ML17306A833

From kanterella
Jump to navigation Jump to search
Insp Repts 50-528/92-17,50-529/92-17 & 50-530/92-17 on 920412-0530.No Violations Noted.Major Areas Inspected:Review of Plant Activities,Esf Sys Walkdowns,Surveillance Testing & Plant Maint
ML17306A833
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 06/29/1992
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17306A831 List:
References
50-528-92-17, 50-529-92-17, 50-530-92-17, NUDOCS 9207210007
Download: ML17306A833 (29)


See also: IR 05000528/1992017

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

R

9

.

5 -525/92-17,

50-529/92-17,

0

5 -550/92-17

2

5

k

N

.

50-92,

5 -529,

d ND-55D

N

.

I/PF-41,

NPF-91.

d NPF-74

Licensee

Arizona Public Service

Company

P. 0.

Box 53999, Station

9012

Phoenix,

AZ 85072-3999

~Fili

N

PI

II

d

N

I

5

i g

Units 1, 2,

and

3

Ins ection

Conducted

roved

B

April 12 through Hay 30,

1992

ong,

se

Reactor Projects

Sec ion

2

ate

igne

Ins ectors

D.

F.

J.

L.

D.

Coe,

Ringwald,

Sloan,

Tran,

Kirsch,

Senior Resident. Inspector

Resident

Inspector

Resident

Inspector

Resident

Inspector

(Rotational

Assignment)

Technical Assistant,

Division of Reactor Safety

and Projects

Ins ection

Summar

Ins ection

on

A r'l

12 throu

h

Ma

30

1992

Re ort Numbers

50-528 92-17

50-529 92-17

and 50-530 92-17

~ltd:

R ti,

it,

gl

dk kkiiti

0 ti

Nltk

four resident

inspectors,

and

one Region

V inspector.

Areas inspected

included:

review of plant activities

engineered

safety feature

system walkdowns

Units

2 and

3

inadequate

thread

engagement - Units

2 and

3

surveillance testing

Units 1, 2,

and

3

plant maintenance

Units .1, 2,-and

3

secondary

chemistry

pH excursion

Unit 2

alert declared

due to partial loss of annunciators

and plant computer-

Unit 3

feedwater isolation valve 0-ring failures

Unit

1

individual plant examination. status

and results

Units 1, 2,

and

3

design basis reconstitution

program results

and status - Units 1, 2,

and

3shift technical

advisor manning - Units 1, 2,

and

3

9207210007

920b29

PDR

ADOCK 05000528

8

PDR

fol1 owup on previously ident ifi ed items,

and

review of licensee

event reports

(LER) Units 1, 2,

and 3.

During this inspection the following Inspection

Procedures

were utilized:

30702,

40500,

41500,

61725,

61715,

61726,

62703,

71707,

71710,

92700,

92701,

and 93702.

Results:

Of the

13 areas

inspected,

one apparent violation in Units 1, 2,

and

3 was identified regarding

inadequate

thread

engagement

(Paragraph

3).

General

Conclusions

and

S ecific Findi

s:

Si nif'ca t Safet

Matters:

None

Violations:

eviations:

One violation Units 1, 2,

and

3

None

0 en Items:

Stren ths Noted:

Weaknesses

Noted:

Two new items were opened,

nine open items were closed.

Licensee

use of Probabilistic Risk Assessment

(PRA)

techniques for safety system unavailability management

continues to be seen

as

a strength.

t

The licensee incorrectly reassembled

a containment

i.solation check valve and did .not discover it through post

maintenance testing.

This issue will be discussed

in

special

inspection report 50-528/92-23.

ersons

Contacted

DETAILS

The below listed technical

and supervisory

personnel

were

among those.

contacted:

rizona Public Service

Com an

APS

R.

  • J
  • R.
  • T
  • C

R.

+R.

  • S
  • W.
  • A.
  • J

D.

G.

  • R
  • J
  • T

R.

Adney,

Baxter,

Bouquot,

Bradish,

Churchman,

Flood,

Fountain,

Friedlander,

Guthrie,

Ide,

Johnson,

Levine,

Mauldin,

Oyerbeck,

Rouse,

Scott,

Shriver,

Stevens,

Plant Manager,

Unit 3

Engineer,

Compliance

Supervisor/gA Audits gA&H

Manager,

Compliance

.Site Nuclear Engineering Director (Acting)

- Plant Manager,

Unit 2

'Supervisor/Acting

Hanager

gA&H

Manager,

Component

and Specialty

Engineering

Site Director, guality Assurance

Plant Manager,

Unit

1

Supervisor,

Compliance

Vice President,

Nuclear

Power Production

Director, Site Maintenance

& Hods

Site Director, Technical

Support

(STS)

Supervisor,

Station Operating

Events

Department

Assistant Plant Manager,

Unit 3

Assistant Plant Manager,

Unit 2

Director, Nuclear Licensing

& Compliance

S'te

Re resentatives

  • J. Draper,

Site Representative,

Southern California Edison

  • H. Benac,

Manager,

El

Paso Electric

(EPE)

  • R. Henry,

Site Representative,

Salt River Project

t

The inspectors

also talked with other licensee

and contractor personnel

during the course of the inspection.

Denotes

personnel

in attendance

at the Exit meeting held with the

NRC

resident

inspectors

on June 4,

1992.

2.

eview of Plant Activities Units

1

2

and

3

40500

61715

71707

and 93702

a ~

Unit

1

Unit

1 entered this inspection period with the reactor defueled

and

a refueling outage in progress.

Mode

6 was entered

when reloading

'he fuel into the reactor

began

on April 15,

1992.

Refueling

activities were completed

and the unit entered

Mode

5 on April 28,

1992.

The unit heated

up to Mode 3,

and went critical on Hay 21,

1992.

The power ascension

was halted at 43X for several

days while

investigating stator water cooling flow problems,

and again at 69X

while resolving feedwater

system problems.

Full power was achieved

on June

1,

1992,

and

was maintained for the rest of the reporting

period.

Unit 2

Unit 2 operated

at essentially

100X power throughout the reporting

period.

Unit 3

Unit 3 entered this inspection period operating at

100X power.

On

Hay 4,

1992,

an electrical

surge occurred in the plant annunciator

circuitry degrading the annunciator

system.

A subsequent

related

failure of the plant computer forced

a power reduction to

approximately

75X.

These conditions precipitated

the declaration of

an Alert at 8:19

AN (NST) on Nay 4 (see

Paragraph

8).

The Alert

condition continued until Hay 6,

1992 at ll:21 PN, at which time the

event

was terminated

and

a plant shutdown

was

commenced.

The unit

remained

shutdown in Node

3 from Hay 7 through

Hay 14 performing

troubleshooting,

repairs,

and testing of the annunciator

system.

The unit was returned to power operation

on Hay 15,

1992,

though

problems with a main feedwater

pump and

a feedwater isolation valve

kept the unit from reaching

100X power operation until Hay 19,

1992.

The unit operated

at essentially

100X for the rest of the inspection

period.

Plant Tour

The following plant areas

at Units 1, 2,

and

3 were toured

by the

inspector during the inspection:

Auxiliary Building

Control

Complex Building

Diesel Generator Building

Fuel Building

Hain Steam Support Structure

Radwaste

Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

(1)

0 eratin

Lo

s

and Records - Records

were reviewed against

technical

specifications

and administrative control procedure

requirements.

(2)

Nonitorin

Instrumentation - Process

instruments

were observed

for correlation

between

channels

and for conformance with

technical

specifications

requirements.

(3)

(4)

~Eh'<< ffi

C

1

d *hift

fA g

b

for conformance with 10

CFR Part, 50.54. (k), technical

specifications,

and administrative procedures.

E ui ment Lineu

s Various valves

and electrical

breakers

were

verified to be in the position or condition required

by

technical specifications

and administrative procedures

for the

applicable plant mode.

The inspector performed

a field verification of containment

integrity in Unit

1 by selecting

several

containment

penetrations

and confirming that they were properly align'ed in

accordance

with licensee

procedures

41ST-lZZ13,

"Containment

Integrity Penetrations

4.6.1.1.a,"

and 41ST-lSI04,

"Containment Spray Valve Verification 4.6.2. l.a,c

and -=

4.6.2.2."

No deficiencies

were identified during this

walkdown.

(5)

(6)

(7)

(8)

(10)

(11)

E ui ment Ta

in - Selected

equipment, for which tagging

requests

had

been initiated,

was observed to verify that,tags

were in place

and the equipment

was in the condition specified.

General

Plant

E ui ment Conditions

Plant equipment

was

observed for indications of system leakage,

improper

lubrication, or other conditions that could prevent the systems

from fulfillingtheir functional requirements.

Fire Protection - Fire fighting equipment

and controls were

observed for conformance with technical specifications

and

administrative procedures.

Plant Chemistr

Chemical analysis results

were reviewed for

conformance with technical specifications

and administrative

control procedures.

~gecurit

Activities observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

included vehicle

and personnel

access,

and protected

and vital area integrity.

Plant Housekee

in - Plant conditions

and material/equipment

storage

were observed to determine the general

state of

cleanliness

and housekeeping.

Radiation Protection Controls

Areas observed

included control

point operation,

records of licensee's

surveys within the

radiological controlled areas,

posting of radiation

and high

radiation areas,

compliance with radiation exposure

permits,

personnel

monitoring devices

being properly worn,

and

personnel

frisking practices.

(i2)~if

T

Eliftt

4

p il

1ti

briefings were observed for effectiveness

and thoroughness.

On April 24,

1992, during shift turnover, the inspector

noted

that the red

"OPEN" light indication for valve SIA-UV-684,

Containment

Spray

(CS) Train A discharge

valve to the shutdown

heat exchanger,

was not illuminated.

Subsequently,

this was

determined to be due to poor light bulb electrical contact.

The inspector further noted that this abnormal control board

indication was not discussed

among control board operators

during the board walkdown portion of the shift turnover.

The

inspector noted that alarms would al.ert operators to a valve

loss of power or out of position condition, that these

alarms

are reviewed during turnover,

and that the management

expectation is for light bulb problems to be identified

sometime during the shift but not specifically during shift

turnover.

The inspector

was also informed that the oncoming

primary side operator

had noted the abnormal

condition and

had

elected to not question

or discuss this during turnover because

a separate

analog valve position indicator showed this valve to

be fully open

and alarms were .not present for an out of-

position or loss of power condition.

The inspector also noted

that the shift turnover procedure,

40AC-90P16,

requires

a

control board walkdown during shift turnover which should

include "...Reasons

for abnormal indications."

The inspector

concluded that this .abnormal

indication should have

been

discussed

during turnover.

'The licensee

agreed with the

inspector's

conclusion.

No violations of NRC requirements

or deviations

were identified.

3.

En ineered

Safet

Feature

ESF

S stem Walkdowns

Units

2 and

3

71710

Selected

engineered

safety feature

systems

(and systems

important to

safety)

were walked down by the inspector to confirm that the systems

were aligned in accordance

with plant procedures.

During this inspection

period the inspectors

walked down accessible

portions of the following

systems:

Unit 2

o

Auxiliary Feedwater

"A" and "B"

Unit 3

o

-

High Pressure

Safety Injection "A" and "B"

o

Auxiliary Feedwater

"A" and

"B"

e

nade

uate Thread

En

a ement

Units

a

d 3

17 0

During

NRC walkdowns of safety-related

systems,

the inspector identified

several

components

which had thread

engagement

less that required

by the

licensee's

program,

documented

in procedure

30DP-9HP02,

"Fastener

Tightening/Preload."

During a walkdown of the high pressure

safety injection (HPSI) system in

Unit 3, the inspector identified three valves apparently

having

inadequate

thread

engagement.

The "B" train HPSI long term cooling

isolation valve,, 3SIB-HV-609, was found to have inadequate

thread

engagement

on the nuts

and bolts connecting the motor operator to the

yoke assembly.

The licensee

stated that .specification

13HN510, Section

.

8.8. 1, indicates that the minimum engagement

required is such that all

the threads of the nut are fully engaged with threads

on the bolt.

This

requirement

is. clarified in procedure

30DP-9NP02,

"Fastener

Tightening/Preload,"

which states that full engagement

is achieved

when

the end of the bolt is flush with the face of the nut.

The inspector

found that the nut on one of the four bolts

on valve 3SIB-HV-609 was

approximately

one thread short of full engagement.

The licensee

initiated Material Nonconformance

Report

(HNCR) 92-SI-3083,

which

concluded that the nuts were larger than the minimum required

and that

the actual

thread

engagement

was greater

than that available with the

vendor-specified

smaller-sized

nuts,

and that the existing configuration

provided adequate

strength for the application.

The inspector also identified apparently insufficient thread

engagement

on the packing gland nuts for 3ECB-HCV-66 and 3ECB-V-52.

The licensee

determined

in HNCR 92-EC-3002 that these

packing gland nuts were thicker

than required,

and that the actual

thread

engagement

was greater

than

that available with the vendor-specified

smaller-sized

nuts.

The

HNCR was

conditionally released,

requiring longer bolts to be installed during the

next refueling outage.

During a subsequent

walkdown of the Auxiliary Feedwater

(AFM) systems

in

Units

2 and 3, the inspector identified 'the following examples of

apparently insufficient thread

engagement:

Unit 3 "A" train

AFW:

3ECA-V-201

3AFA-V-161

3AFA-UV-37

3AFN-V-143

3AFA-V-151

3AFC-UV-36

3AFA-V-2

3AFA-V-67

Packing

Packing

Packing

Packing

Packing

Packing

Packing

Packing

Gland

.Gl and

Gland

Gland

Gland

Gland

Gland

Gland

Retainer

Retainer

Retainer

Retainer

Retainer

Retainer

Retainer

Retainer

Hinge Bolt

Hinge. Bolt

Hinge Bolt

Hinge Bolt

7

Unit 3 "B" train

AFW:

3AFB-V-130

3AFB-V-83

3AFB-V-23

3AFB-Y-94

Packing

Gland Retainer

Packing

Gland Retainer

Packing

Gland Retainer

Packing

Gland Retainer

Unit 2 " " train AFW:

2ECA-V-202

2AFA-V-14

2AFA-HV-32

2AFA-V-67

Packing

Gland Retainer

Hinge Bolt

Packing

Gland Retainer

Packing

Gland Retainer

Packing

Gland Retainer

Unit 2 "B" train AFW:

2AFB-V-.40

Packing

Gland Retainer

2AFB-UV-35'acking Gland Retainer

Hinge Bolt

pl

In .some cases,

nuts were engaged

2 to 3 threads

less

than full

engagement.

The licensee

subsequently

conducted

a walkdown of the

auxiliary feedwater

pump rooms in all three units

and identified some

additional similar thread-engagement

deficiencies.

In addition, after

the end of this inspection report period,

an

NRC inspector identified

that valve I-SIB-HV-609 had less than

SOX thread

engagement

on all four

actuator to yoke mounting bolts.

This deficiency will be described

in a

subsequent

resident

inspection report.

The licensee

determined

in discussions

with the valve vendor that the

packing gland retainer

hinge bolts engagement

of only three threads

is

needed

to provide the required strength.

Since all identified examples

met this criterion,

MNCRs were not required to document the condition.

The licensee's

evaluation is being documented

in Engineering

Evaluation

Request

(EER) 92-AF-004.

The licensee

evaluated

the remaining conditions under

MNCRs 92-AF-1014

(Unit 1), 92-AF-2015 (Unit 2),

and 92-AF-3016 (Unit 3).

The

licensee-identified

conditions in Unit

1 were dispositioned for rework,

which was completed

on May 27,

1992.

The inspector

reviewed the

licensee's

calculation

13-MC-AF-402, which evaluated

the adequacy of the

deficiencies identified in MNCRs 92-AF-2015

and 92-AF-3016.

These

MNCRs

were dispositioned

"use

as is" based

on this calculation,

which concluded

that all identified deficient components

had sufficient strength.

The strength of fasteners

is compromised

by inadequate

thread

engagement,

which in the case of packing gland retaining fasteners,

could result in

the packing blowing out of the valve, potentially degrading

the ability

of the system to perform its safety function.

Additionally, such

a

failure could create

a personnel

or equipment

hazard.

The licensee's.

program controls thread

engagement

during maintenance

and modification

practices to ensure that functional integrity of systems

does not become

degraded.

The inspector's

observations

indicated

a weakness

in program

implementation,

even though

some of the conditions were found acceptable

from a strength perspective.

In response

to the multiple deficiencies

identified, the licensee initiated

an engineering

evaluation to determine

~ the minimum acceptable

thread

engagement,

with the intent of later

performing system walkdowns to assure

conformance to the resultant

requirements.

The failure to comply with the procedure

30DP-9MP02 is

an apparent

violation of NRC requirements

(Violation 50-528/92-17-01).

One apparent violation of NRC requirements

was identified.

Surveillance Testin

- Units

1

2

and

3

61726

Selected

surveillance tests

required to be performed. by the technical

.

specifications

(TS) were reviewed

on

a sampling basis to verify that:

1)'he surveillance tests

were correctly included

on the facility

schedule;

2)

a technically adequate

procedure

existed for performance of

the surveillance tests;

3) the surveillance tests

had been performed at.

the frequency specified in the TS;

and 4) test results satisfied

acceptance

criteria or were properly dispositioned.

Specifically, portions of the following surveillances

were observed

by

the inspector during this inspection period:

Unit

1

Procedure

Descri tion

73ST-1DG02

Unit 2

Integrated

Safeguards

Test, Train

B

'P

d

.

Pedi

42ST-2SG05

ADV Nitrogen Accumulator Drop Test

On Hay 2,

1992, the inspector

observed portions of surveillance test

42ST-2SG05,

ADV Nitrogen Accumulator Drop Test,

and noted

two areas

where

minor performance variations

appeared

to affect the result

by a few psid.

Since this test often only passes

by only a few psid, these differences

could impact the overall result of the test.

Two specific performance

variations were observed.

The first was

how and where

on the accumulator

the temperature

measurement

was taken.

The second

was the inspector

noting that the test

gauge instrument root valve was not fully open,

and

when it was opened

more fully, the pressure

reading dropped

2 psid.

The

inspector discussed

these

performance variations with the System

Engineering Supervisor

who indicated that the System Engineer

had noted

data scatter in the test results

and

had drafted

a series of

recommendations

to minimize this scatter

and raise the margin between

result

and acceptance

criteria.

The inspector

concluded that these

measures

appear to address

any concern raised

by the observed

performance

variations

and encouraged

the licensee to implement these

recommendations

in a timely manner.

The licensee

responded

by stating that the

recommendations

are expected

to be approved

by June 30,

1992,

and

implemented in a timely manner.

Unit 3

~d

Il

74ST-9SS04

72ST-3RX09

36ST-9SB04

36ST-9SB02

No violations

PASS Functional Test

Shutdown Margin

PPS Functional

Test - RPS/ESFAS

Logic

PPS Bistable Trip Units Functional

Test

of NRC requirements

or deviations

were identified.

lant Maintenance - .Units

1

2

and

3

62703

'uring

the inspection period,

the inspector

observed

and reviewed

selected

documentation

associated

with maintenance

and problem

investigation activities listed below to verify compliance with

regulatory

r equirements,

compliance with administrative

and maintenance

procedures,

required quality assurance/quality

control department

involvement,

proper

use of safety tags,

proper equipment

alignment

and

use of jumpers,

personnel

qualifications,

and proper retesting.

The

inspector verified that reportability for these activities

was correct.

Specifically, the inspector witnessed

portions of the following

maintenance activities:

Unit

1

o

Core Reload

o

SIB-UV-614 Terminal Block Replacement

~Un't

2

o

Emergency Lighting Battery Replacement

On April 29,

1992, the "A" emergency diesel

generator

(EDG) tripped on

under-frequency.

CRDR 2-2-0149

was written for root cause of failure

determination.

At the

end of the report period,

CRDR 2-2-0149

was still

open

and the inspector

noted that the preliminary root cause of the trip

appeared

to be

an improperly installed U-ring in an air valve in the

diesel tripping system.

The inspector

noted that preventive maintenance

work order 539S50

was performed

immediately prior to the trip and the

procedure

did not contain specific instructions regarding the proper

orientation of U-rings in these

types of valves.

The'inspector further

noted that improper operation of these valves would not affect the safety

function of the

EDG.

In one case,

the affected valves

are

bypassed

during

an emergency start of the diesel

generator;

therefore,

the valves

10

affect starting capability.

In other cases,

the valves would need to

operate to shut

down the diesel after starting

and therefore

would not

prevent the diesel generator's ability to start (these valves are

routinely tested).

At the exit meeting,

the inspector

emphasized

the apparent similarity

.

between

improper maintenance

practices

regarding these U-rings and other

recent

problems

such

as the Feedwater Isolation Valve 0-ring problems

noted in Paragraph

7 of this report.

The licensee

acknowledged

the

inspector's

comments.

Unit 3

o

CEDH HG Set No.

1 Troubleshooting

o

SGA-UV-184A Troubleshooting

a

o

Hain Transformer, "A" Phase

Grounding Connection

o

Essential

Spray

Pond Filter Hedia Replacement

o

"B" Class

lE Battery Charger Input Breaker Trip Troubleshooting

o

RK/RJ System High Voltage Short Troubleshooting

No violations of NRC requirements

or deviations

were identified.

Secondar

Chemistr

H Excursion - Unit 2

71707

On May ll, 1992, the unit exceeded

the upper

pH limit of 9.6 (an

administrative limit, not .Technical Specifications)

during

a realignment

of the condensate

system to full bypass

flow around the condensate

demineralizes

(CDs) for chemistry test data gathering

and repairs to the

system.

Since condensate

pH is normally kept low in the

pH band of 9. 1-,

9.6 with the

CDs online,

and the band

changes

by procedure to pH=9.3-9.6

with CDs bypassed,

the unit was in a chemistry action level for low pH as

soon

as the

CDs were bypassed.

In anticipation of this, unit chemistry

personnel

planned for and initiated an

ammonia addition

as

soon

as the

CDs were bypassed

and targeted

pH 9.5 as the final goal.

Control of condensate

pH with the

CDs online was normally accomplished

by

controlling the

ammonia addition rate, relying on the

ammonia

removal

by

the CDs'nd online monitoring of pH.

Therefore,

no calculation

was

needed

because

a= balance

was achieved

and maintained.

Chemistry personnel

assumed

that the normal technique

would also work

when raising

pH with the

CDs bypassed.

No calculation

was performed.

Chemistry personnel

were unaware of the time response

characteristics

of

the online

pH monitoring instrumentation.

Without ammonia

removal

due to

the

CDs being bypassed,

a balance

no longer existed.

A calculation would

have provided

an estimate of the amount of ammonia

needed to achieve the

desired

pH.

Chemistry personnel

terminated the

ammonia addition when the

pH read 9.5, yet the system

pH trended

up to

a peak of 9.8.

The

pH

excursion

also raised

condensate

conductivity out of its control

band

resulting in an action level for conductivity as well.

The inspector

concluded that the failure to perform

a calculation for the

ammonia

addition

and the unfamiliarity of chemistry technicians

with the time

response

characteristics

of the

new online

pH monitoring system,

represented

weaknesses

in the administration of the chemistry control

program.

The inspector

acknowledged that this

pH excursion out of the

control

band appeared

to have

no significant adverse

impact on the

secondary

system.

The licensee

agreed with the 'inspector's

conclusion

and will be identifying these

as lessons

learned in an evaluation of the

CD bypass evolution as part of a secondary

chemistry control evaluation,

which is ongoing.

No violations of NRC requirements

or deviations

were identified.

7.

eedwater Isolation Valve

FWIV

0-Rin

Failures

Unit 3

71707

The

NRC inspector's

review of recent

FWIV 0-ring failures indicates that

further licensee

action is necessary

to prevent recurrence.

Additionally, the inspector

noted that

some engineering

evaluations of

these failures lacked

a thorough analysis of the potential for these

failures to impact the safety function of the valve.

On Hay 7,

1992 during fast closure of FWIV's SG-137

and SG-174 in Unit 3,

while performing

a controlled reactor shutdown,

the submanifold

"B" port

0-ring on the "H" 4-way valves failed.

This caused

hydraulic fluid to

leak out of the interface

between the 4-way valve submanifold

and the

actuator

body.

Similar failures occurred

on valve SG-137 in Unit 3 on

June

21,

1991

and August 31,

1991.

The first of these resulted

in a root

cause of failure

EER (91-SG-133)

which focused

on leakage

through

a

solenoid valve, but not the 4-way valve,

even though 4-way valve 0-rings

were found damaged with sections

missing.

The second of these resulted

in a

CRDR (3-1-84).root

cause of failure evaluation which noted .that

one

0-ring had disappeared

completely.

The cause

was evaluated

to be the

high pressure

hydraulic flow turbulence

impacting the 0-ring to the

extent that it was dislodged

and carried into the valve actuator with the

hydraulic flow.

This prompted

an Engineering

Evaluation

Request

(EER 91-

SG-175) to redesign

the submanifold to better "capture" and.hold the 0-

ring in place.

This design equivalent

change

EER was given priority 5

and was not yet complete

when the Hay 7,

1992 failures occurred.

Both

failures in Hay 1992 were found to be due to missing the

same 0-ring as

in the August

1991 failure.

This prompted the licensee

to upgrade the

EER to priority 3 with an expected

completion date within 90 days,

such

that replacement

submanifoldswill

be ready for installation prior to the

next Unit 3 refueling outage,

and for subsequent

failures if they occur.

The inspector considered

the possibility that the 0-rings

had not been

installed,

but since

no leakage

occurred during prior valve testing or

operation this possibility was not credible.

The inspector noted that the

CRDR 3-1-84 evaluation for the August

1991

failure did not include

an assessment

of the potential for safety

function impact due to an 0-ring being in the

FWIV hydraulic closure

system,

nor did it assess

the potential for loss of hydraulic fluid due

to leakage during the closing stroke

such that the FWIV's ability to

close

(perform its safe'ty function) was impacted.

The licensee

determined that the hydraulic accumulators

held approximately

10 gallons

12

8.

of fluid and required

5 gallons to completely close the

FWIV.

Mechanics

estimated

the total leakage

during and after closing to be

a maximum of

two gallons.

Licensee

engineering

management

acknowledged

the need for

thorough safety function impact reviews

and -subsequently

evaluated

both

questions

during their evaluation of the May 7 failures

(MNCRs 92-SG-

3043/3044

and

EER 92-SG-44).

Both evaluations

concluded that the safety-

function would not be impacted.

The inspector further noted that the licensee's

inspection of the

"M"

valve on Unit 3 valve SG-137 also identified other internal 0-rings which

were damaged.

These

were identical to the 0-rings which failed in Unit

1

during April 1991

and for which

a team root cause of failure effort

identified personnel

error during valve assembly

as the cause.

The

inspector also noted that this Unit

1 failure was manifested

by a sudden

~ and sustained

loss of 'accumulator

pressure

due to internal

leakage within

the 4-way valve.

The inspector considered

that the Unit 3 0-rings which

failed appeared

identical to the Unit

1 failures

and that sudden

and

sustained

internal

leakage

could occur during

a closing stroke should the

0-ring fail at that moment. This type of failure would effectively allow

a loss of hydraulic fluid through the 4-way valve similar to the loss

through the submanifold to actuator interface described

above,

although

such

a failure has not been

seen to have

impacted

any

PVNGS

FWIV to date.

The licensee

agreed

and stated that the potential for 4-way valve

internal

leakage to imp'act the

FWIV safety function would be evaluated.

After the report period ended,

on June 9, 1992, Unit 1 experienced

another

apparent failure of an

"M" 4-way valve on FWIV SG-132 while

conducting surveillance testing at power.

Due to the recurring nature of

this failure mechanism,

the inspector will review the licensee's

further

evaluation of the Unit

1 failure in light of the historical failures,

and

will review the licensee's

evaluation of potential internal

leakage

impacting the safety function of the

FWIVs (Followup Item 50-528/92-17-

02).

No violations or deviations of NRC requirements

were identified.

Alert Declared

Due to Partial

Loss of Annunciators

and Plant

Com uter-

Unit 3

93702

On May 4,

1992, while Units

2 and

3 were operating at

100X power and Unit

1 was in Mode 5, Unit 3 experienced

a partial loss of control

room

annunciators

-and

a subsequent

loss of the plant computer.

The Unit

declared

an Alert at 8: 19

AM (MST) and initiated

a downpower to

approximately

75X to meet Technical Specification requirements

associated

with a loss of the Core Operating Limit Supervisory

System

(COLSS).

The

loss of annunciators.occurred

due to a maintenance activity in which a

24V

DC lead from the annunciator

system inadvertently

came into contact

with a 480V AC electrical

bus,

causing

blown power supply fuses

and

annunciator light bulbs,

and damaging

many annunciator

system logic

circuit cards

and

some relay cards that interface

between the annunciator

system

and the plant computer.

The plant computer

became

overloaded

by

the surge of alarm state

changes

and stopped functioning.

13

0

The Alert condition ended

on Hay 6,

1992, following restoration of alarm

and computer

systems

and acceptable

annunciator

system testing.

Unit 3

was then shutdown to Node

3 to continue testing

and maintenance

of the

annunciator

system.

An NRC Augmented Inspection

Team (AIT) evaluated this event,

which is

documented

in Inspection

Report 50-530/92-19.

Ind'vidual Plant Examination Status

and Results

Units

1

2

and

3

37 00

The inspector

examined the licensee's

processes

for performing the

Individual Plant Examination

(IPE) in accordance

with Generic Letter 88-

20, through review of the results,

discussions

with personnel,

and

assessing

the licensee's

use of the

IPE results.

The licensee

had completed the Level

1 Probabalistic

Risk Assessment

(PRA) for internal events

and the Containment Analysis (Level 2)

PRA.

The results

were submitted to the

NRC for staff review on April 29,. 1992.

The licensee

intends to complete their Fire Analysis

and External, Events

analyses

(except seismic)

by June

1994.

The seismic schedule is under

NRC review.

In the area of external

events,

the licensee

has taken

prudent action to minimize external

events

hazards

in providing

mitigating action to preclude tornado

borne missiles.

For example,

the

licensee

had determined that spray

pond nozzles

may be damaged

by tornado

borne missiles.

In response,

the licensee

had established

program

controls

and periodic site inspections for temporary structures

and,

transient missiles.

Another example of proactive

use of IPE/PRA results

was observed

in the

licensee's

use of shutdown risk evaluations.

Shutdown risk evaluations

have

been

performed for the third refueling outages of Units

1 and 2.

The evaluation

team consists of members

from the

PRA group,

outage

management,

and unit operations.

The licensee

has defined critical

safety functions during the outage

and evaluated

the various reactor

coolant system conditions during the outage

against the minimum

acceptable

level of redundancy for each. critical safety function.

As

a

result,

an outage

work activity schedule

was developed

which provided the

minimum levels of redundancy.

Outage

management

was aware of the minimum

levels of redundancy

by use of a critical safety function board in the

outage

work control

area

and assessed

emergent

work advisability using

these criteria.

In the area of emergency

planning, the licensee

plans to integrate

PRA

results

and techniques

into scenario

development to challenge

engineering

and operations

regarding

success

path definition.

PRA event

and fault

trees will be placed in the

TSC and

EOF about June

1992.

The

PRA group

is represented

in the

TSC to take advantage

of this knowledge in dealing

with events.

In the area of training, the licensee

has developed training for

operators

in the results of the

PRA and

has provided insight for the

14

staff on the affects

on plant safety of the discretionary

removal of

safety equipment

from service during operating

and shutdown conditions.

In the area of maintenance,

the

PRA group

had identified risk sensitive

systems to the. maintenance

organization.

For example,

the

IPE/PRA

'rganization

was represented

on the task force established

by the

licensee to review the preventive maintenance

needs of the facility and

to establish

a defensible definition of the necessary

equipment

preventive maintenance

tasks.

System unavailability targets for these

" systems

have

been placed into the facility business

plan

and assured

that

work control supervision

was

aware of the targets

and the allowed

unavailability remaining.

The twelve week schedule,

used to establish

which systems

are available for maintenance

at any time,

was being

reviewed

by the PRA-group to provide planners with guidance

regarding the

advisability of simultaneous

removal

from service of the safety

systems

in a train and to review the relative risk during each

week of the twelve

week schedule.

The inspector

found that the licensee's

IPE/PRA organization

was well

staffed

and

managed

and

had actively assured

that plant

and line

organizations

were

aware of the benefits of a risk based

approach to

decisions

and that these organizations

actively involve the

IPE/PRA

organization in plant activities.'n addition, the licensee

has

established

station goals limiting the system unavailability due to on-

line maintenance

and surveillance for the emergency diesel

generator,

auxiliary feedwater,

and high pressure

injection systems,

with two more

systems to be

added to the program in the near future.

The inspector

established

through interviews of plant operations,

maintenance,

and

engineering staff and management

that the licensee

had generally

developed

a high level of sensitivity at the facility directed

toward

assessing

the advisability of a wide range of plant activities using risk

reduction/avoidance

as

a criteria for controlling safety equipment

unavailability.

No violations of NRC requirements

or deviations

were identified.

10.

esi

n Basis Reconstitution

Pro ram Results

and Status

Units

1

2

and

3

37700

The inspector

examined the licensee's

design basis reconstitution

program

to assess

the degree of progress,

the program,

and the results of the

effort.

The licensee

had established

a procedure set,

in 1991,

assigning

responsibilities

and measures

for:

(1) compiling documents

necessary

to

support the development of a design basis

manual

(DBM); (2) reviewing the

assembled

design

documents

in support of developing

a

DBM; (3)

developing, finalizing, reviewing,

and issuing the

DBM to assure

consistency

in organization,

format and content;

(4) identifying,

screening, prioritizing, tracking,

and evaluating

open items,

(5)

assessing

the impact of open items for safety

and operability concerns

and resolving

such concerns;

(6) controlling and changing

completed

DBMs;

15

P

I

t

0

and (7) defining the criter ia, objectives,

and methodology for ver ifying

and validating the DBHs.

The procedure, for verifying and validating the

DBHs was issued

and the

licensee

was in the selection

phase to obtain

a contractor for the

performance of the verification and validation effort.

None of the

completed

DBHs had yet been validated.

The scope of the effort involves about

75 DBHs, consisting of about

55

systems

and

20 topicals.

The program began in 1989

and is scheduled

to

be completed

about

December

1995.

The level of effort is distributed

about 80X/20X in contractor/utility staff resources,

respectively.

The licensee

had completed

about fourteen

DBMs in 1991

and

had scheduled

about another eighteen .for completion in 1992.

The inspector reviewed

two'ompleted

DBHs in a cursory manner

and examined

one (spray ponds)

in

detail.

The inspector

found that the

DBHs were missing

some significant

information:

for example,

system specific regulatory requirements

and

commitments;

overall

system functional/performance

requirements;

control

=

logic, interlocks,

and sensors;

system setpoints

and bases;

system/component

design capabilities,

requirements

and margins;

reasons

for design parameters;"and

descriptions of how design

and regulatory

requirements

were met.

The'nspector

expressed

the concern to the

licensee's

management

that while there

was

no regulatory requirement for

the development of the

DBMs, the early

DBHs appeared

to be of limited

usefulness.

The licensee

acknowledged

the inspector's

concern

and noted

that recent

DBMs contained

more information.

The inspector's

examination of the spray

pond

DBH identified that the

licensee

had opened

27 open

items

as

a result of the completion of the

DBH.

The open

items were all opened

on June

25,

1991;

however, four had

not been

screened

for importance or affect on system operability until

September

1991, twelve were not screened

until February/March

1992,

and

eleven

had not been

screened

yet.

In addition,

none of the

open items

had yet been referred to engineering for resolution.

Although none of

the open items reviewed identified any issue

which made spray

pond

operability indeterminate,

the inspector

expressed

the concern that

untimely screening

reviews

and untimely referral to engineering for

resolution could cause significant issues

to be unreviewed for a long

period of time.

The licensee

acknowledged

the inspectors

concerns

and

took immediate actions to assess

and correct

DBH open item deficiencies.

This action included

an audit of all open items in the data

base to

ensure that all documentation

had

been

completed

as required

by procedure

and represented

accurately in the tracking data

base.

In addition, the

licensee

revised their open item procedure to enhance

the overall

administrative

process for resolving

open items.

No violations of NRC requirements

or deviations

were identified.

16

Shift

echn'ical

Advisor

STA

Mannin

Units

1

2

and

3

07

12.

During an

NRC review of a

PVNGS Technical Specification

amendment

request,

dated August 28,

1991, to allow reducing the number of STA's to,

a minimum of two on site with three operating units, the

NRC determined

that for a period between July and October

1990,

PVNGS operated with a

total of two STA's on site while all three units were simultaneously

in

mode

4 or above.

The

NRC noted that the

PVNGS Updated Final Safety

Analysis Report

(UFSAR) allowed for a minimum of one

STA when all units

'ere

in operational

modes requiring STAs, but considered

the Technical Specification 6.2.4 language requiring "the STA to be onsite

and

available in the control

room within 10 minutes whenever

one or more

units are in MODE 1, 2, 3, or 4" to be more restrictive, requiring

an

STA

assigned

to each, unit individually when required

due to operating

mode.

By letter dated

December

30,

1991, the licensee

withdrew the portion of

their Technical Specification

amendment

request relating to reducing th'

number of STA's to a minimum of two on site when three units were in

modes

1 through 4.

Furthermore,

licensee

management

committed to revise

the

UFSAR to reflect the need for each unit to have

an individually

assigned

STA when its mode required

one.

The inspector

concluded that the

UFSAR,. and the supporting

language of

the associated

NRC Safety Evaluation Report allowed for different

interpretations

of Technical Specification requirements,

but that the

licensee's

current commitment'for each unit to have

an

STA when in modes

1 through

4 is appropriate for a three. unit site having physically

separate

control

rooms,

thus

no further

NRC action is necessary.

ollowu

on Previousl

Identified Items

Unit

1

92702

Closed

Violation

528 91-04-04

"Control of Motor-0 era'ted

Valve

Desi

n Information" Units

1

2

and

3

92702

This violation resulted

from the licensee's

failure to maintain design

documents

up-to-date.

Followup questions

regarding the method of control

of motor-operated

valve design data

are being addressed

as Followup Item

528/91-25-07.

This item is closed.

No violations of NRC requirements

or deviations

were identified.

eview of Licensee

Event

Re orts

LER - Units

1

2

and

3

90712

and

92700

Through direct observations,

discussion with licensee

personnel,

or

review of the records,

the following LERs were closed.

a.

Unit

1

91-10,

Revision

LO

"Units

1 and

3 Reactor Trips Caused

by Grid

Perturbation"

17

92-02, Revision Ll

"Diesel Generator Surveillance

Performed while

Unit Operating"

b.

~Un't 2

90-04, Revision LO/Ll

"Pressurizer

Safety Relief Valve Setpoints

Out of Tolerance"

The issues

raised in these

LERs are redundant to

LER 50-529/91-

05-LO which is still open.

These

.LERs are closed

and the

issues will be'valuated

as part of the review for LER 50-

529/91-05-LO.

90-01, Revision

LO

"Hanual Reactor Trip"

c.

Unit 3

91-01, Revision LO/Ll

"Safety Valve Setpoints

Out of 'Tolerance"

The issues

raised in these

LERs are redundant to

LER 50-529/91-

05-LO which is still open.

This

LER is closed

and the issues

will be evaluated

as part of the review for LER 50-529/91-05-

LO.

92-01, Revision

LO

"Reactor Trip Following Reactor

Power Cutback

Due to Loss of Hain Feedwater

Pump"

This event

was previously discussed

in Inspection

Report

530/91-50,

Paragraph

15 and is closed

based

on that review.

No violations of NRC requirements

or deviations

were identified.

14.

Exit Heetin

30702

Exit meeting

was held

on June

4,

1992, with licensee

management

and the

resident

inspectors

during which the observations

and conclusions

in this

report were generally discussed.

The licensee

did -not identify as

proprietary any materials

provided to or reviewed

by the inspectors

during the inspection.

18