ML17188A049

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Insp Repts 50-237/97-28 & 50-249/97-28 on 971123-980112. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML17188A049
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/06/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17188A047 List:
References
50-237-97-28, 50-249-97-28, NUDOCS 9802200080
Download: ML17188A049 (30)


See also: IR 05000237/1997028

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION Ill

Docket Nos:

50-237, 5~249

License Nos: -OPR-19, DPR-25

Report No: *

50-237/97028(DRP); 50-249/97028(DRP)

  • Licensee:

Facility:

Location:

Dates:

.:*

. ;: ;

  • Commonwealth Edison Company

Dresden Nuclear Station, Units 2 and 3

6500 N. Dresden Road

Morris, IL 60450

November 23, 1997, to January 12, 1998

Inspectors:

K. Riemer, Senior Resident Inspector

8. Dickson, Resid~nt Inspector

D. Roth, Resident Inspector

Approved by: M. Ring, Chief

Reactor Projects Branch 1

9802200080 980206

PDR

ADOCK 05000237

Q

PDR

II l \\

EXECUTIVE SUMMARY

Dresden Generating Station, Units 2 and 3

NRC Inspection Report No. 50-237/97028(DRP); 50-249/97028(DRP)

.

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This inspection included routine resident inspection from November 23, 1997, to January 12,.

1998.

Operations

The material condition of the HPCI system impacted system availability and required

operator work-arounds to assure HPCI system operability. Repetitive equipment

problems with the gland s~al*condenser level switch caused Unit 3 HPCI to be declared

. inoperable, and the alignment of.the condensate storage tank once caused both HPCI *

systems to be declared inoperable. (Section 02.1) .

The licensee's response to identified errors in the setpoints for system oil temperatures

was poor. The licensee's original explanation of setpoint tolerances was incorrect, and

the situation was not addressed until operators wrote. a second problem identification

form. (Section 02.1)

The operators' response to the automatic reactor trip was good. The inspectors

concluded that the actual safety consequences of this event were low. Operator and

plant equipment response were generally'as expected for an automatic reactor trip from

full power.* The exception involved the response of the feedwater level control (FWLC)

system which over filled the vector vessel; however, in this case there were no adverse

  • consequences from the level overshoot since the HPCI system was already isolated for

troubleshooting efforts. (Section 04.1)

Operations personnel exhibited safe operating practices during the startup of Unit 2 .that

commenced on December 26. Crew briefs and heightened level of awareness briefs

were informative, contingency actions were discussed, and peer checks were performed.

(Section 04.2)

The operations staff was slow to declare the HPCI system inoperable following the gland

seal leak off condenser low level switch failure on December 29, 1997. More than

17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> passed from the first symptom until operations recognized that the system was *

inoperable. Even after recognition, the limiting conditions for operation were not

retroactively entered. (Section 04.3)

Operators generally were knowledgeable .of the HPCI system parameters, settings, and

requirements. The inspectors identified one instance involving turbine lube oil

temperature where the requirements were not known. (Section 04.4)

The licensee failed to follow the procedural requirements to provide feedback to the

problem identifieation form (PIF) originator. Subsequent to the inspectors' review of the

. process, the licensee independently identified this procedural adherence concern and

entered it into the corrective action program. The licensee met the procedural

requirements before the end of the inspection period. (Section 07.1)

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Maintenance

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Collectively, equipment failures and material condition issues involving a control rod drive,

a torus cooling test valve, an HPCI isolation, erratic operation of a. recirc motor generating

set, the offgas system, reactor water cleanup and feedwater level control, represented

challenges and distractions for operators and other plant staff. The issues especially

represented a burden to operato~s who had either to respond to the original event, or to

take additional compensatory actions. (Section M2.1)

The inspectors were also concerned with the licensee's ability to resolve the issues

effectively and eliminate deficiencies. (Section M2.1)

On December 13,. work**performed without referencing a required procedure, combined

with material condition, resulted in a trip of the Unit 3 125 V battery charger and placed

both units unexpectedly into*a two-hour limiting condition for operations. The subsequent

follow up work was not performed in accordance with station administrative procedures.

Specifically, the "condition" met sign off was used when a condition had not been met.

(Section M4.1)

Not all rework was captured into the rework trending program. (Section MB.1)

Engineering

The inspectors concluded that the licensee's root cause team performed a thorough

investigation of the reactor trip, the root cause, and equipment response following the

reactor scram. The licensee's team concluded that the root cause of the event was the

failure to perform the actions identified in GE SIL 500 regarding local power range

monitor spiking. The inspectors' review reached the same conclusion.

The FWLC system response presented a potential challenge to the operators following

the reactor scram. The compensatory actions that the operators were required to take

following a scram on Unit 2 were operator work-arounds. Pending permanent resolution

of the Unit 2 FWLC system issues, the station was relying on operator intervention

following a scram to prevent water intrusion into HPCI steam lines. (Section E1 .2)

Operability evaluations appeared to meet the licensee's requirements. The evaluations

were reasonable* and provided adequate bases for the conclusions. (Section E2. 1)

Plant Support

The s~tup and control of contaminated areas and work in contaminated areas were

usually correct. (Section R4.1)

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The inspectors identified one example of an improper1y secured hose ~hat crossed a

contamination boundary. The hose had been staged in response to a poor1y performing

sump pump. (Section R4.1)

The inspectors were concerned with the lack of attention to detail exhibited by the plant

staff to radiation controls, and that the PIF record showed this to be an emergent trend.

(Section R4.1)

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Report Details

Summary of Plant Status

Unit 2 started the reporting period in a load recovery from the power reduction required for single-

loop operations and 2A feedwater regulating valve (FWRV) work. On December 3, power was

reduced to about 600 MWe for repair of the 2E condensate demineralizer service unit. Recovery

started on December 8, but oscillations on the 2A FWRV delayed full-power operations until

December 12. On December 23, Unit 2 automatically scrammed from full power due to a local

power range monitor (LPRM) spike, and a forced outage was entered (D2F30). Unit 2 was

placed back on the grid by December 27.

Unit 3 maintained full power throughout most of the period. On December 6, load was reduced

to mitigate a fire in the off-gas piping. Several times during the period, load was reduced to

attempt to address problems with the 38 reactor water cleanup demineralizer bed. Maximum

power on Unit 3 was slightly limited to maintain the average turbine control valve positions less

than 85 percent.

Maximum power on both units was limited by feedwater flow. Feedwater flows were limited to

9.735 Mlbm/h to remain within the anticipated-transient-without-scram (ATWS) analysis. The

licensee was pursuing additional analysis to remove this restriction.

I. Operations

01

Conduct of Operations

01.1

General Comments

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations. Overall, the conduct of operations was safe and according to

procedures.

During the inspection period, several events occurred for wtiich the licensee was required

by 10 CFR 50.72 to notify the NRC. The events and the notification dates are listed

below:

11/26/97

12/01/97

12/06/97

(Units 2, 3) Units 2 and 3 HPCI systems declared inoperable after

engineering determined that HPCI system operation could result in air

intrusion into HPCI .system.-

(Unit 3) Failure of torus cooling outboard test valve caused a potential for*

diversion of cooling flow from the reactor during a design basis loss of

coolant accident.

(Unit 3) Control rod inserted into the core during a surveillance test. The

event report was retracted on 12/18/97 after the licensee concluded that

the *event was not an engineered safety feature (ESF) actuation.

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12/12/97

12/22/97

12/23/97

12/29/97

1/07/98 .

{Units 2, 3) Loss of 138 kV line that fed the lift station required operating

the units in lake-bypass mode violating the national pollution discharge

elimination system permit'. Offsite notification made to the Illinois

emergency management agency.

{Unit 2) ESF Actuation - HPCI Isolation during a routine surveillance for

unknown. reasons.

{Unit 2) Full reactor scram from 100 percent power due to a spurious

APRM signal during an unrelated surveillance of reactor vessel high

.pressure scram signals.

{Unit 3)* HPCI system .declared inoperable due to failure of gland seal .

condenser low level switch ..

{Units 2,. .3) Unanalyzed condition that may significantly compromise plant

  • safety identified when calculations showed the. post-LOCA reactor building

temperatures to be significantly higher than the limitihg value stated in the

UFSAR.

02

Operational Status of Facilities and Equipment

  • 02.1 (Units 2. 3) Engineered Safety Feature System

a.

. Inspection Scope (71707)

The inspectors conducted a detailed review of the Unit 2 and Unit 3 High Pressure

Coolant Injection {HPCI) systems to verify operability, assess the performance, and

assess material condition of the systems. The inspectors also performed a cursory

walkdown of the HPCI system to ensure that the alignment procedures, piping and

instrumentation diagrams {P&IO), and the as-built configurations were current. The

inspectors reviewed the following operating procedures, schematics, and the results of

quarter1y operability surveillances against information established in the Updated Final

Safety Analysis Report (UFSAR), Technical Specifications (TS), and the licensee's

operation training manual:

DOP 2300-01 Unit 2(3) HPCI System Standby Operation, Rev. 15

DOP 2300-02 Unit 2(3) HPCI System Turning Gear Operation, Rev. 06

DOP 2300-03 Unit 2(3) HPCI System Manual Startup and Operation, Rev. 24

DOP 2300-M1/E1 Unit 2(3) HPCI System Checklist, Rev. 15

DOS 2300-03 Unit 2(3) HPCI System Operability Verification, Rev 49

DOS 2300-07 Unit 2(3) HPCI Fast Initiation Test, Rev. 18

P&ID M-51, HPCI Piping Unit 2,

P&ID M-374, HPCI System Piping Unit 3.

WR No. 970093784-01 Unit 2 Quarter1y TS HPCI Pump Test (IST Program) dated

Nov. 19, 1997

WR No. 970094986-01 Unit 3 Quarter1y TS HPCI Pump Test {IST Program) dated

Nov.26, 1997

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b.

Observations and Findings

During walkdown of the HPCI systems, the inspectors determined that the alignment of

the systems was in accordance with the operating procedures. The inspectors also noted

that housekeeping for both Unit 2 and Unit 3 HPCI system rooms was good.

The inspector noted several oil l~aks throughout both the Unit 2 and Unit 3 HPCI

systems. The licensee also noted-these leaks and had written action requests (ARs) to

address the deficiencies.

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The Unit 2 HPCI System room was at elevated temperature due to steam leaking past the

HPCI steam supply shutoff valve (2-2301-3) and into the HPCI floor drain sump through

the* HPCI *stop valve above seat drain :line.- ' *

FrontStandard Temperatures

On December 19, the inspectors noted that the alarm setpoints for four temperature dial

switches (Unit 3 HPCI bearing oil cooler outlet temperature, Units 2 and 3 low pressure

bearing drain oil temperature, and Unit 2 thrust bearing oil drain temperature) shown on

the HPCI system front standards appeared to be at different settings than listed in the

Dresden Annunciator Procedures (DANs) associated with the alarms. The inspectors

informed the Unit 3 Unit Supervisor (US), who contacted the system engineer and wrote a

problem identification form (PIF) to document the concern. The PIF was subsequently

canceled by the PIF screening committee:*

The system engineer reviewed the alarm setpoints and concluded that the settings were

within the allowed tolerances based on a review of the instrument maintenance

department (IMO) data cards.

The IMO data card showed that the allowed tolerance for temperature indicator face value

was +/-5°F and the tolerance for the dial switch was+/- 2°F. Using this information, the

system engineer thought that the two tolerances could be added to give an acceptable *

tolerance of+/- 7°F. The inspectors questioned this conclusion, and determined that the

appropriate tolerance for the dial switch was only +/- 2 ° F.

The inspectors also reviewed the instrument maintenance department (IMO) data cards

for the instruments and concluded that the instruments were originally set correctly, but

had subsequently drifted out of tolerance. In one case the temperature dial alarm setting

was greater than 5°F outside tolerance, upscale. In another case,- the setting was 16°F

outside tolerance, downscale. The inspectors informed operations that a concern still

. existed, and operations wrote a new.PIF to document the concern. The licensee

eventually wrote an Action Request (AR) tag to correct temperature switch settings.

The inspectors determined that the out-of-tolerance-temperature switches did not make

the HPCI system inoperable.

Exhaust Drain Pot Alarms

Jhe control room logbooks documented that the Unit 2 HPCI system exhaust drain pot

high level alarms were annunciating at least once a day. The US explained that

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condensation resulting from' seat leakage of the Steam Supply Shutoff Valve (2-2301-3)

caused an abnormal input to the exhaust drain pot via the* stop valve above seat drain

line.

The licensee concluded in Engineering Operational Problem Response/Troubleshooting

Plan (EOPR) 98-02-23-318, Rev. 0, that operations personnel needed to take

compensatory actions to ensure the operability of the HPCI system. The compensatory

actions included the non-licensecfoperators (NLOs) manually draining the exhaust drain

pot once per week. The EOPR suggested that the quantity' drained be evaluated and the

draining frequency adjusted as needed. The inspectors concluded that the EOPR

appeared reasonable.

The Operations*Department declared the HPCI drain pot.~evel high-alarm as a control *

room distraction, and considered the draining to ~e an operator work-around.

HPCI System Availability

As stated in Section 01, 1, three issues resulted in one or both HPCI systems being

declared inoperable during this inspection period. On November 26, both units' HPCI

systems were declared inoperable after engineering determined that air intrusion into

HPCI system could occur due to condensate storage tank (CST) alignment. On

December 22, during a routine surveillance test, the Unit 2 HPCI system unexpectedly

isolated for unknown reasons. On December 29, the Unit 3 HPCI system was declared

inoperable due to failure of the gland seal condenser low level switch. Similar problems

with gland seal condenser level were discussed in Licensee Event Report (LER)

50-249/97-09-00 and LER 50-237/97-013-00, and in Inspection Reports (IR) 97012,

97019, 97024. Additional follow.,.up for all three issues will be tracked through the LER.

c.

Conclusion

The HPCI systems were property aligned in accordance with procedures.

The material condition of the HPCI system impacted system availability and required

operator work-arounds to assure HPCI system operability. Repetitive equipment

problems with the gland seal condenser level switch caused Unit 3 HPCI to be declared .

inoperable, and the alignment of the condensate storage tank once caused both HPCI

systems to be declared inoperable.

The licensee's response to identified errors in the setpoints for system oil temperatures

was poor. The licensee's original explanation of setpoint tolerances was incorrect, and

the situation was not addressed until operators wrote a second PIF .

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03

Operations Procedures and Documentation

03.1

(Units 2. 3) Control Room Rounds

a.

lnspection'sc0pe cr1707)

The inspectors reviewed operator use of panel monitoring sheets.

b.

dbs~rvations and Findings

The use of these sheets helped the.licensee in detecting abnormal trends (e.g., the

valved-out fuel pool cooling discussed in IR No. 50-237/97019;.50-249/97019

Section 03.1). The rounds sheets included a column of normal operating parameters.

The inspectors noted that some values being recorded were not within the normal

operating bands. For example, the torus temperature was 5°F above the listed value .

. Discussions with the operating staff indicated that the bands on the rounds sheets were

not always ttie actual normal parameters, and that some operators did not routinely verify

the parameters against the bands. The values were instead compared to values the

operators knew from TS and operations procedures. The inspectors also noted some

confusion about who performed the primary review of the parameters (US or nuclear

station operators).

The inspectors considered the acceptance of rounds sheets with "normal" operating

parameters that were not normal to be a poor practice. All operators interviewed were

aware that the bands listed on the rounds sheets were not always the actual normal

operating band. The operators explained that when the rounds sheets were created, the

intent was to heighten panel monitoring and trending. The full "normal" bands for all

equipment had not been entirely listed, and equipment outside the "normal" bands may

still be within required bounds.

At the end of the inspection period, the licensee was evaluating improvements to the

rounds sheets.

c.

Conclusions

The use of panel monitoring rounds sheets helped operators identify trends and maintain

panel awareness. However, the operators did not .ensure that the rounds sheets

contained the correct normal operating parameters for all equipment. The inspectors

were concerned that acceptance of the incorrect bands reduced the rounds sheets'

effectiveness.

04

Operator Knowledge and Performance *

04.1

Unit 2 Automatic Reactor Trip

a.

Inspection Scope (71707. 93702)

The inspectors reported to the main control room and observed operator performance

following a Unit 2 automatic reactor trip (scram) that occurred December 23, 1997. The

inspectors reviewed the significance of the event, performance of safety systems, and

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b.

actions taken by the licensee. The inspectors also reviewed station logs, control room

recorder indications, the scram investigation team's results, and assessed the functioning

of the Plant Operations Review Committee {PORC) meeting held to approve a unit

restart.

Observations and Findings

Before the reactor scram, the HPCI system was out of service and isolated due to a

spurious full isolation that occurred on the previous day. All other emergency core

cooling systems {ECCS) were in normal alignments.

Instrument maintenance department personnel were performing Dresden Instrument

Surveillance (DIS) 0500-01, "Reactor Vessel High Pressure Scram Pressure Switch

Calibration." Part of the surveillanee,resulted in actuation of the reactor protection system

{RPS) Channel "B" half scram. This was expected. *While the planned half-scram was

actuated, an unexpecte~ average power range monitor {APRM) high-high signal

occurred, and actuated Channel A of RPS. This resulted in a full scram signal *

Operator Response

Operator response to the transient and performance during scram recovery were good.

The inspectors observed good procedural usage by the operators, formal

communications throughout the event, and effective command and control by the US.

Unit 3 activities were reduced to lirriit distractions to the Unit 2 operators.

Equipment Response

All rods inserted, and the reactor automa~ically shut down. However, not all equipment

responded ideally. The reactor feedwater level control system caused the reactor

pressure vessel {RPV) level to increase above +48." This would have flooded the HPCI

system's steam lines, but the HPCI system was already isolated. This item, and required

operator compensatory actio!'ls to prevent a repeat occurrence, are discussed further in *

Section E1 .2 of this report. The inspectors concluc;ted that the actual safety

consequences of this event were low.

Prompt Root Cause

.

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The licensee formed a prompt root cause team to de_termine the immediate causes of the

reactor trip. A formal root causes investigation was also assigned,* but was not

completed during this inspection period.

The immediate cause of the event was that LPRM 20-24-41 spiked high, causing

APRM 2 to spike high, which in tum generated a trip on RPS Channel "A." Since a trip on

RPS Channel "B" half scram was already actuated due to testing, the RPS scram logic

was satisfied and a full automatic reactor scram occurred.

General Electric {GE) service information letter {SIL) 500, issued October 23, 1989,

discussed the phenomenon of LPRM spiking. The SIL stated that a "whisker" {buildup of

uranium oxide) arcing in the detector caused spikes. The arcing typically eliminated the

whisker. To prevent spikes, the GE SIL recommended that detector breakdown

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(current-voltage) tests be performed at specified intervals to look for whiskers in the

detectors. The SIL also provided guidance on how to bum-off. the whiskers to prevent

spikes.

The licensee found that ComEd's Nuclear Fuel Services had reviewed the SIL, but did not

require performance of all ofthe recommendations in the SIL. Instead, bum-offs were

only performed on problem detectors. The licensee's investigation team concluded that

the failure to perform all of the GE SIL recommendations directly contributed to the spike.

The inspectors assessed the PORC meeting held to review the prompt root causes and

corrective actions prior to plant restart.* The PORC thoroughly discussed the event, the

investigation team's cpnclusions, and the reconimende'd actions prior to restart. The

PORC maintained an appropriate safety-focus during review of the prompt root cause.

c.

Conclusion

The operator response to *the automatic reactor trip was good. The inspectors concluded

that the actual safety consequences of this event were low. Operator and plant

equipment response were generally as expected for an automatic reactor trip from full

power. The exception involved the response of the feedwater level control (FWLC)

system; however, in this case there were no adverse consequences from the level

overshoot since the HPCI system was already isolated for troubleshooting efforts.

The prompt root cause investigation team formed by the licensee performed a thorough

review of the event and subsequent equipment problems. The inspectors concluded that

the prompt root cause of the event was the failure to perform the actions identified in GE

SIL 500 regarding LPRM spiking.

04.2

(Unit 2) Operations Performance During Startup

a.

Inspection Scope (71707)

The inspectors conducted observations of startup activities from forced outage D2F30.

b.

Observations and Findings

During the Unit 2 startup, operations observed were performed in a careful and controlled

manner. Good communications were evident, and the operators were knowledgeable of

the plant conditions and issues. The crew performed correctly and maintained

awareness of the plant status. The shift manager and US maintained correct command

and control during the startup. The US held crew briefs as necessary, and directed entry

into the correct abnormal procedures in response to several instances of double-notching

control rods.

The startup and power ascension of Unit 2 were hampered by some minor equipment

problems such as double-notching control rods. The inspectors concluded that the

actions taken were appropriate to the symptoms and in accordance with plant

procedures.

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c.

Conclusions

Operations personnel exhibited safe operating practices during the startup of Unit 2 that

commenced on December 26. Crew briefs and heightened level of awareness briefs

were informative, contingency actions were discussed, and peer checks were performed.

04.3

Unit 3 HPCI lnoperabilitv

a.

Inspection Scope CT1707)

The inspectors reviewed the operators' initial operability call for the HPCI system on

December 29, 1997~ after the low level switch in the gland seal*leakoff (GSLO) condenser

failed to stop the drain pump.

b.

Observations and Findings

At 0234 on December29, 1997, while performing DOP 2300-01, "Unit 2(3) HP~I System

Standby Operation," Rev. 15, for the Unit 3 HPCI System, the operators started the GSLO

pump to pump down the GSLO condenser hotwell as required by the procedure. The

pump did not stop at the low level switch as designed but continued to pump down the

GSLO condenser. The Unit 3 nuclear station operator (NSO) manua.lly secured the

pump. The US control room logs stated that operability was immediately discussed by

the US, and a previous event was also considered. However, the US concluded that; for

this event, the Unit 3 HPCI system was operable.

The operability issue was revisited later in the shift. An entry made at 0447 in the US log

book showed that the US reviewed the surveillance tests, the UFSAR, emergency

notification system (ENS) requirements, previous ENS calls made for the HPCI system,

the historical limiting conditions for operation (LCO) logs, and the design* basis

documents to determine operability requirements. The US also discussed the issue with

the on-call system engineer. The US again concluded that the HPCI system was

. operable.

The previous event occurred on September 5, 1997, and was discussed in

LER 97-009-00/50-249. The Unit 3 HPCI system was declared inoperable during a

surveillance test due to the failure of the GSLO condenser drain pump low level switch to

shut off the pump at the required low level. This led to cavitation and air entrainment in

the pump suction and air accumulation in the discharge pressure regulating valve sensing

line":.

The licensee continued review of HPCI system operability. Subsequently, the HPCI

system was declared inoperable at 1945, December 29, 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> after the first

symptoms. The inspectors concluded that, due to the similarity between this failure and

the failure of September 5, the length of time was excessive .

12

c.

Conclusion

Operator performance with respect to the initial operability call was weak. While the

operators followed the station's administrative procedures for determining operability,

sufficient data was available to support a more timely declaration of HPCI inoperability.

When operations declared the HPCI system inoperable, the staff entered the appropriate

TS limiting conditions for operation from the time of the operability determination, but not

from the actual first symptom . .The inspector concluded that not entering the limiting

condition retroactively was not the most conservative decision. Information was available

to link the start of the HPCI system problem to the original failure of the GSLO pump to

stop automatically at the GSLO condenser hotwell low level.

This was of concern to the* inspectors because of its similarity to a recent issue regarding

the standby liquid control (SBLC) system. In IR 50-237/97024; 50-249/97024, the NRC

documented an instance in which operations failed to declare the SBLC system

inoperable upon receipt of valid control room alarms.

04.4

(Units 2. 3) Operator Knowledge of HPCI System Parameters

a.

Inspection Scope U1707)

The inspectors questioned .operators about HPCI system indications. The questions were

limited to operator knowledge of the actual HPCI parameters present on the units.

b.

Observations and Findings

The Nuclear Station Operators (NSOs) were generally aware of the HPCI initiation and

isolation signals, the valve interlocks and the operating parameters (temperature and

pressure limitations) of the HPCI turbine lube oil system.

One exception to this occurred during questioning of one Unit 2 NSO. During the

walkdown the inspectors noted that all HPCI system turbine lube oil temperature

computer monitor points on Control Panel 902-3 indicated between 92 to 95°F. The

inspectors then questioned the NSO on temperature limits while the HPCI system was in

standby operation and the expected temperature bandwidth for HPCI turbine lube oil

temperature when he performed his control board walkdown. The NSO answered by

stating that he was not aware of any temperature limitations of the HPCI turbine lube oil

system while in standby operations. Both DOS 2300-03 and DOS 2300-07 required HPCI

oil c0oler discharge temperature be greater than 96°F. The manufacturer's manuals

cautioned that bearing inlet temperatures outside of limits should be avoided to prevent

  • damaging the bearings due to poor oil circulation.

After a discussion of concerns with the inspectors, the US ordered the NSO to place the

HPCI turbine on the turning gear since the oil pump adds a significant amount of heat to

the oil. The US also initiated an AR to calibrate the HPCI sump heater to a higher

temperature to ensure that HPCI oil temperatures are maintained within the design

temperatures. Instrument Maintenance Department (IMO) *personnel adjusted the

controller for the HPCI sump heater on December 23, 1997.

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The inspectors noted that control room hourly rounds sheets did* not include sump oil

temperatures. The licensee was considering adding these parameters to the rounds

sheets.

c.

Conclusions

Operators generally were knowledgeable of the HPCI system parameters, settings, and

requirements. The inspectors identified one instance where the requirements were not

known.

07

  • Quality Assurance in Operations

07.1

Failure to*Follow Integrated Reporting Program Procedure *

a.

Inspection Scope*(71707. 40500)

The inspectors reviewed the licensee's corrective actions procedure, Nuclear Station

Work Procedure (NSWP) A-15, "Integrated Reporting Program," to determine the

station's compliance with the stated requirements. * The inspectors reviewed whether the

PIF process was property followed after PIFs were submitted.

b.

Observations and -Findings *

The licensee documented problems and non-conforming conditions via use of PIFs. *

Licensee Procedure NSWP-A-15, "ComEd Nuclear Division Integrated Reporting

Program," Rev. 1, required a feedback form be provided to the originator of the PIF. The

inspectors identified that the licensee was not sending the required feedback forms to the

PIF originators in accordance with NSWP-A-15.

The licensee was required by TS 6.8.A to implement the applicable procedures

recommended in Appendix A of RG 1.33, Rev. 2, February 1978. Procedures for

administrative controls were recommended in RG 1.33. Contrary to the above, the

licensee failed to.implement the requirement of NSWP-A-15 to provide feedback to PIF

originators. This was a violation of TS 6.8.A (VIO 50-237/97028-01 (DRP);

50-249/97028-01 (DRP)).

Subsequent to the inspectors identification of the failure to initiate the required feedback

forms, but prior to the inspectors' presentation of the finding to licensee management, the

licensee independently identified that the PIF process was not being followed with respect

to the feedback forms. The licensee's Quality and Safety Assessment (Q&SA)

organization identified that the procedure was not being followed across the board with

respect to the feedback issue. The Q&SA department concluded that when the new

requirement was put into the NSWP, the Dresden Staff did not realize the new

requirement and did not change local practices to comply. On December 3, 1997, the

Q&SA department initiated i:>IF 01997-08096 to document that the required feedback

forms were not being distributed to the originators as required by NSWP A-15.

14

I

The licensee commenced generating the required feedback forms following identification

of the issue and provided several examples to the inspectors for review. The licensee

entered the procedure adherence concern, via PIF D1997-08096, into the corrective

action process for long term resolution.

c.

Conclusion *

The licensee failed to follow the procedural requirements to provide feedback to PIF

originators. After the inspectors' review of the process, the licensee independently

identified this procedural adherence concern and entered it into the corrective action

program. The licensee met the procedural requirements before the end of the inspection

period.

..

II. Maintenance

M1

Conduct of Maintenance

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Plant Material Condition

a.

  • inspection Scope {62707. 37551)

The inspectors noted that several material condition issues and self-revealing equipment

failures during the inspection period required plant personnel to take prompt action. The

inspectors reviewed the failures to determine the effect on plant safety.

b.

Observations and Findings

Control Rod Drive (CRD) F1 Unexpected Insertion:

On December 6, 1997, during the performance of DOS 0500-03, "APRM Rod

Block and Scram," functional test, CRD 22-03 (F-1) unexpectedly scrammed to

position 00. The single-rod scram occurred approximately 15 seconds after

receiving an RPS Channel 'B' half scram signal. The licensee performed detailed

troubleshooting of the scram solenoid pilot valve (SSPV) and the RPS/SSPV

logic. The licensee concluded in Prompt Investigation Report No. 0005576052

that rod F-1 had not exhibited any specific characteristics of a degraded or failed

SSPV. Despite this, the licensee concluded that based on previous licensee and

industry experience the resultant single rod scram was consistent with that of a

degraded or failed SSPV. The licensee replaced the SSPV, successfully

performed scram functional testing, and placed rod F-1 back in service.

Unit 3 Torus Cooling Test Valve Failure to Operate:

On December 1, 1997, the torus cooling outboard test valve failed to operate on

demand, resulting in a potential for diversion of cooling flow from the reactor in the

event of a design basis accident. The licensee determined that the cause of the

15

.,

valve failure was due to a faulty auxiliary contact on the open contactor for motor

operated valve MOV 3-1501-388. The licensee replaced the auxiliary contact.

The faulty component was relatively new, and the licensee could not immediately

determine the reason for the. failure.

Unit 2 HPCI Full Isolation:

During performance of DIS 2300-03; "HPCI Low Pressure Isolation Channel

Functio_nal Test,n the HPCI system received a Group IV isolation and HPCI steam

line inboard and outboard primary containment isolation valves (2-2301-4 and 5)

went closed. The licensee could not determine the cause of isolation during

.inspection and. troubleshooting efforts, but replaced the relays that completed the

isolation logi~*(2391~02C and 2391.,.02D). The licensee sent the relays to the*

vendors for analysis.

2A Reactor Re.circulation Motor G.enerator Erratic Operation:

On December 6, 1997, the Unit 2 control room operators received a Recirc Pump

Mismatch alarm. The 2A recirculation pump ran back from approximately

49 percent pump speed to approximately 39 percent pump speed and appeared to

be running back up to the original speed when the unit operator locked-up the

scoop tube. Despite detailed testing and troubleshooting efforts, the licensee was

unable to determine the cause of the event. The licensee installed a temporary

recorder on the pump speed control circuitry to monitor for any future* possible

abnormalities.

3A Offgas Fire:

The 3A steam jet air ejector (SJAE) train did not work properly and was

susceptible to offgas fires. In the past, the licensee repaired and replaced

portions of the Unit 3 offgas system to restore the 3A train. However, during this

inspection period, the licensee experienced an offgas fire on December 6, 1997,

while the operating crew was adjusting the 3A recombiner booster/dilution steam

pressure using the manual bypass valve around the inoperative, isolated pressure

  • control valve. The licensee fixed various leaks and attempted to fine tune the

booster jet pressure control valve (which was identified as oscillating). However,

on January 13, 1998, when the licensee again tried to bring the 3A train in

service, another offgas fire occurred. At the end of the inspection period, the

licensee was evaluating if modifications to the system were.necessary.

38 Reactor Water Clean Up (RWCU) Demineralizer High DIP:

The station experienced repeated difficulties in placing the 38 RWCU

demineralizer in service. The operators eonsistently received indication of a high

differential pressure across the bed when the unit was placed on line. The

operators had to perform multiple power reductions/ascensions to support taking

the demineralizer out of service for maintenance and returning it to service once

the maintenance efforts were complete. At the end of the inspection period, the

licensee was still engaged in troubleshooting efforts to restore the 38

demineralizer.

16

-- ----....:....:=--:::::.::::.:.::-=-- _--.:; _____ ....:.: ___ . _..:.:..:..._--=.. --:: __

--

-* --

.

- --* --* --- ------

  • -

Unit 3 _ HPCI lnoperability:

On December 29, 1997, while placjng the HPCI system in standby, operators

started the GSLO pump to pump down the GSLO condenser hotwell. _The pump

failed to stop when it should have. This caused air entrainment in the pump

suction and air accumulation in the discharge pressure regulating valve sensing

line, Which then caused a reduction in the pump capacity. This event was similar

to a September 5 event Where the HPCI system GSLO condenser pump failed to

stop on the low level switch. Troubleshooting and inspection of the low level

switch in the GSLO condenser revealed no-abnormalities with the-low level

switch. .Further inspection efforts of the HPCI GSLO condenser revealed that

linkages' on the_ high level switch were not intact. This event w~s the third event

where_ the li~nsee's HPCI Sy$tem ,GSLO pump failed to operate properly due to

level switches malfunctioning (Ref. LERs 97-009/50-249 and 97-013/50-237).

Unit 2 Feedwater Level Control System:

The response of the feedwater level control (FWLC) system caused.reactor level

to overshoot following the automatic trip of the reactor on December 23, 1997.

The HPCI steam line would have flooded with water had not HPCI already been

isolated for troubleshooting. The FWLC system presented an additional operator

work-around due to the required operator compensatory actions following a

reactor trip on Unit 2.

c.

Conclusion

Collectively, the above issues represented challenges and distractions for- operators and

other plant staff. The issues especially represented a burden to operators who had either

to respond to the original event, or to take additional compensatory actions.

The inspectors were also concerned with the licensee's ability to resolve the issues

effectively and eliminate the deficiency. In some cases, the plant staff knew what

happened (and took appropriate short term corrective action) but did not know the root

cause of why the problem occurred.

M4

Maintenance Staff Knowledge and .Perfonnance

M4.1

(Unit 3) 125 V Battery Work

a.

Inspection Scope (62707)

The inspectors reviewed an error performed during battery testing that caused the station

to enter a two-hour dual shutdown LCO. The inspectors also reviewed the

documentation of the subsequent battery work.

17

L ------- --- ------- -----*-

__ :........: ___ -=::__..:__ __ -**- --

-

b.

Observation and Findings

Equipment Operation Outside of Procedure

On December 13, workers from the electrical maintenance department (EMO) were

authorized by operators to place the Unit 3 125 VDC charger on equalize-per

WR 970131667. At 0818, shortly after work started, the control room unexpectedly

received the 125 voe battery undervoltage and charger trouble alarms, followed by

battery high discharge alarms; The control room immediately dispatched a high-voltage

operator (HVO) to investigate. The HVO reported that the No. 3 125 voe charger had

tripped. The voltage on the batteries had rapidly dropped to 117 voe, then more slowly

to 115 VDC. The HVO aligned the 3A charger and restored voltage to normal* by 0822.

-*.

-

' * f ~

.

' *

~ :

. :

The electrical maintenance department (EMO) supervisor who was present at the .

batteries reported that he had manipulated the battery charger without a procedure in

hand.

The inspectors discussed the actions with the EMO supervisor. The supervisor stated his

woikers were having difficulty getting readings, so the supef'Visor commenced

troubleshooting. He went to the charger and noted that the charger's toggle switch was

in float. The supervisor believed it should have been in equalize, so he immediately

changed it. He did so without any procedures, without ariy other workers present, and

without verifying the response to his actions~ The toggle switch broke and caused the

charger to trip off, but since the supervisor did not wait to observe the expected

-

response, he did not realize this.

The* supervisor told his worker what he had done, and the workers in the room informed

the supervisor that his actions were incorrect. The HVO responding to the charger

trouble alarms then arrived at the seene, and the supervisor informed the HVO and

operations of the incorrect actions.

The inspector questioned the EMO supervisor about what, if any, distractions were

present. The supervisor stated that no distractions were present, and that he had just

been concentrating on troubleshooting so much that he had failed to maintain his role as

a supervisor, and that he had failed to adhere to the requirements for procedural use.

The EMO supervisor did not perform correctly when he manipulated equipment. The WR

used a "Category 1" procedure, and OAP 09-13 defined the level of use for a Category 1

procedure as "Continuous." Also, the supervisor should not have touched the equipment

in his over~ight role.

Dresden TS 6.8.A.1. required that written procedures be implemented covering the

activities recommended in Appendix A of RG 1.33, Revision 2, February 1978. The guide

recommended procedures covering maintenance work. Dresden Administrative

Procedure (OAP) 09-13, "Procedural Adherence," Rev. 06, required continuous use of a

Category 1 procedure. Contrary to this, on December 13, licensee personnel performed

work without continuously using the appropriate Category 1 procedure. As a

consequence, licensee personnel incorrectly manipulated equipment. The switch

failed, causing the 125 voe battery charger to trip. This was a violation

(VIO 50-237/97028-02 (DRP); 50-249/97028-02 (DRP)).

.

18

Immediate Licensee Response

The licensee immediately removed.the supervisor from duty and took other actions in

accordance with established management principles. The supervisor was tasked with

performing an Apparent Cause Evaluation" and performing other training and

remediation.

The licensee assigned another EMD supervisor to complete the initial work request..

Documentation Errors in Rework

The inspectors reviewed the completed work request (WR 970131.667) and noted several .

errors in how the work request was filled out.

First, it did not refer to the incorrect manipulation, and the work progression sign-off' had

been marked as "N/A.7 The use of the *sign-off was ;at the discretion of the supervisor, so

it was not a vi*o1ation to "NIA" the sign-off. When the battery was tripped and the work

was stopped on December 13, no one chose to fill in the work progression sign-off, so the

WR did not record why work was stopped, nor who stopped it.

Second, the inspectors noted that the Steps 1.1 and 1.2 of the procedure were initialed by

the second supervisor as "CM 12/13/97" for conditions met on December 13. The

inspector noted that the second supervisor did not have the assignment on December 13.

Also, Step 1.2. stated, "Document that Prerequisites are completed on Data Sheet 1, "'but

the second supervisor had marked Data Sheet 1 as "NIA 12/18/97." For.Step 1.2, the

conditions clearly were not met, and the "NIA" should not have been used.

The inspectors discussed the concerns with the second supervisor. The supervisor

stated that he had used "CM" for the first two steps after verifying that the prerequisites

were complete, and that the intent date of "12113/97" was to indicate the day the

conditions were met. The second supervisor stated that he did not review Data Sheet 1

. before marking Step 1.2 as "CM."

Procedure 09-13 also stated that "condition met (C/M) should be entered if an individual

finds that the requirements of a procedure step are already satisfied." The inspector

noted that the requirements of Procedure Step 1.2 were not met, in that the datil sheet

was not filled out.

The use of initials by each line in the procedures was required by the EMO

superintendent, but not by Dresden administrative procedures. Incorrectly using "CM"

was therefore not a violation. The use of "CM" led to a failure to document completion of

prerequisites on Data Sheet 1, and therefore the use of "CM" led to a failure to follow

procedures. No violation is being issued for this example of failure to follow procedures

because the circumstances would be expected to be enveloped by the violation being

issued for the initial failure to follow procedures on the battery .

19

- ---* __;::_____:.:....;_-=-------* ----- - -.--::.:.*-===----==:=::..:_-.::.:..-=.. ____ :__;.....:_

- -


.

    • --

*- - *-- ... -- ---

  • -** --

c.

Conclusions -

On December 13, work performed without referencing a required procedure, combined

with material condition, tripped off the Unit 3 charger and placed both units unexpectedly.

into a two-hour.LCOi *'Fhe subsequent follow up work was not performed in accordance

with station administrative procedures. Specifically, the "CM" sign off was used when a

condition had not been met.

Section 08.1 of Dresden IRS0-237/97024; 50-249/97024 documented a case where the

incorrect. use of "CM" led to the high pressure. coolant injection (HPCI} system being

unavailable. The inspectors were concerned that the second example of "CM" being

used incorrectly occurred. ,

MB

Miscellaneous Maintenance Issues.

MB.1

Tracking of Rework (62707)

In Section EB.2 .of Inspection Report 97019, the inspectors discussed rework tracking.

The inspectors noted that the licensee's methodology was recently changed. To perform

an assessment of rework, the inspectors kept a list of seleCted items that were known to

be rework, then checked if the items were captured into rework tracking. The results

revealed that one of five items was not captured. The licensee was investigating why it

wasn't tracked. Based on the large number of items that were captured, though not .

specifically tracked by the inspectors, the inspectors concluded that one identified

anomaly did not invalidate the total tracking of rework, but was cause for the inspectors to

expand the sample size.

The inspectors also noted that the 125 VDC battery work discussed in Section M4.1 of

this report was not originally identified as rework. The inspectors noted that assigning a

second supervisor to become familiar with and execute work was unnecessary repetition

of work caused by inadequate performance of the original task, and was therefore rework.

The inspectors discussed this observation with the licensee's rework coordinator.

Ill. Engineering

E1

Conduct of Engineering

E1 .1

Root Cause Investigation of Unit 2 Automatic Reactor Trip

a.

Inspection Scope (37551)

The inspectors discussed the event's root cause with the licensee's investigation team,

interviewed individual engineers associated with the investigation, and attended the

PORC meeting where the team presented their results to licensee management.

b.

Observations and Findings

The event response team's charter directed the team to determine the root cause of the

event, evaluate the plant's response, and evaluate the suit~bility for restart .

20

The inspectors determined that the team was self-critical in evaluating the root cause and

did not hesitate to state that the utility's past actions in response to the GE SIL were not

consistent with current policies and practices. After the scram, the station experienced

several more LPRM half scrams. The half scrams occurred on Unit 3 and involved

detectors that had not previously exhibited spiking. For example, Unit 3 operators

received an unexpected Channel "8" half seram on January 5, 1998, due to a spike on

. LPRM 10-24-49. On January 7, 1998, a Channel "B" half scram occurred due to spiking

on LPRM 32-57 A. . The station re~reviewed the SIL and implemented new actions to *

address LPRM spiking. Before the end of the inspection period, the station worked

around the clock to perform the current-voltage curves for all LPRMs that fed the APRMs.

Results of the tests were used to determine the* need for *capacitance discharge (!'whisker

bums") tests on LPRMs, that exhibited the potential for spiking. At-the end of the

inspection period, the licensee was working on a schedule to complete testing on the

remaining LPRMs, as well as future long term actions to address the issue of LPRM

spiking.

The inspectors also reviewed. the team's assessment of the plant equipment response

following the scram. Except for the FWLC system response (discussed in Section E1.2),

plant equipment functioned as expected with only minor anomalies noted. The team

appropriately dispositioned these items.

c.

Conclusion

The.inspectors concluded that the licensee's root cause team performed a thorough: *

investigation of the event, the root cause, and equipment response following the reactor

scram. The licensee's team concluded that the root cause of the event was the failure to

perform the actions identified in GE SIL 500 regarding LPRM spiking. The inspectors

agreed with this conclusion.

E1 .2

Response of the FWLC System Following Unit 2 Automatic Reactor Trip

a.

Inspection Scope (37551)

The response of the FWLC system caused reactor vessel water l~vel to overshoot

following the scram. The overshoot would have flooded the HPCI steam line had HPCI *

not been already isolated for troubleshooting purposes. The inspectors reviewed the

licensee's investigation into the issue and proposed resolution prior to restart.

b.

Observations and Findings

The inspectors noted expected reactor vessel water level response immediately following

the reactor trip. Vessel level dropped to approximately -4" (normal level is +30") due to

shrink; this response was normal and expected. However, upon level recovery reactor

water level rose above +60" and was about 3" above the lower level of the HPCI steam

lines. Per design, at this level the HPCI system would have tripped, but not physically

isolated. The HPCI steam line would have flooded had the system not already been

isolated for maintenance purposes. The configuration of the steam supply piping was

such that the water would have remained trapped in the line after vessel level dropped

back below the trip setpoint.

21

--.:--. ___ __:. ... _:..:::.: __ -*. -------*--* **---

The response of the FWLC system was as designed. However, in *this case, appropriate

equipment response and appropriate post-trip operator response did not prevent a

reactor water level overshoot and potential filling of the HPCI steam lines. Upon receipt

of reactor scram and level drop from 30" (normal) to +2", "setpoint setdown" occurs.

During setpoint setdown, the FWLC system changes the required level setpoint and ramp

rate of the feedwater regulating valve (FRV) so that upon level recovery, water level does

not overshoot and raise the vessel level too high. However, the receipt of "bad quality"

data introduces a time delay in the initiation of setpoint setdown. Bad quality data was

defined as data that was outside the range of the narrow range level indicator scale; on

Unit 2 the narrow range level indicators read from O" to +60". Therefore, when reactor

  • water level dropped to approximately -4", the FWLC system logic received "bad quality"

data and a time delay (between three to seven.seconds) occurred before setpoint

setdown was initiated. This time delay was sufficient to prevent th*e FWLC system from

responding quickly enough to prevent a level overshoot. Since the FWLC. system and

post scram water level drop responses were normal and as .expected, all Unit 2 scrams

from full power have the potential to result in a level.overshoot with the corresponding

effect of putting water.in the HPCI steam line.

Several differences existed between the Unit 2 and Unit 3 FWLC systems that would

have prevented a level overshoot on Unit 3. On Unit 3, the FWLC system was set up in

three element control, whereas on Unit 2 the system was set up in single element control.

The Unit 3 narrow. range level transmitters are scaled from -60" to +60" which would .

  • prevent the receipt of "bad quality" level data following a reactor trip. Also on Unit 3,

when a reactor scram signal is received, the system immediately goes into setpoint *

setdown that aids in vessel level recovery efforts. The licensee's root cause investigation

team concluded that these factors would prevent a similar level overshoot from occurring

  • on Unit 3. The inspectors reviewed the team's results and did not disagree with this

conclusion.

The licensee's resolution to address the response of the FWLC system included both

long term and short term corrective actions. The licensee.plans to modify the Unit 2

FWLC system during the upcoming refueling outage to make it similar to the system on

Unit 3. The licensee planned to rely on operator compensatory actions for the immediate

short term corrective actions. Upon receipt of a scram signal, operators would be

required to analyze feedwater system response and trip off one running feedwater pump

once level turned and started to rise following a reactor.trip. In addition to tripping a

reactor feedwater pump, operators would also be required to take manual control of the

feedwater regulating valves to ensure that level would not overshoot and flood steam

lines. The inspectors reviewed post event charts and concluded that these actions would

be required within the first ten seconds following the reactor scram. The inspectors were

concerned that the station was relying on operator action to prevent water intrusion into

HPCI steam lines following a reactor scram.

c.

Conclusion

The FWLC system response presented a potential challenge to the operators following

the reactor scram. The compensatory actions that operators are required to take

following a scram on Unit 2 constitute an additional operator work-around. Pending

permanent resolution of the Unit 2 FWLC system issues, the station was relying on

operator intervention following a scram to prevent water intrusion into HPCI steam lines.

22

q

_.,_ __ ::_;_ ___ ;.:. -* -- --* . .:

E2

Engineering Support of Facilities and Equipment

E2.1

(Units 2. 3) Operability Evaluations

a.

Inspection Scope (71707. 37551)

The inspectors reviewed recent operability evaluations. Compliance with the

requirements of OAP 07-31, Rev: 07, "Operability Determinations," and the impact on

plant operations were considered. A detailed evaluation of any engineering calculations

used to make the final determinations was not performed.

Operability determinations revi.ewed included: 97-105

97-107

97.,.108

97-'109 97-110

.97-112

"Personnel Air Lock Equalizing Valve - Concern Identified with Material of

Seals"

"Concern of Potential Vortexing in CSTs"

  • "Failure of the Unit 2 125 VDC Alternate Battery to Maintain 105 Voe at

Bus under D.B.A. Condition"

"HPCI Small Bore Lines Do Not Meet UFSAR Design Criteria" ,

"Reactor Building Superstructure Seismic Requirements"

"Post-LOCA Reactor Building Temperatures Beyond UFSAR Limit of

.104°F"

    • * *

b.

Observations and *Findings

  • The operability .determinations reached the following conclusions: 97-105 -

97-107 -

97-108 -

Operable, but degraded. The concern was that if exposed to design basis

accident (OBA) conditions *of 334°F and 63 psia, the airlock equalizing

valves' seats may soften and cause a leak. Based on calculations, the

licensee determined that the outer door would probably not be affected.

Corrective action required was to schedule replacement of equalizing

valves on all airlock doors during D2R15 and 03R15.

Operable, but degraded. The concern was that vortexing may occur and

cause air entrainment in HPCI system. Calculations showed that aligning

the HPCI system suctions to both condensate storage tanks (CSTs) would

be sufficient to prevent vortexing. Also, *postulated breaks inside

containment resulted in a swap to torus suction before reaching CST

vortexing. Postulated breaks outside of containment challenged the CST*

supply. Corrective actions included realigning the CST supplies and

evaluating changing the CST low level switches.

No concern exists. The concern was that the 1000-foot cable-run from the

  • Unit 2 125 voe alternate battery to the *distribution panel resulted in a
  • previously unconsidered voltage drop. Engineering concluded that based

on latest actual battery surveillance tests and calculations, no concern

exists. Although the battery currently met its requirements, engineering

added a request to add additional cells to address expected margin

  • reduction due to aging.

23

97-109-

97-110 -

97-112 -

Operable but degraded. The concern was that several Unit 2 and Unit 3

HPCI system lines were inadequately supported to meet design basis

requirements. The lines included drain pot discharge lines and the gland

seal condenser discharge line to the torus. The licensee concluded that

the lines were operable because the lines met the requirements of ComEd

Nuclear Engineering Standard (NES) No. NES-MS-03.2, "Evaluation of

Discrepant Piping and Support Systems," Rev. 0, and the stresses were

less than twice yield stress. Corrective action planned was to reevaluate

the piping and determine how to restore it to design limits.

Operable but degraded. The concern was that calculations for the reactor

building crane being loaded during ,a safe shutdown earthquake (SSE}

were never performed. Engineering concluded that the 125-ton crane* *

must be limited to 12.5 tons based. on determining that the additional

12.5 tons was insignificant compared with the mass of the crane and

trolley ... For corrective actions, the licensee planned to determine what

  • commitments existed regarding the required analysis, and, if ne.cessary,

perform a detailed analysis for SSE while the maximum crane load was

lifted.*

Operable but degraded. The concern was that recent calculations showed

  • that the post.;.accident temperatures .of. the* reactor building were generally

from 120 to 160°F, whereas the UF~AR limit was 104°F. Engineering

concluded that as long as the outside air 30-day average temperature *

remained below 44 ° F or 68 ° F (the temperature depended on other

compensatory actions), then the safety-related equipment will function.

Corrective actions included direction to shut down the non-accident unit

and other actions to increa*se reactor building cooling, and re-calculation of

temperatures.

Operability determinations were governed by OAP 07-31, Rev. 07, "Operability

Determinations." The performance of the reviewed operability determinations met

DAP 07-31. The engineering used to make operability conciusion.s appeared reasonable.

The operability determinations reflect the status of the design basis at Dresden. The

licensee did not have supporting calculations for some systems. As the calculations are

performed, some calculations raise operability concerns. T1:'1e licensee was dealing with

these issues appropriately, even when the compensatory or corrective actions were

significant.

The licensee used the Dresden Engineering Assurance Group (DEAG} to review the

operability determinations. No PIFs or.rework resulted from the DEAG's reviews of

determinations97-107, 97-109, and 97-110-. The DEAG did comment on determination 97-110 regarding the need to provide a complete basis for corrective actions. The DAEG

review identified "major problems" with the basis for operability and the ci:>rrective actions

related to determination 97-106, "Lack of vent valves on CCSW suction headers,

24

J *

.

-

-

- -*- .. - *- *-*-*-*-*

-

repriming, and leakage criteria,"*and generated PIF No. 01997-08537. Note that 97-106

was not' discussed in this report because it was reviewed in Dresden Inspection Report

No. 50-237/97021; 59-249/97021. The DEAG did not review 97-108 because no concern

was identified.

c.

Conclusions

The operability evaluations.appeared to meet licensee requirements. The evaluations

were reasonable and provided adequate bases for the conclusions.

The scope of the evaluations reflected the current state of the design of Dresden Station,

in that several evaluations resulted from .performing calculations to replace missing or

never-performed calculations. * ;

-

E4

Engineering Staff Knowledge and Performance

E4.1

(Unit 3) Engineering Evaluation of Batteries

a.

Inspection Scope (37551)

.

b.

The inspectors assessed the engineering response to the December 13 event in which

the Unit 3 125 V battery charger was inadvertently tripped.

Observations and Findings

As discussed in Section M4.1, the Unit 3 battery charger was tripped inadvertently during

maintenance. The control room logs and the PIFs written about the event recorded that

the voltage on the batteries had dropped to 115 Voe. The inspectors asked the licensee

if 115 voe was the expected value for the 125 voe batteries.

The licensee had not previously considered the battery's response, because the battery

remained above.105 voe and passed its last surveillance test.

However, a few days after the initial question, the licensee compared the performance

with a vendor-supplied graph of the discharge characteristics of the battery and

concluded that 115 VDC was the expected voltage given the loads on the battery.

c.

Conclusions

The licensee had not performed a detailed reviewed the battery's performance. However:

the licensee eventually was able to show that the battery behaved as it should have.

25

I

..

---*-----=*-** - --~--'

IV. Plant Support Areas

Radiological Protection and Chemistry (RP&C) ..

R4

Staff Knowledge and Performance In RP&C

R4.1

(Units 2. 3) Treatment of Contam_inated Area Boundaries

-a.

lnspe~ion Scope (71750)

The inspectors observed worker performance around contamination area boundaries with

. respect to. the. licensee's. RP&C procedures.

b.

Observations and Findings

Workers generally respected the boundaries placed to control contaminated areas. The

placement of step-off pads and boundaries provided sufficient room for worker:s to work.

Equipment was generally staged or stored correctly and did not present a contamination

control hazard.

On December 19, the inspectors identified that a white hose that:crossed a step-off*pad

in the Unit 2 east torus basement area was not secured at the contamination boundary.

The inspectors informed the licensee and the licensee secured the hose. The licensee

issued PIF 01977-08731 to track the issue, and determined that the hose had originally

been placed to support work on the east low pressure coolant injection "(LPCI) system

comer room sumps. The work was completed, but the 2A east comer room sump was

still not working property since repairs, so the hose was staged as part of a contingency in

case the 28 east comer room sump failed. The licensee also found that the equipment in

use tag on the hose was not up to date.

A search of PIFs revealed four other examples of untaped or improperty marked hoses

(ref. PIFs No. 01997-07363, -07396, -08390, 08607). This was a marked increase from

the number of radiation control PIFs written during the previous months.

Procedure OAP 03-07, Rev. 09, "Control of the serviee air and domestic water systems

and hoses for general station use," Step F.3.e. stated, "IF a RED, WHITE, OR CLEAR

hose must cross the boundary between a contaminated area AND a non-contaminated

area, THEN the hose must be secured at the boundary using Radioactive Materials

Tape." The failure to secure the hose was a violation of OAP 03-07

(VIO 50-237/97028-03 (DRP); 5~-249/97028-03 (DRP)).

The inspectors also saw other examples of poor control of contamination boundaries.

For example, a worker mopping a contaminated area allowed the bucket to cross the

contamination boundary, and other workers placed equipment and work instructions on

contamination boundaries .

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c.

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Conclusions


__ :*_::_ ------ - *--- ... :.: - . --

The setup and control of contaminated areas and work in contaminated areas were

usually correct.

The inspectors identified one example of an improperly secured hose that crossed a

contamination boundary.* The hose had been staged in response to a poorly performing

sump pump.

The safety significance of these' issues was minor. However, the inspectors were

concerned with the lack of attention to detail exhibited by the plant staff to radiation

controls, and that the PIF record showed this to b~ an emergent trend.

V. Management Meetings *

X 1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on January 12, 1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

X3

Management Meeting Summary

On December 22, the NRC Region Ill Regional Administrator and the Director of the

Division of Reactor Projects visited the site, met with senior licensee management, and

discussed current licensee performance. *

27

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'PARTIAL LISTOF PERSONS CONTACTED

G. Abrel, ComEd NRC Coordinator

D. Ambler, Regulatory Assurance Supervisor (Actirig)

  • P. Bernice, Ops Staff *

T. Bezouska, Site Vice President Staff Assistant

- .

R. Fisher, Maintenance Manager *

,

R. Freeman, Site Engineering Manager.

M. Heffley, Site Vice President

C. Howland, Radiation Protection Manager

L Jordan, Training *Supervisor (Actirig) *

w. Liscomb, Site Vi-de President'Staff *  ;

    • * *

P. Stafford, Station Manager (Former Outage/Work Control Manager)

D. Willis, EMO s*uperintendent

' *

i

  • *

D. Winchester, Q&SA Manager

28

L_ ______ _ _:_ __ --------=--- _* _ _:.. -::.::. ___ *.:.._::__:_:__.*-*::.....:....:.

LIST OF INSPECTION .PROCEDURES USED

Inspection Module: 71707.

Operational Safety Verification

Inspection Module: 83822

Radiation Protection

Inspection Module: 62707

Maintenari6e

Inspection Module: 61726 * Surveillance Observations

Inspection Module: 40500

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Inspection Module: 93702

Prompt On-Site Response t9 Events at Operating Power Reactors

Inspection Module: 37551

On-Site Engineering

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-237; 249/97028-01

50-237; 249/97028-02

50-237; 249/97028-03

Closed

None

Discussed*

None

VIO

failure to follow PIF process

VIO

failure to use procedures

VIO

failure to follow radiation protection procedures

29

)

DAN

OAP

DATR

. DEOP

DGA

DOA

DOP

EOPR

FWLC

HPCI

IFI

IPE

IR

ISEG

ISi

LCO

LER

LPCI

LPRM.

NCV

NLO

NOV

NRC

NRR

NSO

NSWP

OE

01 oos

PIF

PORC

RUF SAR

Q&SA

QC

TS

us

VIO

WEC

WR

.

. .

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---. ... -- **--------- ----*

LIST OF ACRONYMS USED

Dresden Annunciator Procedure

Dresden Administrative Procedure

Dresden Administrative Technical Requirement

Dresden Emergency Operating Procedure

Dre.sden General Abnormal Procedure

Dresden System Operating Abnormal Procedure

Dresden System Operating Procedure

Engineering Operational Planning/Troubleshooting Report.

Feedwater Level Control*

High Pressure Coolant Injection

Inspection Followup Item

Individual Plant Evaluation

Inspection Report

Independent Site Engineering Group

lnservice Inspection

Limiting Condition for Operation

  • Licensee Event Report

Low Pressure Coolant Injection

Local Power Range Monitor

Non-Cited Violation

Non-licensed Operator

Notice of Violation

Nuclear Regulatory .Commission .

Office of Nuclear Reactor Regulation

Nuclear Station Operator

Nuclear Station Work Procedure

  • Office of Enforcement

Office of Investigations

Out-of-Service

Problem Identification Form

Plant Operations Review Committee

Revised Updated Final Safety Analysis Report

Quality and Safety Assessment

Quality Control *

Technical Specification

Unit Supervisor

Violation

Work Execution Center

Work Request 30