ML17292B315

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Insp Rept 50-397/98-03 on 980201-0314.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML17292B315
Person / Time
Site: Columbia 
Issue date: 03/31/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292B313 List:
References
50-397-98-03, 50-397-98-3, NUDOCS 9804080246
Download: ML17292B315 (29)


See also: IR 05000397/1998003

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORYCOMMISSION

" REGION IV

Docket No.:

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-397

NPF-21

50-397/98-03

Washington Public Power Supply System

Washington Nuclear Project-2

Richland, Washington

February

1 to March 14, 1998

S. A. Boynton, Senior Resident Inspector

G. W. Johnston, Senior Project Engineer

H. J. Wong, Chief, Reactor Projects Branch E

Attachment

Supplemental Information

9804080246

980331

PDR

ADOCK 05000397

6

PDR

EXECUTIV

S

RY

Washington Nuclear Project-2

NRC Inspection Report 50-397/98-03

~Oer'<~ion

Inadequate self-checking and peer checking resulted in an operator error that

deenergized

nonvital Bus SM-2 and started the Division III emergency diesel generator.

Operations personnel actions in response to the transient were appropriate and prompt.

The licensee's root cause analysis and corrective actions effectively addressed

the

human performance concerns (Section 01.1).

~

One instance was identified in which an operating crew did not demonstrate

a

conservative approach to equipment operation when a nonvital lighting panel, with an

unidentified ground, was reenergized without an understanding of the source of the

ground or a troubleshooting plan to identify the source (Section 01.2).

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Poor material condition of the plant service water (TSW) system resulted in a leak that

challenged the integrity of the control room envelope as water was able to penetrate

through a concrete slab interface in the control room ceiling, a boundary credited by the

licensee's flooding analysis.

The licensee is currently implementing an improvement

plan that should adequately address the material condition deficiencies in theTSW

system (Section M2.1).

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In reviewing the testing requirements for the standby gas treatment system, the

inspector identified the potential for the system floor drains to present a bypass pathway

'round

the filters. In response to the inspector's concerns, the licensee took appropriate

action to verify that the current leakage is acceptable,

and to develop a long-term

monitoring program for this potential unfiltered leakage path (Section E1.1).

Licensee personnel improperly applied surveillance requirement 3.0.2 to program

surveillances in the administrative section of Technical Specifications (TS). As a result,

a 25 percent surveillance interval extension was inappropriately utilized for several

technical programs (Section E8.2).

A number of deficiencies were identified in the implementation of the licensee's leakage

surveillance and prevention program.

Specifically, procedures for performing visual and

integrated leakage inspections on the standby gas treatment system, the containment

monitoring system (CMS), and the post accident sampling system (PASS), were

inadequate

in that they failed to identify all of the appropriate system components to be

monitored (Section E8.3).

-3-

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Licensee corrective actions to address weaknesses

in implementing the transient

combustible control program have not been effective in addressing the root cause and

precluding repeat noncompliances with procedural requirements.

The root cause of

these noncompliances appeared to be a lack of understanding of fire protection

requirements and inattentiveness to fire protection labeling on the part of plant

personnel (Section F1.1).

e ort Details

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The plant began the inspection period at 100 percent power. On February 3, power was

reduced to 70 percent in response to a loss of electrical power to nonvital Bus SM-2. The loss

of electrical power resulted in the loss of one of the condensate/condensate

booster pump sets.

Following equipment restoration, the plant was returned to full power on February 4. On

March 1, power was reduced to 60 percent to facilitate investigation and repair of an apparent

tube leak in main condenser Waterbox C. Subsequent troubleshooting efforts were

unsuccessful

in identifying the leaking tube, and power was returned to 100 percent on

March 5.

On March 11, a failure of the instrument air line to main steam Line D inboard isolation valve

resulted in the inadvertent closure of the valve. The ensuing transient led to the closure of all of

the main steam isolation valves and a high flux reactor scram.

To facilitate troubleshooting and

repair of the broken air line, the licensee placed the plant in Mode 4 on March 12. The plant

remained in Mode 4 for the balance of the inspection period. The details of this event willbe

documented in NRC Inspection Report 50-397/98-05.

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01

Conduct of Operations

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The inspector reviewed the licensee's Incident Review Board (IRB) report conclusions

and the recommended corrective actions of Problem Evaluation Request

(PER) 298-0102, following an inadvertent deenergization of Bus SM-2 on

February 3, 1998.

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The licensee conducted an IRB investigation of the February 3, 1998, deenergization of

Bus SM-2. The result of that IRB review showed that the event was principally due to

human performance induced error. The licensee's identified root cause was that the

reactor operator responsible for the event failed to "fullyinternalize the value of Peer

Checks and Self-Checking."

The event occurred during performance of PPM 2.7.1.A, "6900 Volt and 4160 VoltAC

Electrical Power Distribution System," to transfer Bus SM-1 from Transformer TR-N to

Transformer TR-S to support surveillance testing of Diesel Generator DG-1. The

actions before commencing the transfer included a prejob brief and a discussion of peer

checking.

Step 5.16.10 included action to "green flag" the TR-N/SM-1 Switch CB-N1/1.

The action to green flag a switch is to ensure the indicator flag on the switch agrees with

the lamp indication.

In the actions to transfer to TR-S, Breaker CB-S1 is allowed to

-2-

open automatically.

The switch flag, however,,does

not automatically reset.

Just before

the step,

the operator responded to an alarm on the adjacent panel.

When the operator

returned to the activity, he inadvertently opened the TR-N feeder breaker Switch CB-

N1/1 to Bus SM-2 rather than "green flagging" the CB-S1 switch. The action to green

flag a switch is the same action as manually opening the breaker.

This resulted in the

loss of Bus SM-2 and subsequent

tripping of major loads.

The inspector noted that the

, switches were side by side on the the control panel.

Following the inadvertent loss of Bus SM-2, several major loads in the secondary side of

the plant were lost. These included a condensate

pump and the associated condensate

booster pump. The loss of these two pumps required a prompt reduction of power, by

reducing recirculation flowfrom 100 percent of full power to approximately 65 percent.

A low voltage was also sensed

on Bus SMR, the Division III 4160V vital bus normally

supplied by SM-2, which resulted in a start of the Division III emergency diesel

generator.

From a review of the post event chart traces, the inspector determined that

the event did not compromise any operating limits. This was due to prompt action by

control room operators in reducing reactor power.

In the IRB report, the reviewers noted that the operator responsible for the event had

been under some personal stress and was tired at the time of the event. The inspector

discussed these aspects with the IRB chairman, observing that the IRB report described

these as "noncontributing" causes.

The IRB chairman stated that the individual involved

raised these points as possible contributors to his performance, and that the IRB

discounted them. The IRB interviews of other control room personnel and supervisors

found that the operator had not exhibited outward signs of stress or fatigue. The

operator had recently returned to shift duties from an extended assignment, which had

kept him from normal watch standing duties.

The IRB chairman further stated that

considerable change in control room conduct of operations had occurred over the period

before the operator's return to shift duties.

The chairman,

further, indicated his view

that the operator had not internalized the expectations involved in performing tasks

governed by procedure, especially with regard to self-checking and peer checking.

The licensee's immediate corrective actions included a station wide standdown on

February 3, 1998, to review this event and other recent personnel errors. An entry was

placed in the operations night orders referring to the stand down, reiterating

expectations regarding the contributing factors.

Shift managers were instructed to

evaluate crew members with regard to self-checking.

The operations manager stated

that the concept of peer checking had been emphasized

as a management expectation,

but had been left for each shift manager to implement.

This had led to variation in the

level of expectation and implementation.

Therefore, the operations manager directed

that management expectations with regard to peer checks be documented

in the

appropriate Operating Instructions.

'

Nuclear Safety Assurance Department (NSAD) quality department surveillance

report (298-014) indicated that an NSAD representative

observed the recovery from the

loss of SM-2.

The observer noted the operator logs did not mention that the chemistry

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department was notified of the power reduction greater ttIan 15 percent.

Followup

inquiry by NSAD indicated that the plant laboratory chemistry supervisor believed that

operations notification was adequate.

No primary chemistry sample was taken, as the

noble gas release rate of 919.3 microcuries per second was below the sampling

requirement of greater than 15,000 microcuries per second.

The failure to properly perform PPM 2.7.1A, Revision 3, step 5.6.10, to "green flag" the

TR-N/SM-1 Switch CB-N1/1 was identified as a violation of Technical Specification (TS) 5.4.1.a, which requires, in part, procedures to be developed, implemented and

maintained for each of the surveillances directed by plant TS. This nonrepetitive,

self-revealing and corrected violation is being treated as a noncited violation consistent

with Section VII.B.1 of the NRC Enforcement Policy (NCV 50-397/98003-01).

Licensee

Event Report 50-397/98001-00, relating to the same event, is also closed.

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Inadequate self-checking and peer checking resulted in an operator error that

deenergized

nonvital Bus SM-2 and started the Division III emergency diesel generator.

Operations personnel actions in response to the transient were appropriate and prompt.

The licensee's root cause analysis and corrective actions effectively addressed

the

human performance concerns.

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The inspector reviewed the control room log and problem evaluation requests (PERs) on

a daily basis to evaluate the accuracy of the logs, and the actions taken by the licensee

in response to conditions identified.

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Over the past several months the inspector identified several discrepancies

in the

control room logs that were generally administrative in nature (for example, wrong

individual identified as shift manager, wrong shift manager verifying log entries for a

shift). Although the errors were administrative, the errors made it difficultto determine

whether of one of the shift managers had maintained appropriate watch standing

qualifications. The inspector noted that the shift manager had not been routinely

assigned to the control room during the fourth quarter of 1997. The licensee reviewed

payroll records and interviewed personnel to verify the requirements of 10 CFR Part 55

had been satisfied.

The technical accuracy of the logs was noted to be very good.

On March 1, a control log entry was made for reenergizing a lighting panel in the turbine

building to support work in the condenser bay. This entry was noteworthy in that the

panel in question had an existing work request against it due to an unidentified electrical

ground.

Upon reenergizing the panel a 4-5 amp ground was noted on the supply

bus (MC-2D-A)to the lighting panel.

Subsequent

field walkdowns found the neutral

ground resistor for Transformer 2-21 to be very hot.

This inspector discussed this entry with the responsible shift manager and found that no

troubleshooting activities had been planned or performed to identify the ground prior to

reenergizing the panel.

The shift manager, in clearing the danger tag associated with

the supply breaker, made the assumption that the ground was due to one of the

mercury vapor lamps powered from the panel, based upon experience.

That experience

had shown historically that ifthe ground was in a lamp, the ground would be eliminated

when the lamp cooled down. The inspector disagreed with this approach in that the

decision to reenergize the lighting panel was based upon an assumption and not on

actual data for the existing condition. The result was a potential fire hazard and the

potential for damage to electrical equipment.

The impacted equipment was not safety-

related.

On March 8, control room operators identified what appeared to be an unexpected

oscillation transient on reactor feedwater Turbine B. The shift technical advisor (STA)

had also been touring reactor feedwater pump Room B at the time of the event.

According to the PER initiated for the event, the STA repeated his actions in the pump

room in an attempt to repeat the transient to see ifhe may have caused or contributed

to the event.

Further review by the licensee determined that the actions taken by the

STA were actually benign and that the PER did not accurately reflect those actions. The

inspector also noted that although the operating crew determined the event warranted

the initiation of a PER, no control room log entry was made to note it.

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The technical accuracy of the control room logs was found to be generally very good,

with the exception of the omission of a log entry for a feedwater turbine transient and a

few minor administrative errors.

One instance was identified in which an operating crew did not demonstrate

a

conservative approach to equipment operation when a nonvital lighting panel, with an

unidentified. ground, was reenergized without an understanding of the source of the

ground or a troubleshooting plan to identify the source.

Operational Status of Facilities and Equipment

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The inspectors walked down accessible portions of the following engineered safety

feature systems:

Reactor Core Isolation Cooling

Standby Gas Treatment, Trains A and B

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Residual Heat Removal, Trains A, B, and C

High Pressure Core Spray

Each of the systems was found to be properly aligned for the current operating mode.

No deficiencies were identified by the inspectors that had not already been identified by,

the licensee.

A review of plant logs and operating data indicated that system reliability

and availability remain well above maintenance

rule performance guidelines.

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The inspectors observed the followingwork activities:

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OSP-HPCS/IST-Q701

High Pressure Core Spray (HPCS) System

Operability Test

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WO¹ KRWO

Troubleshoot and Repair Instrument AirLine to

MS-V-22D

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PPM 6.2.4

New Fuel Inspection

Each of the work activities was adequately implemented.

Radiological protection

practices during new fuel receipt inspections and the drywell maintenance

on

Valve MS-V-22D were appropriate.

The ALARAplanning and execution for the work in

the drywell was effective in minimizing the dose to workers.

Foreign material controls

were also properly implemented for these activities.

Operations performance during the high pressure core spray (HPCS) pump operability

test was adequate.

Proper peer checking was observed for control board

manipulations.

Three-way communications were not consistently utilized, contrary to

management

expectations.

The control room supervisor (CRS) authorized the stroking

of manual Valve HPCS-V-6 (HPCS keep-fill pump discharge check valve) out of

sequence

from the procedure.

This change to the order of the procedure was contrary

to the guidance in SWP-PRO-01, "Description and Use of Procedures

and Instructions,"

which states that procedure steps within TS surveillances should be performed in the

sequence

specified unless otherwise designated by the procedure.

Procedure OSP-PCS/IST-Q701

did not specifically authorize this practice.

The system

engineer that was monitoring the surveillance, noted the discrepancy and informed the

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operators that the manual valve had to be stroked with the keep-fill pump operating.

The procedure steps were then repeated satisfactorily in the order specified.

Nlaintenance and Nlaterial Condition of Facilities and Equipment

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The inspector assessed

the licensee's actions to resolve a leak that occurred in the

service water system on the 525-foot elevation of the Radwaste Building. The inspector

also reviewed the licensee's assessment

of the leakage in PER 298-0157.

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On February 20, 1998, electricians were installing electrical conduits in an

Instrumentation and Controls shop, Room C510, on the 525-foot elevation of the

Radwaste Building. During the work, an electrician leaned on a 3/4-inch drain line from

a strainer on a TSW line to a room air conditioning Unit WRA-AC-52. The force applied

broke the pipe nipple, initiating a leak onto the floor. Water was unable to drain into a

local scupper because of an elevated lip. Subsequently, the water flowed out under the

door into adjacent spaces and then flowed into two floor drains. The electricians

initiated action to isolate the leak and informed the control room operators immediately.

Later, the control room operators noted the sound of dripping water in the ceiling

overhead.

An inspection by the system engineer noted that a small amount of water

had gone into the ceiling overhead space and had dripped onto the upper surface of the

ceiling tiles. The engineer noted that the leakage was coming from seams in the floor

slab from the construction joints in the concrete.

The inspector toured the affected area with the system engineer.

From the tour of the

spaces,

the, inspector noted that the floor slab appeared to have been poured during

construction in six separate

pours.

The boundaries between each slab were not cleanly

dressed or troweled. The inspector observed a fine crack between the slabs that

appeared sufficient for water to'penetrate and migrate. This was the apparent cause of

the leakage into the ceiling space above the control room.

A barrier impairment was issued for the floor surface for flooding protection because the

floor is a credited flooding boundary in the fire protection program. A work request

(WR 98000899) was initiated to apply a surface coat to the floor to provide an

impervious flooding boundary.

Immediate action included the staging of plastic sheeting

to provide protection to control panels in the control room.

It is unlikely, due to the

narrow nature of the cracks in the 525-foot floor slab, that substantial amounts of water

could flow into the control room ceiling overhead.

A similar configuration was also

identified for the 484-foot elevation of the Radwaste Building (cable spreading room),

resulting in the issuance of a barrier impairment for that elevation.

These actions

appeared appropriate in addressing the immediate concerns from possible flooding of

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the 525-foot elevation.

The licensee initiated action to review other possible locations in

other buildings that may be similar to the concerns identified in the Radwaste Building.

The design requirement for flooding protection is in Tech Memo 2103, which was

generated for fire barrier analysis, and addresses

penetration seals.

The design

requirement is not identified in the Facility Safety Analysis Report.

Currently the floor is

required to maintain a 4-inch maximum standing water depth. The leakage through

joint cracks in the floor slab does not meet the requirement in the Tech Memo because

of the observed leakage.

The control room envelope integrity has been demonstrated

by surveillance testing and therefore meets the operability requirement in the TS.

However, because of the leakage into the control room, the envelope was considered

degraded due to the barrier impairment issued for the TSW leakage.

The system engineer for the TSW system indicated that a piping replacement program

is in place and a schedule has been developed identifying the portions of piping that are

to be replaced during each refueling outage.

Prioritization of the replacement was from

nondestructive examination and system importance.

The engineer stated the licensee's

goal is eventually to replace all affected piping. The piping replacement scheduled for

Refueling Outage R-13 is small bore supply and return lines to the main steam tunnel

coolers (RRA-CC-8 and 9). The reason for this replacement is that a leak in the main

steam tunnel could result in a plant shutdown.

Other actions to address the material

condition of the TSW piping include a silt/rust inhibitor system that ha's been added to

the system and plans to install an anti-biofouling injection system.

The silt/rust inhibitor

system is currently undergoing testing and troubleshooting.

C.

Poor material condition of theTSW system resulted in a leak that challenged the integrity

of the control room envelope as water was able to penetrate through a concrete slab

interface in the control room ceiling, a boundary credited by the licensee's flooding

analysis.

The, licensee is currently implementing an improvement plan that should

adequately address the material condition deficiencies in the TWS system.

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In reviewing the licensee's implementation of its leakage surveillance and prevention

program for the SGT system (see Section E8.3), the inspector reviewed the testing

performed on the system to ensure it meets its design requirements.

-8-

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Licensee TS 3.6.4.3 requires the SGT system to be tested in accordance with the

Ventilation Filter Testing Program as described in TS 5.5.7. TS 5.5.7 requires the high

efficiency particulate air (HEPA) and charcoal filters of the SGT system to be tested in

accordance with ASME-N510-1989, "Testing of Nuclear AirTreatment Systems," to

demonstrate that penetration and system bypass is less than 0.05 percent.

The inspector reviewed the 1975, 1980, and 1989 versions of ASME-N510 and found

that each of the standards describes the methodology for testing the penetration and

bypass of the HEPA and charcoal filters. In the 1975 and 1980 versions of the standard

an appendix was included regarding the importance of in-place leak tests.

In these

versions it was stated that "an installed system can be assumed to have an efficiency

equivalent to that of the [factory tested charcoal] sample only if:...there are no leaks or

bypasses

in either the individual [charcoalj cells (factory tests) or the installed system

(field tests)." The 1989 version went further and included a specific testing method and

frequency for system bypass leakage.

The purpose of the test was described as

'ollows:

Systems using HEPA filters and adsorber banks may contain

bypass dampers, ducts, conduits, floor drains, pipe penetrations,

etc., which could potentially defeat the purpose of high efficiency

nuclear air treatment components.

Therefore, it is necessary to

perform tests which challenge all these potential bypass leakage

paths...

ASME N510-1989 recommends

a frequency of once per operating cycle for performing

the system bypass leakage test.

The inspector noted that the SGT filtertrain contains a number of fioor drains for

directing the flow of fire protection deluge water to the reactor building floor drain

system.

These drains are normally closed by means of a passive check valve in each

drain line. Several of the drains are located in the exhaust section of the filtertrain, and

as such, present a potential bypass leakage path ifthe check valve failed or was not

properly seated.

In questioning the licensee on testing of these valves, it was

determined that the licensee did not have a program for visually inspecting the valves or

a procedure to measure system bypass leakage from the floor drain system.

In response to the inspector's concerns, the licensee attempted to measure the air flow

into the common header of the SGT floor drain system to evaluate ifany of the check

valves may be leaking by their seat.

Measurements

made with a pitot tube velocimeter

at the outlet of the common drain header found that the air velocity into the header on

both trains was less than that detectable with the instrument (25 ft/min). The licensee

then estimated that leakage flow into the system, via the check valves, was less than

0.5 scfm. The leakage was well within the analysis assumption of 14 scfm.

-9-

Although the leakage rate past the check valves was found to be acceptable, the

inspector questioned the licensee on the need to test this leakage path on a periodic

basis as recommended

by ASME N510-1989.

The licensee reviewed the testing

requirements of the SGT system and did not identify any licensing basis for testing the

bypass flow path.

Specifically, in implementing the testing requirements of

ASME N510-1989, through TS 5.5.7, only testing of the in-place HEPA filters and

charcoal adsorbers

is required.

However, due to the potential consequences

of bypass

leakage, the licensee agreed that testing would be prudent. As a result, the licensee will

be implementing a periodic testing program for the SGT floor drains.

g~cu~si n.

In reviewing the testing requirements for the SGT system, the inspector identified the

potential for the system floor drains to present a bypass pathway around the filters. In

response to the inspector's concerns, the licensee took appropriate action to verify that

the current leakage is acceptable,

and to develop a long-term monitoring program for

this potential unfiltered leakage path.

ES

Miscellaneous Engineering Issues (92903)

E8.1

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9

1 -: lack of written safety evaluation for

removal of information from the fire hazards analysis (FHA) in the Final Safety Analysis

Report (FSAR). A more detailed review'of the changes made to the FSAR found that

the information removed from the FSAR was duplicated in the licensee's combustible

loading calculation.

In removing that information, the licensee also incorporated the

combustible loading calculation into the FSAR by specific reference.

Thus, changes to

the calculation would then be required to be evaluated under the requirements of

.10 CFR 50.59. The inspector found that no changes were made to the calculation in

conjunction with the removal of the information from the FSAR. Therefore, the removal

of the information, in and of itself, did not constitute a change to the facility and did not

require a written safety evaluation.

In response to a number of outstanding calculation modification reports, and several

concerns raised by the inspector, as documented

in NRC Inspection

Report 50-397/97-18, the licensee recently revised the combustible loading calculation.

The inspector verified that a written safety evaluation was performed to evaluate those

changes and the associated

changes to the FHA section of the FSAR.

E8.2

los

resolv d I em 5 -3 7/ 7

8- 4: inappropriate application ofTS4.0.2 to

.allow for a 25 percent extension to certain surveillance intervals. This item was opened

based upon the licensee's use of TS 4.0.2 when scheduling the integrated leakage

surveillances required by TS 6.8.4.a.2 for evaluating primary coolant leakage outside of

containment.

In resolving this issue, the licensee reviewed each of the 72 integrated

leakage surveillances performed, in accordance with TS 6.8.4.a.2, since initial operation.

The licensee found that the use of TS 4.0.2 resulted in 27 instances where the 18-month

surveillance interval was exceeded.

The licensee also found that TS 4.0.2 was applied

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to TS 6.8.4.d.5.

TS 6.8.4.d.5 (Improved Technical Specification (ITS) 5.5.4.e) requires

every 31 days a determination of cumulative and projected dose contributions from

radioactive effluents for the current calendar quarter and calendar year. Although the

application of Surveillance Requirement (SR) 3.0.2 (old TS 4.0.2) is not explicitly

referenced,

a 25 percent extension has been routinely applied to this SR.

As noted in NRC Inspection Report 50-397/97-18, the licensee's implementation of ITS

now allows for the use of a 25 percent surveillance interval extension (SR 3.0.2) for

those surveillances required by TS 5.5.2 (equivalent to old TS 6.8.4.a).

The licensee determined that the root cause of the misapplication of TS 4.0.2

(SR 3.0.2) was personnel error in that there was a general misunderstanding of how

TS 4.0.2 (SR 3.0.2) applied to SRs in the Administrative Controls section.

Specifically, it

was not understood that application of TS 4.0.2 (SR 3.0.2) to surveillances under

administrative TS was not provided unless explicitly referenced.

In response, the

licensee developed a set of rules for determining the applicability of SR 3.0.2 to SRs

that are outside of Sections 3.1 through 3.10 of ITS. The inspector reviewed the

licensee's methodology and found that, ifproperly implemented, the rules would result in

the proper application of SR 3.0.2. The licensee has established

a corrective action to

train licensing personnel and program managers on this methodology.

To meet the 31-day interval requirement of TS 5.5.4.e, the licensee is determining the

cumulative and projected doses from radioactive eNuents twice each month until a TS

amendment

is approved to allow the application of SR 3.0.2.

The failure to perform the integrated leakage surveillances on an 18-month interval was

identified as a violation of TS 6.8.4.a.2 (VIO 50-397/98003-02).

The failure to determine

cumulative and projected dose contributions from radioactive effluents for the current

calendar quarter and calendar year every 31 days was identified as a violation of

TS 5.5.4.e (VIO 50-397/98003-03).

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50-397/97 18-0: undefined process for evaluating and

correcting leakage from the SGT system in accordance with TS 5.5.2.

TS 5.5.2

requires that biennial leakage inspections and periodic visual inspections be performed

on those systems outside of containment that would contain highly radioactive fluids

following a postulated toss-of-coolant accident (LOCA). SGT is included as one of the

systems to monitor under TS 5.5.2.

However, PPM 1.5.6, "Leakage Surveillance and

Prevention Program," Revision 8, the licensee's procedure that implements the TS 5.5.2

program, did not define those components of SGT that need to be monitored for leakage

and did not provide for periodic visual inspections.

Subsequent

to the findings noted in NRC Inspection Report 50-397/97-18, the licensee

initiated a broad review of its implementation of the requirements of TS 5.5.2. This

review included the basis for which SGT is included as a system under TS 5.5.2, and

detailed reviews of the procedures that implement the inspection requirements, as

referenced by PPM 1.5.6.

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SGT System:

Subsequent

evaluations by the licensee have been unsuccessful

in

determining the technical basis for the inclusion of the SGT system in TS 5.5.2.

In fact,

the licensee's original commitment to implementing the leakage surveillance and

prevention program, as described in the FSAR, did not list the SGT system as one of

the systems to be monitored.

In reviewing the operating characteristics of the system, the inspector found that the

system isolates from containment upon the initiation of a LOCA. The leakage from the

containment isolation valves is monitored through the licensee's inservice testing

program.

The only p'ortion of the system downstream of the containment isolation

valves in which leakage would be of concern appeared to be that section of the system

between the outlet of the charcoal filters and the inlet of the fans. Airin-leakage in this

portion of the system would be drawn in to the fans and would bypass the filter unit.

The licensee's analysis for evaluating offsite doses following a postulated LOCA

assumes that 14 scfm of unfiltered air is discharged by SGT. This takes into account

leakage from joints, valve packing, and the fans'haft seals.

The testing, performed

following initial installation of the system verified that the 14 scfm was a conservative

assumption.

The licensee plans to address visual inspections of the SGT system through a revision

to the routine operability surveillance procedures.

CMS: Concerns were also identified with the licensee's leakage monitoring of the CMS.

Prior to the licensee's implementation of ITS, PPM 7.4.6.3.4.2, "Excess Flow Check

Valve Test of Containment Atmosphere and Suppression

Pool Level," was being

credited for the biennial integrated leakage surveillance required by old TS 6.8.4.a.2

'(ITS 5.5.2). However, PPM 7.4.6.3.4,2 only verified operability of the CMS excess flow

check valves and checked for leakage at the containment penetration isolation and test

valves.

No leakage inspections were required for components downstream of the

excess flow check valve. Additionally, the inspector noted that PPM 7.4.6.3.4.2 was

canceled upon implementation of ITS and that a new procedure has not yet been

approved.

A new procedure to test the CMS excess flow check valves was in the review process at

the conclusion of the inspection.

The system engineer was also working with the

TS 5.5.2 program manager to determine what additional components would need to be

inspected as part of the biennial leakage surveillance.

PASS: Similar to the SGT system, a procedure had not been identified for performing

periodic visual inspections of the PASS system.

The licensee is in the process of

determining an appropriate mechanism and frequency for performing these inspections.

The licensee's biennial integrated leakage inspection is proceduralized in PPM

'SP-PASS-B801,

Revision 0, "Post Accident Sampling Leakage Surveillance." The

system engineer's review of this procedure identified a number of components within the

PASS system that are not evaluated during the biennial surveillance.

The components

included, but were not limited to, the isolation valves from the residual heat removal

-12-

system and sampling valves within the PASS sample rack. A revision to PPM

TSP-PASS-B801

has been initiated to incorporate the findings of the system engineer.

Conclusions:

The existing monitoring requirements for the other systems covered

under TS 5.5.2 were found to be generally adequate.

However, the failure of PPM 1.5.6

to adequately address the SRs of TS 5.5.2 for the SGT, CMS, and PASS systems was

identified as a violation of TS 5.4.1.e. (VIO 50-397/98003-04).

V

a

Su

o

F1

Conduct of Fire Protection Activities

F1.1

eciveA

i n

A

a'I

es

o

on

ITr

o

bu il

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ci

The inspector reviewed the licensee's actions to address several examples of

inadequate control of transient combustibles in the reactor building, as described in NRC

Inspection Report 50-397/97-18.

Several walkdowns of vital fire protection areas were

also performed to evaluate the adequacy of those actions.

s

F'i

NRC Inspection Report 50-397/97-18 identified several examples where the

requirements of PPM 1.3.10C, "Control of Transient Combustibles," were not followed

for transient combustible materials left in high radiation areas of the reactor building. In

response to the identified concerns, the licensee performed a root cause analysis and

has implemented a corrective action plan through the associated

PER': The plan

included the issuance of an e-mail message from the plant general manager to

department managers and a discussion between the operations manager and the

operations shift crews of the fire protection concerns.

Additional discussions between

the other department managers and their staffs are planned, but have not yet been

completed.

The licensee's root cause analysis identified weaknesses

in plant staff

knowledge of the requirements of PPM 1.3.10C.

Specifically, it was concluded that

plant staff may not have a clear understanding of what constitutes combustible material

that would require controls under PPM 1.3.10C.

However, the corrective action plan

only called for a review of the root cause and corrective actions for the associated

PER

in update training sessions.

No short-term actions were taken to focus the plant staffs

attention on the transient combustible permit process and the treatment of

combustible-free zones.

On February 18, the inspector identified unattended transient combustibles in a

safety-related instrument rack room on the 501-foot elevation of the reactor building.

The combustible materials were introduced into the room as a part of planned

maintenance activities that also established

a contamination zone and step-off pad in

-13-

the room. The instrument rack room is designated as a combustible-free zone in

accordance with PPM 1.3.10C. As such; unattended transient combustibles are not

allowed in this room. The licensee subsequently initiated PER 298-0144 to document

the procedure noncompliance.

The combustibles were removed from the room and a

transient combustible permit was issued by the plant fire marshal to allow for small

amounts of transient combustibles in the room with the requirement that they be

constantly attended.

On March 6, the inspector again identified unattended combustibles in the same

'nstrument

rack room. The transient combustibles (small plastic containers, tygon

tubing, and electrical multimeter) were apparently staged for an instrumentation and

controls surveillance.

The inspector attended the material until the shift support

supervisor (SSS) arrived. The SSS subsequently left the area without removing the

material or leaving another individual in attendance.

Although the inspector noted to

the CRS that the material found did not comply with the requirements of PPM 1.3.10C,

a PER was not initiated until the inspector discussed this concern with the fire protection

engineer on March 10.

The inspector noted that a sign was posted in the interior of the instrument rack room

indicating that the room is a combustible-free zone. The inspector also noted that the

transient combustible permit, issued following the concerns identified on February 18,

was posted in the stairwell adjacent to the room, but not readily visible to individuals

accessing the room. Both of the two occurrences identified by the inspector indicate

that plant personnel were not being attentive to fire protection program labeling and did

not understand the requirements of PPM 1.3.10C for what constitutes transient

combustible material. The failure of the SSS to constantly attend or remove the material

from the instrument rack room on March 6, and the failure of the CRS to initiate a.PER

for the procedure noncompliance, both underscore the concern.

They also indicate that

the licensee's actions to address personnel knowledge deficiencies in implementing the

transient combustible control program, in response to the concerns identified in NRC

Inspection Report 97-18, were inadequate to preclude repeat procedure

noncompliances.

The failure to take prompt and adequate corrective actions for

improper control of transient combustibles in the reactor building, a condition adverse to

quality, was identified as a violation of 10 CFR Part 50, Appendix B, Criterion XVI

(VIO 50-397/98003-05).

~Cnclusi

n

Licensee corrective actions to address weaknesses

in implementing the transient

combustible control program have not been effective in addressing the root cause and

precluding repeat noncompliances with procedural requirements.

The root cause of

these noncompliances appeared to be a lack of understanding of fire protection

requirements and inattentiveness to fire protection labeling on the part of plant

personnel.

-14-

V. Ma

a emen

eeti

s

X1

Exit Nleeting Summary

The inspectors presented the inspection results to members of licensee management after the

conclusion of the inspection on March 25, 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

~LI en'

Supplemental Information

PARTIALLIST OF PERSONS CONTACTED

D. Coleman, Regulatory Affairs Manager

D. Giroux, System Engineering

D. Hillyer, Radiation Protection Manager

T. Hoyle, Engineering Programs

D. Kobus, Fire Protection

A. Langdon, Assistant Operations Manager

P. Inserra, Licensing Manager

S. Oxenford, Operations Manager

G. Smith, Plant General Manager

J. Kane, Acting Engineering Manager

R. Webring, Vice President Operations Support

INSPECTION PROCEDURES USED

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92902:

IP 92903:

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support

Followup - Operations

Followup - Maintenance

Followup - Engineering

Qgg~ed

ITEMS OPENED, CLOSED, AND DISCUSSED

50-397/98003-01

NCV

50-397/98003-02

VIO

50-397/98003-03

VIO

50-397/98003-04

VIO

failure to properly perform PPM 2.7.1A

failure to perform the integrated leakage surveillances on

an 18-month interval

failure to determine cumulative and projected dose

contributions from radioactive eNuents for the current

calendar quarter and calendar year every 31 days

failure of PPM 1.5.6 to adequately address the SRs of

TS 5.5.2 for the SGT, CMS, and PASS systems

~

~

-2-

50<97/98004-05

VIO

failure to take adequate corrective actions for improper

control of transient combustibles in the reactor building

Qgged

50-397/98001-00

LER

voluntary report of automatic start of HPCS DG due to

operator error

50-397/98003-01

NCV.

'0-397/97018-03

URI

failure to properly perform PPM 2.7.1A

undefined process for evaluating and correcting leakage

from the SGT system in accordance with TS 5.5.2.

50-397/97018-04

URI

inappropriate application of TS 4.0.2 to allow for a 25

percent extension to certain surveillance intervals

50-397/97018-08

URI

lack of written safety evaluation for removal of information

from the FHA in the FSAR

LIST OF ACRONYMS USED

CMS

CRS

FSAR

HEPA

HPCS

IRB

LER

ITS.

LOCA

NCV

NRC

NSAD

PASS

PER

PPM

SR

SGT

SSS

TS

TSW

URI

VIO

WNP-2

containment monitoring system

control room supervisor

Final Safety Analysis Report

high efficiency particulate air

high pressure core spray

incident review board

licensee event report

Improved Technical Specifications

loss-of-coolant accident

noncited violation

U.S. Nuclear Regulatory Commission

Nuclear Safety Assurance Department

post accident sampling system

problem evaluation request

Plant Procedures Manual

surveillance requirement

standby gas treatment

shift support supervisor

Technical Specifications

plant service water

unresolved item

violation

Washington Nuclear Project-2