05000244/LER-1980-008-03, /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed

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/03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed
ML17309A102
Person / Time
Site: Ginna 
Issue date: 10/07/1980
From: Edgar C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17250A679 List:
References
LER-80-008-03L, LER-80-8-3L, NUDOCS 8010140482
Download: ML17309A102 (2)


LER-1980-008, /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed
Event date:
Report date:
2441980008R03 - NRC Website

text

NRC,PbRM 366

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During performance of PT-12.2 for "B" Emergency Generator (EG) bus 16 breaker from B" EG did not close.

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"A" EG was started and tied into bus 1 8, 4

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6 power.

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Binding condition of control relay anti-pump release lever guide pin.

Closing cir.

continuity was verified.

Breaker was observed during test operations, then control relay was replaced.

Breaker then tested successfully 5 times.

Removed relay was examined and guide pin split end was closed slightly, freeing binding condition.

ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ

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