ML17157A803

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Insp Repts 50-387/91-06 & 50-388/91-06 on 910506-10. Violations Noted.Major Areas Inspected:Design,Design Changes,Mods,Bypass Control,Engineering/Technical Support Followup to Identified Deficiencies & Inservice Testing
ML17157A803
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 07/24/1991
From: Eapen P, James Trapp
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17157A801 List:
References
50-387-91-06, 50-387-91-6, 50-388-91-06, 50-388-91-6, NUDOCS 9108260009
Download: ML17157A803 (9)


See also: IR 05000387/1991006

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Report Nos.

0- 87/ 1-06

nd

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Licensee:

enn

lvania P w r

nd Li ht

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Allentown Penns

lvani

1

101

Facility Name:

us uehanna

earn Electric

i n

I

Inspection At:

Salem Townshi

Penns

Ivania

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Inspector:

J. M. T

p, Sr. React r Engineer

System Sections

Engineering Branch, DRS

date

Approved by:

Dr. P. K. Eapen, Chi f

Systems Section, DRS

Ins ection Summa:

Routine Unannounced Inspection on May 6-10, 1991.

Inspection Report Nos. 50-387/91-06 and 50-388/91-06.

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bypass control.

Also included in the scope was engineering/technical

support follow-up to

identified deficiencies and a review of inservice testing.

The control of design changes

is

important to assure that modified systems continue to be capable of performing their intended

safety function after the design changes are implemented.

~Re uit: in general, the modifications reviewed were technically sound.

Piant modification

had been thoroughly "closed out" prior to the system being declared operable.

The Inservice Test /ST) results reviewed were acceptable, well organized and trended.

However, a check valve in the containment instrument gas system "Q" boundary, was not

910826000tyt

910813

PDR

ADOCH, 05000387

O

PDR

included in the IST program.

Consequently this valve was not tested in accordance with

ASME BEcPV Code,Section XI as discussed in Section 4.0.

This inspection found that Engineering/Technical Support follow-up for the deficiencies

reviewed, was thorough.

However, one weakness

was identified in the timeliness of repairs

being made to the Radiation Monitoring System as discussed in Section 3.0.

DETAIL/

1.0

De i n

h n es

nd M

ificati n

Review

(NRC IM 37700)

The objective of reviewing design changes (DCP's) was to ascertain that changes

to

the station's safety systems as described in the Safety Analysis Report were made in

accordance with regulatory requirements,

Technical Specifications, Station Procedures,

and the licensee's Quality Assurance Program.

This objective was accomplished by

performing a detailed review of the following modifications:

l.

88-3032,

"RHRSW Modification-Isolation Valves for RHR Heat Exchangers."

2.

88-3050A,

"Replacement of RHR Pump Room Cooling Coils 2E230 A/C."

3.

89-3030,

"ESW Loop "B" Supply and Return Piping Modification-

Reactor Building Cooling Coils."

These design change packages

(DCPs) were detailed and technically sound.

In

general, the DCPs reviewed incorporated requirements and standards

commensurate

with the safety significance of the design change involved.

The thoroughness of the

DCPs was also evident by the limited number of changes (PCNs) that were made to

the DCPs during installation.

The inspector observed:

~

All design packages were adequately reviewed and approved by the plant

operations review committee prior to release for installation.

~

Post modification testing was performed in accordance'with previously

established

acceptance criteria and the test acceptance criteria were met during

post modification testing.

~

Control room drawings had been modified in accordance with station

procedures prior to declaring the modified system operable.

~

Training of licensed operators on the modified plant systems was conducted

prior to declaring the modified system operable.

~

Station procedures were updated prior to declaring the modified system

operable.

~

ISI and IST Programs were revised to reflect changes in the system design.

However, a formal process for assuring design changes are reflected in the IST

program was not included in modification close out procedures.

One of the modifications reviewed, DCP 88-3032, incorporated the changes

to

facilitate a temporary fire water connection to the RHR service water system in the

event of a station blackout.

This was a licensee initiative to enhance the performance

of installed safety systems.

The systems engineers'ctive

involvement in the modification process was perceived

as an additional licensee strength.

The system engineers provide a focal point for the

modifications from inception.

The system engineers interviewed exhibited detailed

knowledge of the modifications performed on their assigned

systems and the overall

modification process.

Design kickoffand installation kickoffmeetings were observed

to be useful efforts to enhance cooperation and communication between responsible

groups.

The system engineers performed an effective modification close-out process.

One deficiency was identified in the establishment of testing criteria for modification

88-3032,

The RHR service water system is a ASME, Class 3 system.

ASME B&PV

Code,Section XI, Article IWD-5210 (b), states in part that "The contained fluid in

the system shall serve as the pressurizing medium."

PPAL Specification M-1040,

states in section 3.8.1.3 (a), pneumatic pressure

test requirements for Class 3 systems,

that Class 3 water systems must be pressure

tested only by means of water.

For the

RHR service water system the pressurizing medium is water.

A one time exception

was approved by engineering to perform a pneumatic pressure test in lieu of a

hydrostatic test for the "hot-tapped,"3" drain connections.

The failure to perform a

hydrostatic test is not a plant safety issue because the pneumatic test conducted was

comparable to a hydrostatic test in detecting leakage.

However, the engineering

assessment

which allowed the pneumatic test was not thorough because it did not

consider ASME BkPV Code requirements to hydrostatic test these welds.

The licensee's quality assurance

audit group recently completed an audit of the plant

modification system (Audit Report 91-024).

This was a three week audit by a team of

four auditors.

The audit report concluded that the plant modifications program

remains effective and satisfactorily implemented.

No significant technical or design

issues were identified.

The audit report was reviewed and it was found to be an

effective assessment

of the plant modification program.

2.0

Electric

1 and Mechanical B

s

Control (NRC IM 37700)

The inspector reviewed the temporary modifications (bypasses)

to assure that such

modifications were completed in accordance with NRC requirements.

Electrical and

Mechanical Bypass Control procedure AD-QA-484, Rev. 3, was reviewed to verify

that administrative controls for bypass control were adequate.

In addition, the

following two bypasses

were selected to verify that the licensee was implementing

these bypasses

in accordance with the bypass control procedure.

~

2-91-022, "Temporary 250VDC Battery"

~

2-89-005, "Temporary Pressure Transmitter on HPCI"

The following observations were made during the review of the two bypasses

listed

above:

~

The bypasses

were reviewed and approved in accordance with the bypass

control procedure.

The bypasses

were installed in accordance with the installation package.

The records for the installation of bypasses

were complete.

Periodic reviews of the bypasses

were being performed in accordance with the

administrative procedures.

The total number of active bypasses for both units was less than twenty at the time of

this inspection.

This is a reduction from over one hundred bypasses

installed one year

ago.

This reduction of the active bypasses

indicates a strong management involvement

in the control and close-out of bypasses.

The reduction of active bypasses

required a

large engineering effort to transform the long standing bypasses into permanent station

modifications.

This effort provided additional reviews and incorporation of the

modification into plant design documentation.

A review of AD-QA-484, Rev. 3, "Electrical and Mechanical Bypass Control," found

that certain bypasses

are not reviewed by PORC.

To satisfy section 6.5.1,6 of the

technical specifications which requires PORC be responsible for review of all

proposed changes or modifications to unit systems or equipment that affect nuclear

safety, the bypasses

are screened by the technical section.

The screening criteria are

as follows:

Ifthe bypass constitutes a change to the facility or procedures

as described in

the FSAR or it is a test or experiment not described in the FSAR, then a safety

evaluation is written and PORC review is required prior to installation.

Ifthe bypass does not meet the above screening criteria, it may be installed

after approval by a technical supervisor and this bypass does not require PORC

review.

The inspector noted that the above screening criteria were established in a revision of

AD-QA-484. The previous revision of AD-QA-484 screening criteria did not provide

similar guidelines for the PORC review of bypasses.

The inspector observed that a

small number of the older installed bypasses

were not screened for review by PORC

using the present screening criteria.

The inspector discussed

this matter with the

licensee's

representatives.

The licensee stated at the exit meeting that the installed old

bypasses

would be screened

using the latest edition of AD-QA-484 and corrective

actions would be taken, ifneeded.

The inspector found this action to be acceptable.

3.0

En ineerin

rr

tive Action Foll w-u

Two licensee identified deficiencies were reviewed by the inspector to assure that

engineering/technical

resolutions

to deficiencies were performed in a thorough and

timely manner.

The Unit 2 automatic depressurization

system was declared inoperable when the

containment instrument gas header pressure dropped below 135 psig due to a pressure

relief valve (PRV) lifting. Licensee Event Report LER 90-003 was written for the

event which occurred on February 28, 1990.

The LER was updated by the licensee

on June 29, 1990.

The licensee performed bench testing of the PRV on

April 23, 1990; but could not positively identify the root cause for the PRV opening

and failing to reseat.

The internals of the valve were replaced and the valve was re-

installed.

As a long term corrective action the licensee stated that a PRV designed

specifically for gas applications would be installed.

The licensee has completed the

installation of the improved PRV for Unit 2 and is scheduled to install a similar valve

in Unit 1 during the 1992 refueling outage.

The inspector found that the technical

support provided to correct these deficiencies was thorough and timely.

The second licensee identified deficiency reviewed related to the corrective actions

taken to enhance the vent stack radiation monitoring system (SPING).

This radiation

monitoring system experienced

a high rate of failure.

The failure of the SPING places

the plant in a Technical Specification Limiting Condition of Operation (LCO).

Problems with the.SPING were first identified by the licensee in 1983.

An NRC

unresolved item regarding this issue was opened in 1985.

An update of the NRC

unresolved item was provided in NRC Inspection Report 50-387/90-20, at which time

the schedule to start installation of the phase

1 of the SPING upgrade project was

given as December

1990.

At the time of this inspection, the date for phase

1

installation had been delayed until September of 1991.

The engineering which has

gone into the phase

1 effort appears to be extensive and addresses

the problems

presently experienced by the SPING.

However, the delays encountered

in the attempt

to install this modification indicate a potential weakness in the engineering process.

7

Inservice Te t Pr

ram (NRC IM 73756)

The scope of the IST program review was to assure that all valves and pumps which

are required to be tested in accordance with ASME BEcPV code Section XI are

included in the IST program.

In addition, the results of selected IST pump and valve

tests were reviewed to assure the following:

~

Acceptance criteria are met or proper corrective actions were taken.

~

Tests adequately verified the design functions of the components.

~

Test records are maintained.

The 1990 and 1991 quarterly core spray valve exercise data for core spray valve HV-

151-F015A were reviewed.

The test records reviewed were well organized and

complete.

The valve stroke time data were reviewed and trended by the technical

support organization.

The pre-establish

acceptance criteria for valve stroke times were

'et for the data reviewed.

The quarterly core spray flow verification test data were

reviewed for core spray

pump 1P206A.

The test procedure was found to be acceptable.

The test results met

pre-established

acceptance criteria.

The test data were'well organized and trended by

the technical staff.

The overall IST program implementation was effective.

A review to assure that required valves and pumps were included in the IST program,

was conducted for the containment instrument gas system (CIG) and for the core spray

system.

The valves and pumps in the core spray system, selected for review, were adequately

incorporated in the IST program.

No deficiencies were identified with regard to the

core spray system IST program.

The CIG system is divided into a safety related (Q) and a non-safety related section

(non-Q).

The safety related section of the CIG system has

instrument gas bottles to

provide backup pneumatic energy actuation of the main steam system safety relief

valves (SRVs). The SRVs are required during accident conditions as part of the

automatic depressurization

system (ADS). A one inch check valve and a one inch

solenoid operated valve in the CIG system provide double valve isolation between the

Q and non Q portions of the CIG system.

Both valves are included within the Q

boundary.

The solenoid operated valve is provided to close the valve on a

containment isolation signal.

The solenoid valve is included in the IST program and

is routinely leak checked.

The check valves (1-26-018, 1-26-029, Unit 1; and 2-26-

018, 2-26-029 Unit 2), which are located in a ASME, B&PV Code,Section III, class

2 piping system, were not included in the IST program and were not leak tested.

The

licensee has not applied for relief from testing this valve.

The 10 CFR 50.55a

requires that inservice testing be performed on certain ASME Code Class 1, 2, and 3

valves.

Section XI Subsections IWV-1100 defines the scope of valves to be tested

in'erms

of plant shutdown" and accident mitigation.

Since this check valve is required

for accident mitigation it is required to be included in the IST program.

The omission

of this valve from the IST program is an apparent violation (Violation 50-387/91-06-

01).

5.0

nre

Ived Item

-

7

/

-

-

I

ed

Inspection Report 90-08 discussed

a licensee identified deficiency in the main steam

pipe tunnel fan wiring.. The reactor building main steam pipe tunnel coolers are a

non-safety related system.

An error in the wiring of the main steam pipe tunnel fan

resulted in the opposite fan's cooling coils functioning when the fan was in service.

It

also appeared

that the post installation testing was inadequate to identify this concern.

The licensee's immediate corrective action was to open the cooling coils service water

return bypass valve and verify that one fan in service could maintain tunnel

temperature.

Additional corrective actions were to re-wire the fan controls to the

service water valves and to survey the operators for similar type problems.

The

inspector reviewed Engineering Change Order (ECO) 90-6060 which re-wired the

valve controls and corrected plant drawings.

The ECO adequately corrected this

'iring

error.

The results of the operators survey and the technical section's response

to the survey were reviewed and found to be satisfactory.

Based on the above

corrective actions, this unresolved item is closed.

6.~

E~i

The inspector met with those individuals denoted in Attachment I, on May 10, 1991,

to discuss the inspection findings as detailed in this report.

I

P~d

ATTA HMENT I

A.

L~ien ee

  • E. Bragger, Sr. Proj. Eng.

'. Creasy, Pwr. Prod. Eng.

M. Golden, Plant Eng. Supv.

  • R. Harris, Sr. Results Eng.

D. McGann, Pwr. Prod. Eng.

G. Maertz, Pwr. Prod. Eng.

A. Nargoski, QA

T. Nork, Plant Eng. Supv.

  • L. O'eil, Supv. Eng.- Nuclear

R. Paley, Pwr. Prod. Eng.

  • D. Roth, Sr. Compliance Eng.

R. Rarig, Tech. Asst.

D. Ritter, Pwr. Prod. Eng.

T. Sweeny, Pwr. Prod. Eng.

B. Saccone, NPE

  • G. Stanley, Supt. of Plant
  • R. Wehry, Compliance Eng.

B.

NRC

  • S. Barber, Senior Resident Inspector

B. McDermott, Reactor Engineer

  • J. White, Chief, RPS 2A
  • Denotes those present at the exit meeting'conducted

onsite on May 10, 1991.