ML17056B732
| ML17056B732 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 03/14/1992 |
| From: | Eapen P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17056B731 | List: |
| References | |
| 50-220-92-80, NUDOCS 9203260315 | |
| Download: ML17056B732 (62) | |
See also: IR 05000220/1992080
Text
U. S. NUCLEAR REGULATORY COMMISSION
REGION I
~ei~rt
g
QaakkMu.
Ei
N
50-220/92-80
50-220
~i~ngg
.~PN
N
In
tion At
QoOnl~ced
~ln pec~tr
'iagara
Mohawk Power Corporation
301 Plainfield Road
Syracuse, New York 13212
Nine MilePoint Nuclear Power Station, Unit 1
Scriba, New York
February 22 - March 4, 1992
G. Barber, Senior Resident Inspector, DRP
R. Bhatia, Reactor Engineer, DRS
D. Brinkman, Senior Project Manager, NRR
her
n ri
in
NR
Per onnel:
Qb
server'pproved
by:
W. Schmidt, Senior Resident Inspector, DRP
C. Beardslee,
Reactor Engineer Intern, DRS
=P. Eddy, State of New York
.E
Dr. P.. Eapen, Team
der,
Chief, Systems Section, DRS
Date
~l<<i: Pl
E
l
E
'
PDR "'>>>> 9-"orgy
ADOCK 0500022
TABLE OF
ONTENT
Page
EXECUTIVESUMMARY:.;;...;..;..........................;3
1.0
INTRODUCTION
1.1
The AITScope and Objectives
1.2
AITProcess
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2.0
ISOLATIONOF ULTIMATEHEAT SINKEVENT..................
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2.1
2.2
2.3
Screen House Bay Gate Operation
Chronology ofEvents......
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Highlights of the Event....................
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3.0
PERSONNEL AND NUCLEAR PLANT SYSTEMS PERFORMANCE ..., .. 9
3.1
3.2
3.3
3.4
Equipment Performance
Procedure Adequacy
Personnel Performance ..
Management
Assessment
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4.0
GENERIC IMPLICATIONSOF THIS EVENT
5.0
THE LICENSEE'S IMMEDIATEACTIONS
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6.0
CONCLUSIONS ~.................,..............,.....,
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7.0
MANAGEMENTMEETINGS...............................
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TABLE 1 - Chronology of Events
I
FIGURE 1 - Screen House Bay Level Sketch
FIGURE 2 - Normal Flow Configuration of the Screen House Bay
FIGURE 3 - Reverse Flow Configuration of the Screen House Bay
APPENDIX A - NRC Augmented Inspection Team Charter
APPENDIX B - Persons
Contacted
APPENDIX C - Documents Reviewed
I
EXECUTIVE UMMARY
On February 21, 1992, at about 8:30 a.m., licensee personnel inadvertently isolated Nine-
Mile Point Nuclear Power Plant Unit 1 from Lake Ontario, the unit's ultimate heat sink, by
closing all gates that let the water from the lake to the plant's service water bay.
One
service water pump and two circulating water pumps were running at the time of this event.
The water level in the bay rapidly decreased
below the level assumed in the Unit 1 licensing
basis.
The bay level was reduced for about six minutes before the operators opened B gate
restoring water to the bay from the lake.
The running service water pump was secured by
the operators
as it lost suction and.cavitated.
The emergency service water pump was
started as required by procedures,
and this pump had to be secured immediately due to low
discharge pressure.
The only noticeable change in plant conditions due to the brief isolation
of the ultimate heat sink was a two degree Fahrenheit increase in the reactor building closed
loop cooling system.
The reactor had been shutdown since February 16, 1992, and the
reactor system was depressurized
with reactor coolant temperature
at about 143 degrees
Fahrenheit at the time of this event.
An augmented inspection team (AIT) was dispatched by the NRC to determine the
circumstances
that led to this event, its causes,
safety significance and generic implications,
and the adequacy of the licensee's
actions before, during, and after the event.
The AIT
began its assessments
on Saturday, February 22, 1992, and completed its onsite reviews on
February 28, 1992. The AITpresented
its preliminary findings in a public exit meeting on
March 4, 1992.
The AIT concluded that the causes for this event were:
(1) Failure to follow the established
work control process by various levels of personnel in multiple licensee
groups; (2)
Inadequate
management
over view to assure that the workers understood
and followed
established procedures;
(3) Inadequate communications within and among organizations
participating in work activities; and (4) Failure to adequately consider risks associated
with
test activities that affected multiple systems during shutdown conditions.
The consequences
of this event were minimal because
the reactor core and,the reactor
coolant were unaffected by this event, no equipment was damaged,
and no radiation was
released.
The operator response
to the decrease
in level in the intake bay was good.
However, the work control breakdown that led to this event was significant because it caused
the unit to isolate from its ultimate heat sink.
The screen
house bay level dropped below that
required for the safe operation. of the pumps and caused
the Unit to be in an unanalyzed
condition.
The adequacy of the instrumentation in the bay and the licensee's failure to-consider risk
associated
with test activities that affected multiple systems during shutdown conditions were
identified as items that may have potential generic implications.
l.~
Upon being informed of the inadvertent isolation of,Nine Mile Unit 1 from Lake
Ontario on February 21; 1992, the NRC Region I Regional Administrator and senior,
management from the Office of Nuclear Reactor Regulation (NRR) and the Office for
Analysis and Evaluation of Operational Data (AEOD) determined that an Augmented
Inspection Team (AIT) should be formed to review and evaluate the circumstances
and significance of this occurrence.
The basis of the NRC concern was the apparent
inadequacies of management controls of maintenance activities that allowed the event
'o occur.
Accordingly, an AIT was selected, briefed, and the AIT leader dispatched
to the site on February 22, 1992.
1.1
The AIT
c
and Ob'ective
The charter for the AIT (Appendix A) was issued on February 24, 1992.
The
charter directed the team to conduct an inspection and accomplish the
following objectives:
Conduct a timely, thorough and systematic review of the circumstances
surrounding the event, including the sequence of events that led to and
- followed the isolation of the ultimate heat sink;
2.
Collect, analyze and document relevant data and factual information to
determine the causes,
conditions and circumstances
pertaining to the
event including the response of the licensee's staff to the event;
3.
Assess the safety significance of the event and communicate to
Regional and Headquarters
management
the facts and safety concerns
related to the problems identified; and
4.
Evaluate the licensee's review of and response
to the event and
implemented corrective actions,
II
During the period between February 22, 1992 and March 4, 1992, the AIT
conducted
an, independent inspection, review, and evaluation of the conditions
and circumstances
associated
with this event.
The team inspected the gate's
and the pumps in the screen house bay and related indications in the control
room;
held discussions
and formal interviews with personnel involved in this
event; reviewed relevant records including computer printouts before, during,
and after the event, and trends of pertinent plant parameters;
and evaluated the
adequacy of established
procedures,
management
oversight, and personnel
training.
Attachment B is the list of personnel contacted by the AIT and
-Appendix C is the list of documents reviewed by the AIT members.
This inspection was conducted in accordance with NRC Manual Chapter 0513,
Part III, Inspection Procedure 93800, and additional instructions provided in
the AITcharter.
2.0
I
LATI N
F
TIMATEHEAT INK EVENT
2.1
creen H use Ba
ate
rati n
Lake Ontario provides the source of water to Nine Mile Unit 1 to cool the
reactor during'normal operation and accident conditions.
One of the five gates
in the unit's screen
house lets water from the lake to the screen house bay
where 19 pumps take suction for safety and non-safety related purposes.
Figure
1 shows the normal and minimum required bay levels as well as the
elevations where various pumps take suction from the screen
house bay.
The flow of water from the lake to the screen house bay during normal screen
bay gate configuration is depicted in Figure 2.
Water is drawn from the lake
at a location about one thousand feet away from the shore.
The water'nters
the bay through the intake tunnel and gates A and B. The water from the bay
is returned through gate C and the discharge tunnel to a location in the lake
about five hundred feet away from the shore.
A specially designed intake
structure removes debris and other floating bodies from the incoming water.
During winter months, the intake structure has a potential to experience ice
build up and block the flow area.
To prevent such ice build up,
the operators
reverse the flow of water using procedure N1-OP-19.
-Figure 3 depicts the
screen bay gate configuration during reverse flow operation.
In this
configuration water is drawn from the lake through the discharge tunnel and
flows to the bay through gate D, mixed with hot water from the condenser,
and returned to the lake through gate E to the intake tunnel and the intake
structure.
The water that is returned to the lake is warmer and removes ice
build up on the intake structure.
The licensee also refers to this operation as
de-icing operation of the intake structure.
The gates are massive concrete blocks that are typically 6 feet by 9 feet and
weigh about 5,400 pounds.
Electric motors raise and lower gates A
through D.
Gate E is hydraulically controlled.
The controls (push buttons)
for the gates are located in the screen house.
2.2 ghhlf
4
The AITcompiled independently a detailed chronology of events by
interviewing cognizant personnel, reviewing relevant records including
computer printouts before, during, and after the event, and trends of pertinent
plant parameters.
This detailed chronology is provided in Table l.
2.3
Hi hli hts f the Even
The push button that opens the D gate was inoperable for a long time and the
licensee personnel used a piece of a wooden ruler to make the electrical
contact for the motor that operates
the gate.
A work order 163740 was is'sued
on February
10, 1992, to fix this push button circuitry.
1
The implementation of this work request was not fully in accordance with the
licensee's
established
procedures.
For example, maintenance personnel did not
adequately detail the required work and operations personnel did not specify
the required procedures for post maintenance
test.
The electrical circuitry for gate D was fixed adequately on February
10, 1992.
However, during this work, the licensee personnel identified an undocumented
electrical jumper (wire) that bypassed
the mechanical tension overload
protection switch from the drive motor circuit.
On February 11, 1992, a deficiency event report (DER) 1-92-0267 was
generated
to resolve this concern,
as required by the licensee procedures.
However, this DER.was not processed
in a timely manner, and an adequate
operability determination was not made by the operations personnel
as required
.
by the licensee's procedures.
A temporary modification (5395) was initiated
on February
11, 1992, to obtain an engineering resolution for this
undocumented jumper.
The undocumented jumper, the DER, and the
temporary modification were not documented in the work request,
as required
by the licensee's procedure.
Consequently, control room operators were
deprived of this critical information when they reviewed the work request.
This work request was not closed, again as required by the procedure,
when
the original work was completed on February 10, 1992.
On February
11, 1992,
the original work request was revised to restore the
wiring in gate D circuitry to the original design by adding the statement
"Return wiring to normal configuration per dwg C 22303 C, sh. 3,'-'he
personnel'involved in the work understood that the change was to remove the
undocumented jumper from gate D circuitry. However, the brevity, lack of
specificity, and details made this addition to appear no more than a routine
system restoration after fixing the push button circuitry on gate D. Additional
instances of failure to follow licensee procedures
occurred during'the
processing of this change.
For example, the-maintenance
general supervisor
did not review and approve this change; the senior reactor operator did not
review this change adequately for plant impact; the shift supervisor did not
review the change for post maintenance
test requirements;
and no detailed
work instructions or troubleshooting steps were specified.
During early afternoon on February 12, 1992, the jumper was removed
without waiting for the resolution of the DER issued on February
11, 1992, as
required by the licensee's procedures.
-Electrical maintenance
reported the
'completion of the revised work to the station shift supervisor and informed
him that the ability of this gate to close during reverse flow operation cannot
be assured with the mechanical overload switch in the circuit.
The station shift supervisor ordered immediately the reinstallation of the
jumper through the emergency temporary modification process,
and a new
DER (1-92-0286) 'was issued to document and evaluate this action.
All
departments
involved agreed that operation of the gate D could only be tested
~
safely during shutdown conditions and decided to postpone the work on gate D
until the next scheduled unit shutdown in fall 1992.
None of these decisions
or the removal/reinstallation of the jumpers were documented in the work
request.
8
The unit was automatically shutdown on February
16, 1992, due to an
unrelated problem with the turbine stop valves. After this unplanned shutdown,
engineering and maintenance personnel discussed
the possibility of gate D
work in the morning outage work planning meetings.
However, due to the
objections from operations,
this work was not scheduled.
On February 21, 1992, the reactor remained shutdown, depressurized
with the
reactor coolant temperature of about 143'F.
The gate D work was again
discussed at the 6:45 a.m. outage work planning meeting.
The operations
personnel initially objected to this work. However, the operations supervisor
agreed to discuss testing of gate D further with maintenance.
This action
caused inadequate communications between maintenance
and operations and
led to the bypass of the normal work control review process.
At about 7 a.m.,
the station shift supervisor (SSS) agreed to put screen house bay in reverse
flow configuration to allow testing of the gate under differential pressure.
A
specially marked-up electrical drawing (referred to as blue markup), which
was previously approved by another station shift supervisor,
was issued to
electrical maintenance who began the gate D work at about 8:20 a.m.
Electrical maintenance personnel removed the undocumented jumper from the
motor circuitry. The operations personnel cycled the gate 2-3 feet in the
downward direction successfully and then closed the gate fully. An attempt to
reopen gate D was unsuccessful.
This caused the inadvertent isolation of the.,
Unit from the lake at 8:29 a.m.
The isolation occurred while two circulating water pumps (125,000 gpm each)
and one service water pump (20,000 gpm) were removing water from the bay.
As a result the water level in the bay rapidly decreased.
At 8:29 a.m. the control room received the tunnel high differential alarm and
then the screen bay low level alarm, and the control room ordered the opening
of gate D immediately.
A non-licensed operator held the "UP" button closed,
while an electrician held a jumper across the tension overload switch and
commenced
the opening of D gate.
Additionally, the control room ordered
a
licensed operator to open B gate also immediately.
Between 8:30 and
8:35 a.m., both B and D gates were being opened.
gt takes about five
minutes to fully open the gates).
At 8:32 a.m. the running service water pump
cavitated, and it was immediately secured by the operators.
The operators also
attempted to start emergency service water pump No. 11, as required by the
licensee's procedure (SOP-7, Loss of Service Water).
However, this pump
was immediately secured
due to low discharge pressure resulting from low bay
level.
The operators also secured circulating water pump No. 11 to reduce
water removal rate from the bay.
At 8:35 a.m. the bay level was returned to normal.
The licensee started both
emergency service water pumps successfully at 8:38 a.m., and at 8:44 a.m.,
service water pump No. 11 was started and returned to service successfully.
Subsequently,
at 8:45 a.m., both emergency service water pumps were secured
and the bay and other equipment were restored to shutdown operation
configurations.
During this event, the level decreased
from normal 243'0" to 229'" or
about nine feet below the minimum level 238'" for safe operation for about
six minutes.
The control room has an alarm for the bay level.
However, the
set point and the location of this instrumentation in the bay are such that the
alarm is annunciated
when the level is 18" below the required level of238'"
for safe pump operation.
The unit's safety analysis requires a minimum water
level of 238'" in the screen house bay.
Therefore, this event caused the
facility to be in an unanalyzed condition.
The only observed system change was a two degree fahrenheit increase in the
temperature of the reactor building closed loop cooling system.
No
radioactivity was released
and no equipment or structural damage was
observed.
At 9:30 a.m. the license'e conducted a detailed debrief with all personnel
involved in the event.
A stop work order was issued for Unit 1 at 10:30 a.m.
DER 1-92-Q0390 was initiated immediately to document and resolve this loss
of ultimate heat sink event.
The licensee notified the senior resident inspector and the NRC operations
center at 11:30 a.m. and 12:25 p.m., respectively.
Subsequently,
the licensee verified that the non-safety related service water
pump and the safety-related emergency service water system pump were
operable by performing detailed surveillance tests.
3.0
PER ONNEL AND
CLEAR PLANT Y TEM
PERF
RMAN E
The AITassessed
the performance of the personnel
and the plant systems before,
during, and after the event.
The findings of the AITare grouped into three broad
categories:
Equipment Performance;
Procedure Adequacy; and Personnel
Performance.
I
10
3.1
i m
P rf rmance
The equipment performed as expected with the exception of the gate D and the
bay level alarm.
The licensee personnel expected that the gate D would open
from full closure position in spite of the mechanical tension overload switch in
the gate circuitry while the bay is in reverse flow operation.
However, this
switch inhibited the motor from opening the gate as intended.
The bay level
alarm in the control room that annunciated only after the level decreased
18"
below that was required for safe pump operation.
Service water pump No. 11-
and the emergency water pump No. 11 that were affected by the event were
successfully verified operable by the licensee using appropriate surveillance
procedures.
No equipment or structural damage occurred as a result of this
event.
3.2
Procedur
Ad
uac
In general, the licensee's
procedures
were adequate,
and they did not
contribute to this event.
However, procedure (SOP-7) required the operators
to turn on the safety-related emergency service water pumps when the bay
level was below'he suction level for these pumps.
The licensee acknowledged
this concern and agreed to review this matter for resolution prior to the start
up of unit 1 ~
3,3
Pers
nnel P rf rmance
The licensed operators'esponse
to the decreased
level in the intake bay was
good.
However, prior to the event, the performance of various levels of
personnel in multiple licensee organizations, including operators,
during the
preparation, implementation, and documentation of work request 163740 was
inadequate.
The following instances of failure to follow established
procedures by licensee
personnel exemplify a breakdown in the work control process:
(1)
-
Maintenance personnel did not adequately describe the work on the
initial work request issued on February
10, 1992, as required by
licensee administrative procedure AP-5.5, steps 5.1 and 5.2 (See
Appendix C for complete title of documents).
(2)
Operations personnel did not specify the surveillance procedures
to be
used for post maintenance
test, as required by licensee procedure AP-
5.2.4.
11
(3)
Maintenance workers did not record the undocumented
electrical
jumper identified during the conduct of work in the work request, or in
the DER issued to resolve it, as required by the trouble shooting
procedure AP-5.4.2, Section 2.
(4)
The personnel did not close the work request when the work was
completed on February
10, 1992, as required by licensee procedure
AP-5.5.1, step 5.17.
(5)
The change to the work request that authorized the removal of the
undocumented jumper was not reviewed and approved by the initiating
department general supervisor,
as required by the licensee's work
request procedure AP-5.5.1, step 4.10.
(6)
The work request change was not reviewed by the SSS on
February 11, 1992, for post maintenance
tests (PMT) requirements,
as
required by procedure in AP-5.5.1, step 4.3.
(7)
The work request was not adequately reviewed by the senior station
'perator (SSO) for plant impact as required by the work request
procedure AP-5.5.1, step 4.4.
(8)
No troubleshooting procedure was prepared for the test of the gate D
on February 21, 1992, as required by the work request procedure AP-
5.5.1, step 3.19 and troubleshooting procedure AP-5.4.2.
(9)
No post maintenance
test was specified by maintenance for the gate D
work on February 21, 1992, as required by AP-5.5.1, step 4.3.
(10)
The initial DER was processed
inadequately and an operability
determination was not made,
as required by procedure NIP-ECA-01,
section 6.1.2.
(11)
The removal of the undocumented jumper was not recorded in the work
request,
as required by the work request procedure AP-5.5.1.
(12)
The undocumented jumper was removed without authorization from
engineering, contrary to licensee procedure AP-6.1.
12
(13)
- Communications between operations and maintenance were very
informal and incomplete.
Maintenance and engineering did not
adequately explain the details of the work. involved to operations.
This
was contrary to the licensee's work in progress procedure AP-5.2.5,
step 5.2.2, which requires the department supervisor/chief to conduct a
pre-work brief with appropriate personnel.
(14)
The maintenance personnel bypassed
the work control center and went
straight to the SSS on duty, contrary to procedure.
Due to inadequate
documentation of prior work on the work request,
inadequate
communications,
and a lack of a questioning attitude, the SSS
authorized work without fully being aware of the plant impact of the
requested work. This SSS authorization is required in work-in-progress
procedure AP-5.2.5, step 4.1.
(15)
The licensee work request procedure AP-5.5.1, step 4.3 requires the
SSS to perform technical reviews on work requests
when work control
personnel do not perform the review.
The SSS did not perform an
adequate technical review for this work request.
(16)
Step 4.3 of the licensee's work in process procedure AP-5.2.5 requires
the Assistant Station Shift Supervisor (ASSS) to ensure that the post
maintenance
testing requirements
are appropriate to verify 'equipment
function.
Since the maintenance personnel bypassed
the process, it
appeared
that this ASSS function was not executed for this work
request.
(17)
Communications within operations were inadequate.
The chief shift
station operator (CSO) was aware of the closing of gate D and some of
the potential impacts of closing the gate during reverse flow.
However, he failed to communicate that to shift management.
The
ASSS was aware of operation's objections to testing gate D, but he did
not communicate that to the SSS who approved the test.
(18)
Various levels of personnel and supervision in the maintenance
organization did not fully understand
the work request process
and the
significance of various signatures on work request form.
13
3.4
Mana emen
A
men
The AITreviewed management involvement and control for the activities
related to the event.
The team assessed
the adequacy of the implementation of
the licensee's
management
expectation for the work control process.
The team
also reviewed the self assessments
and personnel training in this area.
The AITobserved that the licensee management
expectations regarding the
strict adherence
to established
procedures were not effectively communicated,
monitored, or controlled by supervisors and management during work request
process implementation.
The existence of effective management
and
supervisory assessments
to verify adequate implementation of established
procedures
and constructive feed back to enhance the process were not
evident.
The team observed inadequate
management involvement in assuring the
direction of licensed reactor operator activities.
While the licensee's
procedure GAP-OPS-01
states that the general supervisor of operation is
responsible for the operating shift activities through the SSS, the team
observed that this direction was primarily provided by the CSO and not by the
SSS or the general supervisor of operation.
The team concluded that the lack
of emphasis of the above procedural requirement was a weakness
in the
management of operational activities.
While the licensee conducted special training for questioning attitudes and the
new work philosophy, training appeared
to be lacking to indoctrinate workers
in the bases of procedures
and the role of established
procedures in assuring
operation of the unit within its licensing and regulatory bases.
The licensee's quality assurance
department surveillances identified repeated
instances of failure to follow procedures
and inadequate work requests.
Based
on the team's observations, it appeared
that the licensee's
response
was not
effective in correcting the root causes for these failures.
14
4.0
ENERIC IMPLI ATI N
OF THIS EVENT
The AITreviewed this event for generic implications and identified two items that
- have potential generic implications:
(1) The adequacy of the instrumentation in the
bay; and (2) The licensee's failure to adequately consider risks associated
with the test
activities that affected multiple systems during shutdown conditions.
The team noted that the instrumentation in the screen house bay is neither safety
related nor designed to assure a high level of reliability. However, operators
use the
information from this instrumentation to make decisions regarding the screen house
bay level and the availability of the ultimate heat sink.
Additionally, the location of
the bay level instrumentation was such that it alarmed the control room only after the
bay level decreased
below that is required to ensure adequate
suction for the pumps.
The team observed that the decision to remove the jumper, and the testing necessary
to determine the effects of this action were not adequately reviewed and approved by
the licensee's
operations,
maintenance,
and engineering organizations.
When
maintenance personnel discovered the jumper, they were concerned
because it was not
indicated on the design drawing.
Therefore,
they believed that the jumper was not
part of the original design or was added by a subsequent plant modification. Their
initial inclination was to remove the jumper, however, they knew that this gate
operated successfully for years with the jumper installed.
The engineering
department was contacted,
and a testing strategy was developed.
However, this
strategy did not include the use of an integrated test procedure,
and therefore, did not
receive multi-departmental review.
The licensee's
focus to restore the gate's
electrical configuration per the design was proper.
However, their failure to verify
the design by using an integrated test procedure was a definite weakness.
The team noted that a test could have been developed for shutdown conditions that
included risk reducing compensatory
measures,
such as, (1) using the screen house
overhead crane to augment the D gate lift'withthe jumper removed,
(2) establishing
minimum decay heat levels, (3) establishing minimum cooling water pump
alignment, (4) establishing additional fore-bay level monitoring with operators
stationed. to communicate level changes,
and (5) having a pre-established
course of
action, ifcompensatory
measures
were less than fully successful.
The failure to
generate
an integrated test procedure resulted in a failure to properly consider
shutdown risks.
I'
5.0
THE LI EN EE'S IMMEDIATEA TI N
Immediately following the event, the licensee implemented the following actions:
1.
The acting plant manager issued a stop work order that essentially stopped all
activities, except for the surveillance and other actions required by the unit's
license.
2.
A review of all work requests
was ordered.
3.
.An assessment
organization was formed to investigate the circumstances
leading to this event, plant response
and personnel action before, during, and
after the transient, and the root cause of the event.
The team found the licensee's review of and response
to the event and implemented
corrected actions acceptable.
6.0
NL SINS
The AIT concluded that the causes of the inadvertent isolation of Lake Ontario from
Nine Mile Unit 1 were:
1 ~
Failure by various levels of personnel in multiple licensee groups to follow the
established work control process,
2.
Inadequate
management
oversight to assure that the workers understood
and
followed established procedures,
3.
Inadequate communications within and among organizations participating in
work activities, and
4.
Insensitivity to shutdown risk among multiple licensee organizations.
The consequences
of this event were minimal because
the reactor core and the reactor
coolant were unaffected by this event, no equipment or structural damage,
and no
radiation was released.
The operator response
to the decreased
level in the intake bay was good.
The AIT
concluded that the licensee's procedures
were adequate
and did not contribute to the
event.
However, the work control breakdown that led to this event was significant
because it caused the unit to isolate from its ultimate heat sink causing the screen
house bay level to drop below that was required in the Unit's licensing bases.
C
16
7.0
MANA EMENT MEETIN
The licensee management
was informed of the scope of this AITduring an entrance
meeting at 2:00 pm on Sunday, February 23, 1992.
The licensee management
was,
briefed of the inspection observations routinely and at 10:00 a.m. on Friday,
February 28, 1992.
A public exit meeting was conducted on March 4, 1992 at 10:00 a.m., at the
licensee's training facilities with licensee representatives
identified in Appendix C to
discuss the preliminary inspection findings.
The licensee acknowledged
the inspection
findings and provided the results of their assessment
of the event and the short and-
long term corrective actions for both units.
TABLE 1
HR N L
Y FE
2/10/92
Work Request (WR) 163740 completed and Raise Push Button Circuit on the gate D was
fixed.
While WR 163740, consisting of troubleshooting, was being performed, undocumented
temporary modifications were discovered.
2/11/92
Deviation event report (DER) 1-92-Q-0267 was initiated by electrical maintenance
to identify
that the mechanical tension overload switch was bypassed contrary to the design drawing.
WR 163740 was revised to require the removal of the tension overload bypass on Gate D
circuitry
2/12/92
Revised WR 163740 completed.
Tension overload switch was put back in the gate D motor
circuitry. Limited travel test completed.
Reported to Station Shift Supervisor (SSS) that the jumper was removed.
The SSS orders the reinstallation of the bypass using the emergency temporary modification
process.
( Maintenance was not sure that the D gate willopen without the bypass during a
de-icing operation.)
DER 1-92-Q0286 was issued to address reinstallation of the bypass per procedure.
2/21/92
Ini ial Plan
nditi n
The plant was in cold shutdown with reactor temperature at 143 degrees F, pressure at
0 PSIG.
Major equipment in operation:
Service water pump No. 11
Circulating water pumps No. 11 & No. 12
Shutdown cooling loop No. 11
Reactor building closed loop cooling (2 loops)
Turbine building closed loop cooling (1 loop)
Table
1
Allother equipment was in a normal shutdown line-up for the existing plant conditions.
0645
Operations personnel
stated that they'ay not be able'to support electrical work on .
- gate D.
Operations management
agreed to review the matter
0700
Electrical Maintenance personnel entered the control room to discuss gate D
maintenance with the SSS.
0730
Intake flow to reverse flow configuration per electrical maintenance
request.
0751
Blue mark-up 1-92-50111 issued to electrical maintenance on screen house gates C &
D.
. 0820
Operations working with electrical maintenance on gate D work request for
troubleshooting.
0820- Electrical maintenance personnel removed the undocumented jumper from the gate.
'829
control circuitry. The electrical maintenance
and operations personnel involved in the
testing of the gate D first cycled the gate 2-3'n the downward direction.
The result
of the test was satisfactory.
Then the gate D was fully closed.
An attempt to reopen
gate D was successful.
0829
Tunnel high differential pressure alarm.
0830
Notified by "C" operator that gate D is closed.
- Circulating water intake level low alarm H2-1-3.
- No, 12 circulating pump removed from service.
- "C" operator instructed electrical maintenance to reinstall jumper.
0830- A non-licensed operator held the up button closed while an electrician held a jumper
0835
across
the tension. over load switch and commenced opening of D gate.
In-plant "E" operator opened gate B to restore level.
0832
Service water header'pressure
low alarm H1-4-2.
- service water pump No. 11 removed from service..
CSO attempted to start the emergency service water pump No. 11.
No discharge
pressure
was observed in the Control Room, the pump was immediately shut down.
Table
1
0833
Fire header pressure low H2-2-8 clear.
- electrical fire pump on.
0835
Screen house intake level normal, alarm H2-1-3 clear.
0838
Emergency service water pumps Nos.
11 & 12 on.
- reactor building service water header pressure normal.
0840
Vented No. 11 service water pump.
0844
Service water pump No. 11 on.
- turbine building service water header pressure normal.
0845
11 & 12 emergency, service water pumps off.
0850
Electric fire pump off.
0900
Water intake flow returned to normal..
- Breathing air compressor
restarted (tripped on low service water pressure).
- Fish screen closed and drain valve opened on No. 12 circulating water pump.
- No. 12 water box vents opened.
0902
Attempted start of service water pump No. 12 following venting, high starting current
observed (prolonged); service water pump No. 12 in Pull-to-Lock.
0930
The licensee conducts a debrief with all personnel involved with the event
0935
Yellow hold-out placed on No. 12 Service Water pump.
1130
The licensee informs the NRC Senior Resident Inspector about the event
1225
The licensee notifies the NRC operations center as required by 10 CFR 50.72.
Later licensee assessed
Unit 2 for similar problems.
250
DIESEL
EMERGENCY
CONTAIN.
DIESEL
DIESEL
SERVICE
GENERATOR
SERVICE
SPRAY
FIRE MATER
ELECTRIC
WATER
COOLING
MATER
PUMP
FIRE
PUMP
PUMPS
WATER PUMP
PUMPS
WATER
CIRCULATING
MATER
PUMPS
240
230
220
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221'-9'1I
245'-3II
Lake High Level
ay of Event
L'evel 243'-10"
Low Lake Level
238'-6"
Plant Analyzed Level
229'-6" Estimated
Level Drop Down
This Event
Level Alarm 220'-6"
21'.
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Figure
1
Suction Levels of Pumps in the Screen
House
Bay
DISCHARGE
~ -.TUNNEL
INTAKE
TUNNEL
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FOR tIORMAL OPERATION:
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~ OPEN
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IS T00 COLD, PARTIALLY
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OUTLINE OF
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FIRE PUMPS
SERYICE WATER PUMPS
CIRCULATING WATER PUMPS
COHDEHSERS
TO COHDEHSERS
Figure
2
- Normal
Flow Configuration of the Screen
House
Bay
REVERSED PLOW IN
SPECIAL OPERATIONS
IH TAKE AND-
-> DISCHARGE<
> TUNNELS
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PART PLAN AT UPPER LEVEL
REVERSEO FLOW OPERATION:
GATES, A, 8 & C CLOSED
GATES 0 & E OPEN
4 SLUICE
I-
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4c
t '
tt
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'r
tt,
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I
WELL & OHE SERVICE WATER
PUMP WELL SMOWH UNWATERED
FOR
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IJ
FROM AHD TO COHDEHSERS
Figure
3
- Reverse
Flow Configuration of the Screen
House
Bay
gpss
AEONS,
(4
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+>>*++
APPENDIX A
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION I
476 ALLENDALEROAD
KING OF PRUSSIA, PENNSYLVANIA19406
February
24,
1992
MEMORANDUMFOR:
Marvin W. Hodges, Director, Division of Reactor Safety
Charles W. Hehl, Director,-Division of Reactor Projects
FROM:
Thomas T. Martin
Regional Administrator
SUBJECT:
AUGMENTED INSPECTION TEAM (AIT) CHARTER-
INADVERTENTISOLATIONOF NINE MILEPOINT
STATION, UNIT 1 ULTIMATEHEAT SINK
You are directed to perform an Augmented Inspection Team (AIT) review of the causes,
safety implications, and associated
licensee actions which led to the inadvertent isolation of
the ultimate heat sink at Nine Mile Point Station, Unit 1 on February 21, 1992.
The basis of
the NRC concern is the apparent inadequacies of management
controls of maintenance
activities that allowed the event to occur. The inspection shall be conducted in accordance
with NRC Manual Chapter 0513, Part III, Inspection Procedure 93800, Regional
Instruction 1010.1 and additional instructions in this memorandum.
DRS is assigned responsibility for the overall conduct of this inspection.
DRP is assigned
responsibility for resident inspector and clerical support and coordination with other NRC
offices.
Dr. P. K. Eapen is designated
as the onsite Team Leader.
Team composition is
described at the end of this memorandum.
Team members will work for Dr. Eapen and are
assigned
to this task until the report is completed.
f!K C
El
The general objectives of this AIT are to:
a.
Conduct a timely, thorough, and systematic review of the circumstances
surrounding
the event, including the sequence of events that led to and followed the
February 21, 1992 isolation of the ultimate heat sink;
b.
'ollect, analyze, and document relevant data and factual info'rmation to determine the
causes,
conditions, and circumstances
pertaining to the event, including the response
to the event by the licensee's
operating staff;
Marvin W. Hodges
Charles W. Hehl
C.
Assess the safety significance of the event and communicate to Regional and
Headquarters
management
the facts and safety concerns related to the problems
identified; and
d.
Evaluate the licensee's review of and response
to the event and implemented
corrective actions.
S
OPE
FTHEIN PE TI N
The AIT should identify,and document the relevant facts and determine the probable causes
of the event. It should. also critically examine the licensee's
response to the event.
The
Team Leader shall develop and implement a specific, detailed inspection plan.
The AIT should:
a.
Develop a detailed chronology of the event;
b.
Determine the root causes of the event as a result of the AIT's evaluation and
document equipment problems, failures, and/or personnel errors which directly or
indirectly contributed to the event.
Potential items to be considered:
Licensee staff actions before, during and following the event.
Configuration controls; including previous modifications and event related
system alignments.
Management oversight and administrative controls in place before, during and
~ following the event.
~
Coordination of maintenance
and operations activities before and during the
event.
~
Adequacy and implementation of troubleshooting procedures.
~
'Licensee staff sensitivity to plant conditions.
Schedular impacts due to the then pending restart of the unit.
c.
Determine the expected
response of the plant and compare it to the actual response,
due to the isolation of the ultimate heat sink.
Marvin W-. Hodges
Charles W. Hehl
d.'.
Determine the adequacy of the responses of the operations and technical support staffs
to the event and the initial licensee analysis,
and decisions on NRC notification
including event classification and reportability.
I
Determine the management
response including the scope and quality of short-term
actions and gather information related to the long-term actions intended to prevent
recurrence of this event, including internal and external communications/dissemination
of licensee-identified concerns
and corrective actions.
Determine the relationship of previous events or precursors, ifany, to this event.
Determine the potential generic implications of this event and recommend
lessons
learned, necessity for generic industry communications,
etc.
5CH¹EE
The AIT shall be dispatched to Nine Mile Point Station Unit 1 so as to arrive and commence
the inspection on February 23, 1992.
A written report on this inspection shall be provided to
me within three weeks of completion of the onsite inspection.
TEAM
OMPOSITION
The assigned Team members are as follows:
Team Manager:
Onsite Team Leader:
Onsite Team Members:
Wayne Lanning, DRS
P. K. Eapen,
S. Barber, DRP
R. Bhatia, DRS
D. Brinkman, NRR
Thomas T. Martin
Regional Administrator
Marvin W. Hodges
Charles W. Hehl
CC:
W. Kane, DRA
C. Cowgill, DRP
L. Nicholson, DRP
Team Members
R. Capra, NRR
J. Calvo, NRR
R. Lobel, OEDO
K Abraham, RI
APPE
IX B
PER
N
NTA TED
MhwkP w
'
~Nm-
Pg+ii~n
J. C. Aldrich
P. Allen
D. Althouse
W. Bandla
H. Barrett
- C. Beckham
K. Belden
T. Bockman
R. Burtch, Jr.
P. Candella
A. Curran, Jr.
- K. Dahlberg
M. Dooley
- J. Endries
C. Fischer
D. K. Greene
D. Hosmer
R. E. Jenkins
F. LePine
E. Lighthall
P. Mazzaferro
- M. McCormick, Jr.
B. Mercier
L. E. Pisano
D. Reynolds
J. Rizzo
G. Roarick
A. Salemi
B. Sherman
- J. Spadafore
- B. Sylvia
- T. Syrell
C. Terry
- R. Tessier
S. Wilczek, Jr.
H. Wysocki
QA Unit 1
"C" Operator
System Engineer
Unit //1, OPS
General Supervisor, Operations
Assistant Station Shift Supervisor
Chief, Shift Operator
Mgr. Nucl. Comm.
Site Engineer
Site Licensing
Plant Mgr. Unit 1
Tech Supp. NMP1
President, Niagara Mohawk Corporation
~ General Supervisor, Maintenance
Mgr Licensing
Unit 2 Mgr Outage/Wk Control
QA/Operating Experience
Electrical Maintenance Schedules
Lead Site Engineer
Outage Coordinator
Plant Mgr - Unit 2
Electrician
WCC/OMG
Electrical Maintenance Supervisor
In-plant "E" Operator
Station Shift Supervisor
Director, Emerg. Prep.
Electrician
ISEG
Executive V. P. - Nuclear
Electrician
V. P. - Nuclear Eng.
Mgr OPS
V. P. - Nuclear Support
Electrical Systems Engineer
Appendix B
S Nuclear Re ul t
mmi sion
- R. Capra
C. Cowgill
C. Hehl
- W. Lanning
- R. Laura
S. Young
~ W. Schmidt
D. Brinkman
Project Director, NRR
Branch Chief, RI
Director, "DRP, RI
Deputy Director, DRS
Resident Inspector
Sr. Resident Insp'ector
Sr. Resident Inspector
Sr. Project Manager, NRR
- Denotes those present at the exit meeting on March 4, 1992, attended by the public and
news media.
The team also held discussions with other licensee management,
operations,
maintenance,
engineering and quality assurance
personnel.
IX
REVIEWED
1.
Chief Shift Operator and Station Shift Supervisor logs for February 20, 1992 and
February 21, 1992
2.
Copies of written statements provided by personnel involved in the event.
3.
Internal memorandum to:
R. L. Tessier, From: 'H. T. Barrett, dated: February 21,
1992, Subject:
"Accountability Meeting on Loss of Heat Sink"
4.
Station Shift,Supervisor Instructions dated 02/20/92
5.
Vnit 1 Daily Work Schedule for 02/19/92 - 02/22/92
6.
Work Request No. 163740
7.
Blue Mark-up 1-92-50111
8.
Deviation/Event Reports 1-92-Q-0267, 1-92-Q-0286, 1-92-Q-0390
9.
Operating Procedure Nl-OP-19, Rev. 18, Section 2.0, Reverse Flow:
Screen house
Operation
10.
Condenser vacuum strip chart for 02/21/92
11.
Computer alarm logs for 0746 hours0.00863 days <br />0.207 hours <br />0.00123 weeks <br />2.83853e-4 months <br /> - 1017 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.869685e-4 months <br /> on 02/21/92
12.
Shutdown cooling heat exchanger inlet and outlet temperature strip chart for 02/21/92
13,
Special Operating Procedure Nl-SOP-7, Rev. 01, Service Water Failure
14.
Drawing No. C-18318-C,- Screen & Pump House Service Water Plan Above El 256'0"
15.
Drawing No. C-18319-C, Screen & Pump House Service Water
16.
Drawing No. C-18320-C, Screen & Pump House Service Water
Plan Above'l 233'0"
Sections
1-1 and 9-9
17,
Drawing No. C-18321-C, Screen & Pump House Service Water Section 2-2
18.
Drawing No. C-18322-C, Screen & Pump House Service Water Section 3-3
-
19.
Drawing No. C-18323-C, Screen & Pump House Service Water Section 4-4
Appendix C
20.
21.
22.
23.
Drawing No.
Drawing No.
Drawing No.
Drawing No.
8-8
C-18324-C, Screen & Pump House Service Water Section 5-5
F
C-18325-C, Screen & Pump House Service Water Section 6-6
C-18326-C, Screen &Pump House Service Water Section 7-7
C-18327-C, Screen & Pump House Service Water &Fire Prot. Section
4
24.
Drawing No. C-18328-C, Screen & Pump House Sealing Water &Fire Prot. Plan
Above El 256'0"
.
25.
Drawing No. C-18329-C, Screen & Pump House Sealing Water & Fire Prot. Section
1-1
26.
Drawing No. C-18330-C, Screen & Pump House Fire Prot. Details in Diesel Driven
Fire Pump Room Plans & Sections
27.
Drawing No. DEN 16334, 2500 G.P.M. Fire Pump Elevation 15 HN-410EF-4 Stage
Vertical Turbine Pump
28.
Drawing No. F-63022-C, Sheet 1, Service Water Reactor & Turbine Bldgs., P & I
Diagram ASME Section XIBoundary Diagram
29.
30.
Drawing No. F-63022-C, Sheet 2, Reactor Bldg. Closed Loop Cooling System ASME
Section XI Boundary Diagram
Drawing No. F-63022-C, Sheet 3, Turbine Building Closed Loop Cooling System
ASME Section XI Boundary Diagram
31.
Drawing No. C-18022-C, Sheet
1, Service Water Reactor &Turbine Bldgs P &I
Diagram
32,
33.
Drawing No. C-18022-C, Sheet 2, Reactor Bldg. Closed Loop Cooling System P &I
Diagram
Drawing No. C-18022-C, Sheet 3, Turbine Building Closed Loop Cooling System P &
I Diagram
34.
Drawing No. C-18022-C, Sheet 4, Waste Buildings Closed Loop Cooling System P &
I Diagram
35.
36.
Maintenance History For Screen House Gates, 01/09/80 to 02/04/92
Document No. SDBD-502, Rev. 0, Service Water System Design Bases Document
Appendix C
37.
Drawing No. C-19441-C, SH. 1, SH.4, SH.4A, 3A, Elementary Wiring Diagram 600
Volt Power Board 176 Power Circuits
38.
Drawing No. C-22303-C, SH.3 Interconnection Diagram,. 600 Volt Power Boards 176
39.
Vendor Drawing No. F26192, 46B, Repair Part Catalogue,
Safety Suggestion for
Crane &Hoist, Lubrication Chart, Frequency,
General Instruction for Shepard Niles
'oller
Bearing Hoist
40.
Drawing No. C-22009-C, SH.3, SH.6 Interconnection Wiring Diagram Instrumentation
Systems for Service and Cooling Water
41.
Drawing No. C-18022-C, Service Water Reactor &Turbine Bldgs. P &I Diagrams
42.
Alarm Response
Procedures
(ARP)
N1-ARP-H2(1-3) Circ Water Pump Intake Level Low
N1-ARP-H1(4-2), Service Water Pump Low Hdr Pressure
N1-ARP-H3(4-1), Screen house Low Seal Pressure
N1-ARP-H2(2-8), Fire Header Low Pressure
Nl-ARP-H1(4-3), Screen Wash Pump
43.
Administrative Procedure AP-5.2.5, Rev.01, Work'In Progress (WIP)
44.
Administrative Procedure AP-5.4, Rev.04, Conduct of Maintenance
45.
Administrative Procedure AP-5.4.2, Rev. 02, Troubleshooting
46.
Administrative Procedure AP-5.5, Rev. 02, Work Control
47.
Administrative Procedure AP-5.5.1, Rev. 06, Work Request 48.
Generation Administrative Procedure GAP-OPS-02, Rev. 00, Control of Equipment
Markups
49.
Administrative Procedure AP-6.1, Rev. 03, Control of Equipment Temporary
Modifications
50.
Nuclear Division Interfacing Procedure NIP-ECA-01, Rev. 03, Deviation Event Report
51.
Generation Administrative Procedure GAP-OPS-01, Rev. 00, Administration of
Operations