & 34 Tubes in B Generator Showed Pluggable Indications.Probably Caused by Concentration of Caustics in Crevices | | | 05000244/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000244/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000244/LER-1980-004-01, /01T-0:on 800506,during post-installation Test of Reactor Vessel Head Vent,Dc Power Switches for Both Trains of Low Temp Overpressurization Protection Found in Off Position W/No RCS Vent Open.Cause Unknown | /01T-0:on 800506,during post-installation Test of Reactor Vessel Head Vent,Dc Power Switches for Both Trains of Low Temp Overpressurization Protection Found in Off Position W/No RCS Vent Open.Cause Unknown | | | 05000244/LER-1980-005-01, /01T-0:on 800603,during Performance of Monthly Verification Procedure,Loop a Accumulator Injection Circuit Breaker Found in on Position.Cause Not Stated.Breaker Returned to Off Position | /01T-0:on 800603,during Performance of Monthly Verification Procedure,Loop a Accumulator Injection Circuit Breaker Found in on Position.Cause Not Stated.Breaker Returned to Off Position | | | 05000244/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000244/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000244/LER-1980-006-01, /01T-0:on 800711,during Routine Analysis of Boric Acid Tank Samples,Concentration Exceeded Tech Spec Limit on Three Occasions.Caused by Entry of Ascarite Into Tank. Reagent Check Now Performed W/Sampling | /01T-0:on 800711,during Routine Analysis of Boric Acid Tank Samples,Concentration Exceeded Tech Spec Limit on Three Occasions.Caused by Entry of Ascarite Into Tank. Reagent Check Now Performed W/Sampling | | | 05000244/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000244/LER-1980-007-03, /03L-0:on 800829,controller TC-402R for Channel II Did Not Respond to Change in Input.Caused by Faulty Main Amplifier Bridge Assembly & Low Limit Transmitter.Controller Replaced & Calibr | /03L-0:on 800829,controller TC-402R for Channel II Did Not Respond to Change in Input.Caused by Faulty Main Amplifier Bridge Assembly & Low Limit Transmitter.Controller Replaced & Calibr | | | 05000244/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000244/LER-1980-008-03, /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed | /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed | | | 05000244/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000244/LER-1980-009-03, /03L-0:on 801003,during Performance of PT-12.1 to Verify Operability of 1A Emergency Generator,Part from Barring Device Seen to Fly Out.Caused by Bearings Not Designed to Withstand Operation W/Generator Running | /03L-0:on 801003,during Performance of PT-12.1 to Verify Operability of 1A Emergency Generator,Part from Barring Device Seen to Fly Out.Caused by Bearings Not Designed to Withstand Operation W/Generator Running | | | 05000244/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000244/LER-1980-010-03, /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired | /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired | | | 05000244/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000244/LER-1980-011-03, /03L-0:on 801211,bus 17 Breaker from 1B Emergency Generator Failed to Close.Cause Not Stated.Testing Interval Shortened to Verify Operability 810106 | /03L-0:on 801211,bus 17 Breaker from 1B Emergency Generator Failed to Close.Cause Not Stated.Testing Interval Shortened to Verify Operability 810106 | |
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