ML17306A674

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Backshift Insp Repts 50-528/92-05,50-529/92-05 & 50-530/92-05 on 920126-0229.Violations Noted.Major Areas Inspected:Plant Activities,Engineered Safety Feature Sys, Surveillance Testing & Plant Maint
ML17306A674
Person / Time
Site: Palo Verde  
Issue date: 04/07/1992
From: Vandenburgh C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17306A672 List:
References
50-528-92-05, 50-528-92-5, 50-529-92-05, 50-529-92-5, 50-530-92-05, 50-530-92-5, NUDOCS 9204220052
Download: ML17306A674 (42)


See also: IR 05000528/1992005

Text

. S.

UC

AR

ATORY

SS

ON

GION V

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se

os.

~ice see

50-528/92-05,

50-529/92-05,

and 50-530/92-05

50-528,

50-529,

and 50-530

NPF-41,

NPF-51,

and NPF-74

Arizona Public Service

Company

P. 0.

Box 53999, Station

9012

Phoenix,

AZ 85072-3999

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yi

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Units 1, 2,

and

3

s ect

on

onducted:

roved

B

January

26 through February

29,

1992

an

en urg

,

c sng

le

Reactor Projects

Section

2

ate

sgne

g.

g

L. Coblentz,

F. Ringwald,

J'. Sloan,

L. Tran,

W. Ang,

ns ect on Suaear

Senior Resident

Inspector

Radiation Specialist

Resident

Inspector

Resident

Inspector

Resident

Inspector

Project Inspector

s ectio

o

Ja uar

26 t r u

h Februar

29

199

Re ort

umbers

50-528 92-05

50-529 92-05

and 50-530

9 -05

td:

g ti,

it,

gi

dg ttiitt

d ti

tytt

resident

inspectors

and Region

V based

inspectors.

Areas inspected

included:

review of plant activities

engineered

safety feature

system walkdowns

Unit 2

surveillance testing

Units 2 and

3

plant maintenance - Units 1, 2,

and

3

incore instrument cable withdrawal

Unit

1

plant protection

system setpoint incorrect - Unit

1

essential

spray pond, pump breaker failed to close

on demand

Unit 2

emergency diesel

generator

engineered

safety features

walkdown - Unit 2

startup testing - Units

2 and

3

auxiliary feedwater

pump plant computer alarms - Units 2 and

3

reactor

power cutback - Unit 3

9204220052

920407

PDR

ADOCK 05000528

PDR

0

core operating limit supervisory

system software modification

implementation

Unit 3

quality assurance

and audit program review - Units 1, 2,

and

3

followup on previously identified items.

During this 'inspection the following Inspection

Procedures

were utilized:

35701,

40702,

61726,

62703,

71707,. 71710,

72700,

92700,

92701,

92702,

and

93702.

lLesults:

Of the

14 areas

inspected,

three violations were identified.

Th'ese

involved the failure to follow procedures

during the withdrawal of incore

nuclear instrumentation

(Paragraph

6) and the failure to follow procedures

during surveillance testing of the plant protection

system

(Paragraph

7).

One

violation regarded

lack of documentation

concerning the quality of calibration

gas for containment

hydrogen monitors

(Paragraph

4).

General

Conclusions

a

d

S ecific Fi din s:

Si nificant Safet

Matters:

None

Violations;

Deviations:

Two cited violations - Unit

1

One cited violation

Units 1, 2,

and

3

None

Five new followup items were opened,

seven followup items

were closed,

and

one followup item was left open.

Stren ths Noted:

Operator response

to a Unit 3 tripped condensate

pump

was'rompt

and appropriate.

A senior operator's

prompt

identification of an incorrect reactor trip setpoint

was

also noted.

The

gA audit program was reviewed

and found to

be performance oriented

and focused in areas of relative

importance.

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i tt ti

t

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dt hgd

inattention to

a procedure

resulted

in a missed reactor trip

setpoint discrepancy.

Haintenance

personnel

were observed

departing

from a procedure to withdraw. instrumentation

cable

from the core during refueling.

e sons

Cont

ted

The below listed technical

and supervisory

personnel

were

among those

contacted:

ri ona

ublic Se v'ce

APS

  • R.
  • T

%J

  • S
  • R.
  • E.
  • R.
  • R.
  • S
  • 'g
  • M
  • J

D.

  • G
  • R

T.

R.

  • B

Adney,

Bradish,

Baxter,

Borst,

Bouquot,

Dotson,

Flood,

Fullmer,

Guthrie,

Ide,

Kerwin,

Levine,

Hauldin,

Overbeck,

Rouse,

Shriver,

Stevens,

Whitney,

Plant Manager,

Unit 3

Manager;

Compliance

Engineer,

Compliance

Engineer,

Technical

Data

Supervisor, guality Audits

, Director, Engineering

Plant Manager,

Unit 2

Hanager,

equality Audits and Honitoring

Site Director, guality Assurance

(gA)

Plant Manager,

Unit

1

Manager,

Maintenance

Standards

Vice President,

Nuclear

Power Production

Director, Site Maintenance

& Hods

Site Director, Technical

Support

(STS)

Supervisor,

Compliance

Assistant Plant Manager,

Unit 2

Director, Nuclear Licensing

& Compliance

Technical Specialist II, guality Audits

Site

Re resentatives

  • J
  • M.
  • R.

Draper,

Benac,

Henry,

Site Representative,

Southern California Edison

Hanager,

El Paso Electric (EPE)

Site Representative,

Salt River Project

Denotes

personnel

in attendance

at the Exit meeting held with the

NRC resident

inspectors

on March 5,

1992.

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

eview of Plant Activities

71707

and 93702

a 0

Unit

1

Unit

1 operated

at essentially

100X power until it began

a pre-

refueling power coastdown

on February

10,

1992.

The plant was

shutdown from 92K power on February

15,

1992, to commence

the

Cycle

4 refueling outage.

Cooldown to Mode

5 was promptly

completed,

and'ode

6 was entered

on February

24,

1992.

At the

end of the inspection period, the Unit was in Mode 6 with the head

removed but with no fuel removed

from the reactor vessel.

Unit 2

Unit 2 operated

at essentially

100X power throughout the

inspection period.

Jl~t 3

Unit 3 entered this inspection period in Hode

3 with a reactor

startup in progress,

and went critical at':04

AH (HST) on January

26,

1992.

A normal

powe'r ascension

followed, with 100X power

being achieved

on January

27.

On February 5,

a reactor

power

cutback to approximately

60X power was experienced

following the

manual tripping of the "A" main feedwater

pump (see

Paragraph

12).

Several

Core Operating Limit Supervisory System

(COLSS) failures

occurred following the installation of a

COLSS status

page display

on the plant computer

(see

Paragraph

13).

The software

change

had

been intentionally installed while at reduced

power to minimize

operational'mpact,

but had to be removed prior to returning the

plant to full power on February 6,

1992.

The plant operated

at

'essentially

100X power for the remainder of the inspection period.

ant Tour

The following plant areas

at Units 1, 2,

and

3 were toured

by the

inspector during the inspection:

Auxiliary Building

Control

Complex Building

Diesel Generator Building

Fuel Building

Hain Steam Support Structure

Radwaste Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

(1)

0 erat'n

o s

and

ords - Records

were reviewed against

technical specifications

and administrative control

procedure

requirements.

The inspector

noted that

on February

20,

1992,

a Shift

Supervisor in Unit 2 did not log entry into Technical

Specification Action Statement

3.3.1

when reactor trip

breaker

"8" was removed for preventive maintenance.

On

February

29,

1992, the inspector

noted

a key in the "B"

train spray

pond spray

mode selector switch, with the spray

mode selected.

The key is normally placed in the switch

only during switch operation.

The inspector

was informed

that these

were inconsistent with management

expectations

and administrative control procedure

40AC-90P02,

"Conduct of

- 2-

Shift Operations."

The individuals involved were

counselled.

At the exit the licensee

indicated that there

was no need to enter Action Statement

3.3. 1 when reactor

trip breakers

are opened

and

removed for maintenance

because

the removed breaker is fulfillingthe safety function.

The

inspector considers this to be

a consistency

issue since

Action Statement

3.3.1

was entered

when the "0" reactor trip

breaker

was removed for preventive maintenance

the next day

in Unit 2.

The licensee policy currently is to log all

breaker

removals

as action statement entries,

but is

evaluating this interpretation for possible

change.

onitori

nst

ume tatio

Process

instrument's

were

observed for correlation

between

channels

and for

conformance with technical specification requirements.

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observed for conformance with 10

CFR Part 50.54.(k),

technical specifications,

and administrative procedures.

ttf

-II

I

I

d

I tf Ik

I

were verified to be in the position or condition required

by

technical

specifications

and administrative

procedures

for

the applicable plant mode.

On January

29,

1992, the inspector noted that the oil level

in the "A" AFW pump turbine was about 1/4" above the high

normal

mark on the placard

by the sightglass.

The Auxiliary

Operator

(AO) had checked

on the logs that the level

was

between the scribe marks,

and stated that the level

had

been

like that since the refueling,

and

was slightly higher in

the afternoons.

The level

was between the scribe

marks in

the sightglass

holder.

The inspector discussed

the recent

resolution of this issue

from Unit 3 observations

(see

Inspection

Report 528/91-40,

Paragraph

2.D and Inspection

Report 528/91-35,

Paragraph

2.d) with the Shift Supervisor,

who was also

unaware of the proper oil level

band.

A

mechanical

maintenance

foreman indicated that the level

had

been intentionally left high following the overhaul

during

the refueling to allow for air bubbles to settle out.

The

level

was well within the operability range.

In response

to

this observation,

the l.icensee initiated

a change to the

AO

logs to show that the correct range is between the high

'normal

and low normal marks.

The inspector

concluded that

the licensee

had not fully implemented its program for

maintaining the correct oil level in the

pump turbine,

but

that the followup actions

taken

appeared

appropriate.

E ui ment

Ta

in

Selected

equipment, for which tagging

requests

had

been initiated,

was observed to verify that

tags

were in place

and the equipment

was in the condition

specified.

(6)

dit'ons

Plant equipment

was

observed for indications of system leakage,

improper

lubrication, or other conditions that could prevent the

systems

from fulfillingtheir functional requirements.

'(1)

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f(ghti g

8 Ip

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d

t

observed for *conformance with technical specifications

and

administrative procedures.

(8) ~Ch

t

- th

I

I

ly I

It

I

d

for conformance with technical specifications

and

administrative control procedures.

(9)

~Secur t

Activities observed for conformance with

regulatory requirements,

implementation of the site security

plan,

and administrative procedures

included vehicle

and

personnel

access,

and protected

and vital area integrity.

(10)

la t Housekee

in - Plant conditions

and material/equipment

storage

were observed to determine the general

state of

cleanliness

and housekeeping.

(ll)

adiation Protection Controls

Areas observed

included

control point operation,

records of licensee's

surveys

within the radiological controlled areas,

posting of

radiation

and high radiation areas,

complianc'e with

radiation exposure

permits,

personnel

monitoring devices

being properly worn,

and personnel

frisking practices.

(18)

~SI I

1

gl ift.ht

8

P

I I

I t(

briefings were observed for effectiveness

and thoroughness.

No violations of NRC requirements

or deviations

were identified.

n ineered Safet

Featui e

ESF

S stem Walkdowns

Unit 2

71710

The Unit 2 train A and

B emergency diesel

generators

were walked down by

the inspector to confirm that the system

was aligned in accordance

with

plant procedures.

No violations .of NRC requirements

or deviations

were identified.

Surveillance Testin

Units

2 and

3

61726

Selected

surveillance tests

required to be performed

by the technical

specifications

(TS) were reviewed

on

a sampling basis to verify that:

1) The surveillance tests

were correctly included

on the facility

schedule;

2) A technically adequate

procedure

existed for performance of

the surveillance tests;

3) The surveillance tests

had

been

performed at

the frequency specified in the TS;

and 4) Test results satisfied

acceptance

criteria or were properly dispositioned.

Specifically, portions of the following surveillances

were observed

by

the inspector

during this inspection period:

Unit 2

J?rocedure

escr

tion

42ST-2AF01, "Auxiliary-Feedwater

Pump AFN-POl Operability 4.7. 1.2.A"

42ST-2RC02,

"Reactor Coolant System Mater Inventory Balance 4.4.5.2. 1.C"

36ST-9HP03,

"Containment

Hydrogen Monitoring System Calibration Test,

Channel

A"

~Un't 3

~roced

e

escri t o

74ST-9SS04,

"PASS Functional Test"

During the performance of TS Surveillance Test

(ST) 36ST-9HP03 in Unit

2,

on February ll, 1992, the hydrogen

span

gas that was being

used

as

a

calibration gas for the

ST had chemical

composition certification

documentation

attached to the gas bottle.

The inspector

reviewed the

chemical

composition documentation

and. noted the following:

, The documentation certified the gas to be 95.6

X N2 and 4.4X

Hydrogen.

The documentation

did not specify whether

the percentage

was

by volume or by weight.

TS 4.6.4. 1

requires that the surveillance

be performed using

a

sample

gas containing

a nominal four volume percent

hydrogen, with the balance nitrogen.

The chemical composition certificate was provided on

a vendor

letterhead

of a vendor that was not on the licensee's

approved

supplier list.

The certification was signed but the signature

was

illegible.

No title was provided for the certifier, ie.

gA, gC,

Chemist, etc.

Inspector

Followup Item 529/91-04-02 identified inspector

concerns

- regarding the quality of the calibration gas

used for the subject

surveillance test.

The inspector discussed

the above noted

documentation

observations

and the Inspector

Followup Item with the

system engineer,

the Unit 2 Maintenance

Manager,

Unit 2

IKC test

personnel,

and guality Engineering.

The inspector

was informed that

an

audit had

been performed

on

a prospective

vendor for the calibration gas

and that

gA was working with the vendor to resolve audit discrepancies

and to place the vendor

on the licensee's

approved suppliers list.

However, in the interim,

a sampling inspection of the calibration gasses

in stock had

been performed

and that sampling inspection

had determined

that the calibration gas in stock had chemical certification that could

be traced to the prospective

vendor to allow use of those calibration

gas bottles that were in stock. for ongoing surveillance tests.

The

subject

gas bottle however was determined to have chemical

composition

certification that could not be traced to the prospective

vendor.

The licensee

declared

Containment

Hydrogen Monitor .Channel

A, 2-J-HPA-

E02, inoperable for surveillance

and reperformed the surveillance

using

a calibration gas that had

a chemical

composition certification that

could be traced to the prospective

vendor.

The licensee

stated that the

reperformance

of the

ST resulted in little or no adjustment indicating

that the previously used calibration gas,

although lacking traceable,

certification,

was of the required chemical

composition.

The licensee

also promptly inspected all other span

gas bottles attached to all

Containment

Hydrogen Monitors in all three units and determined that one

monitor in Unit

1 and another in Unit 2 had similar chemical

composition

certification lack of traceability problems.

Similarly, the licensee

reperformed

the

ST on those monitors

and obtained similar results.

10 CFR 50, Appendix B, Criterion XII, requires that measures

be

established

to assure

that tools,

gages,

instruments,

and other

measuring

ahd testing devices

used in activities affecting quality are

properly controlled, calibrated,

and adjusted

at specified periods to

maintain accuracy within necessary

limits.

TS 6.8. l.a requires that

written procedures

be established

covering the procedures

recommended

in

Regulatory

Guide 1.33, Revision 2, February

1987.

Reg Guide 1.33

Revision 2, Appendix A, Section 6.a. requires that procedures

of a type

appropriate to the circumstances

should

be provided to ensure that

tools, gauges,

instruments,

controls

and other measuring

and testing

devices

are properly controlled, calibrated

and adjusted

at specified

periods to maintain accuracy.

Surveillance Test Procedure

36ST-9HP03,

Revision 7, Containment

Hydrogen Monitoring System Calibration Test,

Channel

A, Paragraph

4.0, lists calibration gases

measuring

and test

equipment

used in performance of the

TS 4.6.4. 1 surveillance test.

Procedure

34PR-OME01,

Revision 1,

ANPP METE Control Program,

provides

the licensee's

controls for measuring

and test equipment.

The use of calibration gas that did not have chemical

composition

certification that was traceable

to a national

standard,

for performance

of the subject

ST,

appeared

to be

a violation and was identified as

violation 528/92-05-03.

Inspector

Followup Item 529/91-04-02

was closed

and the item will be followed up as part of the identified violation.

One violation of NRC requirements

was identified.

Plant-Maintenance

Units

1

2 and

3

62703

During the inspection period, the inspector

observed

and reviewed

selected

documentation

associated

with maintenance

and problem

investigation activities listed below to verify compliance with

regulatory requirements,

compliance with administrative

and maintenance

procedures,

required quality assurance/quality

control department

involvement,

pr oper use of safety tags,

proper equipment

alignment

and

use of jumpers,

personnel

qualifications,

and proper retesting.

The

inspector verified that reportability for these activities was correct.

Specifically, the inspector witnessed

portions of the following

maintenance activities:

it

1

Troubleshoot flow interference

in letdown ion-exchanger

discharge

piping

Replacement of PKB and

PKD batteries

Placement of multi-stud tensioner

Incore instrument cable withdrawal

Control element drive mechanism

fan disassembly

Reinstallation of a missing stud in valve SIA-V476 yoke

Preventive

maintenance

of "B" reactor .trip switchgear breaker

The inspector noted that

a mechanical

maintenance

foreman in Unit 2

identified a stud

on the high pressure

safety injection pump discharge

isolation valve SIA-V476 that had loosened

and completely separated

from

the valve.

This stud is one of four. which secure

the manual

operator to

the valve yoke.

The System Engineer determined that the remaining three

studs

had sufficient strength to permit operation of the valve,

and

worked with mechanical

maintenance

to get the stud reinstalled promptly.

The inspector

observed

the reinstallation of the stud.

The licensee

could not determine the cause of the loosened

stud.

The inspector

concluded that the licensee's

identification and corrective action were

appropriate.

Unit 3

~

"E" Charging

Pump Gear

Box Replacement

and Electrical

Retermination

~

Equipment gualification Protective Maintenance of SGA-UV-1135

No violations of NRC requirements

or deviations

were identified.

ncore Instrument

Cable Withdrawal - Un't

1

62703

During a containment tour on February

25,

1992, the inspector

observed

several

tasks in progress

in or around the reactor cavity, in

preparation for the reactor

head li.ft.

At the incore instrument (ICI)

holding platform, the inspector

observed

several

workers attempting to

manually raise fixed ICI ¹55 from the level of the seal table to the

holding platform.

The inspector

raised

a concern with the level of

control applied to this task.

Procedure

36NT-9RI06,

"Withdrawal of the Incore Instruments for Reactor

Refueling Operations," outlines precautions

to be used

when withdrawing

ICIs, including cleanliness

considerations,

limitations on withdrawal

force, protection of components,

avoidance of radiological

hazards,

limitations on axial bending

and

so forth.

Section 8.4.5 requires

ICI

-'7-

withdrawal to be accomplished

using the control element

assembly

(CEA)

hoist, which provides automatic controls for the withdrawal process.

Of 61 fixed ICIs, all but one

had already

been withdrawn several

days

earlier using the control element

assembly

(CEA) hoist, in accordance

with Procedure

36MT-9RI06.

At that time, fixed ICI 155 had

been

found

to be stuck.

The licensee

had written a special

work package

and

radiation exposure

permit

(REP) to cut the seal table closure

cap for

fixed ICI f55, in hopes of freeing the stuck instrument cable.

The

closure

cap

had

been cut out without incident.

At the time of the inspector's

observation,

the

CEA hoist was blocked

from the ICI area

by recently erected scaffolding.

This prevented

withdrawing of fixed ICI $55 in accordance

with procedure

36MT-9RI06.

Due to the additional effort and delay needed to move the scaffolding,

the work group supervisor verbally instructed the task shift leader to

attempt to withdraw the ICI by hand.

The procedure did not cover this

method of handling the ICI.

During initial efforts to free the stuck cable,

one worker pulled from

the ICI holding platform (using

a nylon rope

and shackle

attached

to the

ICI cable)

and

one worker pulled at the seal table, with an

RP

technician standing

by at the seal table to monitor changing

radiological'onditions.

Several

attempts

were necessary

to free the

cable.

When, finally, the ICI pulled freely, the worker at the holding

table hauled the ICI hand-over-hand

approximately

20 feet to the level

of the holding platform.

The inspector

noted the following areas

of concern:

a.

Use of the

CEA hoist for ICI withdrawal automatically limits the

lifting force'o 500 pounds.

While manual withdrawal appeared

unlikely to over-tension

the cable,

no written precautions

existed

to limit the number of individuals pulling on the cable,

or to

prevent pulling in sudden,

forceful jerks to dislodge the-stuck

cable.

The inspector noted that breaking the cable at

a point

inaccessible

from the seal table could have resulted

in

significant engineering

challenges,

work delays,

and potentially

incurrence of considerable

radiation exposure.

b.

By using the hand-over-hand

method,

the ICI might easily have

been

dropped.

This could have resulted in rapid insertion of the ICI

into the core, or in possible

personal

injury to the individuals

at the seal table.

The inspector could find no evidence that

these or other hazards

had

been considered,

and .noted that the

absence

of a procedure

covering the methods

used left the workers

vulnerable to potentially unanalyzed,

unanticipated

contingencies.

, In response

to the inspector's

questions,

the licensee initiated

CRDR

1-2-0084 to assess

the appropriateness

of using

a method of ICI

withdrawal not covered

by the procedure.

During

a later discussion,

the

inspector

asked the Unit I Plant Manager what basic criteria supervisors

were expected to use

when determining whether departure

from a procedure

occasioned

a new, specific work instruction.

The Unit

1 Plant Manager

stated that management clearly expected all significant tasks carried

out on plant equipment to be performed according to a procedure.

The inspector concluded that the licensee's

failure to implement the

requi'rements of Procedure

36MT-9RI06 when withdrawing ICI Cable

855

constituted

a violation of Technical .Specification 6.8.1 (Violation

528/92-05-01).

One violation of NRC requirements

was identified.

ant

otectio

S stem

PPS

Set oint

correct

U 't

9

00

a

d

~)~70~1

On February 4,

1992, at 5:53

PM (MST), the Unit

1 Assistant Shift

Supervisor

observed that

a computer printout on the

"demand typer" in

the Control

Room showed that the Plant Protection

System

(PPS)

channel

"B" number

2 steam generator

(SG) low pressure

setpoint, for reactor

trip and main steam isolation actuation,

was lower than allowed by

technical specifications

following partial performance of the

surveillance test

(ST) 36ST-9SB02,

"PPS Bistable Trip Units Functional

Test."

The setpoint

was approximately

870 pounds per square

inch

absolute

(psia), while the technical specification

minimum allowed value

is 912 psia.

The channel

had previously been declared

operable at 4:27

PH,

and subsequently

Condition Report/Disposition

Request

(CRDR)

1-2-0045

was initiated to assess

the need for corrective actions.

The licensee

determined that the

ISC technician

had incorrectly

performed

a step. in the

ST when

he checked the restoration of the number

I SG setpnint instead of the number

2

SG setpoint

as specified in step

8.11.6.2 of the procedure.

This error was of particular concern

because

it resulted in a reactor trip setpoint

and

a main steam isolation

actuation setpoint

being nonconservative

with respect to the safety

analysis.

The

ST procedure

did not direct an independent verification of this

setpoint.

While licensee

procedures

do not require independent

verification of setpoints,

the licensee is considering placing

independent verification steps for these setpoints

in 36ST-9SB02.

This

evaluation is being documented

in CRDR 1-2-0045.

The inspector will

review the licensee's

evaluation

upon completion.

Corrective actions

completed include returning the setpoint to its

proper value

and completing the

ST performance

and administering

discipline for the

I&C technician.

Other corrective actions

were

recommended

by the licensee's

CRDR evaluator

and are being considered

for implementation.

These

include revisions to ST procedure

36ST-9SB02

to have detailed action steps

required to determine the number

2

SG low

pressure

setpoint value

and

how to adjust it if necessary,

and to

include independent verification of as-left values of variable

setpoints.

Additionally, the licensee

determined that the reactor operator

who

performed the hourly setpoint verification at 5:00

PH,

as required

by

40DP-90P05,

"Control

Room Data Sheet Instructions,"

and

a by Unit

1

Night Order dated January

24,

1992, failed to notice that the setpoin't

was low.

This error was regarded

by the inspector

as particularly

significant because

of the weak performance of a licensed operator in

assessing

the value of -a

PPS setpoint.

The inspector

noted that the

diligence of the Assistant Shift Supervisor in identifying the condition

was in contrast to the performance of the Reactor Operator

who

apparently did not accurately

read the control board indication or

utilize the readily available computer printout to confirm the

indication.

The licensee

administered discipline to the reactor

operator

and revised the Control

Room Data Sheet Instructions to require

the operators to use the computer printout to determine the setpoint

value

and to take appropriate

action if the setpoint is less than

913

psia.

The error made

by the

IEC technician in restoring the channel

from the surveillance,

and the error made

by the Reactor Operator

when

checking the setpoint,

were individually not highly safety significant,

however considered collectively, this event represents

concurrent

failures to ensure that

a reactor trip setpoint

was correct, therefore

the two errors

are being cited

as

a single violation (Violation 528/92-

05-02).

One violation of'NRC requirements

was identified.

ssential

S ra

Pond

ESP

Pum

reaker Failed To Close

On Demand - Unit

~6703

On February

14,

1992, the "A" train

ESP

pump breaker failed to close

when the operator attempted to start the

pump from the control

room.

An

inspection of the breaker revealed that the closing springs

were not

charged,

and the

750G instantaneous

ground relay was flagged.

However,

the

786 lockout relay was not flagged, indicating that

a ground fault

was not present.

The Shift Supervisor directed electricians to

troubleshoot

the breaker.

The inspector

observed

a portion of the

troubleshooting

which involved removing the breaker

from the cabinet,

moving it to

a test fixture in the switchgear

room, testing the breaker;

and returning the breaker to the cabinet.

The inspector noted that this

troubleshooting

was performed without invoking any of the work control

process

and was not done according to any procedure or work document.-

)OR 92-0038

was written to evaluate

whether these activities should

have

been performed under the Work Control

Program.

The Root Cause of

Failure

(RCF) Condition Report/Disposition

Request

(CRDR) concluded that

the apparent

cause of the failure was dirty stabs

on the auxiliary

contact block, although this root cause

could not be confirmed.

Licensee

management

determined that

a more definitive,RCF evaluation

was

not warranted

due to the inability to further examine the breaker in its

failed state.

The inspector

noted that the

CRDR program provides for

non-confirmed

"apparent"

RCF analyses

to be trended for further

.-

evaluation.

The inspector determined that

some

RCF data

was lost as

-10-

soon

as the breaker

was racked

down and tested.

The electricians

performing this troubleshooting did not identify dirt on contact

stabs

which could be removed

and examined,

nor did they identify high contact

resistance.

The inspector

noted that the

CRDR evaluation did not

ascertain

the failure history of this class of breaker

on site, did not

ascertain

the recent racking and operating history of this breaker,

and

did not identify the loss of RCF data during troubleshooting.

Subsequent

discussions -with the System Engineer determined that of the

five known General Electric Hagneblast

breaker failures at Palo Verde,

the root cause

was not confirmed in three of the events.

The inspector

= further noted that while the maintenance

program for Magneblast.breakers

has

been significantly improved since

1990,

two of these failures

occurred since the program was improved.

The licensee

committed to

promulgating

an equipment list to each unit which identifies specific

equipment that would require early engineering

involvement in

troubleshooting to preserve

and examine conditions which might assist

in

. RCF analysis.

The inspector will review the licensee's

actions

and

evaluation of (DR 92-0038

upon completion

(Followup Item 529/92-05-04).

No violations of NRC requirements

or deviations

were identified.

er enc

iesel

Generator

DG

n ineered Safet

Features

ESF

Walkdown

U it 2

7 710

The inspector

reviewed this program area

by performing detailed

walkdowns of the Unit 2 emergency diesel

generator

(EDG) equipment

rooms

and systems,

by verification of selected

subsystem

lineups

and

configurations with plant drawings,

by evaluation of annunciator

and

control panel status,

and by review of operator

logs.

Selected

walkdowns were also performed of the Unit 3

EDG systems for comparison.

The inspector

noted the following items:

'a ~

b.

Several air-to-oil booster relays,

used to provide remote

indication at the local control panel,

were continuously cycling.

The inspector

asked the system engineer whether frequent cycling

of the relays might not affect relay diaphragm performance

or

shorten

diaphragm life.

The system engineer

acknowledged that

continuous cycling did not reflect optimum relay performance,

but

stated that this condition posed

no significant safety risk, since

the relays performed

no control function,

and any significant

reduction in relay performance

would be effectively detected

during regular operator

rounds.

Duct tape

had

been placed beside the sightglass for the jacket

water cooling surge tank, with periodic handwritten markings to

indicate

a sightglass

level of 50 percent,

75 percent,

and

so

forth.

The inspector noted that auxiliary operators

logged

sightglass

level twice per shift,

and used these

informal markings

as

a measurement

aid.

In response

to the inspector's

questions,

the system engineer

stated that this apparent

lack of an effective

sightglass

level marker

had

been

noted

on December

10,

1991,

and

that CRDR,1-1-0170

had

been initiated to resolve the concern.

The

-11-

system engineer stated that

a more effective,

permanent

sightglass

level marker

was being designed for installation

on the tank.

The inspector concluded that none of the observations

made affected Unit

2

EDG operability,

and that the

EDG appeared fully capable of performing

its safety functions in all observed

respects.

No violations of NRC requirements

or deviations

were identified.

Sta t

stin

Units

d 3

700

The inspector

reviewed the data from core physics tests

associated

with

the Unit 2 Cycle 4 refueling and the Unit 3 Cycle

3 refueling to verify

that the results

met acceptance

criteria and that all deficiencies

were

resolved in a timely manner.

Specifically, the data from the following

procedures

were. reviewed

~Unit

72IC-2RX01,

72PA-9RX02,

72PA-9SB01,

72PA-9ZZ07,

72PY-9RX01,

72PY-9RX31;

72TI-,9RI01,

Unit 3

"Core Reloading"

,

"Excore Linear Subchannel

Gain Adjustments"

"CPC/COLSS Input Intercomparison"

"Reload

Power Ascension Test"

"Reload Criticality and

Low Power Physics Testing"

"Reactivity Computer Checkout"

"Fixed Incore Detector Data Collection"

720P-9RX02,

"Determination of Anticipated Critical Position"

72PA-9RX01,

"Power Calibration" (Reviewed

1 of 4 performances)

72PA-9RX02,

"Excore Linear Subchannel

Gain Adjustments"

72PA-9RX03,

"Secondary Calorimetric Power Yerification"

72PA-9SB01,

"CPC/COLSS Input Intercomparison"

72PA-9ZZ07,

"Reload

Power Ascension Test"

72PY-9RX01,

"Reload Criticality and

Low Power Physics Testing"

72PY-9RX31, "Reactivity Computer Checkout"

72TI-9RI01, "Fixed Incore Detector Data Collection"

72TI-9RX02, "Spent

Fuel Inspection"

These procedures

document the calibration of nuclear instrumentation,

the determination of isothermal

and moderator temperature

coefficients,

the determination of group and total control rod worth, the

determination of shutdown margin, the evaluation of core thermal

power,

the calculation of inverse

boron worth', the determination of Core

Operating Limits Supervisory

System

(COLSS)

and Core Protection

Calculator addressable

constant

values,

and the verification of the

secondary calorimetric calculation in COLSS.

The inspector

noted that the peaking factor values

(predicted,

actual,

minimum,

and maximum) for Unit 3 were incorrectly recorded in Appendix A

of 72PA-9ZZ07.

The data form had preprinted

a factor of "x 10 ," but

-12-

the test performer inadvertently duplicated this factor when the data

were transposed

from other sections of the procedure,

such that the

values recorded in Appendix A appeared

with a net factor of "x 10 '

10 '."

The correct values

were within the correct acceptance

criteria,

and the inspector concluded that this was

an administrative oversight.

The licensee

acknowledged

the inspector's

observation.

The inspector

determined that 72PA-9ZZ07 had

been revised 'to eliminate the preprinted

factor before this error was identified.

The inspector found that all the acceptance criteria were met and that

other discrepancies

and questions identified during the performance of

the procedures

were clearly identified and promptly resolved.

No violations of NRC requirements

or deviations

were identified.

uxiliar

Feedwater

AFW

um

Plant

Com uter

PC

Alarms - Un ts

2 and

~37 l~0

On February

25,

1992, the inspector noted that several

PC points were in .

alarm on a group display for AFW pump bearing temperatures

in Units 2

and 3.

The inspector determined that the temperatures

were normal

however the computer alarm points were always in alarm and appeared

to

be in alarm at all temperatures

below 190 degrees

F and

above

200

degrees

F.

The inspector

reviewed control

room deficiency logs

and

noted that this problem was not logged.

The inspector further

determined that Engineering

Evaluation Request

(EER) 87-AF-48, initiated

in November

1986

and completed in October

1988, contained

an

identification of this problem

and resolution.

The resolution

was to

reset the alarm setpoi'nts to those specified in the

EER and referenced

a

Plant

Change

Request

(PCR) written to effect this change.

The licensee

was unable to find any work document written to carry out this intended

resolution.

.The inspector concluded that this deficiency

had not been

tracked for corrective action.

The licensee initiated Condition

Report/Disposition

Request

(CRDR) 9-2-0171 to ensure corrective action

is taken

and to assess

the need for further review of plant computer

alarm setpoint discrepancies.

The inspector will review the licensee's

CRDR evaluation

when completed

(-Inspector Followup Item 529/92-05-05).

No violations of NRC requirements

or deviations

were identified.

Reactor

Power Cutback

RPCB

- Unit 3

93702

On February

5,

1992, at 5:27

PH (NST), while the unit was 'operating at

100 percent

power,

a

RPCB to approximately

60 percent

was experienced

due to the loss of the "B" main feedwater

pump.

The feedwater

pump was

manually tripped by the operators

because

of low feedwater

pump suction

pressure

after the "A" condensate

pump tripped.

The condensate

pump

tripped because

.a circuit card for the condensate

pump flow transmitter

failed.

The inspector

responded

to the control

room and confirmed that the plant

was stable.

The inspector noted that the operators'rompt

action to

- 13-

trip the main feedwater

pump was in accordance

with licensee

procedures.

The inspector concluded that licensee's

actions

were. appropriate.

No violations of NRC requirements

or deviations

were identified.

o e 0

mit

erv'so

ste

C

Soft

't'o

leme t t on

U t 3

92 00

On February 5-6,

1992, while Unit 3 was at approximately

60X power

following a reactor

power cutback

(see paragraph

12), several

COLSS

failures occurred

as

a result of a

COLSS software modification

implemented following the power reduction.

The modification had been

intentionally implemented while at reduced

power to preclude

power

reductions

which potential

COLSS failures

may require.

However,

as the

same software

had

been successfully

implemented in Unit 2,

no problems

were expected

during the Unit 3 implementation.

The operators

considered

COLSS to be in service .following the

implementation,

and

made appropriate entries in the Unit Log following

each failure.

No other operational

impact of the failures was observed.

As a result of the unexplained failures, Condition Report/Disposition

Request

(CRDR) 3-2-0046

and guality Deficiency Report

((DR) 91-0034 were

initiated.

The

CRDR evaluation determined that the failures occurred

because

insufficient memory was available in the computer for a function

involving the "data-logger" routine, which is accessed

hourly by 'COLSS

-as

a result of the modification.

The memory was unavailable

as the

result of a unrelated

December

1991 software modification following

which the memory had inadvertently not been restored for use

by other

programs.

While the

COLSS softwar'e modification was tested

in the

computer lab, the post-implementation

testing did not address

the memory

requirements

or the potential for the unexpected

interaction with the

previous unrelated modification.

The inspector

concluded that this modification implementation

problem

represents

another

example of ineffective control over modifications to

plant computers

and COLSS-related

software.

'Inspector Followup Item

529/90-28-02 is currently open to address

software configuration

controls following other COLSS-related errors.

COLSS errors

are

potentially safety-significant

because

COLSS determines

the Technical

Specification operating

power limit for the plant and because

COLSS is

used to calibrate safety-related

excore nuclear instrumentation.

The

inspector noted that the licensee currently considers

COLSS

as "not

quality related."

The inspector will review the licensee's

actions in

this area

under the above followup item.

No violations of NRC requirements

or deviations

were identified.

-14-

'

14.

t

ss ra c

nd A dit Pro ram Review -

U its

2

and

3

35701

nd

0702

The licensee

had previously proposed to implement

a new Oper ations

Quality Assurance

Plan

(OQAP).

The new-plan

was found by NRC Region

V

to describe

a

QA program that,

when implemented properly, will meet the

requirements of Appendix 8 to 10

CFR Part

50 and is therefore

acceptable.

This conclusion

was concurred with by the

NRC Office of

Nuclear Reactor Regulation

and was transmitted to the licensee

by letter

dated January

30,

1992.

The licensee

expects to implement the

OQAP on

April 29,

1992.

The most significant organizational

change in the

QA organization during

the past year was the selection of a new

QA Director in November

1991.

The inspector

reviewed the Director's qualifications against the Palo

Verde

UFSAR section

17.2. 1.1.5.

The experience

and qualifications were

found to meet or exceed

the minimum requirements

specified.

However,

the inspector noted the licensee

had no documentation

to support that

the Director or other

QA manager qualifications

had been

reviewed

against

UFSAR requirements.

The licensee

acknowledged this comment

and

agreed to consider documenting this review as part of their selection

process.

The inspector

reviewed several

1991

QA audits in the areas of refueling

operations

(Audit 91-06), corrective action (Audit 91-08),

maintenance

and inspection

(Audit 91-12),

and operations/technical

specifications

(Audit 91-16).

The audit scope

and purpose

are documented

in each

report,

and the executive

summary provides

a meaningful

overview of

audit findings.

The report format also includes

a section of results

relative to management

expectations

given to the audit team at the

beginning of the audit by senior

and mid-level management

in the audited

organization.

The inspector considered that answering

these

management

questions

enhanced

the audit results

because

several

important issues

were identified as

a result.

This included the fact that over fifty

percent of questionnaire

survey respondents

during audit 91-08 had

received,

but had not been personally briefed by their supervision or

management,

on the Executive Vice President's

1991 letter on Standards

and Expectations.

The inspector reviewed the audits for indications of

degraded

independence

due to the influence of these

management

questions

on the audit and concluded that audit results

remained

independent

and

appropriate

in scope

and depth.

The inspector

reviewed the

1991

and

1992 audit schedule

and concluded that technical specification

requirements

for audit periodicity were being met.

With respect to the audit findings in the maintenance

and refueling

operations

areas

which preceded

the Unit 3 loss of power event

due to

crane operation

and the Unit 2 core alteration without an

SRO present,

for which escalated

enforcement

was issued in January

1992, the

inspector

concluded the following:

a.

Audit findings appeared

in general

to be performance

based

and

focused

in areas of relative importance.

The findings of

-15-

~

~

0

b.

deficiencies

in areas

such

as

SRO control of refueling activities

and maintenance

performed without procedures

or instructions

indicate that the audit teams

are properly sensitive to the type

of potentially significant performance

problems that

became

apparent

during the above noted events.

The maintenance

audit was

noted to be particularly performance

based.

In the case of findings noted in (a), the

gA audits did not

identify programmatic

issues

related to these deficiencies

which

contributed to the events in Units 2 and 3.

For example the

refueling operations

audit noted weak procedural

control of SRO

responsibilities

and the maintenance

audit noted technicians

working beyond their work order.

Both areas of weakness

were

identified in NRC findings related to the escalated

enforcement

issues.

The inspector concluded that

gA audits found indications

of weakness

in these

areas,

but did not develop programmatic

issues.

c ~

Line management

response

to the audit findings appeared

to be weak

in that these specific deficiencies,

although not presented

as

programmatic

problems,

were not dealt with as indicators of

potentially significant weakness.

Thus, similar deficiencies of

maintenance

practices

and refueling procedures

became

apparent

during

NRC review, of the above noted events.

The inspector further noted that in audits

91-08

and 91-12,

gA

identified that line management

response

to previously identified

programmatic

problems

was not effective.

In one case,

the previous

issue

had

been closed

by gA based

on line management

commitments to

complete

documenting regulatory commitments within procedures

(Corrective Action Report 89-12), which was then not completed.

The

other case

involved lack of preventive maintenance

tasks for warehouse

stored

items (Corrective Action Report 90-01).

This issue

had

been

closed

by gA based

on the promulgation of procedure

requirements

and

required tasks for applicable stored items.

However,

gA subsequently

found numerous

examples of improper program implementation.

The

inspector concluded that line management

response

to gA findings was not

always effective and that

gA appropriately identified these

examples.

Overall the inspector concluded that within the areas

reviewed,

the

gA

program meets regulatory requirements

and that audits

are appropriately

stressing

issues of importance.

The inspector

encouraged

the licensee

to improve auditing effectiveness

at identifying programmatic

weakness,

and for line management

to more carefully examine

gA audit findings of

deficiencies for underlying weaknesses,

to encourage line supervision

and 'management

to increase their attention to such findings in their

area of responsibility,

and

when programmatic

weakness

is identified to

ensure it is resolved without reliance

on further gA auditing.

The licensee

acknowledged

the inspectors

observations,

stressing their

commitment to use

gA findings as

a means of effecting improvement.

In

addition, senior licensee

management

stressed

'that the use of other

I

-16-

indicators,

such

as the Condition Report/Disposition

Request

(CRDR)

program,

were used to inform management

of adverse

trends

which could

signal underlying weaknesses.

The inspector

encouraged

the use of such

programs

as potentially valuable line management

tools, which could

complement

gA program efforts.

No violations or deviations

from NRC requirements

were identified.

15.

ollowu

on

rev ous

de t

ied

tems

92701

and 92702

a.

UUQ~

(1)

C osed

'at

o

5

90-36-0

.

" 'ed

0 erator

ed'cal

cords" -

t

The following three procedures

were implemented

by the licensee

to

manage the licensed operator medical records,

medical

examinations,

and requalification program requirements

for license

renewal.

01PROLC01

-, "Operator Medical

Program"

15ACOLC01 - "Obtaining, Updgrading,

and Maintaining Operator

Licenses"

01DPOLC01 - "Operator Medical Examinations"

The inspector

examined

these

procedures

to determine that the

licensee's

corrective actions

were implemented.

The procedures

addressed

all of the identified concerns

from the Notice of

Violation.

The concerns

included ensuring that the medical

examinations

met the applicable standard.

Further,

the operators

would be examined every two years

as required for maintaining

licensed status.

This'item is closed.

b.

Unit 2

(1)

Closed

Foll owu

Item

529 91-29-03:

"Main Steam Isolation

give

MSIV

Inadvertent Closure" - Unit 2

92701

This item involved an inadvertent closure of MSIV 181 while the

unit was at

100 percent

power.

This item was left open

because

Engineering Evaluation

Request

(EER) 90-SG-221,

which was written

following a previous similar event,

recommended

that the solenoid

which failed during the earlier event

be replaced

every other

refueling outage

and yet the licensee's

work control database

still showed

a replacement

interval of 93 months.

Since this

event,

administrative control procedure

70AC-OEE02,

"Engineering

Evaluation Request,"

has

been revised.

Step 3. 1.7 now requires

that

a Condition Report/Disposition

Request

(CRDR) be initiated to

track

EER disposition actions.

In addition, the inspector

was

informed that

EER 90-SG-221

had

been provided to the Preventive

- 17-

'L

(2)

Haintenance

(PH) Task Force

and this

PM task will be revised to

incorporate

EER 90-SG-221

recommendations

when the

SG system

PHs

are reviewed.

The, inspector concluded that the above actions

appeared

appropriate.

This item is closed.

.

C osed

V olatio

5 9 9 -40-01

" ot

a

c

t

e ic e c'es"

Unit

92 0

This violation addresses

two examples of hot particle control

deficiencies

observed

by inspectors

during the Unit 2 refueling

outage.

(a)

One example involved personnel

who crossed

a Hot Particle

Control Area

(HPCA) going to and from the refueling bridge,

which was

a contaminated

area but not an

HPCA.

Mhen

returning from the refueling bridge, the.personnel

were not

wearing the additional set of rubber gloves specified in the

Radiation

Exposure

Permit

(REP) pre-job briefing.

The

licensee

determined that this occurred

because

of a lack of

understanding

of the special

requirements for this

REP by

the roving Radiation Protection

(RP) technician in

containment

who supported this job,

and due to the personnel

involved not recognizing that they needed

enough gloves for

two transits through the

HPCA.

The licensee's

corrective actions

included reviewing the job

to confirm the appropriateness

of the

REP pre-job briefing

requirements,

briefing the personnel

involved,

and posting

a

copy of the pre-job briefing at the

HPCA entrance

so that

, all

RP technicians

would be aware of the specific provisions

made for this job.

(b)

The second

example involved the failure of RP technicians

to

monitor workers inside

an

HPCA for hot particles at least

every 30 minutes

as required

by the

REP.

Upon

identification of this condition, the workers were monitored

and

no hot particles

were found.

The licensee

counseled

the

RP technicians

involved and reviewed the monitoring

requirements

with other

RP technicians

in Unit 2.

The

Radiological Controls

Problem Report describing the incident

was forwarded to the

RP managers

in Units

1 and 3.

The inspector

reviewed the licensee's

corrective

actions

and

considered

them adequate.

Further inspections

during the Unit 2

refueling outage did not identify additional hot particle control

problems.

Based

on the above, this it'em is closed.

(3)

Closed

Followu

Item

529 91-04-02

"Test

Gas Concentration

ccurac

" Unit 2

92701

This item is addressed

in paragraph

4 of this report.

18 -'

c ~

gnit 3

ol

ow

t

m

30

9 -35-0

" oca

e Test

This item address

the determination of the Root Cause of Failure

(RCF) of the October 7,

1991,

LLRT of 42-inch diameter

Containment

Purge

(CP) valve CPA-UV-2A in Unit 3.

The test pressure

was not

able to be achieved or maintained in this valve,

even though it

had not been manipulated

since its previous

LLRT.

The inspector reviewed Condition Report/Disposition

Request

(CRDR)

3-1-0141,

which documents

the licensee's

evaluation

and

RCF

determination.

The licensee

determined that there

have

been eight

previous

LLRT failures of 42-inch

CP valves installed in the three

units.

Plant

Change

Request

(PCR) 91-13-001

had

been generated

to enable installation of a blind flange

on the discharge of each

penetration

on the basis of these failures, but had not been

implemented.

As a result of this failure and one subsequent

LLRT

failure, the

PCR has

been

approved

and the design is scheduled

to

be complete

by May 15,

1992.

Installation has not yet been

scheduled.

The licensee

determined that seven

hand-wheel

turns

(HWT) of the

manual. operator

were required before disk motion was observed

in

this valve,

and the closing limit switch in the motor operator

was

set at seven

HWT from closed to allow for the valve to coast

closed after limit switch actuation.

The licensee

noted that the

lack of a visual inspection prior to valve manipulation

eliminated'aluable

"as-found" information.

(2)

The licensee determined that the failures most likely occur

because

the disk slips off the tapered

seat if the disk is not

squarely centered

on the seating

surface.

As

a corrective action, the

CRDR recommends that, until the

PCR is

implemented,

a visual inspection of the valve disk position

on the

seat

be performed following valve cycling to ensure it is square

on the valve seat.

This action is being tracked

by the licensee.

The inspector concluded that the licensee

was slow to recognize

and take corrective action =for the many

LLRT failures of the 42-

inch

CP valves,

but that the current corrective actions

appear to

be appropriate.

Based

on the above review and the licensee's

planned actions, this item is closed.

Closed

V'olation

530 91-40-02

"Reactor Startu

Procedure

Not

Followed" - Unit 3

92702

This violation occurred

when Unit 3 operators

withdrew Control

Element Assemblies

(CEAs) in a manner that violated procedure

-19-

430P-3ZZ03,

"Reactor Startup."

This condition was identified by

the inspector at the time of the event.

Upon identification of the incorrect action, the licensee

reinserted

the

CEAs to the

ECRP 500 pcm.position

and performed

the required evaluations,

which revealed

no unexpected

or unsafe

conditions.

The control

room personnel

reviewed the procedure

and

determined that the intent of the procedure

was to stop

CEA

withdrawal at the

ECRP

500 pcm position.

The Assistant Shift

Supervisor directing the startup

was counseled.

Subsequently,

the

reactor startup procedures for all,three units were revised to

more clearly delineate

the required actions.

The inspector

reviewed the procedure revisions.

The procedure

in

effect at the time of the event

was clear to the inspector, =but

'the enhanced clarity of the revised procedure. appears

to reduce

the possibility of misinterpretation

or misunderstanding.

This item is closed

based

on the above review.

0 en

Followu

Item

530 91-50-02

"Steam Generator

Low

ressure

eactor Tri

Set o'nt Shift" - Unit 3

9 701

This item addresses

a condition observed

several

times in Unit 3,

and

now in Unit 2, in which the steam generator

(SG) low pressure

reactor trip (and main steam isolation actuation)

setpoints

in the

Plant Protection

System

(PPS)

have shifted without explanation to

a value below the Technical Specification

minimum allowed value of

912 pounds per square

inch absolute

(psia).

In each

case,

the

shift was to approximately

200 pounds

per square

inch (psi) below

the steam generator

pressure

at the estimated

time of the shift,

consistent with the function of the setpoint

manual

reset

pushbutton.

Only one channel

has

been

observed to shift at

a

time.

The protection

system is required,to

have

3 to 4 channels

operable,

therefore the occurrences

have not resulted .in an unsafe

condition.

The history of this issue

was outlined in inspection report 50-

528/91-50.

Additional information reviewed since that report is

provided below:

On July 20,

1990, in Unit 1, during restoration

from the

partial

performance of a monthly surveillance test

(ST)

(test

PPS channel for one

SG only), technicians

noted that

the setpoint for the second

SG does not get reset.

The

licensee

reset the setpoint

and discussed

the condition with

the vendor.

The monthly ST was revised

and

a change to the

control

room daily midnight surveillance

was submitted to

verify the setpoints

during the daily channel

checks.

-20-

k

.4

On November 8,

1991, the

PPS channel

"B" as-found pretrip

setpoints for both

SGs were found low in Unit 3 during

monthly surveillance testing.

=The trip setpoints

were

unaffected.

CRDR 3-1-0197

was initiated.

A failed diode

was found in the setpoint circuit, and the circuit was

repaired

and retested.

On February 4,

1992, at 5:53

PH (HST), the Unit

1 Assistant

Shift Supervisor

found the

PPS channel

"B" number

2

SG

setpoint low following partial performance of surveillance

procedure

36ST-9SB02,

"PPS Bistable Trip Units Functional

Test," due to the failure to correctly perform a procedural

step.

This event is further discussed

in Paragraph

7 of

this inspection rep'ort.

On February

5,

1992, Unit 2 operators

found the

PPS channel

"B" setpoints

low for both

SGs during the hourly

verification.

At the time,

PHS monitoring had

been

installed in Units

1 and 3, but only in channels

"A" and

"D"

in Unit 2,

so the exact event time was not able to be

determined.

A CRDR was initiated for trending.

The

licensee

completed the

PHS monitoring implementation.

Troubleshooting -of the

PPS did not identify any problems.

Licensee

management

asked the vendor for further analysis of

the condition.

On February 8,

1992,

both SG=-setpoints for PPS channel

"B"

in Unit 2 were detected

low by the

PHS.

A CRDR was

initiated for trending.

The channel

was left in bypass

and

a recorder

was connected to the channel

to monitor the

setpoint

more precisely.

On February 9,

1992,

both

SG setpoints for PPS channel

"B"

in Unit 2 were detected

low by the

PHS.

The recorder did

not capture the event

because it had tripped

on signal noise

before the event occurred;

A CRDR was initiated

for'rending.

The channel

was left in bypass.

The security

access

logs for the remote

shutdown

panel

area

were reviewed

for both this event

and the February

8 event,

and the

licensee

determined that there

was

no basis for further

consideration of any individual intentionally or

accidentally resetting the setpoints

from the remote

shutdown panel.

The licensee

looked unsuccessfully for

potential electromagnetic

or radio frequency interference

(EHI/RFI) sources

around the event time,

and confirmed that

the process

instrumentation

cable shield were grounded

as

designed.

The licensee

determined that the identically designed

pressurizer

low pressure

reset circuit would not show

a setpoint shift if

reset at normally operating pressure,

since the reset

changes

the

setpoint to 400 psi below the current pressurizer

pressure

-21-

,r

(normally 2250 psia),

but the maximum setpoint possible is 1837

psia.

Therefore, if that circuit is vulnerable to the

same type

of problem, the setpoint would remain unchanged

and the problem is

not being observed.

The licensee

does not believe that grounds

are causing the

problem, since grounds

are only known to have occurred nearly

coincident with one of the unexplained

events.

Grounds less

than

the alarm threshold

have not been considered.

The licensee

has discounted

the possibility of EHI/RFI as

a cause

on the basis of its evaluation of the circuit and the statements

of people in the area of the instrumentation

at the time of the

most recent

two events.

In reviewing the Night Order and Control

Room Data Sheet

directing'ourly

verification of the setpoint,

the inspector noted that the

-acceptance

criteria is vague.

The operators

are instructed to

check setpoints

hourly on Control

Board

B05 at "approximately

919

psia" for Modes

1 and 2.

The licensee modified the hourly

verification acceptance criteria to use the alarm typer printout,

which is

a digital representation

of the setpoint.

This item will remain

open pending completion of the licensee's

evaluation of these setpoint

changes.

Units

2

and

3

Closed

Violation

528 529 530 91-4 -0

"Fa'lu

e to

ollow

rocedures"

Units

2

and

9 70

This item involved three examples of failure to follow procedures.

The first two examples

involved the failure of licensed operators

to verify that no trip inputs were present

when the

BOP-ESFAS

channel

was removed from bypass resulting in a Control

Room

Essential

Filtration Actuation Signal

(CREFAS).

The operators

responsible for the first two events

were temporarily removed

from

shift and disciplined.'n addition,

a letter written discussing

the first event,

was sent to all licensed

personnel

in Unit 3 and

to supervisory

and management

personnel

in Units

1 and 2.

Shift

Supervisors

in Units

1 and

2 discussed this event with their

operating

crews.

The inspector reviewed Licensee

Event Reports

530/91-009-00

and 528/91-012-00,

which were written as

a result of

the first two events

and

had

no further questions.

Following the

second

event the licensee verified that the operator

involved was

aware of the first event

and the Vice President of Nuclear

Production discussed

the second

event with the involved operators.

The third example involved

a licensed operator allowing the

Reactor Coolant System

(RCS) level to 'rise enough to overflow the

reactor vessel

flange.

The operator

involved was disciplined,

the

on-shift crew was briefed

on the evolution

and the consequences

of

-22-

C

y

~ ~

C

not maintaining constant vigilance of RCS level.

Subsequent

operating

crews were directed to assign

a dedicated control

room

operator to maintain the required

RCS level until normal automatic.

level control

was restored.

As a result of these

and other personnel

errors,

APS has

instituted additional

management

oversight of operations with

particular emphasis

on coamunications,

command

and control,

and

adherence

to procedures.

In addition,

a special

evaluation of

personnel

performance

issues is being conducted to better

understand

the root causes.

The inspector

has observed

this'dditional

management

presence

in the field and has determined

that this has provided management

with more information regarding

practices

in the field and

a better understanding

by personnel

in

the field of management

expectations.

The inspector will continue

to evaluate

personnel

performance with particular emphasis

on the

use of procedures.

The inspector concluded that the above actions

appeared

appropriate.

This item is closed.

No violations of NRC

requirements

or deviations

were identified.

16.

~Ei

Exit meeting

was held on March 5,

1992, with licensee

management,

during

which the observations

and conclusions

in this report were generally

discussed.

The licensee

did not identify as proprietary

any materials

provided to or reviewed

by the inspectors

during the inspection.

-23-