ML17059B443

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Insp Repts 50-220/96-14 & 50-410/96-14 on 961201-970111. Violation Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML17059B443
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 02/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17059B441 List:
References
50-220-96-14, 50-410-96-14, NUDOCS 9703050278
Download: ML17059B443 (54)


See also: IR 05000220/1996014

Text

U.S. NUCLEAR REGULATORY COMIVIISSION

REGION I

Docket/Report Nos.:

50-220/96-14

50-410/96-14

License Nos.:

DPR-63

NPF-69

Licensee:

Niagara Mohawk Power Corporation

P. O. Bex 63

Lycomihg, NY 13093

Facility:

Nine Mile Point, Units

1 and 2

Location:

Scribe, New York

Dates:

December 1, 1996- January

11, 1997

Inspectors:

B. S. Norris, Senior Resident Inspector

T. A. Beltz, Resident Inspector

R. A. Skokowski, Resident In'spector

Approved by:

Lawrence T. Doerflein, Chief

Projects Branch

1

Division of Reactor Projects

9703050278

97022i

PDR

ADOCK 05000220

8

PDR

4

TABLE OF CONTENTS

page

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EXECUTIVE SUMMARY ........................................~.

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SUMMARY OF ACTIVITIES

Nia'gara Mohawk Power Corporation (NMPC) Activities ...-.............

Nuclear Regulatory Commission (NRC) "Staff Activities

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I ~ OPERATIONS

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Conduct of Operations .'.....,...............

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01.1'eneral

Comments

01.2

Unit 2 Power Reduction for Feed Water Pump Exchange ..

01.3

Unit 2 Missed UFSAR-Required

CRD Housing Support Gap

Inspections .............................,....

07

Quality Assurance

in Operations ................'........

07.1

Unit 1 Housekeeping

08

Miscellaneous Operations Issues........................

08.1

(Open)

LER 50-220/96-11:

Reactor Scram Caused

by the

Main Generator Lockout Relay Trip

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II. MAINTENANCE ..........................:.....

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M1

Conduct of Maintenance

M1.1

General Comments

M1.2

Unit 1 Liquid Poison Pump and Check Valve Operability

il

Surveillance Test

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M1.3

Maintenance

Rule Evaluation of Unit 2 NonSafety-Related

Switchgear-003...................,...........

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III. ENGINEERING...'......... ~...............

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E2

Engineering Support of Facilities and Equipment.......... ~....

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E2.1

Hot Shorts Vulnerability of Unit 2 Shutdown Cooling Valves ..

E2.2

Potential Overpressurization

Concerns

Relative to NRC Generic

96 06

etter 96 06 .. ~... ~..... ~.....

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E8

Miscellaneous

Engineering

Issues

E8.1

(Closed)

LER 50-220/96-09:

Potential Overstressed

Pipe

Supports. Caused by Design Deficiency

E8.2

(Closed)

Special Report:

Inoperability of Unit 1 ¹11

Containment Hydrogen Monitoring System

E8.3

(Closed) URI 50-220/95-25-01:

Emergency Cooling System

Material Deficiencies '................. ~.... ~.....

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E8.4

(Closed)

URI 50-410/95-12-01:

Temporary Scaffolding

Erected Around Unit 2 Liquid Poison Tank for Extended

Period

with no Engineering Evaluation ...,.... ~.......... ~...

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Table of Contents (cont'd)

IV. PLANT SUPPORT

R4

Staff Knowledge and Performance

in Radiological Protection......

R4.1

Repeat Failure to Properly Secure

a Unit 1 High Radiation Area

ate.....

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G

V. MANAGEMENTMEETINGS

X1

Exit Meeting Summary.... ~.......................

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X3

Management

Meeting Summary

ATTACHMENT

17

18

18

'19

19

19

Attachment 1-

PARTIALLIST OF PERSONS CONTACTED

INSPECTION PROCEDURES USED

ITEMS OPENEO, CLOSED, AND UPDATED

LIST OF ACRONYMS USED

EXECUTIVE SUMMARY

Nine Mile Point Units 1 and 2

50-220/96-14

8c 50-410/96-14

December 1, 1996 - January 11, 1997

This integrated inspection report includes reviews of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a 6-week period of resident inspection.

PLANT OPERATIONS

. The December 5, 1996, power reduction at Unit 2 to exchange

operating feedwater pumps

was completed

in accordance

with approved procedures.

The pre-evolution briefing

contained

an appropriate

level of detail for the plant conditions, and discussions

by the

~ operators indicated a thorough understanding

of the upcoming evolution.

t

The licensee demonstrated

good safety perspective

by shutting down Unit 2 upon

identification of the missed Updated Final Safety Analysis Report (UFSAR) required control

rod drive (CRD) housing support gap verifications.

The licensee's inspection revealed

out-'f-tolerance

gaps on 19 of 185 CRDs.

Their engineering supporting analysis, which

determined that the out-of-tolerance gaps did not affect the operability of the system, was

considered technically sound by the inspectors.

Subsequent

changes to the applicable

procedure

appear adequate to ensure the future gap verification.

However, the failure to

completed the UFSAR-required gap verifications was classified as,a Non-Cited Violation.

The inspectors identified an open polyethylene

bag adjacent to the Unit

1 spent fuel pool

that was not properly controlled with respect to foreign material exclusion accountability

due to inattention by personnel.

This was classified as a Non-Cited Violation.

At Unit 1, the inspectors identified several examples of improperly stored ladders.

The

recurring failure to appropriately store and/or secure ladders located near safety-related

and

other important equipment was considered

a weakness.

MAINTENANCE

Unit

1 Operations Department conducted

a liquid poison system quarterly surveillance in a

controlled manner.

Coordination and communications

between Operations

and lnservice

Testing (IST) personnel were very good.

Operations

and IST personnel

knowledge

regarding the evolution was good.

The test data was complete and received

a timely

review.

Unit 2 appropriately included the non-safety-related

electrical switchgears within the scope

of the Maintenance

Rule, and evaluated the risk associated

with on-line maintenance

for

'the switchgear.

IV

Executive Summary (cont'd)

ENGINEERING

Niagara Mohawk Power Corporation (NMPC) notified the Nuclear Regulatory Commission

(NRC) that Unit 2 may have operated

outside its design basis due to the potential for a 10 CFR 50, Appendix R, fire-induced hot short condition that could result in damage to three

shutdown cooling valves.

The licensee took appropriate immediate corrective actions to

address the concern.

NMPC appropriately notified the NRC of potential conditions outside design basis identified

during their review of Generic Letter (GL) 96-06.

The licensee's review identified several

. drywell penetrations

at both units that could potentially exceed the design pressure

during

an accident due to thermal expansion of entrapped

water.

The operability determinations

were adequate

and in accordance

with the guidance provided in GL 96-06; the operability

.

determinations for the Unit 1 core spray high point vent and post-accident

sampling lines

were particularly appropriate

and conservative.

The licensee issued

a voluntary Licensee Event Report concerning potential overstressed

pipe supports for the reactor building closed-loop cooling system.

The supports could

become overstressed

due to.thermally induced longitudinal expansion.

The root cause

evaluation and corrective actions were appropriate.

NMPC evaluation and corrective actions to NRC-identified emergency cooling system

discrepancies

appeared

appropriate.

However, the licensee's failure to implement the

existing technical guidance to ensure adequate

valve packing gland nut thread engagement

was classified as a Non-Cited Violation.

The failure to follow plant procedures

resulted in the installation of temporary scaffolding

around the Unit 2 standby liquid.control (SLC) syste'm tank for an extended

period without

proper engineering

analysis.

This was classified as a Non-Cited Violation.

PLANT SUPPORT

On two occasions,

the inspectors identified the same high radiation area access gate to be

unlocked.

The corrective actions to the first occurrence were ineffective, and the

inspectors considered this a recurring failure of procedural adherence.

(VIO 96-14-03)

REPORT DETAILS

Nine Mile Point Units 1 and 2

50-220/96-14

8L 50-410/96-14

December 1, 1996 - January 11, 1997

SUMMARYOF ACTIVITIES

Niagara Mohawk Power Corporation (NMPC) Activities

Unit 1

Nine Mile Point Unit 1 (Unit 1) started the inspection period at full power.

On December

24, Unit 1 experienced

a failure of ¹11 circulating water pump.

This resulted in a

reduction of power to 78% for approximately 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

Full power operation resumed

and

continued to the end of the report period.

Unit 2

Nine Mile Point Unit 2 (Unit 2) started. the inspection period at full power.

On December 5,

power at Unit 2 was reduced to approximately 55% to support

a feed water pump (FWP)

exbhange.

Unit 2 was returned to full power 38 hou'rs later.

On December 19, Unit 2

conducted

a reactor shutdown to perform control rod drive (CRD) housing support gap

inspections.

The reactor was started up on December 23, and the unit achieved full power

on December 26. The unit maintained essentially full power for the remainder of the

inspection period.

Or anizational Chan

es

On December 1, 1996, Messrs. Martin McCormick and Carl Terry exchanged

responsibilities within the Nine Mile Point nucleai organization.

Mr. McCormick became the

Vice President - Nuclear Engineering

and Mr. Terry became the Vice President - Nuclear

Safety Assessment

and Support.

Nuclear Regulatory Commission (NRC) Staff Activities

Ins ection Activities

The NRC conducted

inspection activities during normal, backshift, and deep backshift

hours.

The results are contained in the applicable sections of this report.

U dated Final Safet

Anal sis Re ort

UFSAR Reviews

A recent discovery of a licensee operating their facility in a manner contrary to the UFSAR

description highlighted the need for additional verification that licensees were complying

with UFSAR commitments,

While performing the inspections discussed

in this report, the

inspectors reviewed the applicable portions of the UFSAR related to the areas inspected.

The inspectors verified that, with the exception of the Unit 2 CRD housing support gap

inspections described

in Section 01.3, the UFSAR wording was consistent with the

observed plant practices, procedures

and/or parameters.

2

I. OPERATIONS

01

Conduct of Operations (71707)

'1,1

General Comments

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety-conscious;

specific events and noteworthy observations

are detailed in

the sections below.

01.2

Unit 2 Power Reduction for Feed Water Pum

Exchan

e

a.

Ins ection Sco

e

On December 5, 1996, a planned power reduction of the Unit 2 reactor was

completed to allow the B FWP to be removed from service due to excessive

seal

leakage.

The inspectors observed

portions of the power reduction because

the B

reactor recirculation system

(RCS) pump was experiencing

higher than normal

tfibration that could have been aggravated

during the evolution,

In addition to

observing the power reduction, the inspectors observed the pre-evolution briefing,

and reviewed applicable plant procedures.

b.

Observations

and Findin s

The inspectors observed

portions of the Unit 2 power redu'ction completed on

December 5, 1996.

Power was lowered to remove the B FWP from service

because

of excessive

seal leakage.

Control rods were inserted until power was

reduced to 90%, then reactor recirculation flow was decreased

until power reached

55%.

The power reduction was preformed in accordance

with approved

Procedure

N2-OP-101D, "Power Changes,"

Revision 3.

The inspectors observed the reactivity manipulation pre-evolution briefing provided

to the crew performing the reactor recirculation flow decrease.

This briefing was

completed in accordance

with Procedure

N2-ODP-OPS-0110, "Reactivity

Management

Program," Revision 7. Since the B RCS pump was experiencing

higher

than normal vibration, which could be aggravated

during the flow decrease,

the

briefing included a review of the emergency downpower actions.

During the

briefing, discussions

by the operators indicated their understanding

of the upcoming

evolution.

Before the power reduction, the RCS pump vibrations were higher than

normal but within the manufacturer's

limits. Before and during the power reduction,

NMPC monitored and trended additional parameters for indication of pump

degradation;

no indications of RCS pump degradation

were observed.

Topical headings such as 01, MS, etc., are used In accordance withthe NRC standardized reactor inspection report

outline.'ndividual

reports are not expected to address

all outline topics.

The NRC inspection manual procedure

or temporary

Instruction that was used as inspection guidance Is listed for each applicable report section.

3

w

During the evolution, management

oversight was provided by the Operations

Manager, who was present in the control room during a majority of the power

reduction.

The power reduction was completed without incident, and Unit 2 was

returned to full power on December 7.

C.

Conclusion

The December 5, 1996, power reduction at Unit 2 for the removal of the B FWP

was completed in accordance

with approved procedures.

The pre-evolution briefing

was thorough, with an appropriate

level of detail for the plant conditions; discussion

by the operators indicated a thorough understanding

of the upcoming evolution.

01.3

Unit 2 Missed UFSAR-Re uired CRD Housin

Su

ort Ga

Ins ections

a I

Ins ection Sco

e

On December 19, the licensee commenced

a shutdown of Unit 2'from 100%

power, as required by technical specification (TS) 3.1.3.8, due to a failure to

perform an UFSAR-required gap inspection of the CRD housing supports (commonly

referred to as>the "shoot-out steel" ). Unit 2 was shutdown and the required

inspections were completed; adjustments

were made to restore the CRD housing

support gap back within specification; and Unit 2 was subsequently

restarted.

The inspectors reviewed the applicable deviation event/reports

(DERs), engineering

supporting analysis, UFSAR sections, TS and plant procedures.

The inspectors also

observed portions of the plant shutdown; visually inspected the CRD housing

support; and reviewed the gap inspection results.

b.. Observations

and Findin s

n

As part of the corrective actions associated

with a previous event, NMPC was

conducting

a review of the UFSAR to validate that necessary

programs and

procedures'were

in place

The review identified that the UFSAR requirement to

inspect the CRD housing support after reinstallation, with particular attention to

maintaining the correct gap between the CRD flange and the housing support, was

not contained in the Unit 2 procedures;

and thus, had not been performed since

initial startup.

The CRD housing supports prevent a significant nuclear transient in the event a

drive housing breaks or separates

from the bottom of the reactor vessel

~ Unit 2 TS 4.1.3.8, "Control Rod Drive Housing Support," requires

a visual inspection to

ensure that the CRD housing support is in place following disassembly.

However,

UFSAR Section 4.6.3.2 states:

"When the support structure is reinstalled, it is

inspected for correct assembly with particular attention to maintaining the correct

gap between the CRD flange lower contact surface and the grid." The gap, as

described

in the UFSAR, Section 4.6.1.2.3, is approximately 1-inch between the

contact surface of the CRD flange and the support grid. This gap allows the CRD

housing support to accomplish its intended function, while providing sufficient

0

clearance to prevent contact stresses

caused by theimal expansion.

Although the

TS-required visual inspections of the CRD support housing were being performed,

the gap w'as not verified to be acceptable.

On December 19, 1996, while Unit 2 was operating at 100% power, NMPC notified

the NRC in accordance

with Title 10 of the Code of Federal Regulations

(CFR),

Part 50.72, that a shutdown of Unit 2 had commenced

in accordance

with TS 3.1.3.8, due to a failure to perform a UFSAR-required inspection.

The failure to

perform the required gap inspections placed the unit in a potentially unanalyzed

condition.

The inspectors observed portions of the plant shutdown and determined

it to be performed in accordance

with Procedure

N2-OP-101C, "Plant Shutdown,"

Revision 11.

While shutdown, the licensee inspected the CRD housing support gap in accordance

with Work Order (WO) 96-16814-00.

They identified that 19 of the 185 CRDs had

gaps that were slightly outside the vendor

recommended

tolerance of 1 inch 2

0.12 inches.

The smallest measured

gap was 0.828 inches, and the largest gap

was 1.190 inches.

The gaps on all CRDs were adjusted back within tolerance.

Unit 2 was restarted on December 23 and the unit achieved full power on

December 26.

Subsequent

to the plant restart, the licensee completed

an

engineering

analysis and determined that the CRD housing support had always been

operable.

This analysis was supported

by General Electric (GE) analysis, and

evaluated both extremes of the as-found inspection results.

Specifically, the largest

gap would not have resulted in an impact load on the housing support that would

exceed the allowable stress.

Therefore, the support would have prevented

any

significant nuclear transient in the event a drive housing broke or separated

from the

bottom of the reactor vessel.

Additionally', the smallest gap still provided sufficient

clearance to prevent contact stresses

caused by thermal expansion.

The licensee

changed

Procedure

N2-MMP-RDS-670, "CRD Support Steel Removal 5 Installation,"

'evision

02, to ensure proper gap verification'would be performed in the future.

The inspectors performed an independent

visual inspection of the CRD housing

support.

The inspe'ctor also reviewed the method used by the licensee to verify the

gap between'the

CRD and the housing support.

No concerns. were identified. The

inspectors'also

reviewed the NMPC engineeiing analysis and the GE supporting

analysis and considered them technically sound.

However, the failure to include the

UFSAR-required CRD housing support gap verification in plant procedures

is a

violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures,

and

Drawings."

This licensee-identified

and corrected violation is being treated as a

Non-Cited Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.

The Unit 1 UFSAR also refers to a 1-inch gap for the CRD support housing;

however, no verification was required.

Previous maintenance

activities at Unit 1

had not required adjustment of the CRD housing support nuts (the nuts used to set

the gap); therefore, NMPC determined that the original gap was maintained.

After

the end of this inspection period, Unit 1 inspected the CRD housing support gaps

during Forced Outage 97-01 (January

17 through 19, 1997).

All gaps were found

within tolerance.

Unit 1 was still evaluating changes to their procedures to ensure

future gap verification.

C.

Conclusion

07

Upon identification of the missed UFSAR-required CRD housing support gap

verification, NMPC shut down Unit 2. The licensee demonstrated

a good safety

perspective

by shutting down the unit instead of attempting to perform an

engineering

evaluation to justify continued operation. 'he licensee's

inspection

revealed out-of-tolerance

gaps on 19 of 185 CRDs.

Their engineering

analysis,

which determined that the out-of-tolerance

gaps did not affect the operability of the

system, was considered technically sound,

Subsequent

changes to the applicable

procedure were adequate to ensure the future gap verification.

Quality Assurance in Operations (71707, 40500)

07.1

Unit 1 Housekee

in

at

Ins ection Sco

e

hc

On November 29, 1996, the inspectors toured Unit 1 reactor and turbine buildings.

Several housekeeping

discrepancies

were identified. The inspectors reviewed the

applicable plant procedures

and discussed

the issues with the Station Shift

Supervisor (SSS) and Unit 1 management.

b.

Observations

and Findin s

Inade uate Control of Forei

n Material Exclusion

FME Areas on the Refuel Floor

During a tour of the Unit 1 refuel floor, the inspectors noted

a large yellow

polyethylene

(poly) bag located approximately one foot from the edge of the spent

fuel pool (SFP).

FME controls were in effect surrounding the SFP.

The bag was

open and contained smaller yellow bags, tags, and trash.

There was no indication

that any contents of the bag fell into the SFP.

No activity was in progress

on the

refuel floor. However, recent activities included new fuel inspection and movement

of n'w fuel bundles into the SFP.

At the time, the area surrounding the SFP was being controlled as a Level 2

cleanliness

local work zone and posted as such.

An FME Material Accountability

Log was present on the refuel floor. The inspectors reviewed the log for the area

surrounding the SFP; however, no log entry for the bag was identified.

The

inspectors informed an operator performing rounds of the poly bag, who then

notified radiation protection

(RP) personnel

and the SSS.

RP directed the operator

to remove the bag and contents from within the FME boundary.

The inspectors discussed

the concern with the Reactor Engineering Supervisor.

The

supervisor stated that the bag originated from work on the refueling bridge.

The

bag had been appropriately recorded

in the Material Accountability Log for. the

0

refueling bridge, and logged out upon removal

~ The inspectors confirmed the log

entries.

The technician who removed the bag from the refueling bridge, however,

placed it within the FME boundary for the SFP area, without logging the bag into

that area.

Although the area surrounding the SFP was conspicuously

posted, the

technician stated he was unaware of this area being FME controlled.

NMPC Procedure

GAP-HSC-02, "Local Work Zones and System Cleanliness

Controls," Revision 05, establishes

administrative controls for maintaining local

work zones.

Section 3 4.3 of GAP-HSC-02 requires

a Material Accountability Log

,to ensure material accountability within Level 1, 2 and 3 work zones.

Plant

management

re-emphasized

the importance of FME controls with the staff.

However, the failure to adhere to Procedure

GAP-HSC-02 is a violation of TS 6.8.1

regarding procedures.

This failure constitutes

a violation of minor'significance and

is being treated as a Non-Cited Violation, consistent with Section IV of the NRC

Enforcement Policy.

Re etitive Occurrence of Unsecured

Ladders Ad'acent to Safet -Related

E ui ment

Unsecured

ladders have been occasionally identified in both units by NRC

inspectors.

In Unit 1, the inspectors discovered unsecured

10-foot A-frame ladders

adjacent to safety-related

components,

such as hydraulic control units and scram

discharge volume vent and drain valves (on August 28, 1996) and containment

spray pump ¹121 (on October 2, 1996).

On November 14, 1996, the inspectors

identified an unsecured

ladder adjacent to the operating feedwater pump.

Although

not safety-related, the feedwater pumps are used for high pressure coolant

injection. The ladders were not in use at the time of discovery, nor. did it appear that

any activity had recently taken place.

On November 29, 1996, the inspectors observed

a 10-foot A-frame ladder adjacent

to the ¹15 reactor recirculation pump (RRP) motor generator

(MG) set.

Although

the RRP MG set is not safety-related,

damage to the MG set would potentially result

in an unanticipated

plant transient.

The inspectors discussed

the issue with the SSS and Plant Manager.

In each case,

actions were taken by the licensee to secure the ladders.

Conclusions

Due to personnel inattention to postings, material accountability controls were

violated on the Unit 1 refuel floor in that an open poly bag was left inside the FME

area arou'nd the SFP.

Also, after use, ladders were occasionally left unsecured

in

the vicinity of safety-related

and other important equipment.

The ladders falling

could potentially render necessary

emergency equipment unavailable or cause

a

plant transient.

The licensee took appropriate corrective action for the

. discrepancies

identified during this inspection.

The above examples were identified by the NRC. The recurring failure to properly

store material is indicative of weak management

oversight with respect to housekeeping.

t

,

7

08

Miscellaneous Operations Issues (90712)

/

0~.1

0 en

LER 50-220 96-11:

Reactor Scram Caused

b

the Main Generator Lockout

~Rela

Tri

The inspectors reviewed the subject Licensee Event Report (LER) and determined

that it satisfactorily described the event.

However, the assessment

of the root

cause analysis and corrective actions will remain open pending the enforcement

conference

related to the reactor overfill event associated

with the reactor scram.

A detailed. review of the issues detailed in this LER is contained

in NRC Inspection

Report 50-220/96-13, Section 02.3.

II. MAINTENANCE

'1

Conduct of Maintenance (61726, 62707)

M1.1

General Comments

/

Using NRC Inspection Procedures

61726 and 62707, the inspectors periodically

'bserved the licensee perform plant maintenance

activities and conduct various

surveillance tests.

In general, maintenance

and surveillance activities were

conducted

professionally, with the WOs and necessary

proceduies

in use at the

work site, and with the appropriate focus on safety.

Specific activities and

- observations

are detailed below.

The inspectors reviewed procedures

and/or

observed

portions of the following maintenance/surveillance

activities:

~ WO-93-31 1 9-00

~ N2-EPM-GEN-5Y555

~ N1-ST-Q8

~ N1-OP-12

~ N1-ST-M1

~ N1-0DP-IIT-01 01

~ N1-0DP-IIT-01 02

~ N1-ITP-01

~ N1-ITP-02

~ N2-MMP-RDS-670

Repair parallel interlock

GE 13.8 kV [kilo-Volt]'Magna-Blast Breaker and

Associated Motors

. Liquid Poison Pump and Check Valve Operability Test

Liquid Poison Sy'tem

Liquid Poison Pumps Operability Test

Establishment of IST [Inservice Testing] Pump and

Valve Acceptance Criteria

Analysis and Trending of IST Results

Ultrasonic. Flow Test

Vibration Measurement

CRD Support Steel Removal 5 Installation

Surveillance activities are Included under "Maintenance."

For exampie, a section involving surveillance observations might

be Included as a separate sub-topic under M1, "Conduct of Maintenance."

8

Unit 1 Li uid Poison Pum

and Check Valve 0 erabilit

Surveillance Test

!ns ection Sco

e

On December 30, 1996, Unit

1 Operations

and Inservice Test (IST) personnel

performed

a quarterly surveillance test of the liquid poison system to verify the

operability of the pumps and associated

discharge check valves.

The inspectors

reviewed applicable licensee procedures

and TSs; observed equipment setup and

testing for one train of,the system; reviewed completed surveillance tests

conducted within the last year; and discussed

the surveillance test results with the

Assistant SSS (ASSS) and IST Supervisor.

Observations

and Findin s

The inspectors observed the surveillance test locally in the reactor building.

Face-

to-face and remote communications were very good and the transfer of information

. went well ~ The inspectors noted good control of'valve manipulations,

and

independent

verifications were adequately performed.

Operator knowledge

regarding certain procedural steps and anticipated system response

appeared

adequate.

The IST technician appeared

very knowledgeable with respect to test

equipment installation and operation.

All test equipment was within current

calibration cycle.

The inspectors verified proper system restoration upon completion

of the surveillance test.

The inspectors reviewed the completed surveillance test procedure.

The test results

received a timely review and evaluation by the ASSS.

The recorded data was

complete and within allowable specification.'owever,

the licensee identified that

one vibrational data point on pump ¹12 was in the "Alert Range."

Although the

pump was still operable,

an increased surveillance'requency

was instituted, in

accordance with NMPC Procedure

N1-ODP-IIT-0101, based upon American Society

of Mechanical Engineers

Code,Section XI requirements.

The inspectors reviewed prior surveillances

and noted that liquid, poison pump ¹12

had exhibited similar vibration in July 1996.

Since July however, the pump

vibrational data had been in the acceptable

range.and

was taken off an increased

surveillance frequency in November 1996, in accordance

with the plant procedure.

The inspectors discussed

the ¹12 liquid porson pump vibration issue with the IST

supervisor, who stated that a definitive cause for the vibration was not known at

this time.

Conclusions

The inspectors observed

a quarterly surveillance test of the Unit 1 liquid poison

system; overall, the inspectors determined that the test was conducted

in a well

controlled manner.

Coordination and communications

between Operations and IST

personnel were very good.

Personnel

knowledge regarding the surveillance was

also good.

The surveillance test data received

a timely review.

Higher than normal

t

c

9

vibration identified on one pump was appropriately trended; although

a definitive

cause

had not yet been determined.

M1.3

Maintenance

Rule Evaluation of Unit 2 NonSafet -Related Switch ear-003

a.

Ins ection Sco

e

The inspectors observed

Unit 2 operators transfer a nonsafety-related

switchgear

(2NPS-SWG003) to the alternate power source in preparation for preventive and

corrective maintenance.

The inspectors evaluated the on-line maintenance

activities

with respect to the Unit 2 Maintenance

Rule Procedures.

The inspectors reviewed

portions of applicable plant procedures,

the WO and holdouts.

(A holdout is a

component tagging process

used to provide protection for personnel

and/or

equipment during operation, maintenance

and modification activities, which is

commonly referred to as tagout within the industry.)

b.

Observations

and Findin s

On January 3, 1997, Unit 2 performed preventive and corrective maintenance

on

circuit breaker 2NPS-SWG003-14, the 13.8 kilovolt (kV) normal feed to nonsafety-

related switchgear 2NPS-SWG003.

Switchgear SWG003 provides power to large

balance-of-plant

loads, including one FWP, three circulating water pumps,

a

condensate

pump and a booster pump, and several nonsafety-related

load centers.

Loss of this equipment could potentially result in a plant scram.

The inspectors observed the pre-evolution brief, and considered the review of

operator actions in the event of a loss of switchgear SWG003 to be appropriate.

The inspectors observed the transfer of switchgear SWG003 to its alternate power

source.

The transfer was completed in accordance

with Procedure

N2-OP-71A,

"13.8 kV AC [Alternating Current] Power Distribution," Revision 2. The WO and

holdout were developed

and approved

in accordance

with the appropriate

procedures.

After maintenance

was completed, switchgear SWG003 was returned

to its normal power source.

Discussions with the SSS indicated appropriate precautions were taken during the

preparation of the holdouts.

The inspectors verified that switchgear SWG003 was

appropriately contained

in the scope of Maintenance

Rule (10 CFR 50.65) and

controlled by Unit 2 Procedure

N2-MRM-REL-0104, "Maintenance

Rule Scope,"

Revision 00.

Discussions with the SSS indicated that Unit 2 appropriately evaluated

the risk associated

with the transfer for switchgear SWG003.

c.

Conclusion

Unit 2 appropriately included nonsafety-related

switchgear SWG003 within the

scope of the Maintenance

Rule, and evaluated the risk associated, with on-line

maintenance

for the switchgear.

t

~

10

III. ENGINEERING

E2

Engineering Suppo< of Facilities and Equipment (37551, 40500)

E2.1

Hot Shorts Vulnerabilit

of Unit 2 Shutdown Coolin

Valves

a0

Ins ection Sco

e

On December 17, 1996, NMPC notified the NRC that Unit 2 was potentially outside

the design basis for 10 CFR Part 50, Appendix R, with respect to shutdown cooling.

A hot short condition could have caused motor operated valves (MOVs) in the

.

residUal heat removal (RHR) system to be driven closed and mechanically damaged,

preventing remote shutdown capability.

The inspectors reviewed the applicable

DER, engineering supporting analysis, and NRC Information Notice 92-18, "Potential

for Loss of Remote Shutdown Capability during a Control Room Fire," and discussed

the issue with the Unit 2 design engineering

and operations staff. The inspectors

-also assessed

the adequacy of the licensee's short term corrective actions.

b.

Observations

and Findin s

During review of a Unit 1 issue related to Appendix R fire-induced hot shorts in

MOVs, NMPC design engineering staff discovered

a similar concern at Unit 2.

In

particular, several MOVs were susceptible to mechanical damage if the hot short

bypassed

the torque switch causing spurious operation and a valve stall condition.

The concern was applicable to 32 of 45 MOVs that would be controlled at the

remote shutdown panel during a control room fire, Appendix R shutdown.

Of the

32 susceptible

MOVs, 28 were part of redundant trains.

Thus, failure of one

redundant MOV would not prevent remote shutdown capability.

However, four

MOVs were determined not to have adequate

redundancy.

The four valves (2RHS" MOV112, 113, 142, and 149) determined to be susceptible

were documented

on DER 2-96-3379, and the licensee made a 1-hour notification

to the NRC in accordance with 10 CFR 50.72.

As. part of their immediate corrective

actions, NMPC closed three of the valves (RHS" MOV112, 142 and 149) and

disconnected

the valves from the power supply such that a control room fire could

not damage these valves and disable. the safe shutdown function.

The fourth valve

(RHS" MOV113) is normally closed and de-energized

to preclude

a fire-induced loss-

of-coolant accident (LOCA) at the high/low pressure interface location.

MOVs 112 and 113 are isolation valves in the RHR suction path for the shutdown

cooling mode, and are required for plant cold shutdown from the control room or

the remote shutdown panel.

MOVs 142 and 149, RHR discharge to radiological

waste isolation valves, are required'to be operable from the remote shutdown panel

prior to and after initiation of RHR system shutdown cooling mode to flush the

stagnant water in the shutdown cooling piping.

Valves

RHS "MOV112, 142, and 149 are normally closed.

Procedural controls were

established,

through the use of a holdout, to preclude spurious operation of the

r

11

valves and possible mechanical damage.

The inspectors verified that the valves

were deenergized,

and that the appropriate procedural controls were in place.

This

remains an unresolved

item pending the completion of the licensee's

analysis and

subsequent

NRC review.

(URI 50-410/96-14-01)

c.

Conclusions

The licensee's identification and immediate corrective actions to address three

shutdown cooling valves potentially susceptible to damage during a 10 CFR 50

Appendix R fire-induced hot short condition were appropriate.

E2.2

Potential Over ressurization

Concerns

Relative to NRC Generic Letter 96-06

a.

Ins ection Sco

e

~ NMPC engineering staff's preliminary evaluations of NRC Generic Letter (GL) 96-06,

"Assurance of Equipment Operability and Containment Integrity during Design-Basis

Accident Conditions," identified specific piping that could potentially be

overpressurized

during a design-basis

LOCA. The overpressure

conditions could

result in piping exceeding the allowable stresses

in several systems; the following

drywell penetrations

have been identified by NMPC:

~ core spray high point vent lines (Unit 1)

~ post-accident

sampling line (Unit 1)

~ shutdown cooling system lines (Unit 1)

~ drywell equipment and floor drain lines (Unit 1)

~ drywell unit cooler lines (Unit 2)

~ reactor recirculation pump seal cooler lines (Unit 2)

As a result, NMPC determined that both units were potentially outside the design

basis and notified the NRC in accordance

with 10 CFR 50.72., To determine the

adequacy of the licensee's

immediate corrective actions, the inspectors reviewed

the applicable DERs, engineering supporting analyses

and GL 96-06, and discussed

the concerns with NMPC engineering

and operations

personnel.

b.

Observations

and Findin s

Unit 1

Unit 1 engineering staff determined that the core spray (CS) high point vent lines

and the post-accident

sampling (PAS) line could potentially overpressurize

and

exceed allowable stresses

during a design basis'OCA.

During a design basis

LOCA, the potential existed for water trapped between the containment isolation

valves (CIVs) to heat up and thermally expand, to the point where piping integrity

was not assured.

On December 13, 1996, NMPC notified the NRC, in accordance

with 10 CFR 50.72, that Unit 1 was potentially in a condition outside the design basis.

NMPC

~

~

12

additionally'issued

DER 1-96-3350 to internally document the concern.

NMPC

considered

both the CS and PAS systems operable, through use of administrative

controls.

Specially, the piping between the CIVs for both systems was drained

every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to maintain an adequate

expansion volume.

NMPC determined that following a postulated

design basis LOCA, the thermal

expansion of the fluid'trapped between the normally closed shutdown cooling.(SDC)

CIVs could potentially result in internal pressure

exceeding

allowable stresses.

The

fluid temperatures

within the SDC piping penetrations

were "hot" as a result of

valve seat and packing leakage.

NMPC's preliminary engineering

evaluation

determined that the already elevated'fluid temperature would reduce the net thermal

expansion

during a design basis LOCA, such that the peak pressure was within the

design basis rating for the pipe.

NMPC design engineering

analyses identified potential overpressure

concerns

associated

with the lines for the drywell equipment drains (DWED) and drywell floor

drains (DWFD). The DWED and DWFD inside and outside CIVs were normally open

and the piping not normally filled with water.

However, the piping would contain

water during pump-down oper'ations.

During the design basis LOCA, the CIVs

would automatically close and could potentially trap water between the CIVs.

Thermal expansion of the trapped fluid could potentially exceed allowable internal

stresses

for the pipes.

Based on the design of the DWED and DWFD outboard

CIVs, NMPC preliminarily determined that the valve disc would unseat at

approximately 150 pounds per square inch (psi), thus providing pressure

relief to

maintain the piping within design basis pressure.

P

On December 20, 1996, NMPC notified the NRC, in accordance

with 10 CFR 50.72, that Unit 1 was potentially in a condition outside the design basis.

NMPC

issued

DER 1-96-3419 to internally document the concern.

Both the SDC and

DWED/DWFD systems were. considered

operable based upon present system

configuration.

The potential overpressure

conditions identified at Unit 1 during the licensee's

review of GL 96-06 remains an unresolved item pending the completion of the

.

NMPC's.evaluation to determine if this condition was outside the design basis and

subsequent

NRC review.

(URI 50-220/96-14-02)

Unit 2

NMPC identified four penetrations

at Unit 2 that could potentially exceed the design

pressure

during an accident due to thermal expansion of entrapped water between

the inboard and outboard CIVs. The penetrations

allow reactor building closed loop

cooling (RBCLC) water to flow into and out of the drywell for drywell unit coolers

and reactor recirculation pump seal coolers.

NMPC documented

the concern in DER

2-96-3427.

On December 20, 1996, NMPC notified the NRC on the condition in

accordance

with 10 CFR 50.72.

13

The engineering

supporting analysis associated

with the DER 2-96-3427 based

continued operability of the equipment on projected valve leakage.

With leakage

considered,

the calculated maximum pressure

expected

during thermal expansion

would not exceed the allowed pressures.

The inspectors reviewed the engineering

analysis and deemed the basis for operability to be consistent with guidance

provided in GL 96-06.

However, this item remains unresolved

pending the

completion of NMPC's evaluation to determine ifthis condition was outside the

design basis and subsequent

NRC review.

(URI 50-410/96-14-02)

C.

Conclusions

NMPC appropriately notified the NRC in accordance

with 10 CFR 50.72 of potential

conditions outside design basis identified during their review of GL 96-06.

The

licensee's review identified several drywell penetrations

at both units that could

potentially exceed the design pressure

during an accident due to thermal expansion

of entrapped

water.

The inspectors determined that the operability determinations

were adequate

and in accordance

with the guidance provided in GL 96-06.

The

operability determinations for the Unit 1 CS high point vent and PAS lines were

particularly appropriate

and conservative.

ES

Miscellaneous Engineering Issues (90712, 92700, 92903)

E8.1

Closed

LER 50-220 96-09:

Potential Overstressed

Pi

e Su

orts Caused

b

Desi

n Deficienc

Ins ection Sco

e

The inspectors reviewed the Unit 1 voluntary LER related to the potential for reactor

building closed loop cooling (RBCLC) system pipe supports within containment to be

overstressed

in the event of a LOCA coincident with a loss of offsite power (LOOP).

The inspectors discussed

the issue and conclusions with Unit 1 Engineering

management

and staff, and evaluated the licensee's root cause determination and

corrective actions.

b.

Observations

and Findin s

On October 21, 1996, during the review of an engineering

analysis related to the

RBCLC system pipe supports,

Unit 1 plant management

determined that the

supports within containment could be overstressed

in the 'event of a LOCA

coincident with a LOOP. The deficiency was identified as the result of an

engineering

evaluation performed in response to similar industry operating

experience

(a LER issued by Haddam Neck Nuclear Station on July 22, 1996).

The

performance of the engineering

evaluation appeared

prudent.

The licensee determined that, in the event of a LOCA with a LOOP, the temperature

of the RBCLC water and piping within containment could increase before power and

flow were restored, resulting in thermally induced longitudinal expansion

and

potential overstressing

and failure of some U-bolt supports.

Ho'wever, the licensee

determined that this deficiency did not result in a significant safety concern as the

piping would remain intact and operable even considering

a subsequent

seismic

event.

The licensee also determined that the plant was not in a condition outside

the design basis.

Particularly, the engineering evaluation determined that the design

basis load combinations for RBCLC, as described

in the UFSAR, did not address

accident loads because

the system was not safety-related.

However, good

engineering practice would have included the accident loads, particularly thermal

stresses

resulting from accident conditions.

The licensee evaluated the RBCLC piping inside containment and identified thirteen

8-inch piping supports

and thirteen 4-inch piping supports requiring modification.

Work requests for repair and/or modification were generated

and added to the work

scope for Refueling Outage

(RFO) 14, scheduled for March 1997.

The inspectors discussed

the LER with the Engineering Manager and a structural

engineer.

NMPC issued the voluntary LER due to the generic implications of the

situation, which was similar'to that discussed

in GL 96-06.

The L'ER satisfactorily

described the event.

The causes

and the corrective actions are detailed and

appropriate.

The inspectors

had no further questions.

c.

Conclusions

The licensee'performed

an engineering evaluation of Unit 1 in response to industry

operating experience

and determined that RBCLC system pipe supports within

containment could be overstressed

in the event of a LOCA coincident with a LOOP;

performance of the engineering

evaluation appeared

warranted and prudent.

The

root cause evaluation and corrective actions to prevent similar occurrence

were

appropriate.

E8.2

Closed

S ecial Re ort:

Ino erabilit

of Unit 1 ¹11 Containment

H dro en

Monitorin

S stem

On November 14, 1996, with Unit 1 operating at 100% reactor power, ¹11

Containment Hydrogen Monitoring System (HMS) was removed from service for

calibration.

During the calibration, a toggle switch failed, delaying completion of the

surveillance until the switch was replaced.

The ¹12 HMS was operable

and in

calibration.

The ¹11 HMS was returned to an operable status on November 16

following toggle switch replacement

and system calibration.

NMPC initiated DER 1-96-3100 to evaluate the toggle switch failure and to

determined corrective actions.

NMPC concluded that frequent use of the toggle

switch resulted in mechanical failure. The toggle switch was a momentary contact,

spring return switch, actuated extensively during monthly calibrations, and did not

impact the safety-related function of the system.

The inspectors'iscussion

with

the system engineer indicated that the associated

toggle switches were recently

installed as part of a modification during RFO13 in 1995.

E

15

Within the past year, numerous toggle switches of this type have failed and were

subsequently

replaced.

NMPC was evaluating the availability of replacement

switches of different design.

NMPC will continue to monitor toggle switch

performance

and replace failed switches, as required.

The licensee found a different

design switch which was being evaluated

as a replacement; they intend to replace

the balance of the switches in the near future.

In addition, NMPC is reviewing the

repetitive failures of the toggle switches for possible 10 CFR 21 reporting

consideration.

NMPC submitted

a special report to the NRC within 14 days, as required by Unit 1

TS 3.6.11-1, Action Statement Table 3.6.11-2 (4a).

The inspectors reviewed the

special report and confirmed that all required information was provided.

Closed

URI 50-220 95-25-81:

Emer enc

Coolin

S stem Material Deficiencies

Ins ection Sco

e

In January 1996, NRC resident inspectors performed

a walkdown of all accessible

areas of the Unit '1 emergency cooling (EC) system and identified two material

condition concerns.

Specifically, several

EC system drain valve packing gland nuts

appeared

to have insufficient thread engagement;

and secondly, supports for the

fire water header connection to the ¹11 EC makeup tank appeared to exceed the

maximum allowable span between supports permitted by NMPC internal standards.

0

The inspectors reviewed the licensee

DERs to assess

corrective actions and

discussed

the results with members of the engineering staff.

Observations

and Findin s

Packin

Gland Nut Thread En

a ement

NMPC documented

the packing gland nut thread engagement

issue on DER 1-96-

0130.

NMPC Standard

Design Specification Procedure,

SDS-006, "Bolt-Torque

Requirements for Unit 1 and Unit 2," Revision 1, provided general guidance for

'hread

engagement.

However, in practice, NMPC did not apply this requirement to

packing gland nuts, even though there was no exception stated within the

procedure.

Maintenance staff were trained to adjust packing so that a valve could

be operated without binding and no packing leakage existed.

NMPC stated that

vendor manuals could be used as guidance, but most vendor manuals did not

specifically address

packing gland nut thread engagement.

Procedure SDS-006, Section 6.1.C, stated that " ..

~ the minimum thread

engagement

for a fastener will be one thread beyond the top of the nut,... [and

that for] any fasteners that do'not obtain thread engagement

greater than one

thread beyond the top of the nut, approval by design engineering

is required."

The

failure to follow Procedure SDS-006, is a violation of TS 6.8.1 regarding procedural

adherence.

This failure constitutes

a violation of minor significance and is being

16

treated as a Non-Cited Violation, consistent with Section IV of the NRC

Enforcement Policy.

NMPC discussed

the packing gland thread engagement

concern with vendors and

other licensees,

and concluded that good maintenance

practice was to ensure

one

thread visible beyond the nut.

SDS-006 was revised to reinforce compliance with

Section 6.1.C. with respect to packing gland nut thread engagement.

Packing

gland nuts currently with insufficient thread engagement

were to be evaluated for

operability on a case-by-case

basis.

Fire Water Header Pi in

Su

orts to ¹11 EC Makeu

Tank

gl

C.

NMPC issued

DER 1-96-0102 to document the potential operability concern

regarding the lack of fire water header piping supports to ¹11

EC makeup tank.

Design Engineering determined that the supports for ¹11

EC makeup tank fire water

supply were adequate for the applied loading and for system operability; however,

a

support was added mid-span as a system enhancement.

The inspectors verified the

support installation and that the engineering drawing represented

the current plant

configuration.

Conclusions

NMPC evaluation and corrective actions to NRC-identified EC system discrepancies

appeared

appropriate..However,

the failure to implement technical guidance to

ensure adequate

valve packing gland nut thread engagement

was a violation of

procedures.

ESA

Closed

URI 50-410 95-12-01:

Tem orar

Scaffoldin

Erected Around Unit 2

Li uid Poison Tank for Extended

Period with no En'neerin

Evaluation

ar

Ins ection Sco

e

In April 1995, during an inspection of the Unit 2 reactor building, the inspectors

identified that the temporary scaffolding around the standby liquid control (SLC)

storage tank did not appear to have been inspected recently.

In addition, the

inspectors questioned

whether an engineering

analysis had been performed

considering the potential safety risk associated

with temporary scaffolding near

safety-related

equipment.

The. Unit 2 Independent

Safety Engineering Group (ISEG)

initiated an investigation after the inspectors

raised the concern.

b.

Observations

and Fihdin s

The inspectors reviewed the associated

ISEG report, dated May 15, 1995.

The

report identified that the attached scaffold tag (¹93-231) indicated the scaffold had

been erected or last inspected sometime in 1993.

Also, ISEG noted that no analysis

had ever been performed.

Scaffold Procedure

N2-MAP-MAI-0301, required an

evaluation of scaffolds in safety-related

areas that were installed for greater than

~

'

17

60 days.

The ISEG report stated that the scaffold was scheduled to be replaced

with a permanent structure by August 31, 1995, in accordance

with a simple

design change

(SDC 2-0398-91).

The ISEG concluded that the engineering

evaluation should have been performed when it was recognized that the scaffold

was to be installed for long term.

The licensee initiated a DER (2-95-2093) after the NRC identified the issue.

NMPC

determined the root cause to be a combination of factors:

inadequate

procedure

adherence;

engineering judgement used in lieu of calculation; management

did not

budget resources

after approving the design change;

and engineering

did not

properly disposition

a May 1992 DER (2-92-2132).,

DER 2-95-2093 also noted that

a modification was requested

in September

1986 to install a permanent

ladder and

platform over the SLC tank, and that the temporary scaffolding was initially installed

in September

1989.

Immediate corrective actions included a seismic evaluation of the scaffolding until

the permanent structure could be installed.

NMPC reviewed all iristalled scaffolds

and identified two others that exceeded

the 60-day requirement;

one at Unit 1 and

another at Unit 2. Both were evaluated for seismic considerations

and found

acceptable.

Actions to preclude recurrence included a review of the associated

maintenance

and engineering procedures,

and emphasis

on procedural adherence.

The inspectors verified that the scaffolding around the SLC tank had been replaced

with a permanent

ladder and work platform.

However, the failure to perform

evaluations of scaffolding erected for greater than 60 days is a violatio'n of Unit 2

Procedure N2-MAP-MAI-0301, Section 5:5.1b.

This failure constitutes

a violation

of minor significance and is being treated as a Non-Cited Violation, consistent with

Section IV of the NRC Enforcement Policy.

c.

Conclusion

The failure to follow plant procedures

resulted in the installation of temporary

scaffolding'around the Unit 2 SLC tank for an extended

period without proper

engineering

analysis.

IV. PLANT SUPPORT

using Inspection Procedure 71750, the inspectors routinely monitored the

performance of activities related to the areas of radiological controls, chemistry,

emergency preparedness,

s'ecurity, and fire protection.

Minor deficiencies were

discussed with the appropriate management,

significant observations

are detailed

below,

4

0

0'

18

Staff Knowledge and Performance in Radiological Protection (71750)

Re eat Failure to Pro erl

Secure

a Unit 1 Hi h Radiation Area Gate

Ins ection Sco

e

At the end of the previous inspection period, the inspectors toured the Unit 1

turbine building and identified that the gate to the turbine deck, a posted high

radiation area, was unlatched.

The inspectors continued inspection of this issue

during this inspection period.

The issue was discussed

with the SSS,

RP

supervision, the Operations Manager, and the Plant Manager.

Observations

and Findin s

On November 29, 1996, the inspectors identified that on the 300 foot elevation. of

the turbine building, the east gate to the turbine deck was not properly latched

and locked, allowing access to the turbine deck and adlacent reheater rooms,

During power operations, the gates to the turbine deck are normally locked and

posted

as "High Radiation Areas." RP and the SSS were notified and the gate was

subsequentlpshut

and latched.

NMPC initiated DER.1-96-3217 to address the

issue.

Reactor power at the time was 100%.

Subsequent

radiation surveys

indicated the highest localized radiation levels (measured

at 30 centimeters) were

approximately 300 millirem/hour (mrem/hr) on the turbine deck and 800 mrem/hr in

the reheater rooms.

The highest on contact readings were 380 mrem/hr and 1000

mrem/hr on the turbine deck and in the reheater rooms, respectively.

Previously, on September

17, 1996, the inspectors identified the same gate not

properly latched and locked.

Subsequently,

and only following further discussion

with the inspectors,

NMPC initiated DER 1-96-2301

on September

27 to address

the issue.

NMPC noted the apparent

cause

as inadequate

work practices,

in that

personnel failed to verify gate closure.

The corrective actions were to (1) counsel

shift personnel with regard to ensuring lockable barriers remained latched, and (2)

repair the gate, which had considerable

"play" and was known to not always latch

upon closure:

The Plant Manager and RP Manager informed the inspectors that the gate being

unlatched did not meet their expectations.

The inspectors

noted that corrective

actions to the September

17 event were ineffective, in that personnel

again failed to

verify proper gate latching upon exiting the area.

Subsequent

to the November 29

event, counselling of shift personnel was again conducted.

An already open work

order to repair the "play" in the gate was immediately initiated upon identifying the

repeat event.

NMPC Procedure

GAP-RPP-08, "Control of High, Locked High, and Very High

Radiation Areas," Revision 03, Section 3.1.3 states that "~.. when practicable, High

Radiation Areas should be locked."

Additionally, Section 3.6.1 requires personnel

to maintain positive access control to High, Locked High, and Very High Radiation

Areas.

The procedure specified that barriers are to remain closed and locked after

t

0'

19

each entry, and that the barriers be checked closed by shaking.

The failure to

ensure that the east gate to the Unit 1 turbine deck, a posted High Radiation Area,

remained locked was not in accordance

with Procedure

GAP-RPP-08 and is a

violation of Unit 1 TS 6.11.

TS 6.11 requires that written procedures

be approved,

maintained and adhered to for all operations involving personnel

radiation exposure.

(VIO 50-220/96-14-03)

c.

Conclusions

On two occasions,

the inspectors identified the same high radiation area access

gate to be unlocked.

The inspectors considered this a recurring failure of procedural

adherence

and attention to detail.

Furthermore, the corrective actions to the first

occurrence were ineffective.

V. MANAGEMENTMEETINGS

X1

Exit Meeting Summary

At periodic intervals, and at the conclusion of the inspection period, meetings were

held with senior station management to discuss the scope and findings of this

inspection,

The final exit meeting occurred on January 27, 1997.

Based on the

NRC Region

I review of this report, and discussions

'with NMPC representatives,

it

was determined that this report does not contain safeguards

or proprietary

information.

X3

Management Meeting Summary

On January 6, 1997, a meeting between the NRC and NMPC management

was held

at the NRC headquarters.

This meeting was requested

by NMPC to present their

bases for disagreeing with the Level IV violation regarding the failure to report the

condition of the Unit 1 blow out panels being outside the design basis when it was

identified in October 1993 (NRC Inspection Repo'it 50-220/96-05).

Results of this

meeting will be provided to NMPC in a separate

correspondence.

This meeting was

open to the public.

0'

'

ATTACHMENT

PARTIALLIST OF PERSONS CONTACTED

Nia ara Mohawk Power Cor oration

R. Abbott, Vice President & General Manager, Nuclear

J. Aldrich, Maintenance

Manager, Unit 1

M. Balduzzi, Operations Manager, Unit 1

D. Barcomb, Radiation Protection Manager, Unit 2

C. Beckham, Manager, Quality Assurance

.J. Burton, Director, ISEG

G. Correll, Chemistry Manager, Unit 1

J. Conway, Plant Manager, Unit 2

K. Dahlberg, General Manager, Projects

R. Dean, Engineering Manager, Unit.2

A. DeGracia, Work Control & Outage Manager, Unit 1

G. Helker, Work Control & Outage Manager, Unit 2

M. McCormick, Vice President, Nuclear Engineering

L. Pisano, Maintenance

Manager, Unit 2

N. Rademacher,

Plant Manager, Unit 1

R. Smith, Operations Manager, Unit 2 ~

P. Smalley, Radiation Protection Manager, Unit 1

K. Sweet, Technical Support Manager, Unit 1

R. Sylvia, Executive Vice President & Chief Nuclear Officer

C. Terry, Vice President,

Nuclear Safety Assessment

& Support

K. Ward, Technical Support Manager, Unit 2

C. Ware, Chemistry Manager, Unit 2

D. Wolniak, Manager, Licensing

W. Yaeger, Engineering Manager, Unit.1

INSPECTION PROCEDURES USED

- IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 90712:

IP 92700:

IP 92903:

On-Site Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

" Surveillance Observations

Maintenance

Observation

Plant Operations

Plant Support

In-Office Review of Written Reports of Nonroutine Events at Power

Reactor Facilities

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

Followup - Engineering

f

OPENED

50-41 0/96-1 4-01

50-220 5.

50-41 0/96-14-02

50-220/96-14-03

50-220/96-1

1

CLOSED

50-41 0/95-1 2-01

50-220/95-25-01

'0-220/96-09

UPDATED

None

ITEMS OPENED, CLOSED, AND UPDATED

URI,

Hot Shorts Vulnerability of Shutdown Cooling Valves

URI

Potential Overpressurization

Concerns

Relative to NRC Generic Letter 96-06

VIO

Repeat Failure to Properly Secure High Radiation Area Gate

LER

Reactor Scram Caused

by the Main Generator Lockout Relay

Tnp

URI

Temporary Scaffolding Erected Around Unit 2 Liquid Poison

Tank for'Extended

Period with no Engineering Evaluation

URI

Emergency Cooling System Material Deficiencies

LER

Potential Overstressed

Pipe Supports Caused

by Design

Deficiency

LIST OF ACRONYMS USED

ASSS

CFR

CIV

CRD

CS

DER

DWED

DWFD

EC

FME

FWP

GE

GL

HMS

ISEG

IST

kv

LER

LOCA

LOOP

MG

MOV

mrem/hr

NMPC

NRC

PAS

ps l

Assistant Station Shift Supervisor

Code of Federal Regulations

Containment Isolation Valve

Control Rod.Drive

Core Spray

Deviation/Event Report

Drywell Equipment Drains

Drywell Floor Drains

Emergency Cooling

Foreign Material Exclusion

Feedwater Pump

General Electric

Generic Letter

Hydrogen Monitoring System

Independent

Safety Engineering

Group

Inservice Testing

kilo-Volt

Licensee Event Report

Loss of Coolant Accident

Loss of Offsite Power

Motor Generator

Motor Operated Valve

millirem/hour

Niagara Mohawk Power Corporation

Nuclear Regulatory Commission

Post-Accident Sampling

pounds per square inch

'

RBCLC

RCS

RF0

RHR

RP

RRP

SDC

SFP

SLC

SSS

TS

UFSAR

URI

VIO

WO

Reactor Building Close Loop Cooling

Reactor Recirculation System

Refueling Outage

Residual Heat Removal

Radiation Protection

Reactor Recirculation Pump

Shutdown Cooling

Spent Fuel Pool

Standby Liquid Control

Station Shift Supervisor

Technical Specification

Updated Final Safety Analysis Report

Unresolved Item

Violation

Work Order