ML17290A976

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Insp Rept 50-397/93-50 on 931130-940110.Violations Noted. Major Areas Inspected:Control Room Operations,Licensee Action on Previous Insp Findings,Operational Safety Verification,Surveillance Program,Maint Program,Event Repts
ML17290A976
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 02/04/1994
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17290A974 List:
References
50-397-93-50, NUDOCS 9402230090
Download: ML17290A976 (24)


See also: IR 05000397/1993050

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

No:

Docket No:

License

No:

Licensee:

Facility Name:

Inspection at:

Inspection

Conducted:

Inspectors:

50-397/93-50

50-397

NPF-21

Washington Public Power Supply System

P. 0.

Box 968

Richland,

WA 99352

Washington

Nuclear Project

No.

2

(WNP-2)

WNP-2 site near Richland,

Washington

November 30,

1993

January

10,

1994

R.

C. Barr, Senior Resident

Inspector

D. L. Proulx, Resident

Inspector

S.

P.

Sanchez,

Resident

Intern

D.

E. Corporandy,

Project Inspector

(December

13-17)

Approved by:

~Summer:

P.

H

ohnson,

Chief

React

Projects

Branch

1

Date Signed

Ins ection

on November

30

1993

Januar

10

1994

Re ort No. 50-397 93-50

Areas

Ins ected:

Routine,

announced

inspection

by the resident

inspectors

and

project inspector of control

room operations,

licensee

action

on previous

inspection findings, operational

safety verification, surveillance

program,

maintenance

program,

licensee

event reports,

special

inspection topics,

and

procedure

adherence.

During this inspection,

Inspection

Procedures

61726,

62703,

71707,

90712,

92700,

92701,

92702

and 93702 were used.

Safet

Issues

Mana ement

S stem

SIMS

Items:

None.

Results:

General

Conclusions

and

S ecific Findin

s

~Stree ths:

None .noted. within the

scope of this

inspection

.

Weaknesses:

Inadequate

management

controls

and chemistry evaluations

resulted

in a

chemical spill and Unusual

Event due to noxious gases

in the radwaste building

(Paragraph

4.a).

9402230090

940208

PDR

ADOCK 05000397

Q

PDR

Operator reasoning

in determining the operability of a containment isolation

valve was poor and untimely.

In addition,

the operators'ubsequent

actions

in responding to the inoperable

valve were weak due to

a poor shift turnover

(Paragraph

4.b).

Licensee

personnel left an unrestrained

compressed

gas cylinder (without a

protective

cap)

near safety related

equipment

and did not properly restrain

several

other compressed

gas cylinders,

which could have resulted

in missile

hazards

(Paragraph

5.b(10)).

The licensee violated

10 CFR 19. 11 by failing to properly post two Notices of

Violation'nvolving radiological working conditions

(Paragraph

5.b(12)).

Contrary to'the vendor manual, electricians

assembled

several

battery racks

with gaps left between the brackets

and cells

(Paragraph

5.c).

The Plant Operations

Committee review of. proposed on-line leak sealing of

valve HS-V-20 was weak.

The licensee failed to perform

an

ASME Section

XI

repair work plan for the on-line leak sealing.

Mechanical

maintenance

personnel's

understanding

of the construction of HS-V-20 was weak.

The

licensee

also did not initiate

a problem evaluation request

when discrepancies

were noted in the closeout of the HS-V-20 repair work procedure.

Weak

vertical

communications

were also evident in the MS-V-20 leak repair,

because

management

was misinformed of the location of the original leak and the

location of the leak sealant

adapters

(Paragraph

7.a).

Weak work coordination

among work control personnel

resulted

in extra outage

time for an emergency diesel

generator

(Paragraph

7.b).

Si nificant Safet

Matters:

None.

Summar

of Violations:

Two violations were identified involving the failure

to initiate

a

PER for

a maintenance

discrepancy

(Paragraph

7.a)',

and two

examples of failure to restrain

compressed

gas cylinders

(Paragraph

5.b(10)).

Four non-cited violations were also noted

(Paragraphs

4.a,

5.b(12),

and 7.a).

DETAILS

Persons

Contacted

V. Parrish,

Assistant

Hanaging Director for Op'erations

  • J. Gearhart,

guality Assurance

Director

  • H. Flasch,

Engineering Director

  • J. Streeter,

Executive Assistant

  • J. Swailes,

Plant Hanager

  • G. Smith, Operations Division Hanager
  • R. Webring, Technical

Services

Manager

  • H. Monopoli, Haintenance

Division Manager

.

  • D. Coleman,

Acting Regulatory

Programs

Manager

  • W. Barley, Radiation Protection

Manager

  • J. Albers, Corporate Radiological

Health Officer

  • H. Kook, Licensing Manager
  • D. Larkin, Engineering

Services

Manager

  • J. Benjamin, guality Assessments

Manager

  • S. Davison,

Plant Support Assessments

Manager

  • J. Peters,

Administrative Manager

  • J. Rhoads,

Acting guality Support

Manager

  • W. Shaeffer,

Operations

Manager

  • T. Hessersmith,

Maintenance

Support

Manager

  • J. Sampson,

Maintenance

Production

Manager

  • B. Hugo, Licensing Engineer

The inspectors

also interviewed various control

room operators,

shift

supervisors

and shift managery,

maintenance,

engineering,

quality

assurance,

and management

personnel.

  • Attended the Exit Meeting

on January

31,

1994.

Plant Status

1

At the start of the inspection period,

the plant was operating at

100%

power.

On December

1,

1993, the licensee

declared

an Unusual

Event

(UE)

(Paragraph

4.a)

due to

a spill of liquid used for the processing of

glycol, which resulted

in the release

of noxious

fumes in the radwaste

building.

The Shift Manager

suspended

operator

rounds

and fire tours in

the radwaste

building for four hours.

The licensee

contained

the spill

and exited the

UE.

The plant continued to operate

at full power (except

for momentary

downpowers to support weekly bypass

valve testing

and

control rod exercises)

until the end of the inspection period.

Previou'sl

Identified

NRC Ins ection

Items

92701

92702

The inspectors

reviewed records,

interviewed personnel,

and inspected

plant conditions relative to licensee

actions

on previously identified

inspection findings:

a.

Closed

Violation 50-397 92-37-05

I

Violation 50-397/92-'7-05 identified that

as of August 15,

1992, the

licensee's

Nuclear Safety Assurance

Group

(NSAG) had not reviewed

'the industry advisory contained

in a March 18,

1992,

BWR

Owners'roup

(BWROG) letter

and

had not made

any recommendations

for

revising procedures,

training, operating activities, or

otherwise'mproving

unit safety associated

with core stability and the

BWROG

advisory.

The inspector

reviewed the licensee'.s

assessment

of the

problem

and subsequent

corrective actions.

The inspector

noted that

the corrective actions

appeared

appropriate to the circumstances

and

that they had

been

completed.

Corrective actions

included revision

of plant procedure

PPH 1. 10.4,

"External Operational

Experience

Review," to add

BWROG documents

containing

recommendations

or

guidelines for plant issues

to the list of documents

requiring

review.

Also, the Supply System

now issues

correspondence

every six

months to all

WNP-2 employees

reminding them of their responsibility

to forward pertinent information to the licensee's

Nuclear Safety

Engineering

group.

This item is closed.

4.

Event Followu

93702

92701

a 0

Unusual

Event Associated with

S ill of Gl col

On December

1,

1993,

the licensee

declared

an Unusual

Event due to

noxious

fumes in the radwaste building.

The licensee

reported this

event to the

NRC pursuant to

10 CfR 50.72.

The noxious

fumes were

caused

by an exothermic reaction

and hazardous spill in the Ozonator

skid which was

used for special

processing

of liquid waste.

The

exothermic reaction

and spill of 100 gallons of liquid were created

by mixing a glycol-water solution with 50% hydrogen peroxide

(H,O,)

solution

and then exposing this mixture to ultraviolet light and

ozone.

The foam that was created

as

a result of this reaction

blocked the air vent on the top of the tank and caused

the tank to

pressurize

and overflow.

Operations

personnel

contained

the spill,

and all personnel

evacuated

the radwaste building.

Approximately four hours later,

a tank containing

an additional

amount of the

H,O, and glycol mixture underwent

a similar foaming

and exothermic reaction, spilling an additional

200 gallons of

solution.

No personnel

were injured and

no safety

systems

were

affected.

However, the Shift Hanager

suspended

equipment operator

rounds

and fire tours for the radwaste building for approximately

four hours.

The Supply System root cause

team found that personnel

had bypassed

several

important processes

and management

directives

that

may have precluded this event.

d

k

d

'

The General Electric Organic Reduction

(GEOR) skid was obtained

by

the Supply System to reduce organic

compounds

in liquid waste to

ionic compounds

and carbon dioxide.

The

GEOR system

uses

ultraviolet light and ozone for this process.

GE designed this

system for use with low concentrations

of organic

compounds.

On

-3-

October 5,

1993, the Plant Operations

Committee

(POC)

approved

Plant

Procedures

Manual

(PPM) 11.2.23,30,

"Operation of the Organic

Reduction System," for implementation to process

100 drums of

glycol.

This procedure

did not discuss

the use of H,O, to

facilitate the processing.

The licensee

did not verify or validate

PPM 11.2.23.30 prior to its use,

as

was the licensee's

practice.

Initial

S stem Startu

The licensee first used the

GEOR system

on October

18,

1993, to

process

the water-glycol mixture.

The individual who wrote

PPM

11.2.23.30

made the final connections for use of the

GEOR system

without procedural

direction.

This individual was the only person

trained to operate

the system.

The processing

was not reducing the

glycol mixture at the desired rate,

and the licensee

was concerned

that they would not meet their commitment date of November

10,

1993,

to the Washington State

Ecology Department for completion of the

processing.

Use of H dro en Peroxide

In early November of 1993,

the licensee

discussed

with a vendor the

use" of H,O, to expedite

the process

and drive the reaction to

completion.

The licensee satisfactorily performed small-scale

laboratory tests with 5% glycol and

5% H,O, .solutions.

The licensee

performed

a second laboratory test using the

same concentrations

of

solution but with heat

added.

The licensee

also considered this

test to be satisfactory,

despite

the release

of a small

amount of

foam.

Licensee

personnel

did not evaluate

the effects'of this

reaction

on

a larger scale operation,

or one using stronger

chemical

concentrations,

and believed the potential

hazards

were minimal.

When purchasing

H,O the licensee

purchased

50% solution to

minimize the

amount of waste generated.

The licensee

did not dilute

this solution prior to its use or revise the procedure to indicate

that the Ozonator would be used with 50% H,O, solution.

Also, the

licensee

did not evaluate

the effect that the ultraviolet light and

the ozone would have

on the process with the addition of H,O,.

These errors led to the event of December

1,

1993.

Licensee

Investi ation

The licensee

formed,a root cause

team to investigate

the event

and.

recommend corrective actions.

The root cause

team determined that

several

Supply System

management

processes

and procedures

were not

followed leading

up to the event.

A general list of the weaknesses

noted included:

~

The Plant Operation

Committee

(POC) did not perform

a

10 CFR 50.59 safety evaluation for installation

and

use of the

GEOR

system.

~

The licensee

did not develop

a formal work plan that detailed

'he glycol processing

from beginning to end,

and

no support

from other departments

was delineated.

~

The author/user

did not perform

a verification and validation

of the procedure.

~

The licensee

did not provide

a method of measuring glycol

concentration

during the process.

Licensee

personnel

brought

a solution of 50% H,O, onsite with a

chemical

permit for only 3% H,O,.

The licensee

did not perform

an Industrial Safety

and Fire

Protection evaluation of bringing H,O, onsite per

PPH ).9. 1,

"Plant Safety Program."

The licensee

did not revise

PPH 11.2.23.30 to reflect the

use

of H,O, in the process.

Hanagement

did not assign. supervisory oversight for the

GEOR

process.

Health Physics

(HP) did not evaluate

the hazards

of using

H,O,

in the radiologically controlled area.

~

Personnel

performing the glycol processing

did not submit

an

ALARA scope

sheet;

therefore,

HP did not assign

a radiation

work permit

(RWP) for the glycol processing.

The inspector

concluded that the licensee

had done

a thorough

investigation

and

had identified the root causes

and initiated

effective corrective actions for the event.

The licensee's

,corrective actions

included procedure

enhancements

and disciplinary

action for the individuals and management

personnel

who were

directly involved.

However,

some of the procedure

adherence

issues

noted'during this event

appeared

to violate

NRC requirements.

The inspector

noted that Section

11.2 of the

FSAR describes

in some

detail the licensee's

methods for processing

radwaste

and does

not

discuss

the method being used

when this event occurred.

The failure

to perform

a

10 CFR 50.59 evaluation for the change in the method

of processing liquid r adwaste

is

a violation of NRC requirements.

However,

because

the criteria of Section VII.B(2) of the

NRC

Enforcement Policy were met, this violation is not being cited

(Non-cited violation

(NCV) 50-397/93-50-01,

Closed).

The licensee

performed the glycol processing

evolution in

a

radiation

area

on the 437-foot elevation of the radwaste building.

The individual performing the setup

and operation of the

GEOR system

signed in on

RWP 2-93-00028 "Supervisory

and Hanagement

Field

Inspections."

The 'scope of this

RWP does

not allow work or other

operations to be performed.

PPH 1. 11.8,

Revision 4, "Radiation Work

Permit," requires in Paragraph

6.4 that if work is to be

added to

an

existing

RWP, the pre-job planning process

must

be followed,

including submitting

an

ALARA scope

sheet.

These

requirements

in

PPH 1. 11.8 were apparently not followed.

HP personnel

stated that

if an

ALARA scope

sheet

had

been submitted,

a new

RWP would have

b.

been

issued.

In addition, the work would have

been

processed

through work control, which would have involved other licensee

groups in the planning

and implementation of the glycol processing.

The failure to follow PPH 1. 11.8 was

a violation of Technical Specification (TS) 6.8. 1.

However,

because

the criteria of Section

VII.B(2) of the

NRC Enforcement Policy were met, this violation is

not being cited

(NCV 50-397/93-50-02,

Closed).

I

The inspector

concluded that other weaknesses

existed that were not

addressed

in significant detail in the root cause

evaluation.

Licensee

managers

were

aware that the glycol processing

evolution

was to take place.

Hanagement

also discussed

the use of a

50% H,O,

solution in this process

during

a morning meeting the week the event

took place.

Although management

appeared

to be knowledgeable of the

glycol processing,

they did not appear to sufficiently question

whether the evolution had

been properly analyzed.

In addition, the inspector

concluded that the controls of PPM

1. 16.6C,

"Conduct of Infrequently Performed

Tests or Evolutions,"

may have

been applied.

PPH 1. 16.6C controls included assigning

a

line manager to ensure that

an unusual

evolution proceeds

smoothly

and in accordance

with Supply System procedures

and policies.

PPH

1; 16.6C also included criteria (e.g. first time tasks,

work done

under

a Technical Specification action statement)

to be used to

determine if the controls for infrequently performed evolutions

apply to any particular task.

The processing

of glycol in the

GEOR

system with H,O, was a'irst-time evolution.

Although the criteria

governing the applicability o'f 1. 16.6C

may not have

been clearly

met, the Plant Hanager stated that the 1. 16.6C process

has suffi-

cient flexibilitythat management

may direct the use of the

PPH

1. 16.6C controls at any time.

The inspector discussed

the above evaluation with the Plant Manager,

who acknowledged

the

NRC comments.

Test Failure of RCIC-V-63

On December

2,

1993,

the licensee

performed surveillance test

PPH

7.4.7.3.3.C,

"Reactor

Core Isolation Cooling

(RCIC) quarterly Valve

Test," for RCIC-V-63.

The valve failed its stroke time test.

At

1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br />

on December

2,

1993,

the operators

noted that RCIC-V-63

exceeded

the closing time (action range)

prescribed

in the

procedure,

but they did not immediately declare

the valve

inoperable.

Instead,

the operators

repeatedly

cycled RCIC-V-63

until they obtained

a satisfactory closing, time.

The inspector

concluded that the operators

performed poorly in responding to this

failed surveillance.

PPH 7.4.7.3.3.C specified

an action range for RCIC-V-63 closing time

of 10 seconds.

This 10-second limit was based

on adequate

isolation

time for environmental qualification of equipment in the reactor,

building.

However, the

TS lists the containment isolation time of

RCIC-V-63 as

16 seconds.

The operators,

at the advice of the system

engineer,

continued to stroke the valve to get decreased

stroke

times.

At 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br />

on December

2,

1993, the Shift Hanager

contacted

the Operations

Hanager.

The Operations

Hanager directed

the Shift Hanager to declare

RCIC-V-63 inoperable.

The operators

then shut RCIC-V-63 and declared

the valve inoperable.

The licensee

initiated

PER 293-1378 to document this problem

and entered

TS

action statement

(TSAS) 3.6.3.a.2,

which states

that if a contain-

ment isolation valve is inoperable,

the affected penetration

must

be

isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

by use of at least

one closed

and deacti-

vated valve, or the plant must

be placed in hot shutdown within the

next

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

A shift turnover

had occurred prior to the swing shift operating

crew deactivating

RCIC-V-63.

Due to

an apparently

inadequate shift

turnover between

the swing and graveyard

crews,

the graveyard

crew

did not deactivate

RCIC-V-63 either.

At 0743 hours0.0086 days <br />0.206 hours <br />0.00123 weeks <br />2.827115e-4 months <br />

on December 3,

1993, the day shift crew discovered

the discrepancy

in following

TSAS 3.6.3.a.2.

and subsequently

deactivated

RCIC-V-63.

Approxi-

mately 13.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />

had elapsed

before the action prescribed

in TS 3.6.3.a.2

was met.

Although the licensee

did not violate the

TS (16

hours total time are allowed for a shutdown), this event indicated

the need for more thorough turnovers

and more timely and appropriate

operability determinations.

Following the event of December

2,

1993, the licensee

reanalyzed

the

isolation time for RCIC-V-63 based

on environmental qualification.

Using

a more up-to-date

and realistic computer

code,

the licensee

determined that for environmental qualification, the maximum isola-

tion time would be

26 seconds.

Because this number

was in excess of

the containment isolation time in the TS, the licensee

modified the

acceptance

criterion for closure of RCIC-V-63 to

16 seconds,

as is

listed in the TS.

PPH 1.5. 1, "Technical Specifications

Surveillance Testing Program,"

required that if components

exceed their action range during

testing,

the component shall

be declared

inoperable

at the time

personnel

recognize that the data

are outside the action range.

In

addition,

Paragraph

4.0.5 of the basis for the

WNP-2 TS states

that

the

ASHE Section

XI "24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> grace period" prior to declaring

a

valve inoperable is not allowed.

This requirement

was clarified in

Generic Letter (GL) 91-18,

"Resolution of Degraded

and Nonconforming

Conditions."

Despite the

NRC and 'licensee

procedural direction, the

licensee

personnel

believed that they had

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to make

an

operability determination.

PPH 1.3. 12B, "Operability Evaluations,"

allowed

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for opera-

bility determinations,

without exempting instances

.when equipment is

obviously inoperable

and should

be declared

inoperable

immediately.

GL 91-18 states that in most cases operability determinations

can

be

made immediately,

but there could be cases

in which additional

information would be necessary

to make the determination within 24

hours.

The

GL noted that in a few exceptional

cases,

more than

24

hours would be required.

PPH 1.3. 12B appeared

to imply that

24

hours (or more)

are allowed for all operability evaluations.

This

apparent

discrepancy

between

PPHs 1.3. 12B and 1.5. 1 led licensee

personne1

to believe that they were not required to act

upon the

degraded

condition immediately.

The inspectors

discussed

the

above

comments with the Plant Hanager,

who acknowledged

the

inspectors'omments.

The licensee

was concurrently reviewing the Supply

System's original actions

taken in response

to

GL 91-18.

Two non-cited violations were noted.

5.

0 erational

Safet

Verification

71707

a.

Plant Tours

The inspectors

toure'd the following plant areas:

Reactor Building

Control

Room

Diesel

Generator Building

Radwaste

Building

Service Water Buildings

Technical

Support Center

Turbine Generator Building

Yard Area and Perimeter

i

b.

The inspectors

observed

the following items during the tours:

(I)

. 0 eratin

Lo

s

and Records.

The inspectors

reviewed records

against Technical Specification

and administrative control

procedure

requirements.

(2)

Honitorin

Instrumentation.

The inspectors

observed

process

instruments for correlation

between

channels

and for

conformance with Technical Specification requirements.

(3) ~hit'l

i

.

Th

i

p t

b

d

t

1

d hift

manning for conformance with 10 CFR 50.54(k), Technical

Speci-

fications,

and admini'strative procedures.

The inspectors

also

- observed

the attentiveness

of the operators

in the execution of

their duties,

and the control

room was observed

to be free of

distractions

such

as non-work related radios

and reading

materials.

(4)

E ui ment Lineu s.

The inspectors verified valves

and

electrical

breakers

to be in the position or condition required

by Technical Specifications

and administrative

procedures

for

the applicable plant mode.

This verification included routine.

control board indication reviews

and conduct of partial

system

lineups.

Technical Specification limiting conditions for

operation

were verified by direct observation.-

(5)

E ui ment

Ta

in

.

Selected

equipment, for which tagging

requests

had

been initiated,

was observed to verify that tags

were in place

and the equipment

was in the condition specified.

(6)

General

Plant

E ui ment Conditions.

Plant equipment

was

(8)

observed for indications of system leakage,

improper lubrica-

tion, or other conditions that would prevent the system

from

fulfillingits functional requirements.

Annunciators

were

observed to ascertain their status

and operability.

'ire

Protection.

The inspectors

observed fire fighting

equipment

and controls for conformance with administrative

procedures.

On January

3,

1994,

the inspector

noted that untreated

wood was

left near the high pressure

core spray

(HPCS)

pump.

Chemistry

personnel

had

assembled

a temporary sampling rig out of two

wooden

mop handles

and

a metal jar for sampling the floor

drains.

The inspector contacted

the Shift Hanager,

who then

directed

an equipment operator to remove the wood.

The Shift

Hanager also contacted

the Fire Harshall,

who determined that

the small

amount of wood (even untreated)

would not pose

a

threat to the overall fire loading of the

HPCS

pump 'room.

The

licensee

contacted

the chemistry personnel

involved and

.emphasized

that untreated. wood is not allowed in vital areas.

Plant Chemistr

.

The inspectors

reviewed chemical

analyses

and

trend results for conformance with Technical Specifications

and

administrative control procedures.

During this inspection period, reactor water conductivity

slowly increased

from about 0. 12 umhos/cm to

a maximum of 0. 19

umhos/cm.

The licensee

determined that

a small tube leak

existed in the main condenser.

The licensee

stated that they

would attempt to perform on-line tube plugging of the leak in

the near future.

The inspectors will follow the issue of

elevated conductivity in subsequent

inspection periods.

Radiation Protection Controls.

The inspectors periodically

observed radiological protection practices

to determine whether

the licensee's

program was'eing

implemented in conformance

with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors

also observed

compliance with Radiation

Work Permits,

proper wearing of

protective equipment

and personnel

monitoring devices,

and

personnel

frisking practices.

Radiation monitoring equipment

was frequently monitored to verify operability and adherence

to

calibration frequency.

On January

1,

1994, the licensee

implemented

the

new

10 CFR Part 20 regulations recently issued

by the

NRC.

The inspectors

noted that the

new regulations

(and the revised licensee

procedures)

define .radiation,

high radiation,

and high-high

radiation areas

at 30 centimeters

(or approximately

12 inches)

from the source.

Previously,

the licensee

defined these

areas

at

18 inches

from the source.

On January

3,

1994, the

inspectors

noted that

a hot spot

was labeled

as

80 rem/hour

on

contact

and

600 millirem/hr at

18 inches.

The inspectors

were

concerned that if the radiation levels. were measured

at 30

-9-

(10)

centimeters

from the source,

the radiation level

may be greater

than

1 rem/hour,

which would invoke high-high radiation

controls.

The licensee

measured

the radiation levels at 30

centimeters

from the source

and determined

the radiation level

to be 700 millirem/hour.

The inspectors

discussed, this

observation with the Radiation Protection

(RP) Manager.

The

RP

manager stated that the Supply System would continue to ensure

that all of the

new 10 CFR 20 regulations

were properly

implemented

and

any posting discrepancies

would be corrected.

Plant Housekee

in

.

The inspectors

observed

plant conditions

and material/equipment

storage to determine

the general

state

of cleanliness

and housekeeping.

Housekeeping

in the radio-

logically controlled area

was evaluated with respect to-

controlling the spread of surface

and airborne contamination.

On December

22,

1993, the inspectors

noticed that

an unsecured

nitrogen,gas

cylinder was lying on the floor next to the "A"

standby

gas treatment train on the

572 foot level of the

'eactor

building.

The cylinder had

no protective valve cap

and

was not restrained

in any way.

The license initiated

PER

293-1430 to document the finding.

During the

same tour, the

inspectors

found the. nitrogen bottles for the containment

atmosphere

control system loose in the restraining racks.

The

restraining bolts were not "snugtight"

as defined per Operator

Aid f89-0075.

The retaining bolts for these bottles

are of

various lengths,

therefore it is possible for the bolts to be

"snugtight" without the bottles being held tightly.

The

initiated

PER 293-1431 to document the finding.

The licensee

replaced

the restraining bolts with'olts of sufficient length

for proper bottle restraint.

This was verified by the

inspector during subsequent

tours.

The inspectors

were concerned that the inadequately

restrained

compressed

gas cylinders noted in these

two examples

could

become

a missile hazard during

a seismic event

and

damage

the

'afety related

equipment

near these cylinders.

PPM 1.3. 19, Revision

15, "Plant Material Condition Inspection

Program,"

Section 4. 1.5.a,

Paragraph

8, requires

compressed

gas bottles to be properly secured

against

a substantial

structural

member in such

a manner

as to preclude

them from

falling over.

In 'addition, the procedure

requires bottles to

be removed at the end of the work function if not properly

secured

in bottle racks.

The failure to restrain the

com-

pressed

gas bottles

as required

by

PPM 1.3. 19 is

a violation of

10 CFR 50, Appendix B, Criterion

V (Violation 50-397/93-50-03).

(11).~Securit

.

The inspectors

periodically observed

security

practices

to ascertain

that the licensee's

implementation of

the security plan was in accordance

with site procedures,

that

the search

equipment at the access

control points

was opera-

tional, the vital area portals were kept locked

and alarmed,

that personnel

allowed access

to the protected

area

were

badged

-10-

and monitored,

and that monitoring equipment

was functional.

(12)

10 CFR 19 Postin

.

As one of the quarterly inspection

items,

,the inspectors

reviewed the notices to the workers posted

pursuant to

10 CFR 19. 11.

The inspectors

determined that

some

of the licensee's

postings

were out of date

and others did not

comply with 10 CFR 19. 11.

On December

14,

1993,

the inspectors

examined

the licensee's

postings

per Part

19. 11.

WNP-2 has three controlled posting

areas for compliance with 10 CFR 19.

The inspectors

noted that

the licensee

posted

references

to where Notices of Violation

(NOVs) could be found for several

NRC inspection reports rather

than directly posting the

NOVs.

10 CFR 19. 11 requires that all

NOVs (and licensee

responses)

involving radiological working

conditions

be conspicuously

posted within two working days of

receipt.

Paragraph

19. 11(b)

exempts other items (e.g.,

the

regulations of 10 CFR 19 and 20, the facility license,

license

conditions,

and operating

procedures)

from posting if the

licensee

references

the location where these

documents

can

be

found.

However,

Paragraph

19. 11(b)

does not exempt

NOVs and

responses

from the conspicuous

posting requirement.

However, the inspectors

noted that the

NOVs and the responses

for NRC inspection reports

50-397/92-35

and 93-18 (which cited

violations concerning radiological working conditions)

were not

posted at the designated

locations.

The licensee

received the

NOV for 92-35

on December

1,

1992,

and the

NOV for 93-18

on

November

14,

1993.

Instead,

the licensee

posted

a note- stating

that these

items could

be found in the Plant Administration

office.

This indicated that licensee

management

was not keep-,

ing personnel fully informed of problems involving radiological

working conditions

one could encounter

upon entering the plant.

The inspectors

informed the Plant Administration Manager of

this discrepancy

on December

6,

1993.

Subsequent

to the

end of

the inspection period,

the Plant Hanager

acknowledged this

violation of the requirements

of 10 CFR 19. 11.

He also stated

that existing

NOVs and responses

related to radiological

working conditions

had

been

posted

as required,

and would be

properly posted

in the future.

Because

the criteria of Section

VII.B(l) of the

NRC Enforcement Policy were met, this violation

is not being cited

(NCV 50-397/93-50-.04,

Closed).

En ineered

Safet

Features

Walkdown

The inspectors

walked

down selected

engineered

safety features

(and

- systems

important to safety) to confirm that the systems

were

aligned in accordance

with plant procedures.

During the walkdown of

the systems,

items such

as hangers,

supports,

electrical

power

supplies,

cabinets,

and cables

were inspected

to determine

whether

they are operable

and in a condition to perform their required

functions.

Proper lubrication and cooling of major components

were

also observed for adequacy.

The inspectors

also verified that

certain

system valves

were in the required position by both local

- 11-

and remote position indication,

as applicable.

The inspectors

walked

down accessible

portions of the following

systems

on the indicated dates:

~Sstem

Diesel

Generators

Divisions 1, 2,

and 3.

Hydrogen Recombiners

Low Pressure

Coolant Injection (LPCI)

Trains

"A"p "B"j and

"C"

Low Pressure

Core Spray

(LPCS)

High Pressure

Core Spray

(HPCS)

Reactor

Core Isolation Cooling

(RCIC)

Residual

Heat

Removal

(RHR), Trains

"A" and "B"

Scram Discharge

Volume

Standby

Gas Treatment

(SGT)

Standby Liquid Control

(SLC)

Standby Service

Water

125V

DC Electrical Distribution,

Divisions

1

and

2

250V

DC Electrical Distribution

Dates

January

6,

1994

November 30,

December

23,

1993

December

15, 23,

1993,

January

3,

1994

December

15,

23,

1993,

January

3,

1994

December

15,

1993,

January

3,

1994

December

15,

23,

1993,

January

4,

1994

December

15,

23,

1993,

January

3 1994

November 30,

December

23,

1993

November 30,

December

23,

1993

November 30,

1993

December

6,

1993

December

27,

1993

December

27,

1993

On December

27,

1993, during

a walkdown of 125V battery B1-2, the

inspectors

noted that

a 1/4-inch gap existed

between

the battery rack and

the end cell.

The inspectors

noted that Section

58. 10 of the Exide

Battery Vendor Manual states

that when replacing

a cell,

"Hake sure the

plastic channel

on the

end rail is in snug contact with the cell."

The

inspectors notified the Shift Manager,

who contacted

the available.

electric shop personnel.

Engineering

personnel

initiated

PER 293-1434 to

investigate this issue

and provide for corrective maintenance.

Electri-

cians wrote

an emergency

Maintenance

Work Request

(HWR) to eliminate the

gap between

the battery cell

and rack.

As

a result of the

inspectors'oncern,

the licensee

examined the other station batteries

and found that

12-

three other batteries

had gaps

between

the

end cells

and the battery

racks.

Engineering

personnel

performed

an operability assessment

and determined

that despite

the batteries

not being in their intended configuration,

a

seismic event would not have impaired the function of the batteries.

The inspectors

noted that

a number of issues

concerning attention to

detail in the material condition of the safety-related

batteries

have

been identified by the

NRC in the past

two years.

The licensee

stated

that recent

improvements

made in the system engineer

walkdown would help

the licensee

to identify and correct their own problems.

The inspector

discussed

these

observations

with the Plant Manager.

One violation was identified.

Surveillance Testin

61726

The inspectors

reviewed surveillance tests

required to be performed

by

the

TS on

a sampling basis to verify that:

(1)

a technically adequate

procedure

existed for performance of the surveillance tests;

(2) the

surveillance tests

had

been

performed at the frequency specified in the

TS and in accordance

with the

TS surveillance

requirements;

and (3) test

results satisfied

acceptance

criteria or were properly dispositioned.

The inspector

observed

the following surveillance:

Procedure

0

Dates

Performed

7.4.6.I.O.I.a

Honthly Hain Steam Isolation

January

6,

1994

Valve

Leakage

Control

System Test, Division

1

No violations. or deviations

were identified.

Plant Maintenance

62703

During the inspection period,

the inspectors

observed

and reviewed

documentation

associated

with maintenance

and problem investigation

activities to verify compliance with regulatory requirements

and with

administrative

and maintenance

procedures,

required

gA/gC involvement,

proper use of clearance

tags,

proper equipment

alignment

and

use of

jumpers,

personnel

qualifications,

and proper retesting.

The inspector

verified that reportability for these

maintenance activities was correct.

The inspectors

witnessed

portions of the following maintenance

activities:

Descri tion

AP3789, Install Design

Change for Alternate

Local

Power

Range Honitor Inputs to

the

ANNA System

Dates

Performed

December

13,

1993

- 13-

AP5598,

Replace

Cell

11

on Battery Bl-2

DJ55,

Perform Furmanite Repair for HS-V-20

DL0301, Replace

Relay

DG-RLY-K16

CWA301; Repair Valve SW-V-2B

DJ5501,

Remove

and Replace

Main Steam Tunnel

Access

Hatch

December

1,

1993

December

16,

1993

December

16;

1993

December

16,

1993

January

6,

1994

a.

Furmanite

Re air of HS-V-20

On December

16,

1993; the inspector witnessed

the injection of

Furmapite,

a temporary sealant,

on HS-V-20.

HS-V-20 is: a safety-

related valve that is required to be closed

(

bl

f

or capa

e

o

being

o provi

e

a pressure

boundary for post-accident

operation

o t e main steam

leakage control

system.

The pressure

boundary

provided

by this valve is normally maintained

b

k 'h

in the

he closed position when the plant is greater

than

5%

ower.

HS-V-20 also

has

an emer

enc

o era

'

y

p

ting procedure

function, which is

an

o power.

on

e

-

esign basis,

to open

and allow for pressure

equalization

across

the main steam isolation valves (to permit their

being reopened

following an isolation).

This was the th'

tt

'

for this valve during this operating cycle.

at on-line leak sealin

is

eak appeared

to be associated

with the Furmanite adapter.

The

work on December

16,

1993,

was performed with li,ttle or no

However, there

was uncert

'

i,

e or no problem.

rtainty among licensee

management

regarding

e location of the leak

and the location of the Furmanite adapters.

Therefore,

the inspectors

performed

an in-depth followup of the

entire evolution associated

with HS-V-20.

Back round

, during

an inspection of the main steam tunnel,

the

On June

20

1993

d

bo

icensee

noted that there

was

a through-wall l

k

th

p cking chamber

on HS-V-20.

The licensee initiated

PER 293-

0909 following this discovery.

The

PER stated that the leak was in

the packing gland of the valve rather than the valve bonnet packin

chamber.

The individual that initiated the

PER did not.

e

observe

the location of the leak.

On June

20

1993 , the

POC reviewed

and approved

a proposal for a

temporary repair of the leak by injecting Furmanite sealant.

The

POC review was performed

by teleconference,

therefore the members

did not have the applicable repair procedures

or diagrams

available

or their review prior to approval of this repair.

Licensee

engineers

prepared

the work package

and

10 CFR 50.59 evaluation

based

on the belief that the leak was in the packing gland

and not

in several

the valve bonnet.

In addition,

the

10 CFR 50.59 eval t'

t d

II

leak."

It a

places that

The repair will seal

the associated

pa

k'peared

that licensee

personnel

had poorly communicated

pac ing

the planned

work to plant management.

First

Re air of Steam

Leak

The licensee initiated

HWR AP4260 to repair the leak in HS-V-20.

Step 4.A stated,

"Perform Furmanite repair to main steam valve

MS-V-20 packing gland per Furmanite procedure..."

The Furmanite

procedure

states

in Step

5. 1, "Drill and tap the valve bonnet wall,

adjacent to the packing chamber..."

When developing this

HWR and

obtaining approval

from the

POC, licensee

management

did not have

the Furmanite procedure

available for review.

This resulted in

licensee

management

being unaware that the furmanite adapters

were

being installed in the valve bonnet packing chamber.

Because

licensee

management

believed that the Furmanite adapters

were being installed in the valve packi'ng gland (this component,

as

identified in licensee

drawings,

is sometimes

called the packing

follower), an

ASHE Section

XI work plan was not developed for the

installation of the Furmanite adapters.

PPH 1.3.30,

"Repair,

Replacement,

and Alteration of ASHE Items," Paragraph

6.8,

"On-Line

Leak Sealing," states,

"Repair work plan is, required to drill and

tap hole size

one inch nominal

and smaller in valve bonnet packing

chamber."

The licensee's

installation of the Furmanite adapters

in

the valve bonnet

packing

chamber without the issuance

of an .ASME

Section

XI repair work plan was

a violation of PPH 1.3.30.

Because

the licensee

took appropriate

corrective actions for this licensee-

identified violation,

and because

the other criteria of Section

VII.B(2) of the

NRC Enforcement Policy were met, this violation is

not being cited

(NCV 50-397/93-50-05,

Closed).

The licensee first became

aware of the apparent

discrepancy

in the

location of the adapters

on September

7,

1993,

when

a maintenance

engineer

reviewed the completed

MWR package.

The engineer

noted

that the Supply System

had intended the adapters

to be put in the

valve packing gland,

but the Furmanite procedure

indicated that they

were installed in the valve bonnet.

Due to this discrepancy,

the

engineer

contacted

the Furmanite contractor

by telephone.

When

asked if he had installed the adapter

in the gland rather than the

bonnet,

the contractor stated that

he installed the Furmanite

adapter

in the gland.

The licensee

engineer

was satisfied with the

statement

of the contractor

and annotated

in the

comments

section of

the

MWR that the adapters

were installed

on the gland rather than

the bonnet wall

as stated

in the Furmanite procedure.

The licensee

did not enter the steam tunnel at that time to confirm the statement

of the contractor.

A PER was not initiated because

the licensee

believed that the issue

was resolved.

The. inspectors

concluded that

a

PER was necessary

at the time the

maintenance

engineer

completed his review because

either:

(1)

PPM

1.3.30 was=-violated because'n

ASHE Section

XI repair work plan was

not prepared;

or (2) the contractor personnel

violated the

HWR for

failing to install the adapters

per the work instructions.

The

failure to initiate

a

PER for the discrepancies

noted in closeout of,

the= HWR AP4260 is

a violation of PPM 1.3. 12,

"Problem Evaluation

Requests,"

and

10 CFR 50, Appendix B, Criterion

V (Violation

50-397/93-50-06).

-15-

Steam

Leak of November

10

1993

On November

10,

1993, the licensee

entered

the steam tunnel

due to

a

,high temperature

annunciator that

had

been received in the control

room on November 5,

1993.

One of the Furmanite

adapters

on MS-V-20

appeared

to be leaking.

The licensee initiated an

HWR to re-inject

the leak area to reseal

the steam leak.

In addition, the licensee

determined that the information obtained

on September

7,

1993,

regarding the location of the Furmanite adapters

was incorrect.

The

licensee

noted that the Furmanite adapters

were installed in the

valve bonnet packing

chamber versus

the previously documented

valve

packing gland.

The licensee

continued to evaluate this apparent

discrepancy,

and initiated

PER 293-1412

on December

16,

1993, to

document that

an

ASHE Section

XI work plan was not completed prior

to the leak repair

as required

by PPM,1.3.30.

The licensee's

failure to prepare

a work plan was identified earlier

as

an

NCV.

Additional Steam Tunnel Entr

On January

6,

1993, the inspector,

along with licensee

personnel,

entered

the main steam tunnel to inspect

HS-V-20 and look for

additional

steam leaks.

Licensee

personnel

pointed out to the

inspector the area that

had

been leaking.

The inspector

noted that

a threaded

plug was seal

welded into the side of the valve bonnet

packing chamber.

This was the location of the leak.

The licensee

had recently backseated

the valve to inhibit further leakage

through

the valve,

because

the Furmanite representative

stated that the

adapters

would soon leak following the repair performed

on

December

16,

1993.

Conclusions

The inspectors

concluded that several

weaknesses

were evident

concerning

the repair of HS-V-20.

Maintenance

personnel

did not

appear

to fully understand

the construction of the valve.

Several

conclusions

can

be reached

due to the m'isunderstanding

by Supply

System personnel

regarding the location of the Furmanite adapters:

the original

PER was incorrect;

most of the

POC reviews did not have

the correct information to make

a proper judgement;

Supply System

management

did not initially understand

the location of the steam

leak;

and Supply System

management

did not fully understand

the

location of the Furmanite adapters.

These

weaknesses

indicated

a

need for more strengthening

of vertical communications

at WNP-2.

The inspectors

also noted that the documentation

in the

HWR was weak

because

the initial HWR described

two different leak locations.

The

followup investigation during closeout

review of the initial MWR was

also weak because

the licensee's

conclusions

were based

upon

telephone

discussion

rather than direct observation.

Finally, the

=initial

POC review appeared

weak because

the repair of the steam

leak was approved

over the telephone with the individuals not having

the work instructions or valve diagrams

in hand.

-16-

The inspectors

discussed

these

conclusions with the Plant Manager.

The Plant Manager

acknowledged

the inspectors'omments

and stated

that the Supply System

was working diligently to improve in each of

the applicable

areas

of performance.

b.

Work Coordination for DG-RLY-K16

On December

16,

1993,

the licensee

took DG-2 out of service for

replacement

of a relay.

The licensee initially planned to replace

this relay and perform maintenance

work on valve SW-V-2B concur-

rently.

The isolation for work on SW-V-2B caused

the service water

system to be inoperable,

which also rendered

DG-2 inoperable. while-

this work in progress.

However,

due to poor work coordination,

the

repair of SW-V-2B and replacement

of the

DG relay were performed in

series,

unnecessarily

extending the outage time for DG-2.

The inspector

noted that

DG-2 was inoperable for a total time of 10

hours

on December

16,

1993.

Had the two jobs

been coordinated

and

worked concurrently,

the outage

time of DG-2 would have

been

7

hours.

The inspector

noted that the

TSAS allows

DG-2 to be out of

service for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> before

a shutdown

must

be initiated,

and that

the licensee still had considerable

margin from the

TS limit.

However, the issue

indicated

a weakness

in work planning which had

unnecessari.ly

extended

the outage time for a safety

system

component.

The inspector discussed this issue with the Plant

Manager,

who acknowledged

the inspector's

comments.

One violation and

one non-cited violation were identified.

8.

Licensee

Event

Re ort

LER

Followu

90712

92700

The inspector

reviewed the following LER associated

with an operating

event.=

LER NUMBER

DESCRIPTION

93-30

Inadequate

Separation

between

Cable Trays

Based

on the information provided in the report it was concluded that

reporting requirements

had

been met, root causes

had

been identified,

and

corrective actions

were appropriate.

However, this

LER described

an

event in which li'censee

personnel

performing walkdowns of cable trays

identified

13 non-compli ances with General

Design Criterion 17.

As of

the date of the

LER, the walkdowns were about

50X complete.

The licensee

stated that other non-compliances

may be found upon completion of the

walkdowns.

LER 93-30 also states that one of the root causes for the discrepancies

was that personnel

who had performed previous cable tray walkdowns were

not trained,

and were not thoroughly familiar with the train separation

requirements.

The safety significance section of the

LER states

that

none of the

individual cable tray deficiencies

posed

a threat to reactor safety.

e

- 17-

However, the

LER states

that the large

number of deficiencie's

may

be

safety significant, or may indicate

a programmatic

problem with train

separation.

Because of the potential

safety significance or programmatic

nature of this event,

the inspector will perform

a detailed onsite

followup and evaluation of this

LER (LER 50-397/93-30,

Open).

No violations or deviations

were identified.

The inspectors

met with licensee

management

representatives

periodically

during the report period to discuss

inspection status,

and

an exit

meeting

was conducted with the indicated personnel

(refer to paragraph

1)

on January

31,

1994.

The scope of the inspection

and the

inspectors'indings,

as noted in this report,

were discussed

with and acknowledged

by the licensee

representatives.

The licensee

did not identify as proprietary

any of the information

reviewed

by or discussed

with the inspectors

during the inspection.