ML17227A682

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Insp Repts 50-335/92-21 & 50-389/92-21 on 921020-921123. Violations Noted.Major Areas Inspected:Surveillance Review, Plant Operations Review,Maint Observations,Fire Protection Review & Regional Requests
ML17227A682
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 12/23/1992
From: Elrod S, Landis K, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17227A680 List:
References
50-335-92-21, 50-389-92-21, NUDOCS 9301070294
Download: ML17227A682 (34)


See also: IR 05000335/1992021

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.IIII.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/92-21

and 50-389/92-21

Licensee:

Florida Power

8 Light Co

9250 West Flagler Street

Miami,

FL

33102

'ocket Nos.:

50-335

and 50-389

Facility Name:

St.

Lucie

1 and

2

License Nos.:

DPR-67

and

NPF-16

Inspection

Conducte

Octobe

20 - November 23,

1992

Inspectors:

. A. Elr

,

Se

R sident Inspector

. A. Sco

,

R

ident Inspector

Approved by:

+~~

Cu +

K. D. Landis, Chief

Reactor Projects

Section

2B

Division of Reactor

Projects

/8 SS g~

Da e

S gned

/

zy'

Date Si

ned

z

Date Signed

SUMMARY

Scope:

This routine resident

inspection

was conducted

onsite in the areas

of

plant operations

review, surveillance

observations,

maintenance

observations,

fire protection review, review of special

reports,

review

of nonroutine events,

onsite followup of events,

followup of headquarters

and regional

requests,

followup of unresolved

items,

and followup of

corrective actions for violations

and deviations.

Backshift inspections

were performed

on October

29 and

November

1, 2,

5,

6,

12,

13,

and

18.

Results:

Plant operations

area:

Operators

planned sensitive plant evolutions

such

as surveillances

well

[paragraphs

3.b.(1)

and 4.a]

and responded

correctly to transients

as

demonstrated

by the planning for and response

to

a dropped

CEA during

a

surveillance

[paragraph 3.b.(l)], response

to a turbine control

oscillation [paragraph 3.b.(3)],

and response

to increased

power level

indication following replacement of several

resistance

temperature

detectors

[paragraph 3.b.(4)].

An operator error. during

an operational

surveillance started

a containment

spray

pump but the initial valve

9301070294

921223

PDR

ADOCK 05000355

8

PDR

lineup,

a procedural barrier to spraying the containment,

was adequate

and 'prevented

damage.

The licensee

conservatively

pursued

extensive

corrective action to preclude recurrence

[paragraph 3.b.(2)].

Surveillance

area:

A number of important surveillances

were performed in a professional

manner

[paragraphs 3.b.(1), 4.a.-d.].

In two instances,

the licensee

promptly repaired

and retested

Unit 2 main feed isolation valves after

they failed

a- surveillance

and within Technical Specification. time

limits.

This demonstrated

a strong communication

and. coordination

network.

Two maintenance

groups

were present for the surveillance test,

and they effectively supported

the repair

and subsequent

satisfactory

retest

[paragraphs

5.d

and S.e].

I

Haintenance

area:

Resistance

temperature

detector output drift of nonsafety-related

detectors

was discovered

by the

I&C department

during replacement

activities.

This condition had caused

Unit 2 to be operated

at slightly

over

100 percent

power for an undetermined

period of time.

Haintenance

shop testing .of the removed

components

demonstrated ability to find

causal

factors

and excellent coordination with the engineering division

[paragraph 3.b.(4)]

~

This issue is presently

unresolved

pending further

NRC evaluation.

Other maintenance

activities demonstrated

competent

shop

actions

and excellent coordination with operating

and test groups

[paragraphs

5.a-e].

Engineering

area:

The engineering division demonstrated

responsiveness

in their evaluations

of the significance of St. Lucie

2 operating

above the, licensed

power

level

and

the relationship of this condition to the safety'nalysis

[paragraph 3.b.(4)].

Reactor engineering

leadership

in performance of

core physics testing

was excellent

[paragraph 4.a].

Engineering

supported

HFIV nitrogen tubing/fitting leak repairs

by allowing the use

of TFE tape in sealing joint applications

[paragraph

S.e].

Engineering

corrective actions to violations were prompt

as

shown in plant change

157-292 to install

mud dauber

caps

on containment

sensing lines

[paragraph

12.g],

and studies to determine

what valves are actually

within the containment isolation boundary

[paragraph

10.]

Within the areas

inspected,

the following violation was identified:

VIO 335;389/92-21-07,

Failure to Adequately Haintain Containment

Vessel

Integrity, paragraph

10.'ithin

the areas

inspected,

the following unresolved

item was identified:

V

URI 389/92-21-06,

Operation

Above the Licensed

Power Level, paragraph

3.b.(4).

'

Within the areas

inspected,

the following non-cited violations were identified

associated

with events

reported

by the licensee:

NCV 335/92-21-01,

Low Temperature

Over Pressure

Technical Specification

Amendment

Implementation Failure,

paragraph

8.a.

NCV 389/92-21-02,

Failure to Implement

New Technical Specification

-Requirements

for Emergency

Bus Undervoltage,

paragraph

8.d.

NCV 389/92-21-03,

Hissed Surveillance

on

a Radiation Honitor Being

Returned to Service

Due to Personnel

Error, paragraph

8.e.

NCV 389/92-21-04,

Hissed Technical Specification Surveillance,

paragraph

8.h.

NCV 389/92-21-05,

Incomplete Technical Specification Special

Report,

paragraph

7.

REPORT DETAILS

Persons

Contacted

Licensee

Employees

D. Sager,

St.

Lucie Plant Vice President

G. Boissy, Plant General

Manager

J.

Barrow, Fire/Safety Coordinator

H. Buchanan,

Health Physics

Supervisor

C., Burton, Operations

Manager

R. Church,

Independent

Safety Engineering

Group Chairman

R. Dawson,

Maintenance

Manager

W. Dean, Electrical Maintenance

Department. Head

J.

Dyer, Plant guality Control Hanager

R. Englmeier, Site equality Hanager

H. Fagley,

Construction Services

Hanager

R. Frechette,

Chemistry Supervisor

J. Holt, Plant Licensing Engineer

C. Leppla,

Instrument

and Control Maintenance

Department

Head

L. HcLaughlin, Licensing Manager

G. Hadden,

Plant Licensing Engineer

A. Menocal,

Mechanical

Maintenance

Department

Head

J. Scarola,

Site Engineering

Manager

C. Scott,

Outage

Manager

J. Spodick,

Operations Training Supervisor

D. West, Technical

Manager

J.

West, Operations

Supervisor

W. White, Security Supervisor

D. Wolf, Site Engineering Supervisor

E. Wunderlich,

Reactor

Engineering Supervisor

Other licensee

employees

contacted

included engineers,

technicians,

operators,

mechanics,

security force members,

and office personnel.

NRC Personnel

  • S. Elrod, Senior Resident

Inspector

  • H. Scott,

Resident

Inspector

J.

Hoorman,

Senior Licensing Examiner

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

and Activities

Unit I began

and

ended the inspection period at power.

Power was reduced

for water box cleaning during November

8 - 9 and for a dropped

CEA on

October

22.

The

CEA dropped

due to

a

CEA control timer card failure

during

a routine surveillance

performance.

The unit ended

the period in

day

56 of power operation

since the September

28 turbine startup.

Unit 2 began

the inspection period at full power and

has run at power

since.

There were small

power reductions for a main turbine valve

malfunction that was repaired the

same day.

The unit. ended the period in

day

101 of power operation

since starting

up on August 13.

Operator license requalification examinations

were given from October

26 - November 6.

12 operators

and

12 senior operators

were examined.

The results will be published in Requalification Examination Report

335,389/92-301.

3.

Review of Plant Operations

(71707)

a.

Plant Tours

The inspectors periodically conducted plant tours to verify that

monitoring equipment

was recording

as required,

equipment

was

properly tagged,

operations

personnel

were aware of plant

conditions,

and plant housekeeping

efforts were adequate.

The

- inspectors

also determined that appropriate radiation controls were

properly established,

critical clean

areas

were being controlled in

accordance

with procedures,

excess

equipment or material

was stored

properly,

and combustible materials

and debris

were disposed of

expeditiously.

- During tours,

the inspectors

looked for the

existence

of unusual fluid leaks,

piping vibrations,

pipe hanger

and

seismic restraint settings,

various valve and breaker positions,

equipment caution

and danger tags,

component positions,

adequacy of

'ire

fighting equipment,

and instrument calibration dates.

Some

tours were conducted

on backshifts.

The frequency of plant tours

and control

room visits by site management

was noted to be adequate.

The inspectors routinely conducted partial walkdowns of ESF,

ECCS,

and support

systems.

Valve, breaker,

and switch lineups

as well as

equipment conditions were randomly verified both locally and in the

control

room.

The following accessible-area

ESF system

and area

walkdowns were

made to verify that system lineups were in accordance

with licensee

requirements

for operability and that equipment

material conditions

were satisfactory:

Unit 2 EDGs,

Unit 2 4160 buses,

Unit

1 and

2 Startup Transformers,

and

Unit

1 and

2 HPSI pumps.

b.

Plant Operations

Review

The inspectors periodically reviewed shift logs

and operations

records,

including. data sheets,

instrument'traces,

and records of

equipment malfunctions.

This review included control

room logs

and

auxiliary logs, operating

orders,

standing orders,

jumper logs,

and

equipment tagout records.

The inspectors routinely observed

operator alertness

and demeanor

during plant tours.

They observed

and evaluated

control

room staffing, control

room access,-

and

operator

performance

during routine operations.

The inspectors

conducted

random off-hours inspections

to ensure that operations

and

security performance

remained

at acceptable

levels.

Shift turnovers

were observed

to verify that they were conducted

in accordance

with

approved. licensee

procedures.

Control

room annunciator status

was

verified.

Except

as noted below,

no deficiencies

were observed.

During this inspection period, the inspectors

reviewed the following

tagouts

(clearances):

2-10-92

Unit 2 Governor Valve ¹4,

9913

Switching order for the return of the

1A and

1B

Startup transformers

-

October 29,

1992,

and

2-6-182

V3540,

shutdown cooling isolation valve.

(1)

On October 22, during

a monthly CEA motion surveillance test

per

OP 1-0110050,

Rev 26, Control

Element Assembly Periodic

Exercise,

Unit

1 had

a dropped

CEA event.

At 8:52 a.m.,

the

first CEA {number 33) selected

in the test

mode slipped

and

then subsequently

dropped.

Operations

appropriately entered

off-normal procedure

ONOP 1-0110030,

Rev 28,

CEA Off-Normal

Operation

and Realignment,

and reduced

power to 70 percent.

The

CEA 33 control timer card

was verified to be failed,

causing the dropped

CEA.

The licensee installed,

tested,

and

adjusted

a replacement

timer card prior to returning the

CEA to

its current group height level.

Operations retrieved the

dropped

CEA without exceeding

associated

TS 3. 1.3. 1 and 3. 1.3.6

time constraints.

CEA testing

was resumed

and satisfactorily

completed

on October 23.

In-House

Event Report 92-068

was

generated

on the event:

(2)

On October

25 at ll:05 p.m., during the performance of a weekly

Unit 2 surveillance test,

an operator inadvertently manually

started

the

2B Containment

Spray

pump.

The operator

had

been

performing

AP 2-0010125,

Containment

Spray Flow Control Valve

Cycling.

The procedure directs the operator to shift the

pump

switch from "Auto" to "Off", cycle the

FCV, then return the

pump switch to "Auto".

The operator

placed the

pump switch in

"Run" vice "Off".

The switch was in the wrong position for

less

than

one second prior to the operator realizing his error

and returning the switch to the. correct position,

however the

pump

had started.

With the associated

FCV in its

normally-closed position,

no water was sprayed into the

containment.

The licensee

found that the episode

was not

reportable

per

10 CFR 50.72

-

3 and

NUREG 1022.

The inspectors

agreed with this finding.

The licensee

was pursuing the following corrective actions:

operations

management

counseled *the individual

on the

importance of self-verification of control board actions;

training staff will evaluate

the adequacy of training;

licens1ng staff was generating

information

LER 389-92-007;

a human performance

enhancement

system evaluation is

planned;

and,

AP 2-0010125 will'e revised to enhance

operator action

regarding

switch operations.

The licensee

took this relatively minor problem seriously

and

was following its corrective actions to completion.

On October 26, the licensee

reduced Unit 2 power by about

10

percent to facilitate correction of a main turbine

DEH control

system malfunction.

Governor valve number

4 position began to

oscillate to the point that the

DEH control

system did not

acknowledge

the valve's position.

The control

system shifted

all the governor valves from automatic sequential

operation

mode to automatic single valve operation

mode

as

a fail-safe,

measure.

Reactor

power decreased

40 to 50

MW, which operations

adjusted for without any problems.

In a controlled manner,

operations

reduced

power to about

90 percent to shut the number

4 governor valve and to allow work on the associated

valve

controls.

The

I8C maintenance

group investigated

and found that the

solenoid pilot valve for the number

4 governor

was operating

erratically,

inducing oscillations in the governor valve.

Per

NPWO 0464/64,

ILC replaced

the solenoid pilot valve within

hours of the initial problem.

The reactor

and turbine remained

in operation with the unit output at approximately

90 percent

power.

The

IKC group displayed their competence

during the

replacement.

On November 5,

1992,

in the process of replacing Unit 2 train

"A" main feedwater

RTDs at power, the licensee

discovered

what

appeared

to be

a positive temperature

indication drift or shift

associated

with the old RTDs.

This drift meant that actual

feedwater

temperature

was lower than previously indicated,

and

thus reactor

power was higher than previously calculated.

The

licensee

replaced five of the six main feedwater

RTDs in both

trains with new calibrated

RTDs of a different brand.

Following RTD replacement

in each train,

power was reduced

(by

8

MWe on 'November

5 and another

6 MWe,on November 6).

The

,

total reduction

was aout 1.6 percent of full power.

Licensee

engineering

evaluation

JPN-SPSL-92-1908

dated

November

16,

1992,

assessed

the as-found

accuracy of the feedwater

RTDs and

concluded that the unit was operating within its licensed

parameters

and that the health

and safet'y of the public were

not affected

by the inaccurate

RTDs.

Pending further inspection this subject will be followed as

URI

389/92-21-06,

Potential

Operation

Above the Licensed

Power

Level.

c.

Technical Specification

Compliance

Licensee

compliance with selected

TS

LCOs was verified.

This

included the review of selected

surveillance test results.

These

verifications were accomplished

by direct observation of monitoring

instrumentation,

valve positions,

and switch positions;

and

by

review of completed

logs

and records.

Instrumentation

and recorder

traces

were observed for abnormalities.

The licensee's

compliance

with LCO action statements

was reviewed

on selected

occurrences

as

they happened.

The inspectors

veri fied that related plant

procedures

in use were adequate,

complete,

and included the most

recent revisions.

d.

Physical

Protection

The inspectors verified by observation

during routine activities

that security program plans were being implemented

as evidenced

by:

proper display of picture badges;

searching of packages

and

personnel

at the plant entrance;

and vital area portals being locked

and alarmed.

Operators

planned sensitive plant evolutions well and responded

correctly

to transients.

One operator error that inadvertently started

a

CS

pump

had minimal plant safety

consequences

but was strongly addressed

by the

licensee.

4.

Surveillance

Observations

(61726)

Various plant operations

were verified to comply with selected

TS

requirements.

Typical of these

were confirmation of TS compliance for

reactor coolant chemistry,

RWT conditions,

containment

pressure,-

control

room ventilation,

and

AC and

DC electrical

sources.

The inspectors

verified that testing

was performed in accordance

with adequate

procedures,

test'nstrumentation

was calibrated,

LCOs were met,

remova'l

and restoration

oF the affected

components

were accomplished

properly,

test results

met requirements

and were reviewed

by personnel

other than

the individual directing the test,

and that

any deficiencies identified

during the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

The following surveillance tests

were observed:

a

~

The inspectors

witnessed

the Unit 2 performance of OP 3200051,

Rev

10, At Power Determination of Hoderator Temperature Coefficient,

on

October

29.

TS 4. 1. 1.4.2 requires that

HTC be determined

at several

frequencies

and thermal

power conditions, during each fuel cycle.

The condition being met in this instance

was to perform the test

within 7

EFPD after reaching

a rated thermal

power equilibrium boron

concentration of 800

ppm.

Since this test involved suspending

certain

TS as allowed by TS

4. 1. 1.4.2,

and was considered

an infrequently performed test,

pre-

planning

and pre-briefing were conducted

per AP 0010020,

Rev 2,

Conduct of Infrequently Performed Tests or Evolutions at St. Lucie

Plant.

The briefing by the Operations

Supervisor

was thorough,

including identification of the participants,

conduct .of the test,

expected

plant responses;

criteria for stopping the test,

and

responses

to unexpected

transients

during the test.

The briefing

met all the licensee

requirements

in procedure

Attachment l.

The surveillance test

was performed

smoothly by the operators

and

was witnessed

by th'e reactor engineer,

assisted

by the

STA.

TS

suspensions

were logged

and the action statements

followed.

The

completed test procedure

was also reviewed

by the inspector.

HTC,

found to be -10.0586

pcm/degree

F,

was within TS limits of +3 to -30

pcm/degree

F.

The inspector

had

no further questions.

b.

OP 1-2200050B,

Rev 3,

1B Emergency Diesel

Generator

Periodic Test

and General

Operating Instruction

V

c.

OP 1-0910023,

Rev 4, Transfer Electrical Alignment on the 4160 Volt

lAB and

480 Volt Loads

d.

IEC 2-1400050,

Rev 23, Reactor Protection

System Honthly Functional

Test

N

All surveillances

were competently performed in a timely manner.

5.

Haintenance

Observation

(62703)

Station maintenance

activities involving selected

safety-related

systems

and components

were observed

or reviewed to ascertain

that they were

conducted

in accordance

with requirements:

The following items were

considered

during this review:

LCOs were met; activities were

accomplished

using approved

procedures;

functional tests

and/or

calibrations

were performed prior to returning components

or systems

to

service; quality control records

were maintained; activities were

accomplished

by qualified personnel;

parts

and materials

used

were

properly certified;

and radiological controls were implemented

as

required.

Work requests

were reviewed to determine the status of

outstanding

jobs

and to ensure that priority was assigned

to safety-

related

equipment.

Portions of the following maintenance

activities were

observed:

'

a.

NPWO 7839/63

- Replace

"B3" power supply socket in the "B" channel

of Unit

1

RPS for Low Flow trip function.

b.

NPWO 5756/65

- Troubleshoot

and replace if required the motor to

Unit

1

HV 08-03,

1C

AFW steam

admission valve.

c.

NPWO 5586/66

- Inspect motor leads in electrical

connection

box of

the Unit 2 2A LPSI motor.

This

NPWO controlled the inspection of the

2A LPSI

pump motor cable

to motor lead electrical

connection.

The joint met the requirements

of FCR 2-4099E.

This

FCR along with FCRs

on certain other motor

l.ead connections

were not added to the operating

drawings during

plant construction,

which was typical of the level of detail during

that time frame.

The licensee

was considering

incorporating the

older group of FCRs into their design basis to assist

in maintenance

performance

and to increase

the level of detail in the design basis.

d.

NPWO 9235/64

-

HCV 09-lA Accumulator Schrader

Valve Repair.

A leaking Unit 2 HFIV nitrogen accumulator valve placed the HFIV in

an

LCO on November

15.

The leak was repaired prior to exceeding

the

4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

LCO time limit.

e.

NPWO 0556/64

-

HCV 09-2B Accumulator tubing/fitting repair.

This Unit 2

NPWO contro'lied the repair of a slow leak in a nitrogen

tubing to fitting joint.

The repairs did not require entry into an

LCO.

Subsequent

surveillance testing of the HFIV required

LCO

entry.

Repair efforts were well planned

and professional.

The

engineering division supported this repair by allowing the use of

TFf thread sealing tape in this location which provided

a positive

seal for this application.

The above maintenance

activities were carried out'atisfactorily.

The

Unit 2 HFIV (valve style not installed

on Unit 1) work did not indicate

preventive maintenance

problems.

6.

Fire Protection

Review (64704)

During the course of their normal tours,

the inspectors routinely

examined facets of the Fire Protection

Program.

The inspectors

reviewed

transient fire loads,

flammable materials

storage,

housekeeping,

control

of hazardous

chemicals,

ignition source/fire risk reduction efforts,

and

fire barriers.

Fire protection efforts for this period were satisfactory.

A new service

building fire main branch

was partially connected

with the existing plant

system.

Compensatory

measures

were highly visible during this connection

activity.

7.

Review of Periodic

and Special

Reports

(90713)

(Closed

- Unit 1)

FPL Special

Report L-92-217, dated July 27,

1992.

This special

report per

TS 4.8..1.1.3 discussed'a

non-valid failure of the

, 1A EDG on July 1.

The

EDG faile'd to continue operating during

a test

because

a coolant temperature

switch indicated

a high engine temperature.

The switch was replaced

and the

EDG satisfactorily tested.,

The licensee

evaluated that the switch would be bypassed

during emergency

operation of

the

EDG, therefore

would not prevent

a safety function from occurring.

The inspector

agreed with the licensee's

evaluation.

This was discussed

in IR 335/92-11,

paragraph

4.n.

TS 4.8. 1. 1.3 required reports of EDG failures to address

the items

recommended

in regulatory position C.3.b of RG 1. 108,

Rev 1, August,

1977.

This report addressed

all the items except

item (6) "define the

current surveillance test interval."

The licensee

is submitting

a

revised report.

There

was

no safety significance to this oversight.

This violation of TS 4.8. 1. 1.3 is not being cited because it was

an

isolated

case of low safety significance

and the licensee's

efforts in

correcting the violation met the criteria specified in Section VII.b of

the enforcement policy.

This oversight is identified as. closed

NCV 389/92-21-05,

Incomplete

Technical Specification Special

Report.

8.

Onsite Followup of Written Nonroutine Event Reports

(Units

1 and 2)

(92700)

LERs were reviewed for potential

generic

impact, to detect trends,

and to

determine

whether corrective actions

appeared

appropriate.

Events that

the licensee

reported

immediately were reviewed

as they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with the current

NRC Enforcement Policy.

(Closed)

LER 335/90-10,

Low Temperature

Overpressure

Protection

[LTOP] Setpoint

Helow Technical Specification Limit Due to Personnel

Error.

This

LER reported

a licensee-identified violation of TS 3.4. 13.

While reviewing

an implementing'rocedure

change for LTOP TS

amendment

104, the licensee,

in error,

made

a non-conservative

additional

change to the

new setpoint values

being implemented.

This error existed for less

than

a month.

This

TS change

was

intended to cover operation

between

10 and

15

EFPY.

The plant had

not yet, reached

10

EFPY during this time and operations

were found

to be within the approved

5 -

10

EFPY parameters.

The licensee

completed

the corrective actions stated

in the

LER

within the time limits discussed.

The appropriate

implementing

procedures

were corrected

'and administrative

documents

were changed.

Though Unit 2 was not directly effected, its

LTOP setpoints

were

found to be satisfactory.

This

LER is closed.

This violation is not being cited because

the licensee's

efforts in

identifying and correcting the violation met the criteria specified

in Section VII.b of the enforcement policy.

This event is identified as closed

NCV 335/92-21-01,

LTOP Technical

Specification

Amendment

Implementation Failure.

(Closed)

LER 335/91-01,

Inadvertent Actuation of Reactor

Protection

System During Mode

3 Testing

Due to Personnel

Error.

With all

CEAs inserted into the core except

one undergoing testing,

and with one Nuclear Instrument

(NI) channel

in "trip" (needed

repair),

an operator selected

the wrong trip test potentiometer

on

the other NI channel

and caused

a reactor trip.

All safety

functions were already satisfied prior to the trip.

No TS

violations were identified.

All corrective actions of the

LER were completed.

Self verification

has

been

a subject for operator training and is revisited

periodically per the routine inspection

program.

The tripped NI

that required repair

was repaired

and is in service.

Based

on the

completion of corrective actions, this

LER is closed.

(Closed

- Unit 1)

LER 335/92-006,

Automatic Reactor Trip on

a

Turbine Generator

Loss of Load Signal

due to Equipment Failure.

This

LER addressed

a reactor trip occurring

on September

24,

1992.

The event

was fully discussed

in IR 335,389/92-20,

paragraph

3.a.(4).

The

LER accurately

described

the event.

This

LER is

closed.

(Closed

- Unit 2) .LER 389/90-02,

480

VAC Bus Degraded

Voltage Relay

Setpoint

Below Technical Specification

Minimum Due to design Error.

This

LER reported

a licensee-identified violation of TS 3/4.3.2

and

Table 3.3-4.

While performing

a design

change

review on July 13,

1990,

the licensee

found

a slightly non-conservative

difference in

setpoints for 480

VAC emergency

bus degraded

voltage relays.

The

setpoints

provided

by engineering for use in 1983 were 89.3 percent

of rated voltage

as

opposed

to 90 percent

subsequently

established

by a

TS amendment.

The existing condition was evaluated

by the

licensee to be still bounded

by the existing engineering

safety

analysis.

The licensee

completed corrective actions stated

in the

LER,

including reviews of other setpoints

on both- reactor units.

The

quality control group, corporate

engineering,

and the technical-

support staff performed the reviews.

The quality assurance

staff

audited the set point reviews (report 90-782),

concluding that the

=-

process

was completed.

Aside from the

some additional

checks that

were performed,

the reviews revealed

no additional

problems.

Based

10

on the licensee's

corrective action,

the limited severity of the

problem,

and the isolated nature of the problem. This

LER is closed.

This violation is not being cited because

the licensee's.efforts

in

identifying and correcting the violation met the criteria specified

in Section VII.b of the enForcement

policy.

This issue is identified as closed

NCV 389/92-21-02,

Failure to

Implement

New TS Requirements

for Emergency

Bus Undervoltage.

(Closed

- Uhit 2)

LER 389/90-03,

Missed Surveillance

on

a Radiation

Monitor Being Returned to Service

Due to Personnel

Error.

This

LER reported

a licensee-identified violation of TS 4.3.3. 1,

which required the "B" main steam line radiation monitor receive

a

post-maintenance

channel calibration

and channel

functional test

prior to being returned to service.

The monitor was released

for

service

on July 25,

1990, following a power supply repair without

being calibrated

and functionally tested.

The event

was primarily a personnel

error but contributing causes

were department

interfaces.

IEC planners

prepare

the work order,

IEC technicians

repair the instrument,

the chemistry department

tests it, and operators

place it in and out of service.

Procedure

gI ll-PR/PSL-4, Instrumentation

and Control Test Control,

was

upgraded

in Rev 25, section

5.4

and Appendix

B (the required testing

matrix) to direct coordination with the chemistry department prior

to releasing

monitors for service.

This violation is not being cited because

the licensee's

efforts in

identifying and correcting the violation met the criteria specified

in Section VII.b of the enforcement policy.

This event is identified as closed

NCV 389/92-21-03,

Hissed

Surveillance

on

a Radiation Monitor Being Returned to Service

Due to

Personnel

Error.

This

LER is closed.

(Closed

- Unit P)

LER 389/90-04,

Inadvertent Actuation of Engineered

Safeguards

Equipment During Time Response

Testing

Due to Personnel

Error.

This

LER reported

a personnel

error in that

a technician

pushed

an

incorrect

push button during

a safeguards

test.

The event

was

discussed

in IR 389/90-28,

paragraph

2.b.

Operators,

having

been

pre-briefed,

recognized that the wrong equipment

had actuated

and

terminated

the test,

realigned

equipment,

and verified plant

conditions.

No plant damage

had occurred.

Other corrective actions

included

a human factors review and

a control

room design review in

the area.

The inspector

had

no further questions.

This

LER is

closed.

.11

(Closed

- Unit 2)

LER 389/90-06,

Inadvertent Actuation of Auxiliary

Feedwater

Equipment During,Monthly Testing

Due to Test Instrument

Malfunction.

This

LER reported

an instance

where

2B and

2C

AFW pumps started

when

not supposed

to during the

AFAS monthly functional test..

The

licensee

found that the condition was caused

by an intermittent

grounding fault inside the test meter case.

Though the vendor did

not specify use of an ungrounded

meter,

the licensee

changed

the

applicable

procedure to require it.

The inspector

reviewed

I&C

procedures

1-0700051,

Rev 12,

and 2-0700051,

Rev 15, Auxiliary

Feedwater Actuation System Monthly Functional Test.

They had both

been

changed to require in Section 8, Materials

and Equipment

Required,

that

a battery-powered digital multimeter

be used.

- This

LER is closed.

(Closed

- Unit 2)

LER 389/91-05,

Missed Surveillance for Safety

Injection Tank Wa'ter Level

and Pressure

Channel

Functional

Test

due

to personnel

error.

This

LER reported

a licensee-identified violation of TS 4.5. 1.2.a.

The licensee

discovered

a missed monthly functional check

surveillance'our

days after the

25 percent

grace time had expired.

They promptly performed the functional check with a satisfactory

result.

The licensee

followed up this event in CAR N-91-074.

The

root cause

was found to be personnel

error but

a strong contributor

was the scheduling

program not providing for system supervisors

to

be absent

and not providing for a positive check that the

surveillance

was actually performed.

The inspector

checked

I&C

procedure

1400190,

Rev 8,- I'&C Department Testing

and Surveillance

Schedule,

and found that the scheduling

form had

been modified to

address

alternate

supervisors

and confirmation that each test

had

been

completed.

The current schedule

was posted

in the hall where

I&C supervisors'ffices

were located

and was obviously in use.

This violation is not being cited because

the licensee's

efforts in

identifying and correcting the violation met the criteria specified

in Section VII.b of the-enforcement

policy.

This event is identified as closed

NCV 389/92-21-04,

Missed

Technical Specification Surveillance.

This

LER is closed.

(Closed,- Unit 2)

LER 389/92-002,

Containment

High Pressure

Channel

"C" Inoperable

due to being capped.

I

This event

was cited

as

a violation of NRC requirements

in IR

389/92-07

and was reported

by this .LER.

The

LER was timely and

properly characterized

the event.

The event is being followed up

under

VIO 389/92-07-03.

This

LER is closed.

(Closed

- Unit 2)

LER 389/92-004,

Manual Trip .Due to Low "A" Steam

Generator

Level.

12

This event occurred

on July 8,

1992,

and was discussed

in IR

335,389/92-11.

The

LER accurately reported the event.

This

LER is

closed.

(Closed

- Unit 1)

LER 335/91-02,

Unplanned Actuation of Auxiliary

Feedwater

System

Components

Due to Personnel

Error While

Troubleshooting

a Problem Discovered

During Monthly Surveillance.

While troubleshooting

at

100 percent reactor

power,

a technician

pulled the wrong fuse in the AFAS channel

"D" cabinet

and started

the

1C

AFW pump.

Both the steam

admission

and trip/throttle valves

opened.

No water was injected into the steam generators.

The licensee

found the major contributor to the error was that the

vendor manuals

were unclear concerning

the types

and locations of

various fuses.

The inspectors

reviewed the licensee

actions listed

in the

LER.

The changes

to the applicable

AFAS technical

manuals

clarified the types

and locations of fuses in the cabinet.

All

other licensee

actions

were completed.

No TS or procedures

had

been

violated

and

no other systems

had

been effected.

This

LER is

closed.

'l.

(Closed

- Unit 1)

LER 335/91-07,

Diesel

Generators

Administratively

Declared

Out of Service

Because

of Particulate

Contamination

in the

Diesel

Fuel Oil Due to Procedure

Deficiencies.

This

LER reported

a licensee-identified

violation of TS 4.8. l. 1.2.d

involving the failure to correctly identify or employ

a chemical

reagent

used in

EDG fuel oil particulate determination.

A

particulate-contaminated

fuel oil shipment

was not detected,

was

introduced into the site's fuel oil storage

system,

and resulted

in

technical

inoperability of three of four fuel oil storage

tanks

and

EDGs.

This event

was cited as

a violation of NRC requirements

in IR

335,389/91-22,

VIO 91-22-01.

See also paragraph ll.j of this

report.

The corrective actions stated

in the

LER text have

been completed.

The inspectors

have observed all phases

of fuel oil sampling,

filtration, and onsite analytical testing.

The inspectors

judged

that the licensee's

actions

should reduce the probability of

recurrence.

This

LER is closed.

Licensee corrective action completion for the

above

LERs was

satisfactory.

9.

Onsite Followup of Events

(Units

1 and 2)(93702)

Nonroutine plant events

were reviewed to determine

the need for .further

or, continued

NRC response,

to determine

whether corrective actions

appeared

appropriate,

and to determine that

TS were being met

and that

the public health

and safety received primary consideration.

Potential

generic

impact

and trend detection

were also considered.

13

Licensee followup of events

discussed

in paragraph

2 was

seen

as timely

and effective.

Followup of Unresolved

Items (Units

1 and 2)

(92701)

(CLOSED - Units

1 and 2)

URI 335,389/91-16-01,

Containment Integrity.

This issue

was unresolved

pending further

NRC review.

The issue

has

subsequently

been reviewed

by the

NRC staff at both Region II and

Headquarters.

NRC review concluded that the licensee

had violated

NRC

requirements

in this area

as described

below.

This URI is

administratively closed.

This URI addressed

a condition occurring

on July =30,

1991.

The licensee

had initiated the Reactor Auxiliary Building Fluid Systems

Periodic

Leak

Test

on containment

spray train "A" per

OP 1-1300054,

Rev 15,

same title.

This procedure essentially

isolated the

CS system at the containment

penetration;

operated

the

CS

pump via recirculation to the Refueling

Water Tank to pressurize

the system,

which would then

be inspected for

leaks;

then restored

the system to the normal configuration.

The-

procedure

referenced

TS 6.8.4.a,

Primary Coolant Sources

Outside

Containment,

as the basic requirement

being met by the test.

Other

TS

LCOs that would be entered

were not referenced.

The procedure

required that

CS drain valve I-V07163, located in the

Auxiliary Building on the containment

vessel

side of test

boundary valve

I-MV-07-3A, be opened

and all water drained

from the spray

header prior

to starting the

CS pump.

This was to ensure that test

boundary valve

leakage

was detected

promptly to preclude

spraying the containment.

Valve I-V07163 was partially opened

and

had drained water for about three

hours

when the inspector questioned

the licensee's

compliance with TS 3.6. 1. 1.

TS 3.6. 1. 1 required that containment vessel'ntegrity

be

maintained in modes .1, 2, 3,

and 4.

This specification's

action

statement

required that, if without containment

vessel

integrity, then

containment

vessel

integrity must

be restored within one hour or the unit

be in Hot Standby within the next six hours.

When notified of the

concern,

the licensee

promptly shut the valve then restored

the

CS system

to the normal configuration while reconsidering

the test.

The inspector

considered

that the

TS 3.6. 1. 1 action statement

was inadvertently entered

but not exceeded

because

a normal unit shutdown could be accomplished

within the four hours remaining in the action statement.

After due consideration,

the licensee

stated that they had not actually

been in TS

LCO Action Statement

3.6. 1. 1, Containment

Vessel Integrity,

because:

The only valves involved in containment

vessel

integrity were those

identified by number in the

TS or perhaps

the

UFSAR.

The licensee

stated that they believed that the

NRC had previously considered

the

situation

when the facility license

was issued

and,

by not

'pecifically

identifying in the

TS the vent

and drain valves or

other fittings, had determined

them to be too small to be

considered.

The licensee specifically stated that all vent, drain,

and test valves

and fittings located in the containment penetration

areas

were not required to be secured

in position

and were not

required to be surveillance

checked at least

once per

31 days per

TS 4.6.1.1.

Additionally, during the

ILRT, the containment

spray check valve

and

flow control valve had

been tested

as

a pair using

ILRT pressure.

[These valves were not separately

tested.

The drain valve in

question

was between

them.]

Subsequent

NRC staff review and onsite inspection

found that:

The essential

element of CONTAINMENT VESSEL INTEGRITY, that was not

adequately

maintained

(as defined in TS definition 1.7),

was

as

follows:

TS 1.7

CONTAINMENT VESSEL

INTEGRITY shall exist when:

a.

All containment

vessel

penetrations required to be closed

during accident conditions

are either:

1.

Capable of being closed

by an

OPERABLE containment

automatic isolation valve system,

or-

2.

Closed

by manual

valves,

blind flanges,

or

deactivated

automatic valves

secured

in their closed

positions,

except

as provided in Table 3.6-2 of

'pecification

3.6.3.1 (for Unit 1) or Specification

3.6.3 (for Unit 2).

Per the

10 CFR 50 Appendix A requirements

for containment isolation,

the area

between

the first automatic

or locked isolation valve

outside containment

and the first automatic or locked isolation

valve inside containment

in a line penetrating

containment is

included in the design basis for containment

vessel

integrity.

TS 3.6.1.1

and 4.6.1.1 apply.

CS drain valve I-V07163 was in the section of pipe included in

containment

vessel

integrity: it drained the

CS line (that

penetrated

containment)

between

the first automatic isolation valve

inside containment

(a check valve)

and the first automatic isolation

valve outside containment.

CS drain'alve

I-V07163 was

a manual

one-inch valve,

was the only valve or isolation device in the drain

line,

and drained to the floor in the Containment

Penetration

Room

in the Auxiliary Building.

The valve had

no mechanical

device to

. seal

or lock it closed.

Other similar containment penetration

vent,

drain,

and test valves in Unit

1 and Unit 2 also

had

no mechanical

devices to seal

or lock them closed.

10CFR Part 50, Appendix J, defined

a containment isolation valve

as

any valve which is relied

upon to perform

a containment isolation

15

function.

The

NRC staff considered

any valve which isolates

a

containment penetration,

no matter

how small, to be

a containment

isolation valve and that therefore

CS drain valve I-V07163 was

a

containment isolation valve and

TS 3.6. 1. 1 and 4.6. 1. 1 applied.

TS 4.6. 1. l.required that

CONTAINMENT VESSEL

INTEGRITY be

demonstrated

at least

once per 31 days

by verifying, in part, that

all containment

vessel

penetrations

not capable of being closed

by

'PERABLE containment

automatic isolation valves

and required to be

closed during accident conditions are closed

by valves, blind

flanges,

or deactivated

automatic valves

secured

in their closed

positions,

except for those inside Unit

1 containment

or listed in a

certain

TS table.

"Secured

in their positions" in the't Lucie TS applied to manual

valves,

blind flanges,

and deactivated

automatic valves.

Standard

Review Plan section 6.2.4,

Containment Isolation System, referring

to closed

manual

valves, blind flanges,

and deactivated

automatic

valves,

equated

"secured

in their position"

and "sealed closed".

These

items should

be under "administrative control" to ensure that

they could not be inadvertently

opened.

Administrative control

includes

mechanical

devices to seal

or lock the fitting closed,

or

prevent

power from being supplied to the valve operator.

The licensee failed to maintain

CONTAINMENT VESSEL

INTEGRITY prior

to November 23,

1992,

in that Containment

Spray drain valve I-V07163

and other non-automatic

containment

vessel

penetration

closure

devices

in both units,

such

as

manual

valves or blind flanges,

while

closed,

were not secured

in their closed positions

as required.

They were not secured

in that there

were

no mechanical

devices to

seal

or lock them closed.

During this time, Units

1 and

2 were

operated

in Mode 1.

The licensee failed to implement the

31 day surveillance

requirement

of Unit

1

and Unit 2 TS 4.6. 1. 1 prior to November 23,

1992.

The

licensee

had

no procedures

to implement the check of all the vent,

drain,

and test valves being secured

in their closed positions.

Additionally, the licensee

had

no approved

complete list of

containment

vessel

penetration fittings and

had

no approved

complete

containment

vessel

penetration

boundary drawings suitable for

developing

such procedures.

Incomplete listings did exist.

Many

major valves were listed in TS Table 3.5.2,

Containment Isolation

Valves,

and the Unit 2 UFSAR had sketches

showing the local leak

rate test alignments.

The Unit 2 UFSAR sketches

also included in-

l'ine valves oth'er than isolation valves with no differentiation

between

the two categories,

Implementing procedures,

including surveillance

procedures

AP 1-

0010125,

Rev 87,

and 2-0010125,

Rev 40,

and associated

APs

1-

0010125A

and 2-0010125A did not include the vent, drain,

and test

'alves.

16

Standard

Review Plan section 6.2.6,

Containment

Leakage Testing,

regarding leak testing of vent, drain,

and test valves,

states

that

... test,

vent,

and drain connections that are

used to 'facilitate

local leak testing

and the performance of the containment

integrated

leak rate test should

be under administrative control,

and should

be

subject to periodic surveillance,

to assure their integrity and

verify the effectiveness

of administrative controls.

This system

had

a Class

E penetration

per

UFSAR Section 6.2.4.2,

Containment Isolation System Design.

Class

E was for lines designed

to be open following a

LOCA to mitigate the effects of the, accident.

They were to have either:

a 0

b.

a check valve in series with a remote manually actuated

valve, or

a remote manually actuated

valve or check valve and

a closed

seismic

Class

I system outside containment.

The

CS system

was

a closed Seismic Class

I system outside

containment with a check valve inside containment.

Opening drain

valve I-V07163 in the containment penetration

area did not meet the

"closed seismic

Class

I system" part of the requirement.

Failure to implement

TS 3.6. 1. 1 and 4.6. 1. 1 is

a violation, VIO

335,389/92-21-07,

Failure to Adequately Maintain Containment

Vessel

Integrity.

ll.

Foll'owup of Headquarters

and Regional

Requests

(Units

1 and 2)

(92701)

a

0

(Open

- Unit 1, Closed

- Unit 2) 335,389/P21-90-005,

Broken Swing

Arms for Check Valves.

This

10 CFR 21 Report concerned

broken cast

swing arms for Borg-

Warner Co. pressure

seal

type check valves.

The swing arms

exhibited hot cracks,

porosity, weld repair,

and inadequate

heat

treatment.

They were manufactured for nuclear service

and were not

commercial

grade

items subsequently

dedicated for nuclear service.

These valves were installed in the

AFW system at another plant.

The St.

Lucie plant was listed

as possibly having

some of these

items.

FPL reviewed this concern

under feedback of operating

experience

program FOP-90-023.

Eight valves were originally identified, four

in Unit

1 and four in Unit 2.

Three were inspected

using visual

and

dye penetrant

techniques

as 'follows:

.

UNIT

.

VALVE

gCIR NO.

RESULTS

1

V-07269

M91-735

SATISFACTORY

1'-07270

M91-736

SATISFACTORY

0

17

b.

C.

V-3215

35612

SATISFACTORY - the swing arm was

stainless

steel

vice the material

described

in the

10 CFR 21 report.

Following the recognition that the Unit 2 valves did not actually

fit the

10 CFR 21 report description,

the licensee

canceled further

inspections

on Unit 2 valves V-3225, 3235,

and 3245.

Unit

1

AFW

check valves

V-12174

and V-12176 are scheduled for inspection during

the Spring,

1993, refueling outage

per

NPWO 3640/61.

This item is

closed for Unit 2 but remains

open for Unit

1 pending the licensee

completing the inspections.

(Closed - Units

1 and 2) 335,389/P21-91-006,

Overspeed

Trip Tappets

for Terry Steam Turbine

Pump Drivers.

This

10 CFR 21 Report addressed

a condition where the "molded head"

type overspeed trip tappet

heads

swelled under high temperature

and

humidity, then

bound

up because

of the loss of clearance

between

the

head

and

a guide.

A redesigned

tappet incorporated

a metal

guided

surface

and greater clearance.

St.

Lucie Units

1 and

2 each

have

a

Terry turbine in the

AFW system.

The licensee

addressed

this issue

under feedback of operating

experience

program FOP-89-143.

The older model tappets

were

replaced

per Unit

1

NPWO 2351/61,

completed

October 21,

1991,

and

Unit 2

NPWO 1592/62,

completed

June

13,

1992.

The inspector

reviewed the

NPWO records

and confirmed that the spare

tappets

held

in stores

were changed

to the

new part.

This item is closed.

The inspectors

responded

to

a

NRC Region II survey request

received

on November 2.

The survey purpose

was to assess

the effectiveness

of QA organizations.

The survey areas

included the

QA organization,

program, relationship to other .assessment

organizations

such

as

ISEG,

CNRB, etc.,

and effectiveness.

The survey

was returned

on

November 3,

as required.

The above Part

21 Reports

(items a.

and b.) were satisfactorily followed

by the licensee.

12.

Followup of Corrective Actions for Violations and Deviations

(Units

1 and 2)(92702)

a 0

(Closed

- Units

1 and 2)

VIO 335,389/90-13-01,

Failure to Ensure

Quality at Least Equivalent to That Specified in the Original Design

Basis or Requirements

- Three

Examples.

FPL letter L-90-250 responded

adequately

to this Notice of

Violation.

(1)

The Unit

1 containment

maintenance

hatch drawbridge

was being

supported

in its stowed position

by

a chainfall vice the

required seismically designed

bolted angle supports.

18

The licensee

changed

GMP M-0311 to identify r'emoval

and

replacement

nf the drawbridge bracing during opening

and

closing of the containment

equipment hatch.

Subsequently,

the

inspectors

have witnessed

both Unit

1 and

2 drawbridges

being

properly positioned

on several'occasions

(2)

When unable to find approved

mounting detail drawings for

hydrogen sampling system containment isolation solenoid valves,

the

shop engineers

informally designed

and installed

significantly different

mountings'he

licensee

addressed

the personnel

error involved here

and

also determined that the installation detail

dt awing did not

'adequately reflect

a modified mounting configuration resulting

from a

PCM.

The inspector

reviewed drawing 8770-8-231,

sheet

27-2,

Rev 7, Instrument Installation Details,

which now

included the mounting details for the seven

containment

isolation valves.

Subsequent

to this violation, the inspectors

.

have inspected field conditions several

times prior to

containment closure.

The valves

have

been

mounted per the

drawing.

(3)

The licensee

used

carbon steel

nuts

on the

1A

ICW pump

casing-to-pump stuffing box joint vice the specified

316

stainless

steel

nuts.

In addition,

a single rubber gasket,

vice the required

f1 a'nge insulation kit, was installed

on

a

safety-related

lubricating water flanged joint'.

These

were found to be personnel errors'n

addition to

counseling

and correcting the specific problems,

the licensee

also verified fastener

hardware

on

a random selection of 11-

safety-related

valves

and

5 safety-related

pumps to see if the

fastener

problem was wide spread.

gC/PSL

LTR BK No.

196, dated

July 16,

1990,

and attached

gC Report

32006 documented

satisfactory 'conditions.

The licensee

also

changed

the

material control

program to add increased

accountability

and

responsibility..at the foreman/supervisor

levels

Based

on the inspecto'r's

review of the licensee's

corrective

actions, this item is closed'

b.

(Closed

- Units

1 and

2)

VIO 335,389/90-23-01,

Failure to Control

Material in Safety-Related

Repairs.

This violation involved two examples of failing to control- materials

used for 'safety-related repairs'ne

example

was the use of

unapproved

replacement

wire material

during

a

RPS selector

switch

replacements

The other example

was the use of an unapproved

sealant

on

a mechanical

seal. leak.

FPL letter L-90-455 responded

to the Notice of Violation.

The two.

items were evaluated

by engineering

and judged acceptable,

however

19

the wire was replaced with vendor-recommended

wire anyway.

The

licensee

determined that these

items,

along with VIO 335,389/90-30-

'lc, were

symptoms of a more fundamental

condition.

The maintenance

manager

issued

an interim letter describing the requirements.

Specific confirmation that all maintenance

personnel

reviewed this

letter was observed

by the inspector.

Subsequent

permanent

action

included:

gI 8-PR/PSL-l,

Rev 17, Identification Control of Haterials,

Parts,

and Components,

established

the licensee's

plan for

controlling material

used in the plant.

This incorporated

the

material

contained

in the maintenance

manager's initial letter.

AP 0010432,

Rev 62, Nuclear Plant

Work Orders,

provided

specific accountability

and direction to foremen/supervisors

concerning materials

used

on

a job.

These

program changes

appear to be effective.

This item is closed.

{Closed - Unit 2)

NCV 389/90-31-01,

Use of Unapproved

Procedures

for

PH of 2C

AFW Pump Governor.

This

NCV involved

a

PH that had not been

FRG approved

several

months

before.

The procedure

was subsequently

approved

and

a revision

has

'ince

been

FRG approved

and issued.

The licensee

also

has

changed

the corrective action request

system to adjust for a company

reorganization.

The inspectors

have frequently interfaced with the

current corrective action request

system

and found it to function

very well.

This item is closed.

(Closed

- Unit.1) VIO 335/91-22-02,

Loss of Containment Integrity

During Refueling.

This licensee-identified violation of TS 3.9.4.c.

involved the

issuance

of a "clearance" for work on

a

CCW relief valve inside

containment

[meaning that the system

was safe to work on] but not

issuing the

NPWO authorizing the start of work.

Unit

1 was being

refueled at the time.

Shop personnel,

thinking that they had

permission,

removed the valve.

This opened

a small flow path into

containment,

violating the refueling TS.

Licensee letter L-92-36 responded

to the Notice of Violation.

In

addition to counseling,

discussion

during training, etc,

the

licensee

changed

the equipment clearance

form per

OP 0010122,

Rev

51,

In Plant Equipment Clearance

Orders,

to require

by checkoff,

specific safety review for several

considerations,

such

as system

redundancy,

sensitive

system status,

mode related or not,

and

containment penetration.

The inspector

concluded that this highly

visible focus will improve coordinated

work control

and strengthen

the procedural

bar riers.

This item is closed.

20

e.

(Closed

- Unit 1) VIO 335/91-22-03,

Failure to Haintain

RCS In-

Process

Cleanliness

Controls.

This licensee-identified violation of Unit

1 TS 3.4.7 involved the

failure to control the quality of water used

by

a diver while high

pressure

water jet cleaning the reactor vessel

flange.

Domestic

water was used,

introducing into the

RCS chlorides

exceeding

the

TS

limit of 150 ppb.

Licensee letter L-92-56 responded

to the Notice of Violation.

In

addition to restoring the

RCS to proper chemistry conditions

and

performing

an engineering

evaluation of the consequences,

the

licensee

concluded that the cleaning evolution was inadequately

controlled

and, took several

steps to improve controls:

Since part of the root cause

involved connecting

the hose to

a

domestic water connection vice

a demineralized

water

connection, i.e., recognizing the correct system,

the licensee

added placards to the point of application,

the service

(domestic)

water hose connections,

warning that the water

cannot

be introduced internally into certain

named

systems,

and

neither internally nor externally into certain other

named

systems.

Additionally, placards

were

made for demineralized

and primary water systems stating that the water cannot

be

added to borated water

systems without specific permission.

Also, primary water placards

stated that it was radioactively

contaminated.

The inspector

has

observed

a number of these

placards installed about the plant.

The licensee shifted high pressure

water blasting inside

containment

from a "skill of the trade" activity to one

proceduralized

by GHP-06,

Rev 0, High Pressure

Water Blasting

Inside th'e Reactor

Containment Building.

While the procedure

has safety precautions

and communications

options, it focuses

on discussion with operations

concerning

proposed

water sources

prior to water blasting.

The licensee

changed

the Unit

1 and Unit 2 reactor vessel

maintenance

sequence

procedures

to include specific notes

at

the appropriate

locations to invoke the maintenance

procedure

for high pressure

water blasting.

The inspector

reviewed

procedures

1-H-0015,

Rev 21,

and 2-H-0036,

Rev 13, both titled

Reactor

Vessel

Haintenance

- Sequence

of Operations,

and found

the notes appropriate.

The inspector judged that these

upgrades will decrease

the

likelihood of this event repeating.

This item is closed.

f.

(Closed

- Unit 1) VIO 335/92-04-01,

Failure to Properly Store

Flammable Hateri als.

21

This violation involved alcohol being stored in plastic containers,

in a crew box, in a safety-related

electrical

equipment

room.

FPL responded

to this violation in letter L-92-99 and supplemented

the response

in letter L-92-125.

The licensee

immediately removed

the flammable material to an authorized

area

and stored it in safety

cans

in a flame-proof cabinet.

They then inspected

other crew boxes

and work areas,

found several

additional

examples,

and corrected

them.

The inspector'bserved

these activities in progress

at the

time.

The licensee

took a number of steps to prevent further

noncompliance,

including:

Following a staff survey to determine needs,'he

licensee

procured

about

50 flammable storage

cabinets for use throughout

the site.

Added standard

service contract requirements

that contractors

must obtain

a flammable storage

cabinet for any flammable

products they

use.'rovided

for crew box identification and for access

to all crew

boxes

by the fire and safety inspectors.

Added inspection of crew boxes to the fire equipment

and

systems

inspection check-off sheet.

Addressed

storage of flammable material

in at least the safety

meetings

on June

11, July 17,

and August 13,

1992.

gCIR IE92-810 documented

a

gC surveillance of the site chemical

control

program (including flammable storage)

on August 27,

1992.

The

gC inspector

found the large

number of areas

~inspected satisfactory.

The inspector

has monitored these

changes

throughout the period

subsequent

to the violation and has also toured the area with the

fire inspectors.

The inspector

concludes that the licensee

has

been

very responsive

to the Notice of Violation and that the flammable

storage.

program is much improved.

This item is closed.

g.

(Open

- Unit 2) VIO 389/92-07-03,

Isolation of Containment

Pressure

Sensing

Line Without Placing Effected Instrumentation

Channels

in

TRIP or BYPASS.

This violation involved the inadvertent

capping of a small

instrument line inside containment.

.Since it was not planned,

the

licensee

did not take actions to place affected instrumentation

in

BYPASS 'or TRIP.

The inspector

had identified several

contributors

i.ncluding:

Lack of plain identification of the tubing stubs sticking into

containment.

'2

Lack of protection of the open tubing ends to prevent insect

entry or the insertion of debris.

The exposed

threads

on the tubing ends inviting the

installation of a cap.

Lack of periodic surveillance to demonstrate

clear passage

through atmospheric

sensing tubing.

Lack of a check prior to entering

a mode where atmospheric

sensing

is required.

FPL letter L-92-172 responded

to the Notice of Violatiori.

In

addition to the licensee

removing the cap,

the licensee

evaluated

the maintenance

and operating history, performed

a

PRA,

and

performed

an engineering

analysis.

Since the system is

a "2 of 4

channel

to operate"

system,

the inspector concurred with the

licensee's

finding,that the safety significance of capping

one line

was small.

h

Other corrective actions

included the following:

The inspector

observed

the licensee

performing

a pressurized

air test of all other Unit

1 and Unit 2 containment

pressure

transmitter

sensing lines

on Hay 7,

1992,

per Unit

1

NPWO

7340/63

and Unit 2

NPWO 7452/64.

The inspector also observed

the initial performance of ILC

Procedure

1400205,

Rev 0,

on Unit 2 per

NPWO 8158/64.

This

initial performance

was receiving full-time jobsite supervision

by an

I&C supervisor.

The supervisor properly stopped

the work

twice to correct procedure errors with temporary

changes

prior

to proceeding.

The licensee installed

mud dauber

caps

on Unit 2 sensing lines

per

NPWO 7613/64

and

PCH 157-292M.

The inspector confirmed

their presence

du}ing a containment

inspection prior to Unit 2

entering

Mode

4 on June

21,

1992.

The inspector

observed

the sensing line labels

added inside

Unit 2 containment during

a containment

inspection prior to

Unit 2 entering

Mode

4 on June

21,

1992.

The licensee

changed

AP 0010728,

Post" Outage

Review, Section

8.3,

Mode

4 prerequisites,

to require

an

I&C signature that

I&C

Procedure

1400205 is completed prior to entering

mode

4 during

a startup.

The inspector

observed this in procedure revision 9.

Items remaining to be inspected

are:

Drawing changes for both Unit

1 and 2.

23

Mud dauber

cap installation for Unit

1 during the Spring,

1993,

refueling.

Tagging of Unit

1 penetrations

during the Spring,

1993,

outage.

Performance

of IEC 1400205

on Unit

1 during the Spring,

1993,

outage.

Corrective action to" date is adequate,

however this item remains

open pending review of drawings

and Unit

1 items.

h.

(Closed

- Unit 2) VIO 389/92-07-04,

Failure to Follow the Procedure

for Setting

Steam Generator

Safety Valves.

This

TS violation involved the use of gages with inadequate

accuracy

to set

SG code safety valves,.

The two gages

were both labeled

as

being outside the procedural

requirements,

-which was not questioned,

and

one

was actually outside the procedural

requirements.

FPL letter L-92-172 responded

to this Notice of Violation.

Immediate corrective action included obtaining proper gages,

repeating

the testing already

accomplished,

and then completing the

setting in the required

manner.

This was verified by the inspector

at the time.

Additional-corrective action

was

based

on the licensee

recognizing

that they

had confused

the gage accuracy

requirements

for setting

code safety valves to +/-

1 percent of the setpoint with the less

stringent

accuracy

requirements

for pump

and valve testing.

additional corrective aetio'ns

included:

Procedure

GNP-0705

was revised to clarify accuracy

requirements,

place the requirements

in the various procedure

sections,

and

add both

a management

approval point and

a

OC

hold point to verify proper gages.

The acceptable

setpoint

range

was reduced to account for possible

gage inaccuracy.

The

inspector

reviewed

GNP-0705,

Rev 19.

Procedure

GMP-02,Rev 5,

Use of %TE by Mechanical

Maintenance,

was revised to spec'ify the required

gage accuracies

for several

purposes.

Procedure

GNP-0017,

Rev 25, Pressurizer

Safety Valve

Maintenance,

had

been

changed to address

gage

accuracy

and

range requirements,

Procedure

GMP-0810,

Rev 12,

Bench Testing of*Safety Relief

Valves,

had

been

changed

to include the requirement that gage

accuracy,

range,

and type

be proper

and

added

the requirement

that the supervisor

and

gC verify the selected

gage.

24,

The licensee

has

made widespread

program evaluations

and changes

to

address

this violation.

Performance

is routinely monitored

as part

of the inspection

program.

This includes -routinely planned

inspections

during the Spring,

1993, refueling outage.

This -item is

closed.

(Closed

- Unit 2) VIO 389/92-11-01,

Failure. to Restore

Peripheral

Components to Service Following Equipment Modification.

This violation involved failure of one [assist]

shop to restore

a

seismic conduit support after removing it to provide another

[principal] shop access

to complete

a modification in the area.

FPL responded

to this violation by .letter L-92-244, dated

September

9,

1992.

FPL evaluated

the as-found conditions

and found that the

subject conduit

and component

had

been operable while not attached

to the support.

The licensee

found that there were two reasons

for

the violation:

AP 0010432,

Nuclear Plant Work Orders,

lacked guidance to

planners

concerning

work order planning

on seismic structures,.

The procedure

was changed to include planning guidance

and

a

post work check for reinstallation of seismic

components.

Personnel

error

on the part of the maintenance

workers

and

" supervisors.

Maintenance

department'supervisors,

planners,.

foremen,

and journeymen

were refreshed

in this area during

refresher training completed

by September

30,

1992.

The inspector

reviewed the licensee's

response,

reviewed

AP 0010432,

Rev 62, Nuclear Plant Work Orders,

reviewed the operability

calculation,

and reviewed the training'records

and lesson

plans with

the maintenance

training supervisor.

The inspector

concurred with

the licensee's

evaluation

and corrective actions.

This item is

closed.

(Closed

- Units

1 and 2) VIO 335,389/91-22-01,

Failure to Translate

TS Requirements

for Fuel Oil Testing.

This licensee-identified violation of TS 4.8. 1. 1.2d involved the

failure to correctly identify or employ

a chemical

reagent

used in

EDG fuel oil particulate determination.

A particulate-contaminated

fuel oil shipment

was not detected,

was introduced into the site's

fuel oil system,

and resulted

in technical inoperability of three of

four fuel oil tanks.

Licensee letter L-92-36 responded

to the Notice of Violation.

In

- addition to correcting procedure

C-121,

"Determination of

Particulate

Contamination;

and

Check for Clear

and Hright Appearance

with Proper Color Diesel

82 Fuel Oil", to identify the correct

reagent,

the licensee

performed the following:

25

The licensee

returned the fuel oil storage

tanks to particulate

specification without violating the

TS time constraints.

A

contractor recirculated

and filtered the storage

tanks.

An outside contractor reviewed the corrected analytical

procedure

and confirmed the procedure to be technically correct

beyond the action stated

in corrective action letter L-92-36,

the licensee

purchased

a portable fuel oil filtration skid for

routine plant use.

This skid has

been

used to receive

and

process

fuel oil shipments

as

an enhancement

to TS

requirements.

The inspector judged that the correcti.ve, actions will decrease

the

likelihood of this event repeating.

This item is closed.

The inspectors

found the corrective actions fot those violations to be

significant and to be .focused

on the generalized

conditions

and root

causes

vice just the specific instance of violation.

13.

Exit Interview

The inspection

scope

and findings were summarized

on November 24,

1992,

with those

persons

indicated in paragraph

1 above.

The inspector

described

the areas

inspected

and discussed

in detail the inspection

results listed below, except for VIO 335/92-21-07,

Failure to Adequately

Maintain Containment

Vessel

Integrity.

Proprietary material is not

contained

in this report.

Dissenting

comments

were not rec'eived

from the

licensee

on November

24.

VIO 335,389/92-21-07

was discussed

with the licensee during telephone

conversations

between

FPL management

and

NRC Region II management

on

December

1,

1992.

The inspection

scope

and findings concerning

VIO

335,389/92-21-07

had" previously

been

summarized

during the exit interview

for IR 335,389/92-16

on August 10,

1992.

Dissenting

comments

from the

licensee

on August

10 regarding that violation are stated

below:

The only valves involved in containment

vessel integrity were those

identified by number in the

TS or perhaps

the

UFSAR.

The licensee

stated that they believed that the

NRC had previously considered

the

situation

when the facility license

was issued

and,

by not

specifically identifying in the

TS the vent

and drain valves or

other fittings, had determined

them not required to be under the

TS

controls.

The licensee specifically stated that all vent, drain,

and test valves

and fittings located in the containment penetration

areas

were not required to be secured

in position

and were not

required to be surveillance

checked

at least

once per

31 days per

TS 4.6.1.1.

The

NRC carefully considered

the licensee's

position

on this matter but

concluded that the licensee

was incorrect

and

had

been in violation of

the subject

TS.

Item Number

335/P21-90-005

389/P21-90-005

Status

open

closed

P21-

P21-

Descri tion and Reference

Broken Swing Arms for Check Valves,

paragraph ll.a.

Broken Swing Arms for Check Valves,

paragraph

11.a.

335,389/P21-91-006

closed

335,389/90-13-01

closed

P21-

VIO-

Overspeed Trip Tappets for Terry

Steam Turbine

Pump Drivers,

paragraph

ll.b.

Failure to Ensure guality at Least

Equivalent to That Specified in the

Original Design Basis or Requirements

'- Three

Examples,

paragraph

12.a.

335)389/90-23-01

389/90-31-01

335,389/91-22-01

335/91-22-02

335/91-22-03

335/92-04-01

389/92-07-03

389/92-07-04

389/92-11-01

closed

closed

closed

closed

closed

closed

open

closed

closed

VIO-

NCV-

VIO-

VIO-

VIO-

VIO-

VIO-

VIO-

VIO-

Failure to Control Haterial in

Safety-Related

Repairs,

paragraph

12.b.

Use of Unapproved

Procedures

for PH

of 2C

AFW Pump Governor,

paragraph

12.c.

Failure to Translate

TS Requirements

for Fuel Oil Testing,

paragraph l2.j.

Loss of Containment Integrity During

Refueling,

paragraph

12.d.

Failure to Haintain

RCS In-Process

Cleanliness

Controls,

paragraph

12.e.

Failure to Properly Store

Flammable

Haterials,

paragraph

12.f.

Isolation of Containment

Pressure

Sensing

Line Without Placing Effected

Instrumentation

Channels

in TRIP or

BVPASS, paragraph

12.g.

Failure to Follow the Procedure for

Setting

Steam Generator

Safety

Valves,

paragraph

12.h.

Failure to Restore

Peripheral

Components

to Service Following

Equipment Hodification, paragraph

12.i.

27

335/92-21-01

389/92-21-02

389/92-21-03

389/92-21-04

389/92-21-05

closed

NCV -

LTOP Technical Specification

Amendment

Implementation Failure,

paragraph

8.a.

closed

NCV - Failure to Implement

New TS

Requirements

for Emergency

Bus

Undervoltage,

paragraph

8.d.

closed

NCV - Hissed Surveillance

on

a Radiation

Monitor Being Returned to Service

Due

to Personnel

Error, paragraph

B.e.

closed

NCV - Hissed Technical Specification

Surveillance,

paragraph

8.h.

closed

NCV - Incomplete Technical Specification

Special

Report,

paragraph

7.

389/92-21-06

open

335,389/92-21-07

.= open

URI - Operation

Above the Licensed

Power

Level, paragraph 3.b.(4),

VIO -- Failure to Adequately Maintain

Containment

Vessel Integrity,

paragraph

10.

Abbreviations,

Acronyms,

and Initialisms

AC

A/E

AFAS

AFM

AP

ATTN

CAR

CCM

CEA

CFR

CNRB

CS

DC

DDPS

DEH

DPR

ECCS

EDG

EFPD

EFPY

ESF

F

FCR

FCV

FOP

Alternating Current

Architect/Engineer

Auxiliary Feedwater Actuation System

Auxiliary Feedwater

(system)

Administrative Procedure

Attention

Corrective Action Request

Component

Cooling Mater

Control

Element Assembly

.-

Code of Federal

Regulations

Company Nuclear Review Board

Containment

Spray

(system)

Direct Current

Digital Data Processing

System

Digital Electro-Hydraulic (turbine control

system)

Demonstration

Power Reactor

(A type of operating license)

Emergency

Core Cooling System

Emergency Diesel Generator

Effective Full Power

Days

Effective Full Power Years

Engineered

Safety Feature

Fahrenheit

Field Change

Request

'low

Control Valve

Feedback of Operating

Experience

Program

.

FPL

FRG

FSAR

GHP

HCV

HPSI

IKC

ICW

ILRT

IR

ISEG

JPN

LCO

LER

LOCA

LPSI

LTOP

LTR BK

H&TE

MFIV

HTC

HV

HW

HWe

HWt

NI

No.

NPF

NPWO

NRC

NUREG

ohm

ONOP

OP

PCM

PCH

ppb

ppm

PRA

PSL

QA

QC

QCIR

QI

RCS

RDT

Rev

RG

RPS

RTD

RWT

,SG

28

(system)

e Electrical Generator]

eactor]

operating license)

blication)

The Florida Power

5 Light Company

Facility Review Group

Final Safety Analysis Report

General

Maintenance

Procedure

Hydraulic Control Valve

High Pressure

Safety Injection (system)

Instrumentation

and Control

Intake Cool,ing Water

Integrated

Leak Rate Test(ing)

[NRC] Inspection

Report

Independent

Safety Engineering

Group

(Juno

Beach)

Nuclear Engineering

TS Limiting Condition for Operation

Licensee- Event Report

Loss of Coolant Accident

Low Pressure

Safety Injection (system)

Low Temperature

Overpressure

Protection

Letter Book

Measuring

5 Test

Equipment

Hain Feed Isolation Valve

. Moderator Temperature

Coefficient

Hotorized Valve

Megawatt(s)

Megawatt(s),

Electrical

[Energy from th

Megawatt(s),

Thermal

[Energy from .the

R

Nuclear Instrument

Number

Nuclear Production Facility (a type of

Nuclear Plant

Work Order

Nuclear Regulatory

Commission

Nuclear Regulatory

(NRC Headquarters

Pu

Unit of Electrical

Resistance

Off Normal Operating

Procedure

Operating

Procedure

Plant Change/Modification

PerCent Milli (0.00001)

Part(s)

per Billion

Part(s)

per Million

Probabilistic Risk Assessment

Plant St. Lucie

Quality Assurance

Quality Control

Quality Control Inspection

Report

Quality Instruction

Reactor Coolant

System

Reactor Drain Tank

Revision

[NRC] Regulatory

Guide

Reactor Protection

System

Resistive

Temperature

Detector

Refueling- Water Tank

'team Generator

St.

STA

TE

,TFE

TS

UFSAR

URI

VAC

VIO

.

29

Saint

Shift Technical

Advisor

Temperature

Element

A Type of Teflon

Technical Specification(s)

Updated Final Safety Analysis Report

[NRC] Unresolved

Item

Volts Alternating Current

Violation (of NRC requirements)