ML17305B676

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Insp Repts 50-528/91-19,50-529/91-19 & 50-530/91-19 on 910512-0615.Violations Noted.Major Areas Inspected:Review of Plant Activities,Engineered Safety Feature Sys Walkdowns, Surveillance Testing & Fire Watch Training
ML17305B676
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 07/23/1991
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305B674 List:
References
50-528-91-19, 50-529-91-19, 50-530-91-19, NUDOCS 9108130068
Download: ML17305B676 (30)


See also: IR 05000528/1991019

Text

Re ort Nos.:

Docket Nos.:

License Nos.:

Licensee:

Faci 1 it

Name:

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

- 50-528/91-19,

50-529/91-19

and 50-530/91-19

50-528,

50-529

and 50-530

NPF-41,

NPF-51

and NPF-74

Arizona Public Service

Com'pany

P. 0.

Box 53999, Station

9012

Phoenix,

AZ 85072-3999

I

Palo Verde Nuclear Generating Station

Units 1,

2 and

3

Inspection

Conducted:

May 12 through June

15,

1991

Ins ectors:

D. Coe,

Senior Resident

Inspector

F. Ringwald,

Resident

Inspector

J. Sloan,

Resident

Inspector

H. Wong,

Region

V Section

Chief,

P. Galon,

Region

V Inspector

( Intern)

P.6.

7- z.p-9/

. Wong,

h ef

g

Reactor Projects

Section II

Ins ection

Summar

Ins ection

on Na

12 throu 4 June 25, 199I

Re ort Numbers

50-528/9 -

9

50-529/9 -

9

an

50-530/91-

9

~AI

d:

I, I,

gg

dg

gggf

I

I

I

resident

inspectors

and

one inspector intern from the Region

V staff.

Areas

inspected

included: previously identified items; review of plant activities;

engineered

safety feature

system walkdowns - Units 1,

2 and 3; surveillance

testing - Units 1,

2 and 3; plant maintenance

- Units 1,

2 and 3; hydrogen

analyzer fai lure due to mispositioned

valve - Unit 1; auxiliary feedwater

(AFW) pump trip throttle valve limits - Unit 1; spray chemical

addition

pump

inoperability - Unit 1; emergency

safeguards

features

actuation

system

(ESFAS)

actuation - Unit 1; maintenance

on wrong components

- Units

2

E 3; radiation

protection

(RP) technician in

a high radiation

area

(HRA) without an alarming

dosimeter - Unit 3; worker responsibility - Unit 3; refueling activities

and

startup

from refueling - Unit 3; valve prematurely released

to operations

- Unit 3; Westinghouse

ARD relay failure - Unit 3; Combustion Engineering

(CE) technical

performance - Units 1,- 2

im 3; "B" charging

pump Technical

Specification

(TS) interpretation - Units 1,

2

E 3; safety analysis error-

Units 1,

2

and 3; essential

and emergency lighting train separation-

Units 1,

2 and 3; fire watch training - Units 1,

2

and 3;

and review of

Licensee

Event Reports

- Units 1,

2

and 3.

9108130068

910723

PDR

ADQCK 05000528

0

PDR

-2-

During this inspection

the following Inspection

Procedures

were utilized:

30702

> 60710

s 61726 ) 62703

s

64704

p 71707

p 71710

p 71711

p 92700

g 92701

p

92702

and

93702

Results

Of the

22 areas

inspected,

3 violations were identified.

The

~v>o at>ons

involved three

examples

of workers not following procedures

which caused

unintended plant events,

a technician

not following the

Radiation Exposure

Permit by entering

a high radiation area without an

alarming dosimeter,

and fire watches

performing duties without being fully

- qualified.-

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters

None

Summar

of Violations

3

Cited Violations

1 - Unit 3,

1 - Units

2 and

3

1 - Units 1, 2,

and

3

Summar

of Deviations

Hone

0 en Items

Summar

Stren ths

Noted

8 items closed,

0 items left open,

and

5 new items opened.

While the Unit 1 spray chemical

addition system malfunction required

an

NRC

Temporary Waiver of Compliance to complete troubleshooting

and repairs. beyond

the time allowed by the Technical Specification Limiting Condition for

Operation,

plant

and engineering

personnel

were aggressive

in conducting

testing to identify the complex multiple causes.

Although the unbolting of an

online reactor coolant

pump seal injection filter during maintenance

occurred

as

a result of

a personnel

error, the prompt action by operations

to mitigate

the consequences

was noteworthy.

In addition, the Prefire Strategies

unit

walkdown and the Equipment gualification evaluation

which discovered plant

deficiencies

and resulted

in immediate

compensatory

actions

represents

proactive plant evaluations.

Weaknesses

Noted

Worker performance

issues

dominated this inspection period.

Of particular

concern

was the unbolting of an onli.ne reactor

coolant

pump seal injection

filter cover which resulted

in

a small unanticipated

reactor coolant leak by

a

mechanic,

with an

RP Technician

and

a

gC Inspector present.

This event

reflected

breakdowns

of several

barriers in the work control process.

The

RP Technician in

a High Radiation

Area without the alarming dosimeter required

by the Radiation Entry Permit represents

the second

instance identified by the

NRC in which this has occurred.

DETAILS

Persons

Contacted

The below listed technical

and supervisory

personnel

were

among

those contacted:

Arizona Public Service

(APS)

R.

  • J

J.

B.

D.

  • C
  • T

P.

L.

W.

E.

  • R
  • R

R.

D.

  • p
  • W.
  • S

F.

  • J

D.

D.

  • p

J.

  • T
  • G

T.

F..

  • R
  • C

R.

T.

J.

  • J

G.

G.

B.

Adney,

N. Bailey,

A. Bailey,

Ballard,

Blackson,

Boswell,

Bradish,

Caudi ll,

Clyde,'onway,

Dotson,

Flood,

Fountain,

Fullmer,

Gouge,

Hughes,

Ide,

Kanter,

Larkin,

Levine,

Marks,

Mauldin,

Maynard,

Minnicks,

YIurphy,

Overbeck,

Radtke,

Riedel,

Rogalski,

Russo,

Schaller,

Schriver,

Scott,

Scott,

Shell,

Waldrep,

Webster,

Plant Manager, Unit 3

Nuclear Safety

& Licensing,

Vice President

Nuclear Engineering,

Director

Quality Assurance,

Director

Central

Maintenance,

Manager

Nuclear Safety,

Engineer

Compliance,

Manager

Site Services,

Director

Operations

Manager, Unit 3

Executive Vice President,

Nuclear

Engineering

5 Construction, Site Director-

Plant Manager, Unit 2

QA Deficiency Coordinator

Quality Audits and Monitoring, Manager

Plant Support,

YIanager

(Chairman Plant Revie

Site Radiation Protection,

General

Manager

Plant YIanager, Unit I

APS Site Representative

Security,

Manager

Nuclear

Power Production;

Vice President

Nuclear Safety,

Manager

Site Maintenance,

Manager

Site Nuclear Engineering Dept., Sr.

Mech.

En

Maintenance

Manager,

Unit 3

RYIS Supervisor,

Chemistry

Technical

Support, Site Director

Operations

Supervisor,

Unit 3

Operations

Manager, Unit I

Audit Supervisor

Quality Control, Manager

Assistant Plant Manager,

Unit

1

Assistant Plant Manager, Unit 2

Assistant Plant Manager, Unit 3

Chemistry General

Yianager

Duality Systems,

Manager

Plant Modification Department,

Manager

Component Specialty Engineering,

Manager

w Bd.)

gineer

Other Personnel

  • A.

J.

  • K.
  • R.

Cordova,

Draper,

Hall,

Henry,

Public Service of New Yiexico Site Representative

Southern California Edison, Site Representative

El

Paso Electric, Site Representative

(EPE)

Salt River Project, Site Representative.

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

  • Attended the Exit meeting held with the

NRC Resident

Inspectors'on

June

20,, 1991.

2.

~P

A.

Unit

1

Identified Items - Units

1

2 and

3

92701

and

92702

(Closed

Foll owu

Item (528/90-54-01:

"Turbine Driven

Auxi >ar

Feedwater

AFM

Porn~Bi Leuc

s

- Units

1 and

3

~92701

This item refers to the licensee's

evaluation of the cause

and

significance of oil levels which have

been

observed

to be above

the high level marks

on the sight glasses

for the turbine

driven

AFW pumps

(AFA-POl) in Units

1 and 3.

The inspector

reviewed Engineering

Evaluation Report

(EER)

91-AF-001, in which the licensee

determined that the oil levels

had increased

due to thermal

expansion after being taken from

storage

{at about

45 degrees

Fahrenheit)

and

added to the

turbine.

The average

bulk oil temperature

in the turbine was

estimated

to be

110 degrees

Fahrenheit,

and the calculation

provided in the

EER demonstrated

that sufficient oil expansion

would occur to result in the observed

high levels.

Instruction

Change

Request

2504S

was submitted to add

a caution statement

to the preventive maintenance

task for oil changes

to warn

personnel

that thermal

expansion

might result in high oil

levels if the oil is not allowed to adjust to normal

room

.

temperature prior to adding to the turbine.

The licensee further determined

in

EER 91-AF-001 that the

observed

levels were not high enough to cause

a turbine

operability concern,

as the level

was about'-3/4

inches

below

the invert elevation of the turbine shaft.

2.

Based

on the above review, this item is closed.

$Clo~sed

Follow~uItem j528/91-01-03:

"Potential for

Small

Break

LOCA Bue to Tube Rupture

in the Reactor

CooMant Pum~SeaT

CooTer

- Units. 1,

2 and 3~9270TI

This item resulted

from the licensee's

identification of the

possibility of a small break intersystem

LOCA which would occur

if tubes in the Reactor

Coolant

Pump High Pressure

Seal

Cooler

failed.

The licensee's

Justification for Continued Operation

(JCO)

was reviewed

by the

NRC staff.

The licensee

revised

the

JCO based

on

NRC staff comments.

In a Nay 20,

1991 letter to

the licensee,

the

NRC accepted

the technical

basis for the

JCO

and the compensatory -measures

committed to by the licensee.

The licensee

committed to initiate an orderly plant shutdown if

Reactor

Coolant System

(RCS) activity exceeds

0.2 uCi/gm dose

equivalent

I-131 for more than

48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />

and

be in at least

Mode

3 within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,

and to modify procedures

to

require initiation of

a plant shutdown within four hours of

identification of RCS activity in the nuclear cooling water

system.

A design modification to correct the identified

deficiency is anticipated

by the licensee

to be completed in

all units

by November

1993.

Based

on completion of the

NRC review of the JCO, this item is

closed.

B.

Unit 2

(Closed)

Followu

Item (529/91-01-01

, "Incorrect Lube Oil

82eB to~ox>>ar

eedwater

um

an

onc

ci

Makeup

~Pum

- Unit 2

92701

The licensee identified several

instances

in which the

incorrect lube oil was

added to various plant equipment.

Incident Investigation Report

( IIR) 3-2-91-003

was initiated to

investigate

these. incidents.

IIR 3-2-91-003

was subsequently

superseded

by Corrective Action Report

(CAR) 91-0005,

which the

inspector

reviewed.

The licensee

appeared

to perform

a thorough evaluation of these

incidents,

including the technical significance of using the

incorrect lube oil.

Procedural

non-compliances

and inadequate

procedures

were determined

to have resulted in the Lube Mianual

not being updated

when the Preventive

Maintenance

(PM) tasks

were revised,

and in

PM tasks

being revised without

documentation of justification.

Additionally, improper or

inadequate

labeling of secondary

storage

containers

was

identified as

an additional deficiency.

The licensee

reviewed

all.PM tasks

to identify differ'ences with the Lube Manual,

and

initiated procedural

changes

to prevent further discrepancies.

All existing differences will be resolved

by Engineering.

The

Lube Manual will become

the source

document for determining the

correct lube oil.

Many corrective actions

have

been

completed,

with the remainder

scheduled for completion

by July 15,

1991.'he

inspector

concluded that the licensee's

actions

were

appropriate

and appeared

adequate.

Based

on this review, this

item is closed..

3.

Review of Plant Activities+71707

and

9~3702

'.

Unit

Unit

1 operated

at essentially

100'X power throughout the reporting

period.

B.

Unit 2

Unit 2 operated

at essentially

lOOX power throughout the

reporting period.

C.

Unit 3

The unit began this inspection period in mode 5.

Reactor startup

from refueling occurred

on Nay 31,

1991

and

was followed by low

power physics testing.

The reactor

was

shutdown

on June

1, 1991,

for control element

assembly indication troubleshooting

and repair.

The next approach

to criticality occurred

on June 2,

1991

and the

plant proceeded

with power ascension

testing.

The plant ended

the

inspection

period at

100Ã power.

D.

Plant Tours

The followin'g plant areas

at Units 1,

2 and

3 were toured

by the

inspector during the inspection:

Auxiliary Building

Control

Complex Building

Diesel

Generator

Building

Radwaste

Building

Technical

Support Center

Turbine Building

Yard Area

and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Logs

and Records - Records

were reviewed against

>>n

d

d

procedure

requirements.

2.

N~lonitorin

Instrumentation

- Process

instruments

were

h

1

d f

conformance with Technical Specifications

requirements.

3.

Shift Staffing - Control

room and shift staffing were

observed for conformance with 10 CFR Part 50.54.(k),

Technical Specifications,

and administrative

procedures.

4.

Equipment Lineu2s - Various valves

and electrical

breakers

were verified to be in the position or condition required

by Technical

Specifications

and administrative

procedures

for the applicable plant mode.

5.

E~ui ment T~a~in

- Selected

equipment, for which tagging

requests

tiad been'initiated,

was observed

to verify that

tags

were in place

and the equipment

was in the condition

specified.

6.

7.

8.

9.

10.

General

Plant

E uipment Conditions - Plant equipment

was

onserved

or

>n >cat>ons of system

leakage,

improper

lubrication, or other conditions that could prevent the systems

from fulfillingtheir functional requirements.

Fire Protection - Fire fighting equipment

and controls were

onoserve~or

conformance with Technical Specifications

and

administrative

procedures.

The inspector

observed

several

examples of deficient thermolag

on safety-related

components

in the Unit

1 Main Steam Support

Structure.

These observations

were passed

to Region

It and

NRR

personnel

performing

a fire protection inspection

(See

NRC

Inspection

Report 528/91-21).

Plant Chemistry - Chemical analysis results

were reviewed for

T

1

i

1S

if'

d

d

control procedures.

Secur~it

- Activities observed

for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

included vehicle

and personnel

access,

and protected

and vital, area integrity.

A tour of the

SAS was included during this report period.

Plant

House~kee

ing - Plant conditions

and material/equipment

storage

were observed

to determine

the general

state of

cleanliness

and housekeeping.

Radiation Protection Controls - Areas observed

included control

point operation,

records

of Ticensee's

surveys within the

Radiological Controlled Areas

(RCA), posting of radiation

and

high radiation areas,

compliance with Radiation

Exposure

Permits

(REP), personnel

monitoring devices

being properly

worn,

and personnel

frisking practices.

The inspector

observed

a radiation worker turn in an alarming

dosimeter

to

a Radiation Protection

(RP) Technician at Unit

One.

The

RP Technician turned off the alarming dosimeter

without reading it.

When questioned,

the

RP Technician replied

that

he

assumed

that based

on his knowledge of where the

radiation worker had been,

the alarming dosimeter

reading

was

not significant and that the Self Indicating Dosimeter

(SID)

was the dosimeter of record for the entry.

The SID indicated

that minimal exposure

had occurred.

The inspector

commented

that all available dosimetry information should

be evaluated

and inconsistencies

resolved

since comparison of redundant

readings

can identify dosimetry failures or unusual

radiation

field patterns.

The licensee

responded

by questioning all

RP

Technicians

on that shift and identified two of eleven

RP

Technicians

who routinely turn off alarming dosimeters

without

reading

them.

Based

on this survey,

the licensee

has affixed

a

sion at the Unit

1 Radiological

Reports

and Access

Control

System

(RRACS) computer terminal advising every

RP Technician

to read alarming dosimeters

when they are returned.

In

addition, the licensee

issued

a

memo to all Unit

1

RP

Technicians

stating the management

expectation that all

dosimetry data will be read

and evaluated.

A copy of 'this

memo

was sent to the

RP Managers

at Units

2 5 3.

No violations of NRC requirements

or deviations

were identified.

4.

En ineered

Safet

Feature

S stem Walkdowns - Units 1,

2 and

3

71710

Selected

engineered

safety feature

systems

(and systems

important to

safety)

were walked

down by the inspector to confirm that the systems

were aligned in accordance

with plant procedures.

't

During this inspection period the inspectors

walked

down accessible

portions of the following systems.

Unit 1:

Safety Injection Train "8"

Emergency Diesel

Generator

"A" and "8"

Unit 2:

Emergency

Diesel

Generator

"A" and "8"

Unit 3:

Emergency

Diesel

Generator

"A" and "8"

No violations of NRC requirements

or deviations

were identified.

5.

S ill~i-U i

i, 2,

d 3

61i26

d 6i725)

A.

Selected

surveillance tests

required to be performed

by the

Technical Specifications

(TS) were reviewed

on

a sampling basis

to

verify that:

1) the surveillance tests

were correctly included

on

the facility schedule;

2)

a technically adequate

procedure

existed

for performance

of the surveillance tests;

3) the surveillance tests

had

been

performed at the frequency specified in the TS;

and 4) test

results satisfied

acceptance

criteria or were properly

dispositioned.

B.

Specifically, portions of the following surveillances

were observed

by the inspector during this inspection period:

~ e

Unit

1

Procedure

o 32ST-9ZZ03

o 73ST-1XI16

De~seri tinn

PBB-S03 Undervoltage

Relay Test

Section

XI Valve Testing - Feedwater

Isolation

Valves

Unit 2

~D

o 73ST-2X116

Section

XI Valve Testing - Feedwater

Isolation

Valves

o 36ST-9SB04

PPS Functional Test - RPS/ESFAS

Logic

Unit 3

Procecfur e

Descri tion

o 72ST-9RXOB

o 72ST-9RX11

o 43ST-3NI01

Incore Detector

Channel

Check

COLSS Ysargin Alarms

Adjustable

Power Signal Calibrations

No violations of

NRC requirements

or deviations

were identified.

6.

Plant Maintenance

- Units l~and

3

62703)

A.

During the inspection period, the inspector

observed

and reviewed

selected

documentation

associated

with maintenance

and problem

investigation activities listed below to verify compliance with

regulatory requirements,

compliance with administrative

and

maintenance

procedures,

required Quality Assurance/Quality

Control

involvement, proper

use of safety tags,

proper equipment alignment

and use of jumpers,

personnel

qualifications,

and proper retesting.

The inspector verified that reportabi lity for these activities

was

correct.

B.

Specifically, the inspector witnessed

portions of the following

maintenance activities:

Unit l

Description

o

Visual inspection of "8" emergency

diesel

generator

(EDG)

o

Change air filters on "8"

EDG starting air system

o

Lube "8"

EDG turning .gear

and bull gear

o

Change

"8" EDG turning gear motor oil

o

Calibration of 1JDGNPI80 (lube oil pressure

at engine for "8"

EDG)

Unit 3

Descry

tion

o

Reload

power ascension

test

o

Reload criticality and low power physics testing

o

CPC "C" troubleshooting

and repair, including retest

using

a

portion of 77ST-9SB03

"CPC Channel

C Calibration"

No violations of NRC requirements

or deviations

were identified.

Hydrogen

Anal zer Failure

Due To Nis ositioned

Valve

Unit l ~92700)

On Yiay 27,

1991, the Unit

1 "A"'ydrogen analyzer failed to meet the

acceptance

criteria of surveillance test 41ST-lHP02,

"Containment

Hydrogen Analyzer Functional Test."

This was later determined

to be

caused

by a mispositioned

reagent

gas valve.

The licensee initiated

Condition Request/Oisposition

Request

(CROR) 1-1-001 to document its

investigation of the event.

This review failed to conclusively determine

the root cause of the valve being mispositioned.

The licensee is

considering

actions to reduce

the possibility of recurrence.

The inspector

reviewed the operability of the "8" hydrogen analyzer since

the previous

successful

surveillance test of the "A" .hydrogen analyzer

and determined that both the hydrogen analyzers

were not 'simultaneously

inoperable for longer than the

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed by Technical

Specifications

and the "8" hydrogen analyzer

was unavailable

less

than

the

30 days allowed by TS.

No violations of NRC requirements

or deviations= were observed.

Auxiliar

Feedwater

(AFM)

Pu~m ~Tri

Throttle Valve Limits-

Un>t

1

00~

On Yiay 28,

1991, during the performance

of a manual test of the overspeed

trip mechanism of the Unit

1 turbine-driven

AFW pump (1AFA-P01) per

41ST-1AF02, "Auxiliary Feedwater

Pump AFA-P01 Operability Test," the trip

throttle valve

( IAFA-UV-54) could not be reset.

The licensee

determined

that limit switch

4 in the Limitorque SNC-4 motor operator for the valve

had,to

be adjusted

by 1/4 hand wheel turn

{HWT) to allow the valve to be

reset.

This adjustment

was performed

and the system

was subsequently

made

operable.

Limit switch

4 was set at 0.5

HWT (about

7 percent

open),

which is within the

0 to

10 percent

open

range specified in the Yiotor

Operated

Valve Database,

01-J-ZZI-004, for this valve, which has

a full

stroke of

7

HWTs.

However, the licensee's

experience

indicates

that

a

switch setting closer to 0.35 percent

open is necessary

for reliable

function of this system feature.

The system is designed

such that, in this mode of operation,

the motor

operator closes until either limit switch

4 or the torque switch act to

stop the motor,

and the limit switch is supposed

to be controlling. If

the motor does

not latch with the valve stem, operators

can jog the motor

further closed to engage

the latch.

This could have

been

done in this

instance,

but was not.

The surveillance

procedure

does not provide

guidance for this contingency,

and apparently

not all operators

were

aware that this action

may

be necessary

in order to allow the valve to be

reset.

The licensee

committed to issue Instruction

Change

Request

24417 to

provide this guidance in the surveillance

procedure.

Additionally, the

licensee

committed to consider revising the setpoint. for limit switch 4.

The inspector

concluded that the additional

procedural

guidance

was

appropriate

to ensure

operators

can reset the valve and reopen it as

necessary.

The licensee's

actions with respect

to this event appeared

to

be appropriate.

Ho violations of NRC requirements

or deviations

were identified.

A dii~e

bill

.

U i

9>>02)

On June

13,

1991, the licensee

requested

a Temporary Waiver of Compliance

for relief from Technical Specification

(TS) Limiting Condition of

Operability

(LCO) 3.6.2.2,

due to the inability of the "8" Spray Chemical

,Addition Pump

(SCAP) to maintain the minimum required flowrate per

ASNE

Section XI.

NRC Region

V granted

the waiver on June

13, documented this

in a letter to APS on June

14,

1991,

and the .licensee

achieved

compliance

on June

16,

1991.

The

SCAP is

a positive displacement

pump,

and the test is performed at

103 psig,

near the pressure

safety valve

(PSV) relief setpoint of

110'sig.

The licensee

determined that the pressure

pulsations

caused

by the

SCAP resulted

in the

PSV "simmering" as it failed to reseat,

thereby

establishing

an unintentional alternate

flowpath and reducing the

effective system flow to below the required value of 0.63

gpm.

During

this test,

the test pressure

is established

by manually throttling the

vent on the Spray Chemical

Storage

Tank with a 1-inch globe valve.

The

operator apparently

increased

pressure

too much, causing

the

PSV to

simmer during normal

SCAP operation.

The licensee

was able to

demonstrate

that the

pump performance

was acceptable

in several

tests

with the

PSV gagged,

"and again in several

more tests after the

PSV was

replaced

and the test pressure

carefully increased

to the required value.

Complicating the evaluation of the system

performance

was the

problem of

gas entrained

in the flow transmitter.

Erratic indication resulted

from

this condition, which was not easily resolved

due to -the absence

of a

high point vent.

The licensee installed

a temporary rotometer flow

indicator and confirmed the presence

of gas in the flow.

The =licensee

implemented

a method of backfilling the transmitter to remove entrained

gas which successfully

resolved

the indication deficiency.

The licensee

previously had implemented

a design

change

in Unit 3 which

inverted the transmitter,

making it easier

to vent.

This design

change

also increased

the

PSV relief setpoint to 120 psig, providing greater

margin for the performance of this test.

The design

change

has

not been

10

implemented

in Units

1 or

2 because'he

licensee

is pursuing deletion of

the

TS requirements

for this system.

No violations of NRC requirements

or deviations

were identified;

10.

Emer enc

Safeguards

Features

Actuation System

(ESFAS) Actuation

- Unit

1

93702T

On Nay 17,

1991, Unit

1 experienced

a Containment

Purge Isolation

Actuation and

a Control

Room Essential

Filtration Actuation due to the

failure 'of the Train "B" Power

Access

Purge

Area Radiation Yionitor,

RU-38.

All equipment

responded

as designed,

and the licensee verified that

the actuation

was spurious

and that

no abnormal radiation levels existed

in the vicinity of RU-38.

The cause of the event

was malfunctioning central

processing

unit and

random access

memory boards

in RU-38, which were old style circuit

boards.

The defe'ctive

components

were replaced with upgraded

new circuit

boards

and the monitor was tested

and returned to service.

Additionally,

the licensee

has accelerated

the schedule for replacement

of old style

boards

in the other monitors in all three units which still have not been

upgraded.

This event is also described

in Licensee

Event Report 91-006-00

(see

.paragraph

22 of this report).

No violations of NRC requirements

or deviations

were identified.

111

Mainte'nance

on Mto~nC~om onents

- Units

2

6

3

62703)

Three events

occurred involving maintenance

on the wrong component.

One

of these

events

involved an inadvertent

leak of the pressurized

charging

system resulting in

a primary to atmosphere

leak inside the auxiliary

building.

The other

two events

involved inadvertent actuations

of safety

equipment,

including an Emergency

Diesel

Generator

(EDG), the Containment

Purge Isolation Actuation System

(CPIAS),

and the Control

Room Essential

Filtration Actuation System

(CREFAS).

A.

Reactor

Coolant

Pump

(RCP)

Seal Injection Filter Changeout

On Hay 24,

1991, three Unit 3 mechanics

were to change

out the "A"

train seal injection filter, 3YiCHNF02A.

However, the workers

unbolted

the inservice

"B" train filter, 3MCHNF02B, due to:

turnover communication errors; fai lure to take the work order into

the contaminated

area

as suggested

by 300P-9MP01,

"Conduct of

Maintenance"; failure to properly verify the identification of

equipment

being worked as specified

by the work order

(WO 495993);

failure to verify the equipment

tagged

out as advised

by 40AC-90P15,

"Station Tagging

and Clearance";

and failure of the

gC inspector

present

to provide

an adequate

backstop.

As soon

as

the bolts were loose

enough,

the mechanics

observed

a

high pressure

stream of water coming out the sealing

surface.

They

attempted

to re-torque

the bolts to stop the leak, but were

unsuccessful

because

the o-ring had shifted.

An auxiliary operator

present

contacted

the control

room and control

room operators

immediately isolated

seal injection stopping the leak,

then

proceeded

with other immediate actions required for loss of RCP seal

injection.

The control

room operator actions

were done promptly to

prevent degradation

of RCP seals,

particularly seals

on an idle RCP.

The inspector

rioted that the

QC inspector

complied with the

requirements

of the

QC Plant Inspection

Report (PIR) which required

the inspector to check

each of the work order hold points,

note

correct equipment,

inspect housekeeping,

verify work authorization

and ensure control of material.

The inspector determined that the

QC'inspector

had verified correct equipment

by comparing the work

'order cover sheet

(W.O. 495772) with the equipment identification

label

on the wall near the filter housing,

but did not look at

enough of the work order to identify that the steps for changing out

the filter had already

been completed

and signed off.

The inspector

concluded that the cursory review by the

QC inspector resulted in

his failing to identify that the wrong component

was being worked

on.

The

NRC inspector discussed

this event with the

QC Manager

and

Quality Assurance

(QA) Director.

The licensee

concluded that the

QC

inspector

met their expectations

during the event.

The inspector

concluded that while certain specific

QC requirements

were met,

QC

personnel

should ascertain

that the correct work instructions for the

correct equipment

are being used

and are being followed.

In this

case,

the

QC inspector

was present for sufficient time that

a review

of the work order status

should

have identified that steps

were

being repeated.

Inadvertent

EDG Start

On May 16,

1991

a Unit 3

I&C Technician

performed part of Section

8.6.2 of procedure

36ST-9SA11

on the "8" train auxiliary relay

cabinet rather than

on the "A" train as specified

by Step 8.6.2. 1

resulting in an inadvertent start of the "8" EDG.

The inspector

noted that Step 8.6.2. 1 had

been

signed off in error.

Inadvertent

CPIAS/CREFAS - Unit 2

On June

5, 1991, while attempting to restore

the alarm setpoint

on

the containment

purge radiation monitor,

RU-34, to the post purge

setting in accordance

with procedure

74RM-9EF40, "Radiation

Monitoring System Operations,"

a Unit 2 Chemistry Effluent

Technician inadvertently

changed

the setpoint

on another radiation

monitor, RU-38, resulting in an inadvertent

CPIAS/CREFAS.

While

generic

procedure

74RM-9EF40 did not specifically identify that work

was to be performed

on RU-34, the technician

was also following

procedure

74RM-9EF20,

"Gaseous

Radioactive

Release

Permits

and

Offsite Dose Assessment,"

step 10.2.2,

which addresses

only RU-34;

and procedure

74RM-9EF42, "Radiation Monitor Alarm Setpoint

12

Determination," step 6.6.6, which also addresses

only RU-34.

The

control

panel for RU-38 is physically located just below the control

panel for RU-34 and the identification tags for RU-34 and

RU-38 are

at the bottom of the respective

control panels.

While the

technician

could have

looked at the

RU-34 identification tag

and

mistakenly 'associated it with the RU-38 control

panel

below, there

is

a keylock switch in both control panels

which must be operated

to

change

setpoints

and

a second

label is present

under

each

keylock

switch with also correctly identifies the monitor.

It'is important for maintenance

workers to follow the maintenance

program to ensure that appropriate

precautions

are followed,

especially

when maintenance

activities

have the potential for

'impacting plant operations.

The inspector

concluded that in each of

these

cases,

the maintenance workers'ailure

to follow the work

control

program directly caused

the events.

In the seal injection

filter event,

the inspector

concluded that the

gC inspector review

of the work order should

have prevented

the occurrence

of the event,

and that 'the prompt actions of plant operators mitigated the

consequences

of this event.

In each of these

cases,

the failure of workers to verify that they

were working on the correct equipment

are examples of

violations of

NRC requirements

(Violation 529/91-19-01

and

530/91-19-01).

The licensee

responded

to the first event

by initiating Problem

Resolution'Sheet

(PRS)

1572; conducting

an investigation; clarifying

the work order

and requiring

a separate

equipment identification

signoff step;

developing

a formal on-the-job training program for

this task; initiating a work request

to add equipment ide'ntification

labels to the filter lids and shield plugs; briefing all mechanics

on self and team verification practices;

evaluating

the

need for a

work order requirement

to check clearance

tags;

and disciplining

'he

APS and contract workers.

The licensee

responded

to the second

event

by initiating PRS

1544;

conducting

an investigation;

including this event in l&C quarterly

training;

and disciplining the

APS and contract

I&C Technician.

The

licensee

is evaluating possible additional corrective action.

The licensee

responded

to the third event

by initiating Condition

Report Disposition Request

(CRDR) 2-1-0004;

conducting

a

Human

Performance

Evaluation

System

(HPES) evaluation;

and disciplining the

worker.

The

NRC inspector

expressed

concern

regarding

the relatively short

interval of time in which these

three events

have occurred

and that

they each involve personnel

errors.

Senior

APS management

also

expressed

concern that each of these

events

occurred

and

was

evaluating additional corrective actions.

One violation of NRC requirements

was identified.

"t

13

Radiation Protection

(RP) Technician

in

a Ki h Radiation

A~rea

KRA

7

On Nay 31,

1991,

a Unit 3

RP Technician

was observed

by the

NRC inspector

-to enter

a posted HRA'ithout an alarming dosime'ter.

The

RP Technician

indicated 'that since

a survey meter

was being used,

an alarming dosimeter

was not required.

In subsequent

discussions

the

RP Technician identified

that

an error had

been

made.

The inspector

reviewed the

RP Technician's

Radiation

Exposure

Permit

(REP)

and confirmed that

an alarming dosimeter

was required for entry into a posted

HRA.

This is

a violation of

NRC

requirements

(Violation 530/91-19-02).

The inspector

concluded that while the significance of this was lessened

by the presence

and proper

use of an operable

survey meter,

the

REP

requirement

was not met.

In addition,

RP Technicians

are expected

to set

the standard for adherence

to

REP requirements.

A similar violation was

issued

in Inspection

Report 528/90-23

and the corrective actions

focused

on better briefings to radiation workers prior to

RCA entries.

The licensee

responded

by initiating RP Problem Report 3-91-020,

disciplining the

RP Technician involved and adding

"REP Compliance"

as

an

additional topic for the next quarterly

RP Technician training.

One violation of NRC requirements

was identified.

Marker ResRonsibilit

- Unit 3

71707)

The inspector

observed

two examples

in which workers did not follow

through with identified plant problems.

The first example occurred

on

June 4, 1991, during the performance of 72ST-9RX08, "Incore Detector

Channel

Check."

Limitations and Precautions,

step

5. 1, states

that

"Reactor

power should

be at steady state

above

20%

.

. ." and step 7.3

requires

the performer to initial that "Limits and precautions

have

been

read

and understood."

The test

was performed with BDELT power at 19.7%

power yet

no annotation

in the test log was present

documenting

the

apparent

discrepancy.

The performer told the inspector that

an

assumption

had

been

made that this limit- had

been

met because

BDELT was

within the general

Reactor

Engineering definition of their

20% power

plateau.

The inspector

acknowledged

that the minor deviation in power

level

was not significant.

The second

example occurred

on June

13,

1991,

when the inspector

identified posted

Survey

Map 326

on the

120 foot elevation of the

Auxiliary Building to be dated April 16,

1991,

when the latest

survey

map

had

been

performed in Nay 1991.

The inspector identified that

an

RP

Technician

had identified this out of date survey

map

a couple of days

earlier.

The Lead Technician stated that this did not meet their

expectations

in that when the out of date survey

was identified by the

RP

Technician, it should

have

been

updated

immediately.

The

NRC inspector

acknowledges

that local survey

maps

are for worker assistance

and that

up-to-date

surveys

are available at the

RP control point.

However, the

14

local survey maps, if not updated,

may give out of date radiological

information to workers.

This matter is also discussed

in Inspection

Report 50-528/91-23.

The inspector concluded that while the individual significance of these

two problems

were minor, the failure of the individuals to identify and

initiate corrective action reflects

a failure of workers to meet

management

expectations

and to initiate appropriate corrective actions

when deficiencies

are identified.

The licensee

acknowledged

the

inspector's

comments

and is evaluating possible corrective action.

No violations of NRC requirements

or deviations

were identified.

Refuelin

Activities and Startup

From Refuelin

- Unit 3

60710

and

7T7TT7

The inspector walked

down significant portions of the unit, with special

attention to the Emergency

Oiesel

Generators

and "8" High Pressure

Safety

Injection Train,

and concluded that the unit appeared

to be ready to

resume

power operations.

The inspector

observed

the approach

to criticality, portions of low power

physics testing,

and preparations

for performance of the rod shadowing

factor/radial

peaking factor measurement

per procedure

72PA-9ZZ07,

"Reload

Power Ascension Test," Appendix L.

In general

the licensee

conducted

these activities acceptably.

Inspector

questions

with regard

to

a lack of guidance for determination of Group

5

CEA rod worth were

resolved

based

on the minimal impact on safety significance.

The inspector

noted that initials were missing from the review block for

three reviews of the

CECOR Snapshot

Record

(72PA-9ZZ07, Appendix 8).

These occurred over

a short period of time.

The procedure

states

that

the review should

be performed at approximately hourly intervals.

This

apparent

discrepancy

was pointed out to the reactor engineering

supervisor,

who evaluated

the omissions

and determined that adequate

reviews

had occurred.

One additional

comment from power ascension

testing is in paragraph

13 of

this report.

No violations of NRC requirements

or deviations

were observed.

Valve Prematurely

Released

t~o 0 erations

- Unit 3 (61726)

Valve SI-652 was tagged

out and the actuator partially disassembled

for

an

MOV grease

inspection.

When the actuator

was reassembled,

the limit

switch clutch was not re-engaged.

The work step associated

with this

step (step 4.7 of Work Order 493034) specified reinstalling the limit

switch but did not address

re-engaging

the clutch.

The clearance

was

released

before the work was complete

and when operations

stroked the

valve,

the position indication did not change

and the actuator

backup

breaker tripped

on overload.

This occurred

because

the limit switch

never

moved from its open position

and the torque

bypass

switch remained

15

closed disabling the torque switch function.

An engineering

evaluation

of the valve concluded that

no damage

occurred

and the valve could

be

declared, operable.

The inspector

concluded that the work order

needed

to

be more detailed

and that there

was

an over-reliance

on "skill of the

craft" to remember

to re-engage

the limit switch clutch when the switch

is installed.

The inspector further concluded that there

appeared

to be

poor communications

and

a failure of the foreman to ensure that the work

was complete prior to releasing

the clearance.

The licensee

acknowledged

arid agreed with the inspector's

comments

and is evaluating corrective

actions

No violations of

NRC requirements

or deviations

were observed.

Wrestle

house

ARU Rela

Failure - Unit 3

92700)

On May 22,

1991, following the failure of a Westinghouse

ARD 660-UR relay

in a Unit 3 auxiliary relay cabinet,

the .licensee

issued Material

Nonconformance

Reports

(MNCRs) 91-ZA-9004 and 91-ZJ-9004

because

of the

potential for common

mode failure.

The relay failed due to epoxy,

possibly from the relay internals, interfering with the plunger.

The

licensee

has identified 54 continuously energized,

harsh

environment

relays of this type in safety-related

applications

in each unit,

and

has

initiated Root Cause of Failure

(RCF) Engineering Evaluation

Requests

91-ZA-016 and 91-ZA-033.

Another

ARD 660-UR relay failed the previous

month in Unit '2 and,was

sent to Westinghouse

for RCF evaluation.

This

vendor's

RCF evaluation

provided additional

information, but was

inconclusive.

The licensee

has

requested

that the relay be returned for

inclusion in the licensee's

RCF evaluation.

The licensee

is also

evaluating

the testing

program for each specific affected relay.

The licensee

has

reviewed the history of Westinghouse

ARD relays

regarding

the deterioration of the coi 1 encapsulation

(epoxy) material

and the cracking of relay cases

of continuously energized

relays.

Subsequent

to this inspection period, Westinghouse

issued

a Part

21

report dated

June

24,

1991 regarding

the

ARD relays

and others with

potential

epoxy deficiencies.

The inspector will review the licensee's

RCF evaluation

upon completion

(Followup Item 530/91-19-03).

No violations of NRC requirements

or deviations

were identified.

Nuclear

Steam

Supp~1

S stem

(NSSS)

Vendor Technical

Performance-

Units 1, 121 3~71707

Several

recent technical

products

from the

NSSS vendor have

been identified

by the licensee

to have quality discrepancies.

The products that

contained quality discrepancies

were:

AD

CECORE coefficient files provided for the Unit 3 restart in June

1991 were in error.

The error was discovered

by the licensee's

Nuclear Fuels

Management

personnel

who reviewed the results.

16

B.

C.

The mini-incore instrument replacement

project

had

a data collection

unit which did not work and

had never

been tested

by the

NSSS

vendor.

In addition, minor computer

program errors inhibited full

testing of the mini-incore instruments.

Control

Element Assembly

(CEA) lower gripper coil leads

were

reversed

to eliminate coil movement which is believed to have

contributed to the damaged insulation,

momentary grounding,

and

slipped/dropped

CEA events.

Inadequate

testing of this design

change failed to identify a problem which occ'urred during low power

physics testing in which with CEA

1 fully withdrawn and

CEA

Regulating

Group

3 inserting,

spurious

reed switch position

indications

caused

Control Element Assembly Calculator

(CEAC) input

data errors.

Tkis design

change

was

removed prior to the

continuation of critical plant operations.

D..

Loose Parts

Event Analysis Computer .is experiencing

a memory lock-up

error and co'ntinuous

alarm, which is design related.

The inspector

acknowledged

the licensee's

review and testing

programs

which identified these

problems

and encouraged

continued

commitment to

this effort.'he inspector further acknowledged

the licensee's

efforts

to develop

some technical

resources

in-house to diminish reliance

on

vendor technical

support,

including that provided

by the

NSSS vendor.

The inspector

was concerned

in that reliance is placed

on the

NSSS vendor

to provide accurate

and reliable technical

responses

to address

regulatory concerns.

The licensee

responded

by stating that they are

presently

addressing

these

concerns

with the

NSSS vendor.

See also

paragraph

19 of this inspection report.

No violations of NRC requirements

or deviations

were identified.

18:

"8"

Ch

i

1 i~lifi ~ilTE)

Uni ts 1,

2

3

71707

This issue relates

to

TS 3.3.3.5 for the remote

shutdown

panel

and the

fact that the "B" charging

pump is necessary

for safe

shutdown

under

certain postulated fires.

The "B" charging

pump circuits, are listed

under

TS 3.3.3.5.

The inspector

noted that Unit

1 recognized

the

need to

enter Limiting Condition. for Operation

(LCO) 3.3.3.5.b

when the "B"

charging

pump was inoperable

on April 10,

1991.

The lack of timely

resolution of the ensuing

disagreement

over whether entry into the

LCO

was appropriate

resulted

in Unit 2 not entering this

LCO on May 20,

1991.

The "B" charging

pump was restored within 7 days

and therefore

the

LCO

was met.

The inspector

concluded that the lack of timely resolution of

this

TS interpretation resulted

in inconsistent plant administrative

actions

and encouraged

the licensee to resolve

TS interpretation

issues

promptly.

The licensee

acknowledged

the inspector's'omments.

No violations of

NRC requirements

or deviations

were identified.

17

19.

Safet

Anal sis Error - Units 1,

2 and

3 (92700)

A significant non-conservative

error in the initial subcritical

power

level assumption

used in the continuous

Control

Element Assembly

(CEA)

bank withdrawal analysis

was identified by Asea

Brown Boveri/Combustion

Engineering

(ABB/CE) when investigating differences

between results of

calculations

by

a Korean utility and

CE.

CE notified the licensee of the

'error

on Nay 24,

1991.

The erroneous

power level

was calculated

by the

ORIGIN computer code,

which apparently

had two errors.

One error was the

omission of a conversion factor (238 g/mole U-238)

and the other was

an

incorrect factor in the burnup of the

CEA modeled

by ORIGIN.

The result

was that the initial subcritical

power level

(when

1% subcritical) for

the

CEA bank withdrawal analysis

was too high by a factor of about

5000.

During the Unit 3 reactor startup

from the'ycle

3 refueling outage,

the

licensee

complied with the administrative restrictions

recommended

by

CE

to compensate

for this error.

This involved maintaining Reactor Coolant

System

(RCS) boron concentration

above the hot full power critical boron

concentration until the shutdown

CEAs were fully withdrawn.

The licensee

determined

the following relevant information in its

discussions

with CE:

o

The ORIGIN calculation applies at least to all

CE 16x16 reactors,

and is not generally repeated for each reactor

or fuel cycle.

o

The Palo Verde reactors

are at greater risk than other utilities

because their shutdown

banks

have

more reactivity and

a larger

initial reactivity insertion rate (0. 18% delta rho/inch).

The worst

case withdrawal is shutdown

bank "B," due to its large

bank rod

worth.

o

The safety analysis

assumes

a trip on high logarithmic power.

The

power spike from a continuous withdrawal event initiated at

a higher

power level is less significant than if initiated at

a lower power

level,

due to the lower startup rate

(SUR).

o

Two administrative

methods

prevent this faulty initial condition

from being

a problem,

because

the combination of lower core

reactivity (due to boron concentration)

or lower reactivity

insertion rates

prevent the worst case initial conditions

from

occurring.

Either of the two following methods will compensate

for

the error in the analysis:

Require all part-length

CEAs

(PLCEAs) to be inserted

whenever

shutdown

CEAs are inserted.

This inserts

an

8% penalty factor on

the planar radial

peaking factor which results

in

a

DNBR trip when

the

CPC trip is enabled at 10E-4 percent

power.

This trip occurs

much earlier than the high logarithmic power trip would occur.

CE

and the licensee

have concluded that the regulating

banks

are

limiting under this condition.

~ P.

'

i

18

Require

RCS boron concentration

to be maintained greater

than the

hot full power critical boron concentration

whenever

shutdown

CEAs

are not withdrawn.

o

CE and the licensee

have confirmed that the safety analysis is

conservative with respect

to current operating practices.

The

licensee

is verifying if its procedures

already

implement these

restrictions

under all conditions,

and Night Orders

are in place

until appropriate

procedural

changes

are

implemented.

o

Based

on discussions

with Shift Supervisors,

the licensee

has

determined

the operating practice

has

always

been to withdraw the

shutdown

CEAs prior to the

PLCEAs during startup.

o

CE performed additional evaluation

and determined that the Palo

Verde safety analysis

remains valid.

Licensee

personnel

went to

CE

headquarters

to review the vendor's calculations

and analysis.

CE

letter V-19-196, dated

June

17,

1991,

documents

that adequate

protection exists

due to the Core Protection Calculator trips

without reliance

on administrative controls.

This letter concludes

that the

NRC Safety Evaluation Report for this event remains valid.

Additionally, CE concluded that these errors

do not result in

consequences

which are reportable

under

10 CFR 21.

The licensee

does

not regard this event

as reportable.

No violation of NRC requirements

or deviations

were identified.

20.

Essential

and

Emer enc

Li hartin Train S~earation

- Units 1,

2 and

3

During the performance of Prefire Strategies

unit walkdowns,

the licensee

identified that the power cables for both trains of Emergency Lighting

and Essential

Lighting for the control

room all passed

through the "A"

Essential

Switchgear

room.

This condition is

common to all three units.

On May 29,

1991, the licensee

issued

a Conditional

Release

to Material

Nonconformance

Report

(MNCR) 91-QD-9084 specifying compensatory

measures,

which include implementation of design modifications in all units within

four months to properly separate

the trains.

Additionally, each unit

issued

a Night Order advising operators

of the condition, since

a fire in

the "A" Essential

Switchgear

room could disable all control

room

lighting.

The Night Order instructs operators

to shutdown the unit from

the control

room if all lights are lost as

a result of a fire, but leaves

the decision to evacuate

and remotely shutdown to the Shift Supervisor.

During an event of this nature,

the licensee

anticipates

that- lighting

from annunciators

and indicators,

in addi tion to the available

flashlights,

would provide adequate

illumination to safely conduct the

shutdown

from the control

room.

Based

on the physical

separation

of cables within the area

and the fire

suppression

capability, the inspector

concluded that this was

a low

probability event.

The inspector

reviewed the

MNCR and concluded that

licensee

actions

were prudent

and adequate,

No violation of

NRC requirements

or deviations

were identified.

19

21.

Fire Watch Trainin~Units 1,

2 and~364704)

In

a letter dated April 1, 1991, the

NRC Region

V Office requested

APS to

provide certain information regarding

the fire watch training program at

Palo Verde.

APS provided

a response

in a letter dated

Nay 31,

1991 which

confirmed that

12 of 155 personnel

who had conducted

roving fire watches

during the time period of interest

were not fully qualified.

The basis

for not being fully qualified included,

no fire watch training (5

people),

incomplete fire watch training (2 people),

and not current for

annual retraining

(5 people).

APS took immediate actions to verify that

the personnel

who were currently performing fire watch duties

were in

fact fully qualified and to develop

a list of qualified fire watches.

The failure to ensure that fire watches

had

been fully trained or had

completed re-training prior to performing fire watch duties is

a

violation of NRC requirements

(Violation 528/91-19-01).

A review of the

Nay 31,

1991 response

by .APS and discussions

with

Employee

Concerns

personnel

who performed the training program review for

APS, identified that the formal fire watch training program consists

of

two parts,

a computer-based

portion and

a classroom practical

course.

This training is specified in procedure

14AC-OFP04

and detailed in

procedure

15AC-OTR09.

In addition, on-the-job training has

been

documented

by the use of "qualification cards" which include

documentation

of the completion of the formal training, reading

and

understanding fire watch procedure

14AC-OFP04,

performance of a 'fire

watch under instruction of a qualified fire watch,

and

a final checkout

with the work group supervisor.

However, completion of the qualification

card is not considered

to be

a requirement prior to being qualified as

a

fire watch.

Procedure

14AC-OFP04

was stated to have

been

covered during

the formal 2-part training program.

A "Fire Watch Orientation Guide" has

been distributed which serves

to facilitate completion of the

qualification card

and will contain updated

procedure

14AC-OFP04 which is

currently being revised.

The

APS review focused

on the formal training

and not the comp/etion of the qualification card.

Based

on the review of the training for fire watches

used for

compensatory

measures

and the training deficiencies identified,

APS

expanded its review to "hot work" fire watches.

APS initial results

indicate that

some "hot work" fire watches

were also performed

by

individuals

who had not been given requalification training.

IIR

3-1-91-041 is being prepared

by the Fire Department regarding this

review.

22.

One violation of

NRC requirements

was identified.

Review of Licensee

Event

Re orts - Unit

1 (90712

and

92700

The following LERs were reviewed

by the Resident

Inspectors.

Unit

1

- a.

Closed)

LER 528/88-06-Ll/L2: "Surveillance Interval

Exceeded

For Incore Detecto~r

S stem,~ Unit

1

92700

This report refers to the March 21,

1988, discovery that

a

Surveillance

Test

(ST) was not performed prior'o Narch 20,

1988,

as

20

required

by Technical Specification (TS) 4.3.3.2.a.

This event

was

initially reviewed

and documented

in

NRC Inspection

Report

528/88-14.

The licensee

determined that the event

was

caused

by a cognitive

personnel

error, but that the lack of a formal tracking mechanism

for conditional

STs

was

a contributory cause.

The inspector

reviewed the procedures

developed

or revised

as

a result of this

event

and

has discussed

ST tracking

on several

occasions

with the

licensee.

Additionally, no

ST performance intervals

have

been

reported

as having

been

exceeded for approximately

one year.

The

inspector

concluded that the licensee's

corrective actions

have

adequately

addressed

tracking of STs

such that recurrence

of this

event is less likely.

Based

on this review, this item is closed.

Closed

LER 528/90-02-LO/Ll:

"Un uglified Air Re ulators

in

DV Contro

ir S stem -

Un ts

1,"

2 and

3

92700

This

LER describes

the

May 23, 1990, discovery of unqualified air

regulators

in the Atmospheric

Dump Valve (ADV) control air system.

This

LER also served

as

a Part

21 report, in that the procurement

documentation for the regulators

required

Environmental

Qualification

(EQ) and seismic qualification.

The

LER describes

the

procurement activities associated

with these regulators.

Even

though the supplier claims these

were supplied

as

commercial

grade

materials,

licensee

records

indicate that documentation

supporting

environmental

and seismic qualification were received,

though this

documentation

cannot

now be located.

Additionally, a

1986 Material

Nonconformance

Report

(MNCR) regarding

a subsequent

purchase for

Unit 3, for which qualification documentation

was not provided,

was

dispositioned

by changing

the quality classification to

a

non-quality class.

Justification for the quality class

change

has

not been located

by the licensee.

The licensee

determined

that no ineediate operability concern

existed,

and subsequently

procured

and installed qualified

regulators

in the

ADV control air system.

The licensee

asserted

that programmatic

changes

in its procurement

and design

change

programs

have

been

made over the years

since these

regulators

were

purchased

which would prevent recurrence

of this event.

Additionally, the licensee

completed

a review (Quality Deficiency

Report 90-0317,

Incident Investigation Report 3-2-90-025) of a

sample of purchase

orders

(POs) to evaluate

the transportability of

the lack of adequate

engineering specifications

and the inadequate

PO-review

and approval

process.

This evaluation

concluded that,

with 95 percent confidence,

the error experienced

in the procurement

of the regulators

is absent

from more than

95 percent

of. the

populati'on of "Q" class

POs with field material requisitions

referencing

home office specifications.

Based

on this review, this

LER is closed.

21

c.

(Closed)

LER 528/91-06-LO:

"ESF Actuation Due To Radiation

Nonitor Fai ure

- Unit

1

92700

This event is described

in paragraph

10 of this report.

This

LER is

closed.

23.

Exit Meet~in

An exit meeting

was held on June 20, 1991, with licensee

management

during which the observations

and conclusions

in this report were

generally discussed.

The licensee

did not identify as proprietary

any

materials

provided to or reviewed

by the inspectors

during the

inspection.

~ b

I

0

I