ML17180A748

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Insp Repts 50-237/94-03 & 50-249/94-03 on 940228-0405. Violations Noted.Major Areas Inspected:Engineering & Technical Support & Related Mgt Activities
ML17180A748
Person / Time
Site: Dresden  
Issue date: 05/06/1994
From: Langstaff R, Shafer W, Vanderniet C, Walker H, Yin I
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17180A746 List:
References
50-237-94-03, 50-237-94-3, 50-249-94-03, 50-249-94-3, NUDOCS 9405160302
Download: ML17180A748 (27)


See also: IR 05000237/1994003

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-237/94003(DRS); No. 50-249/94003(DRS)

Docket Nos. 50-237; 50-249

Licenses No. DPR-19; No. DPR-25

Licensee:

Commonwealth Edison Company

Executive Towers West III

1400 Opus Place - Suite 300

Downers Grove, IL 60515

Facility Name:

Dresden Nuclear Power Station - Units 2 and 3

Inspection At:

Dresden Nuclear Power Station, Dresden, IL

Inspection Conducted:

February 28 through April 5, 1994

Inspectors:

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ri. GWiJ kef:~r

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NRC Consultants: J. T. Haller (Parameter, Inc.)

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Date

5/6/J;J

Date

5!tc/£<1

Date

D. C. Prevatte (Powerdyne Corporation)

Observer:

L. A.

Love~Tedjoutomo (Atomic Control Board, Canada)

Approved By:

5j/94

D te

Inspection Summary

Inspection conducted February 28 through April 5, 1994 (Reports

No. 50-237/94003CDRS); No. 50-249/94003CDRSll

Areas Inspected:

An announced team inspection of engineering and technical

support and related management activities. The inspection was conducted

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utilizing portions* of inspection procedures 37700, 92701, 92702, and 92720 and

draft inspection procedure 37550 to ascertain whether engineering and

technical support was effectively accomplished and assessed by the licensee.

Results:

Based on the items inspected, overall performance in engineering and

technical support was considered acceptable. The level, quality, and

timeliness of engineering and technical support for the plant appeared to be

acceptable.

Most of the individuals contacted were knowledgeable and

motivated and displayed a strong sense of ownership in their areas of

responsibility, however, there were some-exceptions as noted in this report.

Significant improvements were noted in the Site Engineering and Construction

Organization, however, there were several findings where engineering

activities had not been thorough and the necessary attention to detail was

lacking. Little improvement was evident in the Systems Engineering

Organization.

The most significant weakness appeared to be in the control of temporary

alterations and lack of compliance to plant procedures.

The most significant

strength appeared to be the Site Engineering and Construction Organization

management's motivation and commitment to improvement.

Two violations, one with.two examples and one with three examples 9 were

identified. Violations included weaknesses in design control and a lack of

compliance to procedures.

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DETAILS

1.0

Pri~cipal Persons Contacted

Commonwealth Edison Company CCECo)

  • * * * *
  • *

H. Massin, Site Engineering Construction Manager

G. Spedl, Station Manager

S. Elderidge, Modification Coordinator

R. Jackson, System Engineering Team Leader

R. Robey, Site Quality Verification Director

J. Shields, Regulatory Assurance Supervisor

J. Smentek, Site Engineering Construction Engineer

D. Spencer, Lead Electrical - Plant Support

M. Strait, System Engineering Supervisor

J. Williams, Site Engineering Construction Supervisor

R. Wroblewski, NRC Coordinator

U. S. Nuclear Regulatory Commission

  • *

R. Crlenjak, Acting Deputy Director DRS

M. Leach, Senior Resident Inspector

P. Hiland, Chief, Projects Section lB

C. Phillips, Resident Inspector

W. Shafer, Chief, Maintenance and Outage Section

A. Stone, Resident Inspector

  • Denotes those present at the exit meeting on April 5, 1994.

Other persons were contacted as a matter of course during the

inspection.

2.0

Licensee Action on Previous Inspection Findings

A number of problems or concerns identified in past NRC inspections were

reviewed for appropriate corrective actions.

The items reviewed and the

inspectors' evaluations of the actions to address these issues are

discussed in this section. *

2.1

(Closed) Unresolved Item (237/249/91025-02)

Procedures were not

followed in providing fire watch coverage.

Licensee personnel indicated

that fire watch coverage was not required since the fire barriers

involved were non-rated barriers located in the same fire area.

Procedure DFPP 4175-01, "Fire Barrier Integrity and Maintenance," was

revised to clarify rated and non-rated fire barriers. This item is

closed.

2.2

(Clbsed) Inspection Follow-up Item (237/249/93008-01) -- Evaluation to

examine the possibility of conducting a temperature effectiveness test

on the LPCI/CCSW heat exchangers.

Plans had been made to conduct a

temperature effectiveness test on the LPCI/CCSW heat exchangers;

however, due to the difficulties involved, the tests might not be

conclusive.

The present method of performing preventive maintenance on

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these exchangers appeared to be sufficient to assure proper operation.

This item is closed.

2.3

{Closed) Inspection Follow-up Item (237/249/93008-03) -- Expanded

acceptance criteria, used in the testing of the emergency diesel

generator cooling water pump, did not meet ASME code requirements.

Revision 11 of procedure DOS 6600-08 was issued to eliminate acceptance

criteria for the diesel generator cooling water pump flows.

The

acceptance criteria was revised to be consistent with ASME code

requirements and was included in table 10 of the Dresden In-Service

Acceptance Criteria Manual.

This item is closed.

2.4

CCl~sed) Inspection Follow-Llp Item (237/93015-01) -- There was no method

or criteria for identifying excessive stem nut wear on motor operated

valves. Although there was still no method or criteria for measuring

excessive stem nut wear, discussions with licensee personnel indicated

  • that maintenance personnel were aware of the stem nut wear problem and

the stem nut was visually inspected in place for signs of excessive wear

during normal MDV preventive maintenance activities.

In addition, a

search was underway for a reliable and economical method for measuring

stem nut wear including acceptance criteria.

2.5

{Closed) Inspection Followup Item (237/249/93020-09) -- Root cause

investigation and corrective actions for spurious group V primary

containment isolations due to flow spiking. This item is closed based

on the review associated with licensee event report (LER} 237/92-45

supplement 2.

2.6

{Open) Unresolved Item (237/249/93030-0lCDRS)) -- Acceptability of using

sampling inspection for quality control (QC) hold points.

Random

sampling was used to verify QC hold points for inspections required by

ANSI/ASME NQA-1, "Quality Assurance Program Requirements for Nuclear

Power Plants," 1989, and ANSI/ASME NQA-2, "Quality Assurance

Requirements for Nuclear Facility Applications," 1989.

On December 3,

1993, licensee personnel requested an interpretation from the American

Society of Mechanical Engineers (ASME} concerning the use of sampling

for required inspection activities.

No interpretation had yet been

provided at the time of this inspection. This item will remain open

pending receipt and* review of the interpretation provided by ASME.

2.7

{Open) Violation 237/249/93030-02{DRS) -- The procedure, which

controlled the use of measuring and test equipment (M&TE}, did not

provide appropriate qualitative or quantitative criteria for performing

evaluations of tested and inspected equipment when measuring and testing

equipment (M&TE} were determined to be lost or were found to be out of

calibration.

An action plan had been developed to provide necessary

improvements in the M&TE area.

Many of the actions, required by the

plan, had not been implemented.

At the time of the inspection,

Procedure DAP 11-22, "Control of Measuring and Test Equipment," had not

been revised and the review of instrument evaluations back to January,

1993, had not been completed. This violation will remain open pending

additional review when commitments have been completed.

2.8

{Closed) Violation (237/93030-03) -- Measures were not established to

assure that deficiencies and deviations identified by contract quality

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2.9

2.10

3.0

3.1

control inspectors on observation reports were corrected.

Licensee

personnel reviewed observation reports initiated in 1993 and initiated

problem identification forms (PIFs) for observation reports which had

not been resolved.

Licensee and contractor personnel began using PIFs

to document problems identified by contractors. The inspectors

interviewed contract QC inspectors and confirmed PIFs were being used in

lieu of observation reports. This violation is closed.

(Closed) Inspection Follow-up Item (237/93030-04) -- There was no

investigation to determine the cause of the miswiring of the limit

switch for the high pressure coolant injection (HPCI) containment

isolation valve, which resulted in a failure of the valve to open in May

of 1993.

Licensee personnel's investigation identified the causes as

failure to follow work instructions and inadequate emphasis on

implementation of change documents (such as the field change request

which implemented modification Ml2-2-92-001G).

As part of the

corrective action, licensee personnel provided training to Site

Engineering and Construction (SEC) personnel involved in the

modification process. This item is closed.

(Open) Unresolved Item (237/249/93034-06) -- A portion of the Unit 2

core spray leak detection instrument lines had not been tested. This

item was reviewed and the majority of the work was still pending.

This

item will remain open.

Licensee Action on Licensee Event Reports

The inspectors reviewed the action taken on a number of licensee event

reports (LERs) for appropriate corrective actions.

The LERs reviewed

and the inspectors' evaluations of the actions to address these issues

are discussed in this section.

(Closed) Licensee Event Report 237/87-010 -- This LER 9 dated February 2,

1987, reported that the embedment plate for support Mll50-D-62 on the

Unit 2 Core Spray system had pulled away from the ceiling 1/8

11 to 1/4

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During the review of records related to this LER 9 the inspectors noted

that calculations concluded that the damage was caused by water hammer.

The water hammer was not reported in LER 87-010 or by a separate LER.

Licensee personnel committed to update LER 87-010 to include

documentation of the water hammer, root cause evaluation, and corrective

actions.

Licensee personnel performed a walk down of the system and found no

other damage.

The damage to the support was repaired and an embedment

plate assessment program was completed at both the Dresden and Quad

Cities stations. The hardware changes made to correct the damage to the

pipe supports appeared to be adequate.

This item is closed.

3.2

(Closed) Licensee Event Report 237/91-012: This LER, dated October 3,

1990, reported significant corrosion on Unit 2 pipe support M-3212-05 at

the base plate and on the.exposed portion of the concrete expansion

anchors.

The cause was attributed to corrosion induced by standing

water in the HPCI steam tunnel.

The standing water was due to ground

water in-leakage. Licensee personnel resolved the problem by injecting

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hydrophilic.polymer resin into the concrete cracks where the in-leakage

was found.

This item is closed.

3.3

{Closed) Licensee Event Report 237/92-045-2 -- This LER supplement,

dated January 28, 1994, provided follow up information on an isolation

condenser group V isolation due to spurious flow spikes. The cause of

the flow spikes was determined to be process noise from operation of the

shut down cooling system.

To reduce the number of spurious group V

isolations, licensee personnel revised operating procedures to isolate

the system when not required by Technical Specifications.

Licensee

personnel planned to supplement the LER to correct information

concerning the corrective actions. The inspectors reviewed the

procedural changes and no concerns were identified. This item is

closed.

3.4

{Closed) Licensee Event Report 237/93-001: This LER, dated December 23,

1992, reported a pipe support removal to allow the installation of a new

support on the isolation condenser clean demineralized water fill system

without analyzing for this condition.

The inspectors reviewed the

corrective actions taken to resolve the problem and considered them to

be acceptable. This item is closed.

3:5

{Closed} Licensee Event Report 237/93-012:

This LER, dated May 18,

1992, reported that the Unit 2 emergency diesel generator breaker failed

to auto-close as required.

The LER indicated that the Bus 24-1 main

supply breaker linkage arm which, upon breaker operation, positions the

breakers cell mounted auxiliary switches, had been bent.

Upon opening

of the main bus supply breaker, the auxiliary switch did not change

position to indicate to the diesel generator breaker closing logic

cir~uit that the main supply breaker was open.

Thus the incoming diesel

generator breaker closing logic was blocked.

Corrective actions

included the replacement of the cell switches and linkage arms with a

new design mechanism similar to that used in the 4.16KV upgrade

modification. This item is closed.

3.6

{Open) Licensee Event Report 237/94-006:

This LER, dated February 5,

1994, reported that Unit 2 shutdown cooling pump motors 2A, 28 and 2C

had been replaced with motors which had different electrical

characteristics and*the protective relay settings had not been changed

or evaluated for the new motors.

Subsequent evaluation and analysis

resulted in resetting the relays to accommodate the replacement motors.

During a review of the documentation and analysis which documented the

revised relay settings, the inspectors noted that the consultant who

developed the new settings, expressed concern regarding the motor

acceleration current versus time characteristics.

An attachment to a

letter dated February 10, 1994, stated that the consultant could not

verify that the settings would allow acceptable motor starting. The

CECo Systems Protection Department concurred and strongly recommended

that the station conduct testing to determine the motor starting

characteristic curves at the earliest convenience.

When queried,

licensee personnel were unable to find evidence that testing had been

con.ducted.

This LER wi 11 remain open pending performance of the testing

and the NRC review of the test results.

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4.0

Inspection Objectives

The objectives of the inspection were to determine if engineering

activities supporting the Dresden Power Station were properly

coordinated and effectively controlled and implemented.

The inspectors

focused on the identification and resolution of technical issues and

problemst design changes and modifications, and internal assessments of

engineering. This was accomplished by observation of work activities,

interviews with selected personnel (including engineers and engineering

management), and reviews of records, procedures, and associated

documentation.

4.1

Performance Data and System Selection

The selection of systems and components for emphasis during this

in~pection was based on a review of data from licensee event reports,

latest SALP information, and discussions with cognizant NRC personnel.

The systems selected were the Reactor Containment, Standby Liquid

Control System and Standby Gas Treatment systems. Modifications and

records for specific electrical, mechanical, and instrumentation

components of these systems were selected for review.

Activities and

documentation involving other systems and components were selected and

reviewed during the inspection to supplement the selected systems.

Consideration was given to the systems and components considered most

safety significant.

4.1.1 Reactor Containment

The inspectors reviewed selected records and walked down the accessible

portions of the reactor building. The following observations were

noted:

4.1.1.1 Containment Isolation Valves Operability Assessments

The inspectors reviewed two operability assessments performed by Site

Engineering and Construction (SEC) personnel. These assessments, dated

March 8, 1994 and March 10, 1994, concerned the HPCI, reactor water

cleanup, and isolation condenser containment isolation valves.

The

assessments were performed in response to Electric Power and Research

Institute testing of motor operated valves (MOVs) which indicated that

higher actuator thrust might be required for certain types of MOVs.

Based on the assessment results, the Unit 3 HPCI containment isolation

valves were declared inoperable on March 3, 1994.

As a result, the

Unit 3 refueling outage, D3Rl3, was started early. This issue will be

followed through the LER reporting system (LER number 94-006).

The assessment concluded that the Unit 2 HPCI containment isolation

valves were operable because of sufficient margin provided by MOV

upgrades completed during a May 1993 outage.

The other valves evaluated

also had sufficient margin to be considered operable.

No concerns or

problems with the operability assessments were identified.

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4.1.1.2 Design of.the Containment Hardened Vent System

The inspectors reviewed modifications Ml2-2-90-029 and Ml2-3-90-029,

which required the addition of a hardened containment wetwell vent to

meet Generic Letter 89-16.

Installation of the modification was

completed February 11, 1993.

The following design inadequacies or

weaknesses were noted:

a.

Inoperability of Containment Vent and Purge System -- The hardened

containment vent was specifically required for conditions beyond

the original plant design/licensing bases which include loss of

offsite power and failure of,non-safety-related systems such as

the instrument air system.

Although the new vent valves added by

this modification were capable of being operated upon loss of

normal instrument air, the existing containment vent and purge

system valves, which are in the vent path, were designed to fail

closed upon loss of power or instrument air. Since the existing

valves could not be opened, the system would be inoperable for the

event for which the system was intended. These valves also could

not be operated manually because they had no manual operators and,

in case of an accident, they could be inaccessible due to high

radiation levels.

b.

Failed fuel events were not properly considered -- Failed fuel

events were not considered in the design of these modifications.

It was evident from statements in Generic Letter 89-16, as well as

other related documents, that failed fuel was intended to be

addressed.

c.

The effects of entrained water were not properly considered -- The

system would be required to handle significant masses of water and

the effects of this water were not adequately considered.

Some of

these effects were the weight of the water, the potential for

water hammer, and the reduction in venting capacity.

Examples of

where these effects weren't properly considered were Calculation

XCE065.0200.001, "Determination of Required Hardened Wetwell Vent

Flow Rate and Vent Pipe Size," Revision 0, which did not consider

the flow capacity reduction, and operating procedure DOP 1600-21,

"Draining Augmented Primary Containment Vent System," Revision 0,

which prohibited system draining for containment pressures greater

than 1.86 psig, making this procedure unusable for the targeted

accident.

d.

The strengthened vent system was incomplete -- The hardened vent

line exhausted into the non-hardened ventilation ductwork located

outside the turbine building which connected with the plant stack.

There was no evidence that the weight of the water, the dynamic

exhaust effects, and the potential for backup into the other

branches of this ductwork was considered. There was no evidence

that the stack would handle the water.

e.

Radiant Heating was Not Considered -- The purchase specification

for the hardened wetwell vent valves and associated hardware

identified 120° F as the maximum temperature for the valve

operators and associated equipment.

No consideration was given to

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f.

radiant heating from the adjacent vent piping containing 310° F

steam.

Design of Backup Air Accumulators

Accumulator Sizing -- The backup air accumulators were installed

to provide air for operation of the valves installed during the

modifications. Only starting air pressure and pressure loss due

to valve stroking were used to determine the size of the backup

air accumulators. Other factors which should have been considered

were (1) minimum pressure to operate and hold the valves against

the maximum differential pressure and flow conditions, (2) system

leakage for the event duration, and (3) potential cooling during

the event.

Accumulator Testing -- Modification test procedure, M12-3-90-029~

did not require adequate testing of the leak tight integrity of

the valves' air operator systems. A minimum pressure to which the

system could decay and still be operable for the required number

of cycles was not established. The minimum pressure specified did

not account for pressure losses for the five operating cycles and

due to cooling. A starting pressure corresponding to the minimum

instrument air supply pressure and a test period correlated to the

accident duration were not established.

Licensee personnel contended that the design was consistent with the BWR

Owners Group (BWROG) recommended design criteria for this system and

that NRR had agreed with the BWROG design criteria. The inspector's

review of the NRC/BWROG correspondence revealed no statement which

concurred with the design criteria or limited the design requirements to

a long-term loss of decay heat removal event but which would not entail

significant fuel failure or other factors. This matter will be

forwarded to the Office of Nuclear Reactor Regulation for further

review.

4.1.1.3 Containment High Energy Line Break Vulnerability

The reactor building closed cooling water (RBCCW) system provided

cooling water to two heat loads inside the drywell, the drywell coolers

and the reactor recirculation pump seals.

MOVs were provided at both

the RBCCW supply and return containment penetrations, however, these

valves are not automatic.

The RBCCW piping inside containment is not

designed against a high energy line break event and no credit can be

taken for operators closing these valves until ten minutes into the

event. Therefore, in a loss of coolant accident, the primary

containment could be bypassed through the open containment isolation

valves and the RBCCW head tank vent line.

The MOVs, in the RBCCW supply and return lines, were non-automatic

containment isolation valves for the RBCCW System.

These valves, 2(3)-

M0-3706 and 3769-500, were not included in the Technical Specification

3/4.18 Primary Containment Isolation Valve List. These valves were

subject to 10 CFR 50, Appendix J, testing and were included in the

containment local leak rate testing program.

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In order to reduce the significance of this issue until final

resolution, licensee personnel have incorporated a requirement to close

these MOVs in case of a coolant accident in the abnormal operating

procedures.

The inclusion of this valve closing requirement in the

emergency operating procedures is under review.

This matter will be forwarded to the Office of Nuclear Reactor

Regulation for further review and generic implications.

4.1.2 Standby Liquid Control System *

During the review of records for the standby liquid control (SBLC)

system, the inspectors noted some design errors in modifications Ml2-2-

84-119 and Ml2-3-84-119.

These two modifications were installed in 1986

and 1987, to address an anticipated transient without scram (ATWS).

The original design pressure for the system was 1,275 psi. With two-

pump operation, as required by the modification, the new injection

pressure was calculated to be 1,330 psig. There were no indications

that the increase in pressure was recognized by the licensee and, as a

result, the design pressure of the piping and components was not

increased to accommodate two-pump operation.

During discussions on the matter, licensee personnel stated that the

piping was physically the same as the 1,500 psi design pressure piping

located elsewhere in the system and, therefore, the piping could be

expected to withstand the additional pressure without detrimental

effects. Based on this information, the direct safety significance of

the design verification oversight appeared to be low; however, the

discrepancies indicated a lack of thoroughness and verification in the

design process at the time of the modifications.

Additional errors noted included the following:

a. *

Inadequate Post-Modification Testing -- Post modification tests

required that the system operation be demonstrated with two pumps

discharging at 1,275 psig.

Post-modification testing did not

require that the system perform at the required design conditions

and, therefore~ the testing was not adequate.

b.

Technical Specification not Updated -- During the inspection, the

inspectors noted that Section 3/4.4 of the Technical Specification

had not been updated to require surveillance testing at the higher

pressure.

c.

Inadequate System Testing Procedures -- Test procedures for the

SBLC pumps and system had not been revised to require testing at

the higher pressure. These procedures, as noted during the

  • inspection, were:

(1)

DOS 1100-01, "Standby Liquid Control System Pump Test,"

Revision 15.

(2)

DOS 1100-03, "Standby Liquid Control Injection Test,

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Revision 16.

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(3)

DOS 1100-04, "Quarterly Standby Liquid Control System Pump

Test for the Inservice Testing (IST) Program," Revision 10.

d.

Standby Liquid Control Design Basis Document Errors -- The

inspectors reviewed portions of the Standby Liquid Control Design

Basis Document, DBD-DR-139, Revision A, which was issued

September 22, 1993.

The system pressure errors described above

were found to be included in this document.

These problems indicated a lack of accuracy, thoroughness and

verification in the design process. The ability of the modified

system to perform as required had never been demonstrated.

The

inaccuracies in the DBD provide a flawed design basis for future

modifications, operability determinations, procedure changes,

etc., all of which could affect the safe operation of the plant.

This failure to provide adequate design control is an example of a

violation of Criterion III of 10 CFR 50, Appendix B

(237/249/94003-0l(DRS)).

During discussions near the end of the inspection, licensee

personnel indicated that steps had been initiated to correct the

design errors and impacted documents.

The SBLC system DBD had

been withdrawn from use and was to be thoroughly checked.

Steps

were in progress to ascertain the quality of the other issued

DBDs.

An example of one violation was identified in this area.

4.1.3 Standby Gas Treatment System

4.2

The inspectors reviewed selected records and walked down the accessible

portions of the standby gas treatment (SBGT) system.

In this area, the

inspectors reviewed an operability assessment for the SBGT system, dated

January 26, 1994. The evaluation documented a decision that the SBGT

system was operable even though the control room SBGT system temperature

indicators provided inaccurate readings. The control room indicators

were not used for operating procedures and the SBGT system surveillance

procedures were revised to use local temperature indicators instead.

The local temperature indicators provided more conservative data than

the control room indicators. Although this operability assessment

appeared to be acceptable, operating for an extended period in this

condition was not considered desirable, since the inability to use these

control room temperature indicators added to the normal operator

workload.

Observations of Plant Conditions

Early in the inspection, the inspectors performed walkdowns to determine

the material condition of the plant.

Indications of equipment problems,

housekeeping and other unusual conditions were noted.

Both units were

operating during this portion of the inspection. Plant conditions were

also observed during the review of modification and other engineering

support activities throughout the inspection.

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None of the problems noted appeared to have an immediate safety

significance or a significant effect on the operation of the plant.

Most equipment in need of repair had been previously identified by

licensee personnel. Overall, the facility appeared to be in better

material condition than during the previous engineering and technical

support inspection. The deficiencies noted, however, indicated that

more attention needed to be focused on less traveled and less accessible

portions of the facility.

The following adverse or unusual conditions were noted:

a.

HPCI System Pipe Supports -- The inspectors observed a significant

difference between Unit 2 and Unit 3 HPCI support and restraint

arrangement for the pump discharge and cooling water return to the

condensate storage tank line, at the pipe riser elbow.

The piping

configuration for both units were similar in this area.

For

Unit 2 the restraint was an anchor made from a dead weight support

and for Unit 3 the restraint was a sliding support.

On March 10, 1994, a PIF was written for the Unit 2 anchor as-

found condition.

The anchor was not analyzed in the original

piping analysis, and was not analyzed during the IEB 79-14

walkdown and evaluation program.

The operability analysis

performed on March 11, 1994, determined that the design stresses

were within the FSAR limits. The inspectors reviewed the records,

and noted that the rigid support was upgraded in 1970 by adding

bracing and a vertical column below the support.

During

construction, the interface between the pipe and the support

surface was inadvertently welded up; this in effect changed the

rigid support into an anchor.

A walkdown to determine IE Bulletin

79-14 discrepancies failed to identify this discrepancy.

Since the dead weight support in Unit 3 had not received an

upgrade similar to the one in Unit 2, the adequacy of the support

was in question.

Licensee personnel presented the Support

calculations, performed in 1983 appeared to be adequate.

This

matter is considered resolved.

b.

SBGT System Damper Operator -- Grease was noted on the electrical

connection for the limit switch housing on the operator for

ventilation damper MO 2/3-7505A.

The damper was the inlet

isolation damper for the "A" train of the SBGT system.

Because of

the location, the grease could have been coming from inside the

actuator limit switch housing.

Excessive grease in the limit

switch portion of the actuator housing could adversely affect

operation of the actuator. Licensee personnel agreed to remove

the limit switch housing cover during the next maintenance outage

for the SBGT system "A" train to determine the source of the

grease. Although the system engineer was aware of the grease, he

did not realize that grease might be inside the limit switch

housing and could adversely affect the actuator.

c.

RBCCW system -- The inspectors noted that the RBCCW system

included several valves that were missing nuts from packing

glands, pipe hangers disconnected or not supporting load, and

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d.

e.

several small pipes rubbing on other pipes or hard surfaces.

Although these problems were not individually significant,

collectively, they showed how vibrations resulting from the RBCCW

pump and line cavitations were affecting the system.

4KV Switchgear -- During a walkdown of some safety-related 4KV

switchgear areas, the inspectors noted that the majority of bolts

on the rear panels of safety-related switchgears 23-1 and 24-1

were missing or not secured: These panels cover the switchgear

bus bars and need to be securely closed to prevent any possible

personnel injury or bus grounding. Additionally, several breakers

had been removed from their respective cubicles and neither the

breakers or the cubicle openings were properly covered. Although

no requirement existed, covering the breakers and the openings

with the provided covers was considered to be a good maintenance

practice for prevention of personnel injury and dust and dirt

intrusion.

One breaker~ removed from the cubicle in the Unit 2 Turbine

Building 4KV Room, was found to be unrestrained. This was not in

accordance with Dresden Operating Procedure (DOP) 6500-04,

"Racking Out 4160 Volt Manually Operated Air Circuit Breaker,"

which required that *breakers removed from cubicles be restrained

to prevent rolling.

The failure to follow an approved station

procedure is an example of a violation of Criterion V of

10 CFR 50, Appendix B (237/94003-02A(DRS)).

Temporary Wooden Barriers -- During plant walkdowns, the

inspectors noted that temporary wooden structures had been erected

in front of safety-related motor control centers 28-1 and 39-1 to

serve as protective barriers during Unit 3 maintenance activities.

Discussions with licensee personnel indicated that the possible

impact of these barriers on plant operations had not been

evaluated.

When Unit 3 shut down for the outage, this ceased to

be a problem.

Licensee personnel were aware of the concern about

evaluations of unusual conditions during plant operations.

An example of one violation was identified in this area.

4.3

Engineering and Technical Support

Engineering and technical support at the Dresden Power Station was

provided by two separate organizations. Systems engineering support was

provided by the technical services organization and the site engineering

and construction (SEC) organization provided the support for design

changes and modifications.

The inspectors reviewed the engineering

support provided by both organizations.

4.3.1 Systems Engineering Support

Systems engineering support was provided by the plant technical staff.

  • Systems engineers provided oversight for the assigned systems; these

engineers focused on daily operations-and maintenance activities of the

assigned systems or system components.

The engineers aided plant

operations and maintenance personnel in resolving technical issues and

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problems and* were involved in complex maintenance evolutions in the

assigned systems.

They also coordinated potential design changes with

other engineering organizations.

While conducting facility tours, the inspectors noted several material

condition problems with the RBCCW system and 4KV Switchgear. These

conditions were very visible and should have been identified by system

engineers, backup system engineers, or supervisors while performing

system walkdowns in accordance with System Engineering Memo SEM-01,

System Engineering System Walkdown Guidance.

A review of several system

engineering walkdown check sheets indicated that system engineers made

routine walkdowns but apparently failed to conduct thorough system

walkdowns in accordance with the intent of management guidance.

The experience and qualifications of system engineers was mixed.

The

inspectors noted several system engineers with less than two years

experience.

The apparent inexperience of some of the system engineers

appeared to be a problem in some areas.

Licensee personnel were aware

of this condition and, during the past year, had developed a formal

training program for systems engineers.

Most engineers appeared to have a reasonable understanding of the

assigned system functions and attributes; however, some engineers did

not always appear to be knowledgeable of the assigned systems and system

related problems. Adequate involvement of system engineers in plant

support activities was not always evident.

S9me system engineers did

not appear to be involved and some were less than aggressive in their

approach to involvement in activities relating to the assigned systems.

This was demonstrated by less than thorough system walkdowns and a lack

of *involvement of system engineers in the resolution of inspection

concerns. Repeated requests had to be made to get system engineering

involvement in NRC concerns during the inspection.

Based on the inspection results, the inspectors concluded that the

technical support for station activities, provided by systems

engineering, was adequate.

Even though systems engineers had been

relieved of direct responsibility and involvement in design changes,

very little improvement was noted in the System Engineering Organization

-since the E/TS inspection conducted a year ago.

4.3.2 Site Engineering and Construction

The site engineering and construction (SEC) organization had the primary

responsibility for coordination, evaluation, development, and

installation of design changes and modifications. This organization was

divided into four groups which included engineers with mechanical,

electrical and other engineerfng specialties. The primary purpose of

SEC was to develop and coordinate plant modifications, including design,

safety reviews, installation, and post modification testing in the

respective discipline.

Each modification was assigned to an engineer

actively involved in all phases of the modification. The engineers

completed walkdowns, as necessary, to ensure proper design

implementation and resolution of installation problems.

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Communications and coordination between site engineering and other plant

organizations such as systems engineers, plant management, operations,

maintenance, construction, and other plant personnel was effective.

Based on the inspection results, the inspectors concluded that, in most

cases, the SEC engineers were experienced and qualified. A substantial

improvement was evident. Most engineers appeared knowledgeable of the

assigned areas and appeared well motivated in their areas of

responsibility. The level, quality, and timeliness of engineering and

support in this area appeared to be good with a few exceptions. A

discussion of the exceptions follows.

4.3.2.1 Review of Modification Packages and Records

The inspectors reviewed selected portions of both open and closed

modification packages and supporting records, with emphasis on the

selected systems.

The records were reviewed to verify the packages were

complete and accurate, the modifications were adequately controlled, and

regulatory requirements were met.

The review included verification that

the description of the modification, the 10 CFR 50.59 safety screening

or evaluation, installation instructions, documentation of work

performed, post-modification testing requirements and test records were

adequate.

In some cases, other supporting records associated with the

modifications, such* as calculations and drawings, were selected and

reviewed to verify the adequacy and accuracy of the engineering process.

The 26 modification packages reviewed were:

Ml2-0-91-019F

Ml2-2-91-020

Ml2-2-91-022

Ml2-3-89-004

Ml2-3-91-022

Pl2-2-90-718

Pl2-3-91-731

Ml2-2-84-119

Ml2-2-90-028

Ml2-2-93-004

Ml2-3-90-013A

Ml2-3-93-004

Pl2-2-91-660

Pl2-3-92-612.

Ml2-2-88-60

Ml2-2-90-029

Ml2-3-84-119

Ml2-3-91-020

Pl2-2-90-710

Pl2-3-91-729

Problems or concerns noted during the review were:

Ml2-2-89-004

Ml2-2-91-021

Ml2-3-88-60

Ml2-3-91-021

Pl2-2-90-713

Pl2-3-91-730

a.

Ml2-2-90-029 ~- This modification installed the hardened wetwell

vent required by Generic Letter 89-16.

Problems with this

modification are discussed in Section 4.1.1.2 of this report.

b.

Ml2-2{3l-84-119 -- These modifications installed changes to the

SBLC system to comply with the ATWS rule.

Problems with this

modification are discussed in Section 4.1.2 of this report.

c.

Ml2-3-90-13A -- This partial modification (including Addendum 1

and 2) was required to add an alternate 125V DC battery system,

including a battery charger, a battery and connecting cables, to

the Unit 3 safety-related DC control system. This would allow the

normal battery system to be removed from service for required

testing without having to enter into a duel unit LCO. This partial

modification was completed in January of 1993.

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The inspectors noted that control room drawing 12E-2322B,

"Overall key Diagram, 125V DC Distribution Centers, Dresden

Nuclear Power Station Units 2 & 3," Revision C, dated July 3,

1991, had not been marked or revised to show the Unit 3 alternate

battery, battery charger or cabling additions, however, the

diagram did show the similar additions which had been made for the

Unit 2 modification.

Procedure DAP 02-09, "Control of Critical Drawings," required that

control room drawings be revised or updated to reflect the correct

plant configuration. The failure to implement the requirements of

this procedure and update the control room drawing with this

design change is considered an example of a violation of

Criterion V of 10 CFR 50, Appendix B (249/94003-02B(DRS)).

  • Most of the modification packages and supporting records appeared to be

adequate.

With the exception of the noted deficiencies, records

indicated that modifications were adequately controlled and were

consistent with regulatory requirements.

The inspectors concluded that

th~ modification process was effective.

An example of one violation was identified in this area.

4.3.2.2 Review of Exempt Change Program

An Exempt Change (EC) Program had recently been developed to expedite

the review and approval of modifications of minor significance and with

low potential to significantly reduce the margin of nuclear safety.

This process replaced the former minor change process which was no

longer used.

These minor modifications were called "Exempt Changes" and

were process modifications which were exempt from the specific

requirements of the modification and minor plant change processes.

The inspectors concluded that the EC process provided a viable and

effective method to control minor modifications of low significance.

The records reviewed indicated that exempt changes were adequately

controlled, were consistent with regulatory requirements and the process

was effective.

4.3.2.3 Temporary Alterations

The inspectors reviewed the methods used to control temporary

alterations (TAs).

The methods were described in procedure DAP 07-04,

"Control of Temporary System Alterations," Revision 17.

The procedure

appeared to be inadequate in some areas. For example, a one time

justification was required for TAs to be installed more than 90 days.

Periodic review and justification for continued installation was not

required.

The Dresden Temporary Alteration Report, dated March 31, 1994, was

reviewed.

The report listed 48 open TAs, which was more than twice the

recently established goal of less than 20 open TAs.

The TA procedure

defined a TA to be an alteration expected to be installed for less than

six months.

Thirty of the TAs listed in the report had been open

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greater than six months and 10 had been open longer than two years.

This appeared to be a misapplication of the TA procedure.

Li c.ensee personnel stated that some recent changes had been made to

improve control and reduce the number of TAs.

A report of open TAs was

issued to management and the individuals assigned open TAs monthly.

Although some steps, such as the establishment of goals to reduce open

TAs, have been taken, management emphasis and action is needed to ensure

that appropriate action is taken and that thorough and adequate control

is provided for TAs.

Significant systems engineering involvement

appeared to be needed to eliminate and prevent the installation of

unneeded TAs.

Based on the review of the TA process and selected TA packages, the

inspectors considered the methods used to control TAs to be weak.

Problems were noted with five of the seven TA packages reviewed and the

number of TAs had increased approximately twenty percent in the last

year. Several problems involving both safety and non-safety-related

hardware were noted in this area. A discussion of these problems

follow.

4.3.2.3.1 Review of Temporary Alteration Records

The inspectors reviewed seven TA packages to verify proper control.

Problems or concerns were noted with five of the seven TAs.

The

packages reviewed and the results follow:

a.

TA II-33-93 -- This TA allowed the injection of "Furmanite" to

repair a leak in the valve packing area of valve 2-220-l02 in the

Unit 2 reactor recirculation system.

Installation of the TA was

completed May 27, 1993.

A hole was drilled into the valve yoke and sealant was injected

into the packing area to eliminate or reduce the leak.

The

engineering evaluation, performed at the time of installation,

failed to consider potential over pressurization of the valve due

to the sealant injection process.

Licensee personnel estimated

that the worst case injection pressure applied to the valve could

have been as high as 4700 psig which was considerably higher than

the valve's rated pressure of 3600 psig.

NRR is currently

reviewing control of the Furmanite process throughout the

industry.

The inspectors also noted that the valve affected by the TA formed

part of the reactor coolant pressure boundary, which was addressed

by Section 3.6 of the Technical Specifications. The screening

evaluation, included in the package, incorrectly concluded that no

safety evaluation was required.

During this inspection, an operability assessment for the valve

was performed and documented.

In addition, a safety evaluation as

required by 10 CFR 50.59 was performed.

The inspectors did not

identify any concerns regarding the operability evaluation and the

safety evaluation. Prior to this inspection, SEC personnel

recognized that oversight weaknesses existed with the sealant

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b.

injection process as early as May, 1993.

However, formal tracking

of plans to develop a controlling document was not initiated until

February, 1994.

The emphasis for such tracking was largely due to

problems experienced with TA II-1-94 (feedwater pump suction valve

sealant injection repair); Information Notice (IN) 93-90,

"Unisolatable Reactor Coolant System Leak following Repeated

Applications of Leak Sealant;" and an industry notification

concerning sealant injections.

TA II-34-93 -- This TA disabled the Reactor Feed Pump (RFP) motor

cooling fan intake and exhaust damper controls to keep the dampers

in the fully opened position.

Installation of the TA was

completed June 11, 1993.

The TA was installed to ensure adequate cooling of the RFP motor

during the summer, since there had been problems with the

temperature control system.

The motor was cooled by continued

circulation of outside air through the ventilation ductwork with

all dampers fully open. This TA was left installed through the

winter with no evaluation of the possible adverse effect of over

cooling the motor.

With the dampers fully open, extremely cold

air from outside could be blown into the RFP motor by the

continuously running cooling fans.

During the inspection, the

systems engineer reviewed the computer point history data for the

RFP stator winding and noted that the lowest temperature was above

ambient.

The warm air that prevented the over cooling was

determined to be coming from the full open recirculation damper,

In addition, there was a lack of documentation of the problems

that required the TA.

Records only indicated that the exhaust

damper was broken.

Discussions with the responsible systems

engineer indicated that none of the dampers in the RFP motor

cooling system, including supply air damper, exhaust air damper,

and recirculating damper were found in their expected positions,

Some internal linkage slippage had also been identified. However,

there were no indications that action had been taken to correct

these problems to restore the temperature control system to proper

operations.

The control of this TA was inadequate. The system was allowed to

operate during the winter in an un-evaluated condition and the

corrective action to restore the temperature control system to

acceptable operations was not timely. This matter was discussed

with licensee personnel.

c.

TA II-60-93 -- This TA allowed the installation of inlet and

outlet pressure gauges on a refrigeration control unit heat

exchanger for control room heating, ventilation, and air

conditioning equipment.

Installation of the TA was completed in

December, 1993.

No problems or concerns were identified with this

TA.

d.

TA II-1-94 -- This TA allowed the installation of a "Furmanite"

clamp on the 2A RFP suction valve bonnet to body flange to stop or

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reduce*water leakage to an acceptable level. Installation of the

TA was completed January 11, 1994.

After the "Furmanite" clamp installation and sealant injection,

water leakage returned to the previous leakage rate in less than

one day.

The failure of the TA appeared to be improper control of

the "Furmanite" process.

The curing temperature for the sealant

compound not being specified in the work procedure and was not

monitored during "Furmanite"-injection.

Engineering Department

Technical Information Document TID-MS-06, "Injection Leak Seal~nt

Application General Use," December 30, 1991, did not require

monitoring of curing temperature during injection.

The work package required that a responsible engineer from SEC be

present when sealant compound was injected into the "Furmanite"

clamp.

This item was assigned to the mechanical maintenance

department and SEC was not involved in the work.

These concerns

were discussed with cognizant licensee personnel.

e.

TA III-21-92 -- Eight thermocouples, two pressure transducers, two

flow transducers, and one axial shaft displacement probe were

installed, under this TA, to monitor system parameters and to

assist in the determination of causes for RFP seal failures.

Installation of the TA was completed June 29, 1992.

f.

g.

In reviewing the package, the inspectors noted that there were no

design documents to identify the location. of the instruments, the

hardware to be used, the hardware accuracy and the functional test

requirements.

In 1988, the RFP supplier recommended changing to another type

seal. The recommended seals were purchased and installed in all

Unit 2 RFPs in late 1992.

No Unit 2 RFP seal failures had been

reported since. The inspectors concluded that the TA was not

adequately engineered and that the change appeared to have little

or no actual value since the change in the type of seal had

apparently solved the problem.

These concerns were discussed with licensee personnel.

TA Ill-22-92 -- This TA was implemented to bypass a switchboard

mounted fuse holder which included a solid copper link rather than

an actual fuse.

Installation of the TA was completed July 2,

1992.

No problems or concerns were identified with this TA.

TA 111-40-92 -- This TA involved the existing 7-second time delay

feature of the degraded grid voltage protection scheme for the

Unit 3 safety-related 4.16KV bus 33-1.

Installation of the TA was

completed October 30, 1992.

On March 10, 1994, the inspectors reviewed the control room copy

of the drawing 12-3345, Sheet 2, "Schematic Control Diagram, 4160V

Bus 33-1, 4KV Swgr. Bus 40 Feed Bkr., Unit 3," Revision AF, dated

March 9, 1993, titled and noted that the markings on the drawing

did not agree with the TA.

The markings indicated that the relay

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time delay was 2-seconds rather than the required 7-seconds. The

replaced relay was still indicated as an instantaneous relay,

rather than the installed time delay relay, as called for in the

TA documentation.

Procedure OAP 02-09, "Control of Critical Drawings," required that

control room drawings be revised or updated to reflect the correct

plant configuration.

The failure to implement the requirements of

this procedure and correctly- update the control room drawing with

the plant configuration for this temporary alteration is

considered an example of a violation of Criterion V of 10 CFR 50, Appendix B (249/94003-02C(DRS)).

Examples of two violations were identified in this area.

4.3.2.4 Review of Safety Evaluations and Screenings

The inspectors reviewed the methods used to perform 10 CFR 50.59 safety

screenings and evaluations. Records of the screenings and evaluations

were reviewed for the selected modification, exempt change and temporary

alteration (TA) packages to verify completeness, accuracy, and

compliance with regulatory requirements.

Procedure OAP 10-02, "10CFR50.59 Review Screenings and Safety

Evaluations," Revision 8, was reviewed and found to be well written and

concise. Several minor weaknesses were noted and discussed with

licensee personnel for possible procedural improvements.

Licensee

personnel acknowledged these weaknesses and indicated that the procedure

would be revised.

During the review of modifications M12-2(3)-93-004, the inspectors noted

that an unreviewed safety question was identified during the original

10 CFR 50.59 safety evaluation performed for the modifications.

Due to

discussions with the Office of Nuclear Reactor Regulation regarding the

issue, the modification was subsequently redesigned to eliminate the

unreviewed safety question.

As a result of the identification of this

problem, Information Notice 93-89, "Potential Problems with BWR Level

Instrumentation Backfill Modifications," was issued. The inspectors

considered the identification and resolution of this issue to be a

positive application of the 10 CFR 50.59 safety evaluation process.

Safety evaluations or screenings were usually performed and were

acceptable.

The modification and TA packages reviewed contained the

required 10 CFR 50.59 safety screenings or evaluations and they appeared

to be well documented.

Some of the packages contained additional

supporting information.

Procedure OAP 10-02, if properly implemented,

provided sufficient controls to ensure that proper 10 CFR 50.59

screenings and safety evaluations were performed and documented as

required.

Based on the review of records and subsequent discussions

with licensee personnel, the inspectors concluded that the safety

screenings and evaluations were acceptable.

4.3.2.5 Review of Calculations

In order to complete the assessment of the design change and

modification process, the inspectors reviewed portions of selected

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calculations that were performed or revised to support the selected

modifications. Calculations were reviewed for completeness, accuracy,

validity of assumptions, and conservatism with emphasis on how well the

calculations supported the respective modification.

Some of the

calculations were performed by licensee personnel while others were

performed by contractors.

Based on the review of calculations, the inspectors concluded that,

overall, calculations were acceptable. Several calculation errors were

noted. Although most of the indivi~ual problems in this area were not

considered to have a significant effect on equipment function,

improvement was needed in this area. This matter was discussed with

licensee personnel.

The following concerns were noted during the review of calculations:

a.

Calculation 8982-19-19-2, "Calculation for Contactor/Interposing

Relay Coil Voltage at Pickup,"

Revision 1, dated December 22,

1992 -- Revision 0 of this calculation identified the marginally

acceptable conditions for the contactor coils associated with the

modifications Pl2-3-92-611, 612, 613 and 614.

However, the

results and conclusions of this calculation, including.Revision 1,

indic~ted that the minimum pickup voltage acceptance criteria was

not met by six circuits. These control circuits were identified

as those for the following motor loads:

HPCI auxiliary coolant pump,

HPCI pump area cooling unit,

reactor protection system MG set 3B,

reactor building cooler recirc pump,

motor operated valve 202-4A and

motor operated valve 202-48.

Licensee personnel indicated that these six circuits had been

analyzed and the conditions had been resolved or justified.

Documentation could not be located to support this response.

Licensee personnel advised that they would continue to search for

the documentation and, if the records could not be found the

conditions would be reanalyzed and new documentation prepared.

The inspectors considered this to be an inspection follow up item

pending NRC review of the documentation and resolutions

(249/94003-03(DRS)).

b.

Calculation XCE065.0200.001, "Determination of Required Hardened

Wetwell Vent Flow Rate and Vent Pipe Size," Revision 0, dated

July 19, 1991 -- Details of this calculation were discussed in

Section 4.1.1.2 of this report.

c.

Piping stress analysis for the LPCI p1p1ng system -- During a

visit to a CECo design contractor on March 16, 1994, the

inspectors noted that only one uniformly hot temperature was used

in the original piping analysis for the HPCI system.

The

inspectors counted five different temperature combinations.

Since, in some cases, thermal loads were dominating loads,

licensee personnel agreed to re-run the piping stress analysis for

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the LPCI piping system in a simplified manner.

The review focus

was placed on the heat exchanger 28-1503 outlet nozzle.

This heat

exchanger had the largest design loading imposed on the over-

stressed structural wide flange in Unit 2 southwest corner room.

The piping stress analysis showed significantly higher loadings in

some directions. This raised a question on the validity of some

of the earlier piping stress analysis.

Licensee personnel also agreed to re-run the seismic and dead

weight analyses and to perform a technical audit on the previous

piping stress analysis. This matter is unresolved pending review

of the stress analysis and audit {237/249/94003-04}.

4.4

Errors in the Updated Final Safety Analysis Report

During the inspection the inspectors noted several errors in the

recently rebaselined Updated Final Safety Analysis Report {UFSAR}.

These errors were:

a.

b.

On page 2.4-2, the statement is made that the Probable Maximum

Flood {PMF} level is 528'- 0".

Table 2.4-1 states that the

maximum flood is 508'-0".

Licensee personnel determined that the

correct PMF level was 528'- O", which is higher than the plant

ground elevation of 517' - 0".

The inspectors reviewed procedure

DOA 0010-04, "Floods," and noted that the procedure addressed this

type flood.

Several questions were raised and licensee personnel

issued a PIF to ensure that the issue was adequately addressed.

On page 6.2-4, the description of the primary containment airlock

was not correct.

c.

On page 6.2-17, the pressure in the suppression chamber was

described as 29 psia from an initial pressure of 0.5 psia. These

terms should have been psig.

d.

Table 6.5-2 of the UFSAR used incorrect units to reflect pressure

drops in standby gas treatment system. Specifically, "ft H20"

rather than "in H20" was used.

The multiple errors in the UPSAR indicated that the checking and review

of changes was inadequate to assure that the document was correct.

Licensee personnel indicated that the noted errors would be corrected.

5.0

Self-assessment of Engineering Activities

Self-assessment of engineering activities at the Dresden Station

consisted of audits and a special assessment of some engineering

activities.

In addition, some assessment of engineering activities was

accomplished by cause investigation and correction when problems

occurred. Overall, the various assessments covered the spectrum of

engineering support activities.

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5.1.

Sit~ Quality Verification Audits

5.2

The inspectors reviewed recent Site Quality Verification {SQV) audit and

special assessment records and interviewed personnel to determine the

effectiveness of the self-assessment of engineering activities. Audits

of the engineering group were normally conducted yearly with additional

audits of supplemental engineering activities conducted as needed.

Records of three SQV audits of engineering or engineering related

activities were reviewed and found to be adequate.

The SQV audit records indicated that the scope of the audits performed

was adequate to cover engineering activities. Findings and

recommendations noted appeared to be appropriate. The audits were not

always effective in finding engineering weaknesses.

For example, the

problem with the misuse of temporary alterations, noted during the

inspection, was not identified during these audits.

Corrective Actions Records {CARs) were issued for audit findings and

were incorporated into the NTS program.

CARs were also tracked by a

redundant SQV tracking system.

During one of the audits, SQV identified

problems in documenting TAs on control room drawings; however, actions

taken to correct the problem were not thorough.

As part of the response

to .CAR 12-9.3-034, a review of all open TAs was performed to ensure that

control room drawings properly reflected the TAs.

The inspectors

identified a TA which was not properly reflected on the applicable

control room drawings. This issue is discussed in Section 4.3.2.3.1 g.

of this report.

The inspectors considered the audits to be adequate.

Identification of

engineering weaknesses and follow up to ensure effective action was

taken on findings did not always happen.

No other concerns were

identified in this area.

Special Assessments of Engineering

Corporate SQV was primarily responsible for special assessments of

engineering.

No overall assessments of engineering had been performed

by this group in the last two years.

In response to continued problems associated with the maintenance of

drawings, however, SEC management used an outside consultant, Failure

Prevention, Incorporated, to study the problem.

The consultants'

report, "Organizational & Programmatic Assessment of the Critical

Drawing/Design Change Interface at the Dresden Nuclear Station," dated

December 1993, made several recommendations and provided useful insight.

As ~ result of the study, the changeover from manual to electronic

storage of critical drawings was accelerated, and organizational changes

were made to ensure qualified personnel updated critical drawings.

The

inspectors considered SEC management's use of an outside consultant to

study process and organizational problems a positive imitative.

5.3

Trending and Corrective Action

The inspectors reviewed the methods used by engineering to trend

equipment problems, investigate problems for cause, and provide adequate

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corrective action to correct both the identified problem and the cause.

Significant problems or failures were documented on PIFs, which were

used as a mechanism for investigation to determine root causes and

initiate actions to prevent recurrence. Trending and corrective action

are discussed separately in the following sections.

5.3.l Trending

  • The inspectors reviewed the methods used to track problems, detect

repetitive equipment failures and trend hardware and other quality

related problems. A tracking system had been developed to track~ sort

and allow oversight of equipment failures and other potential problems.

The tracking system used a matrix to collect and sort information into

functional groups. Because of past problems with inadequate trending,

an oversight of this system was provided by the root cause committee.

The systems engineers were responsible for monitoring failure

information to detect repetitive hardware failures and problem trends in

the assigned systems or system related components.

A significant

problem had recently occurred in this area. Repetitive failures of the

reactor coolant level instrumentation had not been detected and

corrective action had not been taken, even though many failures had been

documented.

Because of this instrumentation issue, licensee management

had provided additional emphasis on trending of significant hardware

failures, however, it was too early to evaluate the results of this

action.

Another trending method used was the Component Failure Analysis Report,

which utilized information from the nuclear plant reliability data

system.

This system allowed a review of industry failure and trending

information on selected plant components.

Discussions with licensee

personnel indicated that, if failure rates were above the industry

average for the specified components, the issues were referred to the

appropriate system engineers for investigation and possible action.

The inspectors concluded that, although an acceptable trending program

appeared to be in place, additional management attention was needed to

ensure adequate implementation.

Some actions had been taken in this

area, however, the results could not be determined at this time.

5.3.2 Corrective Action

The inspectors reviewed the methods used for root cause investigation

and corrective action for hardware and other quality related problems.

Significant problems or failures, which required a review for cause of

failure, were documented on PIFs to track the problems for cause

investigations and resolutions. Systems engineers were normally

assigned follow up action for PIFs written on their assigned systems.

In order to improve the correction system, the threshold level for

writing PIFs had been reduced.

In addition, a root cause committee had

been developed. This committee met each workday to discuss items

requiring root cause investigation and possible corrective action. The

inspectors attended several of these daily meetings and concluded that

the use of the root cause committee was an effective method for

implementing the root cause program.

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Based on the review of the corrective action program, the review of

selected PIFs, attendance at several root cause committee meetings and

discussions with licensee personnel, the inspectors concluded that

actions taken to improve root cause investigations and corrective

actions had been effective and that the corrective action program was

acceptable.

In most cases, PIFs were written, properly processed,

evaluated for cause and the actions taken were appropriate and timely.

Improvements in the corrective action program were evident.

5.3.2.1 Nuclear Tracking System

The Nuclear Tracking System (NTS) was the method used for tracking

commitments, discrepancies, and material deficiencies. The system

database was managed by the Regulatory Assurance Group and each item was

assigned to a cognizant supervisor and individual. The system appeared

to be dynamic in nature with growing acceptance and usage.

The inspectors noted that the number of items receiving extensions and

the new items written exceeded the number of items closed for both

engineering groups for the past four months.

This trend had resulted in

an increasing backlog of open items assigned to the engineering staff.

Significant attention had been placed on the closure of items to ensure

that overdue items were promptly addressed and, as a result, the daily

NTS reports had very few items that were listed as overdue.

At the time

of the inspection, the increasing backlog did not appear to be a

problem, however, unless the trend is reversed, future difficulties will

be encountered.

Licensee personnel stated that extensions to scheduled

du~ dates now require approval of the responsible supervisor.

During discussions with licensee personnel, several individuals

commented that all open items had the same importance and the priority

was driven by the scheduled closure date, rather than safety or

operational significance. This was discussed with engineering

management who agreed that there was no formal prioritization of items

once the items were placed in the system.

Licensee personnel stated

that it was the responsibility of the supervisors to manage individual

workloads and, through that function, set priorities of assigned items.

A review of many open items found no evidence of significant items being

ignored or delayed due to work on less significant items.

5.3.2.2 Review and Evaluation of NRC and Industry Information

The inspectors evaluated the effectiveness of the methods used for

review and evaluation of NRC and industry information. This review

included the methods used to assure that vendor, industry, and NRC

generic information was controlled, distributed, and evaluated and that

corrective actions were taken as appropriate.

The Regulatory Assurance Department had the overall responsibility for

coordination of review and evaluation of this information.

Upon the

receipt of a notice or other information an initial screening for

applicability was performed.

Distribution to the responsible organization for impact evaluation and

determination of possible required action was coordinated with corporate

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engineering.. Assigned departments were required to provide a response

to Regulatory Assurance, noting any plant impact, with recommendations

for action if needed.

All of the applicable NRC and industry

information was tracked by Regulatory Assurance until the issues were

closed. Regulatory Assurance was also responsible for assembly of the

response package and preparation of the cover letter if a response was

required.

In order to determine the effectiveness of this system, the inspectors

selected the methods for handling supplier service information letters

(Slls} and NRC information notices (IN) for review.

These reviews are

discussed below:

a.

Service Information Letters -- The inspectors reviewed the methods

used for the dissemination and response to vendor SILs.

Several

SILs were reviewed and were found to be adequately tracked and

addressed by the technical staff. The individual responsible for

the SILs was knowledge of the current status of the SILs selected

and readily retrieved documentation for review.

b.

Information Notices -- Problems had been previously identified

with the program for controlling information notices. A review of

the program indicated that these problems still existed, however,

because the corrective actions for these issues were still

pending, no further assessment in this area was completed.

The licensee's lessons learned program, which provided interface and

communication on problems at other CECo plants, appeared to be working

effectively.

For example, the inspectors noted that Dresden systems

engineering was aware of and was tracking an incident that happened at

Quad Cities where a reactor recirculation pump inadvertently went to

fast speed while the unit was shutdown causing severe vibration and

possible damage.

Although the evaluation was ongoing, the systems

engineer appeared knowledgeable of the problem, actions taken and the

status.

Unresolved Items

Unresolved items are* matters* about which more information is required in

order to ascertain whether they are acceptable items, violations or

deviations.

An unresolved item noted during the inspection is discussed

in Section 4.3.2.5 c. of this report.

7.0

Inspection Follow-up Items

Inspection follow up items are matters which have been discussed with

licensee personnel, which will be reviewed further by the inspector, and

which involve some action on the part of the NRC or the licensee or

both.

An inspection follow up item, noted during the inspection, is

discussed in Section 4.3.2.5 a. of this report.

8.0

Exit Meeting

The inspectors met at the Dresden Nuclear Power Station with licensee

representatives {denoted in Section 1) on April 5, 1994, to summarize

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the purposer scope, and findings of the inspection. The inspectors

discussed the likely informational content of the inspection report with

regard to documents or processes reviewed by the inspectors during the

inspection, noting that three documents were identified as proprietary

during the inspection. Details of these documents are not discussed in

this report.

Licensee personnel were asked to identify any proprietary

information or material discussed during the exit meeting.

Licensee

personnel did not identify any information or material as proprietary.

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