ML17146A376

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Resident Insp Repts 50-387/86-06 & 50-388/86-04 on 860315-0415.Violations Noted:Improperly Controlled Maint Work in Reactor Bldg Recirculation Plenum & Inoperability of Two Scram Discharge Vol Level Transmitters
ML17146A376
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 05/02/1986
From: Strosnider J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17146A374 List:
References
50-387-86-06, 50-387-86-6, 50-388-86-04, 50-388-86-4, IEB-80-17, NUDOCS 8605130226
Download: ML17146A376 (28)


See also: IR 05000387/1986006

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

Report

Nos.

50-387/86-06

50-388/86-04

Docket Nos.

50-387

CAT

C

50-388

CAT

C

License

Nos.

NPF-14

NPF-22

Licensee:

Penns

lvania Power

and Li ht

Com an

2 North Ninth Street

Allentown

Penn s

1 vani a

18101

Facility Name:

Sus

uehanna

Steam Electric Station

Inspection At:

Salem Townshi

Penns

lvania

Inspection

Conducted:

March

15

1986 - A ril 15

1986

Inspectors:

R.

H. Jacobs,

Senior Resident

Inspector

L.

P 'sc

, Resident

Inspector

Approved By:

. Strosnider,

Chief, Reactor Projects

Section

1B,

DRP

s/~/z~

date

Ins ection

Summar

~d:

i

t

7:

2

1

of plant operations,

licensee

events,

open items, surveillance,

maintenance,

and the Unit

1 Refueling Outage.

Results:

The inspector

noted that corrective maintenance

is required

on the

125

VDC Station Battery lighting system (Detail 2.2. 1);

an unusual

event

was

declared

due to

a contaminated/injured

man (Detail

3. 1);

an

open states link

was identified during the performance of the

HPCI overspeed

test (Detail 5. 1);

and post-maintenance

testing of motor operated

valve maintenance

needs

to be

reviewed (Detail 5.2. 1).

Three violations were identified.

One violation concerned

improperly controlled

maintenance

work in the reactor building recirculation

plenum (Detail 5.2.2).

The

second violation concerned

the inoperability of two

SDV level transmitters

(Detail 6.6).

The third violation concerned

SDV level transmitter isolation

valves which were not locked open

as required

by station administrative controls

(Detail 6.5).

8605130226

860507

PDR

ADOCK 05000387

I

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PDR lj

get

c

>,l

L

DETAILS

4

1.0

Followu

on Previous

Ins ection

Items

Closed

Unresolved

Item

388/84-34-14

Evaluate

Diesel Generator

Fre uenc

Oscillations

During the Unit 2 Loss of All AC Power event in July 1984,

the

'A'mergency

Diesel

Generator

(EDG) exhibited large frequency osci lla-

tions after

a manual start

and was subsequently

manually tripped by

the operator.

Further testing of the diesel

generator

following the

event could not reproduce

the oscillations.

The licensee

issued

scram recovery action item 2-84-04-21 to conduct

a review of the

EDG

performance

records

to determine if there

had been

any previous prob-

lems with oscillations.

In Inspection

Report 50-388/85-13,

the inspector

reviewed the

licensee's

assessment,

which included recommendations

for additional

testing of the diesel

generators.

The site staff had not completed

its evaluation of the recommendations

at the time of the followup.

The licensee's

corporate

engineering staff recommended

additional

testing of the diesel

generators

in PLI-37643 dated January

14,

1985.

The two monthly tests

recommended

were: (1) measuring

the output of

the governor

load sensor with an amplifier during manual operation;

and (2) measuring

the resistance

of the

speed

reference resistor

used

in emergency operation.

Plant staff review of the recommendations

found that the devices

are currently tested

in other surveillance

procedures

(18-Month Tests),

and that due to the history of reliable

operation of the devices,

the increased

testing

frequency

was not

warranted.

In addition the licensee

recently performed modifications

to the governor oil cooler, which should

improve the governor

response.

The inspector

reviewed the associated

surveillance

tests

and the re-

cent results for indications of degradation.

No unacceptable

items

were noted.

1.2

Closed

Violation

388/85-06-07

Emer enc

Li htin

Batter

Power

Su

1

Not 8-Hour Rated in Fire Zone 2-2A

In February

1985,

the inspector identified that the emergency light-

ing battery

power supply unit installed in the stairwell to the Re-

mote Shutdown

Panel

at the

670 feet elevation of the Unit 2 Reactor

Building (Fire Zone 2-2A, Core Spray

Pump

Room) did not meet the re-

quirements of 10CFR50,

Appendix R,Section III.J.

The installed light was manufactured

by Exide,

and was physically

different from the Dual-Lite Model units used in other safety-related

areas.

On July 19,

1985 the non-conforming battery

power supply was

replaced with a Dual-Lite 8-hour unit under

WA V50318.

The

NCR

14

85-0114

was subsequently

closed.

The inspector verified that the

new

light was installed.

2.0

Review of Plant

0 erations

2. 1

0 erational

Safet

Verification

The inspector toured the control

room daily to verify proper manning,

access

control, adherence

to approved

procedures,

and compliance with

LCOs.

Instrumentation

and recorder traces

were observed

and the sta-

tus of control

room annunciators

was reviewed.

Nuclear Instrument

panels

and other reactor protection

systems

were examined.

Effluent

monitor s were reviewed for indications of releases.

Panel

indica-

tions for onsite/offsite

emergency

power sources

were examined for

automatic operability.

During entry to and egress

from the protected

area,

the inspector

observed

access

control, security boundary integ-

rity, search activities, escorting

and badging,

and availability of

radiation monitoring equipment.

The inspector, reviewed shift supervisor,

plant control operator

and

nuclear

plant operator

logs covering the entire inspection period.

Sampling reviews were

made of tagging. requests,

night orders,

the

bypass

log, Significant Operating

Occurrence

Reports

(SOORs),

and gA

nonconformance

reports.

The inspector

observed

several shift, turn-

overs during the period.

No unacceptable

conditions were identified.

2.2

Station Tours

The inspector toured accessible

areas of the plant including the con-

trol room, relay rooms,

switchgear

rooms,

cable

spreading

rooms,

pen-

etration areas,

reactor

and turbine buildings, diesel

generator

building,

ESSW pumphouse,

and the plant perimeter.

During these

tours, observations

were

made relative to equipment condition, fire

hazards,

fire protection,

adherence

to procedures,

radiological

con-

trols and conditions,

housekeeping,

security,

tagging of equipment,

ongoing maintenance

and surveillance

and availability of redundant

.

equipment.

2.2.1

125

VDC Station Batter

Li htin

S stem

During a tour of the Unit

1 and Unit 2 reactor buildings

on

March 31,

1986,

the inspector

noted that

some of the

125

VDC Station Battery Emergency lights were on,

some were

off, and

some did not have light bulbs installed.

The in-

spector

reviewed lighting drawings

EL-64 and the

FSAR to

determine

the correct configuration requirements.

FSAR

Section 9.5.3

states

that the

125

VDC lighting fixtures

are normally energized

from the normal

AC subsystem,

and

automatically transfer to the

125

VDC system

on loss of

power.

The

FSAR also states

that continued energization

of

the

lamp w'ith AC power during normal operation

reduces

the

load on the battery chargers

and maintains

the

lamp fila-

ment at

a temperature

that limits the initial current

surge

when the

DC voltage is applied to the lamp,

and also allows

the lights be monitored continuously.

It appears

that cor-

rective maintenance

is required to ensure

the emergency

lighting system

meets

the

FSAR commitments'any

of the

.

areas

needed

to shutdown outside

the control

room currently

do not have operable light fixtures.

This item is

unresolved.

(387/86-06-01;

388/86-04-01)

3.0

Summar

of 0 eratin

Events

3.1

Unit

1

Unit

1 continued with its second refueling outage

which commenced

on

February

15,

1986.

The Unit reached

Operational

Condition

4 on April 8,

1986.

The, outage activities are discussed

in Detail 7.0.

The licensee

declared

an Unusual

Event at 7:00 p.m.,

March 21,

due to

a contaminated

injured man.

The individual was replacing the control

rod drive housing support underneath

the reactor vessel

when the

platform grating

gave way.

He fell about

10 feet to the subpi le

floor injuring his right knee.

He was in full protective clothing

(PC) using

a respirator,

but

some contamination

soaked

through the

clothing.

He was decontaminated

prior to being sent off site.

Con-

tamination levels

on the individual's skin were about

1-3K dpm/100cm 2

when

he was transported

via ambulance

to the Berwick Hospital.

The

hospital

had been alerted

and

was prepared

to minimize contamination

spread.

An HP technician

rode with the individual in the ambulance

and

an

HP supervisor

went to the hospital.

The Unusual

Event was

terminated at 7:57 p.m.

when the individual was transported

to the

hospital.

He was completely deconned

and all contaminated

materials

were brought back to the site.

Surveys of the hospital

and ambulance

showed

no spread of contamination.

The individual is a PP5L employee

and

has

a. broken

knee

cap.

Undervessel

work was halted until an in-

vestigation

was conducted

and the grating reinforced.

On April 8, the annual

emergency drill was held and involved full NRC

participation.

An assessment

of the drill will be included in In-

spection

Report 50-387/86-07;

50-388/86-08.

3.2

Unit 2

Unit 2 operated

at or near

100 percent

power for most of the inspec-

tion period.

Scheduled

power reductions

were conducted

throughout

the period for control rod pattern adjustments,

surveillance testing,

and scheduled

maintenance.

P

4.0

Licensee

Re orts

4. 1

In-Office Review of Licensee

Event

Re orts

The inspector

reviewed

LERs submitted to the

NRC:RI office to verify

that details of the event were clearly reported,

including the

accuracy of description of the"cause

and adequacy

of corrective

ac-'ion.

The inspector determined whether further information was re-

quired from the licensee,

whether generic implications were involved,

and whether the event warranted onsite followup.

The following LERs

were reviewed:

Unit

1

on High Radiation

Signal

86-006,

Unplanned

Engineered

Safety

Feature Actuation

When 'States

Link'ightened

86-007, Division I

LOCA Isolation Occurred

Due to Blown Fuse

Unit 2

    • 86-004, Reactor

Scram (Manual)

Due to Main Transformer Overheating

~Previously discussed

in Inspection

Report 50-387/86-02;

50-388/86-01

~*Previously discussed

in Inspection

Report 50-387/85-36;

50-388/85-32

4.2

Review of Periodic

and

S ecial

Re orts

Upon receipt, periodic

and special

reports

submitted

by the licensee

were reviewed

by the inspector.

The reports

were reviewed to deter-

mine that they included the required information; that test results

and/or supporting

information were consistent with design predictions

and performance specifications;

that planned corrective action was

adequate

for resolution of identified problems;

and whether

any in-,

formation in the report should

be classified

as

an abnormal

occurrence.

The following periodic

and special

report

was reviewed:

Monthly Operating

Report

March 1986, dated April 11,

1986.

The above report was found acceptable.

5.0

Monthl

Surveillance

and Maintenance

Observations

5.1

Surveillance Activities

The inspector

observed

the performance of surveillance

tests

to de-

termine that:

the surveillance test procedure

conformed to technical

specif'ication requirements;

administrative

approvals

and tagouts

were

obtained before initiating the test; testing

was accomplished

by

qualified personnel

in accordance

with an approved surveillance

procedure;

test instrumentation

was calibrated; limiting conditions

for operations

were met; test data

was accurate

and complete;

removal

and restoration

of the affected

components

was properly accomplished;

test results

met Technical Specification

and procedural

requirements;

deficiencies

noted were reviewed

and appropriately resolved;

and the

surveillance

was completed at the required frequency.

These observations

included:

TP-152-006,

HPCI Overspeed

Trip Testing Using Auxiliary Steam,

performed

on April 7,

1986.

During the performance of TP-152-006 witnessed

by the inspector

on

April =7,

1986,

the

HPCI turbine exceeded

the acceptable

overspeed

trip setpoint of 5059-5265

RPM.

The turbine tripped at 5289

RPM.

After adjustments

by mechanical

maintenance,

the test

was reperformed

successfully

on April 8.

While setting

up for the test,

on April 7,

IEC technicians

were to

open states

links AA-5 and AA-8 in terminal

panel

TB1C016-Al to de-

feat the low steam

supply pressure

isolation to HPCI.

When the panel

was opened, it was found that the links were already

open,

but no

tags were

on them.

The system status file was searched,

and

no work

was being performed which authorized

opening these links.

The

licensee initiated

SOOR 1-86-109 to investigate

the cause.

The

results of the investigation will be reviewed in a subsequent

inspection.

(387/86-06-02)

5.2

Maintenance Activities

The inspector

observed

portions of selected

maintenance activities to

determine that the work was conducted

in accordance

with approved

procedures,

regulatory guides,

Technical Specifications,

and industry

codes or standards.

The following items were considered

during this

review:

Limiting Conditions for Operation

were met while components

or systems

were

removed

from service;

required administrative approv-

als were obtained prior to initiating the work; activities were ac-

complished

using approved

procedures

and

gC hold points were

established

where required;

functional testing

was performed prior to

declaring

the particular component

operable; activities were accom-

plished

by qualified personnel;

radiological controls were imple-

mented; fire protection controls were implemented;

and the equipment

was verified to. be properly returned to service.

P

F

5.2.1

Motor 0 crated

Valve Maintenance

On March 20,

1986, while performing SE-149-002,

RHR Divi-

sion II Logic System Functional Test,

the recirculation

system discharge

bypass

valve (1F032B) did not automatical-

ly clo'se

on receipt of a

LOCA signal.

This function is

part of LPCI injection.

The licensee

investigated this

occurrence

and determined that

a lead in the auto-closure

logic was

landed improperly at the motor operated

valve

(MOV).

The lead

was found terminated at terminal

TB-82 and

to correct the problem,

the lead was

moved to terminal

TB-81.

The valve was subsequently

tested satisfactorily.

Unit

1 was in Operational

Condition

5 and the auto-closure

function of this valve was not required to be operable,

The inspector

reviewed this occurrence

to determine its

cause.

This valve actuator

had been recently worked for

MOV environmental qualification (Eg) preventive maintenance

(PM) under

WA P-53156.

The inspector

reviewed this work

package,

electrical

schematics

E-151 sheet

14, Ml-B31-275

( 16) and connection

drawings

E-379.

The inspector also

reviewed work packages

and applicable

schematics

for sever-

al other valves which received

MOV Eg

PMs this outage.

During the work performed

on

1F032B, the actuator

was de-

terminated,

disassembled,

and reworked.

All leads

were

removed

from the limit and torque switch assemblies.

Form

MT-GM-021-2 was filled out with the required verifications

for lead removal

and installation.

The form indicates that

a lead was removed

from and reinstalled to TB-82 (Cable

¹RKlg1506E).

E-151 sheet

14 and E-379,

show that TB-82 is

a spare limit switch contact.'pparently,

the work group"

removing the lead

on March

5 misread

the termination

number

and the individuals reterminating

the lead

on March

7 put

it back

on TB-82 since it was indicated that this was the

terminal

from which it was removed.

All other leads re-

moved'and

reterminated

matched

the print.

This error was

not identified during post-maintenance

testing of the

valve.

The only operational

retest required after mainte-

nance completion

was to stroke

and time the valve, verify-

ing proper valve performance

by control

room indication.

Since only the auto-closure

function of the valve was dis-

abled,

the retest

was inadequate

to identify this problem.

The work plan and Equipment

Release

Form did not require

any further testing to declare

the valve operational.

How-

ever,

due to the outage

schedule,

the

system

Logic

System'unctional

Test (LSFT) was performed prior to declaring the

recirculation or

RHR system operational,

although the

LSFT

was not required to be performed after this maintenance.

The licensee

performed

MOV E(} PMs on

37 valve actuators

during this outage.

These valves are in the

RHR, Core

Spray,

HPCI, RCIC,

RHRSW,

RWCU and Feedwater

systems.

The

inspector determined that in each

case,

according to the

outage

schedule,

either the system

LSFT was scheduled

to be

performed after completion of the valve maintenance

or the

valve does not have

an auto-closure

or opening function.

Therefore,

for this outage

the adequacy

of these

valves

following the

Eg

PMS is not a concern.

However, the retest

specified for the

PM should

be adequate

for the work per-

formed.

The inspector discussed

this issue with the Main-

tenance

Supervisor

Qho indicated they would review this.

This issued is considered

unresolved.

(387/86-06-03)

Recirculation

Plenum Work

On March 27,

1986, while observing

maintenance

on the reac-

tor building recirculation

plenum,

the inspector

noted that

access

hatches

to both the recirculation

fan supply and

discharge

sides of the recirculation

plenum were

open at

the

same time

Work was ongoing inside the upper

(supply)

portion of the plenum, but

no work was ongoing

on the dis-

charge side.

The inspector also noted that fuel movement

was in progress

on Unit

1 and

no

LCO had been entered for

loss of secondary

containment integrity.

The inspector

discussed

this condition with the Unit

1 and Shift Supervi-

sors.

Both individuals were

unaware that the plenum hatch-

es were open.

The work inside the recirculation

plenum

had

been authorized

by shift supervision with the understanding

that the access

hatch would be opened

to allow ingress

and

egress

only and that the access

hatch would be replaced

(although not tightened) while the work was underway.

Equipment

Release

Form (ERF) A-43692 was released

at 7:45

a.m.

March 27, to permit access

to the recirculation

plenum.

The

ERF stated that

a

man will be stationed at the

hatch during the access

period.

It did not indicate that

more than

one hatch would be'opened

or that the hatch would

only be opened for ingress

and egress.

As noted above,

when the inspector

observed that the access

hatch to the

lower plenum was opened,

there

was

no one stationed at the

hatch.

The work in the plenum was authorized

by WAs P60063

and P51875,

and involved preventive

maintenance

on the re-

circulation fans

and dampers.

This work is normally per-

formed during

a two-unit outage

when

secondary

containment

is not required.

This maintenance

needed

to be performed

during this pe'riod to satisfy environmental qualification

requirements.

~>>

J

The recirculation

plenum houses

the 'A'nd 'B'ecircula-.

tion fans

and their isolation dampers.

Upon receipt of any

zone ventilation isolation signal,

the recirculation fan in

AUTO LEAD will start to recirculate

the air in the isolated

ventilation zones (I, II and/or III) to minimize the con-

centration of radioactive

gases

in the event of an acci-

dent.

The Standby

Gas Treatment

System

(SGTS) takes

a

suction

on the discharge

side of the plenum to maintain

a

negative

pressure

in the reactor building and filter the

offsite release.

If the recirculation

fan in AUTO LEAD

fails to develop 0.5 in. W.C. pressure

across

the fan, af-

ter

a time delay,

the running fan will stop

and the standby

fan will start.

In this case,

the standby

fan (OV201A) was

tagged out.

Therefore,

the two open hatches

on the suction

and discharge

sides of the plenum would tend to equalize

pressure

across

the fan and

may have prevented

the running

fan from developing

the required 0.5 in. W.C. If the run-

ning fan tripped off, there would be

no recirculation flow.

Previous

experience

has

shown that without recirculation

fans,

the drawdown times for the

SGTS system to drawdown to

a 0.25 inch vacuum in the different ventilation zones,

would be exceeded.

Therefore, this condition

may have de-

graded

secondary

containment integrity.

When the inspector notified the control

room of the condi-

tion of the recirculation

plenum,

the Shift Supervisor

im-

mediately halted fuel movement.

The work in the recircula-

tion plenum was

secured

and the hatches

reinstalled.

Fuel

movement

was

recommenced

at 12:45 p.m.

March 27.

The main-

tenance

supervisor

indicated that both plenum hatches

were

open at the

same

time from approximately

10:00 a.m. to

12:00 a.m.,

a period of two hours.

The licensee

prepared

a

Significant Operating

Occurrence

Report

(SOOR) to evaluate

the incident.

Technical Specification 3.6.5. 1 requires maintaining

secon-

dary containment integrity when the reactor is in Opera-

tional Conditions

1, 2, 3, or when fuel handling is in

progress.

In this case,

Unit 2 was at power and fuel move-

ments were ongoing in Unit 1.

Opening

and leaving

open

both recirculation

plenum hatches

for two hours degraded

secondary

containment integrity.

This was contrary to the

directions

on the Equipment

Release

Form and the under-

standing of the operators.

Since the operators

were un-

aware of the condition of the recirculation

plenum,

no

Limiting Condition for Operation

was entered for not

main-'aining

secondary

containment integrity.

The release

of

this work was inadequately controlled and is

a violation of

AO-QA-306, System/Equipment

Release.

(387/86-06-04)

10

6.0

Ino erable

Scram Dischar

e Volume Level Transmitters

6.1

Summar

of Event

On April 10,

1986,

in Operational

Condition 4, licensee

I&C techni-

cians

noted contradictory

scram discharge

volume

(SDV) level indica-

tions during an operational

hydrostatic test.

Subsequent

investiga-

tion found that the isolation valves to two SDV level transmitters,

which provide reactor protection

system

(RPS) signals,

were closed.

Further review identified that the valves

had been closed

since the

installation of the level detectors

in May 1985.

The cause of the

inoperable

instruments

was the inadequate

close-out of a modification

package.

Due to the nature of the instrumentation circuits and the

surveillance test requirements,

the inoperable detectors

would not

have

been detectable

during normal plant operation.

6.2

S stem Descri tion

The

scram discharge

volume receives

the water displaced

by the motion

of the control

rod drive pistons during

a reactor

scram.

Should this

volume fill up to

a point where there is insufficient volume to ac-

cept the displaced

water control rod insertion would be hindered.

The reactor is therefore tripped when the water level

has

reached

a

point high enough to indicate that it is filling up, but the volume

is still great

enough to accommodate

the water from the movement of

the rods

when they are inserted.

In addition, if at the completion

of a scram the level of water in the

scram discharge

volume is great-

er than the trip setting,

the

RPS cannot

be reset until the discharge

volume has

been drained.

Four nonindicating level float switches

(one for each channel)

pro-

vide scram discharge

volume high water level inputs to the four RPS

channels.

Two switches

are installed

on each

instrument

volume.

In

addition,

a level indicating switch (tr ip unit), with transmitter,

in

.each

channel

provides

redundancy with the level switches.

This ar-

rangement

provides

sensor diversity,

as well as redundancy,

to assure

that

no single event or common-mode failure could prevent

a scram

caused

by

SDV high water levels

Both the four level transmitters

and

four float switches

are required to be operable

by Technical Specifi-

cations Table 3.3. 1-1.

All eight detectors

have the

same trip set-

point of 88 gallons

and are calibrated

on the

same

frequency (every

18 months).

IE Bulletin No. 80-17, "Failure of 76 of 185 Control

Rods to Fully

Insert During

a Scram at

a

BWR", and the subsequent

five supplements,

described deficiencies with the

SDV design.

In response

to the bul-

letin (PLA-770 dated

May 26,

1981),

the licensee

stated that delta-

pressure

level switches would be installed to provide diversity for

scram initiation.

The commitment

was included in the Unit

1 Oper-

ating License dated July 17,

1982,

as License Condition 2.C.(17).

11

The License Condition stated that prior to startup following the

first refuel'ing outage,

diverse

and redundant

SDV instrumentation for

each

instrumented

volume, including both delta pressure

sensors

and

float sensors,

were to be incorporated

into the

scram discharge

volume system.

6.3

Plant Modification Record

(PMR)82-578, which installed the level

transmitters,

was completed

on- May 2,

1985.

A letter was also sent

to

NRR (PLA-2470)

on May 20,

1985 stating that the design modifica-

tions required

by the License Condition had been

implemented.

Descri tion of Event

On April 10,

1986

an operational

leak test

was in progress

on Unit l.

The unit was in Operational

Condition 4 and was nearing completion of

the

second refueling outage which commenced

on February

15,

1986.

As

part of the surveillance test SE-100-002,

ASME Class

1 Boundary Sys-

tem Leakage/Hydrostatic

Pressure

Testing,

a full reactor

scram

was

manually initiated from the control

room.

At approximately

11:00

a.m.,

IAC technicians

who were performing unrelated

work in the upper

relay room,

noted contradictory

SDV level indications

on panel

1C635.

The Al detector

was indicating upscale

h'igh as expected,

but the

A2=

detector

was indicating downscale

low.

The technicians notified the

control

room and the discrepancy

was investigated.

Operators dis-

patched

to the reactor building

found valves

147F160C

and

D and

147F155C

and

D locked closed,

thus isolating level transmitters

LT-C12-1N016C and

D from the instrument

volume.

As noted above,

these

level transmitters

provide

a reactor protection

system

scram

signal

on high level in the

scram discharge

volume.

Further license

review identified that the system checkoff list (COL) incorrectly

required

these

valves to be locked closed.

The valves for the other

two level transmitters

were found open,

and were correctly aligned in

the

COL.

6.4

Licensee

Investi ation and Corrective Action

Following identification of the isolated level transmitters,

the

li-'ensee

took immediate corrective actions to realign the Unit

1 iso-.

lation valves

and to verify the status of Unit 2, which was operating

at

100 percent

power.

The checkoff list for Unit 1, CL-155-0012,

was

revised to restore

the 'C'nd 'D'evel transmitters,

and the valves

were properly aligned.

The level indications in the upper

and lower

relay panels

were verified to be proper.

The Unit 2 checkoff list

was verified to be correct,

and the isolation valves were physically

checked

to be in the proper position.

A Significant Operating

Occurrence

Report

(SOOR 1-86-113)

was issued

to describe

the event

and to initiate an investigation

and corrective

action.

The licensee

evaluated

the event

and determined it not to be

reportable

in accordance

with 10 CFR 50.72 '

12

On April 20,

1985, during the Unit

1 first refueling outage,

the Con-

trol

Rod Drive Hydraulic System

was lined up by operations

checkoff

1 ist COL-OP-155-001-2,

Revision 4.

This valve lineup listed the

"normal positi'on" for the eight level transmitter

isolation valves

as

locked closed.

The valves were locked closed in the

COL because

the

modification to install the level transmitters

had been only partial-

, ly completed,

and this incomplete installation

was to be is'olated

from the instrument volume.

The modification

PMR 82-578,

was com-

pleted.and

declared

operational

on May 2,

1985.

Prior to declaring

a system operable,

the modification process

re-

quires the completion of Operational

Readiness

Form AD-gA-410-8.

The

form requires that the Operations

section

head

sign the checklist to

indicate that the required actions

are complete.

One of the required

actions

includes updating operating procedures'his

section of the

form was signed

on May 2,

1985.

Licensee

review, following the

event, identi'fied that during the modification closeout

process,

the

operations

section did not identify that the

COL needed

to be revised

to place the

new level transmitters

into service.

The Document

Re-

view sheet,

Form AD-gA-410-3, completed

by the responsible

engineer

did not list any operating

procedures

that required revision.

This

was also true for the

OMISS Abstract.

Both of these

documents

should

have noted that the

COL needed revision,

and normally would have

alerted the Operations

section that

a change

was required.

The level transmitter modification was reviewed

and closed out on

May 2,

1985.

Later the

same

day,

members of the control

room oper-

ating staff noted that the valves were still closed

on the

COL, and

a procedure

change,

(PCAF 1-85-562)

was issued

to open the isolation

valves for the 'A'nd 'B'etectors.

The

PCAF did not address

the

'C'nd 'D'ransmitters.

During the investigation it could not be

determined

why the other two detectors

were not realigned,

but it

appears

there

may have

been

a drawing error at the time which showed

the 'C'nd 'D'etector valves already

locked open.

6.5

Although the licensee

investigation

was not complete

by the

end of

the inspection period,

the root cause

appears

to be the inadequate

closeout of the completed modification.

NRC Followu

Review

The inspectors

reviewed the operating

procedures,

checkoff lists,

surveillance

procedures,

system drawings

and the modification package

related to the

scram discharge

volume to determine

the cause of the

isolated valves

and to determine

whether the inoperability should

have

been detected

previously.

Inspector

review of the modification package

and applicable

documents

confirmed the licensee's

findings.

As discussed

in section 6.4, the

cause of the isolated level detectors

appears

to be

an error made in

the closeout of the

SDV modification package.

13

The level transmitters

are required

by Technical Specifications

to

have

a monthly functionaT and 18-month calibration surveillance test

performed

on them.

The monthly functional test consists of injecting

a signal into the circuit in the relay

room to verify the circuit

response.

The isolation valves are not manipulated during this test,

and the level transmitter is not disturbed.

The

18 month survei 1-

lance test requires

the manipulation of the transmitter isolation

valves,

but since the system

had just been

placed in service

in Hay

1985, this surveillance test

had not yet been

performed.

It is

possible that this inoperability would have

been identified during

the calibration procedure

which is scheduled

for November

1986.

All

of the surveillance tests

performed

on the isolated detectors

met the

acceptance

criteria.

The post-modification testing that was performed

also did not verify that the level transmitters

were connected

to the

process.

The system

schematic

diagrams

were reviewed to determine if the

post-trip review process,

following one of the three reactor

scrams

during this period,

should

have detected

the inoperability of the

level transmitters.

The level transmitters

provide inputs to the

RPS

trip system,

SDV high level alarms,

and plant computer points.

The

inputs to the

RPS

system

are in series with the float switch inputs;

so that as long as the float switches

operate

properly, the

RPS sys-

tem will respond

as designed

on

a

SDV high level condition.

The

alarm

and computer point contacts

are in parallel

so that any input

will provide the indication.

Due to this circuit configuration,

the

inoperability of the transmitters

could not have

been detected

by

control

room indications or the plant computer printouts.

The only

direct indication available is the level meters

in the relay room,

which would only indicate during

a scram.

The inspectors

conducted

a walkdown of the Unit

1 and Unit 2

SDV in-

stallations.

Several

discrepancies

were identified with the Unit 2,

'OL and drawings.

Administrative procedure

AD-QA-302, System Status

and Equipment Control, states

that root valves (first valves off

process

line) that supply safety related instrumentation will be

locked open.

During the walkdown of the Unit 2 system it was noted

that four of the isolation (root) valves were not locked open,

as

were the. other twelve valves.

The checkoff list CL-255-0012 also

listed these

valves

(247155A,

B,

C,

and

D) as

open rather than locked

open.

This does

not appear

to be consistent with the administrative

procedure.

The system drawing was also incorrect.

P&ID H-2147

shows

that isolation valves

247F115A

8

B and

247F160A

8

B are locked closed

while they should

be locked open.

This item is

a violation.

(388/86-04-02)

6.6

Technical

S ecification Adherence

Technical Specification Limiting Condition for Operation

(LCO) 3.3. 1

requires that during Operational

Conditions

1, 2,

and

5 (with any

control rod withdrawn), the reactor protection

system instrumentation

lf

%y

'I

channels for the

scram discharge

volume high wat'er level transmitters

be operable.

Table 3.3. 1-2 states, that two operable

channels

per

trip system

are the minimum required.

With the

number of operable

channels

less

than the required

Minimum

operable

channels

per trip system,

for both trip systems,

at least

one trip system is to be placed in the tripped condition within

1

hour and the unit is to be in at least

Hot Shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

(if starting in Operational

Condition

1 or 2).

6.7

Contrary to the above,

between April 20,

1985 and April 10,

1986 two

scram discharge

volume high water level transmitters

were inoperable,

in that their isolation valves were

shuts

This is

a violation.

(387/86-06-05)

Safet

Si nificance

As described

in sectiop 6.2,

the two level transmitters that were

found isolated provide inputs to the reactor protection

system.

One

detector

from each

RPS trip system

was affected.

The remaining

two

level transmitters,

one per division, were sufficient to provide

a

reactor

scram signal

on high scram discharge

volume water level, as-

suming

no single fai lure.

In addition,

the four float switches,

which provide diverse

and redundant initiation signals

were operable.

Inspector

review of completed surveillance

tests verified that the

float switches

were operable,

and that there

has not been

a history

of failures of these detectors.

Each

SDV instrument

volume is monitored

by two other level detectors,

which provide alarm functions.

One float switch on each

volume pro-

vides

a "not drained" alarm,

and another

provides

a

Rod Block Signal.

The four high level float switches also provide

a high level alarm,

in addition to the

RPS signal.

Therefore, if any leakage

had oc-

curred, it would have

been annunciated

in the control

room.

During

normal operation

the

SDV vent and drain valves are open, allowing any

leakage

to drain from the volume.

The level transmitters

were installed during the Unit

1 first refuel-

ing outage

in May 1985.

Therefore,

the unit did operate

safely,

and

in accordance

with Technical Specifications,

for approximately three

years with only the four float switches

operable.

The objective of

the design modification which installed the additional transmitters

was to provide diversity,

so that

a single

random failure or poten-

tial

common cause failures could be accomodated.

Investigations

and

test performed

by

BWR licensees

have

shown that crud buildup,

human

error, manufacturing defects,

hydrodynamic forces

and environmental

concerns

have led to past

common-cause

failures with the float

switches.

The level transmitters

were added to the Technical

Speci-

fications by the licensee

following the modification.

15

Although the isolation of the level transmitters

appears

to be of

minimal safety consequence,

the adequacy of the. closeout

and testing

of safety-related

modifications must be viewed as

a safety concern.

Since the

same controls are

used

on other safety-related

modification

activities, this area

should

be addressed

in the licensee's

correc-

tive action.

6.8

Summar

of Findin

s

Technical Specification 3.3. 1, which requires

four SDV level

transmitters

to be operable

in Operational

Conditions

1, 2,

and

5,

was violated.

The valves to two of the level transmitters

were isolated

on April 20,

1985,

and Unit

1 operated

from June 8,

1985 until February

15,

1986 when the unit shutdown for a

refueling outage.

(There were three short forced outages

during

the period).

The isolated valves were discovered

on April 10,

1986.

The level transmitters

were left isolated after the completion

of a modification due to

a failure in the modification closeout

process.

The checkoff list was not revised during the closeout

process,

and the operating

procedures

were not identified as

needing revision

on the Document

Review Form, or the

OMISS ab-

stract.

Two of the detectors

were later valved in when identi-

fied by operations

personnel.

The closeout

process

needs

to be

reviewed for adequacy.

Post-modification testing did not verify

that the detectors

were connected

to the process.

Due to the configuration of the

SDV level circuitry, and indica-

tion, the licensee

could not have

been

expected

to identify the

isolated detectors

during normal plant operation.

The

SDV high

level alarm contacts

are paralleled with the float switch contacts

so that either device will actuate

the alarm.

Therefore, if the

float switches

responded

as designed,

the failure of the level

transmitter

would be masked.

The

same

type of circuitry exists

for the computer points.

Review of the post-trip data would not

have

shown

any abnormal

occurrences.

The level transmitter in-

dication in the relay room, observed

during

a scram,

was the

only method to identify the isolated detector.

The closed

valves would have

been manipulated

by the 18-month calibration

procedure,

but it was not due to be performed until November

1986.

Since the isolated level transmitters

provided redundant sig-

nals,

and the four float switches

were fully operable,

the fact

that the detectors

were inoperable

appears

to be of minimal

safety significance.

The unit operated for approximately three

years prior to the installation of the level transmitters.

16

Several

procedural

and drawing problems

were noted during the

investigation.

Although the station administrative

procedures

require that instrument root valves

be locked open,

the Unit 2

checkoff list did not lock open all of the level transmitter

isolation valves.

In addition, the Unit 2 system drawing,

P&ID

M-2147, incorrectly stated that four of the isolation valves

were normally locked closed:

The'alves

were found in the cor-

rect position.

The licensee

investigation

has not been

completed

and more in-

formation

may become available at

a later date.

This will be

reviewed during

a later inspection.

7.0

Unit

1 Refuelin

Outa

e Activities

7. 1

Refuelin

Outa

e

Summar

During this period, Unit

1 continued its second refueling outage

which began

February

15,

1986.

Major outage work during this period

consisted

of restoration of Division I systems,

bulk work and resto-

ration of Division II systems,

refueling, integrated

system testing,

and preparations

for startup.

It was noted in the last report peri-

od, that

some linear indications were identified on the

steam dryer

and support block during in-vessel

inspections.

These indications

did not require repair.

Refueling began

on March 21 and was complet-

ed March 28.

'Due to an excessive

number of failures of snubbers,

the

licensee

was required to remove

and test

more than

1000 snubbers.

Outage critical path time was not impacted.

Following refueling com-

pletion,

4KV bus outages

were conducted

to install

a degraded

grid

voltage modification.

The bus outages

were followed by loss of

offsite power and

LOCA testing

which was completed April 7.

The

reactor

vessel

head

was reinstalled

and Operational

Condition

4 en-

tered

on April 8.

The Operational

hydrostatic test

was completed

on

April 11.

Leaks identified during the test,

including leaks in the

reactor vessel

head piping and two control rod drives,

were repaired.

At the end of the report period,

the outage

was still on schedule with

reactor startup

expected

to occur on April 18.

7.2

Desi

n Chan

es

and Modifications

The inspector

observed

portions of selected modification activities

to determine that:

Limiting Conditions for Operation

were met while

components

or systems

were

removed

from service;

required administra-

tive reviews

and approvals

were obtained prior to initiating the

work; the installation conformed to the'rawings

and other design

documents; activities were conducted

using formal work control proce-

dures;

and

gC hold points were established

where required.

17

Portions of the following activities were 'observed:

PMR 84-3113,

Degraded Grid Voltage Protection,

performed

under

CWO C51225

on March 21,

1986 (1A202

4KV Bus).

No unacceptable

conditions were identified.

7.3

Com lex Surveillance

Test Witnessin

The inspector

observed

the performance of portions of certain

complex

18-Month Surveillance tests to determine that:

the Technical

Speci-

fication (TS) surveillance

requirement

was covered

by an approved

procedure;

that prerequisites

were completed;

special

test equipment

was calibrated;

required data

was accurately

recorded;

appropriate

revision of the test procedure

was available

and in use

by test per-

sonnel;

system restoration

was accomplished

upon completion of test-

ing; and the surveillance

was performed within the time frequency

specified

by the Technical Specifications.

Portions of the following tests

were observed:

SE-124-C02,

18-Month Diesel Generator 'C'uto Start

and

ESS

Bus

1C Energization

on Loss of Offsite Power - Plant Shutdown,

performed

on April 4,

1986.

SE-124-D02,

18-Month Diesel Generator 'O'uto Start

and

ESS

Bus

1D Energization

on Loss of Offsite Power

Plant Shutdown,

performed

on April 7,

1986.

SE-124-207,

18-Month Diesel Generators 'B'nd 'D'uto Start

and

ESS

Buses

1B and

1D Energization

on Loss of Offsite Power

with a

LOCA - Plant Shutdown,

performed

on April 7,

1986.

SE-124-107,

18-Month Diesel Generators 'A'nd 'C'uto Start

and

ESS

Buses

1A and

1C Energization

on Loss of Offsite Power

with a

LOCA - Plant Shutdown,

performed

on April 5,

1986.

The following items were noted:

During the performance of SE-124-107,

the 'C'SW pump did not

start automatically

as designed.

In addition, the 'C'SW

pump

and

1A RHRSW pump could not be manually started

from the control

room.

Licensee investigation later found that relay

44AX1 had

not picked up.

It was replaced.

A data review following the

test

found that timing relay 62A-20302 for the

1C

RHR pump was

'out of tolerance.

It was also repaired.

During SE-124-D02,

the inspector

noted that

speed oscillations

occurred

on the 'D'iesel

generator

following the

shutdown of

the

RHR pump.

Frequency

decreased

to approximately 58.5 several

times before the test

was completed.

t

lt

18

During the performance of SE-124-C02,

the inspector

noted

some

discrepancies

with the procedure

changes

that were issued prior

to the test.

PCAF 1-86-486

added

an additional prerequisite for

the test,

but the step

was not added to Attachment

A for signing

for completion of the prerequisite.

The change

added ventila-

tion fan

1V210C

(RHR Pump

Room Unit Cooler) since drywell cool-

ing fan

1V414A was out of service.

Just prior to starting the

test,

the inspector discussed

the discrepancy with the test di-

rector,

who then noted the error in the

PCAF.

In addition, the

PCAF had not been properly incorporated into the procedure.

The

test director then issued

a

new

PCAF to the procedure

and

had

the additional

fan started

as required.

The inspector

had

no

further

concerns'.0

Alle ation - Dravo

C

On March 31, the inspector received

an allegation via telephone

from a

recently terminated

Dravo, Inc.

QC inspector.

Dravo, Inc. is the con-

structor for the fifth diesel. generator

(D/G) project.

The individual

indicated that

he

had

been terminated

for refusing to perform an inspec-

tion on bolts to be

used with Unistrut supports.

He indicated that

he

refused

to perform the inspection

because

a Non-Conformance

Report

(NCR)

was outstanding,

relating to the bolts.

His concern

was that Dravo im-

properly used

a Gibbs

& Hill document to authorize cutting of the bolts,

and questioned

whether it was acceptable

to cut these bolts.

The inspector

reviewed

NCR Number 361, Construction Site Procedures

(CSP)

8. 1 "Non-Conformance

Reports",

CSP 8.4 "Configuration Control

and Informa-

tion Request",

Quality Control Procedure

(QCP) A-10 "Control of Noncon-

forming Items",

and Information Request

( IR) PP&L-009.

The inspector also

discussed

this incident with the

PP&L Assistant

QA manager for the fifth

D/G project,

the Dravo, Inc.

QC Site Supervisor

and

a

PP&L engineer.

On

February

27,

1986, Information Request

PP&L-009 was issued

requesting

per-

mission to cut 1/2"-13 x

1 3/16" and 1/2"-13

x

1 1/2" bolts to

a length of

1/2" and 15/16" respectively.

The bolts were to be used with Unistruts

and were too long.

On February

27, the

IR was resolved indicating that

the bolts could be cut.

The

IR was written on

a Gibbs

& Hill (G&H) IR

form.

The nonconformance

specified

on

NCR ¹361 dated

March 25,

1986 was

that IR PP&L-009 was prepared

on the wrong form (Attachment

C rather than

Attachment

F to

CSP 8.4)

~

The

NCR specified that this was nonconforming

because

the approval authorities

and distribution are different.

The

NCR

was dispositioned

"use-as-is"

on March 26 based

on the fact that it was

an

isolated

case

and that the

IR was properly dispositioned

by PP&L Nuclear

Plant Engineering.

However,

the

NCR was apparently

not dispositioned at

the time the individual refused to perform the inspection.

In reality, the

PP&L and Gibbs

& Hill IR forms are virtually identical

forms.

The incorrect form was

used but was processed

in accordance

with

procedure.

The

NCR originator

and the

NCR log indicated that

a "Hold" Tag

was not issued for this

NCR.

Therefore,

no equipment

was placed in a

19

"hold" status.

The governing procedures,

gCP A-10 and

CSP 8. 1, however,

do not recognize

issuance

of an

NCR without a "hold" tag although the pro-

cedures

do not explicitly state that

NCRs must use "hold" tags.

Since

this issue

does not relate to the safety

impact of the allegation, it will

not be further addresssed.

The potential

safety concern relates

to use of the cut bolts.

Since the

bolts were only shortened,

the strength properties of the bolt are not

affected.

The bolts were to be used in Unistrut as part. of a conduit sup-

port and the bolts would be engaged with a spring nut.

PP&L engineering,

which was the proper design authority,

approved

the cutting and use in

this application.

The inspector

reviewed

PP&L Specification

C-1055,

"Technical Specification for Routing

and Installation of Conduit and

Conduit Supports

in the 'E'iesel

Generator Building", which indicates

that 1/2" diameter bolts are acceptable

for this application

and the spec-

ification does

not preclude bolt cutting.

Therefore,

there is no safety

concern 'with the use of these bolts.

This allegation is closed.

9.0

Reactor

Hi

h Pressure

Switch Head Connection

On March 6,

1986 during the current Unit

1 refueling outage,

the licensee

identified that the head correction calculations of PS-B21-1N023A,

B,

C,

D

(Unit

1 reactor vessel

steam

dome pressure

switches)

were in error.

These

pressure

switches

provide input to the reactor protection

system

(RPS) to

scram the reactor

on high pressure.

The head correction calculational

error was in the non-conservative

direction by 9.7 psig.

The nominal trip

setting in the Technical Specifications

(TS) is 1037 psig.

The allowable

value is 1057 psig.

The licensee

reviewed past calibration data

from 1982

to the present

and identified no cases

in which the unit was operated with

the pressure

switch setting exceeding

the Technical Specification allow-

able value

due to this head correction error.

The calculational error did

cause

the "As Left" setting of the switches following a calibration to be

in excess

of the nominal trip setting of 1037 psig

on many occasions.

The

surveillance

procedure,

SI-158-303,

specifies

an "As Left" value for these

switches to be less

than or equal

to the nominal trip setting,

so that

between calibrations,

instrument drift should not cause

the pressure

switch setting to exceed

the allowable valves.

However,

since the allow-

able value was not exceeded,

no Technical Specification violation occurred.

The head correction calculation error resulted

from using

an improper ele-

vation for the pressure

switches.

The licensee

reviewed

head correction.

calculations for the corresponding

Unit 2 pressure

switches

and

50 other

Unit

1 and Unit 2 instruments.

No other discrepancies

were identified.

The inspector

reviewed portions of the pressure

switch surveillance

data

and elevation data for other

instruments

and identified no discrepancies.

The calcul'ations

were performed

by the

same individual and appear to be

isolated occurrences.

The inspector

had

no further concerns.

20

0.

~Ei

tl

On April 18,

1986 the inspector discussed

the findings of this inspection

with station

management.

Based

on

NRC Region I review of this report and

discussions

held with licensee

representatives,

it was determined that

this report does

not contain information subject to

10 CFR 2.790

restrictions.