ML17058A673

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Insp Repts 50-220/91-02 & 50-410/91-02 on 910104-0215. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Protection & Surveillance & Maint
ML17058A673
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 03/07/1991
From: Meyer G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17058A672 List:
References
50-220-91-02, 50-220-91-2, 50-410-91-02, 50-410-91-2, NUDOCS 9103220147
Download: ML17058A673 (44)


See also: IR 05000220/1991002

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report Nos'.:

Docket Nos.:

50-220/91-02

50-410/91-02

50-220

50-410

DPR-63

License Nos.:

'PF-69

Licensee:

Niagara Mohawk Power Corporation

301 Plainfield Road

Syracuse,

New York 13212

Facility:

Location:

Dates:

Nine Mile Point, Units

1 and 2

Scriba, New York

January 4 through February 15, 1991

Inspectors:

W. A. Cook, Senior Resident Inspector

R. R. Temps, Resident Inspector

R. A. Laura, Resident Inspector

M. S. Miller, Reactor Engineer

N. S. Perry, Resident Inspector - Ginna

C. E. Sisco, Operations Engineer, DRS

D. J Vito, Proj

t Engineer, DRP

Approved by:

lenn W. Meyer, Chief

Reactor Projects Section N

. 1B

Date

2

Ins ection Summar:

This inspection report documents routine and reactive inspections during day and backshift hours

of activities

including:

plant

operations;

radiological

protection;

and

surveillance

and

maintenance.

~Result:

One violation was identified involving the improper procedure revision and implementation of

an Appendix J exemption at Unit 1.

One non-cited violation was identified at Unit 1 involving

improper setting of emergency

condenser

isolation setpoints.

One'non-cited

violation was

identified at Unit 2 involving surveillance testing of source range monitor rod block functions

during refueling.

Executive

ummar

'ine Mile Point Combined Inspection Report

Nos. 50-220/91-02 and 50-410/91-02

PLANTOPERATIONS: Operator performance at Unit 1 was satisfactory during this inspection

period.

Operator response

to the February 5, 1991 recirculation pump trip was good and their

prompt and conservative actions to minimize the pressure transients due to turbine control system

problems were observed to be satisfactory.

Unit 2 operator performance was also assessed

to

be satisfactory during this inspection period.

Outage completion and unit start-up activities were

observed, including special turbine testing, and operator command and control ofthese evolutions

was satisfactory.

Operations staff response

to the electro-hydraulic system leak on 1/23 was

good, particularly in rapidly reducing reactor power and securing steam to the condenser prior

to any automatic protective function actuations.

SURVEILLANCEAND MAINTENANCE: Various surveillance and maintenance activities

were observed

or reviewed

during this inspection

period

and

no specific problems

were

identified.

Actions at Unit

1 to address

Generic Letter 89-13 regarding service water system

issues were determined to be thorough and timely. Turbine torsion testing observed at Unit 2

was considered well planned and executed.

The inspectors identified a Non-Cited Violation after

review of the Unit 2 source range monitor rod block surveillance test Technical Specification

(TS) violation, in accordance with the NRC Enforcement Policy.

ENGINEERINGANDTECHNICALSUPPORT:

Several unresolved items were reviewed and

closed by the inspectors.

One unresolved

item involving the Unit

1 emergency

condenser

isolation setpoint TS violation (LER 90-22) was reviewed and the inspectors identified a Non-

Cited Violation. Inspector followup of an unresolved item involving the implementation of an

Appendix J exemption identified a violation ofprocedural revision and review requirements.

The

inadequate

procedure

revision

resulted

in conflicting operating

and

emergency

operating

procedures

and was evidence of a poor licensing staff and station staff interface.

A detailed review of the Unit 2 Safety Parameter

Display System (SPDS) modification was

conducted

and the inspector concluded

that Niagara Mohawk had satisfactorily addressed

the

Operating License Condition C. (8) requiring the SPDS to be operational following the first refuel

outage.

SECURITY AND SAFEGUARDS:

The inspectors

considered

the contingency plans and

heightened security measures

in response

to the increased threat of terrorist activities due to the

Persian Gulf War to be satisfactory.

0

DETAILS',0.

PLANT OPERATIONS

1.1

Unit 1

At the beginning of the report period, the Unit 1 reactor was in cold shutdown to repair main

steam

isolation valve (MSIV) 01-02

and

to identify and repair the

sources

which were

contributing to an increasing drywell leakage rate.

Repair of the MSIV 01-02 was discussed in

Inspection Report 50-220/90-10.

The unit restarted and the turbine synchronized to the grid on

January 9, 1991.

The

plant

ope'rated

at

power

until it automatically

scrammed

on

February

12, 1991, due to a pressure oscillation from a turbine control valve going partially

closed.

Based on the estimated repair time and other factors, the plant manager decided to enter

the mid-cycle surveillance ou'tage, originally scheduled

to commence on March 1, 1991

~

On February 11, 1991, the Region I Regional Administrator closed Confirmatory Action Letter

88-17, Supplement

1.

A.

Following repair of MSIV 01-02 and satisfactory post-maintenance

and local leak rate

testing,

the Unit

1

reactor

was

taken critical on January 9, 1991.

The generator

was

synchronized

to the grid'on the following day and

subsequently

increased

to full power.

Maintenance

repairs to correct drywell leakage

appeared

effective as evidenced

by the low

leakage rate observed following the startup (( 0.5 gpm).

B.

On February 5, 1991, the motor generator (MG) set for the 12 reactor recirculation pump

(RRP) tripped due to a ground.

This initiated a down-power transient on the plant.

Operators

responded

to the event, power was stabilized and later brought back up to 87%.

In three-loop

operation,

the unit Technical

Specifications

(TS) impose

a limit of 90%

reactor power.

Following repairs to the RRP MG set, the 12 RRP was restarted on February 7, 1991 and four-

loop operation recommenced.

The inspector determined that operator response to the event was

proper and the appropriate TS limits and procedure requirements for idling and restoring 12 loop

were followed.

Assessment of the repairs to the MG set are discussed in Section 2.1.A of this

report.

C.

On January 25, 1991, small power oscillations as a result of reactor pressure oscillations

were observed.

Reactor power was reduced slightly and the condition cleared.

Over the

following two days, the condition repeated itself intermittently. Initial troubleshooting efforts

focused on the low oil level for the turbine's hydraulic control system and speculation that this

was causing pressure surges in the hydraulic system. 'owever, once oil level was restored to

the normal range, the pressure oscillations still occurred.

On January 27, 1991, pressure control

was switched from the Electronic Pressure Regulator (EPR) over to the Mechanical Pressure

Regulator (MPR) to allow testing of the EPR.

The EPR was examined extensively and no

problems were found.

Additionally, a computerized

data acquisition system

was placed in

service to monitor and record for later analysis, various parameters

in case the oscillations

reoccured.

On February 7, 1991, while on the MPR, the oscillations occurred again.

Reactor power was

reduced and the condition stabilized.

Analyses of the data acquisition system's data indicated

that changes in hydraulic pressure were not the cause of the oscillations.

Also, the oscillations

occurred while on the MPR which indicated the oscillation problem was a result of common

elements downstream of the MPR or EPR.

The system engineer determined that the most likely

source of the problem was the torque tube, which is located in the front standard,

and controls

the turbine control valves position.

Additional data obtained by the data acquisition system on

control valve response

added credence to the belief that the problem was in the front standard.

Niagara Mohawk had

numerous

conversations

with the turbine vendor and

an expert in

mechanical hydraulic control systems was arranged to be sent to the site.

However, before the

vendor arrived on February 12, 1991, one of the control valves went rapidly to the 50% closed

position and then back to full open.

This induced a pressure

transient on the reactor which

caused reactor power to increase and the reactor to automatically scram as a result of the high

flux condition.

The plant shutdown,

as designed,

and a plant cooldown to cold shutdown was

initiated as a result of management's

decision to enter the mid-cycle outage early. The inspector

concluded that Niagara Mohawk was pursuing identification of the pressure surges in a timely

and conservative

fashion.

Additionally, operator response

to the automatic shutdown

was

satisfactory.

1.2

iinit2

r

During this inspection period the containment integrated leak rate test was performed, final

preparations for reactor startup from the first cycle refuel outage were made and the reactor was

taken critical on January

19, 1991

~

Augmented NRC coverage was provided by region based

inspectors during reactor startup.

A forced shutdown from 12 percent power was required on

January 23, 1991, due to an Electro Hydraulic Control (EHC) piping weld crack.

Repairs were

affected and the reactor again taken critical on January 24, 1991. At the end of the period, the

reactor was operating at 100% power.

A.

A review of completed valve line-ups performed on safety related systems to support

reactor startup followingthe refuel outage was performed by the inspector.

The review consisted

of ensuring independent verification ofvalve positioning was exercised for safety related valves,

the required valve positions were correct by confirming actual position and valve line-up sheets

were properly completed.

Six systems were reviewed for adequacy and are listed below:

N2-OP-33, High Pressure

Core Spray

N2-OP-36A, Standby Liquid Control

N2-OP-74B, Major Components Power Supplies

N2-OP-57, System Power Supply Lineup

N2-OP-82, Containment Monitoring Leakage (CML)

N2-OP-35, Reactor Core Isolation Cooling (RCIC)

The inspector found the valve line-ups were properly executed with only two minor deficiencies.

These

deficiencies

were discussed

with operations

management

and satisfactorily resolved.

Overall, the inspector concluded

that startup valve line-ups were adequately

performed

and

verified by the operators.

B.

The inspector conducted

a review of the training organization to verify that procedures

and programs

were in place

to identify plant modifications that require changes

to plant

procedures,

changes

to operator training programs,

and changes

to the Unit 2 simulator.

The

inspector reviewed a sampling of the plant modifications implemented during the refuel outage

and verified that operators were trained on the modifications, plant procedures

were properly

revised, and that the plant simulator was scheduled to be modified to reflect these modifications.

The inspector concluded that the training program and procedures were adequate to identify plant

modifications requiring changes

to the operator training program and that the Unit 2 operating

staff had been satisfactorily trained on the recent modifications made to the station.

C;

During a walkdown of control room panels, the inspector identified that Uninterruptible

Power Supply (UPS) 2VBA*UPS2Ahad a blown fuse on the inverter. Following the,inspector's

questioning of this condition, operators submitted a work request to replace the blown fuse.

The

inspector questioned

the operability of the UPS per Technical Specification 3.8.3.1

and was

subsequently informed that the blown fuse did not impact operability of the UPS in its present

power supply lineup.

Operations

management

did commit to evaluate

the alarm response

procedure 852100 No. 116 and make any necessary

changes

to ensure that UPS trouble lights

are clearly understood by the operators.

4

I

The inspectors also observed several shift briefings and turnovers conducted by the station shift

supervisors.

The briefings and turnovers were'thorough,

informative and professionally

conducted.

D.

On January

16,

1991, while performing an inspection for EHC system leakage,

the

turbine trip logic was reset.

Contrary to expectations, turbine speed selection indication changed

from "all valves closed" to "1800 rpm" when the speed selection changed.

The closed turbine

stop valves (TSV) began to open, resetting the existing condenser low vacuum containment

isolation bypass.

In that the unit was shut down, the condenser low vacuum signal initiated an

MSIV isolation signal (the MSIVs were already shut).

Niagara Mohawk reported the event per

10 CFR 50.72, and an occurrence report (OR) was initiated.

The inspector observed much of the troubleshooting performed on the system and discussed

th'

problem with the responsible I&C staff. No component or equipment failures could be found,

consequently an operating procedure change was made to alert operators to the potential for an

1800 rpm signal resulting from a turbine trip reset and pointing out that, in the event of such a

signal, approximately 10 seconds were available (while the TSVs open) for the operator to select

"all valves closed"

and avoid the isolation signal.

In addition, operator training would be

conducted on this change.

The OR was forwarded to the system engineer for review and will

remain open until a final engineering determination on corrective action is completed.

The inspector concluded that a reasonable attempt had been made to isolate and recreate the cause

of the event.

Corrective action taken to date (procedure revision and training), while not a

solution to the problem, provides sufficient interim compensatory action.

E.

During low power operations on January 23, 1991, a significant oil leak in the EHC

system was identified by an operator on rounds.

Prompt actions were taken by the control room

operators to reduce power, secure steam to the turbine and the condenser

and then secure the

EHC pumps.

This included initiating the steam condensing mode of the B residual heat removal

system and starting the reactor core isolation cooling system to control reactor pressure and level.

Subsequently,

a controlled plant shutdown was performed.

The inspector determined that approximately 150 gallons of EHC oil leaked from the system.

The leak w'as identified to be from a crack in a piping weld.

The apparent cause of the weld

crack was cyclic fatigue due to vibration.

The weld was repaired and all other welds in the

system were examined via dye penetrant testing and found to be acceptable.

The inspector concluded

that the operators performed well by identifying the leak and then

placing the plant in a safe condition.

Their prompt actions avoided any automatic protective

system actuations.

2.0

MAINTENANCEAND SURVEILLANCEOBSERVATIONS

2.1

gni~1

A.

The following activities were observed:

1

Drywell hydrogen sampling in accordance with procedure N1-CSP-W343.

Troubleshooting and repair to reactor recirculation pump motor generator set 12

per Work Request 187782.

The cause of the MG set ground was determined to

be two worn spots in the epoxy coating of the stator windings which exposed the

metal windings. This, in conjunction with the carbon and copper dust inside the

machine,

set-up a conductivity path which allowed one of the three phases

to

ground-out and caused

the MG set protective relaying to actuate.

A vendor

representative

was called in and repair of the epoxy coating was performed,

as

well as, cleanup of, the machine's internals.

These activities resulted in clearing

the ground condition.

Preventive maintenance procedure N1-MPM-070-A409 on the 12 reactor building

closed loop cooling (RBCLC) heat exchanger (HX).

Zebra mussels and some

silting were found in the HX during the inspection of the service water side.

The

inspector observed cleanup of the HX and performance of an air pressure test to

test integrity of the tube sheet welds prior to an operational pressure

test with

water which was satisfactory.

No performance or procedural problems were identified.

B.

Prelimina

Review of Generic Letter

GL

8 -13 Re ardin

ervice Water S

tern

Problems Affectin

fet -Related

i ment

t

The inspector reviewed GL 89-13 and its supplement and held discussions with the appropriate

system engineers to determine current and planned practices at Unit 1 to address the requirements

of the GL. The inspector determined that for Unit 1, the systems which fall under the general

heading of service water as described in the GL are:

service water (SW), emergency

service

water (ESW), emergency diesel generator (EDG) cooling water and the containment spray raw

water (RW) supply.

Each of these systems has its own suction source in the screenwell house.

The inspector determined that the following programs are in place or planned for each of the

systems:

I

B.1

SW and ESW

These two systems provide cooling water to various heat exchangers

and area coolers in the

reactor and turbine building. The ESW system provides backup to SW in the event of loss of

. off-site pow'er and supplies specific loads only. The only safety-related load cooled by SW or

ESW are the reactor building closed loop cooling (RBCLC) heat exchangers.

By the definition of GL 89-13, RBCLC is a closed system and is thereby exempt from the GL

requirements.

However, the inspector notes that this system does have its own water chemistry

monitoring and surveillance program.

The only safety-related loads cooled by RBCLC are the

post-accident sampling system and control. room emergency ventilation system.

These two loads

are a small part of the total cooling demand on the RBCLC system.

It appears

that there is

adequate margin to accommodate

any degradation in SW or ESW cooling water supply to the

RBCLC HXs due to silting or fouling.

Potential silting or biofouling of reactor building area

coolers was determined not to be of safety significance, in that, they do not support operability

of safety-related equipment located in the spaces they cool.

The inspector determined that for the SW and ESW systems,

the following maintenance

and

testing activities are (or have been) performed:

Allof the RBCLC heat exchangers (11,12, and 13) were opened and inspected during the

1988-90 outage.

Extensive repairs and post-repair vibration testing were done as a result

of flow-induced damage to the tubes and tweeners.

The SW side of one HX is inspected every three months which results in all three HX's

being inspected on a 9-month cycle.

Power Ascension Test, Nl-PAT-11, was performed on the RBCLC HXs during the

startup program to verify operability and verify they met their design basis.

This data

willbe used to baseline future tests.

The area coolers are inspected by various preventive maintenance

procedures.

These

procedures

are being revised to include opening them up to allow inspection for silting

or biofouling'.

Performance of the ESW system

is checked periodically by procedures

N1-ST-Q13

(quarterly) and N1-ST-R16 (each refueling) to check the pumps'erformance,

to obtain

vibration data and to verify operability of the downstream check valves.

B.2

There are four loops of CS and each loop has its own CS HX with associated cooling supplied

by its own RW cooling pump and piping.

The inspector determined that:

One of the four CS HXs is opened up and inspected on the tube side (raw water) every

three months resulting in inspection of all four HXs on an annual basis.

Heat transfer capacity was demonstrated during the power ascension program on one of

the HXs.

Results

indicated

degraded

performance

(a level II test exception

was

generated)

and the HX was opened.

Scaling on the lower one-third of the tube bundle

was identified and was attributed to incomplete drainage of the HX.

The physical

arrangement of the connection point ofRW to the HXprecludes draindown ofabout one-

third of the tubes and both inlet and outlet plenums following operation.

The operating

and surveillance procedures

were. modified to ensure complete draindown of the HX's

tube side via installed vent and drain valves following operation.

Quarterly and refueling surveillances are done to monitor RW pump vibration and flow

characteristics for signs of degraded performance.

B.3

ED

Coolin~ Water Su

I

The inspector determined that:

Performance of each EDG cooling water pump is monitored quarterly as part of the In-

Service Testing (IST) program.

Procedure

N1-MPM-079-A412 is performed annually and involves opening

up and

cleaning the associated

heat exchangers.

~

B.4

Zebra Mussel Intrusion

GL 89-13 also addressed

the issue of biofouling of service water systems.

Until recently, this

was not a concern at the site.

However, Lake Ontario is currently experiencing infestation of

mollusks referred to as Zebra mussels.

Niagara Mohawk has implemented a monitoring program

to detect the presence of zebra mussels in their larval (velliger) stage,

as well as, adult stage.

A treatment system was recently installed and was approved by the New York State Department

of Environmental Conservation (DEC), for the application of a molluscicide (Clamtrol) to the

various SW systems (including the fire water system).

A limited number of treatments are

allowed by the DEC each year with treatments

based

on the velliger monitoring program,

presence ofadult mussels on the substrate racks and on breeding habits.

The inspector observed

a molluscicide treatment on January 16, 1991, on the SW and fire water headers.

Post-treatment

results indicated that an effective treatment had been performed.

The'inspectors determined that

procedures were being properly followed.

B. 5

QmalllA

I

Niagara Mohawk responded to GL 89-13 by letter dated February 16, 1990, and in a supplement

letter,

which provided

more

detail

as

to programs

to

address

each

GL issue,

dated

December

10, 1990.

The inspector verified that the stated programs were in place and that

future activities were identified and were being tracked by the responsible system engineers.

The

inspector. concluded that Niagara Mohawk was addressing the issues of GL 89-13 in a timely and

comprehensive

manner.

2.2

iinit2

A.

-

Portions of the following special tests were observed by the inspectors:

Integrated Leak Rate Test per N2-TSP-CNT-@001.

Turbine Torsion Test per N2-STP-9.

Turbine Valve Surveillance Test per N2-STP-24, performed for post-

modification testing.

The performance of these tests were assessed

to be well controlled and executed in a cautious and

deliberate manner.

The interface between operations and the system engineering test directors

was observed

to be good.

When problems arose,

the tests were stopped

and the problems

appropriately resolved.

B.

While reviewing a completed source range monitor and rod block function check per N2-

ISP-NMS-W008,

an Instrument and Controls (I&C)supervisor identified the rod block check

portion was not performed on December 3, 1990.

The reactor was in mode 5 (refueling) at the

time of the discovery.

In addition, at the time of the supervisor's review, the surveillance test

frequency had been exceeded by 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

This resulted in a violation of TS Table 4.3.6-1 for

the surveillance frequency.

I

The I&C technician who performed the test did not perform the rod block checks

due to

conflicting plant conditions.

The technician noted this in the procedure, but failed"to obtain a

proper review to determine if this exception was acceptable.

The supervisory review of the

surveillance was not performed in a timely manner and thus when the error was detected,

a

violation of TS had already occurred.

The missed surveillance was reported to the station shift supervisor (SSS). The SSS directed that

all activities involving core alterations be stopped.

However, three hours later a management

review of these actions determined that at least one rod block channel should have been placed

into the tripped conditions within one hour ofdiscovery.

The failure to take this action resulted

in a violation of TS Table 3.3.6-1, Action Statement 6.1.b.

A Niagara Mohawk review ofpreviously performed N2-ISP-NMS-W@008 tests was performed

and identified that on September

19 and September

25,

1990, the rod block checks

were

similarly not completed.

On these occurrences,

the supervisory reviews did not detect the missed

rod block test exceptions.

Based on the identification of these two additional missed rod block

checks,

the plant manager

directed

a 100% review of all completed I&C surveillances

be

performed and a sampling of other departments'ompleted

surveillance tests be performed.

No

additional TS violations were identified.

However,

several

instances of minor procedural

adherences

and misuse of notes were found in other I&C tests.

Other corrective action directed

by the plant manager included training on procedural adherence

and an accountability meeting.

The inspector concluded that the safety significance of the three missed rod block surveillance

tests was low because the rod block function was proven to be functionally operable during the

next performance of the test.

As noted above, several I&C technicians marked the rod block

checks section of the test as Not Applicable, wrote a note in the remarks section as justification,

and did not obtain a proper technical review. Also, I&Csupervision did not detect this problem

on two other occasions.

When it was finally identified on December 7, 1990, the review was

not timely and resulted in a third violation. The improper use of notes and inadequate technical

review of completed surveillance tests were the root cause of similar TS surveillance violations

a few years ago.

However, Niagara Mohawk did identify these missed rod block checks and

performed a thorough review to determine the scope ofthe problem. Additionally, the corrective

actions described in the associated LER (90-19) appeared

to be thorough and satisfactory.

In that these TS surveillance violations were ofminor safety significance, were promptly reported

to the NRC, were identified by Niagara Mohawk and corrective actions taken appear

to be

thorough, no Notice ofViolation is being issued in accordance with the NRC Enforcement Policy

stated in 10 CFR 2, Appendix C, Section.V.G.

NON-CITED VIOLATION(50-410/91-02-01)

.10

C.

(Closed) Violation (50-410/90-09-01):

Two examples of the failure to adhere

to

procedures

by mechanical

maintenance

technicians

were identified during safety

related

preventive maintenance on hydraulic cont'rol units.

Niagara Mohawk admitted to the violation,

as stated.

The plant manager conducted an accountability meeting with all personnel involved

and disciplinary actions were taken. Procedural adherence was reinforced withinthe maintenance,

department.

The inspector verified that the corrective action stated in the Niagara Mohawk

response

to this violation (letter dated January 2, 1991) were adequately implemented.

This

violation is closed.

D.

After engineering

review of data obtained during surveillances

on the standby

gas

treatment system, per procedure N2-OSP-GTS-R001, itwas dete'rmined that although acceptance

criteria were met, the. drawdown time was greater than expected.

A retest of the system was

initiated on January 17, 1991.

During performance of the procedure preliminaries, the A train

fan tripped twice when given a manual initiation signal.

The problem was determined to be a

relay which failed to latch properly.

The relay was replaced,

and the surveillance

was

successfully performed with a satisfactory drawdown time.

The inspector observed portions of the surveillance, and noted that timing of the drawdown was

started

when

the fan started

rather

than

when

the signal

was initiated.

The fan starts

approximately five seconds after signal initiation.

Plant personnel indicated that the accident

analyses takes credit for drawdown time from when the fan starts, so the method of timing used

during the surveillance test was appropriate.

The inspector concluded that the surveillance test

was adequately performed.

3.0

ENGINEERING AND TECHNICALSUPPORT

3.1

iinit i

A.

(Closed) Unresolved Item (50-220/88-34-09):

.L'ack of proper identification of post-

accident instrumentation on the control boards.

Following identification ofthis concern Niagara

Mohawk implemented,

on an interim basis,

the use of colored

dots to identify accident

assessment

instrumentation.

After a detailed evaluation and operator input, Niagara Mohawk

implemented,

on November 7, 1990, a design change to identify all control panel accident

assessment

instrumentation with distinctive 3/4 inch red tape affixed above each ofthe indicators.

The inspector

conducted

a control panel

walkdown and verified the accident

assessment

instrumentation was properly identified.

This unresolved item is closed.

11

B.

(Closed)

Unresolved

Item (50-220/88-34-08):

Adequacy of electrical and physical

separation of the redundant control room post-accident monitoring components.

By letter dated

May 19, 1989, (NMP1L 0401), Niagara Mohawk committed to develop and implement a long

term action plan to address electrical and physical separation of control room Regulatory Guide (RG) 1.97 Category

1 instrumentation.

To support the long term plan, various short term actions

were undertaken by Niagara Mohawk to ensure the as-built configurations were in compliance

with RG 1.97.

These action items were previously reviewed and found acceptable

by the

inspector

and

documented

in Inspection

Report 50-220/89-35,

Section

3.1.

Using

the

information gathered

from the short term plan, elements of the long term action plan were

developed

as documented

in an October 29,

1990 letter (NMP1L 0534).

The inspectors

reviewed the long term cable separation program for RG 1.97 Category

1 instrumentation which

is a subset of the broader Design Basis Reconstitution Program.

The inspector concluded the

action plan being implemented by Niagara Mohawk was satisfactory and adequately

addressed

the commitments made for this item.

This unresolved item is closed.

C.

(Closed) Unresolved Item (50-220/90-09-02):

This item was open pending review of the

LER for the improper setting of the emergency condenser isolation setpoint,which did not meet

the design basis.

LER 90-22, issued November 19, 1990,. was reviewed by the inspector.

Niagara Mohawk's conclusion

as to the root cause for this condition was inadequate

design

documentation.

Further, the root cause which allowed the condition to continue after it was

initially'iscovered was a programmatic failure. The inspector agreed with this assessment.

Due to the low safety significance of the event, prompt reporting of this violation to the NRC,

the condition was self-identified and that appropriate corrective actions, as described in LER 90-

22, have been taken, the violation for non-conservative

setpoints was not cited, in accordance

with the criteria in the NRC Enforcement Policy of-10 CFR Part 2, Appendix C,Section V.G.

NON-CITED VIOLATION(50-220/91-02-01)

D.

(Closed) Unresolved Item (50-220/90-09-03):

This item was open pending Niagara

Mohawk investigation of NRC identified deficiencies with implementation of the Appendix J

water seal methodology on the containment spray discharge check valves.

The unresolved item

included three concerns.

Inspector review of these concerns follows:

C

D.1

Steps were added to Nl-OP-14 describing an alternate water seal method that did not

receive NRC review and approval. Further, the addition ofthe steps caused the entire subsection

of N1-OP-14 (Section H.7) dealing with the water seal to be confusing as to its applicability and

implementation, based upon interviews with several licensed operators.

e

12

Niagara Mohawk root cause analysis identified that:

The procedure

steps

were added

at the behest of the operations

department for the

potential scenario where no containment spray pumps are running and a water sealing

function is needed.

The change to add these steps to Nl-OP-14 were approved via

, routing the change to SORC'members

vice a routine SORC meeting.

Review of letters between Niagara Mohawk and NRC staff made it clear that the NRC

wanted to be informed of the method(s) of implementing the water seal.

The corporate licensing group which was tasked with oversight of the water seal project

were unaware of the change made to Nl-OP-14 by the operations department,

and the

. operations department was unaware of the fact that the NRC had to be informed of any

methods used for establishing a water seal.

Operators did not receive training in the simulator for the Section H.7 changes.

This was

considered

one reason

why operators

were confused

over its implementation

when

questioned by the inspector.

Niagara Mohawk speculates

that had training been given,

the procedural problems might have been identified and properly resolved.

D.2

This concern dealt with a revision to the Niagara Mohawk Safety Evaluation 89-13 which

appeared

to add a commitment to enter the containment spray system Limiting Condition for

Operation (LCO) for certain conditions, specifically, torus cooling or makeup mode.

The

inspector identified that these instructions were not reflected in the appropriate sections of N1-

OP-14.

Further discussions with operations management

determined that an assumption

was

made that the operators entered the LCO anytime these conditions were established.

This was

found not to be the case.

Consequently, Nl-OP-14 has been revised to caution operators to enter

the applicable LCO when in the torus cooling or torus makeup modes.

D.3

The ALARAreview for Safety Evaluation 89-13 did not appear to be comprehensive,

in

that, the modification ofvalves 80-40 and 80-45 to manually operated (normally open) had been

judged by Niagara Mohawk to be of minor radiological significance since the valves would not

have to be operated to mitigate or recover from an accident.

However, the inspector identified

that EOP-10, Drywell Flooding, requires operation of these valves per Section H.8, Nl-OP-14.

A subsequent

Niagara Mohawk evaluation of this issue concluded

the same.

However, the

ALARAgroup was not faulted for the inadequate

evaluation

as they were informed that the

valves would only be operated during routine plant evolutions.

The inspector agreed with this

assessment.

0

13

~nclusicn

I

The inspector considered

these three concerns to be resolved and Item 50-220/90-09-03 closed.

However, the inspector concluded that Nl-OP-14 was revised, on May 7, 1990, per Safety

Evaluation 89-13, and as a result conflicted with EOPs. Two specific examples were identified.

First, Section H.7 of Nl-OP-14 states that following a design basis Loss of Coolant Accident

(LOCA), two containment spray pumps should remain in operation when containment pressure

is greater than 3 psig and one pump should remain in operation when less than 3 psig, in order

to maintain a long term water seal.

However, EOP-4 states to terminate containment sprays

when drywell pressure is less than 3.5 psig.

Secondly, EOP-10 directs performance of Section

H.8 of Nl-OP-14;

Section H.8 requires alternate closing/opening operations of valves 80-40

and/or 80-45.

However, in the event of a LOCA, the radiation field in the vicinity of these

valves would likely preclude operation of the valves.

Both of these conditions were not

identified during the procedural

revision process

for incorporating the water seal

steps

to

operating procedure Nl-OP-14.

The two Emergency Operating Procedure conflicts and the

inadequate

and confusing water seal implementation

steps in Section H.7 of N1-OP-14 are

contrary to Technical Specification 6.8.1

and ANSI 18.7-1972 regarding proper procedure

revision and review.

This is a VIOLATION. (50-220/90-02-02)

Assessment

Niagara Mohawk's root-cause analysis for this event revealed numerous other procedural and

programmatic deficiencies.

Additionally, lessons learned transmittals have been prepared and

disseminated

to corporate and site personnel.

The root-cause analysis, as well as, preliminary

corrective actions taken were discussed with the resident staff.

Niagara

Mohawk's overall root-cause

was

that the failure to adequately

implement

the

Appendix J water seal commitment was poor managerial methods.

The inspectors concurred

with this broad conclusion, but remained concerned

that the interface between the corporate

licensing group and the station warrants further examination,

in that, this project was the

responsibility of the licensing group.

Particularly troubling to the inspectors

was that the

exemption to Appendix J was a specific issue in the Restart Action Plan and thus was supposed

to have received

a higher level of attention and review.

Despite these additional oversight

functions and review processes,

the water seal methodology was poorly implemented.

32

Unit 2

A.

~D

On September

13, 1985, the NRC submitted the results ofits Nine MilePoint Unit 2 SPDS pre-,

implementation audit to Niagara Mohawk and requested

that Niagara Mohawk respond to'he

concerns which resulted from the audit. Niagara Mohawk responded to these concerns in a letter

dated November 15, 1985, which delineated the corrective actions to be taken for each area in

question.

NRC concurred with the proposed corrective actions and included a License Condition

(C.(8)) in the Nine Mile Point Unit 2 Facility Operating License dated July 7, 1987.

The

License Condition indicated that Niagara Mohawk shall have an operational SPDS that includes

.the enhancements

described in their 11/19/85 letter prior to startup following the first refueling

outage.

During the current inspection period, the inspectors reviewed the implementation of the Nine

Mile Point Unit 2 SPDS to determine ifLicense Condition C.(8) had been met.

Issue //1

Man-in-the-Loop

Testing,

Validation

and

Verification

Documentation

Centralization

The inspectors determined that adequate man-in-the-loop testing was performed to verify that the

SPDS displays and parameter

set provide the necessary

safety status information during both

normal and abnormal plant conditions.

The testing involved the imposition of various plant

scenarios on the Unit 2 simulator and having control room personnel and test observers evaluate

the dynamic performance of the SPDS.

Several modifications were made following the test to

correct system problems and improve usability. In addition, a followup man-in-the-loop test was

performed to validate these modifications.

The inspectors found that all documentation,

both internal and external to Niagara Mohawk,

relating to the design, construction, installation, validation and verification of the Unit 2 SPDS

was in Niagara Mohawk's possession.

This resolved an NRC audit comment relating to the

centralization of SPDS.validation and verification documentation.

15

Issue ¹2

Content of Field Verification and Validation Testing

Following the man-in-the-loop testing, SPDS computer operational testing was performed.

The

system was tested by the insertion of predetermined

raw data inputs and verification of data

manipulation and validation, alarm setpoints,

display functions,and

system

response

times.

Testing also included the performance of calibration procedures on instrument loops providing

SPDS inputs and verifying that input point values (at the SPDS computer) corresponded

with

calibration inputs, thereby validating sensor to display response of SPDS.

Test exceptions were

minor and have been satisfactorily resolved.

The inspectors concluded that the field testing was

successfully completed and appropriately addressed

the testing aspects of SPDS validation and

verification.

Issue ¹3

Evaluation of SPDS Reliability

In the November 19, 1985 letter, Niagara Mohawk indicated that a computer log would be

maintained to document SPDS system failures, their duration, and the equipment that failed. The

inspectors reviewed procedure N2-COMP-L.WS.01, Liquid Radwaste Computer System Power-

Up/Power-Down Procedure.

This procedure has been temporarily changed to include the SPDS

availability log which willbe maintained by system support engineering.

While the procedure

notes that the log should be evaluated periodically to assess SPDS reliability, goals for reliability

were not indicated.

However, reliability goals were noted in the SPDS design documentation.

The inspectors

concluded

that this commitment had been adequately

addressed

by Niagara

Mohawk.

Issue ¹4

Use of BWROG Parameter Set at NMP2

On September 7, 1990, Niagara Mohawk submitted to NRC its evaluation of the adequacy of

the BWROG parameter

set used for the Unit 2 SPDS.

This met the commitment noted in the

November 19, 1985 letter.

Issue ¹5

Human Factors Improvements

Niagara

Mohawk

implemented

the

human

factors

recommendations

noted

in

the

November 19, 1985

letter,

as well as,

other recommendations

which have

resulted

from

validation testing.

The inspectors

verified that these

changes

had

been

implemented

by

observation of the affected SPDS displays.

16

Issue ¹6

Radioactivity Control SPDS Display

The NRC pre-implementation audit noted that the display ofradioactivity control parameters was

not concise because too many instruments (two annunciators, two displays, and two strip chart

recorders)

would have to be observed

by the operators

to assess

the status of necessary

parameters.

Niagara Mohawk responded to this concern by adding the necessary radioactivity

control parameters

to the SPDS Level II displays.

In their summary report dated January

11, 1991, the independent engineering consultant that

performed the SPDS validation and verification stated that the Unit 2 SPDS displays were

adequate to ensure that the information provided willbe readily comprehended by the operating

staff with one exception.

The consultant felt that placing four trend plots on the Radioactivity

Control SPDS

display may not'provide sufficient resolution for indication of the trended

parameters

and that Niagara Mohawk should evaluate this after the operators gained experience

with the SPDS.

Niagara Mohawk disagreed with the consultant's position because they felt that

the current display does provide adequate resolution and also because

the current display was

responsive to the NRC pre-implementation audit concern.

The inspectors observed the SPDS

Radioactivity Control display and found the resolution of the trended parameters to be adequate,

Issue ¹7

Continuous Display of SPDS in Control Room

In response to an NRC audit concern, Niagara Mohawk committed to ensuring that at least one

screen of the Honeywell System in the control room willbe dedicated to the SPDS mode at all

times.

Niagara Mohawk has included this requirement in Operating Procedure OP-91B, SPDS.

The inspectors noted, during numerous visits to the control room, that one of the Honeywell

screens

was indeed committed to SPDS.

During the review of the Operating Procedure OP-91B, the inspectors noted a precaution related

to the SPDS Level II display of group isolation valve status.

In particular, since input signals

to the SPDS computer are provided by valve control power, it is possible for the computer to

indicate a valve as closed even if it is open, if power is lost to the isolation valve control

circuitry or to optical isolators in the circuitry.

This could result in faulty indication of a

containment isolation valve group on the associated

SPDS Level II display.

When questioned

as to the possibility of physically modifying the circuitry to eliminate this problem, Niagara

Mohawk indicated

that the problem

is not unique in the industry

and

that the physical

modifications

needed

to

resolve

this problem

would be

extensive

and

costly

and

not

commensurate

with a comparable improvement in safety.

Niagara Mohawk has included a

discussion of this potential problem in the operations training lesson plan for SPDS.

The

inspectors concluded that the issue had been adequately addressed

by Niagara Mohawk.

17

Som'mary

The inspectors

concluded that the Unit 2 SPDS has undergone appropriate modification and

testing and has been properly validated and verified to ensure

compliance with applicable

regulatory requirements and guidelines provided in NUREG 0737, Supplement 1, NUREG-1342,

and the Standard Review Plan.

Niagara Mohawk adequately

addressed

and responded

to the

specific SPDS commitments which resulted from the 1985 NRC pre-implementation audit of the

Unit 2 SPDS.

The inspectors concluded

that in adequately

addressing

these specific SPDS

commitments, Niagara Mohawk had successfully met Facility Operating License Condition C. (8).

B.

(Closed) Unresolved Item (50-410/88-201-01):

Molded case breaker testing deficiencies

involving a lack of guidance for adjustable trip'relay settings.

To address this issue Niagara

Mohawk conducted a comprehensive walkdown ofall safety-related molded case circuit breakers

(MCCBs) and motor control centers to identify which MCCBs have adjustable trip settings.

In

addition, the generic testing procedure, N2-EPM-GEN-V582, was revised to incorporate the

necessary

acceptance criteria for magnetic trip testing.

These corrective actions were reviewed

and found acceptable during a previous inspection (reference Inspection Report 50-220/90-23,

Section 3.4).

During this inspection period the inspector verified that the appropriate design

drawing, AE-003, "Overload Heater List," was revised per Engineering Design Change (EDC)

2E10330 and that the associated

electrical maintenance

procedures

were properly revised to

correctly identify the required trip settings.

This unresolved item is closed.

3.3

ll

1

d2

eneric Letter 8 -10 Res

n e R view

. By letters dated December

14,

1990, (NMP1L 0556 and NMP2L 1267) Niagara Mohawk

responded

to GL 89-10, Supplement 3, Consideration of the Results of NRC sponsored Test of

Motor-Operated Valves, dated October 25, 1990.

This GL supplement specifically requested

licensees

to complete a plant specific safety evaluation of the susceptibility to failure under

accident conditions of motor-operated valves in the high pressure core injection (HPCI), reactor

core isolation cooling (RCIC), reactor water cleanup (RWCU) and isolation condenser

(IC)

systems, ifapplicable.

For the impacted systems (Unit 1 - RWCU and IC, Unit 2 - RWCU and

RCIC) Niagara Mohawk concluded that the isolation valves would function satisfactorily under

accident full-flowconditions.

18

4

The inspector reviewed the supporting safety assessments

forboth units (Calculation No. S14-33-

V001, dated December

11, 1990, for Unit 1 and Safety Assessment for NRC Generic Letter 89-

10, Supplement 3, dated December

13, 1990 for Unit 2) and concluded that they adequately

addressed

the specific assessment

considerations outlined in Supplement 3. However, following

discussions with Headquarters

and region-based

specialists,

the inspector was informed that a

more detailed technical evaluation of the utilities'eneric Letter responses

would be conducted

by a schedule not yet established.

Consequently,

this inspector's review is complete, but the

formal NRC technical assessment of Niagara Mohawk's response

to Generic Letter 89-10 will

be conducted in a subsequent

inspection.

4.0

REVIEW OF LICE<NSEE EVENT REPORTS (LERs) AND SPECIAL REPORTS

4.1

Unit

1

The following LERs were reviewed and found satisfactory:

LER 90-19, Reactor scram due to spurious trip of neutron monitor caused by noise.

LER 91-01, Reactor scram due to spurious non-coincident logic trip signal.

Special Report dated January

25,

1991, (NMP77309), dealing with inoperability of the

12

Containment Hydrogen Monitoring System was reviewed and found acceptable.

4.2

~Jni ). 2

The following LERs were reviewed and found satisfactory:

LER 90-17, Personnel error results in inadvertent actuation of the standby gas treatment

system.

LER 90-18, Standby liquid control system declared

inoperable due to excessive

pipe

stress caused by a failed mechanical snubber.

LER 90-19, Technical Specification violations ofrod block checks due to procedural non-

compliance and inadequate work practices.

(see Section 2.2.B)

5.0

SE<CURITY/SAI<EGUARDS

A.

(Closed)

Unresolved

Item (50-220/88-30-01

and 50-410/88-29-01):

This item was

recently updated in a security inspection conducted the week of December

17, 1990.

The item

was left open pending repair of certain areas.

These areas were repaired soon after the security

team's visit and verified to be proper by the resident staff.

This item is closed.

0

19

'.B.

The inspectors discussed the heightened Security Guard Force preparedness

measures and

contingency plans initiated as a result of the increased potential for terrorist activities with respect

to the Persian Gulf War.

The inspectors found these measures

satisfactory.

6.0

MANAGEMENTMEETINGS

Management/Exit Meetings conducted by Region Based inspectors during this inspection period:

ate

~ub'eet

R~eort No

~ln pec~tr

1/25/91

2/1/91

2/15/91

2/15/91

EP Program Review

EOP Review - Unit 2

Effluents

HP/Transportation

91-03/91-03

91-80

91-05/91-05

91-04/91-04

Amato

Walker

Jang

Furia

7.0

PRELIMINARYINSPECTION FINDINGS

At periodic" intervals and at the conclusion of the inspection,

meetings were held with senior

station management

to discuss the scope and findings of this inspection.

Based on the NRC

Region I review of this report and discussions held with Niagara Mohawk representatives,

it was

determined that this report does not contain safeguards or proprietary information.