ML17228B530

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Insp Repts 50-335/96-06 & 50-389/96-06 on 960331-0522. Violation Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maintenance & Plant Support
ML17228B530
Person / Time
Site: Saint Lucie  
Issue date: 06/07/1996
From: Chou R, Mark Miller, Sandin S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17228B528 List:
References
50-335-96-06, 50-335-96-6, 50-389-96-06, 50-389-96-6, NUDOCS 9606210165
Download: ML17228B530 (63)


See also: IR 05000335/1996006

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-335,

50-389

License

Nos:

DPR-67,

NPF-16

Report

No:

50-335/96-06,

50-389/96-06

Licensee:

Florida Power

& Light Co.

Facility:

St. Lucie Nuclear Plant, Units

1

8

2

Location:

9250 West Flagler Street

Hiami,

FL 33102

Dates:

March 31 - Hay

1 1,

1996

Inspectors:

H. Hiller, Senior Resident

Inspector

S. Sandin,

Resident

Inspector

=R. Chou,

Reactor Inspector,

paragraphs

H1.2, H2.2,

H2.3

J. Coley, Reactor Inspector,

paragraphs

Hl.3, Hl.4,

H3.1

D. Lanyi, Project Engineer,

paragraph

02. 1

Approved by: K. Landis, Chief, Reactor Projects

Branch

3

Division of Reactor Projects

9606210ib5

960607

PDR

ADOCK 05000335

6

PDR

EXECUTIVE SUMMARY

St. Lucie Nuclear Plant, Units

1

& 2

NRC Inspection

Report 50-335/96-06,

50-389/96-06

This integrated

inspection

included aspects

of licensee

operations,

engineer-

ing, maintenance,

and plant support.

The report covers

a six week period of

resident inspection.

0 erations

~

A condition of unidentified

RCS leakage

through the

CVCS system

was

appropriately identified and addressed

by operators;

however,

operators

were nonconservative

in declaring

an

NOUE (paragraph

01.2).

~

Operators

responded

properly

and in

a timely fashion in shutting

down

the Unit

2 turbine in response

to low auto stop oil pressure

following

testing

(paragraph

01.3)

~

A non-licensed

operator

showed

good attention to detail during

RAB tours

in identifying an uncompensated

breach

in a fire-rated wall (paragraph

01.4).

Operators

performed well during

a Unit

1 shutdown for refueling

(paragraph

01.5).

Operators

performed well during reduced

inventory operations of Unit

1

(paragraph

01.6).

ESF system

walkdowns identified weaknesses

in the accuracy of operations

procedures

(paragraph

02. 1, 03. 1).

~

Management

changes

resulted

in the naming of an interim operations

manager

(paragraph

06).

Maintenance

Observations

of valve repacking

and modifications indicated acceptable

maintenance

activities

(paragraph

M1.2).

~

Maintenance of pressurizer

code safety valves

was performed in

accordance

with approved

procedures

by knowledgeable

personnel

(paragraph

H1.3).

Inspectors

identified one case of maintenance

being performed without a

properly verified procedure

at the job site

(NCV 96-06-02,

paragraph

H1.4).

Integrated

safeguards

testing resulted

in

a failure of the

1B

EDG output

breaker to close.

Operator

and test personnel

performance

was excellent

(paragraph

M2. 1).

Reviews of polar crane

load tests

and observation of reactor vessel

head

lift indicated satisfactory

performance

(paragraph

H2.2).

a

~

Reviews of main steam safety valve testing indicated proper performance

of test activities

(paragraph

H2.3).

Preparations

for the inservice inspection of the Unit

1 reactor

vessel

were found to be in accordance

with applicable

requirements

and

showed

'ood

outage planning

(paragraph

N3. 1).

~E

4

~

Engineering

personnel

showed

poor attention to detail in the preparation

of an engineering

package

which resulted

in an uncompensated

breach of a

fire barrier

(NCV 96-06-01,

paragraph

01.4).

Engineering

support in response

to

a failed motor for HVS-4A precluded

a

TS required

shutdown

(paragraph

E2. 1).

~

A failure of engineering

personnel

to promptly document

a nonconforming

condition affecting approximately seventy

instruments

was identified

(NCV 96-06-03,

paragraph

E4. 1).

~

A number of findings relating to configuration control resulted

in an

unresolved

item (URI 96-04-05,

paragraph

E7. 1).

~

P missing orifice plate

was identified in the

ICW system during as-built

verification inspections

(NCV 96-06-04,

paragraph

E7. 1).

Multiple examples of UFSAR inaccuracy

were identified

(URI 96-04-09,

paragraph

XI) .

Plant

Su

ort

An audit of turbine building fire extinguishers

identified differences

between

the plant

and the

UFSAR (paragraph

F2).

An audit of fire brigade

member qualifications resulted

in

a violation

for failure to maintain current physicals

(VIO 96-06-05,

paragraph

F5).

Re ort Details

t

Summar

of Plant Status

Unit

1

Unit

1 entered

the inspection period at

100 percent

power and operated

at full

power until April 29,

when the unit was shut

down for refueling.

The unit

entered

Hode

6 on Hay 7.

At the close of the inspection period the unit was

preparing for defueling.

Unit 2

Unit 2 entered

the inspection period at

100 percent

power and operated

at full

power until April 9,

when power was reduced to 85 percent

due to through wall

leaks in circulating water system piping.

The unit was maintained at 85

percent while repairs

were affected.

Following repairs,

the unit achieved

full power on April 20; however, difficulties encountered

with turbine

overspeed

testing

on April 20 necessitated

removal of the turbine from

service.

The unit was maintained in Hode

2 until April 21,

when the generator

was tied to the grid.

The unit was returned to full power on April 22 and

maintained full power through the

end of the inspection period.

I. 0 erations

Ol

Conduct of Operations

Ol. 1

General

Comments

71707

Using Inspection

Procedure

71707, the inspectors

conducted

frequent

reviews of ongoi'ng plant operations.

In general,

the conduct of opera-

tions was professional

and safety-conscious;

specific events

and

noteworthy observations

are detailed in the sections

below.

01.2

Unit 2

RCS Leaka

e and Unusual

Event Declaration

40500

71707

93702

Description of Event

On Harch 31, Unit

1 experienced

RCS leakage

in excess of TS limits and

ultimately declared

an Unusual

Event.

The timeline of the 'event

was

as

follows:

10:38 a.m.

11:55 a.m.

12:00 p.m.

12:25 p.m.

Operators

placed the

2A purification ion exchanger

in

service after securing the deborating

ion exchanger.

During logtaking th

RCO noted that

VCT level

had dropped

3

percent

over the previous hour.

This decrease

equated to an

approximate

1.6 gpm loss of inventory.

Operators

entered

ONOP 2-0120031,

"Excessive

Reactor Coolant

System

Leakage."

Charging

and letdown flows were verified

to be matched

and

no containment radiation or leakage

collection increases

were noted,

indicating that the leak

was outside containment.

NLOs were dispatched

to look for

leaks.

An

RCS inventory balance

was

commenced.

Operators

logged the existence of a 1.6

gpm indicated leak.

12:45 p.m.

12:55 p.m.

1:00 p.m.

2:30 p.m.

3:02 p.m.

Annunciator N-5,

"Letdown Pressure

Hi/Lo," wa's received,,

letdown flow was noted to increase

to approximately

84 gpm,

and indicated

VCT level

change

was noted to increase

in

step-wise

fashion to 29 gpm.

CVCS ion exchangers

were bypassed

(isolated

from system)

and

VCT level decrease

stopped.

Results of RCS inventory balance

indicated that

an average

leak rate of 7.43

gpm had existed over the previous hour.

An NOUE was declared

and t'erminated

as

a result of the

observed

leak rate.

NRC Operations

Center notified per

10

CFR 50.72(a)(1)(i) for

a declared

emergency.

Classification of Event

The inspectors

responded

to the site

and found the plant in a stable

condition.

Discussions

with the

NPS and

ANPS indicated that the

NOUE

was declared after discussions

with plant management

following the

completion of RCS inventory balance.

The inspectors

reviewed

EPIP

3100022E,

Rev 29, "Classification of Emergencies,"

Event/Class

1.A,

"Abnormal Primary Leak Rate."

Classification

as

an

NOUE required the

following conditions:

RCS water inventory balance

indicates:

a.

greater

than

1 gpm unidentified leakage.

OR

b.

greater than

10 gpm identified leakage.

OR

2.

Inspection reveals

any

RCS pressure

boundary leakage.

OR

3.

Indication of leaking

RCS safety'or relief valve which causes

RCS

pressure

to drop below 1600 psia."

The inspectors verified that operators

had properly implemented

ONOP 2-

0120031,

"Excessive

Reactor Coolant System

Leakage,"

up to, but not

including, step 2.L.2, which required isolating

CVCS letdown.

Additionally, the inspectors verified that

an

NOUE was not required

during the event,

based

upon

a strict reading of the applicable

EAL.

Operators

stated that the

NOUE was not declared

when unidentified

leakage

was determined to exceed

1 gpm because

the rate

was not

determined

by inventory balance;

rather, it had

been derived from VCT

level indications over time.

Additionally, operators

stated that

some

confusion existed over whether the leakage constituted

RCS leakage,

as

the operators

had confidence that the leakage

was occurring outside of

containment

(as evidenced

by charging

and letdown flows being matched)'.

Finally, operators

stated that,

as the condition had arisen shortly

.

after placing the purification ion exchanger

in service,

they had

a

strong

sense that the leak was related to that evolution.

The licensee

stated that the ultimate decision to declare

the

NOUE was

based

upon the

results of the

RCS inventory balance

(7.43

gpm at 1:00 p.m.), but that

the declaration

was delayed

due to the cessation

of the indicated

leakage

when the

CVCS ion exchangers

were isolated at 12:55 p.m., which

called into question the need for a declaration.

Notwithstanding the

accuracy of the operators'ecision

with respect to procedural

requirements,

the inspectors

concluded that the lack of an

NOUE during

the event represented

a nonconservative

decision

on the part of

operators

in that:

Operators

had indication of an approximate

1.6

gpm leak at ll:55

a.m.

Discussions

with the

NPS indicated that

a reluctance to

declare

an

NOUE based

upon

VCT level indication existed,

due both

to the specific

EAL criteria referencing

an inventory balance

and

concern that the level instrument might have

been inaccurate.

However, the inspectors

noted tha't two level transmitters

were

available which reported

VCT level to the control

room.

While

sharing

a common reference leg, the existence of two instruments,

and the ability to perform a channel

check (which would have

shown

agreement

between the two transmitters),

could have provided

confidence in the observed level decrease.

~

Operators

logged the 1.6 gpm leak rate at 12:25 p.m.

and noted

that searches

for the leak were continuing

and that the leak was

persisting'.

At this point, the leakage

had

been identified for

approximately

one half hour, allowing for assessment

and decision-

making.

~

At 12:45 p.m., leakage

was noted to increase

to 29 gpm.. At this

point, the leakage

source

had still not been identified and the

condition had clearly degraded.

The licensee

investigated

the occurrence with respect to Emergency

Plan

execution

(documented

on

CR 96-483).

The inspectors

found the

licensee's

evaluation.to

be comprehensive

and noted that the licensee

concluded that operators

were slow to declare the

NOUE.

As a result of

the'licensee's

investigation,

corrective actions

were developed

which

included:

~

Developing

a better definition for what constituted

RCS leakage.

~

Evaluating the need for an

EAL interpretation

document.

~

Revising

EPIP

EAL 1.A to require

an

NOUE for RCS leakage that

results in an entry into the

AS for TS 3.4.6.2

(which specified

RCS leakage limits) and submitting

a revision to the

Emergency

Plan to remove the I gpm unidentified

RCS leak rate criteria

from'he

EAL in deference

to

NUHARC guidance,

which allows

up to

10 gpm

unidentified leakage prior to an

NOUE.

~

Revising the

RCS inventory balance

methodology to allow shorter

calculational

periods for determining

RCS leakage during off-

normal conditions.

Root Cause

Determination

As a result of this event,

the licensee

formed

an Event Response

Team to

determine root cause

and corrective actions.

The inspectors

followed

the activities of the team

as they proceeded.

The team employed

a

methodology which delineated all possible

sources

of inventory loss

and

which systematically eliminated possibilities for which adequate

bases

existed.

In general,

the inspector

found the licensee's

actions well-

founded;

however,

the inspector

found that the timeliness of the team's

actions suffered

from a lack of obtaining input from the operating

crew

after the event.

The

ANPS and

NPS both provided written statements

detailing the event before leaving the site the day of the event.

Other

crew members did not prepare

such statements,

and data which was

key to

determining the most likely root cause

(concerning valve position

and

manipulation)

was not obtained in a comprehensive

way until the third

de of the investigation.

The team was unable to conclusively determine

the root cause of the loss

of inventory event;

however,

a plausible root cause

was determined.

Through reviews of existing plant data,=- the team concluded that the loss

of inventory occurred through the lifting of CVCS relief valve V2520,

which provided overpressure

protection to the low pressure

portions of

the letdown line downstream of the pressure

control valves.

Inventory

balances

of lost

VCT level versus

Holdup Tank level (the destination for

water relieved through V2520) confirmed this valve as the most probable

point of inventory loss.

The licensee

subsequently

bench tested

the

relief valve and found its leakage

and setpoint to be within acceptable

values.

Consequently,

the licensee

determined that the valve lifted, to

varying degrees,

as

a response

to actual

high pressure

conditions.

Following the event,

the licensee

performed valve lineup verifications

of the

CVCS system.

In so doing, the licensee identified that

V2382

(ion exchanger

downstream isolation)

was not fully open

(as required),

such that

a backpressure

could have developed

which would approach

the

V2520 lift setpoint of 200 psig.

The licensee

theorized that

a slight

mispositioning of the valve could have led to

a less than fully opening

of V2520 (which would account for the initial 1.6

gpm leak rate),

which

was then exacerbated

when valve lineup checks

(to identify the source of

the leakage

during the event) resulted

in an operator checking the valve

in a closed direction, further increasing

the backpressure

and exceeding

the relief valve's setpoint.

The licensee verified, through

a system

pressure test, that no additi'onal

leakage

path existed in the affected

portion of the system,

thus limiting the possible

leakage

paths to the

relief valve lift described

above.

As corrective action for the identified root cause,

the licensee

installed

a local pressure

gauge in the low pressure

portion of both

units'VCS letdown lines to aid operators

in diagnosing

system

performance.

Additionally, the licensee

enhanced

-procedural

guidance

on

verifying valve positions to include

an emphasis

on ensuring that valves

which are to be open are left in a full open position following a

position check.

Conclusion

In conclusion,

the inspectors

found the following with respe'ct to this

event:

Operators

showed

good attention to plant parameters

in identifying

the subject leak and took actions consistent with ONOPs in

addressing it.

The failure to declare

an

NOUE while the subject leak was active

was considered

a nonconservative

decision

on the part of

operators;

however,

operators

were in strict compliance with EPIP

EALs.

The licensee's

investigations of both the decision making behind

operators'mplementation

of the

Emergency

Plan

and the root

causes

of the leakage

were comprehensive

and sound.

The timeliness of the Event Response

Team's efforts in determining

root cause

was

hampered

by a failure to debrief the entire

operating trew following the event.

01.3

Unit 2 Down ower

71707

93702

On April 20, Unit 2 operators

were performing testing of the turbine

overspeed trip function.

The licensee's

procedure for performing this

evolution required that the Overspeed

Test Handle

on the turbine front

standard

be held in the

"TEST" position during the test.

With the

Overspeed

Test Handle in "TEST," auto-stop oil pressure

was

hydraulically prevented

from decreasing

to

a point that would result in

a turbine trip when

a mechanical

overspeed trip was induced

as

a part of

the test.

Following a satisfactory test of the mechanical

overspeed trip function,

operators

were required to verify that,

upon placing the Overspeed Trip

Lever in "Reset," auto-stop oil pressure

returned to greater

than

90

psig;

however,

upon taking the specified action,

operators

noted that

pressure

returned to only 76-80 psig.

The evolution was repeated

several

times with the

same result.

Operators

maintained

the position

of the Overspeed

Test Lever in "TEST," and

a unit downpower

commenced

at

3:55 p.m. with the goal of reducing

power to below 15 percent,

where

a

turbine trip would not result in a reactor trip.

With the mechanical

overspeed

system inoperable

(due to the Overspeed

Test Lever in the

"TEST" position),

overspeed

protection

was provided

.

solely by OPC,

an electronic

system which energized oil dump solenoids

to close turbine control

and interceptor valves

on

an overspeed

condition.

TS Surveillance

Requirement 4.3.4.2 stated that the

overspeed

protection

system required

by the associated

LCO would be

demonstrated

operable,

in part,

by cycling all stop, control, reheat

stop,

and interceptor valves through

a complete cycle once per month.

Operators

interpreted this requirement to imply that all of the

specified valves

must

be able to respond to an overspeed

condition for

the overspeed

protection

system to be considered

operable.

As the

OPC

would have only actuated

two of the four sets of valves specified

by the

Surveillance

Requirement

(due to the condition of the Overspeed

Test

Handle),

operators

considered

the turbine overspeed

system required

by

TS to be inoperable

and, at 4:30 p.m., entered

TS 3.3.4 Action b, which

required that the turbine

be isolated

from the Main Steam

System within

six hours.

A turbine downpower

was

commenced

and, at 4:55 p.m., the

licensee notified the

NRC Operations

Center that

a shutdown required

by

TS had

commenced,

as required

by 10

CFR 50.72.

The inspector

responded

to the site

and observed

the shutdown'.

The

inspector

found control

room conditions to be well-controlled, with a

minimum of noise

and crowding.

Operators

communicated well and the

cpnsistent=use

of repeatbacks

and formal communication

was noted.

The

only questionable

attribute observed

was the direct involvement of the

NPS

and

ANPS at portions of the control

boards at various times,

as

opposed to the expected

performance

standard that'hey maintain

a broad,

"big picture,"

command

and control position.

As electrical

load was reduced to minimal levels,

a main generator

reverse

power annunciator

was received

and,, at 7:04 p.m., operators

promptly tripped the turbine.

With the turbine isolated

from the Main

Steam System,

operators

exited the applicable

TS AS.

The licensee

performed troubleshooting

on the auto-stop oil system

and determined

that debris

had partially clogged

a flow restricting orifice in the oil

line supplying the system.

The debris

appeared

to remove itself from

the system in time,

and oil pressure

returned to pre-test levels.

In

evaluating the event,

the licensee

determined that the oil pressure

observed directly following the test would have

been sufficient to

prevent

a trip, and

OP 2-0030150,

"Secondary

Plant Operating

Checks

and

Tests,"

was revised to allow pressures

as low as

70 psig to be observed

before. prohibiting the release

of the Overspeed

Test handle.

The inspector

concluded the following with respect to this event:

Operators

properly interpreted

TS requirements

regarding

operability of the turbine overspeed .protection

system.

Operators

performed professionally in removing the turbine from

service.

SRO

command

and control was,

at times,

too narrowly focused.

~

01. 4

Un lanned

Breach in Fire Barrier

71707

37551

On April 22,

a Unit

1

SNPO reported to the control

room his

identification of two holes in a wall in the pipe penetration

room.

The

two 10 inch diameter holes were bored in the wall as

a part of the

implementation of PC/N 001-196,

"Containment Air Conditioning for

Refueling Outages,"

and supported

the installation of connections

to

CCW

piping for temporary chilled water which was to be directed to the

containment

fan coolers during outage

work to affect containmhnt

cooling.

The licensee. noted that

UFSAR Section 9.5A, section 3.11, described

the

wall in question

and stated that it was required to be functional in a

non-degraded

condition.

AP 1800022,

"Fire Protection Plan,"

was

referenced

and it was found to allow such

a breech,

provided that either

continuous fire detector

coverage

or

a continuous fire watch was

provided.

A continuous fire watch was established

and the holes were

covered with wooden barriers

(to support ventilation requirements).

The inspector

reviewed

ENG-gI l. 1,

Rev 0, "Engineering

Packages,"

and

found that requirements

were provided for preparers

of engineering

packages

to consider plant safety issues

during the implementation of

design

changes.

The inspector

reviewed the subject

PC/H and found that:

A section entitled "Plant Safety During

Implementation/Restoration"

discussed

the modification exclusively

from the standpoint of CCW system operability.

An attachment entitled "Fire Protection

Review Checklist" included

a specific line item prompting the preparer to consider whether

the engineering

package installed, modified, or altered the

function of fire barriers.

The question

was answered

"no."

The inspector

concluded that the licensee's

engineering

personnel

performed

an inadequate

review of the subject modification with respect

to fire protection considerations.

The licensee's

corrective actions

were documented

in

CR 96-551,

and included:

~

A review of pre-job barriers

which should

have prevented

the

event.

0

~

Fire protection process

reviews

and enhancements.

~

Strengthening

the engineering

process

and its potential

impacts

on

fire barriers.

The inspector

concluded that the licensee's

failure to properly consider

the in-process

effects of the subject modification constituted

a

violation of the licensee's

procedures

covering engineering

packages.

However, the inspector

found that the licensee's

operators

were

effective in identifying the condition

and that corrective actions,

both

to the field condition

and the process

issue,

were appropriate.

This

licensee identified and corrected violation is being treated

as

a Non-

Cited Violation, consistent with Section VII.B.1 of the NRC'Enforcement

Policy

(NCV 335/96-06-01,

"Failure to Consider Fire Barrier Operability

in Engineering

Package" ).

Unit

1 Shutdown

40500

71707

On April 28, Unit

1 commenced

a reactor

shutdown to begin

a refueling

outage.

At 10:49 p.m., during the shutdown,

operators

experienced

difficulties when

CEA

1 failed to insert properly with the rest of the

CEAs in its group.

The shutdown

was placed

on hold at approximately

88

percent

power while I&C performed troubleshooting

on the

CEA.

Visicorder data

suggested

that the hold coil for CEA

1 was not releasing

to allow the

CEA to insert.

The inspector

was present

and verified that

the

CEA was still tripable

and was within 7.5 inche's of the other

CEAs

in Regulating

Group 7, thus satisfying

TS requirements for continued

operation.

A troubleshooting

plan was assembled

under

AP 0010142,

Rev 19, "Unit

Reliability - Manipulation of Sensitive

Systems,"

which included placing

the

CEA on

a parallel

bus with CEA 68, replacing the timer module, the

pull down power switch,

and the lift power switch for CEA 1,

and then

divorcing the

CEA from the parallel

bus in accordance

with the vendor

technical

manual.

The inspector

attended

a

FRG meeting conducted to

review the troubleshooting

plan.

A quorum was present,

and the issue

was discussed

appropriately.

The inspector witnessed

the module

replacements

and the subsequent

operability tests

performed

by

operators.

No d'eficiencies

were identified.

Shutdown

recommenced

at 2:15 a.m.

on April 29.

Node.2

was entered

at

6:35 a.m.

and the reactor

was tripped

as

a part of a pre-planned test to

verify the mechanical

freedom of CEAs.

TS 3. 1.3.4 required

CEA drop

times of less

than or equal to 3. 1 seconds.

The inspector

reviewed the

data obtained

from the test

and found the average

drop time to be 1.97

seconds,

with the longest time being 2.50 seconds.

Overall, the inspector

found the conduct of the shutdown to be good,

with operators

communicating formally and with the consistent

use of

repeatbacks.

Particularly notable

were consistent

and conscientious

refe'rences

to annunciator

response

summaries

by operators

as

annunciators

were received.

This performance

was repeated

by'everal

operators

involved in the shutdown

and was viewed as

a strength in

licensed operator

performance.

Reduced

Inventor

0 erations

71707

During the inspection period, Unit

1 entered

a reduced

RCS inventory

condition to support

steam generator

nozzle

dam installation.

The

following items were observed

during this evolution:

~

Containment

Closure Capability - Instructions

were issued to

accomplish this;

men

and tools wer'e

on station.

A dry run of

closing the equipment

hatch

was performed prior to the draindown.

The inspector

reviewed penetrations

open at the time of the

draindown

and verified that closure capability was provided.

RCS Temperature

Indication - Two CETs were available

on each

SPDS

channel.

RCS Level Indication - Independent

RCS wide and narrow range level

instruments,

which indicated in the control

room, were operable.

An additional

Tygon tube loop level in the containment

was

installed

and was visible to a dedicated

operator in the control

room via a television monitor.

During the draindown,

the camera

became

inoperable.

The inspector noted that the draindown

was

immediately secured

and

an operator

was dispatched

to the level

tube to provide direct input to the control

room via radio.

~

RCS Level Perturbations

- When

RCS level

was altered,

additional

operational

controls were invoked.

At plant daily meetings,

operations

took actions to ensure that maintenance

did not

consider performing work that might effect

RCS level or shut

down

cooling.

RCS Inventory Volume Addition Capability - The

B HPSI

pump and the

B charging

pump were available for inventory addition,

as were two

trains of shutdown cooling.

RCS Nozzle

Dams - The purpose of the draindown

was to install the

nozzle

dam's.

Vital Electrical

Bus Availability - Operations

would not release

busses

or alternate

power sources for wor k during this outage.

~

Pressurizer

Vent Path - The manway atop the pressurizer

has

been

removed to provide

a vent path.

02

Operational

Status of Facilities and Equipment

02. 1

En ineered Safet

Feature

S stem Walkdowns

71707

The inspectors

used Inspection

Procedure

71707 to walk down accessible

portions of the following ESF systems:

~

During the week of April 7, the inspector

performed

a walkdown of

the Unit

1 Intake Cooling Water System.

This consisted of a

review of the following procedures

and engineering

drawings

and

verification of current system alignment.

OP 1-0640020,

Rev 41,

"ICW System Operation"

ONOP 1-0640030,

Rev 19, "Intake Cooling Water System"

ONOP 1-0030131,

Rev 62, "Plant Annunciator Summary"

Other Procedures

10

'

Applicable Engineering

Drawings

~

UFSAR Sections

7.3, 7.4 and 9.2

A number of minor discrepancies,

involving procedural

typographical

errors

and omissions,

were noted.

These conditions

were documented

by the licensee

in PMAI 96-083.

Equipment

operability, material condition,

and housekeeping

were acceptable

in all cases.

A number of more significant items, involving

procedural

accuracy

and the maintenance

of the

UFSAR, were also

identified,

and are documented

in paragraphs

03. 1,

E7 and Xl,

respectively.

Of particular concern

were the following procedural

errors:

~

TS 4.7.4.1,

"SURVEILLANCE RE(UIREMENTS" for INTAKE COOLING

WATER SYSTEM

This surveillance required,

in part, that "At leapt two

intake cooling water loops are demonstrated

OPERABLE:

a 0

At least

once per

31 days

by verifying that each valve

(manual,

power operated

or automatic) servicing safety

related

equipment that is not locked,

sealed,

or

otherwise

secured

in position, is in its correct

position."

All valves supplying

ICW to safety related

equipment,

with

the exception of the temperature

controlled automatic valves

TCV-4A and 4B, were locked.

TCV-4A and

4B were verified

"Throttled" (verify flow per

SNPO log) as part of the

CCW A

and

B Train Tests

performed monthly

(AP 1-0010125,

Rev 107,

"Schedule of Periodic Tests,

Checks

and Calibrations,"

Check

Sheet 7).

As the temperature

controllers which actuated

these

valves

had both manual

and automatic

modes of

operation,

the inspector discussed

this method of

verification with the acting Operations

Supervisor

and

Licensing.

Although the initial and quarterly alignment

check specified the controller. in automatic,

Operations

still considered

the valve operable if the controller was in

the manual

mode.

CR 96-1148

was prepared to evaluate this

condition.

AP 1-0010123,

Rev 100, "Administrative Control of Valves,

Locks and Switches,"

Appendix J, "Intake Cooling Water Valve

List," checked the general

condition

and alignment of ICW

valves to the

TCW and

CCW heat exchangers.

The temperature

controlled automatic valves TCV-14-4A and

4B were verified,

by procedure,

to be in the automatic

mode,

the

same

as the

initial system lineup.

This appendix

was verified

quarterly.

The two different methods of verifying TCV-14-4A and

4B

'0

position, i.e. controller in auto

(OP 1-0640020

and

AP 1-

0010123)

and throttled

(AP 1-0010125),

were inconsistent.

CR 96-1148

was prepared to evaluate this condition.

~

1-EOP-99,

Rev

15

Table

1 Safet

In 'ection Actuation Si nal

(Page

4 of 4)

verified that

"Two (2)

ICW Pumps lA and

(1B or 1C) are

ON.

The

1C

ICW Pump could

be aligned to the

A ICW Header,

in

which case, this verification would be incorrect.

During the week of April 14, the inspector

performed

a walkdown of

the Unit 2 Intake Cooling Water System.

This consisted of a

review of the following procedures

and engineering

drawings

and

verification of current

system alignment.

~

OP 2-0640020,

Rev 28, "Intake Cooling Water System

Operation"

~

ONOP 2-0640030,

Rev 18, "Intake Cooling Water System"

~

ONOP 2-0030131,

Rev 51, "Plant Annunciator Summary"

~

Other Procedures

~

Applicable Engineering

Drawings

~

Unit 2

UFSAR Sections

7.3, 7.4

and 9.2

A number of minor discrepancies,

involving procedural

typographical

errors

and omissions,

were noted.

These conditions

were documented

by the licensee

in PMAI 96-084.

Equipment

operability, material condition,

and housekeeping

were acceptable

in all cashs.

A number of more significant items, involving

procedural

accuracy

and the maintenance

of the

UFSAR, were also

identified,

and are documented

in paragraphs

03.1,

E7 and Xl,

respectively.

Of particular concern

were the following procedural

errors:

~

TS 4.7.4,

"SURVEILLANCE REQUIREMENTS" for INTAKE COOLING

WATER SYSTEM

This surveillance required,

in part, that "At least

two

intake cooling water loops shall

be demonstrated

OPERABLE:

a ~

At least

once per 31 days

by verifying that each valve

(manual,

power operated

or automatic) servicing

safety-related

equipment that is not locked,

sealed,

or otherwise

secured

in position, is in its correct

position."

All valves supplying

ICW to safety related

equipment,

with

the exception of the temperature

controlled automatic valves

TCV-14-4A and 4B, wer e locked.

TCV-14-4A and

4B were

verified "Throttled" (verify flow per

SNPO log)

as part of

the

CCW A and

B Train Tests

performed monthly

(AP 2-0010125,

12

Rev 59,

"Schedule of Periodic Tests,

Checks

and

Calibrations",

Check Sheet 7).

As the temperature

controllers which actuated

these

valves

had both manual

and

automatic

modes of operation,

the inspector discussed

this

method of verification with the acting Operations

Supervisor

and Licensing.

Although the initial and quarterly alignment

check specified the controller in automatic,

Operations

still considered

the valve operable if the controller was in

the manual

mode.

AP 2-0010123,

Rev 69, "Administrative Control of Valves,

Locks and Switches,"

Appendix J, "Intake Cooling Water Valve

List," checked the general

condition and alignment of

ICW'alves

to the

TCW and

CCW heat exchangers.

The temperature

controlled automatic valves

TCV-14-4A and

4B were verified

in the automatic position, the

same

as the initial system

lineup.

This appendix

was verified quarterly.

The two different methods of verifying TCV-14-4A and

4B

position, i.e. controller in auto

(OP 2-0640020

and

AP 2-

0010123)

and throttled

(AP 2-0010125),

were inconsistent.

CR 96-1148

was prepared to evaluate this condition.

~

2-EOP-99,

Rev 12.

Table

1 Safet

In 'ection Actuation Si nal

(Page

4 of 5)

verifies that

"Two (2)

ICW Pumps

(2A or 2C)

and

2B are

ON.

The

2C

ICW Pump could be aligned to the

B

ICW Header,

in

which case, this verification would be incorrect.

The inspectors

performed

a walkdown of the accessible

portions of

the

HPSI system

on Unit 2 the week of May 6. 'his consisted of a

review of the following procedures

and engineering

drawings

and

verification of current system alignment including:

OP 2-0410020,

Rev 29,

"HPSI/LPSI Normal Operation"

ONOP 2-0030131,

Rev 51, "Plant Annunciator Summary"

ONOP 22-0410030,

Rev 9,

"High Pressure

Safety Injection"

Applicable Engineering drawings

UFSAR Section 6.3

Equipment operability, material condition,

and housekeeping

were

acceptable.

Equipment labeling was in good condition and easily

accessible.

The inspector did note that one of the dogged

doors

leading into the area

was left ajar while an operator

was

performing his rounds in the area.

A number of minor procedural

deficiencies

were identified and forwarded to the licensee for

disposition.

13

'2.2

E ui ment Clearances

71707

The inspectors

independently verified the following equipment clearances

for correctness:

a ~

b.

1-96-04-369

on

ICW A Header

CW Pump s'upply line - This clearance

consisted of three tags isolating the

ICW A Header

CW Pump supply

line.

All tags were in place

and the valves in the correct

position.

2-96-04-075

on HVS-4A centrifugal

fan for RAB main supply system-

This clearance

consisted of one tag isolating the electrical

supply to the HVS-4A.

The tag was in place

and the breaker in the

correct position.

03

Operations

Procedures

and Documentation

03. 1

Off-Normal 0 eratin

Procedures

Annunciator

Res

onse

Summaries

71707

During system walkdowns documented

in this report

and in IR 96-04, the

inspectors identified

a number of deficiencies

in ONOPs which described

actions to be taken

on the part of operators,

and included information

to help diagnose

problems,

when annunciators

alarmed.

The inspectors

reviewed the individual findings from the two IRs and summarized

the

findings in the table below.

System

Unit

1

CS

Unit 2

CS

Unit

1

ICW

Unit 2

ICW

Safety System Total

Unit

1 IA

Unit 2 IA

All Systems Total

ONOP

Set oints

10

15

ONOP

Other

18

24

"ONOP Setpoints,"

as referred to in the table,

are differences

between

the setpoint for a given annunciator,

as defined in the

ONOP,

and the

TEDB,

a design

document which contained setpoints for each instrument.

"ONOP Other,"

as referred to in the table,

are cases for which other

attributes of a given response

summary were incorrect.

Attributes in

this case

included'wrong specified

sensing

element,

wrong

CWD reference,

and wrong specified operator action.

14

06

If one

assumed

that the annunciator

response

summaries

were, at one

time, correct,

the errors identified would tend to imply weaknesses

in

.

the configuration control process,

as ongoing changes

to the plant were

not factored into procedures.

The inspectors

examined the licensee's

configuration control process,

and initial conclusions

are provided in

paragraph

E.7. of this report.

Weaknesses

in annunciator

response

summaries

have

been identified both

by the

NRC and the licensee for some time.

In response,

the licensee

dedicated

an individual to rewriting and verifying the summaries.

The

effort was estimated

by the licensee to take two man-years.

With the

exception of those

items described

in paragraphs

E.7, the deficiencies

totaled in the table

above were

deemed

as not representing

violations of

NRC requirements,

as requirements for these

instances

are,

under TS,

applicable only to safety-related

annunciators.

With very few

exceptions,

annunciators

at St. Lucie are non-safety related.

Consequently,

the errors

noted were

deemed to represent

a weakness

in

operations

procedures.

Operations

Organization

and Administration

On April 4, the licensee

announced

the reassignment

of J.

West,

Operations

Hanager,

to the outage

management

organization.

Hr. West was

replaced,

on an interim basis,

by Hr. H. Johnson,

previously Operations

Hanager at Turkey Point.

Additionally, the licensee

announced that

an augmented

gA effort was

being initiated to support the Unit

1 refueling outage

and that

a

Hanagement-on-Sh'ift

effort was being initiated which would station

FPL

management

observers

in the plant's control

rooms to observe

operator

performance

in the areas of conduct of operations

and procedural

adherence.

08

08.1

Hiscellaneous

Operations

Issues

S ent Fuel

Pool Current Licensin

Bases

Review

On Harch

26 and 27, the

NRC St. Lucie Project Hanager

performed

an audit

on both St. Lucie Units'ompliance with the current licensing basis

regarding the spent fuel pool

and core offload activities.

Details of

the findings are in Attachment

1 (Spent

Fuel Storage

Data Tables).

No

discrepancies

were found at either unit.

However the licensee

has

stated that they intend to complete several

administrative

improvements.

These included:

~

Unit

1

Haintaining

SFP temperature

below 150'F - the licensee

intended to have

a procedure

in place prior to the

outage similar to Unit 2 procedure

OP 2-1600023,

Rev

58,

page

26 of 69.

The inspector verified that

OP 1-

1600023,

Rev 59, "Refueling Sequencing

Guidelines,"

included,

as step 1.C.3,

a verification that fuel pool

15

~

Unit

1

~

Unit

1

II. Maintenance

temperature

was less

than

140'F prior to off-load.

This change

was in place prior to the Unit

1 outage.

Maintaining

a minimum boron concentration

of 1720

ppm

in the

SFP - the licensee

intended to have

h procedure

in place prior to the outage.

The inspector verified

that

OP 1-1600023,

Rev 59, "Refueling Sequencing

Guidelines,"

as step 1.F, included

a verification that

boron concentration

was greater

than or equal to 1720

ppm prior to offload.

This change

was in place prior

to the Unit

1 outage.

Preparing

and producing

a heat load calculation to

verify the SFP's ability to accept

a full-core

offload.

The calculation could not be located during

the audit.

The inspector verified that this

calculation

(the results of which were included in

PC/H 054-196)

had

been prepared

and approved prior to

the Unit

1 refueling outage.

H1

Conduct of Maintenance

Ml. 1

Observation of In- rocess

Corrective Maintenance Activities

The inspectors

observed

maintenance activities

on the components listed

below to determine if the activities were conducted

in accordance

with

regulatory requi'rements,

technical specifications

(TS), approved

procedures,

and appropriate

industry codes

and standards.

H1.2

Observation of Valve Packin

and Modification

62700

The inspectors

observed

portions of valve repacking

and modification

activities to verify that the maintenance

and modification activities

were performed in accordance

with the applicable

procedures

and work

orders.

The procedure

used

was M-0043,

Rev 17, "Valve Packing."

The

inspectors

observed portions of the following valve maintenance

or

modification activities.

Valve

No.

Val ve

Function

Location

W/0 or Procedure

Used

Activities

1403

1405

1200

MV-02-2

.Isolation

Pressurizer

Isolation

Pressurizer

Safety

Pressurizer

Isolation

Charging

Pump

Discharge

M-0043

M-0043

PWO 61/3604

H-0043

Packing

Packing

Modification

Packing

Safety Relief Valve 1200

had previously been identified to be leaking.

The repair included replacement of the valve stem,

but the licensee

16

could not procure

an identical

stem.

Therefore,

the licensee

enlarged

the valve stem hole for a larger stem.

The modification process

and

requirement for a liquid penetrant

exam1nation

were stated

in work order

PWO 61/3604.

The inspectors

determined that all the valve repackings

and the modification stated

above were performed in an acceptable

manner.

Work Order:

95-02643-01C

Jack

and

La

New Pressurizer

Safet

Valves

62703

Due to seat

leakage

problems

experienced

with the previous design

pressurizer

safety valves,

FPL elected to replace these

valves with a

new, forged body, design

which accommodated

a flexi-disc seat

enhancement.

During site verification nitrogen seat set pressure

and

bubble tests

conducted

in accordance

with Work Order 95-026432-01B,

Crosby's Technical

Manual 8770-5460,

Rev 10,

and

HP H0017,

Rev 33, two

of the

new valves, Serial

Nos.

N84217-00-0002

and N84217-00-0004 failed

to pass

the seat leak test.

As a result,

the valve bonnets with the

valve internals for the two valves that failed were required to be

disassembled

from the valve body so the valve seats

could be .lapped.

From Hay 6-8, the inspector

observed

the "Jack and Lap" activities

conducted

in accordance

with

PWO 95-02643-01C

by a Crosby Valve and

Gage

Company representative,

FPL maintenance

personnel

and site engineering.

The inspector

also observed that the retest of both valves

was conducted

in accordance

with

PWO 95-026432-01B

and

HP M0017.

The valve retests

were satisfactory

and all work activities observed

were conducted

in

accordance

with the approved written instructions

by knowledgeable

personnel.

WO 95028905-01

Clean

Com onent Coolin

Water Heat

Exchan er

62703

On May 8, the inspector

observed

maintenance

personnel

performing heat

exchanger

tube hydrolazing operations

on Component Cooling Water Heat

Exchanger

lA in accordance

with

PWO 95-028905-01.

During review of the

work package for this cleaning

and repair activity the inspector noted

that the information copies of the control procedures

had not been

verified as the correct revision with the control document, initialed,

and dated

as required

by Document Control

Procedure

gI 6-PR/PSL-1.

The

procedures

involved were HMP-14. 1,

Rev 6,

"Component Cooling Water Heat

Exchanger

Cleaning

and Repair,"

GMP-02,

Rev 13,

"Use of H&TE By

Mechanical

Maintenance,"

and

HP H-0064,

Rev 1, "High Pressure

Hydro-

Blasting of Heat Exchanger

Tubes

and Associated

Equipment."

The

inspector subsequently

verified that the procedures

in question

were in

fact, the correct revision.

However,

upon being notified,

FPL

maintenance

supervision

personnel

stopped all work on the Component

Cooling Water Heat Exchanger until the cause of this discrepancy

could

be determined.

Corrective actions

included replacing the lead

maintenance

technician

on this job and conducting briefings with

maintenance

personnel

on all shifts to ensure that outage

maintenance

personnel

knew they were personally responsible for ensuring

work was

conducted

in accordance

with current revision of procedures

and that

procedures

were stamped,

signed,

and dated

as required.

This failure

17

constitutes

a violation of minor significance

and is being treated

as

a

Non-cited Violation consistent

with Section

IV of the

NRC Enforcement

.

Policy.

The

NCV was identified as

NCV 335/96-06-02,

"Failure to

Document Verification of Current Procedure

Revisions."

Maintenance

and Haterial Condition of Facilities and Equipment

OP 1-0400050 "Periodic Test of the

En ineerin

Safe uards

Features"

61726

On Hay 2, the inspector attended

the infrequent test briefing given by

the Hanagement

Designee

and Test Specialist prior to the performance of

integrated

safeguards

testing

on Unit 1.

The overview portion of the

brief discussed

the purpose of the test

and emphasized

the importance of

using

STOP principles, i.e., Stop-Think-Operate-Prove.

All individuals

involved in the test then divided into groups for a detailed specific

test brief.

The inspector concluded that the brief was thorough

and

covered the necessary

items.

At approximately

11:30 a.m., all test personnel

were on-station

and the

safeguards

test

commenced.

Shutdown cooling was secured

and lineups

performed prior to inputing an

ESFAS signal concurrent with a

LOOP.

When the

LOOP was initiated by opening both startup transformer output

breakers,

operators

observed that the

1B

EDG started,

however,

the

EDG

output breaker failed to close.

The

ANPS immediately brought this

failure to the attention of both the Test Specialist

and

Management

Designee.

The Management

Designee directed the

ANPS to place

shutdown

cooling back-in-service

and restore offsite power.

To provide

as

much

information as pbssible for troubleshooting,

no attempt

was

made to

close the

1B

EDG output breaker.

Operators

took timely and appropriate

action in response

to a loss of the operating

instrument air compressor

which with degraded

instrument air pressure

caused

the

AOV FCV-3306

"SDC

return valve" to fail in the full open position.

This limited the

amount of RCS flow which could

be directed to the

SDC heat exchangers.

Operators

entered

the applicable Off-Normal Operating

Procedures.

Within minutes,

the 480

VAC AB swing bus

was realigned to the

A

electrical

side which allowed operators

to restore

instrument air.

By

approximately

12:44 p.m., operators

had restored offsite power.

The

safeguards

test

was secured

and exited at 1:29 p.m.

The inspector

judged operator

response

and support

by maintenance

as good.

The licensee

performed troubleshooting of the

1B

EDG output breaker

and

associated

circuitry throughout the day.

The root cause for the failure

was determined

to be

a failed relay in the bus undervoltage circuit.

The failure of the relay resulted

in a failure to satisfy

bus

undervoltage

interlocks required for the

EDG output breaker to close

onto the

1B3 bus.

The licensee

recommenced

testing the evening of Hay 2.

The inspector

witnessed

the conduct of the

LOOP/SIAS portion of the test.

Operator

performance

was found to be very good, with clearly centralized

command-

18

and-control

maintained

by the Unit ANPS.

Communications

were

formal,'nd

repeatbacks

were consistently

used.

The observed

portion of the

test produced satisfactory results.

Overall, the inspectors

found the coordination

and execution of the

observed portions of this test to be excellent.

Polar Crane Testin

Unit

1 Reactor Vessel

Head Lift

62700

The inspectors

reviewed the adequacy of load testing for the polar crane

(to verify that the maximum lifting load would not exceed

the maximum

rated load)

and subsequently

observed

the reactor

head lift.

Procedures

and documents

reviewed for both the polar crane testing

and reactor

head

lift were the following:

CR 96-613,

Rev 0, "Evaluation of Polar Crane

Load Test"

Procedure

1-LOI-HH-45, Rev 4, "Unit 1 Reactor Containment Building

Polar Crane

Load Test of Hain Hoist Gear

Box to 125 percent of

Rated

Load"

Procedure

1-M-0015,

Rev 27, "Reactor Vessel

Haintenance

- Sequence

of Operations"

The polar crane in the reactor building is used for the removal

and

installation of the reactor

head

and related parts.

The original rated

capacity for the polar, crane

was 350,000 lbs for the main hoist.

Recently,

the licensee identified problems with the polar crane gear

box

and decided to rhplace it.

ANSI B30.2 requires that the polar crane

with the replaced

gear

box be retested for load capacity.

Two tests

were performed.

In the first test,

the vendor scale

read 435,000 lbs;

but the scale

on the main hoist scale

read 356,000 lbs.

Because of the

discrepancy

in scale readings,

the licensee

had the vendor scale

sent to

a lab for verification.

The vendor scale

was determined to be reading

too high and

needed to be calibrated.

The final calibrated

load was

similar to the polar crane

main hoist reading.

In accordance

with ANSI

B30.2Property "ANSI code" (as page type) with input value "ANSI</br></br>B30.2" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., the licensee

used

80 perce'nt

(280,000 lbs) of the 350,000 lbs

reading

as the rated load.

The licensee

wanted to take full advantage

of the rated loads for the

crane

and performed

a second test.

The second test

was terminated

prematurely

because

a refilling hose for the water

bag test load was

broken.

The final reading for the scale before the hose

broke was

357, 180 lbs.

The licensee

used

80 percent

(285,744 lbs) of the tested

load

as the maximum rated load to lift the reactor

head.

In preparation of the reactor

head lift, the li'censee's

engineers

reviewed the previous loads lifted for the reactor

head

and identified

that the loads

were between

280,000

and 320,000 lbs for the reactor

head

and related

items

such

as bolts, nuts,

lead shielding, shielding support

frame, etc.

The engineers

also reviewed

CE Instruction Hanual

8770-

12276,

Rev 0, entitled "Hajor Component Lifting/Lowering Interfaces for

19

Reactor

Vessel

Head Upper Guide Structure,

ICI plate;

Core

Support'arrel

for the Florida Power

and Light Company,

St. Lucie Unit 1," which

stated that the estimated

load

on the crane for the reactor vessel

head

lift was 267,968 lbs.

From the sketches

included in the manual,

the

licensee

engineers

concluded that this weight included the

head

and the

lift device (tripod) but did not include the studs or lead shielding.

The licensee's

engineers

removed

as

many miscellaneous

items

as

practical prior to lifting the reactor

head to ensure that the rated

capacity of the polar crane would not be exceeded

during the lift.

The inspectors

observed

the preparation of the reactor

head,

removal of

the miscellaneous

items,

and installation of the lifting device

(tripod).

During the reactor

head lifting, the inspectors

observed that

the head

was effectively lifted and lowered onto three cribbings

on the

floor to support the reactor

head.

The maximum load cell reading during

the lift was 255,570 lbs.

The inspector determined that the preparation

and lifting of the reactor

head

was acceptable

and met all requirements.

Document

Review of Main Steam Safet

Valve Set ressure

Testin

62700

The licensee

completed setpressure

testing for 16 Hain Steam safety

valves for Unit

1 during the early part of the refueling outage..

The

procedures

used for the testing

and calibration of HLTE were:

GHP M-0705,

Rev 27,

"Hain Steam Safety Value Maintenancy

and

Setpressure

Testing"

gI-12-PR/PSL-l,

Rev 21, "Calibration of Measuring

and Testing

Equipment"

gI-12-PR/PSL-2,

Rev 20, "Control

and Calibration of Measuring

and

Test Equipment

(H&TE)"

The inspectors

reviewed

16 packages

of testing records

and found that

all of them met the requirements

of Procedure

GMP H-0705 and were

acceptable.

The

16 valves were divided into train "A" and "B" as

shown

below:

Train A

Train

B

Valve No.

8201,

8202,

8203,

8204

8205,

8206,

8207,

8208

8209,

8210,

8211,

8212

8213,

8214,

8215,

8216

The required records

and data for the setpressure

testing

are contained

in Appendix B, "Determining Safety Valve Setpressure

with Air

Setpressure

Device," of GHP M-0705.

The MME used

For testing the main steam safety valves included

a

Ten valves,

8203 to 8208 and 8213 to 8216,

as listed in

CR 96-597,

were

found to have

a setpressure

outside the acceptable

boundaries

during the

first test

and required evaluation for tolerance

change

based'on

fuel

analysis.

The acceptable

ranges

were defined

as

a

1 percent of

midpoints

985 psig or 1025 psig.

20

H3

specific pneumatic motor and several

pressure

gauges.

The calibration

for the motor and most of the gauges

in the pre-calibration

occurred

one

week before work started

and in the post-calibration

one or two days

after the work was completed.

The exception

was the pre-calibration for

gauges

M-222 and M-288 six months prior to use.

The inspectors

questioned

the licensee

as to the pre-calibration validity for these

two

gauges.

The licensee

explained that the pressure

gauges

had not been

used since the last calibration

and the effective calibration date

had

not expired.

Thus the previous calibration was still valid and could be

used

as

a pre-calibration.

The inspectors

concurred in the licensee's

explanation

and verified that all the gauges

had post-calibration

immediately after the tests

were completed

and that all the gauges

were

found to be within the allowable range

and acceptable.

The inspectors

also reviewed the

H&TE checkout log and history for the pressure

gauges

used in the testing

and identified that gauges

H-222 and M-288 had not

been

used since October

15,

1995 when they were post-calibrated.

The

inspectors

concluded that the licensee

performed

adequate

setpressure

tests for the main steam safety valves

and used validated pressure

gauges for this test.

Maintenance

Procedures

and Documentation

M3.1

Inservice

Ins ection

ISI

Unit

1

73052

The inspector

reviewed documents

and records,

and observed activities

as

delineated

below to determine

whether

ISI activities were conducted

in

accordance

with applicable

procedures,

regulatory requirements,

and

licensee

commitments.

The inspector's

objective

was to examine the

licensee's

steam'enerator

examination

and evaluation activities

and the

10-year ultrasonic examination of the reactor vessel.

The applicable

code for this ISI is the

ASME B&PV Code,

Section XI, 1983 Edition with

Summer

1983 Addenda.

St Lucie Unit

1 is presently in the first outage

of the third 40 month period, of the second

10-year

ISI interval.

This

is the thirteenth refueling cycle for Unit 1.

Eddy current acquisition activities were conducted

by ABB/Combustion

Engineering.

Primary analysis of eddy current data

was conducted

by

Zetec in Issaquah,

Washington,

and the secondary

analysis

was conducted

by ABB at the Florida Power

and Light NDE Laboratory in West

Palm Beach,

Florida.

The Unit 1, 10-year Reactor Vessel

examinations

were conducted

by Southwest

Research

Institute (SwRI).

H3.1.1

Review of Procedures,

Guidelines,

and Licensee

Documents

The following documents

were reviewed

by the inspector during the

assessment

of ISI activities.

FPL Eddy Current Examination

Procedure

NDE 1.3,

Rev 8,

Entitled:

Eddy Current Examinations of Non Ferromagnetic

Tubing Using Multi-Frequency Techniques

HIZ-18/HIZ-30

21

FPL Document CSI-ET-96-11,

Rev A, Unit

1 Steam Generator

Eddy Current Examination

Plan

FPL Letter of Response

to

GL 95-03,

Dated June

23,

1995

FPL Safety Evaluation JPN-PSL-SENP-95-112,

Rev 1, Entitled:

Cracking of Westinghouse

Alloy 600 Mechanical

Steam

Generator

Tube Plugs

PC/N 125-195M,

Rev 1, Entitled:

Steam Generator

Tube

Plugging

and Plug Repair

St.

Lucie Unit

1 Eddy Current Data Analysis Guideline

and

Performance

Demonstration,

Dated

Hay 1996

SwRI Procedure

SLC-AUT-14,

Rev 1,

Change

1, Entitled:

Automated Ultrasonic Inside Surface

Examination of Pressure

Piping Welds

SwRI Procedure

SwRI-AUT2, Rev 9,

Change

1, Entitled:

Automated Ultrasonic Inside Surface

Examination Indication

Resolution

and Sizing

SwRI Procedure

SLC-AUT15, Rev 2,

Change

1, Entitled:

Automated Ultrasonic Inside Surface

Examination of Ferritic

Vessels

Greater

Than 4.0 Inches in Thickness

U

FPL Document

PSL-100-AOA-95-1,

Rev 0; Dated April 5,

1995,

Entitled: Request

For Authorization of Alternative

Examination

NRC Safety Evaluation of FPLs Request for Authorization of

Alternative Reactor

Pressure

Vessel

Examinations

For St.

Lucie Plant, Unit

1

SwRI Procedure

SLC-PDI-AUTI, Rev 0,

Change

1, Entitled:

Automated Ultrason'ic Inside Surface

Examination of Ferritic

Vessel

Wall Greater

Than 4.0 Inches in Thickness

SwRI Procedure

SLC-PDI-AUT2, Rev 0,

Change

1, Entitled:

Automated Inside Surface Ultrasonic Flaw Evaluation

and

Sizing

The inspector's

review of the above

documents

revealed

they were

in accordance

with the applicable

ASME Code,

Technical

Specifications,

licensee

commitments,

and industry guidelines.

In

addition, the inspected

noted that, the licensee's

augmented

eddy

current examination plan, plug-a-plug tube plugging activities

and

alternative reactor pressure

vessel

examinations

revealed

good

outage planning

had

been

performed

and component safety should

be

enhanced,

based

on these

defensive barriers.

22

Observation of Steam Generator

Eddy Current Acquisition and Steam

Generator

Plug-A-Plug Repair Activities (73753) Unit

1

From Hay 6 until Hay 9, the inspector

observed

portions of the

licensee

eddy current data acquisition

and the Westinghouse

tube

plug cleaning activities.

These activities were conducted

in

accorda'nce

with .the approved

procedures

delineated

above

and the

FPL Examination Plan.

Review of SwRI Ultrasonic Examiner Performance

Demonstration

Records

at the Electric Power, Research

(EPRI) In Charlotte

N.C.

On Hay 10, the inspector

and

a representative

from FPL frisited the

EPRI

NDE Center to review the performance

demonstration

examination results for the four SwRI data analysts that would be

used

by FPL to examine the Unit

1 reactor

vessel.

This review was

necessary

because

FPLs relief request entitled "Request for

Authorization of Alternative Examination Hethods," which was

applicable for Unit

1 reactor pressure

vessel

welds

and which had

limiting conditions that prevented

100 percent

examination

coverage,

had two alternative

examinations

proposed

by the license

that

had changed

since

NRC had approved the relief request.

The first change

was that the licensee

had initially stated that

a

full vee 45'hear

wave examination

would be performed to the

extent practical to compensate

for recorded limitations.

However,

the current

SwRI examination

procedures

did not have this

examination

method in them.

The second

change to the April 1995

Relief Request

stated that

FPL would employ (as they became

available) additional examinations,

inspections

and/or techniques

that would provide

a substantial

increase

in the examination of

areas currently missed

under the current examination techniques.

To comply with their commitment to employ examination techniques.

that provide

a substantial

increase

in the examination of weld

areas currently missed,

FPL had

SwRI qualify to the performance

demonstration

examinations

conducted

by the

EPRI

NDE Center for a

single side weld access

examination.

These examinations

are

conducted

in accordance

with Appendix VIII of later editions of

the

ASHE Code.

The editions of the

Code which include Appendix

VIII have not been

approved for use

by NRC at this time.

The

applicable

ASHE Section XI Code presently requires that

a weld be

examined

from two directions

(both sides of a weld).

Therefore,

to supplement

the Unit

1 Reactor Vessel

examinations with these

new alternative techniques

the licensee

invoked paragraph

IWA-2240

of the applicable

ASHE (ode which stated that "alternative

examination

methods,

or newly developed

techniques

may be

substituted for the methods specified provided the inspector

(the

Authorized Nuclear Inspector) is satisfied that the results

are

demonstrated

to be equivalent or superior to those of the

specified method."

23

Although the ANI had approved the single side weld examination

techniques,

the inspector

had the following questions

concerning

the single side weld access

test parameters

and the examiner's

performance.

How many of the defects were'n the test blocks were

on the

far side of the weld?

Was the depth location of the defects

represented

on both

sides of the weld?

How many of the far side weld defects

were notches

verses

cracks?

What was the effective focal length of the

SwRI Duplex Send

and Receive transducers?

How effective

had the

SwRI examiners

been during their

qualification effort on the far side weld indications?

Could an examiner

pass the test

and miss

one or more far

side weld indications?

Detection Criteria delineated

in Paragraph

8. 1.(2)(b) of

SwRI Procedure

SLC-PDI-AUTl stated that "if an indication

cannot

be confirmed with at least

2 channels, it will be

considered irrelevant."

SwRI one sided examinations will

only have two channels

active, representing

two different

exam1nation

angles.

Far sided weld indications should

be

oriented at

a slightly different angle than near side weld

indications

because

defects

tend to follow the weld heat

affected

zone

on both sides of the weld.

Is it logical to

presume that

100 percent detection capability will be

achieved with both angle

beam transducers

on indications

when weld location

and defect orientation differ?

EPRI's

Performance

Demonstration Administrator reply to the

inspector's first question

was that there

was

no weld in the test

blocks

used for the single side access

weld qualification test.

EPRI's position was that the weld would not make

a significant

difference in the ability to detect or size indications in the

carbon steel

reactor vessel.

The inspector

however,

was concerned

that the acoustical

differences

between the vessel

base material

and the weld,

and the defect orientation differences

had not been,

at least analytically defined

and factored into the difficultlyof

the performance

demonstration test.

Therefore,

the performance

test

may not be ultrasonically representative

of the reactor

vessel

welds.

24

Discussions

with EPRI personnel

and review of documents

and

examiner test results satisfactorily resolved the questions listed

above other than those that related to the failure of the test

sample to include

a weld.

On Hay,13,

the inspector returned to the St. Lucie facility to

continue his examination of inservice inspection activities.

At

that time, the inspector

addressed

this concern with the

appropriate

licensee

management

personnel

and determined

the

licensee position on this matter.

Continuation of the inspection

will be reported in

NRC IR 96-08.

H8

Miscellaneous

Maintenance

Issues

H8.1

, Closed

VIO 389 95-01-02

"Failure to Follow Procedure

2-LOI-T-89

ara ra

h 4.a.4"

92902

The inspector

reviewed the licensee's

corrective actions related to the

subject violation.

The violation described

the licensee's

failure to

follow procedure

2-LOI-T-89 in February,

1995, which resulted

in'econnecting

switched electrical

leads to E/P 2110(.

An inadequate

independent verification failed to identify the discrepant

condition.

This caused

a loss of letdown flow when LCV-2110( did not open after it

was returned to service

and required charging

be temporarily secured

until the redundant

level control

was placed in service.

The inspector verified that corrective actions to avoid further

violations were completed.

STARs 950119,

950339,

950341,

and 950342 were

issued to document corrective actions.

The new Administrative

Procedure,

ADH-17.06,

Rev 0, "Independent Verification" was issued April

4,

1995.

The inspector

reviewed training department

records

and

verified that Maintenance

Personnel, i.e.,

I&C, Electrical,

and

Mechanical disciplines,

completed training on this event

and that both

I&C and Electrical

completed training on the requirements for

independent verification (Mechanical did not perform independent

verification and, therefore,

did not receive training in this area).

.

All disciplines incorporated

the

STOP principles into the on-the-job

training/task performance

evaluation portion of the Maintenance

Continued Training Program.

Technical staff and Operations

did not receive training on this event or

Independent Verification as part of these corrective actions.

Operations

incorporated training on independent verification into their

routine requalification training program.

This violation is closed.

25

III. En ineerin

E2

E2.1

Engineering Support of Facilities

and Equipment

HVS-4A Motor Re lacement

37551

On April 6, Unit 2

RAB main supply fan HVS-4A experienced

a failed motor

inboard bearing which tripped the motor, alerting operators

to the

condition.

The licensee

entered

the action statement

of TS 3.7.8,

which

required that the inoperable ventilation train be restored

to operable

status

or that the unit be shut down.

As the licensee

had

no replacement

motor

on site, multiple corrective

actions

were pursued

which included finding a direct replacement

and

repairing

and rewinding the existing motor.

The licensee

pursued

parallel

paths to resolve the issue.

The licensee

located

a safety related

replacement

motor,

however,

the

motor was not qualified for a harsh radiation environment,

as required

by design.

The licensee

implemented

a plan to install the subject motor

and to erect

a shield wall between the motor and the Unit 2 shield

building ventilation system filters which were responsible

for the

majority of the predicted

dose to the motor.

The subject modifications

were conducted

under

10

CFR 50.59.

The inspector

reviewed JPN-SPSL-96-0130,

"10

CFR 50.59 Safety Evaluation

for Temporary

Use of Non-Eg Motor for RAB Supply

Fan HVS-4A," which was

approved

on April 10.

The

SE considered

the compatibility of the

new

motor to the application,

the required shielding design,

and the seismic

considerations

for the shielding installation.

While differences

existed

between

the motors,- the

SE found the replacement

to be

acceptable.

The inspector

compared the two motors'haracteristics

and

compared the

new motor to the specifications

in Equipment gualification

Documentation

Package

299-A-451-4.7,

Rev 1.

No deficiencies

were

identified with the licensee's

determination of the interchangeability

-of the motors (with the radiation shield installed).

Upon testing of the

new motor, the licensee

found that the motor's

supply breaker tripped

on the first start following the rotational

check

run.

The cause

was attributed to higher,

more prolonged, starting

cur rents

drawn by the

new motor by virtue of increased

efficiency 'in the

design.

The inspector

noted that the licensee's

SE evaluation

had

concluded that,

as the operating currents of the two motors were

identical,

no effects

on breaker settings

were required.

Revision

1 to

the

SE was subsequently

issued

which stated that the

Long Time Delay

setting of the breaker trip function may be increased

such that

approximately

10 seconds

would be allowed for starting currents to

subside.

The inspector witnessed

subsequent

testing

and verified proper

fan rotation

and the absence

of breaker trips.

The inspector

concluded

that the original

SE had inadequately

considered

the starting

characteristics

of the

new motor.

26

The inspector

reviewed the Procurement

Engineering evaluation of the

new

motor's vendor data.

The licensee

found that the vendor evaluation of

the motor's bearing rating did not consider the specific installation

arrangement

of the motor.

The vendor's evaluation

considered rotor

weight and seismic factors in establishing that bearing loading was

acceptable.

The licensee's

installation required the consideration

of

loading due to

a series of fan belts driven by the motor (changing

radial loading from the vendor's

assumption).

The loading was

reevaluated

by the vendor,

considering

the specifics of the application

and was found to be acceptable.

The inspector

found the licensee's

review of vendor data to be detailed

and effective in identifying this

concern.

E4

E4.1

, Concurrent with the acquisition of the

new motor, the licensee

forwarded

the old motor to Tampa Armature, with whom the licensee

had previously

established

a process for rewinding and repairing safety-related

motors

through its Procurement

Engineering organization.

Work on the motor was

completed

and the. motor arrived

on site

on April 12.

By this time, the

replacement

motor had

been installed

and was in the final phases

of

testing

and qualification.

However, in pursuing this parallel path,

the

licensee

demonstrated flexibility and timeliness in having

a second

motor available

should problems

have developed

in the replacement

motor.

The installation of the motor and shield wall were completed,

and the

fan returned to service

on April 13, allowing the licensee to exit the

subject action statement.

The inspector

concluded that the licensee's

organizations

had

been effective at addressing this failure and that

good prior planning,

including the development of multiple success

paths,

resulted

in avoiding

a TS-required

shutdown.

Engineering Staff Knowledge and Performance

Failure to Prom tl

Document

Nonconformance

37551

On April 29, the inspector reviewed

CR 96-589,

which documented

the fact

that containment air conditioning, recently employed

by the licensee

in

outages

on -both units,

had resulted in containment

temperatures

which

were lower than those

assumed

in instrument calibration uncertainty

analyses.

The

CR reported that reviews of strip chart data for

containment

temperatures

during the outages

had indicated that

temperatures

had

been

as low as 70'F,

whereas calibration temperature

had

been

assumed

to be no less

than 80'F.

The inspector

noted that the

CR had

been presented

to and signed

by the

NPS who, programmatically,

was to consider the

CR for oper ability

concerns.

However,

no list of affected

instruments

was included in the

CR.'he inspector

asked

the licensee

how the

NPS could have

made the

operability determination without more data,

to include the individual

affected

components.

- The licensee

stated that the

CR originated in

engineering

and that engineering

personnel

had performed

an evaluation

prior to preparing the

CR.

The evaluation

had determined that adequate

27'argin

existed in the uncertainty analyses

to accommodate

the noted

reduced

temperature.

The inspector obtained

a copy of the subject evaluation

and noted that

the affected

instruments

included

35 Unit

1 instruments

and

39 Unit 2

instruments,

many of which provided inputs to the

RPS

and

ECCS systems.

The evaluation

documented

the results of calculations

and evaluations

made to justify the continued operation of these

instruments with

calibration temperatures

as low as 70'F.

While the evaluation

concluded

that the operability of the affected instruments

was not challenged,

no

quantitative information was provided.

The inspector discussed

the issue with the licensee

and found that the

condition (the temperature disparity) was'dentified

approximately

10

days prior to the initiation of the

CR.

10 CFR 50, Appendix B,

Criterion XVI, "Corrective Action," specifies that measures

shall

be

established

to assure that conditions

adverse

to quality, such

as

nonconformances,

will be promptly identified and corrected.

The

glossary of the

FPL guality Assurance

Manual

(an attachment to the

Topical guality Assurance

Report, defines

a nonconformance

as

a

"...deficiency in characteristic,

...documentation,

or procedure

which

renders

the quality of an item unacceptable

or indeterminate."

The

inspector concluded that the subject temperature

discrepancy constituted

a deficiency in characteristic

which rendered

the calibration

(setpoints) of numerous safety related

instruments

indeterminate.

The inspector

reviewed

IP-803,

Rev 3, "Implementation of Condition

Reports at Juno Beach,"

and IP-805,

Rev 0, "Condition Reports."

The

inspector

noted 'that both procedures

contained

guidance

which included

"...Any individual who becomes

aware of a problem or discrepant

condition should take immediate actions that they are qualified to take

and initiate

a Condition Report..."

Additionally, IP-803 included, in

step 5.1.2.2.3(l)A "In all cases if an operability assessment

is

required the

CR should

be transferred

to the appropriate site..."

IP-

805, Appendix 2, contained

examples of conditions requiring the

origination of a CR.

Example 6, "Discrepancies

Associated with Alarms,

Setpoints,

Calibration," required

a

CR for "Conditions that may affect

equipment operability."

As

a result of these

procedural

requirements,

the inspector

found that

a programmatic

weakness

did not exist regarding

requirements

to document the subject

nonconformance.

The inspector

concluded that the licensee failed to identify the subject

nonconformance

in

a timely manner,

as required

by 10 CFR 50 Appendix B,

the licensee's

Topical guality Assurance

Manual,

and

IP-803

and IP-805.

However, the inspector

concluded that this was the result of an

individual failure,

as

opposed to

a programmatic

one.

Additionally, the

inspector

noted that the conditions which constituted

the nonconformance

were licensee identified and were aggressively

addressed.

This failure

constitutes

a violation of minor safety significance

and is being

treated

as

a Non-Cited Violation, consistent with Section

IV of the

NRC

Enforcement Policy

(NCV 335,389/96-06-03,

"Failure to Promptly Document

28

E7

E7.1

Non-Conforming Conditions" ).

guality Assurance

in Engineering Activities

0 en

Unresolved

Item 335 96-04-05

37551

URI 96-04-05

documented

a number of findings observed

during system

walkdowns in March that suggested

a potential configuration control

weakness.

In order to determine

whether or not

a programmatic

weakness

existed,

the inspectors

expanded

the walkdowns to include the

ICW

systems for both units.

After completing the

ICW system walkdown and

reviewing the results of previous

IA and

CS system walkdowns, the

inspectors identified

a design control issue.

On April 18, the inspector discussed

with engineering

the numerous Unit

1

ICW discrepancies

between

the

UFSAR, Engineering

Drawings,

and

PC/M

341-192

(which modified the

ICW pumps'ubrication

sources).

On April

23, the licensee

performed

an as-built configuration check at which time

it was determined that flow limiting orifice SO-21-5A on Unit

1

ICW.

Header

A CW Pump supply line was not installed

(IHE 96-035).

SO-21-5A

and

5B were two orifices installed

by this

PC/M on both

ICW headers

to

limit the non-safety related

ICW flow to the

CW pumps should the non-

seismic piping fail during

a DBE.

The licensee

issued

Equipment

Qearance

number 1-96-04-369 which realigned

ICW header

B

CW pump flow

to all

CW pumps

and isolated the

ICW header

A CW pump supply line.

The

licensee

performed

an operability assessment

(CR 96-554) which

concluded'hat

the

ICW system

was still within the design flow limits.

The

inspector

reviewed the subject

CR and found the results acceptable..

An investigation

by the licensee

was unable to definitively conclude

whether the orifice plate

had not been installed during the design

modification or had not been reinstalled during

a subsequent

maintenance

activity which replaced

a portion of piping.

The inspector

concluded

that the failure to ensure that the flow limiting orifice SO-21-5A was

installed

was

a configuration management

control problem.

This licensee

identified and corrected violation is being treated

as

a Non-Cited

Violation consistent

with Section VII.B.1 of the

NRC Enforcement Policy

(NCV 335/96-06-04,

"Unit

1

ICW Flow Orifice Found Hissing" ).

Three

PC/Ms reviewed

by the inspector during system walkdowns were not

properly implemented:

~

PC/M 109-294

On January

6,

1995, the licensee

closed out

PC/M 109-294 [Setpoint

change to the Hydrazine

Low Level Alarm (LIS-07-9)] without

assuring that affected procedure

ONOP 2-0030131,

"Plant

Annunciator Summary,"

was revised.

This resulted

in the summary

for annunciator

S-10,

"HYDRAZINE TK LEVEL LO," showing

an

incorrect setpoint of 35.5 inches.

29

~

PC/H 268-292

On February

14,

1994, the licensee

closed out

PC/H 268-292

[ICW

Lube Water Piping Removal

and

CW Lube Water Piping Renovation]

without assuring that affected

procedure

ONOP 2-0030131,

"Plant

Annunciator

Summary,"

was revised.

This resulted

in the

summary

for annunciator

E-16,

"CIRC WTR PP

LUBE WTR SPLY

BACKUP IN

SERVICE," incorrectly requiring operators verify the position of

valves HV-21-4A 5 4B following a SIAS signal

using control

room

indication.

These valves

no longer received

a SIAS signal,

were

deenergized,

and

had

no control

room position indication.

~

PC/H 341-192

On Hay 16,

1994, the licensee

closed out

PC/H 341-192

[ICW Lube

Water Piping Removal

and

CW Lube Water Piping Renovation].

The

as-built

Dwg. JPN-341-192-008

was not incorporated

in Dwg. 8770-G-

082,

"Flow Diagram Circulating and Intake Cooling Water System,"

Rev ll, sheet

2, issued

May 9,

1995, for PC/H 341-192.

This

resulted

in Dwg.

No 8770-G-082 erroneously

showing valves

I-FCV-

21-3A L 3B and associated

piping still installed.

In a majority of the cases,

the Engineering

Package

did not specifically

identify which documents

required updating

and in all cases

there

was

no

indication that

an as-built verification of drawings or procedures

was

either required or performed prior to closeout.

The inspector

identified this as

a weakness

in implementing

PC/Hs which failed to

assure

the correct translation of the design basis into drawings

and

procedures.

These failures to incorporate

design

changes

into applicable

drawings

and procedures

are identified as additional

examples of URI 96-

04-05.

At the close of the inspection period, the licensee

was aggressively

pursuing

a program to identify any other configuration problems

and

correct programmatic

weaknesses

in this area.

Activities initiated by

the licensee

included:

The Configuration Management

Control

Group revised gI 3-PR/PSL-l,

"Design Control," as part of corrective action to STAR 8952066

issued

December

4,

1995, which identified that the

PC/H closeout

process

was inadequate.

This revision incorporated

the process

employed at the licensee's

Turkey Point facility.

The process:

2.

3.

Revises

PWO closeouts,

gC reviews,

and completion of

walkdowns, if required.

Initiates

a more timely update to JPN drawings at

ITOP

completion.

Documents identification and completion of PHT, Procedures,

and Training for PC/M closure.

PHAI 96-03-311,

due June 8,

was to address

additional

concerns

in

this area.

30

S2

~

Engineering

issued

CR 96-798 to perform

a generic review of the

.

complete plant/engineering

change

process

and identify necessary

corrective actions.

The inspectors

broadened

the scope of this review to include instrument

setpoints

affected

by PC/Hs.

Pending completion of this phase of the

review, this will remain

an URI.

IV. Plant

Su

ort

Staff Knowledge and Performance

in EP (93702)

One non-conservative

emergency classification

was identified in this

report.

See

paragraph

01.2 of this report for details.

Status of Security Facilities

and Equipment

(71750)

On Hay 11, the inspector

conducted

an after hours walkdown of portions

of the protected

area perimeter.

The inspector

found the fence to be in

good repair, lighting levels to be adequate,

and gates to be properly

closed

and locked.

F2

Status of Fire Protection Facilities

and Equipment

(92904)

On Hay 6 and 7, the inspector

performed

a followup inspection of several

fire protection/prevention

program deficiencies

noted in IR 95-12.

Specifically,

items 5.a. 1.A (Fire Protection Training, gualification and

Requalification)

[see section

F5] and 5.a.3.B.(2)

(Routine monthly fire

protection surve'illances

on fire extinguishers

and hoses).

The second

item involved

a review of the monthly fire extinguisher

inspection

and included

an observation that the extinguisher installed

in Unit 2 Turbine Building lower elevation location T-44 was not the

kind described

in the Unit 2

UFSAR Table 9.5A-80 (Turbine Bui]ding Fire

Extinguishers).

The licensee

corrected this discrepancy.

The inspector

performed

a 100 percent audit of all installed fire

extinguishers

in the Unit 2 Turbine Building lower elevation.

Of the

eighteen installed,

three at locations T-13, T-16 and T-18 were not of

the kind described

in the Unit 2

UFSAR Table 9.5A-BD (Turbine Building

Fire Extinguishers).

This discr epancy

was identified to the Fire

Protection Supervisor.

The licensee identified two additional

instances

of installed fire extinguishers

not of the kind described

in the Unit

1

UFSAR Table 9.5A-BD at locations T-8 and T-12.

Both discrepancies

are

documented

in

CR 96-748

and 96-749.

The fact that

a previous discrepancy

of this nature

was identified in IR

95-12, led the inspector to conclude that

no apparent

followup was

performed.

The licensee

now documents

discrepancies

identified by

inspectors

using Condition Reports.

This issue will be tracked

under

a

URI.

See

paragraph

X.1.2.

1

F5

31

Fire Protection Staff Training and gualification (92904)

On Hay 6 and 7, the inspector

performed

a followup inspection of several

fire protection/prevention

program deficiencies

noted in IR 95-12.

Specifically,

items S.a. 1.A (Fire Protection Training, gualification and

Requalification)

and 5.a.3.B.(2)

(Routine monthly fire protection

surveillances

on fire extinguishers

and hoses)

[see section F2].

The first item involved

a review of the methodology

used to track the

status of Fire Brigade Medical Examinations.

The licensee

added

a

separate

data field to the

REHACS computer printout for Fire Brigade

Physicals.

The inspector reviewed both

a current

REHACS printout and,

the

Emergency

Team Roster

issued April 11.

The Emergency

Team Roster

was issued monthly listing Primary Radiation,

Primary First Aid 8,

Personnel

Decontamination,

Interim First Aid 5 Personnel

Decontamination

Teams

as well as the Fire Team members.

Eleven of the sixty-two Fire

Team members listed

showed expired annual

medical

examinations

on

REHACS.

The inspector verified through

an independent

review of

individual medical files that these

Fire Team members

medical status

shown by

REHAC was accurate.

Check Sheet

1

(AP 1-0010125,

Rev 107,

"Schedule of Periodic Tests,

Checks

and Calibrations"

- later converted to

OP 1-0010125,

Rev 0) was

, completed for each shift.

Item 2A of this check sheet listed the Fire

Team Leader

(NWE) and the five members of the Fire Team.

The inspector

reviewed all Check Sheet

1's for the month of April and determined

the

following:

1.

Nine of the eleven Fire Team members with expired medicals

were

assigned

a total of sixty shifts.

2.

Two Fire Team Leaders

not listed on the Emergency

Team Roster

were

assigned

a total of thirty-one shifts.

3.

One Fire Team member with an expired medical not listed

on the

Emergency

Team Roster

was assigned

one shift.

A cursory review of REHACs further

showed that not all licensed

operators

were not current

on the biannual respirator physical,

respirator fit, and

SCBA training.

The inspector notified the on-shift

NWE and

NPS of the

above findings.

The licensee

immediate corrective actions

included

a review of the

medical status of the on-shift Fire Team members

and initiation of a

root cause

investigation.

CR 96-679

was written to document the

results.

The licensee's

failure to adequately

monitor the status of the fire

brigade

members

annual

physical

examinations

is identified as

a

violation VIO 335,389/96-06-05,

"Failure to Maintain gualifications of

Fire Brigade Hembers".

f,

32

The inspector

reviewed

and agreed with the investigation results

documented

in the subject

CR.

This investigation

concluded that the

process

used to document

and track the qualification of the fire brigade

members

was fragmented,

and where available,

not effectively utilized.

The inspector

noted that

a large portion of the administrative control

was previously exercised

by an individual in the Operations

Department

who tracked

and scheduled training for operators.

This individual has

since retired from FPL in February of this year at which time medical

examinations,

respirator fits, and

SCBA training was

no longer tracked

by the Operations

Department.

V. Mana ement Meetin

s and Other Areas

Xl

Review of UFSAR Commitments

X1.1

A recent discovery of a licensee

operating their facility in a manner

contrary to the

UFSAR description highlighted the need for additional

verification that licensees

were complying with the

UFSAR commitments.

While performing the inspections

which are discussed

in this report the

inspectors

reviewed applicable portions of the

UFSAR that related to the

areas

inspected.

The inspectors verified that the

UFSAR wording was

consistent with the observed plant practices,

procedures,

and

'arameters.

Results

from System

Walkdowns

Minor deficiencies

were noted with respect to the Intake Cooling Water

System walkdowns performed during this period.

These

issues

were

forwarded to the'icensee

for resolution.

They were

as follows:

Unit

1

UFSAR Table 7.3-2 "ICW Hdr.

A Disch. to

TCW Heat Exchanger

Isolation Valve HV-21-2" is incorrect.

Should read

"ICW Hdr.

B

Disch...."

Unit

1

UFSAR Figure 9.2-1a,

"Flow Diagram Intake Cooling Water

Lube Water System,"

has not been revised to show

ICW/CW

modifications performed

by PC/M 341-192.

Unit

1

UFSAR Table 7.4-1,

"Instruments

Required to Monitor Safe

Shutdown,"

under Intake Cooling Water

System

has not been revised

to delete

1

"3)

Intake cooling water

pump lube water pressure

FIS-21-3A, 3B, 3C,

3D, 3E,

3F (Non-safety)"

Unit

1

UFSAR Figures 7.4-9,

10 and

11, "Intake Cooling Water

Pump

lA, 1B and

1C Logic," have not been revised to remove annunciator

E-15 logic which has

been

spared out.

33

Unit

1

UFSAR TCV 14-4A and

4B operation

Section 7.4.1.5 describes

control of ICW system operation

as

follows:

"Following actuation of the pumps,

the intake cooling water system

is designed

to operate with automatic temperature

controlled

modulation of the intake cooling water flow through the component

cooling heat exchangers.

The heat

exchanger outlet flow control

valves

(TCV 14-4A and

TCV 14-4B) are controlled by pneumatic

temperature

controllers TIC-14-4A and TIC-14-4B which sense outlet

temperature

on the component cooling water side of the heat

exchangers.

The temperature

controllers

are provided for

efficient system operation during normal plant operation.

The

control valve pneumatic controls

have

been designed

and qualified

as seismic

Class

I to assure

proper operation of the control

valves during safe

shutdown.

As temperature

increases,

intake

cooling water flow is automatically increased.

The control valves

are pneumatically operated

and fail wide open

on loss of

instrument air.

In the event of loss of air the intake'ooling

system will operate

in the full unmodulated

flow mode."

Section 9.2. 1.5 describes

instrumentation

application

as follows:

"The second

automatic valve in the system is the butterfly valve

(one in each

header)

at the outlet of the component cooling water

heat exchanger.

This valve automatically controls outlet water

flow from the heat exchanger.

It is modulated

opened

and closed

according 'to the outlet water temperature

of the shell side of the

component cooling water heat exchanger."

Although normally operated

in automatic,

the manual

mode of

controller operation is allowed.

Unit 2 UFSAR Table 9;2-3, "Intake Cooling Water System

Instrumentation Application," incorrectly lists the lubricating

water strainer differential pressure

instruments

as PDS-21-25AI,-

25A2,

-25B1,

25B2 with a range of 0-3 psig.

This should read

PDIS-21-25-1A1,

-1A2, -181,

-1B2 with a range of 0-3 psid.

This

also applies to the range for the

TCW inlet strainer differential

pressure

instruments

PDIS-21-7A, -78.

Unit 2 UFSAR Section 9.2. 1.2,

"System Description," in the first

paragraph

states,

"Butterfly valves

I-TCV-14-4A and 4B,

(one in

each header),

located at the outlet of the component cooling water

heat exchanger,

automatically control outlet water flow from the

heat exchanger.

They are modulated

by the outlet water

temperature

of the shell side of the component cooling water heat

exchanger."

Although normally operated

in automatic,

the manual

mode of

controller operation is allowed.

34

~

Unit 2

UFSAR Section 9.2. 1.2,

"System Description," in the second

paragraph

states,

"The turbine cooling water heat

exchangers

and.

blowdown heat exchangers

are supplied

by nonessential

headers

which are automatically isolated

on SIAS by valves T-MV-21-2 and

3. If these

valve operators

were to be reopened locally after

a

postulated

accident,

an alarm and valve open indication is

produced

in the control

room.

Under administrative control

and

procedures,

the control

room operator in such

a case

would reclose

the valves from the control room."

The only alarms that the inspector identified were

E-22 and

E-23

ICW HDR A (B) MV-21-3 (2) OVRLD/SIAS FAIL TO CLOSE which under

Operator Action - Valid Alarm state:

2.

(B) Manually close valve (if required).

It was unclear

how the procedural

guidance

implemented the

UFSAR

described

design feature.

~

Unit 2 UFSAR Table 7.3-2,

"ICW Hdr.

A Disch. to

TCW Heat Exchanger

Isolation Valve MV-21-2," is incorrect.

Should read

"ICW Hdr.

B

Disch...."

10

CFR 50.71(e)

requires

the licensee to periodically update the

UFSAR

six months after each refueling.

The Unit

1

UFSAR Figure 9.2-la, Table

9.2-1,

Table 7.4-1,

Figures 7.4-9,

10 and ll were not updated following

completion of the Unit ICW/CW modifications.

These

items are

added to

URI 335,389/96-04-09,

"Failure to Update

UFSAR", pending further

NRC

review.

X1.2

Results

From Other Inspection Efforts

While performing inspections

described

in this report, the following

UFSAR inconsistencies

were identified:

-The inspector noted,

in reviewing

UFSAR section 4.2.3.2.3(b)(1),

that the minimum time required for CEAs to drop at normal

operation

and upset conditions from any withdrawn position to 90

percent of full insertion

was specified

as 2.5 seconds.

The

inspector

noted that this value differed from UFSAR Table 4.2-1,

which specified

a maximum time of 3. 1 seconds,

consistent with TS.

The inspector

brought this to the attention of the licensee.

The

issue

was documented

in

CR 96-0898.

~

An audit of Unit 2 fire extinguishers

identified three locations

which differed from the

UFSAR.

See

paragraph

F2 of this report.

X1.3

Conclusion

These

items are

added to URI 335,389/96-04-09,

"Failure to Update

UFSAR", pending further

NRC review.

35

X2

Exit Heeting

Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on Nay 13.

The licensee

acknowledged

the findings presented.

No dissenting

comments

were

received.

36

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

Bladow, W., Site guality Manager

Bohlke,

W., Site Vice President

Buchanan,

H., Health Physics Supervisor

Burton, C., Site Services

Manager

Dawson,

R., Business

Manager

Denver,

D., Site Engineering

Manager

Fincher,

P., Training Hanager

Frechette,

R., Chemistry Supervisor

Fulford, P., Operations

Support

and Testing Supervisor

Harple, C., Operations

Supervisor

Heffelfinger, K., Protection Services

Supervisor

Holt, J.,

Information Services

Supervisor

Johnson,

H., Operations

Manager

Kreinberg, T., Nuclear Material

Management

Superintendent

Harchese,

J.,

Maintenance

Hanager

O'Farrel,

C., Reactor Engineering Supervisor

Olson,

R., Instrument

and Control Maintenance

Supervisor

Pell, C., Outage

Manager

Scarola, J., St. Lucie Plant General

Manager

Weinkam, E., Licensing Manager

Wood, C., System

and Component

Engineering

Manager

White,

W., Security Supervisor

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation,

and corporate

personnel.

IP 37551:

IP 40500:

IP 61726:

IP 62700:

IP 62703:

IP 71707:

IP 71750:

IP 73052:

IP 73753:

IP 92902:

IP 92904:

IP 93702:

37

INSPECTION

PROCEDURES

USED

Onsite Engineering

Effectiveness of Licensee

Controls in Identifying, Resolving,

and

Preventing

Problems

Surveil,lance

Observations

Maintenance

Program

Implementation

Maintenance

Observations

Plant Operations

Plant Support Activities

Inservice Inspection

- Review of Procedures

Inservice Inspection

Followup - Maintenance

Followup - Plant Support

Prompt Onsite

Response

to Events at Operating

Power Reactors

~oened

50-335,389/96-06-05

Closed

50-389/95-01-02

50-335/96-06-01

50-335/96-06-02

50-335)389/96-06-03

50-335/96-06-04

Discussed

50-335)389/96-04-05

50-335)389/96-04-09

ITEMS OPENED,

CLOSED,

AND DISCUSSED

VIO

"Failure to Maintain gualifications of Fire

Brigade Members"

VIO

"Failure to Follow Procedure

2-LOI-T-89,

paragraph

4.a.4"

NCV

"Failure to Consider Fire Barrier Operability in

Engineering

Package"

NCV

"Failure to Document Verification of Current

Procedure

Revisions"

NCV

"Failure to Promptly Document Non-Conforming

Conditions"

NCV

"Unit

1

ICW Flow Orifice Found Hissing"

URI

"Configuration Control

Management"

URI

"Failure to Update

UFSAR"

LIST OF ACRONYHS USED

Auxiliary Building

ASEA Brown Boveri

(company)

Administrative Procedure

38

ANI

ANSI

AOV

AP

ASNE Code

ATTN

BRPV

CC

CCW

CE

CEA

CET

CFR

CR

CS

CVCS

CW

CWD

DBE

DPR

DWG

EAL

ECCS

EDG

EOP

EP

EPIP

EPRI

Eg

ESF

ESFAS

F

FPL

FR

FRG

GL

GHP

gpm

HPSI

HVS

ICI

ICW

i.e.

IHE

IP

IR

ISI

JPN

lb

LCO

LCV

Authorized Nuclear Inspector

American National

Standards

Institute

Air Operated

Valve

Administrative Procedure

American Society of Hechanical

Engineers Boiler and Pressure

Vessel, Code

Attention

Boiler and Pressure

Vessel

Cubic Centimeter

Component

Cooling Water

Combustion

Engineering

(company)

Control

Element Assembly

Core Exit Thermocouple

Code of Federal

Regulations

Condition Report

Containment

Spray

(system)

Chemical

5 Volume Control

System

Circulatory Water

Control Wiring Diagram

Design Basis

Earthquake

Demonstration

Power Reactor

(A type of operating license)

Drawing

Emergency Action Level

Emergency

Core Cooling System

Emergency Diesel

Generator

Emergency Operating

Procedure

Engineering

Package

Emergency

Plan Implementing Procedure

Electric Power Research

Institute

Environmentally qualified

Engineered

Safety Feature

Engineered

Safety Feature Actuation System

Fahrenheit

The Florida Power

& Light Company

Federal

Regulation

Facility Review Group

[NRC] Generic Letter

General

Haintenance

Procedure

Gallon(s)

Per Minute (flow rate)

High Pressure

Safety Injection (system)

Heating

and Ventilating Supply (fan, system, etc.)

Incore Instrument

Intake Cooling Water

that is

In-House-Event

Report

Inspection

Procedure

[NRC] Inspection

Report

InService Inspection

(program)

(Juno Beach).,Nuclear

Engineering

pound

TS Limiting Condition for Operation

Level Control Valve

0

39

LIS

LOI

LOOP

LPSI

LTOP

H&TE

MMP

HV

HWO

NCV

NDE

NLO

NOUE

NOV

NPF

NPS

NRC

NUHARC

NWE

ONOP

OPC

PC/M

PDIS

PDR

PHAI

PMT

psia

psld

Pslg

PSL

Pub

PWO

QA

QC

QI

RAB

RCO

.RCS

REMACS

Rev

RII

RPS

SCBA

SDC

SFP

SIAS

SNPO

SPDS

SRO

St.

STAR

SwRI

Level Indicating Switch

Letter of Instruction

Loss of Offsite Power

Low Pressure

Safety Injection (system)

Low Temperature

Overpressure

Protection

(system)

Measuring

& Test Equipment

Mechanical

Maintenance

Procedure

Motorized Valve

Haster

Work Order

NonCited Violation (of NRC requirements)

Non Destructive

Examination

Non-Licensed

Operator

Notice of Unusual

Event

Notice of Violation

Nuclear Production Facility (a type of operating license)

Nuclear Plant Supervisor

Nuclear Regulatory

Commission

Nuclear Management

and Resources

Council

Nuclear Watch Engineer

Off Normal Operating

Procedure

Overspeed

Protection Circuit

Plant Change/Hodification

Pressure

Differential Indicating Switch

NRC Public Document

Room

Plant Management Action Item .

Post Maintenance

Test

Pounds

per square

inch (absolute)

Pounds

per square

inch

differential)

Pounds per'quare

inch (gage)

Plant St. Lucie

Publication

Plant Work Order

Quality Assurance

Quality Control

Quality Instruction

Reactor Auxiliary Building

Reactor Control Operator

Reactor Coolant System

Radiation

Exposure Monitoring and Access Control System

Revision

Region II - Atlanta, Georgia

(NRC)

Reactor Protection

System

Self Contained

Breathing Apparatus

Shut

Down Cooling

Spent

Fuel, Pool

Safety Injection Actuation System

Senior

Nuclear Plant [unlicensed]

Operator

Safety

Parameter

Display System

Senior Reactor [licensed] Operator

Saint

St. Lucie Action Request

Southwest

Research

Institute

TCW

TEDB

TS

UFSAR

URI

VAC

VCT

VIO

40

Temperature

Control Valve

Turbine Cooling Water

Total

Equipment Data Base

Technical Specification(s)

Updated Final Safety Analysis Report

[NRC] Unresolved

Item

Volts A1ternating Current

Volume Control Tank

Violation (of NRC requirements)

Attachment:

Spent

Fuel Storage

Data Table

ATTACHMENT 1

UNIT 1 SPENT FUEL STORAGE DATA TABLE

Facility

SFP Related Technical

Specifications

Name: St. Lucia

Parameters:

Electrical Power Systems - Shutdown

(3.8.1.2)

Unit Number: Unit 1

Limiting Value or Condition:

Specifies required A.C. power during movemant of

irradiated fuel or crane operation with loads over tha

SFP

Decay Time (3.9.3)

?72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> prior to fuel rnovamant

Crena Travel - Spent Fuel Storage

Pool Building (3.8.7)

Loads > 2000 Ibs shell not be moved over irradiated

fuel eesemblias

in tha storage pool

Storage Pool Water Level (3.9.11)

Maintain a23 feet water over fuel seated in the

storage racks

Fuel Pool Ventilation System - Fuel Storage

(3.8.12)

Ona fuel pool ventilation system operabla whenever

irradiated fuel is in tha spent fuel pool

Spent Fuel Cask Crena (3.8.13)

Maximum load handled by cask crane shall be S25

tons

Decay Time - Storage Pool

(3.9.14)

Irradiated fuel assemblias

shell have decayed E1180

hours or ~1490 hours prior to movamant of cask into

cask compartment

Fuel Storage Criticality (5.6.1.e and

5.6.1.b)

Maintain k

S0.95, decor(bas nom)nai storage pitch,

pool boron concentration ) 1720 ppm, boreflax

installed in Region

1 end Region 2 storage racks;

specifies fuel assembly enrichment/exposure

limits for

storage in Region

1 end Region 2

Fuel Storage Drainage (5.6.2)

Fuel Storage Capacity (5.6.3)

Fuel pool can not be drained below elevation 56 feat

Storage oapacity is M1706 fuel essamblias

SFP Structure

Location: Above grade in fuel handling

building (FHB). Fuel pool floor elevation is

21.5'; cask area floor elevation is

18.0'8770.G.074

Rev 10)

Saismio Classification of SFP Structure and Building:

FHB & SFP designed

es e seismic Class

I structure

(UFSAR 3.8.1.1.2); Spent fuel racks designed to

~aisrrMO Category I requirements

(UFSAR 9.1.2.2.3)

Gross SFP Volume: 47008 fte (including

cask storage area) to 60'ormal water

level.

Derived from drawings 8770%965

Rav

1 & 8770-G-074 Rav 10.

SFP Temperature for Stress Analysis: Normal Operating

'hermal

loads analyzed with 150'

water at weil and

32'

external air temperature; Aocident oonditions

used bulk water temperature of 217'

with external

eir temperature of 40'. Both one)yeas assumed

linear

thermal gradients.

(PSL1 rereck lioansa amendment,

Safety Analysis Report. June 12, 1987, popes 4-9 & 4-

10)

Leakage Collection

Liner Type: Stainless'teal

type 304; fuel

pool floor 0.25

plate, liner walls 0.188

plate, cask pit floor 1.0

plate.

(8770-

4965

Rev

1 + UFSAR page 9.1-4e)

Leakage Monitoring: Network of stainless steel angles

attached to the outside of tha pool liner wells end the

underside of tha pool liner floor (8770-G-830 sh.2, Rev

2 & 8770.G-894 Rev 5).

Drainage Prevention

Location of Bottom Drains: Nona.

(8770.G.830 sheet 4, Rav 1. 8770.G 830

sheet 1, Rav'4, and sheet 2, Rav 2)

Elevation of Gate Bottom Relative to Stored Fuel:

Gate

bottom is et elevation 36.25'8770 G-830 sh. 2).

This is above the top of fuel seated in tha racks.

UNIT 1. SPENT FU EL STO RAG E DATA TABLE

Siphon Prevention

Lowest Elevation of Connected

Pipinp

Rolative to Fuel: Above top of fuol. Fuol

pool coolinp suction lino penatratas

pool

(inst at elevation 58.0'; return line

panatratas

pool liner et elevation

59.26'8770-G-830

sheot 1).

Fuel pool

puriflicotion ay<<tom piping panatratas

fuel

pool liner at an elevation of 68.0'nd

59.0'8770.G.830

sheet 2) Top of fuel

assembly seated in storage rocks is

35.0'.

Anti.Siphon Dovicos: Fuel pool return lino has 0.5

hole

and purification suction line has 0.25'olo p(acod

1'olow

normal water lovel.

(8770.G.078, sheet 140, Rav 9)

Make.up Capability

Safety.Related

Source:

intake coolinp

w<<ter

Normal Source:

RWT or PWT depending

on fuel pool boron concantr<<tion

(OP 1.

0350020 Rev 21, page 11).

Saismio Classification snd Quality Group:

Intake

cooling water makeup capability is Saismio Category

I

group C. (8770-G-082, sh. 1, Rev 43)

Reactivity

Limits on ~ and Enrichment: For both fuel

pool regions k~ 60.95 with the pool

flooded with unborotad water. Fresh fuel

limited to C4.6 w/o; Region 2 hea

additional restrictions booed on T.S. Figure

6.8-1

Soluble Boron Credit for Accidents: Yas, assembly

mislood (PSL1 rerack license emandmant,

Safety

Andysis Report, June 12, 1887, pages 3-2 & 6.8).

Reactivity Control

Solid Noutron Poisons:

Boraflax sheets

placed between storage calls in both

Region

1 ond 2.

Number of Fuel Storage Zones: Two based on

assembly bumup and initid enrichment.

ared or Split Spent Fuel Pools

SFP Design Inventory Cases

No. of SFPs:

Ona

Normah 1620 ossambliee

(PLA submittal

to support PSL1 fuel pool rerack, pages 3-

28 & 3-31, June 12, 1987).

No. of SFPs Recaivinp Discharge from a Single Unit:

Ona; all Unit 1 fuel is in Unit 1 pool.

Emergency/Abnormal:

1857 aasamblias

(PLA

submittd to support PSL1 rerack, pages 3-28 & 3-31,

June 12,'1987)

SFP Design Heat Load (MBTU/hr)

and Temperature

('F)

Normd: 18.42EB; 133.3'F with 1 fuel

pool cooling pump. (PLAsubmittd to

support PSL1 fuel pool rarock, page 3-33,

June 12, 1987)

Emergency/Abnormal: 33.71EB;

150.8'

with 2 fuel

pool cooling pumps; 187'

with 1 pump in oporation

(Sof<<ty Evd. by NRR rd<<tod to License Amendment

91, M<<di 11, 19SS)

SFP Cooling System

No. of Trains: 2 pumps in pardlel:

1 hast

exchanger.

No. of SFPe Served by Each Train: one

(8770-G-078, ah. 140, Rev 9)

ucensed to Withstand Single Active Component

Failure: Yes. Sae section 5.2.1, Hest Removal

~Ce sbitit)(, from SER issued by NRC offlica of NRR

related to Amendinent 91 to Unit 1, doted March

11,19SS.

Electrical Supply to SFP Cooling

System Pumps

Qualification ond Independence

of Power

Supply:

SFP Cooling pump 1A is a load on

the essential portion of 480V motor

oontrol oantsr 1A-8. SFP Coolinp pump 18

is a load on the essential section of motor

control oanter 18-8. These MCC's ore not

class 1E. (8770 G-275 sheet 8, Rev 8)

Load Shod Initiators: Undarvoltago or ovarcurrent.

(8770 G-2'76 sheet 1, Rev 12, & sheet 8, Rev 8)

Backup SFP Coolinp

System Nome:

None.

Qualification: N/A.

SFP Hast Exchanger Cooling Water

(8770 G-083, sheet 1, Rav 42)

System Noma: Component Cooling Water

Qualification:

Some portions of CCW important to SFP

coolinp are eeismio I safety class C; others ore safety

aloes D.

Attachment

3

UNIT 1 SPENT FUEL STORAGE DATA TABLE

Secondary Cooling Water Loop

(8770.G.082, sheet 1, Rev 43)

System Name: Intake Cooling Water

Qual(5cetion:

Seismio

I safety doss C

Ultimate Hest'Sink (UHS)

SFP Cooling System Hast

Exchanger Performance (Highest

Capability Hest Exchanger if not

identical)

(8770-2017 Rav 2)

Typo: Atlantic Ocean/Big Mud Creek

Design Heat Capacity (BTU/hr): 32.0E6

SFP Side Row: 1.50E6 Ibm/hr

SFP Temperature:

150'F

SFP Cooling Loop Return Tamp: 128.7'

UHS Design Temperature:

85'

(UFSAR p. 8.2-2)

Type: tube end shell

Cooling Water Row:

1.78ES Ibm/hr

Cooling Water Inlet Temp: 100'

Cooling Water Outlet Tamp:

118'FP

Related Control Room Alarms

(ONOP 1-0030131, Rev 62)

Parameter(s):

Fuel Pool High/Low Level,

Fuel Pool High Temperature,

Fuel Pool

Pump Discharge Header Pressure-Low,

Fuel Pool Pumps Motor Overload, Fuel Pool

Room High Temperature,

Fuel Pool Exh.

HVE Low Row/Motor Overload, CCW Flow

to Fuel Pool Heat Exchanger High/Low.

Noble Gee Radiation Alert.

Setpoint: a 2'rom nomind level, 137.5', 18 psig,

pump trips, 110~ F, (13800 ofm, W3600 gpm or

S 2850 gpm, ee established by Chemistry Dept.

Location of Indiootions

SFP Lovol: Nono

SFP Temperature:

Local roedout (8770-G-078, Sheot

140, Rav 8)

SFP Cooling System Autometio

Pump Trips

FP Boiling:

Parameter(s):

Nona other then tha

alactrioel trips listed obovo.

Staff Aooaptenoa of non-Seismio

SFP

Cooling System Based on Seismic

Category

I SFP Ventilation System: Fuel

pool oooling system end fuel pool

vontilation system era not seismio oetagory

I. (8770:G 879 Rav 28 & 8770.G-125 Sh.

FS.W-3)

Indapandanca:

independent alactriod tripe for each

pump. (8770.G-275, sheet 8, Rav 8)

Off.site Consequenoes

of SFP Boiling Evduetad:

Yae.

(L-87-537, December 23, 1887, Attachment 6)

If Yas, Was Filtration Credited: No.

SFP/Reactor System Separation

Heavy Load Handling

Separation of SFP Operating Boor from

Portion of Aux. or Reactor Bldg. that

oontains Reactor Safety Systems:

SFP

ares completely enclosed: ventilation

system directs dr to FHB stack.

SFP Ares Crone Qudified to Single Failure

Proof Standard IAW NUREG-0612 end/or

NUREG-0554: No. (FSAR Tables 9.1-6 and

8.6-1)

Separation of Units et Multi-UnitSites:

St. Lucis Units

1 & 2 have separate fuel handling buildings end

ventilation systems.

Routine Spent Fuel Assembly Transfer to ISFSI or

Alternate Wet Storage Location:

No

Attachment

UNIT 1 SPENT FUEL STORAGE DATA TABLE

Operating Practices

Administrative Control Limit(s) for SFP

Temperature during Refueling: None based

on most recent Rev to fuel shuffle

procedure.

Frequency of Full Coro Off loads: 650

percent of outapes

Typo of Off.load Performed durinp most

recant refueling: partial cora off-load (fuel

shuffle)

Administrative Control Umits for SFP Cooiinp System

Redundancy

and SFP Make-up System Redundancy:

OP

1-1600023, Rav 68, page 8, requires Fuel Pool Cooling

& Purification System to ba in normal operation prior to

baginninp refueling evolution.

This means that electric

power required to ba svaleb(e to both fuel pool coolinp

pumps (OP 1-0360020, Rav 21, pepe 2 & 3). No

requirements for redundancy of makeup source.

Administrative Controls on Irradiated Fuel Decay Time

prior to Transfer from Reactor Vessel to SFP:

Yes. (OP

1-1600023, Rev 68, page 20 of 60, Survaillances

Performed Durfn

Rafuelin

For Units with planned refueling outsgas scheduled to

begin before April 30, 1996, type of Off-load planned

for next refueling and planned shutdown date:

Full

core; expected shutdown 4/28lge.

Attachment

0

UNIT 2 SPENT FUEL STORAGE DATA TABLE

Facility

Nemo: St. Lucia

Unit Number: Unit 2

SFP Related Technical

Spacifioations

Parameters:

A.'C. Sources - Shutdown (3.8.1.2)

Limitinp Value or Condition:

Specifies required A.C. power durinp

movement of irradiated fuel or crane operation

with loads over the fuel storage pool.

Decay Time (3.8.3)

Reactor subcriticd a72 hours prior to fuel

movement in RPV.

Crane Travel - Spent Fuel Storage Pool

Buildinp (3.9.7)

Loads )1800 Ibs prohibitod from travel over

fuel assemblies

in fuel storogo pool.

Water Lava) - Spent Fuel Storage Pool

(3.9.11)

Maintain 823 feat water over top of irradiated

fuel sooted in storage racks.

Spent Fuel Cask Crone

(3.9.12)

Maximum load handled by cack crone shdl be

S 100 tons.

Fuel Storage Criticality (5.8.1.s)

Maintain k

~0.85, specifies nominal pitch of

assemblies

in storogo racks, raquiroe pool

boron concentration E1720 ppm, defines

Region

I end Region II enrichment/bumup

requirements for storoga.

Fuel Storepe Drainage

(6.8.2)

SFP ehdl not be drdned below elevation 68

feat.

Fuel Storage Capacity

(6.8.3)

SFP shdl contain <1078 eesembliee.

SFP Structure

Location: Above grade in fuel handling

buildinp (FHB). Fuel pool floor devotion ie

21.60';

oeek area floor devotion is 17.6'.

(2988-G-073

Rav 18 & 2998-G-074 Rav

12)

Seismic Classification of SFP Structure end

Building: FHB & SFP designed

oe eaiemio Class

I structure (UFSAR 3.8.4.1.3 & 2998.G.078

~heat 140, Rev 6). Spent fuel rocks designed

to seiemio Category

I requirements

(UFSAR

8.1.2.1)

Gross SFP Volume: 62809.(ts (includinp

oosk storage ares) to 80'ormal water

level. (2998.8584

Rev 3 & 2998-G-074

Rav 12)

SFP Temperature for Stress Andysis: SFP

designed for s water temperature of 212'

during tho winter. (UFSAR p. 8.1-6a)

Leakage Collection

uner Type: 304 Stainless steel (UFSAR p.

8.1-4); pool liner wdls 0.188

plate, pool

floor liner 0.825 . Cask ares floor plots

1.0., ooek ares wdl plate 0.6

. (2998.G-

830 sheet 1, 2aaa-ea51

Rev 3, 2998-

8952

Rev 4,

& 2998.ea53

Rev 3)

Leakage Monitoring: Network of stainless steel

ongles attached to the outside of the pool liner

walls and underside of tha pool liner floor.

(2998-G-884

Rav 9)

Drdinape Prevention

Location of Bottom Drdne: None, (2998-

G-830 sheet 1, Rev 7)

Elevation of Gate Bottom Relative to Stored

Fuel: Above top of stored fuel. Gets bottom

elevation is 38.25'2888.6951

Rev 3) ~ Unit

2 fuel sesembliea

aro 168.6

lonp.

Top of fuel

sooted in the storage racks is elevation

35.2'.

(2998.18511

Rav 0)

Attachment

UNIT 2 SPENT FUEL STORAGE DATA TABLE

Siphon Prevention

Lowest Elevation of Connected

Piping

Relative to Fuel: Above top of fuel.

Fuel

pool cooling auction line penetretes

pool

liner et elevation 68.0'2998.6953

Rav

3); return line panatrstes

fuel pool liner at

eleVation 59.25'2998 6952

Rev 4).

Fuel pool purifioetion system piping

penatrstes

fuel pool liner et en elevation of

58.0'nd 59.0'2998-8951

Rev 3 &

2888-7415

Rav 2). Top of fuel storage

racks is

36.25'.

Anti-Siphon Devices:

Fuel pool cooling return

line hss 0,5

hole placed 1.0'elow the normal

pool water level.

Fuel pool purification suction

line has s 0.25

siphon breaker hola placed

1.21'elow the normal pool water level.

(2998 G-078 sheet 140, Rev 5)

Make up Capability

Safety Related Source:

Intake cooling

water

Normal Source:

RWT or PWT depending

on fuel pool boron concentration.

(OP 2-

0350020 Rav 17, page 10)

Seismio Clessificat)on and Ouslity Group:

Intake cooling water makeup capability is

Seismio category

I group C. (2898-G-082

sheet 2, Rav 40)

Reactivity

Limits on ~ end Enrichment:

For both

fuel pool regions ~ ~0.95 with the pool

flooded with unborated water.

Fresh fuel

limited to s4.5 w/o; Region II has

additional restrictions based on T.S. Figure

5.6-1.

Soluble Boron Credit for Accidents:

Yas.

(Safety Evaluation prepared by

NRR for PSL2 rarack license amendmant,

Section 2.1.3)

Reactivity Control

Solid Neutron Poisons:

No. Region I calls

contain unpoisonad

SS L-shaped inserts.

Racks use flux trap design.

Number of Fuel Storage Zones:

Two based on

assembly bumup and (nit(d enrichment.

tered or Split Spent Fuel Pools

No. of SFPs:

Ona

No. of SFPs Receiving Discharge from a Single

Unit: Ona; eil Unit 2 fuel is in Unit 2 pool.

SFP Design Inventory Cases

Normah 884 aesamblias

(12 refueling

batches) with tha most recant refueling

batch oooled for 5 days; other batches

discharged following an 18 month fuel

cycle. (CE latter L-CE-10558, September

7, 1984)

Emergency/Abnormeh

1113 aesamblias

comprising 11 refueling batches,

each of which

was discharged following an 18 month fuel

cyc(e end a full oora offload of 217 essemblias

which has cooled for 7 days.

(L-CE-10558)

SFP Design Hast Load (MBTU/hr)

end Temperature

('R (from Safety

Evaluation by Office of NRR

supporting rarack of the St. Lucis

Unit 2 fuel pool, October 16,

1984)

Normal: 16.9E6 BTU/hr; (137'

with one

pump in operation.

Emergency/Abnormal:

31.7E6 BTU/hr, (150'

with both spent fuel pumps operating.

SFP Cooling System

No. of Trans: 2 pumps snd 2 hast

axchangars.

Ehhar pump csn serve either

heat exchanger.

No. of SFPs Served by Each Train: Ona

(2998-G-078 sheet 140, Rev 5)

Ucansad to Withstand Single Active

Component Failure:

Not explicitly mentioned in

rerack Safety Evaluation prepared by NRR to

support fuel pool rereck. issued October

16,1884.

FPL's rereck PLA submittal

presented

results of both normal snd abnormal

cora offloads assuming a single failure.

Earlier

SE's (NUREG-0843, p. 9-5) give 160'

es

expected tamp. following a full cora offload

with 1 fuel pool cooling pump in operation.

Attachment

UN[T 2 SPENT FUEL STORAGE DATA TABLE

Electrical Supply to SFP Cooling

System Pumps

Backup SFP Cooling

Qualification and Independence

of Power

Supply: SFP Cooling pump 2A is e load on

tha essential portion of 480V motor

control oenter 2A-8. SFP Cooling pump

28 is a load on the essential portion of

me%or control center 28-8.

Fuel Pool

Cooling system is Class IE.

System Noma: Nona.

Load Shed Initiators: Undervoltage or

ovarcurrent.

(2988 G-276 sheet 39, Rev 3, sheet 42, Rev 4

& 2998 G-27S sheet A, Rev 5 + 2998.G.

274

Rev 12 & 2998-G-274 sheet 2, Rev 6)

Qudificetion: N/A

SFP Heat Exchanger Coding Water

(2898-G-083

Sh.1, Rav 31)

Secondary Cooling Water Loop

(2898.G-082 Sh. 2, Rav 40)

Ultimata Heat Snk (UHS)

System Noma: Component Cooling Water

System Name: Intake Cooling Water

Type: Atlentio Ocean/Big Mud Creek

Qualification:

Seismic I safety doss C

Qualification:

Seismic I safety class C

UHS Design Temperature:

86'F

(UFSAR p.

8,2.1a)

SFP Cooling System Hest

Exchanger Performance (Highest

Capability Heat Exchanger if not

identical)

(2988-16809, Rev 0)

FP Related Control Room Alarms

(ONOP 2-0030131, Rev 60)

Design Hant Capacity (BTU/hr): 32.0EB

SFP Side Flow: 1.60EB Ibm/hr

SFP Temperature:

160'

SFP Cooling Loop Return Temp: 128.7'

Parameter(s):

Fuel Pool Pump Discharge

Header Pressure Lo, Fuel Pool Pump

Overload, Hi/Lo CCW Flow to Fuel Pool

Hest Exchanger,

Fuel Pool Room Temp. Hi,

Fuel Pool Exhaust fane Lo Flow/Overload.

Fuel Pool High/Low Level or High Tamp (2

annuno. channels)

Type: tube end shell

Cooling Water Flow: 1.78EB Ibm/hr

Cooling Water Inlet Temp: 100'

Cooling Water Outlet Temp: 118'

Satpoint:

18 psig, N/A, a3700 gpm or

6 2860 gpm, 110', 0.08'g or 1130 scfm,

a138'

or RB deviation in pool water level

from nomind value (2 channels).

Location of Indications

SFP Level: Local coals

SFP Temperature:

Looal readout (2898.G-078

sheet 140, Rev 6 end 2998-G-078 sheet 100)

SFP Cooling System Automstio

Pump Tripe

Parameter(s):

Nona other then the

alectricd tripe listed above.'ndependenoa:

Independent alectricd tripe for

each pump.

(2898.G-276 sheet 23, Rev 4,

sheet 39, Rav 3, end sheet 42, Rev 4)

SFP Boiling:

Staff Acceptance of non-Seismio SFP

Cooling System Based on Seismio

Category I SFP Ventilation System:

Fuel

Pool Cooling System is Seismio Category I.

(2898-G-078 sheet 140,

Rav 6) Portions

of tha Fuel Pool Ventilation System ere

Seismio Close I, safety class 3. (2898-G-

878

Rav 22 and 2998 G.878 sheet 3,

Rav 20)

Off-site Consequences

of SFP Boiling

Evdueted:

No.

If Yee, Wae Filtration Credited:

SFP/Reactor System Separation

Separation of SFP Operating Floor from

Portion of Aux. or Reactor Bldg. that

contains Reactor Safety Systems:

SFP

area completely enclosed; ventilation

system directs air to FHB stack.

Separation of Units at Multi-UnitSitee:

St.

Lucio Unite 1 & 2 have separate

fuel handling

buildings and ventilation systems.

Attachment

UNIT 2 SPENT FUEL STORAGE DATA TABLE

Heavy Load Handling

Operating Practices

SFP Area Crane Qudifiad to Single Failure

Proof Standard IAW NUREG-0612 and/or

NUREG-0554:

No, (FLO-2999-751 snd UFSAR section

8.1.4.3.2)

Administrative Control Umit(s) for SFP

Temperature during Refueling: Yes, ensure

fuel pool temperature 6150'.

(OP 2-1600023

Rav 39, page 26)

Frequency of Full.Cora Off loads:

S50

percent of outagae

Type of Off-load Performed during most

recent refueling: full core offload

Routine Spent Fuel Assembly Transfer to ISFSI

or Alternate Wat Storage Location: No

Administrative Control Umits for SFP Cooling

System Redundancy

and SFP Makeup System

Redundancy:

OP 2-1600023

Rev 38, pages

25 & 26 requires that both fuel pool cooling

pumps and related systems be avd)able.

Makeup source from tha RWT to ths fuel pool

is also required to be available.

Administrative Controls on Irradiated Fuel

Decay Time prior to Transfer from Reactor

Vessel to SFP:

Yee. (Page 19 of OP 2-

1600023

Rev 39)

For Unite with planned refueling outages

~chedulad to begin before April 30, 1896 type

of Off.load planned for next refueling snd

planned shutdown data: N/A; next Unit 2

refueling outage tentatively scheduled for 4/97.

I,

Attachment