ML17227A329

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Insp Repts 50-335/91-27 & 50-389/91-27 on 911223-920127. Violation Noted.Major Areas Inspected:Plant Operations Review,Maint Observations,Surveillance Observations,Review of Nonroutine Events & Fire Protection Review
ML17227A329
Person / Time
Site: Saint Lucie  
Issue date: 02/25/1992
From: Elrod S, Landis K, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17227A327 List:
References
50-335-91-27, 50-389-91-27, IEB-88-003, IEB-88-3, NUDOCS 9203100083
Download: ML17227A329 (27)


See also: IR 05000335/1991027

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/91-27

and 50-389/91-27-

Licensee:

Fl ori da

Power

& Light Co

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License Nos.:

DPR-67

and

NPF-16

Inspection

Conducted:

De ember 23,

1991 - January

27,

1992

Inspectors:

S.

A. lr', Senior Resident

Inspector

/j'

zs

gz

Date Signed

M. A.

ot,

ident Inspector

/

Approved by:

.

D.

L

dis, Section Chief

Division of Reactor Projects

Date Signed

S ss

Pz-

a'te Signe

SUMMARY

Scope:

This routine resident

inspection

was

conducted

onsite

in the

areas

of plant

operations- review, maintenance

observations,

surveillance

observations,

review

of nonroutine

events,

fire protection

review,

. and

followup of previous

inspection findings.

Results:

This

inspection

addressed

normal

at-power

activities

and

two

downpower

evolutions for repairs

conducted

on Unit 2.

Unit

2

passed

400

days

of

continuous

operation this inspection period.

Surveillance

and maintenance

were

well coordinated

with plant operations

in

a

number of areas.

One occasion

where

operators

did

not practice

meticulous

equipment

status

control

was

observed.

Within the areas

inspected,

the following violation was identified:

VIO 335/91-027-01

- Failure

to Follow Equipment

Control

Procedures,

paragraph

2.b.

Within the areas

inspected,

the following noncited violations were identified:

NCV 389/91-027-02,

Engineered

Safety

Features

Actuation

Channel

Out-of-

Service

Due to Personnel

Error, paragraph

6.a.

9203100083

920225

PDR

ADOCK 05000335

G

PDR

NCV 335/91-027-03,

Technical

Specification

required

plant

vent

stack

radiation

sampler

and monitor inappropriately out-of-service,

paragraph

6.b.

NCV 335/91-027-04

Failure to Follow Work Control Procedure,

paragraph

8.

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

D.

  • 'G
  • J
  • H.

C.

R.

R.

R.

  • R.

'C.

L.

G.

A.

T.

L.

N.

C.

D.

J.

W.

D.

E.

Sager,

St. Lucie Plant Vice President

Boissy, Plant General

Manager

Barrow, Fire/Safety Coordinator-

Buchanan,

Health Physics Supervisor

Burton, Operations

Manager

Church,

Independent

Safety Engineering'Grou

Dawson,

Maintenance

Manager

.

Englmeier,

Nuclear Assurance

Manager

Frechette,

Chemistry Supervisor

Leppla,

Instrument

and Control Supervisor

McLaughlin, Licensing Manager

Madden, Plant Licensing Engineer

Menocal, Mechanical

Supervisor

Roberts,

Site Engineering

Manager

Rogers, Electrical Supervisor

Roos,

Services

Manager

Scott,

Outage

Manager

West, Technical

Manager

West, Operations

Supervisor

White, Security Supervisor

Wolf, Site Engineering Supervisor

Wunderlich,

Reactor Engineering Supervisor

p Chairman

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

mechanics,

security force members,

and office personnel.

NRC Employees

  • S. Elrod, Senior Resident

Inspector

  • M. Scott,

Resident

Inspector

  • Attended exit interview

2.

Acro'nyms

and initialisms used

throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

Unit

1

began

the

inspection

period

returning

to

power following a

refueling outage.

The unit ended

the inspection

period in day

35 of power

operation.

Unit

2

began

and

ended

the

inspection

period

at

power,

day

417 of

continuous

power operation.

a 0

Plant Tours

The

inspectors

periodically conducted

plant tours

to verify that

monitoring

equipment

was

recording

as

required,

equipment

was

properly tagged,

operations

personnel

were aware of plant conditions,

and plant housekeeping

efforts were

adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean areas

were being controlled in accordance

with procedures,

excess

equipment

or material

was

stored properly,

and combustible materials

and debris

were disposed of expeditiously.

During tours,

the 'inspectors

looked for the

existence

of unusual

fluid leaks,

piping vibrations,

pipe hanger

and seismic .restraint

settings,

various valve

and breaker positions,

equipment caution

and

danger

tags,

component

positions,

adequacy

of fire fighting

equipment,

and

instrument

calibration

dates.

Some

tours

were

conducted

on backshifts.

The frequency of plant tours

and control

room visits

by site management

was noted to be adequate.

The inspectors

routinely conducted

partial

walkdowns of ESF,

ECCS,

and. support

systems.

Valve,

breaker,

and

switch

lineups

and

equipment

conditions

were

randomly verified both locally .and in the

control

room.

The following accessible-area

ESF

system

and

area

walkdowns were

made to verify that system lineups

were in accordance

with licensee

requirements

for operability

and

equipment material

conditions we'e satisfactory:

Unit

1

ECCS space,

Unit 2 fan'ooms,

Unit

1

SFP area

and

FHB system,

and

Unit 2

SFP area

and

FHB system.

b.

Plant Operations

Review

The

inspectors

periodically

reviewed shift logs

and

operations

'records,

including data

sheets,

instrument traces,

and records

of

equipment

malfunctions.

This review included control

room logs

and

auxiliary logs,

operating

orders,

standing

orders,

jumper logs,

and

equipment tagout records.

The inspectors

routinely observed

operator

alertness

and

demeanor

during plant tours.

They

observed

and

evaluated

control

room staffing, control

room access,

and .operator

performance

during routine

operations.

The inspectors

conducted

random off-hours inspections

to ensure

that operations

and security

performance

remained

at acceptable

levels.

Shift turnovers

were

observed

to verify that

they

were

conducted

in accordance

with

approved

licensee

procedures.

Control

room annunciator

status

was

veri.fied.

Except

as noted below,

no deficiencies

were observed.-

During this i nspection

period,

the inspectors

reviewed the following

tagouts

(clearances):

1-12-2

Administrative Control of Equipment tags

44 - 52 for

valves

V08562 to V08570 on the "A" train MSIV, and

1-11-259

LS-14-2A, Level switch to

CCW surge tank.

On

December

23,

in Mode

1,

while transferring

the Unit

1

electrical

power

source

from the startup

transformers

to the

Unit

1 auxiliary transformers,

the

control

room operators

observed

indications of improper switchgear functioning.

After

the

transfer,

a current

reading

on

the A-train auxiliary

transformer

feed

ammeter

showed

the

auxiliary transformer

breaker

to be closed,

however,

the breaker position indicating

lights were both dimly lit.

Operators

also

observed

that the

startup

transformer

breaker

position lights

showed

that

the

startup

breaker

was still closed.

The operators

immediately

stopped

power ascension

activities,

notified their management,

and investigated

the condition.

They

determined

that both circuit breakers

were closed,

and that the

startup

transformer circuit breaker

would not

open remotely.

The

problem

was

found to be

a poor contact

in the auxiliary

transformer circuit breaker control circuit.

While troubleshooting

these circuit breakers,

the

operators

racked out the

1A startup transformer circuit breaker,

moved it

several

feet

away from the switchgear,

and tested it. It was

reinstalled within minutes.

TS 3.8. 1. 1. required,

in part,

two

physically independent circuits between

the offsite transmission

network

and

the onsite

Class

1E distribution system

be operable

while in Modes

1, 2, 3,

and 4.

The action statement

required,

in part,

return

to service

of inoperable circuits within 72

hours.

The licensee

met this time requirement.

However,

when

the

operators

racked

out the

lA startup

transformer circuit

breaker,

they did not declare it inoperable

per

TS 3.8. 1. 1 nor

did they log this action in the

TS Equipment Out-Of-Service

Log

per

OP 0010129,

Rev

18,

Equipment

Out of Service.

The licensee

stated that the reasoning

followed was the

same

as the reasoning

that allows temporary disablement of the

EDG start circuit while

manually rotating

the

EDG prior to surveillance

runs without

declaring it out of service

and testing

the other

EDG.

The

inspector

judged this logic faulty since safety considerations

allowed to support

required

surveillances

do not necessarily

apply

to

troubleshooting

and

repair.

Also,

the

actions

described

above

were not consistent

with known licensee

policy

and routine

inspector observations

of the

removal

fromservice

process:

Unit

1

TS 6.8. l.a requires that'ritten

procedures

shall

be

established,

implemented,

and maintained

covering the activities

recoranended

in Appendix

A of Regulatory

Guide 1.33, Revision 2,

February

1978.

Appendix A, paragraph

1 included procedures

for

equipment control

and for log entrys.

This was

implemented

on

site in part

by

OP 0010129,

Rev 18,

Equipment Out-0f-Service,

which required that all equipment required

by TS shall

be logged

in the Equipment Out-of-Service

Log when that equipment

has

been

determined

to

be inoperable.

Failure to declare

the A-train

offsite circuit out-of-service

and

log the condition in the

Equipment Out-of-Service

Log when that equipment

had

been

made

inoperable

by

removing

the circuit breaker

was

a violation

of

TS 6.8. 1.

This is

VIO 335/91-027-01,

Failure to Follow

Equipment Control Procedures.

On January

19, the licensee

discovered lightly wetted lagging

on

Unit

2

valve

V12424,

the

4A heater

feedwater

inlet valve

(nominally operating

at

330

degrees

F,

450 psig).-

This 24-

inch, carbon steel,

Pacific brand,

gate

valve was

a secondary

plant valve and not directly safety-related.

By January

21, the

lagging

was

removed,

exposing

a through wall pinhole leak in the

valve

body.

The

same

day,

the

licensee

downpowered

to

approximately

60 percent

power to investigate this leak,

and

also

investigate

a

TCW heat

exchanger

tube

leak

and

clean

condenser

waterboxes.

Ultrasonic

and magnetic particle testing

and inspection of the area

around the pinhole revealed that the

valve

base

material

was

sound.

Previous

inspection

of the

adjacent

pipe,

performed

during

the last outage,

revealed

no

degradation

from erosion.

The

licensee

concluded

that

the

pinhole

was

a casting flaw (porosity) that would not propagate.

A licensee

contractor

sealed

the pinhole

on January

23 with

a

leak repair plug and external

band following restoration of the

valve to normal operating

temperature.

Following these repairs,

the plant

was returned

to its normal configuration.

Permanent

weld repair using heat treatment,

was deferred until the April

1992 refueling outage.

On

the

morning

of January

26,

the

licensee

observed

a

lubricating oil leak

from

2B main feedwater

pump

instrument

tubing.

The 'tubing from the lubricating oil

pump di.scharge,

was

bent at

a point beneath 'a pressure

gage.

The cause

and time at

which the

bend

occurred

were

unknown.

Oil was leaking

from a

tubing fitting that

was

cracked

around

one-fourth

the

circumference.

The unit was

down-powered

to approximately

45

percent for replacement

of the tubing.

A new tubing assembly

was

preassembled

and

staged

prior to field work commencing.

Power

ascension

in the early afternoon

of the

same

day

was

uneventful.

c.

Technical Specification

Compliance

Licensee

compliance

with selected

TS

LCOs

was verified.

This

included

the review of selected

surveillance test results.

These

verifications

were

accomplished

by direct observation of monitoring

instrumentation,

valve positions,

and switch positions,

and

by review

of completed

logs

and records.

Instrumentation

and recorder

traces

were observed for abnormalities.

The licensee's

compliance with LCO

action

statements

was

reviewed

-on selected

occurrences'-

as

they

happened.

The inspectors

verified that related plant procedures

in

use were adequate,

complete,

and included the most recent revisions.

d.

Physical

Protection

The inspectors verified by observation

during routine activities that

security

program plans

were being implemented

as evidenced

by: proper

display of picture badges;

searching of packages

and personnel

at the

plant entrance;

and vital area portals being locked and alarmed.

The licensee's

attention

to plant conditions

and

prompt correction of

degradations

was

a

key factor in continued excellent plant performance.

The failure to declare

equipment

out-of-service for troubleshooting

and

maintenance

is considered

an isolated instance.

3.

Surveillance

Observations

(61726)

Various

plant

operations

were verified to

comply with selected

TS

requirements.

Typical of these

were confirmation of TS compliance for

reactor coolant chemistry,

RWT conditions,

containment

pressure,

control

room ventilation,

and

AC

and

DC electrical

sources.

The inspectors

verified that

testing

was

performed

in

accordance

with

adequate

procedures,

test

instrumentation

was calibrated,

LCOs were met,

removal

and restoration

of the affected

components

were

accomplished

properly,

test results

met requirements

and

were reviewed

by personnel

other than

the individual directing the test,

and that

any deficiencies

identified

during the testing

were properly

reviewed

and

resolved

by appropriate

management

personnel.

The surveillance tests

discussed

in the following

paragraphs

were observed:

a.

OP 2-0110050,

Rev ll, Control

Element Assembly Periodic Exercise.

b.

18C

1-0700051,

Rev

11, Auxiliary Feedwater

Actuation System Monthly

Functional

Test.

c.

OP 2-0700050,

Rev 26, Auxiliary Feedwater'eriodic

Test,

Data Sheets

"A" and "8", for the

2A and

2B pumps.

OP 2-2200050,

Rev 37,

Emergency

Diesel

Generator

Periodic Test

and

General

Operating Instructions:

During this surveillance,

performed

on

December

26,

1991

the

EDG

performed well, however

one of the two solenoid-operated

valves that

refi 1 1

the

fuel

day

tanks

failed

to function

automati cal ly'.

Independent

local

and

remote

tank level

alarms

functioned properly

and

manual

valve operation

was easily

accomplished

and successful.

The

operator

replaced

a

blown fuse

and

the circuit functioned

correctly during subsequent

automatic

operation.

Subsequent

review

showed that, following the tank level alarm,

the

12 cylinder engine

was capable of almost

two hours of operation with no operator action.

The surveillance

test

required

one

hour of operation

plus

a

few

minutes for startup,

and

shutdown.

The licensee initially credited

operator

action

concerning

fuel

transfer

and

considered

the

surveillance satisfactory.

Subsequent

inspector

review of Unit

2

TS 3/4.8. 1

showed

that

TS

surveillance

step

3 required that the operator "verify that the fuel

transfer

pump

can

be started

and transfers

fuel

from the storage

system to the engine-mounted

tank."

The inspector

reviewed

RG

1. 108,

Rev

1,

and

determined

that

the

surveillance

would

be considered

a valid test

per criterion e.(3),

which, involved

a successful

start,

successful

loading to at least

50

percent of full load,

and continued operation for at least

one hour.

Since these

two criteria are not always compatible

and

TS 4.8.1 deals

directly with TS operability, the inspector questioned

the licensee's

determination.

The licensee,

then reclassified

the surveillance

as

failed, carried

out required

TS actions,

and though troubleshooting

could find

no faulty components,

replaced

the

alarm module since

these

had failed

more frequently than other components.

Since

the

degree of operator

action allowed during surveillances

was not clear,

the inspector

intends

to clarify it through correspondence

with NRC

Region II and Headquarters

staffs.

OP 3200051,

Rev 8, At Power Determination of Moderator Temperature

Coefficient:

'nit

1 following post-refueling startup,

and

Unit

2

near

300

ppm

RCS boric acid

concentration

per

TS 4.1.1.4.2.

This test is

an infrequently performed evolution per

AP 0010020,

Rev

0, Conduct of Infrequently Performed Tests or Evolutions at St. Lucie

Plant.

The

required

pre-evolution

briefings

were excellent

and

oversight

and attention

to detail

by management,

SROs,

RCOs,

and the

reactor

engineers

was meticulo'us.

Both tests

reached, satisfactory

conclusions.

The

above

tests

were carried

out satisfactorily with good coordination

among

the participating

groups,

non-licensed

operators,

and

licensed

operators.

f.

OP 2-2200050,

Rev 38,

Emergency

Diesel

Generator

Periodic Test, for

the

28

EDG.

4.

Maintenance

Observation

.(62703)

Station

maintenance

activities involving selected

safety-related

systems

and

components

were

observed/reviewed

to ascertain

that

they

were

conducted

in accordance

with requirements.

The following items

were

considered

during

this

review:

LCOs

were

met;

activities

were,

accomplished

using

approved

procedures;

functional

tests

and/or

calibrations

were

performed prior to returning

components

or'ystems

to

service;

quality control

records

were

maintained;

activities

were

accomplished

by qualified

personnel;

parts

and

materials

used

were

properly certified;

and

radiological

controls

were

implemented

as

required.

Work requests

were

reviewed

to determine

the

status

.of'utstanding

jobs

and

to

ensure

that

priority

was

assigned

to

safety-related

equipment.

Portions

of

the

following maintenance

activities were obs'erved:

a.

NPWO 4874/65

provided work control instruction for the

bench testing

of the

1A

ICW MFA relay (f4 on

CMD 832);

b.

NPWO

6843/64

provided

work

control

instruction

for

the

troubleshooting

and. subsequent

testing of the pressurizer

pressure

SIAS module

BA 106

on channel

"HA";

c.

NPMO

6939/63

provided

work control for the

troubleshooting

and

calibration of FT 2212-1 loop for the Unit

1 charging

header flow;

d.

NPWO

4870/65

provided

work control for the

troubleshooting

and

component

replacement

of the "in sync" light on the

1C instrument

bus

inverter;

e.

'PMO 6880/64 provided work control for the removal

and calibration of

PI

1102D, Unit 2

"HD" channel

RCS pressure,

that

had drifted in its

calibration;

and,

5.

f.

NPWO 6894/64 provided work control for the troubleshooting

and repair

of 2C

AFW pump discharge

flow recorder

FR 09-2C.

l

The

above

observed

activities

were

performed

acceptably

with

good

interface with operations

personnel.

Fire Protection

Review (64704)

During the course of their normal tours,

the inspectors

routinely examined

facets of the Fire Protection

Program.

The inspectors

reviewed transient

fire'oads,

flammable

materials

storage,

housekeeping,

control

of

hazardous

chemi ca 1 s,

and fire barri ers.

The observed fire protection'ctivities

and fe'atures

were acceptable.

6.

Onsite

Followup of Written Nonroutine

Event

Reports

(Units

1

and

2)

(92700)

LERs were

reviewed for potential

generic

impact, to detect trends,

and to

determine

whether corrective

actions

appeared

appropriate.

Events that

the

licensee

reported

immediately

were

reviewed

as

they

occurred

to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with

the current

NRC Enforcement Policy.

LER 335/91-09

w'as closed.

a.

(Open - Unit 2)

LER 389/91-06,

Engineered

Safety, Features

Actuation

Channel

Out of Service

Due to Personnel

Error.

This

LER reported

a licensee-identified

TS violation where

RAS

channel

"0" had been

placed in bypass

in lieu of the required tripped

state

when taken out of service.

The channel

remained

in this state

for 69 hours7.986111e-4 days <br />0.0192 hours <br />1.140873e-4 weeks <br />2.62545e-5 months <br />,

exceeding

the

TS 3.3.2 "return to operable

or be placed

in trip" statement

of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

.The difference

between

"bypass"

and

"trip" positions for the

RAS channels

is that the resulting trip

logic is two out of three

when bypassing

one channel

and one out of

three

when tripping one channel.

The

licensee

had

completed

or initiated the following corrective

action via the in-house corrective action

systems

as stated

in the

LER text:

counselled

the responsible

licensed

personnel;

issued

open item notice 91-26 (2) requesting training department

evaluation of the event

as

a training item;

repaired

the faulted channel;

issued

open

item notice

91-26

(4) requesting

review of the

equipment out of service

process;

and,

issued

open

item notice

91-26

(5) for human factors

oriented

modification of the bypass

key.

The tentative

due date for items 91-26-(2),

(4),

and

(5) above is

March

1,

1992.

The last

two actions

above

are also

addressed

by

Corrective action request

1'22691

from the

gA department

on site.

The

RAS

channel

bypass

key will be modified to have

a chain

and

instruction tab attached.

The instructions will remind the operator

of the appropriate

TS instruction and required deviation log entry to

be

made

when the

key is used.

The

human factors

approach

to

RAS

bypass

key use

should provide

a positive reminder of proper usage.

LER 389/91-06 will remain

open

pending corrective action completion.

Failure

to trip the

RAS signal

as

required

by

TS is closed

NCV

389/91-027-02,

Engineered

Safety

Features

Actuation

Channel

Out of

Service

Due to Personnel

Error.

It is not being cited

because

the

licensee's

corrective

actions

associated

with this event

met

NRC

Enforcement Policy Section

V.G criteria for not issuing

a Notice of

Violation.

b.

(Closed - Unit 1)

LER 335/91-09,

Removal

of the Plant

Vent Stack

Monitors From Service Resulted

in a Condition Prohibited

by Technical

Specification.

This

LER reported

a licensee-identified

TS violation where the plant

vent

stack

particulate

sampler;

iodine

sampler,

and

noble

gas

activity monitor

was

taken

out of service

without initiating

appropriate

TS 3.3.3. 10 required alternate

sample collection.

With

the unit in

Mode 6, this condition existed for approximately

12

hours.

During this time period, there

were

no activities that could

have resulted

in an abnormal

gaseous

release.

The root cause

was

a cognitive personnel

error by utility licensed

operators

for referencing

an inappropriate

TS requirement pertaining

to radiation monitoring instrumentation.

TS 3.3.3. 1 required

one

channel

of noble

gas effluent monitor of the plant vent system to be

in service

during

Modes

1,2,3,

and

4.

TS 3.3.3. 10 required

particulate,

iodine,

and

noble

gas monitoring at all times via the

sampler/monitor

or

by grab samples.

The

stated

corrective

action

of the

LER were

completed.

The

licensee's

corrective

actions

associated

with this event

met

NRC

Enforcement Policy Section

V.G criteria for not issuing

a Notice of

Violation. It is identified as closed

NCV 335/91-027-03,

TS Required

Plant

Vent

Stack

Radiation

Sampler

and

Monitor Inappropriately

Out-of-Service.

The

above

events

indicated

a minor lack of attention

to detail

by the

operations

department.

Per the information on similar events

provided in

the

LER text,

these

types of operator oversight

had

been occurring

on

a

two

to

three

year

cycle.

When

implemented,

the

human

factored

modification of the

RAS

bypass

key

should

reduce

the likelihood of

operator error.

7.

Onsite Followup of Events

(Units

1 and 2)(93702)

Nonroutine plant events

were reviewed to determine

the

need for further or

continued

NRC response,

to determine

whether corrective actions

appeared

appropriate,

and to determine that

TS were being

met

and that the public

10

health

and

safety

received

primary consideration.

Potential

generic

impact

and trend detection

were also considered.

The operational

actions

observed

and

reviewed

during this period

were

acceptable

and addressed

in other portions of this report.

Followup of Inspection Identified Items

(GE

HFA Relay Failures

to Latch)

(Units

1 and

2) (92701)

~Sno sis

Engineered

safety features

and loss of offsite power testing at the St.

Lucie site

have

identified

GE

HFA relay failure-to-latch

conditions

contrary to

GE Service Letter

190.1

and

a resultant

GE

10CFR Part

21

notification

(NRC Bulletin 88-03).

GE Service Letter 190. 1 stated that,

for older latching relays

in Class

1E service, utilities should perform

certain latch tests

and replace

relays failing the test with new

HFA -1xx

(Century Series)

relays manufactured after November

1, 1987.

For Class

1E

service, field adjustment

was not an option,

and

vendor

manual

GEK-45486

provided

no

instructions

for adjusting

the

latching function.

All

latching-type relays manufactured after November 1, 1987, would be checked

for the condition at the factory.

Not only'ave older (but field tested)

HFA latching

relays

subsequently

fa'iled to function reliably while

installed in safety systems,

so have relays manufactured after November

1,

1987.

Use and Function of Latchin

Rela

s at St. Lucie

St. Lucie Unit

1 had

14

and Unit 2 had

6 safety-related

latching

HFA 154

series

relays.

The

14 Unit

1 Class

1E latching relays

served:

3

CCM pumps

1A, 18,

1C;

3

ICM pumps

lA, 1B,

1C;

2 Reactor cavity cooling fans

2 Auxiliary building supply fans

2 Reactor support cooling fans

2

ECCS

room exhaust

fans

.1

HVS 2A, 2B;

1

HVS 4A, 4B;

1

HVE 3A, 3B; and

1

HVE 9A, 9B.

The

6 Unit 2 Class

1E latching relays

served:

3

CCW pumps

2A, 2B,

2C; and

3

ICM pumps

2A, 2B,

2C.

The primary purpose

of

loss of power,

control

were

running

when

loss

automatically restarted

these

latching relays

was

to preserve,

during

a

system

knowledge

o'f which individual

components

of power occurred.

These

components

would be,

when power returned.

These

relays mechanically latch closed

when operated

and are electrically

reset

by

a small coil.

Some

models at other sites

could also include

a

manual

reset

button.

The relays

were mounted

on vertical surfaces

and the

11

plate-shaped

armature

operated

in

a horizontal

direction rather

than

"up-and-down."

Closing force

was

provided

by

an electromagnetic

coil,

opening

force

was

provided

by

a spring.

The U-shaped

latch,

which sat

above the top edge of the plate-shaped

armature,

had

a roughly rectangular

notch in the end

on each side.

The notches

were about

1/8 inch wide by

1/8

inch

deep.

When

the

relay

actuated,

the

armature

would

move

horizontally and the latch

be pulled down by another spring - trapping the

armature in both notches.

Previous

Failures of Rela

s to Reliabl

Latch

NRC Bulletin 88-03,

based

on

a

GE

10

CFR Part

21 notification, identified

potential latch engagement

problems affecting series

51B (151B),

54 (154),

71b

(171B),

and

74

(174) latching relays.

The bulletin focused

on the

relays failing to remain closed

[as during seismic events, etc.]

At St.

Lucie, the failure to remain latched

would result in no automatic signal

to start

and

would require

operator

action

to carry out the safety

functi on.

In the fall of 1990,

The

2B

ICW

pump relay failed to latch in service

during

a

LOOP test.

The relay had insufficient clearance

between

the

U-shaped latch

and the armature.

This relay was replaced

under

NPWO

5553/62.

Recent

licensee

inquiry found that this relay's

date

code

was

14GT (July 1981).

In the fall of 1991,

the

1A

ICW

pump relay failed to latch in service

during

a

LOOP test.

The relay

had insufficient clearance

between

the

U-shaped

latch

and the armature.

This relay was adjusted

to meet the 1/32

inch criteria under

NPWO 4473/65.

The licensee

then reinspected

all 20

Class

1E relays

under

NPWOs

2287/66

and

4950/65

per Bulletin 88-03

requirements.

Four additional

relays

latched

intermittently or

had

insufficient latch engagement.

Relays failing the inspection were:

Date

Code

14UC (July 1988)

Date

Code

14UC (July 1988)

Date

Code

14TC (June

1988

Date

Code

14VC (August 1988)

Date

Code

14FU (June

1982)

1A

ICW pump

1B

CCW pump

1

HVS

2B

1

HVE 3B

2B

CCW pump

This

was

25 percent

of the

Class

1E latching relays installed

at St.

Lucie.

The licensee,

being

unsure

whether

the

relay settings

were

drifting or had

been initially mis-set,

planned

to monitor them again in

the Spring of 1991 during the next Unit 2 refueling outage.

Bulletin 88-03

inspections

were

performed

at St.

Lucie in

1988

and

reported

complete

by

FPL letter L-88-392 of September

22,

1988.

Three of

20 relays, for the

2A, 2B,

and

2C

CCW pumps,

were previously

154E relays

and tested

satisfactory.

Four of the remaining

17 failed the inspection

and were replaced with 154E relays.

These four were for the

2A and

2B

ICW

pumps,

1HVS 2B,

and

1A ICW pump.

12

Evaluation of NRC and Vendor Literature

Subsequent

to the test failures,

the licensee

found that very

new relays

not only had full, rather

than

1/32 inch, latch

engagement

but also

had

about

1/32

inch additional

available

armature

movement after latching.

FPL-GE staff conversations

confirmed this

as

a standard

practice.

Inspector

review found that

NRC Bulletin 88-03 attached

Figure-2 did not

show the correct location of the 1/32 inch latch engagement,

did not show

the notch in the

end of the latch,

and did not discuss

additional

armature

movement

toward the coil with the latch engaged.

Figure-2 did show shims

[items

114,

1,17

(use

as required)] behind the latch mounting screw.

"Use

as required" is contrary to the options in the vendor

manual

and Service

Advice Letter.

GE stated

in vendor

manual

GEK-45486 that

HFA 154 Series

relays

are

cal,ibrated

at the factory

and

under

normal

conditions will require

no

further adjustments.

Oetailed field adjustment

of the latch

was

not

addressed.

The manual

did address

several

other adjustments, if required:

Contact burnishing;

Changing

contacts

from

Normally-open

to

.Normally-closed

and

vice-versa;

Adjustment of coil pickup voltage

(a spring tension adjustment);

Ensuring all contacts

open or close

simultaneously

with 3/64 inch

wipe

when in the

operated

position - contact

arms

may

be

bent

slightly to accomplish this;

and

Check to see that the armature

latches

in when operated

by hand

and

opens readily when reset.

GE service letter

190. 1,

which

the bulletin

was

based

on,

added

a

requirement:

When latched,

both latch legs

must

engage

[overlap] the armature

by

1/32 inch.

GE service letter 190; 1 also

added

two adjustment

checks:

The clearance

between

the top of the molded contact carrier

and the

top of the relay armature

must

be 1/32 inch minimum.

With the armatur'e fully depressed

against

the pole piece,

check that

the latch is fully rotated

by pulling up

on the latch assembly - no

motion is allowed.

The latch

mechanism

was

mounted

to the

case

in the

same

manner

as

a

contact.

Adjustment

by shimming to obtain proper latching did not appear

13

to

be difficult, and in fact this is what the factory did.

The biggest

problem

was

that

the

vendor

manual

did not

have directions

and part

. numbers,

nor did it recommend

a periodic

reinspection

of the latch

function.

t

The inspector

concluded that the

GE .manufacturing

conditions resulting in

the .service letter

and

NRC Bulletin

may not

have

been corrected,

thus

-these failures to latch could

be

a

symptom of

a generic

safety

problem.

Additionally, recently obtained

information supported

the conclusion that

the inspection criteria disseminated

by

NRC Bulletin 88-03

may well have

been

incorrect

or subsequently

changed.

NRC review with the

vendor

appears

appropriate

and

has

been requested

via

NRC Region II.

The licensee's

corrective

actions

following reinspection

of the relays

initially included repair of one relay along with replacement

of the other

ones.

While the

sketch

accompanying

Bulletin 88-03

showed

"use

as

necessary"

shims,

and

the

repair

was clearly within the skill

and

capabilities

of the

experienced

relay

engineer

making the repair,

the

vendor literature

only addressed

replacement

of relays

and

the plant

repair

procedures

and

NPWO, did not specifically authorize

the actions

taken.

Unit 2

TS 6.8. l.a required that written procedures

be established,

implemented

and maintained

covering the activities

recommended

in Appendix

A of Regulatory

Guide '1.33,

Revision

2,

February

1978.

Appendix A,

paragraph 9.e,

includes

procedures for obtai ning permission to work.

This

was

implemented

on site

by

AP 0010432,

Rev 57, Nuclear Plant Work Orders,

which required that all corrective maintenance

work be authorized

through

the

NPWO

and

conform

to

equality: Instructions,

Administrative,

and

Maintenance

Procedures.

Repair of the relay violated

AP 0010432.

The

licensee

took action

to replace

the relay in question

even

though it .

functioned

properly,

review

shop

decisions

involved,

and

change

maintenance

procedure

0960066,

Rev 4,

General

Electric

Type

HFA Relay

Testing

and

Setup

Procedure,

to address

latch

adjustment.

Based

on

frequent

observations

of licensee

maintenance

actions,

the

inspector

judged that this was

an isolated event.

This violation is not being cited

because

of

,lack of safety

significance

and

because

the

licensee's

corrective actions

met

NRC Enforcement Policy Section

V.A criteria for not

issuing

a Notice of Violation.

This is closed

NCV 335/91-027-04,

Failure

to Follow Work Control Procedure.

Followup of Inspector Identified Items

(Attendance at

FRG Meetings)

(Units

1 and 2) (92201)

The

inspector

had

previously

observed

that

the

gA and

ISEG staffs

frequented

FRG meetings

as observers.

The licensee

management

viewed this

as inhibiting candid conversation

and

asked

the

two groups

to reconsider

their needs.

After several

months,

the inspector

again reviewed this area

to determine if this policy change

had

a detrimental effect

on gA and

ISEG

operations.

Interviews with supervisors

of both organizations

revealed

that they

had

each

analyzed their operations

and determined

that routine

"observation" of FRG meetings

was not central

to their planned activities.

Additionally, the Site guality Group had provided

a regular

FRG member,

so

14

important information

was readily available,

and audited

the

FRG

on

an

annual

basis.

The inspector

concluded

that the activities of these

two

groups

were

not adversely

affected

by not frequenting

FRG meetings

as

observers.

10.

Followup of Headquarters

and Regional

Requests

(Units

1 and 2)(92701)

During this inspection period,

the

NRC staff had the resident

inspectors

complete

a survey

on the containment

hatch closure

equipment at this site.

The licensee

actions

in this area

were acceptable.

11.

Exit Interview (30703)

The inspection

scope

and findings were

summarized

on January

31,

1992,

with those

persons

indicated

in

paragraph

1

above.

The

inspector

described

the

areas

inspected

and

discussed

in detail

the inspection

findings listed

below.

Proprietary material

is not contained

in this

report.

Dissenting

comments

were not received

from the licensee.

Item Number

Status

Descri tion and Reference

335/91-027-01

389/91-027-02

Item Number

Open

VIO - Failure to Follow Equipment Control

Procedures,

paragraph

2.b.

Closed

NCV - Engineered

Safety

Features

Actuation

Channel

Out of Service

Due to

Personnel

Error, paragraph

6.a.

Status

Descri tion and Reference

335/91-027-03

Closed

NCV - TS Required Plant Vent Stack

Radiation Sampler

and Monitor

Inappropriately Out-of-Service,

paragraph

6;b.

335/91-027-04

Closed

NCV - Failure to Follow Work Control

Procedure,

paragraph

8.

12.

Abbreviations,

Acronyms,

and Initialisms

AC

AFW

AP

ATTN

CCW

CFR

CWD

DC

DPR

ECCS

Alternating Current

Auxiliary Feedwater

(system)

Administrative Procedure

Attention

Component Cooling Water

Code of Federal

Regulations

Control Wiring Diagram

Direct Current

Demonstration

Power Reactor

(A type of operating license)

Emergency

Core Cooling System

.

15

EDG

ESF

FHB

FT

GE

HFA

HYE

HVS

ICW

LCO

LER

LOOP

LS

MSIV

NCV

NPF

NPWO

NRC

OP

ppm

psi 9

QA

RAS

RCO

RCS

Rev

RG

RWT

SFP"

SIAS

SRO

TCW

TS

V IO

Emergency

Diesel

Generator

Engineered

Safety Feature

Fuel Handling Building

Flow Transmitter

General Electric Company

A GE relay designation

Heating

and Ventilating Exhaust (fan, system,

Heating

and Ventilating Supply (fan, system,

e

Intake Cooling Water

TS Limiting Condition for Operation

Licensee

Event Report

Loss of Offsite Power

Level Switch

Main Steam Isolation Valve

NonCited Violation (of NRC requirements)

Nuclear Production Facility (a type of operati

Nuclear Plant Work Order

Nuclear Regulatory

Commission

Operating

Procedure

Part(s)

per Million

Pounds

per square

inch (gage)

Quality Assurance

Recirculation Actuation Signal

Reactor Control Operator

Reactor

Coolant System

Revision

[NRC] Regulatory Guide

Refueling Water Tank

Spent

Fuel

Pool,

Safety Injection Actuation System

Senior Reactor [licensed] Operator

Turbine Cooling Water

Technical Specification(s)

Violation (of NRC requirements)

etc. )

tc.)

ng license)