ML17262A877
| ML17262A877 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 01/18/1992 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17262A876 | List: |
| References | |
| 50-244-90-99-01, 50-244-90-99-1, NUDOCS 9206090262 | |
| Download: ML17262A877 (48) | |
See also: IR 05000244/1990099
Text
ENCLOSUIUK1
I
FINALSALP REPORT
U. S. NUCLEAR REGULATORY COIVllVHSSION
REGION I
SYSTEMATIC ASSESSMENT OF LICENSEE
PERFORMANCE
FINALSALP REPORT 50-244/90-99
ROCHESTER GAS AND ELECTRIC CORPORATION
R. E. GIJI'WA NUCLEAR POWER PLANT
r
ASSESSMENT. PERIOD: OCTOBER 1, 1990-
JANUARY 1S, 1992
9206090262
920604,
ADOCK 05000244
8
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TABLEOF COXH~PlTS
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INTRODUCTION,...'
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SUMMARYOF RESULTS .'...........
II.A
Overview
II.B
Facility Performance Analysis Summary
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III.
PERFORMANCE ANALYSIS..........
III.A Plant Operations
III.B
Radiological Controls
III.C
Maintenance/Surveillance
III.D Emergency Preparedness
III~E
Security
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Engineering/Technical
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III.G
Safety. Assessment/Quality
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IV.
SALP EVALUATIONCRITERIA........... ~.................
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I.
INTRODUCTION
The Systematic Assessment of Licensee Performance-(SALP) is an.integ'rated NRC staff
effort to collect the available, observations and data;on.a periodic basis md.to evaluate
" - '-.~ <"'-'licensee:performance+ased~upon..thirinformation..-SALP
is"supplemental&wormal
., regulatory processes, used,to.ensure
compliance with:NRC rules and regulations.
SALP is
intended to be sufficiently diagnostic to provide a rational basis for allocating NRC resources
and to provide meaningful guidance to the licensee management to promote quality and safety
of plant operation,
This report is the NRC's assessment of the licensee's safety performance at the R. E. Ginna
.Nuclear Power Plant for the period October 1, 1990 through January
18, 1992.
A NRC SALP Board, composed of the staff members listed below, met on March 5, 1992 to
review the collection of performance observations
and data to assess
the licensee performance
in accordance with Chapter NRC-0516, "Systematic Assessment of Licensee Performance".
The guidance and evaluation criteria are summarized in Section IV of this report.
The
Board"s.findings and,recommendations
were forwarded to the NRC Regional Administrator
for approval and issuance.
Chairman:
C. Hehl, Director, Division of Reactor Projects (DRP)
Members:
W. Lanning, Deputy Director, Division of Reactor Safety (DRS)
R. Cooper, Deputy Director, Division of Radiation Safety and Safeguards
(DRSS)
J. Linville, Chief, Projects Branch No. 3, DRP
T. Moslak, Senior Resident Inspector
K Butler, Director, Project Directorate I-3 (PD I-3), Office of Nuclear Reactor Regulation
(NRR)
A. Johnson, Project Manager, PD I-3, NRR
/;
I
II.
SUMMARYOF RESULTS
II.A
Overview
..RG&E management
continued to be substantially involved in monitoring'routine activities,
supporting the development of several program initiatives, and promoting increased
engineering support to site activities.
These efforts have been successful in maintaining
performance at the levels noted in the previous SALP with improved performance in certain
areas.
. The plant continued to be operated in a safety conscious manner with operators appropriately
responding to plant challenges and aggressive management
involvemen't in the resolution of
operational events. 'owever, procedure inadequacies
and deficiencies in assessing
the impact
of certain maintenance
tasks on plant operations indicate the need for continued attention-to-
detail in the control of plant activities.
While improvements have been made in this area,
management involvement, is,needed to ensure plans for long term improvement are effective.
The licensee has strengthened
the overall performance of the facility. Performance in the
areas of Maintenance, Security and Emergency Preparedness
was superior.
Manage'ment's
commitment to sustained high quality performance was evident through support given to
program initiatives and hardware upgrades.
Notwithstanding, some concerns worthy of
additional management
attention were identified in emergency response training and staffing
depth raising questions regarding the support in that area.
Overall, a.strong interface between operations and corporate engineering has expedited the
resolution of operational problems and the timely implementation of comprehensive corrective
actions.
Although progress was made in the Engineering and Technical Support area,
engineering assurance
deficiencies identified in addressing Service Water System design issues
indicate continued management
attention is warranted.
Sound safety controls were established for the refueling outage to ensure availability of
residual heat removal and electrical distribution systems.
Management took a conservative
approach to emergent outage issues to minimize personnel dose and contaminations.
Radiological control and quality assurance
programs. were conscientiously implemented w'ith
improvements being made in the areas of monitoring and self assessment.
However,
deficiencies were noted in REMP QA/QC programs and laboratory technician training.
II.B
Facility Performance Analysis Summary
Fun 'n
Ar
Rating Trend*
- "Rating,"Trend**
,~Thi
P
1.
Plant Operations
2.
Radiological Controls
3.
Maintenance/Surveillance
4.
5.
Security
6.
'ngineering/Technical
Support
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2 Improving
1, Declining
2 Improving
'
7.'afety Assessment/Quality
Verification
2
- June 1, 1989 to September 30, 1990
- October 1, 1990 to January
18, 1992
III.
PERFORMANCE ANALYSIS
III.A'lant Operations
III.A.1
Analysis
Plant operations was rated Category 2 in the previous assessment
period.
Past strengths
identified in this area included experienced professional operators, excellent emergency
operating procedures,
and strong statio'n management involvement in daily.plant activities.-
Weaknesses
in procedure adherence
and independent verification of system alignments were
identified early in the assessment
period; however, improvements in these areas were noted
later in the period.
During this period, the licensee continued to demonstrate a strong commitment to safe and
high quality operations;
Senior corporate and site management
were actively involved in
plant activities and,promptly;responded,to
operational events.
This was demonstrated
by the
detailed investigation conducted by senior corporate management into the causes for the
temporary disabling of, Engineered Safeguards instrumentation.
Management developed
comprehensive corrective actions in response to this event.
Actions included a quarantine of
suspect procedures followed by a detailed review for any similar procedural inadequacies,
and
modification of the procedure change process to require operational review by licensed
personnel.
Briefings were also conducted for each operating'shift to emphasize
management's
expectations for operators to maintain a questioning attitude and stressing the
importance of attention-to-detail and thorough review before authorizing work.
Operator professionalism,, conduct of control room operations,
and response to off-normal
plant conditions were excellent.
Immediate operator action following trips was appropriate.
Plant challenges that could have resulted in a reactor trip were met on several occasions by
prompt and decisive operator response.
Operators demonstrated
a sound understanding of integrated plant operations by quickly
identifying deficient conditions, such as feedwater flow disturbances
caused by electrical
interference from the diesel fire pump start circuitry. However, in one event concerning the
disabling of Engineered Safeguards
instrumentation, the operators performance in identifying
deficient conditions was mixed,
Although the shift supervisor demonstrated
a questioning
" attitude and understanding of!the plant, the control room foreman who was implementing the.
procedure lacked sufficient guidance and understanding to assess
the impact of the.,use oi.the
procedure on plant operations.
Procedure adherence
and independent verification of system alignments significantly improved
during the period.
New administrative procedures were developed and site-wide training was
effective in these areas.
Operators consistently followed procedures.
n
Plant housekeeping
continued to be excellent throughout this yssessment
period.
During the
.. outage, supervisors consistently. ensured that loose material was,expeditiously removed from.
-'.job sites"Kfter work'completion"and'that<the.formalized
housekeepingq)rogram;was-:
implemented.
In addition to personnel conscientiously keeping the shop, and plant areas clean
and orderly, management'instituted
a vigorous painting program to brighten various plant
areas.
These efforts resulted in significant improvements in plant appearance.
During the outage, site control of plant activities was excellent.
While in reduced coolant
inventory conditions, management briefed personnel on potential challenges to plant, safety.-
and deferred several activities to ensure the reactor coolant system'evel would not be,
perturbed and safety equipment availability would not be impacted.
The operator training program was satisfactory.
During the initial operator licensing
examination, all five senior reactor operator candidates
and three reactor operator candidates
passed the exams.
During the requalification examination, two reactor operators and three of
five:senior.reactor:operators.passed
the exams.
There were no crew failures,
The
Requalification Program was not evaluated due to the limited number of individuals fess than
12) examined.
Examination materials developed by the Training Department were well
developed and maintained.
The various plant departments
and Training Department worked closely together.
Operators
were promptly trained on plant modifications such as the Advanced Digital Feedwater Control
System (ADFCS) and the zebra mussel control measures.
Training materials were promptly
updated
as a result of strong communications between plant departments
and the training
organization.
The curriculum committee was effective in assuring that personnel were
receiving pertinent subject matter with.the appropriate level of detail.
Involvement by
the,'raining
organization in daily plant planning meetings and the use of a computerized
networking system to respond to inquiries and suggestions affecting training also enhanced
the
timeliness'of improving training material.
Inappropriate operator action on two occasions led to degraded safety system conditions.
The
cause of the first, involving the deenergization of vital bus 18 while performing a routine
monthly emergency diesel generator load test, was not readily apparent.
Management
directed corporate engineering to extensively evaluate the event.
The probable cause was
attributed to an operator prematurely closing the generator output breaker before
'ynchronization.
Issues developed in this evaluation were thoroughly reviewed and
adequately resolved by the Operations and Training Departments.
The second event, which
occurred during the outage, involved temporarily removing the Residual Heat Removal
System from service to stop a Component Cooling Water System valve packing leak which
developed during valve maintenance.
In response,
management initiated a human
performance evaluation to identify the root cause and establish corrective actions.
The cause
was found to be unclear communications between the operations and maintenance
departments that resulted in the valve being electrically backseated.instead
of manually
-,.backseated prior to.maintenance.
Both, events were of short duration.
The licensee
,:.,=-responded
appropriately.and,quickly,.restored
plant equipment to mrvice:~~
lay'm~m~
Overall, the plant was operated safely as indicated by appropriate operator response to plant
challenges,
a reduction in the number of reactor trips, and aggressive management
involvement in the resolution of operationalproblems.
However, procedure;.inadequacies
and
deficiencies in assessing
the impact of certain maintenance
tasks on plant operations indicate
- the need'for continued attention-to-detail in the control of plant activities.
Excellent
housekeeping
was the direct result of conscientious worker practice and management
support.
A strong interface betw'een the Operations Department and corporate engineering expedited
the root cause analysis process and the implementation of corrective actions.
Operator
training reflects close interdepartmental coordination, ensuring that personnel are provided
effective training on plant modifications.
III.A.2
Performance Rating:
Category 2
III.B Radiological Controls
III.B,I
Analysis
The Radiological Controls area was rated Category 2 in the last assessment.
Strengths
included responses,to
audit and.inspechon
findings and AI.ARAreviews of routine and
modification work.
Weaknesses
were noted in staffing, supervisory oversight of field
activities, quality assurance in the Radiological Environmental Monitoring Program (REMP),
training, posting and updating surveys of the plant, and communications between Radiation
Protection (RP) personnel.
The SALP board commented that the fillingof Radiological
Controls vacancies
and assuring the effectiveness of training programs for health physics and
environmental laboratory technicians were areas for improvement.
A well defined and staffed RP organization was in place at the end of the assessment
period.
, Complete staffing of the RP organization resulted in the correction of-several weaknesses
including impi:oved posting and updating ofsurveys, and improved communications within
" -.
the Radiation Protection Organization.
During the I'ast assessment
period a decline in the
quality of oversight of field work was caused by the loss of RP management personnel and a
shortage of permanent RP technicians.
To address this weakness,
Rochester Gas and Electric
(RG&E) augmented
the RP Organization with the addition of a Health Physicist position and
eight RP Technician positions.
During this assessment
period the licensee hired qualified
personnel to fillthese newly created positions.
Several programmatic improvements resulted
from the increased staffing levels, including the appointment of Lead Technicians and a
Quality Improvement Specialist.
. The RP Technician training program showed improvement-since the.-last-assessment
period-
- and is now considered to be a strength:
An excellent training;,program. on the radiological,
hazar'ds of'specific"systetnswas"initiated'for.new
RP Technicians";-;~additional RG&E.:..
= initiative involved incorporating the systems training lesson plans into the continuing training
for all permanent RP Technicians.
The training program for co'ntractor RP technicians is, also
considered to be strong.
Enhanced RP training was given to decontamination technicians in an effort to improve work
practices.
Preliminary review of the program'indicated that. the decontamination technician
training was effective and is considered a good program initiative.
RG&E's ALARAprogram continued to effectively reduce annual personnel exposures.
Notwithstanding significant high exposure challenges, RG&E continued to maintain
cumulative annual exposures ALARA. A strength in this area continued to be the effective
use of mock-ups prior to high exposure jobs.
RG&E restructured the ALARAorganization
with dedicated "staffing. This resulted in an effective organizational structure for
implementation of the ALARAprogram.
The ALARAgroup was actively involved in testing
new equipment, such as the insulation removal and transfer system used in radiation areas.
The ALARAarea is considered to be another program strength.
RG&E's program for assurance of quality is considered to be generally sound with some
areas in need of improvement.
An effective program'was in place for tracking and assuring
appropriate followup of RP program weaknesses.
A weakness was noted which indicated that
improvement was needed in the area of management review of procedural changes.
For
example, a surveillance requirement specified in the technical specifications was omitted from
a ventilation testing procedure during a procedure revision.
Subsequent
management
review
of the procedure revision did not identify the omission.
Similar examples were noted in
controls of revisions to plant operations procedures.
Another area of weakness involved the
lack of sufficient technical QA review in environmental laboratory audits which is discussed
below.
The resolution of technical issues from a safety standpoint by the station staff is considered to
be generally effective.
Management attention to reducing the number of personnel
contaminations and minimizing dose was excellent.
RG&E's evaluation and corrective
actions for an operational event involving a leaking secondary source was also considered
to
very good. 'However, RG&E's identification and resolution-of some technical issues were not
performed in a timely manner.
These issues included evaluating the adequacy of the
certification of personnel dosimeters
used during-power entries, source checking of neutron
survey meters and area 'radiation monitors,
and in-place testing of HEPA filters.
RG&E's program for processing and transporting radioactive material is considered very
good.
The licensee implemented several initiatives in the radwaste program.
The initiatives
included upgrading the radwaste handling and transportation procedures,
having a consultant
evaluate the program and make recommendations for improvements,
and completing an
" -extensive effort to remove all ex'cessive radioactive material. from the~site.
RG&E had an
.'effective program'or training individuals 'involved in.the radwaste'and.transportation
"program..'Superv'isory
"oversight of"'this"area was also considered very;good;=.
During the previous assessment
period weaknesses
were identified in.theZKMP laboratory
QC program and REMP laboratory technician training.
These weaknesses
continued.
As of
the last inspection, the REMP laboratory technician was not qualified to independently run
the REMP laboratory and received little supervisory oversight in this position.
A new
individual was appointed to;this. position. later. in the assessment
period... QA audits. of-,the
REMP focused on administrative rather than technical aspects of the program and, therefore,
did not probe for technical weaknesses.
Technical weaknesses
were identified in REMP
analytical procedures by the NRC but not by the licensee's QA Department.
In contrast, however, the licensee's radioactive liquid and gaseous effluent control program
was effectively..implemented.
Well written.procedures combined with an effectively trained
"staffresulted'.:in"good procedure adherence,.and:.release
permits met the TS requirements for
sampling and analysis.
The licensee's upgrading of the radiation monitoring system was
noteworthy and excellent.
Staffing of,the RP organization improved during the assessment
period and is now considered
to be appropriate.
The training program showed improvement and is considered to be strong
with the exception of training in the environmental monitoring area.
RG&E's ALARA
program continued to effectively reduce annual personnel exposures.
RG&E's program for
assurance of quality is considered to.be generally sound with continued weakness in the
The resolution of technical issues from a safety standpoint
.by the station staff is considered to be generally effective.
RG&E's program for processing
and transporting radioactive material is considered very good.
The licensee's radioactive
liquid and gaseous effluent program was well implemented.
III.B.2
Performance Rating:
Category 2
III.C Maintenance/Surveillance
m.C. 1
Analysis
During the previous.SALP, Maintenance/Surveillance
was rated Category 2, Improving. The
assessment
determined that maintenance
and surveillance activities-were well planned, and
capably performed.
Corporate and site management actively supported a strong maintenance
program.
Maintenance procedure upgrading and development of a reliability centered
maintenance approach were positive initiatives.
Problems were noted in the area of
procedural adherence;
however, progress was noted later in the SALP period.
Min nn
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[ '.Overall; tnaintenance activities.were effective in supporting. the-safemd-reliable
operation of
the plant.
This effectiveness was evident by a decrease in forced shutdowns and reduced
challenges to plant safety systems.
Corporate and site management'actively
monitored routine
maintenance activities and strongly supported programmatic initiatives to assure high
reliability of plant systems.
Development of a reliability centered maintenance program has
steadily progressed
to improve preventive maintenance effectiveness.
State-of-the-art
diagnostic techniques,
such as'infrared thermography, were routinely used. as. predictive,
maintenance tools.
The planning of daily and weekly preventivelcorrective maintenance
activities continues to be thorough.
During the refueling outage, management effectively
controlled contracted activities.
A highly trained, stable work force continued to be a major strength of the maintenance
, organization..Past
training program weaknesses
were adequately addressed.
The licensee
-" 'maintained.a~rigorous
maintenance training program that incorporated a technician annual
refresher program, consolidated health'physics
team training; and recent plant modifications.
Training was enhanced
through the extensive use of mock-ups, including cut-away electrical.
breakers, full-size steam generator lower shells, motor operated valves, and assorted
valve/piping manifolds.
The licensee continued to shift to a more hands-on approach to
maintenance training from the traditional classroom descriptions of task performance.
This
training, combined with low'technician*turnover and adequate staffing resulted in an
~
effective maintenance work force.
Priority maintenance work load was well controlled and remained low. The overall backlog
increased~slightly
as a result. of scheduling more preventive maintenance
tasks to support the.~<<
reliability centered maintenance program.
Appropriate management
attention was given to
. the effort through increased staffing.
The rework rate remained low.
The licensee made good progress in the upgrade of maintenance procedures.
Recently issued
upgraded maintenance procedures were comprehensive
and consolidated within the body of
the procedure acceptance criteria and vendor technical manual data and illustrations.
Tasks were consistently well planned, controlled, and coordinated through a formalized work
control system.
Work packages were well prepared by the maintenance planner, with
relevant acceptance criteria identified in the governing maintenance procedure, supporting
~
work instructions, or associated quality control procedures.
Pre-job and post-job briefings by
maintenance
foremen were well conducted.
Post maintenance
testing was systematically
performed.
However, documentation within the work package of the as-found and as-left
equipment condition was generally brief, providing limited feedback information for the
maintenance analyst during subsequent review.
10
.,Procedure revisions and subsequent
training proved to be effective in;improving procedure.:.
adherence
and independent verification-of system configuration.>>= Theimplementation,of an
.'"';"inadequate'corrective"maintenanceyrocedure
that led.to the temporary. disabling of
.
Engineering Safeguards instrumentation was an isolated event,.resulting from an oversight in
the pre-PORC procedural review process.
Although this event was important, it did not
reflect a programmatic breakdown.
An extensive quarantine of suspect procedures and
subsequent
review identified no similar inadequacies.
The maintenance organization demonstrated
an excellent capability to assess
and.resolve
several emergent plant equipment problems.
In addition to completing repairs to aging
service water system components,
the licensee demonstrated
the ability to effectively analyze
and correct emergent problems while maintaining a sound safety perspective by resolving rod
control system malfunctions and promptly identifying undervoltage monitoring system circuit
card design deficiencies.
= 'The-overall: material. condition "of equipment and-systems
was well maintained.
Age-related
wear contributed to a degraded material co'ndition for certain components in the service water
system.
The licenseemas
appropriately addressing
these plant aging concerns.
A Service
Water System Reliability Optimization Program was established that willsystematically
replace aging containment air coolers, fan motor coolers, and assorted service water system
valves/piping during future outages.
~rveill nce
The overall surveillance program continued to be effective in verifying the operability of
.safety related equipment-and satisfying Technical Specifications.
Surveillances were
performed on schedule,
were adequately documented,
and testing deficiencies were properly
-dispositioned.
Test, results were trended for each component tested to detect degradation.
Surveillance procedures were clearly written containing precautions,
acceptance criteria, and
specific responsibilities of test personnel.
Licensee, control of surveillance testing was very
good.
Procedures
were adhered to and expeditiously performed to minimize system
unavailability. Following surveillance testing, independent verification of system realignment
ensured proper equipment restoration.
$gmmary
In summary, maintenance activities were effective in supporting the safe and reliable
operation of the plant.
Steady progress was made in the maintenance procedure upgrade
program and reliability centered maintenance program, with new procedures
and diagnostic
methods being implemented.
Management continued to strongly support and closely monitor
maintenance activities.
Plant material condition was well maintained and equipment aging
concerns were adequately being addressed.
Surveillance testing was well planned and
conscientiously carried out.
III.C.2
Performance Rating:
Category
1
11
..III.D Emergency Preparedness
III.D.1
Analysis
During the previous SALP,: Emergency Preparedness
(EP) -was,rated Category 1. - There was
noteworthy management involvement, good training, excellent exercise performance,
and a
good relationship with the State and surrounding counties.
In the November 1990 partial-participation,.exercise,
degrading plant conditions were. readily
recognized by licensee personnel.
Positive interactions were noted among members of the
Emergency Response
Organization (ERO).
The NRC identified a weakness in timeliness of
Protective Action Recommendations
(PARs), but overall performance showed the ability to
protect public health and safety.
During the September
1991 full-participation exercise,
degrading plant conditions were again readily recognized.
Use of the plant simulator during
this exercise was a positive and productive initiative to improve training realism.
Licensee,
";; --.accident assessment
durin~the exercise. demonstrated sound technical knowledge of the plant.
Emergency classifications were timely and conservative.
The licensee corrected the previous
exercise weakness concerning timeliness of PAR issuance.
For both exercises,
the licensee's
post-exercise critiques were thorough.
Overall, emergency exercise performance was
proficient.
For the November 1990 exercise, the as-submitted 'scenario lacked detail in areas such as "
anticipated actions of ERO personnel, trending analysis of key reactor parameters,
and off-
site monitoring data.
Corrections were made before the exercise.
For the September
1991
exercise, the submitted scenario exhibited improved quality of presentation
and technical
content.
- During this period, two plant events required emergency plan activation.
Each was quickly
recognized and properly classified as, an Unusual. Event.
In response,
site management
demonstrated
a conservative,
safety-conscious
approach.
Effective event response
was also
demonstrated
when a severe ice storm swept through Wayne and Monroe Counties in, March
1991.
Because of extensive damage to transmission lines and power distribution equipment,
the counties activated their Emergency Operation Centers (EOCs).
Licensee personnel
manned EOC stations to coordinate power restoration.
The licensee quickly determined that
the siren system was to be considered unreliable because of storm damage.
To compensate,
local fire department and law,'enforcement, personnel were briefed by-EP personnel on Route=
Alert measures
to be implemented in a nuclear emergency.
This licensee response
showed
proficiency and competence in responding to a non-nuclear off-site event.
Emergency response facilities were well maintained.
Administrative and emergency response
procedures were generally. well written. The licensee's
10 CFR 50.54(t) audit was
appropriate in scope and content.
Audit results were provided to state and county officials.
'II
12
.
Corrective. actions were generally prompt and effective, but findings were maintained within.
'.,; two separate. tracking systems:
During.the transition to a,single;trackingaystem,.some.
minor
'..'. '.items were.not carried. over into'the~new system..
NRC review of the Technical'Support Center (TSC) ventilation system:noted'an
inability to
'ell
whether the system had shifted to the accident (recirculation) mode.
The licensee
initiated a review to establish the best method of doing so.
'he NRC found that on-shift personnel lacked the-capability of performing. dose assessment "
for a postulated steam generator tube rupture.
Other licensee personnel had that capability,
but they were not always promptly available, and the licensee's ability to properly classify
some events was impacted.
The cause appeared to involve procedure and training
inadequacies.-
The licensee took timely action to implement an appropriate interim procedure
and additional training.
'he'EP:program-,mn
site md'off-site,-was administered by the. Director, Corporate Radiation
Protection.
Two full-time people with technical backgrounds were assigned to maintain the
emergency plan and its implementing procedures,
conduct drills and exercises,
ensure
readiness of emergency response facilities and equipment, and interface with off-site support
groups.
Management participation was evident by maintenance of ERO qualifications and
participation in drills and exercises.
NRC contact with one county identified satisfaction with
the licensee interface.
However, the'following weaknesses
were identified:
the emergency"
plan did not fully reflect the current program; there were several months in which the
equipment inspection and the pager test logs were not documented;
some discrepancy
corrective actions were not reviewed; and drill/exercise records lacked formality and
consistency.
- Overall, NRC review found good program performance, but minor
weaknesses.'n
administration and management.
EP training, except dose and core damage assessment,
was the responsibility of the Training
Department.
However, rather than provide training'in EP throughout the year, and thus
enable continued familiarity with the emergency plan and its implementing procedures,-
essentially all EP training was completed within a two-month window prior to the September
1991 exercise.
After considering the potential contribution of more frequent and regular EP
training, Rochester
Gas and Electric Company initiated action to revise the training cycle.
All ERO positions were filled~at least three deep, but some key managers were assigned more
than one ERO job.
Long-term ERO staffing was therefore potentially strained.
The licensee
stated the intention of qualifying more individuals in ERO positions.
Course requirements
necessary
to satisfy each ERO position were subject to management
review and approval.
Lesson plans for ERO training were excellent.
Reactor operators
received classroom and simulator training in accident classification, off-site notification and
PAR development.
A noteworthy initiative was the use of mock-ups for drills and exercises.
13
- The.training program was well-defined,and,.except for on-shift. dose projections, provided an.
'."-excellent:contribution to emergency preparedness:effectiveness.as,
demonstrated
by the overall
'.."-" .'rofici'ent'.performance'during
"exercises'. actual events,.and.walk-throughs.
In summary, the'licensee effectively responded
to actual events and to exercise scenarios:
Procedural and training weaknesses
were found during follow-up of on-shift inability to assess
potential dose consequences,
but-procedures
were otherwise very good and training was
otherwise very effective.
Considerable licensee effort:was expended on the working
relationship with'the State and the county authorities, and effective results, were indicated:
NRC.review identified several weaknesses
in program administration and management,
but
the licensee's ability to protect public health and safety was maintained.
III.D.2
Performance Rating:
Category
1, Declining
Board Comments;
- The board was concerned that program support had
.idegraded'resulting
in'the identified weaknesses.
III.E Security
Analysis
During the previous SALP period the licensee's performance was rated as Category 2,
Improving. This was based on the licensee's implementation of an effective and sound
security program and taking steps to upgrade and enhance the program.
However,
weaknesses
in auditing, deficiency correction, and lesson plans detracted from the
effectiveness of the program.
During<this SALP period, the licensee exhibited a strong commitment to improve the,
program further.
This was most notable in the significant ongoing upgrades
and
enhancements of systems and equipment, in particular, commencing replacement of the
perimeter intrusion detection system.
The licensee also completed modifications of the
security access control facility that included a third new explosives detector, new hand-held
metal detectors,
and a redesigned
search area.
Other upgrades included the perimeter
barrier'nd
the assessment
system, and the purchase of a new security computer system, which was
.
'being assembled
at the end ofrthis assessment
period.
In addition, plant and corporate
security management personnel remained active in organizations. involved in nuclear plant
security matters.
These significant commitments of capital improvements and involvement
are indicative of management's
interest in and support of an effective'ecurity program.
During the period, the security force was responsive to potential challenges.
For example,
following a lightning strike that disabled a number of high mast lights, corrective measures
were rapidly initiated to ensure that site security could not be compromised.
The licensee
also implemented appropriate increased security measures during the Persian Gulf conflict.
14
- Licensee oversight of the contract security force continued, to.be..effective.. Members of the
"'-":security: force exhibited.-a professional: demeanor,.high,morale;iand~were
knowledgeable of .,,-
- - *"'<their duties".'Staffing'of'thersecurity~force
was consistent with~program-:needs,
as indicated'by
maintaining an effective security program with the minimal use of overtime.
The turnover
rate was significantly below national average.
The licensee's training and requalifiication program was well developed and effectively
administered,
as evidenced. by a minimum.of personnel errors.. Security training personnel
completed several instructor courses and provided feedback into the Security Officer Training
Program for the enhancement of all officers. Additionally, the weaknesses
in the lesson plans
identified during the last SALP period were effectively corrected.
The lessons learned during
day-to-day program implementation were being incorporated into the formal lesson plans.
During the annual emergency preparedness
exercise several scenarios that challenged the
... security-force were incorporated, including responding to an uncontrolled discharge of a
" ..'-;".'~ "flammablematerial.and~the".seizure
of a nonvital area by.a disgruntled employee.
The drill
scenarios were realistic, well developed and were conducted, in a professional manner.
The
post-drill critiques also provided meaningful training for the security force.
The exemplary
performance of the security force during the drill reflected an effective training and
qualification program.
The licensee improved its annual security program audit by engaging'independent
security
consultants to evaluate overall program performance.
The audit was comprehensive in scope
and depth; management's
corrective actions in response
to the audit findings were prompt and
effective.
The licensee also developed and implemented a formal surveillance program
during this period to monitor the day-to-day operation of the security program and, force.
In.
addition, improvements were made in the tracking of equipment deficiencies to effect more
timely repairs.
The licensee's Fitness-for-Duty (FFD) program was reviewed during the assessment
period.
Although some minor problems were encountered
during the initial implementation of the
program, these were rectified promptly and the licensee was found to be responsive to the
spirit and intent of the rule.
The licensee's security event reporting system:and procedures were found to be well
understood and consistent with the NRC'regulations.
No event occurred'that required a one-
hour report, indicating a strong and effective program.
Loggable events were appropriately
tracked and corrective actions were timely and effective.
Under the provisions of 10 CFR 50.54(p), the licensee submitted one revision to the Training
and Qualification Plan; and one complete revision and two minor revisions to the Physical
Security Plan.
The revisions were. technically sound and demonstrated
a thorough knowledge
and understanding of NRC requirements
and security objectives.
15
.$gmmarr.
- "," '
-" "The licensee con6nued" to implement<improvements in an'effecfive~dqerformance-oriented.-
security program.
Management attention to and support of the program were clearly evident
. by the significant commitment of capital improvements for upgrades and enhancements
in
systems, equipment and the training of personnel.
The efforts expended to improve an
effective program during this period are commendable and demonstrated
the licensee's
commitment to a high quality security program.
m.E.2
Performance Rating:
Category
1
III.F
Engineering/Technical Support
m.F. 1
Analysis
In the last SALP, performance was rated Category 2 in this functional area.
Improvements
were noted in the corporate and site engineering interface on major modifications, timeliness
of work packages,
decreased
major modification backlog, and safety analyses content.
Competency of the engineering staff and the commitment to a large configuration
management program were also noted.
The last SALP also noted weaknesses
in overall
'ngineering assurance
practices.
During the current assessment
period, site and corporate engineering support was evident for
day-to-day plant operation.
Participation of corporate engineers at plant daily meetings and
the effective and widespread
use of a computerized network enabled corporate engineering to-
quickly respond to safety concerns and support the site in identifying root causes and
resolving safety-related component failures., Examples of good engineering support included
the evaluation and technical justification for the. acceptability of an elongated steam generator
manway stud,
resolving the cause of a vital bus deenergization during a surveillance test, and
the well prepared root cause analyses of the recent "A" service water pump motor failure.
Other good examples were the comprehensive root cause analysis of a failed pipe hanger
supporting moisture separator reheater drain lines, the identification of a circuit card design
deficiency in the Anticipated Transient Without Scram (ATWS) Mitigating System Actuation
Circuit, and resolution of the cause of electrical. interference in the feedwater control system.
Reviews of recently completed modification packages
showed they were well planned and
exhibited good safety perspectives
and responsiveness
to site needs.
The advanced digital
feedwater control system effort displayed excellent engineering planning, effective
communications throughout the organization, strong engineering and continuous management
oversight.
In performing extensive instrument upgrading for the feedwater system,
engineering initiative was evident in the development of predesigned
tubing and instrument
supports and the development of the generic spacing of varied tubing sizes.
Other significant
modifications that were thoroughly prepared and effectively performed were the seismic
16
-, upgrading of. the diesel generator air start system, replacement of pressurizer insulation,
installation of chlorination equipment:in the. service water, system,-.and~pgrading.of
the
" raliatio'n monitoring system~'Coordination'of the steam.generator~tube'sample.removal
to;:~
study fouling also showed good engineering.
The engineering evaluation, which led to expansion of the erosion/corrosion (E/C) program
and the inclusion of small bore piping into the program, following the rupture of a turbine
casing drain line reflected a commitment to personnel safety.
Effectiveness of&e,E/C
program continued to be demonstrated
as shown in the replacement of two and the repair of,
five components during the 1991 outage.
Outage planning and the control of modifications during outages continued to be a licensee
strength.
Engineering played a major role in this success by thorough advance planning and
continual attentiveness
throughout the project completion.
Engineering support was notable
in the unplanned replacement of the service water discharge valves and piping elbows for
'-'both component cooling-water heat exchangers.
The engineering department actively responded to the. prior SALP concern regarding overall
engineering assurance by developing a comprehensive engineering process upgrade program
dedicated to improving engineering performance.
An objective engineering self assessment
pointing to many areas in need of improvement followed by an independent contracted study
formed the basis of the Iirogram. '-The program'as
management approval, but its
implementation began late in the assessment
period and its effectiveness could not yet be
evaluated.
Improvements in the design modification process and quality of root cause, corrective actions,
and calculations were noted during NRC review of. the electrical distribution system.
However, the NRC review of the service water system performed late in the assessment
period identified a number of concerns related to engineering support.
These concerns
included instances of inappropriate engineering review and use of non-controlled calculations,
instances where prior testing was not compared to current system configuration, incomplete
testing verification of current system configuration, and discrepancies in the Updated Final
Safety Analysis system description.
Because the service water issues were identified late in
the assessment
period, their evaluation is presently in process.
These findings point to
": weaknesses
in engineering support of service. water issues.
The piping and instrument drawing upgrade, completed the past assessment
period, was
further enhanced by a new drawing change request methodology and,tracking system that has
made the drawing change process more effective.
An extensive in-house structural
arrangement drawing upgrade and reformatting was just completed and provided accurate
portrayals of existing plant equipment.
The relatively unchanged
engineering work request
backlog is appropriately reviewed and prioritized.
Paperwork closeout delays are being
addressed.
17
The engineering approach to design bases document (DBD) reconstitution was underway..
. Preliminary work on three pilot DBDs"led to a massive, electronic-indexing. of.all Ginna
.
"licensing documents'; attachments "and calculations.. The electronic&ndexing'of all.prior.
Ginna licensing data, combined with the capability to recall information'was a creditable
engineering accomplishment.
There is active participation with the Westinghouse owners
group effort that has three systems nearing completion.
The configuration management
program commitment is to complete system and topical DBDs by the end of 1994.
Engineering participation in licensing matters continued to be strong and engineering keeps
abreast of current and anticipated. actions and resolution of issues from a safety perspective.
High quality submittals with good engineering bases enabled recapture of construction time
and extended the operating license.
High quality finite element analyses and seismic
.
modeling facilitated the containment structure verification that the existing pre-stress
continues to meet original design requirements.
Submittals of post accident response
.instrumentation. safety evaluation issues and responses
to the probabilistic risk assessment
generic.letter~were.timely.and
demonstrated. competent engineering.
Overall, engineering
support of licensing has been excellent.
Recent additions of qualified and experienced engineering personnel were beneficial as
evidenced by the work done in-house on probability risk assessment,
the comprehensive
equipment Q-list, and the widespread availability and use of electronic databases.
The
technical competence of engineering personnel. noted in'prior SALPs continues to-be a-
licensee strength, and effective support of day to day plant problems has contributed to
continued high plant availability.
. In summary,'ngineering
during this assessment
period.was effective in support of plant
operations, evaluation of problems, and determination of root causes.
Modifications were
- well planned and implemented and exhibited good initiatives and safety perspectives.
Engineering support was also strong when unplanned equipment replacement was needed.
Support of licensing has been excellent.
Management dedicated considerable resources
to
improve engineering performance and recent staff additions benefitted the organization.
The
results of major inspections were mixed with strengths observed in the engineering support of
'lectrical distribution system and weaknesses
in the engineering support of the service water
system.
Continued drawing upgrades reflected good engineering; and, DBD efforts were
underway.
Performance Rating:
Category 2
18
III.G Safety Assessment/Quality Verification
III.G.1
Analysis
During the previous SALP, Safety Assessment/Quality
Verification was rated Category 2.
Programmatic improvements in administrative controls and "engineering.depth mere made-
within the Quality Performance organization.
Quality assurance
was more effectively used as
a management tool.
Self-assessment
concerns needed to be tracked to completion.
During the current SALP period, management
support and participation in licensing-matters
continued to be strong and the licensee continued to keep abreast of all current and
anticipated actions that could impact plant operations.
The licensee continued to make
changes to plant programs, adjust corporate and plant organizational structure, and align
corporate management to better focus on problem areas identified in previous SALP periods.
.. New engineering and professional staff were added to augment the corporate and plant
'-organization..""The goals;and.commitment
to,safety. were promulgated by senior corporate
officers.
Management and plant personnel demonstrated
the ability to be constructively self- .
critical of their programs.
Several proposed amendments
to the facility operating license were of high quality.
These
proposed amendments
indicated a safety conscious attitude and resulted in timely issuance.
Examples included the extension to'he'Ginna'operating"license
to recapture the construction"
period, a reformat of technical specifications, and an addition to technical specification
requirements.
The licensee's resolution of generic issues was good.. Recent revisions to the.Ginna Inservice
Inspection gSI) and Inservice Pump and Valve Testing /ST) Programs demonstrated
a
thorough understanding of codes and regulations.
The licensee's resolution of issues
~ contained<in NRC Generic Letters,,Bulletins and Information Notices were timely and
reflected effective prioritization of work.
Several voluntary safety-related improvements demonstrated
a safety conscious attitude.
Two
sources of preferred power through two independent station transformers from the offsite
transmission network were completed.
Human factor improvements in the control room were
implemented during the refueling outage.
10 CFR 50.59 safety reviews were technically sound, thorough and well documented.
The
annual
10 CFR 50.59 reports were timely and complete.
A major modification, which was
indicative of the licensee's thorough safety reviews, was the installation of an Advanced
Digital Feedwater Control System (ADFCS). The licensee's
safety evaluation supporting this
modification was particularly detailed and addressed
the potential challenges to the Reactor
Protection System by component failures in the original analog feedwater.control system.
19
. 'he, Nuclear Safety Audit and Review Board.(NSARB),effectively,provided an oversight role
" :by periodically reviewing, the activities of.the. Plant Operations.Review~Committee
(PORC),.-
. " "-.'reviewing.plant'events and'.evaluating."the:adequacy
of the.QA;program=~louring,this. SALP=
period, NSARB effectiveness:has
been enhanced. by. including m..independent consultant.and.a
representative from another utility as board members.
In general, the. PORC provided strong decisive control for assuring that quality procedures
and safety reviews were developed.
During meetings, priorities were established,
discussions
were candid and thorough, and final committee approval was consistently:based
on
satisfactory resolution of pertinent safety= issues.
One significant event, however, occurred as
a result of an inadequate review of a maintenance procedure.
This inadequ'ate review resulted
in the inadvertent disabling of the safeguard logic instrumentation.
Subsequently,
stronger
controls revising plant procedures were implemented.
.The.Licensee Event, Reports (LERs), which-were submitted by the licensee, were well written
'. and submitted~a untimely manner., All.LERs.issued, gave appropriate attention to discussion
of root causes,
safety significance of events, and corrective actions.
, The licensee has initiated several enhancements
to the corrective action process.
These
changes included improved guidance in the corrective action procedures,
development of,a
formalized root cause analysis process and implementation of a computerized corrective
action tracking system.
In general, the licensee's identification of deficiencies, corrective actions and root cause
determinations were effective.
Notable examples included the circuit card design deficiencies
for the Undervoltage Monitoring/Protection System and the ATWS Mitigation System
Actuation Circuitry. In contrast, quality assurance
deficiencies were identified in the control
of engineering processes
with regard to the Service Water System design and operation.
'"Additionally,
the identified. weaknesses
in-the.REMP..QA/QC programs during the last SALP
period continued into this period.
These deficiencies indicate that continued management
attention in quality assurance
is wairanted.
Management's
use of the Quality Performance. Department enhanced plant performance.
During quarterly QA/QC subcommittee meetings, which were attended by senior corporate
and site'management,
the results of audits;~ the:findings.of the, quality assurance,surveillances,
and details surrounding recent plant experiences
were critically=discussed.
A general
- -
- -
indication of plant performance was provided to management
based on the number of initiated
audit finding corrective action. reports, field change requests,
maintenance work requests,
.
nonconformance reports, and corrective action reports.
20
- gym'~'
".. -':Senior management~as'i'ctively:involved"in,technical
issues which-ensured;a.high
quality of=
licensee support performance...Management
at all levels was.closely, involved in the operation
and maintenance of the plant.
Operational decisions were. made on the basis of safety
implications.
10 CFR 50.59 safety reviews were detailed and thoroughly documented.
The
Nuclear Safety Audit and Review Board provided an effective oversight role of the plant
activities and the PORC.
Although PORC was generaHy effective in their reviews, procedure
revisions and safety evaluations,
an inadequate procedure review resulted in the. disabling of
safeguards logic instrumentation.
-The Quality Performance Department refined its assessment
method which resulted in an improvement in effectiveness.
Quality assurance
weaknesses
in
controlling engineering processes
and in the REMP indicate the need for continued
management
attention.
III.G.2
Performance Rating:
Category 2
21
IV.
SALP EVALUATIONCRmt&IA
"'"" '
":"."."License'eaperforman'ce"is msessedeinrselecte'd
functional areas,<<dependinggon~whether
the
.facility is in a construction or operational phase.
Functional areas normally represent areas
significant to nuclear safety and the environment.
Some functional areas may not be assessed
because of little or no licensee activities or lack of meaningful observations in that area.
Special areas may be added to highlight significant observations.
The following evaluation criteria were used, as applicable, to assess
each functional area:
1.
Assurance of quality, including management involvement and control.
2.
Approach to the identification and resolution of technical issues from a safety
standpoint.
3.
':Enforcement history.
4.
Operational and construction events (including response to, analysis of, reporting of,
and corrective actions for).
5.
Staffing (including management).
6.
Effectiveness of training and qualification programs.
The performance categories
used when rating licensee performance are defined as follows:
Q~te
ry l
Licensee management attention to and involvement in nuclear safety or
safeguards activities resulted in a superior level of performance.
NRC willconsider reduced
levels of inspection effort.
~ate ~ory 2.
Licensee management
attention to and involvement in nuclear safety or
safeguards activities resulted in a good level of performance.
NRC willconsider maintaining
normal levels of inspection effort.
~Cate o
3
Licensee management, attention to and.invoivement in nuclear safety or
safeguards activities resulted in an acceptable level of performance; however, because of the
NRC's concern that a decrease
in performance may approach or reach an unacceptable level,
NRC will consider increased levels of inspection effort.
N. i iii ii '<<
ii
iii
performance.
These cases would include instances in which a.rating could not be developed
because of insufficient licensee activity or insufficient NRC inspection.
22
R
~ The SALP Board may assess
a performance trend,. ifappropriate.
-The trends are:
'" ~Im r~n"-'icensee performance
as )determined.to.be improVingAuring'the,assessment '-
period.
~Dectinin
Licensee performance was determined to be declining during the assessment
period and the licensee had not taken meaningful steps to address this pattern.
Trends are normally assigned when one is definitely discernable and a continuation of the
trend may result in a change in performance during the next assessment
period.