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LER-1980-008, /03L-0:on 800910,during PT-12.2 Test for B Emergency Generator,Bus 16 Breaker Did Not Close.Caused by Guide Pin Split End Opening & Binding Control Relay Antipump Release Lever.Split End Closed |
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| 2441980008R03 - NRC Website |
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NRC,PbRM 366
,(7-77+>
U. S. NUCLEAR REGULATORYCOMMISSION
~O 7
8 CON'T
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80-008/03L-0 LtCENSEE EVENT REPOR~
CONTROL BLOCK:
Q1 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)
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1 Q20 0
0 0
0 0
0 0
0 Q3.4 1
1 1 1QP~QE 9
LICENSEE CODE 14 15 LICENSE NUMBER 26 LICENSE TYPE 30 57 CAT 58 soUROE LLJOB 0
5 0
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2 4
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9 1
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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During performance of PT-12.2 for "B" Emergency Generator (EG) bus 16 breaker from B" EG did not close.
(T. S ~ 6. 9 ~ 2. b(2)) ~
"A" EG was started and tied into bus 1 8, 4
and was capable of supplying to redundant bus 14 in the event of a loss of off-site F
6 power.
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8 9
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SYSTEM
CAUSE
CAUSE COMP VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SVBCODE
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Q12
~B Q13 R
E L
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X Q14
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RIRO EVENT YEAR REPORT NO.
CODE TYPE NO.
Q17 REPERP
~80
+
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Q~
~03
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+0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDX PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB.
SUPPLIER I MANUFACTURER Qls ~E Qls
~EQ20
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Q23 gJ QE pJ QEE 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o
Binding condition of control relay anti-pump release lever guide pin.
Closing cir.
continuity was verified.
Breaker was observed during test operations, then control relay was replaced.
Breaker then tested successfully 5 times.
Removed relay was examined and guide pin split end was closed slightly, freeing binding condition.
ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ
~z Q>>
z Q34 NA 7
8 9
10 11 PERSONNEL EXPOSURES 7
8 9
11 12 13 PERSONNEL INJURIES 45 7
8 9
FACILITY
~SO METHOD OF STATUS
% POWER OTHER STATUS ~
DISCOVERY s ~ Qss ~Q20 NR
~BQEI 8
9 10 12 13 44 45 46 DISCOVERY DESCRIPTION Q32 Operator observation LOCATIONOF RELEASE Q NA 80 80 80 80 7
8 9
11 12 80 LOSS OF OR DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
z Q4, NA 8
9 10 PUBLICITY IS D
DESCRIPTION 46 KZ ~>Q44 NA 7
8 9
10
~ 4IGIPF PREPARER Clair Edgar NRC USE ONLY 80 2
68 69 80 o PHDNE 3 1 5 524-4446, ext ~ 248
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