ML17291A915

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Insp Rept 50-397/95-19 on 950605-20.Violations Noted. Major Areas Inspected:Control Room Operations During Reactor Startup
ML17291A915
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 07/20/1995
From: Pellet J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17291A912 List:
References
50-397-95-19, NUDOCS 9507260023
Download: ML17291A915 (23)


See also: IR 05000397/1995019

Text

ENCLOSURE 2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-397/95-19

License:

NPF-21

Licensee:

Washington Public Power Supply System

3000 George Washington

Way

P.O.

Box 968,

MD 1023

Richland,

Washington

99352

Facility Name:

Washington Nuclear Project-2

Inspection At:

Richland.

Washington

Inspection

Conducted:

June 5-20.

1995

Inspectors:

S.

McCrory, Reactor

Engineer,

Operations

Branch

Division of Reactor Safety

T. McKernon, Reactor

Engineer,

Operations

Branch

Division of Reactor Safety

R. Lantz. Reactor

Engineer.

Operations

Branch

Division of Reactor

Safety

D. Proulx, Resident

Inspector/WNP-2

Approved:~ on

.

e

e

.

ie

,

pera ions

rane

Division of Reactor Safety

'7-2.o - '/5

a e

Ins ection

Summar

A~tt d.

d

tt

.

d

1

p tt

1

t.

1

p

during reactor startup.

Results:

~0erations

~

Command. control

(which included procedure

use

and compliance)

~

and

communication of the control

room shift operators

were adequate

for safe

operation

but marginal in some areas

(Sections

1.2, 1.3,

and 1.4).

9507260023

950720

PDR

ADQCK 05000397

8

PDR

-2-

~

Corrective action measures

to date continued to be ineffective in

producing significant improvements

in performance in command

control,

and communication

(Section 2).

~

The operations staff continued to accept

and tolerate

conditions'onduct.

attitudes,

and performance that were conducive to errors

(Sections

2. 1 and 2:2).

~

The operations

organization did not effectively assert its leadership

role at the facility, especially outside of the operations

department

(Section 3).

~

The licensee's

50.59 evaluation,

which allowed deleting the shift

turnover procedure,

was superficial

and flawed (Section 1.3)

~

Licensee oversight

management

observations,

although fulfilling

managements

expectations,

were not routinely at the level of detail

and

interaction required to improve individual performance of watchstanders

(Section 4).

Summar

of Ins ection Findin s:

~

Violation 397/9519-01

was opened

(Section 1.3).

Attachments:

~

Attachment

1

- Persons

Contacted

and Exit Meeting

~

Attachment

2 - Management

Oversight Observation

Summary

-3-

DETAILS

1

SUSTAINED CONTROL ROOM OBSERVATION (71715)

As a result of multiple plant events reflecting problematic licensee operating

performance.

the

NRC determined that it was necessary

to conduct

an extended

observation of licensee control

room crew performance to confirm that control

room operating

crews were performing in accordance

with licensee

expectations

and procedures.

Recent

events

indicated that while the operating staff may

have

been

aware of and cognitively attempted to meet licensee expectations,

in

times of increased

stress

they often reverted to habitual

behavior patterns

that were no longer acceptable.

Those included, failure to maintain

command

and control,

use of very informal communication techniques,

failure to inform

other crew and management

of actions

and issues,

failure to use effective

team-building

techniques,

and informal procedure

use

and adherence.

The

intent of the inspection

was to observe control

room crew perf'ormance during

startup activities with a focus

on human performance

issues.

including command

and control practices.

crew briefings.

communication

frequency

and

effectiveness,

procedure

use

and adherence,

and log-keeping.

Two inspectors

were assigned to perform extended

observations

in the control

room on

a rotating basis.

The inspectors

used specific guidance,

specially

prepared for the inspection,

to focus thei r observations.

They took detailed

observation

notes which were provided to the team leader at the end of each

observation

period.

Additionally, they debriefed with the team leader daily.

After the departure of the inspection

team,

the resident inspector continued

control

room observations

as

a part of the inspection.

A third inspector,

assigned

as the team leader,

was responsible for

integrating the observations

of the other inspectors

and for interfacing with

the facility licensee.

In addition to reviewing the observation results,

the

team leader interviewed pertinent plant staff personnel'eviewed

various

licensee documentation'nd

observed daily outage closeout

and startup status

meetings.

1. 1

Control

Room Observations

During the period of June

5 - 12,

1995, the inspectors

observed activities in

the control

room.

These activities included operations

surveillance testing,

control

room operators'ommunication

practices,

control board operations,

shift-turnover, prejob briefings,

outage activities, supervisory oversight.

log taking,

command

and control.

and others.

During the observation period,

the plant transitioned

from outage activities to initial plant startup

and

power ascension

to about

15 percent

power.

The inspectors

observed

various

crew compositions

on day and night shift periods.

During the refueling outage

and preparations

for reactor plant startup,

two

crews were assigned

to the shift, with the additional licensed

personnel

utilized to help with the administrative

requirements

and production work of

the shift.

One crew was designated

as the on-shift crew, including

a shift

manager.

control

room supervisor.

lead reactor operator,

and reactor

operator.

Substantially

above average

background noise levels in the main control

room

were

a historic and well known control

room characteristic

at WNP2.

The noise

was generated

from various sources,

including ventilation, the plant computer,

and the physical configuration of the control

room and back panels.

At the

beginning of the observation

period. while the plant was in the last phase of

an outage, it was apparent that the operators

were challenged

not only by the

ambient noise.

(e.g.. ventilation and plant process

computer)

but also by the

number of simultaneous

functions being conducted in the control

room area.

These activities included surveillance testing of the fire protection system,

standby

gas treatment

system work, shift technical adviser's

work, operations

work control activities,

alarm annunciation

response.

and

a number of other

activities.

It was apparent that the number of ancillary functions

contributed'o the congestion

and noise level of the control

room without

contributing directly to the operation of plant systems

or components.

1.2

Command

and Control

The inspectors

observed

instances

of weak

command

and control during the

inspection period.

There were several

trainees

in the control

room at any

given time.

and they were frequently used to take logs'ormally without

direct supervision.

At one point, operators-in-training

were assigned

the

task of taking instrumentation

recordings

and data logging and failed to alert

the control

room supervisor or lead reactor

operator of an out of limit

drywell temperature

condition.

Average drywell temperature

was required to be

maintained

above

70 degrees

F for stress

consideration of large support

structures

in the drywell.

Across

a full day of log-taking,

encompassing

three shifts. all average

readings

were below 70 degrees

F, with no red

circled readings

and no action taken.

The control

room logs contained

a large

note (paragraph)

that di rected adjusting reactor

component cooling flow to

RCA-FC fan cooler units to maintain average

drywell temperature

greater

than

or equal to 70 degrees

F.

While preparing the next day's logs, the shift crew

recognized the out-of-limit readings

and secured the drywell fans to increase

drywell temperature to specification.

They then informed plant engineering

and requested

an, evaluation of the consequences

of the low temperatures.

The

inspector also noted that the day shift control

room supervisor

had not

reviewed the logs.

Control

room shift management

acknowledged the lapse in

adequate

oversight of the operator trainees

and failure to review the data

logs.

During the

same time period. the inspectors

observed

another

instance in which

prompt and thorough action was not taken in response

to an out-of-limit log

reading.

The control

room logs for Battery

Room 2 specified that

IMMEDIATE

action was required

when

room temperature

was less than

74 degrees

F (the

Technical Specification

minimum was

60 degrees

F).

Two consecutive

log

-5-

readings

indicated less

than

74 degrees

F during the day shift (8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

apart).

The readings

were red circled, but no action was taken to increase

the temperature.

The day shift had noted that the room heater

was not

working.

When the evening shift took the next log readings

which was still

less

than

74 degrees

F

~ they investigated

and found that only the heater

controller was malfunctioning, in that it would not automatically shut off.

A

clearance

had been prepared.

but not hung.

Therefore,

the evening shift

manager

decided to turn on the heater to restore the

room temperature

and

monitor heater

performance

and

room temperatures

more-frequently.

The

inspector noted that although this was

a positive action to restore

and

maintain the battery

room temperatures

above specified limits, the direction

given to the operator for maintaining battery

room temperature

was vague.

The

control

room supervisor only told him to maintain the temp above

74 degrees

F.

The di rection did not give

a range within which to control the temperature.

In another instance,

a number of outage work or surveillance

work packages

were not logged out as completed

by the control

room staff.

As

a consequence,

the control

room supervisor

and assistant

control

room supervisor

had to

subsequently

retrieve the packages

from the work control center.

Corrective

action was taken to change the sequence

of package

review and signout from the

control

room.

An inspector

observed

the control

room supervisor receive

a phone call from

technicians

in the field who were conducting

main steam isolation valve

position logic tests.

The technicians

requested

status of the main steam

isolation valve position indications in the control

room,

and requested

the

main steam isolation valve isolation logic push buttons

be depressed

to reset

the logic.

The control

room supervisor

went to the appropriate

panels

noted

the valve positions,

and then reset the logic by depressing

the two reset

push

buttons.

The control

room supervisor

then reported his actions to the

technicians.

The control

room supervisor told the reactor operator that the

logic was reset

when the reactor operator questioned

the control

room

supervisor

on the status of the test.

This same control

room supervisor

stated later that he routinely depressed

all main control board logic reset

push buttons during turnover.

This was confirmed during observation of

turnover.

The inspector

asked the management

oversight observer if the above

actions

by the control

room supervisor were appropriate.

The management

oversight observer stated that it was inappropriate for the control

room

supervisor to operate

panel

switches

except in cases of an emergency,

and that

the control

room supervisor

should remain in a position of oversight

and

di rection of activities.

(On Harch 3,

1995.

management

had communicated,

in

the form of an electronic

memorandum, explicit expectations

that shift

supervisory

personnel

not operate

equipment controls except in an emergency.)

The practice of resetting logic during turnover was also noted

as

inappropriate.

however. this expectation

had not been promulgated to the crews

prior to the inspector's

observation.

-6-

The inspectors

noted frequent

changes of the panel reactor operator

between

the shift crews.

and in one instance,

for approximately

one minute, only the

nondesignated

reactor operator

was in the "at the controls" portion of the

control

room.

All of the other operators

and senior operators

were either

outside the control

room or at the work table in between the instrument

panels.

Management

stated that this was permitted

by Technical

Specifications.

but was not

a desired situation.

The inspector also noted

that when the switch between

panel

operators

was done, little or no status

turnover was given to the operator taking the boards..

Towards the end of the observation

periods

the inspectors

noted

a marked

improvement in control

room decorum.

A focused. alert.

and directed effort

was placed

on transitioning into the plant startup procedure.

Activity in the

control

room was orderly and nonintrusive to the activities of the control

board operators.

The prestartup briefings were focused

and well conducted.

Control of the approach to criticality was good as were the coordination of

heatup

~ reactor core isolation cooling test preparation,

and placing the

turbine bypass

valves in automatic.

1.3

Procedure

Ade uac

While conducting main steam isolation valve isolation logic tests,

the crew

received

an unexpected full main steam isolation valve isolation.

The main

steam isolation .valves stroked

from full open to full shut.

After

investigation,

the crew discovered

the procedure

was inadequate if the reactor

mode selector

switch was not in the

"Run" position.

Additionally, the

procedure did not identify expected

main control board alarms.

The inspector

observed

good response

by the crew and others to evaluate the cause of the

unexpected

isolation signal.

This was reported to the

NRC and

a Problem

Evaluation Request

was written.

While conducting reactor

core isolation cooling turbine testing,

the operators

started the reactor

core isolation cooling turbine and received

an unexpected

alarm which indicated

low cooling water flow to the lubricating oil cooler.

The procedure failed to establish

cooling water to the lubricating oil cooler.

During an automatic start of the turbines this valve opens to supply

lubricating oil cooling.

On June 9,

1995,

an inspector

observed

the shift and relief turnovers in the

control

room.

The inspector

noted that most of the operators

were on 8-hour

shifts.

However,

one pair of reactor operators

was

on 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts to cover

the absence

of the third reactor operator.

This pair of reactor operators

turned over in the middle of the shift rather than with the rest of the crew

at the beginning of the shift. The inspector

noted that the operators

on

12-hour shifts did not fill out and sign

a shift turnover checklist.

The

shift turnover checklists generally directed

the operators to discuss

important plant parameters

to ensure that

a formal and precise

exchange of

information occurred.

-7-

The inspector discussed

this observation with the shift manager,

the

operations

manager,

and the plant manager.

These licensee

representatives

stated that turnover between the operators

on the 12-hour shifts without the

checklist did not meet management's

expectations.

They stated that use of a

separate shift turnover checklist

was expected

whenever

an operator turnover

occurred

more than 30 minutes later than the crew turnover..

The inspector

researched

the licensee's

procedures

to ascertain

what

expectations

concerning shift and relief turnover

had been

communicated

by the

licensee in plant procedures.

The inspector

noted that the licensee did not

have

a plant operations

committee

approved

procedure that contained the

requirements

for shift and relief turnover.

Technical Specification 6.8. l.a.

referenced

Regulatory Guide 1.33,

and required

a procedure for "Shift and

Relief Turnover ."

In addition, Technical Specification 6.8.2 required

each

procedure of Technical Specification 6.8. 1 to be reviewed by the plant

operations

committee

and approved

by the plant manager.

Technical Specification 6.8. l.b required procedures

to implement the requirements of

NUREG-0737.

Item I.C.2 of NUREG-0737 'equired

turnover procedures

to include

a shift and relief checklist.

Because

the licensee did not have

a plant

operations

committee approved

procedure for shift and relief turnover that

included

a shift turnover checklist, this was

a violation of Technical Specifications 6.8. l.a. 6.8. l.b,

and 6.8.2 (Violation 397/9519-01).

In further researching this issue,

the inspector

noted that the licensee at

one time had

a turnover procedure for the operators,

but this procedure

had

been deleted recently.

The expectations

for shift turnover had been relocated

to Operating Instruction 19.

Operating instructions

were internal department

instructions that were not reviewed by the plant operations

committee.

Mainly, they contained

recommendations

for good operating practices that the

operators

were not specifically bound to follow.

The inspector

found that the shift turnover procedure

had been deleted

as part

of the procedures

improvement program.

The licensee's

program included the

goal of deleting or streamlining all procedures

that appeared to be

unnecessary

or burdensome.

When performing the

10 CFR 50.59 evaluation for

deleting the shift turnover procedure

requi rements,

the licensee

performed

an

inadequate

review of Technical Specification 6.8. l.a, Regulatory Guide 1.33.

and

NUREG-0737.

As part of the

10 CFR 50.59 reviews. the licensee did not

actually read the requirements.

The reviewers

performed

a word search,

using

an electronic version of their licensing basis

documents.

to determine

where

requirements

or commitments

were located.

In this instance,

the reviewer

used

a word string that did not match the exact words of the Final Safety Analysis

Report or Regulatory Guide 1.33.

Therefore,

the inspector

noted that the

licensee's

system for performing

10 CFR 50.59 evaluations

using the electronic

database

was not always fully effective in identifying requirements

and

commitments.

-8-

The inspector

informed licensee

management of this issue.

The licensee

acknowledged

the inspector's

finding and drafted

a procedure for the shift and

relief turnover.

However. the licensee's

new procedure for shift turnover

still contained

weaknesses,

and was not in accordance

with NRC requirements

and licensee

procedure writer s guidelines.

To address

the inspector's

concern,

the licensee

issued

a deviation to Plant

Procedures

Manual 1.3. 1 "Conduct of Operations-Department

Policies.

Programs

and Practices."

to reinstate

the shift and relief turnover requi rements in

formal plant procedures.

The licensee

added Section 4.20. l.h stating that if

an individual relieved

a position 30 minutes past the crew's turnover.

a shift

turnover checklist should

be filled out.

Howevers

the licensee did not appear to follow its own guidance in developing

this procedure

as

shown in the examples

below.

WNP-2 Plant Procedures

Manual

1.2.2 "Plant Procedure

Preparation"

defines the use of the word "shall" as

"used to denote regulatory requirements'xternal

commitments'nd selective

specific management direction."

Plant Procedure

Manual 1.2.2 defines

use of

the word "should" as

"used to denote

recommendations

but not enforceable

regulatory requirements

and managements

expectations."

When these

concerns

were conveyed to the licensee,

the licensee's

response

was to assert that most

other licensees

treated the situation

manner similar to the one that they had

chosen.

The revision to Plant Procedures

Manual 1.3. 1. Section 4.20 'tated that

control

room staff should fill out and sign

a shift turnover checklist

in accordance

with Operations

Instruction 19.

The inspector

noted that

a shift and relief turnover checklist was

a requirement of NUREG-0737

and was committed to by WNP-2 in thei r Final Safety Analysis Report.

Section 4.20 of this procedure

also stated that

a licensed operator

should only be relieved by a licensed operator.

The Technical

Specifications

required certain positions to be filled only by licensed

individuals.

~

Finally. Section 4.20 stated that the operators

should not take the

watch if they were unfit for duty,

and the offgoing operator

should not

allow himself to be relieved if he believed that his relief was unfit

for duty.

Fitness for duty requirements

for licensed operators

are

found in 10 CFR 26.

and

10 CFR 55.

1.4

Communications

1.4. 1

Shift and Relief Turnover Observations

The oncoming crew individually conducted turnover,

which included various log

and equipment status

reviews

and

a main control

room board walkdown and

discussion with the off-going watch.

The inspectors

noted good information

exchange

during operator turnovers while performing control board walkdowns.

-9-

The on-coming shift crew members

were advised of specific control board status

and on-going work activities.

After all members of the oncoming crew relieved

the shift, the enti re crew assembled

in the control

room for a shift brief,

which lasted

from 10 to 30 minutes.

The brief was led by the control

room supervisor.

and each operator

was given

an opportunity to discuss

his observations

during turnover.

Communications

observed

during shift briefings were marginally adequate.

The inspectors

noted that several

of the briefers

spoke too softly to be easily heard over

the control

room background noise.

In some instances.

either the shift

manager or

a management

observer

would request the briefer to speak

louder,

but this did not always occurs

and that portion of the brief was missed

by

some of the crew.

The day-shift manager

conducted

good post-Plan-of-the-Day

meeting crew briefings that clarified the objectives for the day,

lessons

learned.

and items of significance.

Howevers

in one instance.

shortly after

shift turnover on the night shift,

an inspector

asked the shift manager

about

the activities that were to be accomplished

during the shift and thei r

priorities.

The shift manager

admitted that he did not know and had to obtain

the information from the management

oversight observer.

During one turnover.

an off-going shift manager

gave permission for personnel

to enter the drywell under vessel

area,

to remove shielding

and other

materials.

This permission

was given over the phone directly from the shift

manager to the technicians

requesting

the entry.

The off-going control

room

supervisor

had received the request

by phone originally. and

had attempted to

get the shift manager's

permission

by talking loudly across

the control

room.

Both the control

room super visor and shift manager

had to request

a repeat of

the other's request/report

due to inability to hear clearly.

Finally, the

shift manager

picked up the phone

and took the call directly.

After granting

the permission,

the shift manager

did not make

a positive report to the

control

room supervisor

that he had granted the permission.

After turnover,

the inspector

asked the

new shift manager

why personnel

had entered the

drywell, to which he stated for inspection

and evaluation of potential

needed

work: he did not know the reason for entry primarily was to remove staged

material.

The inspectors

noted several

other examples

where turnover

information was either incorrect

or incomplete.

During another turnover'

high pitched,

recurrent

alarm at

a back panel

of'he

control

room, initiated two-three times per minute throughout the turnover

.

The alarm was

a security alarm, which was the result of security testing

badges

whose access

had been

revoked.

This was

an unnecessary

distraction to

the turnover.

1.4.2

General

Communications

Control

room communications

were sometimes difficult because of multiple

activt,ties being conducted

simultaneously

and the background noise level.

At

times. inconsistent

acknowledgements

of control panel

alarms were observed.

Typically. communications

conducted

during more formal settings

such

as the

performance of surveillance tests

were more disciplined.

Communications

were

-10-

generally adequate;

however,

the inspectors

observed

several

examples

where

communications

reverted to informal jargon or lax discipline that was

sometimes ineffective and did not meet

management

expectations.

Communications

recipients

accepted

inappropriate

communications,

indicating

a

lack of questioning attitude.

During testing of relays for proper operation of Valve RCC-V-6. the reactor

operator controlling the test in the control

room directed the assisting

reactor operator to "watch the 6 valve,

need it open when I start the pump."

After the evolution was completed.

the inspector

asked the assisting

reactor

operator what he understood

the direction to mean, to which he stated

he was

not sure,

but thought that he was being told to verify Valve RCC-V-6 opened

after the second reactor

component cooling pump was started.

The reactor

operator stated that he thought it only had

an auto-close feature.

but that

the di rection he received

made him think it might auto-open.

A shift

technical

advisor in senior reactor operator

upgrade observation training

stated that he too thought the valve would auto-open

based

on the direction

given by the first reactor operator.

When the valve did not auto open, the

reactor operator

attempted to open the valve.

After the third attempt,

Valve RCC-V-6 stroked open.

The reactor operator then checked the appropriate

valve logic prints and verified that the valve would only auto close,

and had

a 10-second

time delay for both an auto-close

and manual

open.

The original

di rection from the reactor operator

was unclear

and confusing.

Several

instances

were noted

when nonspecific communication were used.

"Still

got 176 (no system or units)," "the va1ve position relays?

(no system said),"

watch Valve 6 (no system),"

"1825,

CRD Pump Swap (configuration not

specified)." were examples of communications

observed that were not specific

and subject to misinterpretation.

The inspector

also noted

a frequent lack of

positive feedback

from the performer of an order that the task was

accomplished.

For example, after

a

pump was started

as ordered,

the reactor

operator did not routinely report back to the control

room supervisor that the

pump started

normally.

Several

instances

were noted when the control

room

supervisor did not acknowledge reports,

and the reactor operator did not

insist on an acknowledgement.

All of these

were contrary to the

communications

expectations

of licensee

management.

The inspector

noted that operators

in the control

room did not utilize

headphones.

The inspector also noted the practice of yelling across

the

control

room from the back panels while conducting the main steam isolation

valve logic checks.

Phone jacks were available,

but not utilized.

When

questioned,

the operators

stated that they had always conducted this test in

the manner observed.

and did not know if the phone jacks worked.

Similarly,

the inspector

observed that phone jacks were not utilized during testing of

the reactor core isolation cooling turbine.

After the reactor core isolation

cooling turbine was started

from the control

room.

a muffled noise

came over

the radio in the control

room.

The control

room supervisor

keyed the mike and

requested

a repeats

to which the reply came s".owly but still not very clear,

"STOP

THE RCIC TURBINE."

The control

room supervisor

then ordered the turbine

tripped.

The poor

communications

delayed tripping the turbine for

-11-

approximately 30-45 seconds.

The inspector

asked if phones

were considered

for this or other tasks.

especially in high noise areas.

The operators

stated

that phones

were not used,

and that they were not sure that the capability

existed.

When the test

was attempted

again.

the oper'ators

used the control

room phone

and

a local phone in the reactor core isolation cooling room for

direct communications

between the control

room and the reactor core isolation

cooling pump room.

The reactor operator

stated that the communications

were

much clearer.

A note on the microfiche printer in the control

room said do not use the print

feature since it burned paper.

However, the note was not conspicuous,

and did

not cover the button to print.

The shift technical

advisor used the printer

which resulted in a strong

smoke smell in the control

room.

That invoked

action from the control

room supervisor,

a reactor operator.

and security

personnel.

Although the response

by control

room personnel

was rapid and

appropriate.

the incident was

an unwarranted distraction to the crew that

could have been prevented

through adequate

communication of the equipment

deficiency or proper controls to prevent operation of the print button.

2

IHPACT ON PERFORHANCE

The preceding information provided numerous

examples of weak performance

on

the part of WNP2 personnel

that help to form the basis of the

NRC conclusion

that operational

performance

has not improved significantly from that

summarized in

NRC Inspection Report 50-397/95-07.

The lead inspector

integrated

and analyzed these observations

with information obtained through

interviews.

review of licensee documents'nd

observation of peripheral

activities such

as the morning and afternoon status

meetings.

After

completing the integration

and analysis,

the inspection

team concluded that

several

conditions existed that created

an envi ronment favorable to a high

frequency of performance errors

and high consequences

when errors occurred.

The conditions

and the resultant

behaviors did not create

an immediate safety

concern nor constitute

a failure to comply with regulatory requirements.

with

one exception

as described

in Section 1.3 above.

However, they did represent

conditions

and behaviors

conducive to poor performance that could result in or

aggravate

adverse

operational

consequences.

2. 1

Conditions Conducive to Poor

Performance

The high control

room ambient noise level

has

been

recognized for some time as

a condition that adversely

impacts

communication in the control

room.

Further.

such

a condition can induce

an additional stress

level for operators

required to work in such

an environment for extended

periods of time.

This

can increase

the incidence of errors.

-12-

The layout of the personal

work stations

in the control

room near the systems

controls'ndicators.

and alarms

increased

the vulnerability to operational

errors.

The placement of the shift technical

advisor work station

and

administrative processing

work stations

in near'proximity to the control

room

watch stations

increased

the amount of activity in the area that was not

related dir ectly to controlling the plant.

Two different standards

of conduct of operations

were implicitly promoted

by

procedures

and policy.

There was

a definitive checklist of requi red

communication techniques

in Section 4. 10.3 of Plant Procedures

Manual 1.3. 1,

"Conduct of Operations,"

which began with the statement:

"In addition to

standard

Communication Techniques,

the following are required During Abnormal

Conditions or (when) Entry into the

EOPs is necessary."

Further,

an inspector

who had recently observed

crew performance

in the licensee's

simulation

facility. observed

a significantly different level of performance in the

control

room during extended

observations.

Actual control

room behavior

was

much less

formal and rigorous.

An observation

by a licensee control

room management

oversight participant

regarding inconsistent

and poor electrical distribution component labeling

prompted

management

to consider training plant staff to cope with inconsistent

or poor labeling rather than revising the priority or pace of the label

upgrade

schedule to correct the problem.

Poor labeling had been previously

identified

as contributing to errors

made while establishing

a clearance

for

electrical

maintenance

(NRC Inspection

Report 50-397/95-07).

Other equipment

and component labeling concerns

or weaknesses

have also been reported in NRC

Inspection

Reports

50-397/94-12,

94-26.

and 94-27.

NRC inspection activities regularly identified procedural

inadequacies.

deficiencies,

or weaknesses

that affected plant operations

and activities in

the plant.

(Refer to

NRC Inspection Reports

50-397/94-12,

14,

17,

19.

21, 24.

27. 32. 34, 95-03.

05,

07,

and 09.)

During the inspection,

additional

procedural

problems

were identified,

some of which contributed to unplanned

plant responses.

Licensee

management

indicated that there was

a focused

program for improving alarm response

and abnormal

operating procedures:

however.

improvement of other procedures

was expected to result from the

regular biennial

reviews.

None of the procedural

problems identified during

the inspection related to alarm response

or abnormal

operating

procedures.

While many of the procedural

problems were licensee identified and

some

had

di rect impact on system

or equipment operation or testing,

the licensee

was

not pursuing

a comprehensive

approach of enhanced identification and

correct>on of nonalarm or abnormal

procedural

problems.

The plant and operation

managers

reenforced

a policy of making shift

supervision

and licensed operators

responsible for correcting the various

performance

weaknesses

identified by both the licensee

and

NRC inspectors,

in

this and previous inspections.

However. it was unclear that the licensee

had

assured

that the shift operators

and supervisors

were adequately trained

and

equipped to carry out that responsibility.

After the crew involved in the

April 9.

1995. reactor water cleanup

system event

(NRC Inspection

-13-

Report 50-397/95-17)

was reconstituted.

the

new crew received

a day of team

building training which consisted

largely of discussion

topics

and reviews of

previous events.

Apart from that and an expressed

intent to implement

a

general

reconstitution of crews in October

1995, operations

management

did not

identify to the inspectors

any aggressive efforts in progress

or planned to

enable operators

to correct the operational

performance

weakness

identified in

this and other

recent inspection reports.

2.2

Behavior Conducive to Poor

Performance

During an outage/startup

status

meeting,

the electrical

maintenance

manager

displayed

a lack of aware'ness

of or sensitivity to shutdown risk concerns.

The manager

complained that the control

room was interfering with the timely

and efficient completion of some relay testing

by prohibiting his workers from

starting

some of the work in accordance

with their schedule.

An operations

representative

at the meeting

had to point out to the manager that the actions

of his workers would have rendered

both diesel

generators

inoperable during

the time the testing

was being performed.

Even after that, the manager

continued to focus

on getting operations to cooperate to permit his people to

complete their scheduled

work.

On two separate

occasions.

control

room observers

(one.

a licensee

management

oversight observer)

witnessed

periods in which only one licensed operator

was

in the control

room in the vicinity of the equipment controls,

instruments,

and annunciators.

In both cases.

when the situation

was pointed out to the

on-shift crew, the response

was essentially that Technica'I Specifications

only

required

one operator to be in the controls area while shutdown.

In both

cases'he

shift was staffed with an augmented

crew,

and in neither case

was

an emergency condition present that warranted

leaving the area of the controls

staffed with only one operator.

In the instance

observed

by the

NRC

inspector,

the sole operator

was

engaged

in a surveillance test

and not fully

attentive to general

plant indications.

Neither case

appeared

an appropriate

alloCation of augmented

crew resources

available.

As previously discussed.

an inspector

observed

a shift manager

and control

room supervisor

shouting to one another

across

the control

room while the

control

room supervisor

attempted to be

a link with another party on the

telephone.

After two failed attempts at information exchange,

the shift

manager

came to the phone

and spoke with the party directly.

An inspector

observed

two operators

performing

a surveillance test which

required

them to be on opposite sides of an electrical cabinet.

Rather than

using the phone jacks installed to assist

communications for that type of

activity. the operators

shouted

over and around the cabinet.

During

a test of the reactor core isolation cooling system.

operators

were

using radios to communicate

between the control

room and local areas of the

plant where conditions for radio communication were known to be poor.

The

local operator called for a trip of the reactor core"isolation cooling turbine

during the test but because of poor radio conditions, it took an additional

30 to 45 seconds

to clarify the communication

and then trip the turbine.

Instances

of nonadherence

to procedures

were observed with regard to the

battery

room and drywell temperature

logs as noted in. Section 1.2 above.

An additional

instance of confusing communications

during

a valve relay test

is described

in Section 1.4.2 above.

3

OPERATIONS ORGANIZATION LEADERSHIP ROLE

NRC Inspection Report 50-397/95-07

noted that operations

department

ownership

of the plant was not evident

and gave several

supporting

examples.

During an

interview for this inspection,

the operations

management

expressed

strong

disagreement

with that perspective.

The principal example of how ownership

was being exercised

was to point out that augmenting the control

room crews

during the outage

had been effective in controlling outage activities.

A

closer examination of that situation by the inspectors

revealed that augmented

crews were more effective in dealing with the challenges

and obstacles

created

by support organizations.

Many of those challenges

and obstacles

arose

as

a

result of poor planning and scheduling.

lack of sensitivity to operational

impact.

or

a lack of recognition of operations'eadership

authority.

Moreover, operations

had not communicated,

at middle and upper

management

levels.

standards

of conduct

and performance for activities in the plant

control

and equipment

spaces

that applied to all site personnel

regardless

of

their organizational

alignment.

To the extent that any such attempt

was

made,

it relied on the on-shift operators

to police and correct performance

deficiencies

on the part of support personnel.

It has already

been noted that

the operators

themselves

did not sustain the desired level of performance

and

leadership

by example. without the added responsibility to effect performance

and behavior

changes

in support organization personnel.

4

LICENSEE MANAGEMENT OVERSIGHT EFFECTIVENESS

The inspectors

observed

management

oversight of the operating

crews.

The

inspectors

noted that. in most instances'eedback

took the form of

end-of-shift briefings with the shift manager

and written input to operations

department

management

of broad issues

and performance

suggestions.

The

inspectors

witnessed

some

management

oversight feedback briefings during shift

turnover.

The oversight

managers

appeared

to be fulfillingtheir role in

accordance

with management

expectations.

However, their activities

had not

been

focused

on feedback to improve individual operator

performance,

such

as

were described

in Section 2.2 above,

An inspector

reviewed the written feedback

provided by the oversight managers.

The inspector

concluded that management

oversight activity had.produced

many

-15-

good findings.

The operations

manager

summarized

the strengths

and weaknesses

from the oversight observations

which is provided in Attachment 2.

However,

the inspector concluded. after discussions

with the plant and operations

managers'hat

the licensee did not consider aggressive

action warranted to

address

most of the observed

weaknesses

identified by the oversight managers.

Moreover. the observations

of the

NRC inspectors

highlighted earlier in this

report contradicted

some of the strengths

summarized

from the oversight

observations:

~

Communications:lax or informal communications

~

Crew turnovers:important

information not transferred

~

Procedure

compliance:fai lure to act promptly for log readings

~

(juestioning attitude:failure to understand

battery

room temperature

control capability

~

Surve'i llance Tracking:test completions not logged initially

5

CONCLUSIONS

Operations

management

had taken

some corrective actions to improve the

performance of operations

department staff. including

a performance

measurement

process to track and trend performance

data that provided

comparisons

between operating

crews.

Howevers

most of the corrective actions

taken or planned were of low intensity and loosely structured or focused.

Many of the observations

made

by the inspectors

were similar to previous

observations

made during recent inspections.

The inspectors

concluded that

a

number of conditions existed that presented

continual challenges to successful

operating

crew activities and decision making.

Those continual challenges

were characterized

as conducive to potential failure because

they represented

barriers to successful

operating activities or provided incentives to err.

The operations

organization

was often ineffective when attempting to assert

its leadership

role due to weaknesses

within operations

and resistance

or

insensitivity from support organizations.

ATTACHMENT 1

Persons

Contacted

and Exit Meeting

1

PERSONS

CONTACTED

Washin ton Public Power

Su

1

S stem

  • V. Parrish

~ Vice President

Nuclear Operations

  • P. Bemis, Regulatory

and Industry Affairs Director

~J.

Swai les.

Plant General

Manager

  • C. Schwarz,

Operations

Manager

  • D. Swank,

Licensing Manager

  • B. Hugo. Compliance

Engineer

U.S. Nuclear

Re ulator

Commission

  • K. Brockman,

Deputy Director, Division of Reactor Safety

  • J. Pellets

Chief, Operations

Branch, Division of Reactor Safety

  • J. Clifford. Project Manager, Office of Nuclear Regulatory

Research

  • D. Corporandy,

Acting Chief. Reactor

Projects

Branch

E, Division of Reactor

projects

The inspectors

also interviewed various control

room operators'hift

supervisors,

shift managers,

management observers'nd

management

personnel.

  • Denotes those

who attended

the exit meeting

on June

20 '995.

2

EXIT HEfTING

An exit meeting

was conducted via teleconference

on June

20,

1995.

During

this meeting,

the inspectors

reviewed the scope

and findings of the report.

The licensee

acknowledged the inspectors'indings.

The licensee did not

identify as proprietary any of the information provided to, or reviewed by,

the inspectors.

ATTACHMENT 2

(Developed by the Licensee)

MANAGEMENT OVERSIGHT OBSERVATION STRENGTHS

l.

,

Increase

in performance in communications

(three (3) part, formality).

2.

Crew turnovers:

good quality.

3.

Annunciator response

4.

Management

involvement in critical activities.

5.

STAR techniques

- pulling fuses'anging

tags.

6.

Procedural

compliance

- crews ensuring strict compliance with

procedures.

7.

Professionalism.

8.

Crew briefs for evolution.

9.

Questioning attitude

- excellent for nonroutine evolutions

- need

improvement for routine.

10.

Ops crew interactions with management

personnel.

ll.

Attention to detail

- good

STAR techniques

caught problem with NCTL.

12.

Technical'pecification

awareness/reference

for evolutions.

13.

Surveillance Tracking - annunciator/test

in progress.

14.

Response

to emergencies

- injured personnel.

15.

Teamwork during outage

improving.

16.

Computerized

T/S/LCO logs.

17.

Attitude.

-2-

HANAGEHENT OVERSIGHT OBSERVATION WEAKNESSES

1.

Communication

- three (3) part communication,

inconsistent for routine

evolutions.

2.

Support personnel

needs

improvement in support of Operations activities

such

as

LOOP/LOCA testing.

3.

Look ahead at evolution - prepared for activities coming up.

4.

Procedure

compliance

- analysis paralysis.

5.

HCR noise level high, hindering communications.

6.

Lead

CRO - some inconsistencies

between

crews in providing leadership

for shift.

7.

Backing each other up

- inconsistent

between

crews.

I.e..

S/D clg

removal

from service.

8.

Schedule discipline

- need to be more knowledgeable of schedule.

9.

SH involvement in low valve (value) activities, provide more oversight.

10.

Admin load for CRS high,

needs

work.