ML17188A046

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Forwards Insp Repts 50-237/97-28 & 50-249/97-28 on 971123- 980112 & Nov.On 971206,efforts to Restore Unit 3 a Train of Offgas Sys Resulted in Offgas Sys Fire
ML17188A046
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/06/1998
From: Grant G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Kingsley O
COMMONWEALTH EDISON CO.
Shared Package
ML17188A047 List:
References
50-237-97-28, 50-249-97-28, NUDOCS 9802200066
Download: ML17188A046 (3)


See also: IR 05000237/1997028

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION Ill

  • Mr.* Oliver D. Kingsley

President, Nuclear Generation Group

Commonwealth Edison Company

ATTN: Regulatory Services

Executive Towers West Ill

  • *

1400 Opus Place, Suite 500 * * *

Downers Grove, IL 60515

801 WARRENVILLE ROAD

LISLE, ILLINOIS 60532-4351

February 6, 1998

  • .; ..... '

SUBJECT: *

NOTICE OF VIOLATION AND NRC INSPECTION REPORT

NO. 5~237/97028(DRP); 50-249/97028(DRP)

Dear Mr. Kjngsley:

This refers to the inspection conducted from November 23, 1997, to January 12, 1998, at the

Dresden facility. The purpose of the inspection was to determine whether activities authorized by

the license were conducted safely and in acc0rdarice with NRC requirements. During this period,

routine resident inspections were performed. The enclosed report presents the results of these .

inspections .

Overall, the plant operations were safe. However, plant material condition and some

maintenance activities continued to challenge the operators. On December 6, 1997, efforts to

restore the Unit 3 A train of the offgas system resulted in an offgas system fire. On

December 13, work performed by the staff caused an unplanned entry into a two-hour limiting

condition for operation. On .December 23, Unit 2 automatically scrammed due to a spurious

average power range monitor (APRM) signal during an unrelated surveillance of reactor pressure

vessel high pressure scram signals. Following the scram, the feedwater control system caused

the reactor vessel water level to increase high enough to flood the HPCI system, but the HPCI

system was still isolated. On three occasions during this inspection period, one or both HPCI

systems were inoperable due to material condition and design issues. Some of the* material

condition issues were repeat items that the station had not been able to resolve successfully.

Based on the results of this inspection, the NRC has determined that violations of ~RC

requirements occurred. The first violation involves a failure to implement part of the corrective

actions process. The inspection found that corrective actions for this violation had already been

implemented. The second violation was of concern because inappropriate actions performed

during maintenance resulted in an unplanned entry into a two-hour dual-unit limiting condition for

operation. The third violation was of concern because it appeared indicative of an increasing

trend of errors in controlling contamination area boundaries.

.

.

The violations are cited in the enclosed Notice of Violation (Notice), and the circumstances

surrounding the violations are described in detail in the subject inspection report.

9802200066 980206 -.

PDR

ADOCK 05000237

G

PDR

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0. Kingsley

-2-

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response, in part, to

detennine whether further enforcement action is necessary to ensure compliance with regulatory

requirements.

In accordance with 1 O CFR 2. 790 of the NRC's "Rules of Practice," a copy of this letter, its

enclosures, and yourresponse will be placed in the*NRC Public Document Room.

Sincerely,

'

.,

  • .!

'

  • .. ;; !.

. /s/ G~ E~ Grant

Geoffrey E. Grant,* Chief

Division of Reactor Projects

Docket Nos.

50-237; 50-249

License Nos. DPR-19; DPR-25

Enclosures:*

1.

2.

Notice of Violation

Inspection Report

No. 50-237/97028(DRP)~

50-249/97028(DRP)

.

cc w/encls:

M. Wallace, Chief of Staff

D. Helwig, Senior Vice President

G. Stanley, PWR Vice President .

J. Perry, BWR Vice President

D. Farrar, Regulatory

Services Manager

I. Johnson, Licensing Director

DCD - Licensing

M. Heffley, Site Vice President

T. Nauman, Station Manager Unit 1

P. Stafford, Station Manager Units 2 and 3

F. Spangenberg, Regulatory Assurance

.Manager

Richard Hubbard

Nathan Schloss, Economist

Office of the Attorney General

State Liaison Officer

Chainnan, Illinois Commerce

Commission

DOCUMENT NAME: G:\\DRES\\DRE97028.DRP

To receive e co

of this document, Indicate In the box "C" c Co

wtthout attach/encl "E" = Co

wtth attach/encl "N" c No copy

OFFICE

Riii

Riii

NAME

Grant

DATE

021(p1

OFFICIAL RECORD COPY

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*--- ------*- -*--- *---* ****------*---*- **-- -- ---- *- --* -*- -- --- .

0. Kingsley

Distribution:

Docket File w/encls

PUBLIC IE-01 w/encls *

A Beach w/encls

Deputy RA w/encls

Riii Enf. Coord. w/encls

SRI Dresden w/encls

Project Mgr., NRR w/encls

DRPw/encls

  • .....

-2-

TSS w/encls

DRS (2) w/encls

Riii PRR w/encls

RAC1 (E-Mail)

CAA 1 (E-Mail)

  • ~ DOCDESK (E-Mail)

Project Mgr., Unit 1, NRR w/encls